ML18152A100

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Insp Repts 50-280/89-24 & 50-281/89-24 on 890730-0902. Violations Noted.Major Areas Inspected:Plant Operations, Maint,Surveillance,Ler Review & Followup on Inspector Identified Items
ML18152A100
Person / Time
Site: Surry  Dominion icon.png
Issue date: 09/27/1989
From: Fredrickson P, Holland W, Larry Nicholson, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A101 List:
References
50-280-89-24, 50-281-89-24, NUDOCS 8910100061
Download: ML18152A100 (24)


See also: IR 05000280/1989024

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

50-280/89-24 and 50-281/89-24

Licensee:

Virginia Electric and Powef Company

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

Facility Name:

Surry* 1 and 2

License Nos.:

DPR-32 and DPR-37

Inspection Conducted:

Inspectors:

July 30 - September 2, 1989

Inspector

q -J.c,-39

Date Signed

J. W. York,

C/-2& **fY}

Date Signed

L.

Approved by:

1-::z_/t., -8y

Date Signed

-z --i1

P. E. Fredrickson, Section

Division of Reactor Project

Date

i gned

SUMMARY

Scope:

This routine resident inspection was conducted o.n site in *the areas of plant

operations, plant maintenance, plant surveillance, licensee event report

review, and followup on inspector identified items.

Certain tours were conducted on backshifts or weekends.

Backshift or weekend

tours were conducted on July 30, August 1, 6, 7, 13, 20, 25, 27, 31, and

September 2.

Results:

During this inspection period, three violations were identified.

The

violations identified were:

Failure to comply with the requirements of Technical Specification 3.0.1

with regards to the action statement (paragraph 3.f (4)).

Failure to follow

when

performing

operability test

(paragraph 6.a).

procedures as required by Technical Specification 6.4

periodic test 1-PT-15.lC,

involving

the

monthly

for the turbine driven auxiliary feedwater

pump

2

Failure to test station batteries within the specified intervals as

In addition, apparent violations were identified for:

Failure of personnel to follow procedures regarding high radiation area

access requirements (paragraph 3.b).

This apparent violation will be

reviewed by the NRC for appropriate enforcement action.

Failure to take appropriate corrective action for past problems identified

during performance of maintenance activities (paragraph 5.a).

This

apparent violation will be reviewed by the NRC for appropriat.e enforcement

. action.

One inspector followup item (paragraph 3.b) was identified for followup on

licensee evaluation of differences in dosimetry readout.

One inspector followup item (paragraph 5.b) ~was identified.for followup on

licensee review of electrical contractor breaker overhaul practices.

One inspector followup item (paragraph 8) was identified for followup on

the licensee's review of internal station communication issues. *

A weakness (paragraph 9) was noted in the licensee's process for determining

reportabil ity of events as required by 10 CFR 50. 72.

A strength (paragraph 3.d) was noted regarding the housekeeping and cleanliness

condition of the Unit 1 safeguards valve pit and pump pit areas .

REPORT DETAILS

1.

PERSONS CONTACTED

2.

Licensee Employees

  • W. Benthall, Supervisor, Licensing
  • R. Bilyeu, Licensing Engineer
  • R. Blount, Superintendent of Technical Services
  • E. Brennan, Supervisor, Mechanical Maintenanc~
  • D. Christian, Assistant Station Manager
  • 0. Erickson, Superintendent of Health Physics
  • E. Grecheck, Assistant Station Manager
  • M. Kansler, Station Manager
  • J. McCarthy, Superintendent of Operations

G. Miller, Licensing Coordinator, Surry

  • J. Ogren, Superintendent of Miintenance
  • T. Sowers, Superintendent of Engineering
  • A. Price, Site Quality Assurance Manager

Other licensee employees contacted included ctintrol room operators, shift

technical advisors, shift supervisors and other plant personnel.

  • Attended exit interview .

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

Plant Status*

Unit 1 began the reporting period in power operation. The unit operated

at power for-the duration of the inspection period.

Unit 2 began the reporting period in a cold shutdown condition.

The

licensee completed the majority of maintenance activities in preparation

for heatup above 200 degrees F.

Operation activities accomplished during

this period included fill and vent of the RCS, establishment of proper

primary plant chemistry, and drawing of a pressurizer bubble.

In

addition, special testing of the

2H emergency electrical bus was

completed. At the end of the inspection period, the unit remained in cold

shutdown.

3.

Operational Safety Verification (71707)

a.

Daily Inspections

The inspectors conducted daily inspections in the following areas:

control room staffing, access, *and operator behavior; operator

adherence to approved procedures, TS and LCOs; examination of panels

containing instrumentation and other.RPS elements to determine that

required channels are operable; and review of control room operator

. I

I

2

logs, operating orders, plant deviation reports, tagout logs, jumper

logs, and tags on components to verify compliance with approved

procedures.

b.

Weekly Inspect_ions

The inspe~tors conducted-weekly inspections in the following areas:

verification of operability of selected ESF systems by valve

alignment, breaker positions, condition of equipment or components,

and operability of instrumentation and support items essential to

system actuation or- performance. Pl ant tours were

conducted which

included observation of general plant/equipment conditions, fire

protection and preventative measures-, control of activities - in

progress, radiation protection controls, physical security controls,

plant housekeeping conditions/cleanliness, and missile hazafds.

The

inspectors routinely monitored the temperature _of the AFW pump

discharge piping to ensure that increases in temperature were

properly m_onitored and evaluated by the licensee.

During this inspection period, th~ licensee identified two problems

- associated with.the radiological protection program at the station.

Both problems were identified by the licensee as violations of TS 6.4.B.

The license and regulatory requirments, a description of the

apparent violations, and the licensee's corrective actions are as

follows.

10 CFR 19.12 requires in part that all individuals working in or

frequenting any-portions of a restricted area shall be instructed to

observe, to the extent within the workers control, the applicable

provisions of the Commission *regulations for the protection of

personnel from exposure to radiation occurring in such areas.

  • -

TS 6.4.8."l requires, in part, that con_trol of entry_ of personnel into

radiation* areas greater than

1 * rem/hr be provided by locked

barricades to prevent unauthorized entry.

The TS also requires that

any individual or group of individuals permitted to enter a high

radiation area be provided with a radiation monitoring device which

continuously indicates the dose rate in the area.

TS 6.4.D requires that radi~tion control procedures be followed.

The

licensee's Radiat_ion Protection Plan, Chapter II, Attachment 11-1

requires, in item 2, that individuals obey posted, verbal, and

written HP instructions.

