ML18152A063

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Insp Repts 50-280/96-05 & 50-281/96-05 on 960505-0615. Violations Noted.Major Areas Inspected:Plant Operations, Maint,Engineering & Plant Support
ML18152A063
Person / Time
Site: Surry  Dominion icon.png
Issue date: 07/15/1996
From: Branch M, David Kern, Poertner W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A064 List:
References
50-280-96-05, 50-280-96-5, 50-281-96-05, 50-281-96-5, NUDOCS 9607230436
Download: ML18152A063 (33)


See also: IR 05000280/1996005

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.:

50-280/96-05 and 50-281/96-05

Licensee:

Virginia Electric and Power Company

Innsbrook Technical Center

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

May 5 through June 15, 1996

Inspectors:

Approved by:

D. M. Kern, Resident Inspector

W. K. Poertner, Resident Inspector

R. D. Gibbs (section 3.9)

F. N. Wright (section 5.0)

J. W. York (section 4.0)

P. ~~lo~~;;)

G. ~B"eisle~

Reactor Projects Branch 5

Division of Reactor Projects

SUMMARY

Scope:

7-/'J...-9'-r

Date Signe

This routine resident inspection was conducted on site in the areas of plant

operations which included plant status, draining the Unit 2 RCS to reactor

vessel flange level, POTT gas release to containment, Unit 2 reactor trip

during startup, Unit 2 restart, Unit 1 power reduction due to high sulfate

concentration in SGs, Unit 1 power reduction due to relay failure, inoperable

control room air handling units, inoperable charging pump service water pumps,

outage commitment review and open item followup review; maintenance which

included review of Unit 2 rod testing to satisfy NRC Bulletin 96-02,

replacement of Unit 2 Rod M-10 CROM rod travel housing, rod system testing for

DCP verification, RWST recirculation pump suction valve repairs, AAC diesel

generator testing, Unit 2 TDAFW pump operability testing, Unit 2 MG-6 relay

9607230436 960715

PDR

ADOCK 05000280

G

PDR

ENCLOSURE 2

2

failures, Unit 2 CW REJ replacements and maintenance program review;

engineering which included review of safety and oversight committee

activities, review of engineering documents, engineering interface with other

groups, problems with safety related batteries, problems with safety related

relays - type MG-6, 125 VDC system ground detection equipment, and 480 VAC

ground detection equipment, plant support which included occupation radiation

exposure control program changes, external and internal .exposure controls,

control of radioactive materials and contamination, surveys and monitoring,

maintaining occupational exposures ALARA, UFSAR review in the radiation

protection area; and review of UFSAR commitments.

Plant Operations

During the planned draindown of the Unit 2 RCS to reactor vessel flange level,

operator performance was judged to be good with excellent command and control

demonstrated.

Communication within the control room was also good.

However,

problems were encountered with the radio-phone used to communicate with the

operator in containment who was locally monitoring standpipe level* (paragraph

2. 2).

Failure to isolate relief valve 2-DG-RV-202 resulted in a PDTT gas release to

containment.

The failure to ensure that the system was aligned to support the

work order task requirements and failure to ensure that the equipment was

prepared for maintenance prior to approval of the work order is identified as

violation 50-281/96-05-01, Inadequate System Isolation (paragraph 2.3).

Steam dump and feedwater regulation valve control instrumentation design

requires operators to use manual control during r~actor startups and low power

operation.

Manual control has made SG level control during reactor startups a

highly challenging activity.

On ~une 6, Unit 2 tripped from 16 percent power

due to high B SG water level. Safety systems responded as designed.

Operators responded to the reactor trip in a safe and well controlled manner

(paragraph 2.4).

Evolution briefings and communications were good during the Unit 2 restart and

operator performance and supervisory oversight during the startup were

excellent. Several minor equipment problems were experjenced during the Unit

2 restart on June 7.

Operators responded promptly to each equipment problem

(paragraph 2.5).

A resin intrusion to the Unit 1 SGs forced a downpower to 30 percent reactor

power on June 7.

Immediate actions to reduce power level and to stop the

resin intrusion in addition to ongoing efforts to improve condensate polisher

operations demonstrated appropriate concern for SG integrity (paragraph 2.6).

Operations' decision to initiate a reactor shutdown after identification of a

failed RPS relay was a conservative decision based on available information.