HP procedure 5.3.20, Initiating, Using, Extending, and Terminating an

RWP, Section 4.3.1.d, requires checkout of a survey meter and high

radiation area keys for entry into a high radiation area, if required

by a RWP.

On Augu~t 7, *1989, licensee personn~l informed the inspector that an

individual was observed on the excess letdown flats, a locked, posted

t .

3

high radiation area in the Unit 2 containment.

The i~dividual was

performing work in the area without authorization from HP to eriter

the area.

Radiation levels in the area ranged from a 1.2 R/hr hot

spot to 80 mrem/hr general area dose rate. When questioned by an HP

technician, the individual related that he called the HP rover on the

  • plant communication system but did not get any response.

The

individual then entered the excess letdown flats by circumventing the

locked high radiation barrier (a- ladder) via a charcoal filter

bunker, and climbed into the area. The HP rover directed the worker

to immediately exit the area and report to the HP control point.

HP

determined the worker's dose for the entry to be 3 mrem.

Failure of

personnel to follow the station radiation protection procedures by

_ obtaining HP authorization * and access keys prior to entering a

locked, high radiation area, as required by 10 CFR 19.12 and TS 6.4.D,

is identified as

an

example

-Of

apparent violation

281/89-24-04.

When licensee management* became aware of the event, all work in the

RCA was halted.

On August 8, 1989, special 1 and 1/2 hour sessions

were conducted with all radiation wo.rkers at the station concerning

compliance with station HP requirements.

During the meetings, senior

station manigement made it clear to the station and contractor staffs

that adherence to procedures ,and attention to detail in all areas

wer~ required. Those who believed differently were told to consider

terminating their employment at the station.*

The second problem, whi~h occurred on August 9, involved two contract

workers entering a high radiation area in the Unit 2 containment

without a dose rate meter.

After approximately five minutes, the

workers realized their mistake and exited the area. Similar to the

first instance, when the problem became known to HP personnel,

immediate actions were taken. The licensee identified the violation

in a deviation report and excluded the workers that were involved

from the RCA.

HP determined that the two workers' doses were 3 mrem

and 5 mrem for the entry.* Dose r'ates in the area ranged from 5

mrem/hr to* 150 mrem/hr.

Addition*a1 corrective actions included

posting of watches at the entrance of each high radiation area to

  • ensure that workers have proper instructions and radiological

equipment prior to entering the area.

Failure of personnel to have a

dose rate monitoring device when entering a high radiation area, as

required by HP procedure 5.3.20, 10 CFR 19.12, and TS 6.4.8.1 is

identified as another example of apparent violation 281/89-24-04.

Both violations were immediately identified to the inspector and

discussions were held with licensee management.

In each case, the

persons involved were terminated from working at the station.

Licensee management made it known to all employees that termination

would be the action taken for future violations of radiological

requirements. These two events are a continuation of four previously

identified NCVs (IR No. 280, 281/89-23).

The inspector also noted

- - - - -


- -

4

that a similar violation of high radiation access areas occurred in

May 1988 ..

On August 17, *. 1989, the licensee informed the inspector that a

maintenance worker received a radiation dose in

excess o.f his

assigned administrative limit when working on a c.heck valve. in the

Unit.2 containment._ The administrative overexposure was recorded on

the worker's gonad dosimetry as being approximately 821. mrem.

This

dose, when added to the worker's previous.e~posure, totaled 1802 mrem

for the. quarter; 52 mrem higher than the assigned administrative

limit of 1750 mrem.

The licensee conducted an investigation into the

administrative overexposure and concluded that all actions taken by

the mecha~ics and HP technicians on the job were appropriate. * The

licensee further concluded that all personnel involved were familiar

with the exp6~ure rates in the area and responded proactively to stay

time limits and SRO readings.* However, the licensee was in the

process of eva,luating the differences between the readings of the

SRDs and the TLDs when the report period ended.

This issue will be

reviewed by regional HP inspectors during subsequerit inspections and

is identified as

!FI 280,281/89-24-06,

followup

on

l~censee

evaluation of differences in dosimetry readouts.

c.

Biweekly Inspections

d.

The inspectors conducted biweekly inspections in the following are~s:

verification review and walkdown*of safety-related tagouts in effect;

review of samplin'g program (e.g., primary and secondary coolant

samples, boric acid tank samples, plant liquid and gaseous samples);

observation of control room shift turnover; review of implementation

of the_ plant problem identification system; verification of selected

portions of containment isolation lineups; and verification that

  • notices to workers are posted as requi.red by 10 CFR 19.

Other Inspection Activities

Inspections included areas in the Units 1 and 2 cable vaults, vital

battery rooms, steam safeguards areas, emergency switchgear rooms,.

diesel generator rooms, control room, auxiliary building, Unit 1 *and

Unit 2 containments, cable penetration areas, independent spent fuel

storage facility, low level intake structure, and the safeguards

valve pit and pump pit areas. Reactor coolant system leak rates were

reviewed to ensure that detected or suspected leakage from the system

was recorded, investigated, and evaluated; and that appropriate

actions were

taken, if required.

The

inspectors

routinely

independently calculated RCS leak rates using the NRC Independent*

Measurements Leak Rate Program (RCSLK9).

On a regular basis, RWPs

were reviewed and specific work activities were monitored to assure

they were _being conducted per the

RWPs.

Selected radiation

.

protection ; nstruments were peri odi ca 1 ly checked, and *equipment

operability and calibration frequency were verified .

5

During the inspector's tour of the Unit -1 safeguards valve pit and

pump pit areas, it was noted that these areas had recently been

decontaminated and released -s* cleari areas.

Of particular note wis

the condition of the valve pit area where several safety-related MOVs

are located .. The inspe~tor noted that all components appeared to be

in good working order and that the general cleanliness in this

difficult-to-access area was excellent. The inspector believes that

the conditions observed during this tour is a positive indicator of

improvements in working and material condi~ions.

On August 22, 1989, during a routine walk.down of 'the Unit 1 SI

system, the inspectors noticed that the flow orifice for flow element

FE-1946 was installed backwards.

This is the flow element that

measures discharge flow from the low h.ead SI pump 1-SI-P-lB.

The

inspectors identified this discrepancy to the licensee-and expressed

concern over the operabi 1 i ty of * the pump and the method -for

installing fiow orifices. The licensee declared the pump inoperable

at- *1535 hours on August 22 and entered a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> LCO to reverse the

orifice and test the pump.

The pump was tested.satisfactorily and

returned to service at 0800 hours0.00926 days <br />0.222 hours <br />0.00132 weeks <br />3.044e-4 months <br /> on August 23.

Further discussion

regarding the installation of this Orifice is inclOded in paragraph

5.

e.

Physical Security Program Inspections

In the course of monthly activities, the inspectors included a review

of the licensee Is physical . security program.

The performance of

various shifts of the security force was observed in the conduct of

daily activities to include: protected and vital areas access

controls~ * searching of personnel, packages and vehicles; badge

issuance and retrieval; escorting of visitors; and patrols and

compensatory posts.

f.

Licensee 10 CFR 50.72 Reports

(1)

On July 31, 1989, the licensee made a report in accordan~e with

10 CFR 50. 72 concerning to the tripp;'ng of the auxiliary

building normal ventilation supply and exhaust fans. These fans

will trip on a SI signal so that the ventilation system is

realigned to filtered exhaust (emergency alignment); however, no

SI signal was present.

The licensee initially determined that

the fans tripped due to a decrease in air pressure in the fan's

pneumatic control header caused by the opening of four air

operated dampers.

At the time of the event, the dampers were

being opened by control room operators as* part of a normal

evolution.

Additional engineering investigation revealed that

the actuation occurred due to a combination of leaking

mechanical connections on the pneumatic control header, and the

operation of the four dampers, reducing the IA header pressure

below the trip setpoint.

An LER was submitted on this event on

August 30, 1989.

The inspectors will address the licensee's

corrective actions during closeout of the LER.

(2)

(3)

( 4)

6

On August 13, 1989, the licensee made a report in accordance*.

with 10 CFR 50.72 regarding an inadvertent ESF actuation of one

of the two auxiliary building emergency ventilation fans.* The

actuation was due to improper landing of electrical leads on.a

pressure swi.tch, causing* the automatic operation of the

11811

train emerg.ericy ventilation fan.

Immediate corrective actions

included proper retermination of the electrical leads and

returning the emergency ventilation fari

to service.

The

licensee initiated an HPES review of this problem and will

address the resultant findings * after management review.* The

licensee will also submit an LER.

The inspectors will review

the HPES findings and licensee's corrective actions during

closeout of the LER.

On August .14, 1989, the licensee made a report in accordance

with 10 CFR 50.72 concerning an automatic start of the Unit 2

118

11 charging pump (high head SI pump).

The event was caused by

a operator inadvertently bumping the pump start switch* out of

the

11 pull to lock" position (the switch was not properly engaged

in. that positi.on).

The pump auto-started due to low discharge

header pressure.

The low pressure indication was based on the

fact that no other pumps were running due to the unit being in a

cold shutdown condition. During the event, the charging pump

discharge flowpath was isolated.for other testing, preventing

fl ow to the RCS.

This. event occurred on August 13 and was

determined to not be reportable; however, a determi~ation was

made the next day that the. event should be reported as an

information call.

  • On August 15, 1989, the licensee made a report in accordance

with 10 CFR 50.72 concerning the failure to accomplish the

required TS stirveillance testing on the Unit 1 RPS permissive

interlock P-10

prior to unit startup.

The

surveillance

- requirements are contained in TS 4.1.A.2 and TS Table 4.1-A.

The licensee discovered the problem during an ongoing review of

the TS surveillance requirements.

After identification of the

missed survei]lance to the SNSOC, the licensee entered TS 3.0.1,

which requires that the unit be placed in hot shutdown within

the . next six hours.

The licensee prep a red a JCO for the

discovered condition; and, after review and approval by .the

SNSOC,

the licensee exited TS 3.0.1.

Testing on the P-10

interlock logic was completed on August 16, and at that time a

SNSOC review determined that all required testing had been

accomplished.

The licensee made a followup call to the NRC.

After review of the event by the NRC on August 16, the licensee

was questioned with regards to their exiting TS 3.0.1 without

either taking the shutdown action required by TS 3.0.1, or

completing the P-10 surveillance requirement of TS 4.1.A.2.

The

licensee concluded that after the JCO had been prepared and

approved addressing compensatory measures,

the appropriate

g.

(5)

7

actions had been completed to exit TS 3.0.1.. After further*

discussion of this issue with the NRC, licensee senior manage-

ment

agreed that incorrect action was taken and the correct

action .in the case. would ha~e been to comply with TS 3.0.1 or

request discretionary enforcement.

Failure to comply with the

requirements

of

TS 3.0.1

is

identified

as

_violation *

280/89-24-01.

On August 18, 1989,_ the licensee made a report in accordance

with 10 CFR 50.72 regarding an inadvertent ESF actuation of the

Unit 2

11A

11 train Phase 1 recirculation mode transfer system.

The **a.ctuation was

caused. by

inadvertent touching of an

electr.ical contact by an.electrician while connecting a jumper

to an adjacent circuit in accordance with a modification

procedure.

The licensee will submit an LER on this eyent.

Restart Readiness Assessment Review - Unit 2

During this

inspection

period, the

inspectors monitor~d

the

licensee 1 s managem~nt review of all functional areas associated with

the ret~rn to operation of Unit 2 .. These functional areas included

operations, maintenance,

surveillance, engineering, radiological

controls,

safety assessment,

and

quality

verification.

The

management team involved in these reviews included the Station

Manager, the two Assistant Stat ion Managers, the Quality assurance

ManagerL and th~ Assistant Vice President, Nuclear Operations.

The

initial reviews of each functional area were held on August 1, 1989.

The review~ consisted of the superintendents of the functional areas

addressing why their area of responsibility should be considered

ready for restart.

The following items were reviewed in each functional area:

Operations

-

Material

condition

walkdowns,

housekeeping

walkdowns, safety_system lineups, chemistry control readiness,

annunciator review,

system status log requirements, action

statement log requfrements, temporary modification log status,

post-maintenance testing, selected critical valve third checks,

and required startup training.

Maintenance"" Material condition walk.downs, work order backlog,

MOV

issues,

check valve iss~es,

steam generator issues, .

preventative maintenance status, and electrical 4160V and 480V

breakers.*

Surveillance -

Periodic testing program, American Society of

Mechnical

Engineers

Section

XI

program,

erosion/corrosion

program, and Type Band C testing.

Engineering -

EWR backlog review, Type 1 backlog review,

technical reviews of DCPs and EWRs, MOV issues, snubbers, root

8

cause evaluations, applicable JCOs, el~ctrical terminations, ESF

testing, IA system, and drawings update.

Radiological Controls -* Contaminated area reduct1on, personnel

contamination reports, exposure evaluation, hot spot reduction,

contamination

controls,

lead

shielding,

HP

technician

availability and effectiveness, and radiological engineering

controls.