The relay replacement and testing activity was well coordinated between

operations, maintenance, and the system engineer (paragraph 2.7).

Immediate corrective actions for inoperable main control room AHUs were

appropriate.

The operating crew demonstrated a good questioning attitude

3

by promptly identifying that the main control room AHUs were degraded

(paragraph 2.8).

Operators promptly responded to a low discharge pressure indication and

reestablished charging pump service water flow in an expeditious manner

(paragraph 2.9).

Unit 2 refueling outage commitments and items of regulatory interest were

completed during the Unit 2 refueling outage (paragraph 2.10).

Long term corrective actions associated with the violations associated with

the Unit 1 RCS draindown event described in NRC Inspection Reports Nos.

50-280/95-20 and 50-281/95-20 were completed prior to commencing the Unit 2

refueling outage (paragraph 2.11).

Maintenance

Technicians promptly diagnosed and replaced a failed rod control circuit card

during low power physics testing (paragraph 2.4).

Unit 2 control rod testing to satisfy NRC Bulletin 96-02 was conducted.

The

inspectors verified that test prerequisites and reactor plant conditions

including reactivity shutdown margin were properly established.

Communication

repeatbacks between technicians at the rod control cabinets and the test

coordinator were clear (paragraph 3.1).

Unit 2 control rod testing was performed in a professional manner and clearly

demonstrated RCCA operability prior to reactor startup from the refueling

outage (paragraph 3.1).

The licensee's corrective actions for control rod M-10 position indication

problems were satisfactorily completed (paragraph 3.2).

Control Rod System testing results for DCP verification met procedural

acceptance criteria (paragraph 3.3).

The work activity on the RWST recirculation pump suction valve was

accomplished in accordance with the work package requirements and the

maintenance activity was well coordinated to minimize the time that the freeze

seal was required to provide isolation for the work activity (paragraph 3.4).

Alternate AC Diesel Generator testing was performed in accordance with the

test procedure and good command and control was exhibited by the operators

conducting the procedure (paragraph 3.5).

Unit 2 turbine driven auxiliary feedwater pump testing was successfully

completed to satisfy TS and IST program requirements.

Operators were familiar

with the test procedures and communicated clearly. Mechanical problems

identified during the test were appropriately resolved (paragraph 3.6) .

4

The number of MG-6 relay failures during testing were high.

The licensee

continues their evaluation of the cause and potential reportability (paragraph

3.7).

Eight CW REJ were replaced during the Unit 2 refueling outage.

Work packages

for this maintenance were comprehensive (paragraph 3.8).

Maintenance personnel were well qualified for their positions, work areas were

orderly and well maintained, the plant material condition was excellent, and

procedures were clear and concise (paragraph 3.9).

Engineering

After a review of the meeting minutes for the MSRC for the period of January

through May 1996, the inspectors observed that the committee was successfully

performing the functions delineated in the committee's procedure (paragraph

4. I).

A continuing strength exists in the area of materials/metallurgical solutions

to corrosion, erosion problems identified at the site (paragraph 4.2).

During a review of engineering interface with other groups, the inspectors

concluded that there was an excellent interface between engineering and the

groups they supported (paragraph 4.3) .

No concerns were identified during review of station battery problems

(paragraph 4.4).

The licensee is reviewing MG-6 relay failures for potential reportability

pursuant to 10 CFR 21 (paragraph 4.5).

Design concerns were identified in the ground detection schemes for the 480

VAC Distribution System and the 125 VDC Distribution System.

Inspection

Followup Items were established to track these issues (paragraphs 4.6 and

4.7).

Plant Support

Radiation exposure control program changes reviewed were found acceptable

(paragraph 5.1).

The licensee was implementing adequate RP controls and monitoring individual

occupational radiation exposures in accordance with the requirements.

All

individual doses reported were within 10 CFR Part 20 limits (paragraph 5.2).

Overall, the licensee appeared to have a good contamination control program

(paragraph 5.3).

The licensee was utilizing ALARA techniques, developing challenging ALARA

goals and making progress in reducing collective doses for the staff

(paragraph 5.4) .

5

Review of the UFSAR with respect to radiation protection did not identify any

discrepancies (paragraph 5.5).

LER 50-281/96-002 was closed (paragraph 5.6) .