. Safety Assessment - NRC commitments, commitment tracking system

items,

operational

events, . HPES * recommendations,

industry

experience, North Anna startup issues review for applicability,

, TS changes, and SNSOC reviews of deviation report backlog.

The inspectors attended this meeting and agreed with the licensee's

conclusion that, in general, there was too much work outstanding to

allow an effective restart decision process. Presentations by the QA

Manager and the HP _Superintendent were * noted to be thorough and

comprehensive.

Within the areas inspected, one violation and one

apparent violation were identified.

4.

Operational Readiness Assurance Program ~ev,ew - Unit 2 (71710)

During the inspection period, th~ inspectors conducted a review of ihe

licensee's QA organization's overview of activities associated with Unit 2

operational readiness assurance program implementation.

The inspectors

noted that the QA performance group conducted independent wa l kdowns on

portions of the IA, SI, AFW, and CCW systems located in U_nit 2

containment.

All of these systems were previously walked down by the

systems engineers.

The QA wa l kdowns were performed to provide an

assessment of the systems engineers. wa l kdowns.

A list of discrepant

conditions found by QA, some of which had been identified by engineering;

and others that appeared not to have been identified, was submitted to

engineering for review.

Some of the conditions noted by QA were as

fo 11 ows:

Valves not labeled - Of the ten valves identified by QA as not having

tags, one valve was missed by the systems engineer.

Incomplete bolting thread engagement - During the walkdown of Unit 1,

incomplete bolting thread engagement was also*found on some of the*

components, but all of these were evaluated by design engineering as

acceptable (full thread engagement is not required to _develop the

full strength of a bolt). The systems engineers us~d the experience

gained on Unit t to determine that similar thread engagements found

on Unit 2 were acceptable.* Evaluations_ were made by the systems

engineers but were not recorded on inspection documentation.

Teflon tape on threaded connections in the IA system and at solenoid

operated valves in the SI system - Engineering stated that the use of

9

teflon tipe is not an operational c6hcern and will not result in the

failure of a component to perform its intended fun~tlon.

Material. discrepancies. such as leaks, missing bolts on junction

boxes, br9ken electr1cal conduit connections, supports not painted,

and rust on some components -

Nine of the twenty-seven items

identified by QA were a1so identified and recorded by the systems

engineers.

Most of the 1 eaks -and rusty areas were eva 1 uated by the

systems engineers during the walkdowns as not being significant and

~ere therefore not recorded.

Some of the other discrepanci~s were

not pa rt of the wa 1 kdown criteria, nor the wa 1 kdown boundary, or

occurred due to work or some other activity after- the systems

engineers performed their walkdowns..

.

Two 1/2 inch diamet~r lines ~nd four level transmitters not a~pearfng

to meet seismic class I requirements - Instead of performing the

calculations to determine whether the supports or lack of in certain

areas would have been adequate in a seismic event, the decision was

made to add or modify supports.

Paint splatter on SI piping - Unit 1 also had paint splatter on some

of the piping and* the condition was evaluated, as not being

detrimental.

The painting work procedure was recently revised to

address splatter protection.

The systems engineers had been instructed to make some decisions during

the walkdown based on the experience gained in the review and resolu.tion

of Unit 1 walk.down items ..

The QA engineers had conducted their overview

walkdowns of selected systems based on original requirements stated in the

engineering package.

These original requirements were to identify ,all

di~crepancies and not to. use engineering judgement in deficiency

identificatio.n.

EWR 88-584A, which was used for walkdowns, had a field

.change added to clarify the systems engineers instructions for the Unit 2

walkdown.

On August 18, 1989, QA, systems engineering, and an NRC inspector entered

the Unit 2 containment to determine the status of the items identified in

the previous QA walk.down.

The items that engineering stated would be

corrected before startup were either completed or in the progress of being

completed. Another walkdown *by QA and systems engineering was performed

on August 21, 1989.

This walkdown was performed on the CCW system from

the containment penetratio~s to the reactor containment air recirculation

coolers.

This area was chosen because a QC inspector had written a

station deviation on rusted piping penetrations in this area.

No

additional significant issues were identified curing this walkdown.

The

inspectors concluded, based on review of the systems engineers and QA

walkdowns, that appropriate resolution of disparities identified in the

walkdowns for Unit 2 were adequate.

Within the areas inspected, no violations or deviations were identified .

5.

10

Maintenance Inspections (62703 & 42700)

During the inspection period, the .inspectors re~iewed maintenance

activities to assure -compliance with the appropriate procedures.

Additional effort. was focused on verifying that previously identified

problems had been adequately corrected.

a.

Maintenance Corrective Action Issues

'

.

A review of several work packages revealed inconsistencies in

maintaining system cleanliness and the methods for obtaining torque

va 1 ues for system fasteners.

These are two areas that have been

previously identified as being deficient.

For example, IR 280,

281/88-28 issued a violation identifying a pr6grammatic breakdown in

the controls and procedures used to maintain system foreign material

exclusion.

In addition, several examples of improper torquing were

identified during. the service water SSFI inspection (IR 280,

281/88-32), and a violation was issued in a letter dated May 18,

1989.

The inspectors focused on. these two areas of inconsistencies

and identified numerous examples, as detailed below, where the

corrective actions taken in response to the above violations were

ineffective. The inspectors also focused on installation of orifices

after identifying a case where an orifice was installed incorrectly.

Failure to take appropriate corrective actj6ns for previously

  • identified.maintenance problems is tdentified as apparent violation

280, 281/89-24-05. .

-

Near the end of the inspection period, the licensee implemented a new

administrative procedu~e to address the cleanliness requirements.

Also, a new maintenance procedure for orifice plate inspections was

implemented.

These procedures were identified to the inspectors;

however, their effectiveness has not been determined and wil 1 be

reviewed during future inspections.

(1) Cleanliness Control

The licensee opened and repaired several SI check valves during

the inspection period. These check valves were worked because

of identified internal and/or body to bonnet* leakage concerns,

. Some of the valves identified as having internal leakage are

interface va 1 ves between the RCS and the SI system.

The

inspectors reviewed the work associated with several check

valves in the Unit 2 SI system.

This work was performed on 6

inch Velan check valves in accordance with maintenance procedure

MMP-C-Sl-195.

The specific valves and accompanying work orders

reviewed by the-inspectors are as follows:

2-SI-79

2;..SI-88

Work Order #3800084254

Work Order #380084170

2-SI-91

2-SI;..226

2-SI-24"1 *

11

Work Order #3800084320

  • Work Order #3800071696

Work Order #3800084253

During these reviews, the inspectors were informed that on

August 14, 1989, a bolt was inadvertently dropped into the body

of SI check valve 2-SI-79. The bolt was from a machine that was

being installed and adjustEid for lapping the valve seat.