REPORT DETAILS

Acronyms used in this report are defined in paragraph 9.0.

1.0

PERSONS CONTACTED

Licensee Employees

  • Benthall, W., Supervisor, Procedures
  • Blount, R., Superintendent of Maintenance

Christian, D., Station Manager

  • Cramer, R., Maintenance

Crist, M., Superintendent of Operations

  • Erickson, D., Superintendent of Radiation Protection
  • Hayes, D., Supervisor, Administrative Services
  • Lovett, C., Supervisor, Licensing
  • McCarthy, J., Assistant Station Manager, Operations & Maintenance
  • Meekins, A., Supervisor, Construction Engineering
  • Sowers, T., Superintendent of Engineering
  • Stanley, B., Nuclear Oversight

Other licensee employees contacted included plant managers and

supervisors, operators, engineers, technicians, mechanics, security

force members, and office personnel.

2.0

PLANT OPERATIONS (40500, 71707, 92700)

The inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operational safety and

compliance with TSs and to maintain overall facility operational

awareness.

Instrumentation and ECCS lineups were periodically reviewed

from control room indications to assess operability.

Frequent plant

tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping.

Deviation reports were reviewed to assure that potential

safety concerns were properly addressed and reported.

2.1

Plant Status

Unit 1 operated at power the entire reporting period.

On June 7 power

was reduced to less than 30 percent due to high sulfate concentrations

in the steam generators (paragraph 2.6).

The unit returned to 100

percent power on June 8.

On June 11 a reactor shutdown required by TSs

was initiated due to a failed relay (paragraph 2.7).

The power

reduction was stopped at 58 percent when the relay was replaced and

tested.

The unit was returned to 100 percent power later that same day.

Unit 2 began the period shutdown for refueling.

Entire core offload was

completed on May 13.

Core reload was completed on May 26, *and the head

was set on May 27.

A reactor trip occurred on June 6 prior to placing

2

~

the generator online {paragraph 2.4).

The unit was returned to service

on June 7 and obtained 100 percent power on June 10 (paragraph 2.5).

2.2

Draining the Unit 2 RCS to Reactor Vessel Flange Level

On May 7, the inspectors witnessed draining of the RCS from

approximately 22 percent in the PZR to a level just below the reactor

vessel flange.

This draining was part of the refueling evolutions

necessary to remove the reactor head.

During previous RCS draining

evolutions, problems had been noted associated with verification of

actual RCS level.

As required by procedure 2-0P-RC-004, Draining The

RCS To Reactor Flange Level, revision 9, two cold calibrated PZR level

transmitters were used for the initial RCS level indication while level

was still in the PZR.

During the draindown the licensee utilized

several methods to verify level changes in the RCS.

Portions of the

RVLIS were maintained functional for trending purposes only.

Additionally, the inventory balance used a temporary recorder to more

accurately measure BRT level changes.

The reactor vessel level

standpipe performed as designed and there was good agreement between

local indication and CR standpipe indication.

The inspectors observed that normal operator staffing was augmented

which allowed the operator in charge to concentrate on the task at hand.

Operator performance was judged to be good with excellent command and

control demonstrated.

Communication within the CR was also good.

However, problems were encountered with the radio-phone used to

communicate with the operator in containment who was locally monitoring

standpipe level. These observations were discussed with operations

management.

The following day the inspectors monitored additional

radio-phone communication between the CR and containment and noted

improvements.

2.3

POTT Gas Release to Containment

On May 18 at 10:22 a.m., the ventilation vent vent radiation monitors

went into alert and the operator noticed that overhead gas pressure had

decreased by approximately 2 psi.

At 10:27 a.m. the operator isolated

the POTT from the overhead gas header and terminated the release to the

Unit 2 containment atmosphere.

The operators determined that the

release path was through relief valve 2-DG-RV-202 that had been removed

from the system to perform setpoint testing.

When the valve discharge

flange had been disconnected a vent path to containment was established

from the overhead gas header through the POTT.

The calculated release

was a small fraction of TS allowable limits (less than 12 percent).

The inspectors reviewed the work order and tagout associated with the

maintenance activity.

The relief valve was removed by WO 00334395, Test

RV 2-DG-RV-202.

The WO referenced tagging reports 2-96-CH-0067, 2-96-

RC-004, 2-96-RC-008, and 2-96-RC-0010.

The inspectors determined that

the tagouts referenced did not establish an adequate isolation boundary

to perform the maintenance activity.

VPAP-2002 section 5.7 requires the

Shift Supervisor to align systems to support work activities and

3

equipment be prepared for maintenance prior ta WO approval.

The failure

to ensure that the system was aligned to support the work order task

requirements and failure to ensure that the equipment was prepared for

maintenance prior to approval of the work order is identified as

violation 50-281/96-05-01, Inadequate System Isolation. Specifically,

the Shift Supervisor failed to ensure that relief valve 2-DG-RV-202 was

isolated from the overhead gas header.

2.4

Unit 2 Reactor Trip During Startup.

Reactor startup was performed on June 5 following completion of RFO 13.

The inspectors noted that individual responsibilities and startup

activities were thoroughly discussed during the pre-evolution control

room brief.

The unit achieved criticality at 5:56 p.m. on June 5 and

commenced low power physics testing.

On June 6, Shutdown Bank A Group 2 control rods failed to withdraw

during low power physics testing.

I&C technicians quickly determined

that the lift phase card for the affected group had failed.

The

inspectors monitored troubleshooting and repair activities.

Communications between operations and maintenance personnel were precise

and the failed circuit card was promptly replaced.

Low power physics testing and turbine checks were successfully

completed.

The inspectors continued to monitor reactor operations from

the control room as operators prepared to connect the Unit 2 main

generator to the off-site power distribution grid. Surry control

systems require operators to maintain manual steam dump and feedwater

regulation valve control while at low power levels. This is a

challenging activity which requires close coordination between several

operators to maintain SG water levels within the desired band as steam

flow rate changes.

At about 15 percent reactor power the SG steam flow

rates began oscillating and operators had difficulty adjusting feedwater

flowrate sufficiently to compensate for SG level swell.

At 11:45 p.m.

the reactor tripped from approximately 16 percent power due to high B SG

water level.

Safety systems responded as designed and the unit was

stabilized in a hot shutdown condition.

The Unit 2 SRO maintained good

direction and control of recovery activities.

The inspectors concluded

that operators responded to the reactor trip in a safe and well

controlled manner.

The post trip review confirmed that SG steam flow oscillations had

developed and that the B SG had swelled to the high level turbine trip

setpoint. Technicians determined that the B feedwater regulation valve

bypass valve (2-FW-HCV-255B) had failed to fully close when operators

attempted to reduce B SG level prior to the trip. This valve

malfunction and other minor equipment problems were corrected prior to

the June 7 reactor restart.

The inspectors determined that the post

trip review evaluated the trip and prerequisites for restart in

appropriate detail.

Station management informed the inspectors that

feedwater control system modifications were being considered to improve

SG level control at low power levels.

4

2.5

Unit 2 Restart

2.6

Reactor startup, following the post trip review, was performed on

June 7.

The shift supervisor clearly discussed the previous reactor

trip and stressed the fact that there were no time constraints on the

reactor startup.

The inspectors monitored startup activities to

evaluate equipment and operator performance.

Evolution briefings and

communications during the startup were good.

The main turbine D reheater intercept valve (2IR) failed to open during

turbine startup testing. Mechanics disassembled the hydraulic actuator

and identified a deteriorating o-ring which may have blocked control oil

flow.

The inspectors observed the actuator disassembly and noted that

foreign material exclusion controls were good.

Theo-ring was replaced

and intercept valve 2IR was successfully retested.

Maintenance

personnel informed the inspectors that they would review the PM scope

for these hydraulic actuators based on the degraded o-ring.

The

inspectors concluded that intercept valve 2IR corrective maintenance was

performed in a timely and high quality manner.

Several minor equipment problems emerged during the startup.

One of the

two generator output breakers (OCB-G-202) failed to close when placing

the generator on-line.

Steam dumps began to drift open beyond the

desired position without operator demand while in manual control.

B SG

feedwater regulation valve response was sluggish, requiring operators to

maintain the valve in manual control until the unit was at approximately

30 percent power.

Operators responded promptly to each equipment

problem.

The inspectors concluded that operator performance and

supervisory oversight during the startup were excellent.

Unit 2 was

placed on-line at 9:34 p.m. on June 7, ending a 36 day refueling outage.