The

bolt was later found and retrieved from the RCS primary loop

piping.

As a result of the above incident, the inspectors reviewed the

licensee's program for foreign material exclusion, including

compliance with their response to an NRC enforcement action

taken last year involving programmatic weaknesses in this area.

The licensee's response, dated December 9, 1988, stated that the

Superintendent of Maintenance issued a standing order to ensure

that foreign material is prevented from entering a system or

componerit during the performance of maintenance activities. The

inspectori reviewed maintenance standtng order 88-1, dated July

29, 1988, System Cleanliness, and concluded that implemen-tation

of this order has been ineffective. Specific deficiencies noted

are as follows:

Item 4 of the standing order mandates that requirements be

deviated into a procedure to either install a temporary

cover on all openings or an individual be assigned to

continuously monitor the openings and an

inspection

performed *to ensure ~leanliness immediately prior to

sealing the opening.

This was not accomplished in that

MMP-C-SI~l95 did not contain the specific requirements.

Item 7 of the standing order require~ that all personnel,

including contractors,

performing ~ork. that involves

opening a system or component sha 11

read and sign to

acknowledge that they have read the standing order.

Contrary to this requirement, personne 1 performing work

inside *the check valves did not read and sign to indicate

an understanding of the *standing order.

The inspectors concluded that the licensee has not effectively

implemented th.e corrective actions developed in response to

previous violations regarding

foreign material

exclusion.

Discussions with maintenance department personnel and a sampling

of other maintenance procedures indicates that this weakness was

widespread in most work involvin*g open systems. Additional

examples of this weakness are discussed in paragraphs 5.a(3) and

5.a(4).

Compliance with instructions specified in maintenance

standing orders is further hampered by the fact that the main~

tenance department does not have a procedu~e that defines the

12

implementation and use of standing orders.

In addition, the

maintenance department does not have a program in place to

ensure that craft personnel are aware of the standing order

requirements.

Although it was evident that an effort was made

to establish and maintain an accountability area for work on

check val~e 2-SI-79, a decision was made within the maintenance

department to proceed with the job in lieu of developing an

acceptable meth1?d of foreign material exclusion.

The dropped

b~lt into check valve resulted in expending 2.735 mrem to *find

and retrieve it, and also required the RCS water level to be

maintained for a longer period of time in a reduced inventory

condition.

The weaknesses in th~ implementation of the

cleanliness program for maintehance activities associated with

the preceeding check valve repairs are identified as an example

of apparent -violati~n 280, 281/89-24-05,

for failure to take

appropriate corrective action for past problems identified

during performance of maintenance activities.

(2)

Fastener Torquing Issues

During this inspection* period, the licensee identified several

problems associatE!d with appropriate materi.al identification/

torquing of the check valve fasteners. Based 6n these identified

discrepancies, the inspectors reviewed the follo~ing work

packages

with

regards

to the

licensee's

program

for

indentification and torquing of fasteners:

2-SI-79

Work Order #3800084254

2-SI-88

Work Order #3800084170

2-SI-91

Work Order #3800084320

1-SI-FE-1946

Work Order #3800076509*

The inspectors reviewed maintenance standing order 89-1, dated

May 22, 1989, Torque Values.

Upon examining the above listed

work packages, the inspector noted that the following items of

the standing ord_er were not being adhered to in some of the

packages:

Item 1 of the standing order states that all torque values

  • listed in procedures wi 11

be verified by maintenance

engineering prior to torquing, and this individual will

initial the torque value* in the procedure. In the work

packages for 2-SI-91 and 1-SI-FE-1946, torquing values for

the flange bolts were not verified and initialed by

maintenance engineering as

required.

It was

later

deter.mined that the 2-SI-91 valve hinge bolts

were

overt_orqued without any reference in the procedure of the

required torque value.

13

Item 5 of the standing order states that if a maintenance

engineering representative is not available on sit~. torque

value verification may be made by telephone and noted on

the proce_dure or work order.

In work packages for 2-SI-91

and l-SI-FE-1946, tcirque value verification was not noted

on the procedure or work order.

Iri the package for check valve 2-SI-88, a maintenance

transmittal form stated that if the hinge bracket bolts

were ASTM SA 193 grade 86~ to torque the bolts to SO*to 75

ft-lbs, but if the bolts were grade 88, to torque the bolts

to 16 to 25 ft-lbs.

The transmittal further stated that if

the bolt material cannot be verified; torque to the lower

rang~ of values. Although the material for this valve was

not identified in the package, hinge bracket bolts inside

the valve were torqued to 50 ft-lbs .

. A review of the above work packages revea 1 ed an inadequate

implementation of the corrective actions specified in the

standing order dealing with torque values. Incorisistenci~s were

noted regarding the method for obtaining and documenting the

necessary torque values.

The inspectors selected additional

  • maintenance flange and va 1 ve procedures and found numerous

examples of inadequate implementation of the standing order.

The licensee performed an ehgineering evaluation arid determined

th~t the ~pplted torque was acceptable for 2-SI-88 and 91.

The

eva 1 uat ion was documented in EWR 89-579 and reviewed by the

inspector. The weaknesses in the implementation of the torquing

requirements for maintenance* activities associated with the

preceeding check valves and orifice flange repairs is identified

as

an

additional* example

of

apparent

violation

280,

281/89-24-05.

(3)

Flow Orifice Installation

As noted in paragraph 3.d of this report, the inspectors

discovered that flow orifice for flow element FE-1946 was

installed backwards in the Unit 1 SI system. This orifice is a

bevelea-type plate that is used to measure the discharge flow

from a low head SI pump.

Installation of the orifice in a

reverse orientation introduces an indeterminate error in the

indicated flow value.

The licensee documented this discrepancy via station deviation

Sl-89-1869. The last time this orifice was worked was on June

12, 1989, per work order 3800076509, which invoked procedure

MMP-C-G-201.1;

Corrective Maintenance

Procedure

For

Blank

Flanges, Spectacle Flanges and Orifice Plate Flanges, dated June

10, 1988. Steps 5.4.6 and 5.4.7 of this procedure required the

mechanic to obtain orientation information from operations and

maintenance engineering prior to installation.

The procedure

( 4)

14

used on June 12 indicates that the mechanic obtained the correct

orientation information.

Step 5:4.9 of the procedure required

the

mechanic

to install

the orifice and document

the

orientation.

This step was signed as being performed, but the

orientation was not documented.

The inspectors also noted that

the maintenance procedure does not re qui re an independent

verification of the orifice installation.

Whil.e verifying the inspector's conclusion that the orifice was

installed backwards, the licensee's systems engineer noted that

flow orifice 1-SI-FE.-1941 was also installed backwards.

This

condition was documented via station, deviation Sl-89~1880.

The

licensee implemented a walkdown of selected safety-related

orifices and found one additional orifice installed backwards.

The licensee has had problems with properly installing flow

orifices.

The

inspectors

previously

identified

reversed

orifices in the AFW system as documented in IR 280, 281/88-18.

Further licensee inspections at that time revealed additional

orifices in safety-related systems installed backwards and

resulted in a violation dticumented in IR 280, 281/88-28, dated

August 12, 1988 .. The weaknesses in the* maintenance program for.

ensuring the correct installation of orifices are identified as

an_additional example of apparent violation 280, 281/89-24-05.

The inspectors also reviewed MMP-C-G-201.1 for compliance with

the cleanliness and torquing standards, and found additional

examples where corrective actions were inadequate.

For example,

the orifice flange was broken and remade without a vi sua 1

inspection and verification to ensure system cleanliness as

required by maintenance standing order 88-1.

In addition, the

torque values used were not verified by maintenance engineering

as required by maintenance standing order 89-1.

The weaknesses

in this procedure with regards to cleanliness and torquing

control are identified as an additional example of apparent

violation 280, 281/89-24-05,

PORV Block Valve Repair

The inspectors reviewed the failure of the pressurizer PORV

block valve 2-RC-MOV-2536 that occurred on July 24.

Mechan,cs

had

completed the installation of a new motor operator

(Limitorque) and had turned the valve over to the electricians

for wiring and testing. The wiring of the valve operator was

performed and the work was independently QC-verified prior to

clearing the tags for thrust testing.

A subsequent attempt to

cycle the valve resulted in the valve going hard into the seat,

cracking the ~pper bearing housing.

The cause was determined to

be incorrect wiring that resulted in the torque switch being

bypassed in the closed direction .

15

The inspectors reviewed the following dricumentation ~ertaining

to this event:

Work Orde~ #3800083005, authorizing disionnecting and

reconnecting the motor operator.

Maintenance Procedure EMP-C-MOV-11, Disconnect and Connect

MOV's.

Station Deviation S2-89-672, identifying the failure.

EWR 89-537, dated 8/6/89, Evaluate RC Valve

(2-RC-MOV-2536).

EWR 89-522, dated 7/29/89, Evaluate RC Valve Internals

(2-RC-MOV-2536).

EWR 89-137, dated 7/3/89, Evaluation/Standardization Of

Rising Stem MOVS.

Maintenance Procedure EMP-C-MOV-151- Testing MOVs Using

MOVATS System:

The corrective actions performed by the licensee involved

disassembly and inspection of the valve body. The valve i.s a 3

inch 1500 lb. Velan gate valve equipped with a SMB-00 Limitorque

motor operator.

Engineering estimated that the force exerted

during this event was between 39,000 and 43,000 lbs. The valve

has a one time allowable limit of betwee~ 19,000 and 20,000 lbs.

for the temperatures the valve was experiencing at the tim* of

ove~thrusting. The valve seats were liquid penetrant tested and

the indications were removed by grinding and/or lapping.

In.

addition, a new stem and wedge were installed.

The motor

operator was removed, diassembled and repaired by replacing the

damaged parts. Station engineering, with concurrence from the

valve manufacturer, concluded that a total valve replacement was

not required.

The licensee was unable to determine a definitive cause of the

wiring error. Interviews with the electrician and QC inspector

involved did not reveal any defective technique or cause for the

error.

Both individuals believed that the valve- operator was

properly wired when they left the job site.

The procedures

reviewed by the inspector appeared to be correct with no

apparent contribution to the problem.

The inspector did note,

however, that sev~ral additional problems were identified with

the wiring during an as-found inspection following the event.

Step 5 .11. 6 of procedure EMP-C-MOV-11 documented the as-found

inspectio*n, the findings* of which included defective control

wire lugs, excess1ve grease in the compartment, heat shrink

markers not shrunk, annunciator wiring loose, and a motor lead

connection less than hand tight.

The inspector discussed the

b.

16

specifics pertaining to these problems with the station

engineers and maintenance staff, and concluded that the cause

was

predominantly

a

result of poor

workmanship.

The

Superintendent of Mai ntenailce agreed and offered commen_ts that

indicated that this is an isolated case involving the poor

workmanship of a specific electrician. This is plausible given

the large number of Limitorque overhauls performed over the last

several months with rel~tively few

problems

noted,

The

inspectors will continue to monitor the performance of the

. electrical maintenrnce staff involved in MDV work.

The inspector reviewed the procedure (EWR 89-522) that inspected

and repaired the PORV block valve for compliance with the system

cleanliness requirements of maintenance department standing

order B8-1 (reference paragraph 5.a(l) for inftirmation on this

standing order).

The valve is located above the pressurizer,

just upstream of the PORV.

Although. step 4.2 of- EWR 89-:522

states that foreign material exclusion is i~portant and requires

temporary covers or constant surveillance, there was no evidence

that an independent visual inspection was performed prior to

system closure as required *by item 3 of the standing order.

In

addition, documentation that a~l a~plicable tndividuals had read

and und~rstood the standing order prior to beginning wcirk could

not be produced as required by i tern 7 * of the standing order;

The weaknesses in this procedure regarding cleahliness control

  • is identified as an additional example of apparent violation

280, 281/89-24-05.

.

480 Volt Switchgear Failure

On August 13, the inspector witnessed starting of the Unit. 1 outside

recirculation spray pump 1-RS-P-2A in accordance with* surveillance -

procedure 1-PT-17.3.

The amber breaker disagreement light came on

indicating a problem.with the 480 volt breaker 1-RS-PM0-2A.

This

condition was documented via station devfation Sl-89-1834; and work

order 3800084724 was issued to investigate the failure.

Results of

this investigation indicated that the trip rod in the breaker control

device was not adjusted in accordance with the vendor manual.

The licensee reviewed the procedures and technique used by an outside

contractor that perfotmed overhauls on the breaker and found them to

be adequate.

Discussions with the breaker manufacturer indicated

that the trip rod adjustment is set and should not vary with age or

breaker. cycles. Corrective action performed by the l_itensee included

randomly selecting five breakers from Unit 2 and verifying the

correct trip rod adjustment. After inspection of three of the five

breakers, the licensee determined that some misadjustment was

apparent.

The licensee conducted a review in the training center of the steps

i nvo 1 ved in the adjustment process; the inspectors witnessed this

17

review.