The unit achieved 100 percent power on June 10.

Unit 1 Power Reduction Due to High Sulfate Concentration in SGs

On June 7, resin from the condensate polishing system passed by the

system strainer causing elevated Unit 1 SG sulfate levels. All three

generators exceeded the vendor specified Action Level II limit (100

ppb).

Operators reduced reactor power to 30 percent as required by the

vendor until sulfate levels were returned below 20 ppb.

Sulfate levels

returned to allowable values at 7:12 a.m. on June 8, and a power

increase to 100 percent was commenced.

The unit was returned to 100

percent at 6:38 p.m. that same day.

The inspectors have noted that the

licensee has recently increased their sensitivity to SG chemistry

quality and has a low threshold for initiating associated DRs.

The

inspectors concluded that immediate actions to reduce power level and to

stop the resin intrusion in addition to ongoing efforts to improve

condensate polisher operations demonstrated appropriate concern for SG

integrity.

The licensee initiated a category 2 RCE to investigate the

resin intrusion .

2.7

2.8

5

Unit 1 Power Reduction Due to Relay Failure

On June 11 at 11:23 a.m., Unit 1 commenced a reactor shutdown to hot

shutdown in accordance with TS 3.7 due to a failed relay in the reactor

protection system circuitry.

Relay 1-RP-RLY-TTXA failed to reenergize

and smoke was detected in the relay cabinet during RPS system testing.

At the time of the relay failure the A main reactor trip breaker was

open and the A reactor trip bypass breaker was closed to allow testing.

TS Table 3-7.1 item 18, reactor trip breakers, allows one reactor trip

breaker to be bypassed for two hours for surveillance testing.

The

operating crew did not want to reclose the A reactor trip breaker based

on the failure of the relay and entered a six-hour action statement to

hot shutdown.

The relay was replaced, tested, the A reactor trip

breaker was reclosed and the bypass breaker reopened at 1:20 p.m. with

the unit at 58 percent power.

A power increase to 100 percent power was

commenced at 1:26 p.m. and the unit was returned to 100 percent power at

3:39 p.m.

The inspectors monitored portions of the power reduction and return to

100 percent power operation and verified that the appropriate

notifications were made to the NRC.

The inspectors also observed

replacement and testing of the failed relay by maintenance personnel.

The inspectors determined that operations' decision to initiate a

reactor shutdown was a conservative decision based on available

information.

The relay replacement and testing activity was well

coordinated between operations, maintenance, and the system engineer.

Inoperable Control Room Air Handling Units

At 5:05 a.m. on May 13, control room AHU 1-VS-AC-2 was secured and

control room AHU 1-VS-AC-l was started to support testing of the main

control room chiller 4C service water pump.

When AHU 1-VS-AC-l was

started the operators noticed that the ventilation noise level in the

control room was abnormally low.

Investigation by the operating crew

determined that the filter and coil differential pressure was below the

allowable value of 0.16 inches H20 indicating reduced flow through the

AHU.

AHU 1-VS-AC-l was declared inoperable which initiated a seven-day

TS action statement in accordance with TS 3.23 and control room AHU 1-

VS-AC-2 was restarted.

When AHU 1-VS-AC-2 was restarted ventilation

noise and flow were determined to be lower than when AHU 1-VS-AC-l was

in service and the filter and coil differential pressure did not meet

the minimum acceptable value of 0.16 inches H20 when checked by the

operators.

At 5:15 a.m., main control room AHU 1-VS-AC-2 was declared

inoperable making both Unit 1 ma~n control room AHUs inoperable.

TS 3.23 does not address the inoperability of both AHUs and the operators

entered a six-hour action statement to hot shutdown in accordance with

TS 3.0.1.

The HVAC maintenance crew and system engineer were contacted to

troubleshoot the AHUs.

Initial troubleshooting efforts focussed on

potential blockage of the supply ductwork.

No blockage was identified .

6

Subsequent troubleshooting identified that the counterweight arms on the

AHU backdraft dampers were out of position.

The counterweight arm for

l-VS-AC-2 was returned to the proper position and filter and coil DP

returned to normal.

Ventilation flow was verified using an anemometer

and the AHU was declared operable at 8:21 a.m. exiting TS 3.0.1 and

entering a seven-day action statement in accordance with TS 3.23.