From

the

review, the* licensee

concluded that the

misadjustment was not an jmmediate safety concetn due to the large

margin of tolerance available. The licens~e further determined that

if the misadjustment was in.one directton, the* breaker would still

perform its function if it* successfully passed post-maintenance

testing.

If the misadjustment was in the other direction, the

breaker would not operate -as required to make the adjustment.

Although the licensee was able to demonstrate that safe breaker*

operation was

not a concern,

the

inspector questioned the

contractor's overhaul practices* in assuring quality. The licensee was

1n the process of reviewing this issue when the inspection period

ended.

This issue is identified as !FI 280r 281/89-24-07, followup

on

licens~e review of electrical conttactor breaker overhaul

practices.

Within the areas inspected, one apparent violation was identified.

6.

Surveillance Inspections (61726 & 42700)

During the ~eporting peri~d, the inspectors reviewed various

surveillance acti*vities: to assure compliance with the appropriate

procedures as follows:

Test prerequisites were met.

-

Tests were performed in accordance with approved procedures.

Test- procedures appeared to perform their intended function.

Adequate coordination existed among personnel involved in the test.

Test data was properly collected and recorded.

Inspection areas included the following:

a.

AFW Testing

The inspectors reviewed the survei 11 ance test performed on AFW

turbine-driven pump l-FW-P-2, on August 1, 1989.

This test was

conducted using periodic test procedure l-PT-15.lC, Turbine Driven

Auxiliary Feedwater Pump (l-FW-P-2), dated July 25, 1989.

The

inspectors expressed concern that the turbine speed was adjusted from

3965 RPM to 4200 RPM prior to obtaining test data.

This situation

was the subject of previous concerns because of the potential to

overpressurize the downstream piping.

For example, if th~ turbine

speed is adjusted up during a pump run, the possibility exists that

during the * next pump start the turbine governor may a 11 ow enough

overshoot

to

overpressurize

the

downstream

components.

Overpressurization is of particular concern when considering the type

of governor used on the ~urbines and the lack of a relief valve in

the discharge piping.

Although it appears that the piping was not

18

overpres~urized during the above tase, the lic~nsee is planning to

replace the governor and add a relief valve.

An additional concern

of the inspectors was *that the adjustment of speed prior to *obtaining

pump data may mask the existence of an inoperable pump.

The

licensee agreed with the above inspector's concerns, and

documented the problem via station deviation report Sl-89-1791.

The

test was again performed on August 2 and determined to be acceptable.

The adjustment of the turbine speed on /August *1, is not a 11 owed by

procedure 1-PT-15.lC, and is identified as violation 280/89-24-02,

for failure. to follow procedures as required by TS 6.4.

The

inspectors discussed the issue with operations supervision and

believe that ~ppropriate sensitivity to concerns of this nature has

been fully disseminated to the operations staff.

b.

Battery Survei 11 ance Testing

C,

The

inspectors

reviewed

the

status

of electrical

battery

surveillances and

ex~ressed concern

regarding the number

of

surveillances performed outside the allowable grace period provided

by TS.

Discussions with the engineering group that* tracks the

. performance of periodic tests indicate that from August 1988, until

August 1989, 11 out of a total of 617 battery surveillances were not

performed within the period allowed by TS.

The inspectors reviewed

other selected tests and concluded that the battery tests are an

exception in that the remainder of surveillance tests are, as a ~ule,

performed as scheduled.

On

August 22, the inspector discussed the above concern with

a~plicable maintenance management.

It appears that although

engineering is notifying the correct _persons within the electrical

maintenance department of pending tests, these key personnel are not

ensuring compliance with the s~ecified test intervals.

TS. 4.6.C.1

requires cert_ain battery tests to be performed within specified time

intervals (every week, month, 3 months, etc .. ).

TS 4.0.2 further

allriws a 25 percent grace period for testing intervals to accommodate

normal test schedules.

The failure to comply with the allowable

TS intervals for station battery tests is identified as violation

280~281/89-24-03.

Unit 2

11H

11 Bus Special Testing

During the last week of this inspection period, the inspectors

witnessed performance of sel_ected portions of special tests 2-ST-238,

ESF Actuation wHh Instantane*ous UV - ,H Bus; and 2-ST-240, ESF

Actuation with Delayed UV (5 Min) - H Bus.

The purpose of the tests

was to verify loads sequencing onto the 2H electrical bus following

the injection of an ESF signal along with a simultaneous and a

delayed UV condition on the emergency bus.

The inspectors reviewed.

the official copy of the test procedures prior to performance of the

test. and witnessed the actual testing, including th~ actions of the

test directors. Testing was conducted in a satisfactory manner.

19

Within the areas *inspected, two violations were identified.

7.

Licensee Event Report Review (92700)

The inspector~ reviewed the LER's listed below to ascertain whether NRC

reporting requirements were being met and to determine appropriateness of,

the corrective actions. The inspector's review also included followup on

implementation of corrective actipn and review of licensee documentation

that all required corrective actions were complete.

LERs that identify

violations cif regulations and that meet the criteria of 10 CFR, Part 2,

Appe~dix C;Section V are identified as NCVs in the following closeout

paragraphs.

NCVs are considered firs.t-time occurre.nce violations which

meet the NRC Enforcement Policy for exemption from issuance of a Notice of

Violation.

These items are identified to allow for proper evaluations of

corrective actions in the event that similar events occ~r in the future.

(Closed) LER 280/88-07, Control/Relay Room Chillers Inoperable D_ue to

Inadequate Service Water Flow.

The issue involved tripping of one of the

subject chillers with a second chiller in a maintenance condition._ this

condition is contrary to TS 3.14.

The immediate corrective action

involved returning the chillir to service after manually adjuiting the SW

flow to the chiller condenser.

The manual adjustment was n*ecessary

because the normal

pressure control valves were out of servi~e.

Additional corrective actions included replacement of the SW pressure

control valv~s.

The inspector ~erified that the pr*ssyre control valves

had been replaced and that the system was operating satisfactorily. This

LER is closed.

8.

Allegation on Gai-tronics Communication Pa~ing Syste~ (RII !9~A-0056)

a.

Background:

b.

An anonymous individual, herein after referred to as the alleger,

contacted a Region II inspector on June 10, 1989, and reported that

50

percent of the

Gai-tronics

(paging/communication

system

throughout the plant) does not work, and that the trend over the last.

few yea~s has been to have more of the stations out of service.

Allegation Inspection:

The Gai-tronics system is a five channel public address and intercom

system.

The system is normally used in daily operational activities

to communicate messages between individuals in the station.

In the *

event of an emergency, the system is used to alert station personnel

of any abnormal occurrence or emergency situation and to communicate

emergency messages between individuals.

There are a total of four

communications systems, including Gai-tronics, that are used in the

station. The inspectors reviewed a number of work orders related to

the Gai-tronics system and the average number of days necessary to

complete these orders. A discussion with the head of the electrical

maintenance -group (group responsible for the maintenance on this

20

system) revealed that a problem does exist in maintaining the system.

Part of the problem is due to plant personnel stuffing rags in the

speakers*, *damaging the handsets, etc.

Currently, an effort is

underway to improve both the Gai-tronics and, the power telephone

systems .. A task group .is evaluatin*g locations for communications

units and state-of-the art improvements for the Gai-tronics system.

The task group will submit a report, along with recommendations, to

corporate management within ~he next three months.

c.

Conclusions:

Fifty percent of the Gai-tronics communication system being out of

order could not be substantiated.

However, the fact that problems

exist in maintaining the system*was admitted to by the licensee. The

  • licensee has a task group that is scheduled to sub~it ~o corporate

management within the next three months, a proposal for improving

this communication. system. This situation does not constitute an

immediate safety. concern nor is it a restart item for Unit 2.

However, this item is identified as IFI 280, 281/89-24-08, followup

on the licensee's review of internal station communication issues.

9.

Actio~ on ~reviou~ Inspecti6h Findings (92701)

(Closed)

URI

280/89-21-03,

Additional

review of reportability in

accordance with 10 CFR 50. 72 of two events which resulted in lass of

safety-related components.

The issues involved the tripping of the

control room air conditioning units, and the air binding of the charging

pump SW pumps.

The loss of the charging pump SW pumps resulted in the

charging pumps becoming technically inoperable.

Additional reviews by

the NRC concluded that these two events should have been reported in

accordance with 10 .CFR 50.72.

Since identification of the issue, the

licensee has redefined their reporting threshold. Therefore, the inspector

believes that this issue is resolved.

However, the item did identify a

weakness in the licensee's past process for determining reportability of

events in*accordance with 10 CFR 50.72.

10.

Exit Interview

The inspection scope and findings were summarized on September 5, 1989,

with those persons indicated in paragraph 1.

The inspectors described the

areas inspected and discussed in detail the inspection results listed

belo~.

The licens~e acknowledged the inspection findings with no dissent-

. ing comments.

The licensee did not identify as proprietary any of the

materials provideo to or reviewed by the inspectors during this

inspection.

The following violations were identified:

Failure to comply with the requirements of TS 3.0.1 with regards to the

action statement (paragraph 3.f(4), 280/89-24-01) .

. .

21

Failure to follow procedures as required by TS 6.4 when performing.

periodic test 1-PT-15.lC, involving the monthly operability test for the

turbine driven AFW pump (paragraph 6.a., 280/89-24-02).

Failure to test station batteries within the specified intervals as

required by TS 4.6.C (paragraph 6.b; *280, 281/89-24-03).

-In addition, apparent violations were identified for:

Failure of personnel to follow procedures regarding high radiation

area access requirements (paragraph .3.b).

This apparent violation

will be reviewed by the * NRC for appropriate enforcement action

(281/89-24-04).

.

Failure to take appropriate corrective action for past problems

identified during performance of maintenance activities (paragraph

5.a).

This apparent violation will be reviewed by the NRC for

appropriate enfor2ement ~ction (280, 281/89-24-05).

One !FI (paragraph 3.b) was identified for followup on licensee evaluation

of differences in dosimetry readout (280, 281/89-24-06).

One !FI (paragraph 5.b) was identified for followup on licensee review of

electrical contractor breaker overhaul practices (280, 281/89-24-07).

One !FI (paragraph 8) was identified for followup on the licensee's review

of internal statio~ communication iss~es (280, 281/89-24-08).

A weakness (paragraph 9) was noted in the l icensee 1 s process for

determining reportability of events as required by 10 CFR 50.72.

A strength (parag~aph 3.d) was noted regarding housekeeping and

cle*anliness conditions of the Unit 1 safeguards valve pit and pump pit

areas ..

11~

INDEX OF ACRONYMS AND INITIALISMS

AFW

ccw

CFR

cw

DCP

EMP

ESF

ESW

EWR

F

FT-LB

HP

HPES

AUXILIARY FEEDWATER

COMPONENT COOLING WATER

CODE OF FEDERAL REGULATIONS

CIRCULATING WATER

DESIGN CHANGE PACK.AGE

ELECTRICAL MAINTENANCE PROCEDURE

ENGINEERED SAFETY FEATURE

EMERGENCY SERVICE WATER

ENGINEERING WORK REQUEST

FAHRENHEIT

FOOT-POUND

HEALTH PHYSICS

HUMAN PERFORMANCE EVALUATION SYSTEM

-.

!

IA

IE

I FI

IR

JCO

LB

LCD

LER

MDV

MREM/HR

NCV

NRC

OP

PM

PORV

PSI

PSIG

PT

QA

QC ,

RCA

RCS

REM

RPM

RPS

RWP

SI

SNSOC

SRO

SSFI

SW

TLD

TS

. URI

UV

vs

22

INSTRUMENT AIR

INSPECTION AND ENFORCEMENT

INSPECTOR F.OLLOWUP ITEM

INSPECTION REPORT

JUSTIFICATION FOR CONTINUED OPERATION

POUND

LIMITING CONDITION FOR OPERATION

LICENSEE EVENT REPORT

MOTOR OPERATErr VALVE

MI LU REM/HOUR

NON-CITED VIOLATION

NUCLEAR REGULATORY COMMISSION

OPERATING PROCEDURE

PREVENTATIVE MAINTENANCE

POWER OPERATED RELIEF VALVE

POUNDS PER SQUARE INCH

POUNDS PER SQUARE INCH GAUGE

PERIODIC TEST

QUALITY ASSURANCE

QUALITY CONTROL

RADIOLOGICALLY CONTROLLED AREA

REACTOR COOLANT SYSTEM

ROENTGEN EQUIVALENT MAN

REVOLUTIONS PER MINUTE

REACTOR PROTECTION SYSTEM

RADIATION WORK PERMIT

SAFETY INJECTION

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

SELF-READIN~ DOSIMETER

SAFETY SYSTEM FUNCTIONAL INSPECTION

SERVICE WATER

THERMOLUMINESCENT DOSIMETER

TECHNICAL SPECIFICATIONS

UNRESOLVED ITEM

UNDERVOLTAGE

VENTILATION SYSTEM