The

counterweight arm for main control room AHU 1-VS-AC-l was repositioned

and the AHU was declared operable at 4:09 p.m.

The inspectors reviewed the TS requirements and monitored licensee

troubleshooting efforts.

The licensee initiated a root cause evaluation

to determine the cause of the failures and will issue a LER describing

this event and corrective actions to prevent recurrence.

The inspectors

determined that the licensee immediate corrective actions were

appropriate and that the operating crew demonstrated a good questioning

attitude by promptly identifying that the Unit 1 main control room AHUs

were degraded.

2.9

Inoperable Charging Pump Service Water Pumps

At approximately 1:51 a.m. on May 6 a charging pump service water low

pressure alarm was received in the Unit 2 control room.

At the time of

the event, Unit 2 was in cold shutdown and the charging pump service

water system was not required to be operable.

At approximately 1:55

a.m. a charging pump service water pump low pressure alarm was received

in the Unit 1 control room.

The operators verified that the standby

service water pumps auto started, however, discharge pressure did not

return to normal.

The operators declared both flowpaths to the charging

pump service water pumps inoperable, immediately responded to the MER

and vented service water pump 1-SW-P-lOA.

After venting air from the

system, pump discharge pressure returned to normal and service water

pump 1-SW-P-lOA was declared operable at 1:56 a.m.

Unit 1 service water

pump 1-SW-P-lOB was vented and returned to service at 2:19 a.m.

returning both Unit 1 charging pump service water pumps to service.

During the approximate one minute time period that both Unit 1 service

water flowpaths were inoperable, Unit 1 was in a six-hour action

statement to hot shutdown in accordance with TS 3.0.1. Charging pump

temperatures remained within allowable values throughout the event.

Charging pump bearing temperatures only increased approximately

4 degrees fahrenheit.

The Unit 2 charging pump service water pumps were

also vented and both pumps were returned to service at 2:30 a.m.

The licensee initiated a Category 1 Root Cause Evaluation to determine

the cause of the air intrusion into the charging pump service water

system.

The licensee determined that the air was the result of divers

previously working in the Unit 2 A high level intake structure 96-inch

and 48-inch CW and SW lines.

The divers had been performing a PM to

clean the piping of marine growth.

The air exhaled by the divers

accumulated in the piping and when valve 2-SW-MOV-201B was opened for

testing, air was transported to the suction of the charging pump service

water pumps.

Previous cleaning evolutions had been accomplished with

the high level intake structure isolated and drained.

The inspectors

i

I

--


7

reviewed the event and discussed the issue with operations and station

management.

The licensee plans to develop a procedure that addresses

the use of divers to clean station piping and develop an Operations

Checklist to control manipulation of service water during periods of

high maintenance activity.

The inspectors determined that the operators

promptly responded to the low pressure indication and reestablished

charging pump service water flow in an expeditious manner.

Licensee

actions to strengthen control of maintenance activities in the CW and SW

systems were appropriate.

2.10 Outage Commitment Review

Prior to Unit 2 startup following refueling, the inspectors reviewed the

status of licensee's actions to meet commitments related to the

refueling outage.

The inspectors verified that the work was completed

to meet the following commitments and items of regulatory interest:

AAC diesel connection to Unit 2.

The licensee completed

installation and testing of the AAC diesel during the refueling

outage.

Testing of the AAC diesel is discussed further in

paragraph 3.5.

Flow test recirculation spray heat exchangers.

The licensee

performed procedure 2-0SP-SW-007, Service Water Flow Test of

Recirculation Spray Heat Exchangers 2-RS-E-IA and 2-RS-E-ID,

revision 0, to establish service water flow through the RSHX.

Replace SG alloy 600 tube plug.

The licensee reolaced the alloy

600 tube plug in the A SG cold leg.

Rod control system surveillance testing.

rod control system surveillance testing.

further in paragraph 3.3.

The licensee completed

This item is discussed

Implement corrective actions for RCS draindown event. The licensee

completed the corrective actions discussed in the response to EA 95-223 prior to commencing the Unit 2 refueling outage.

This item

is discussed further in paragraph 2.11.

Revise GOP I.I to reference GL 95-07.

The licensee revised GOP

1.1 to reference GL 95-07 prior to restart of Unit 2.

Visual inspections of pressurizer instrument nozzles.

The

licensee and inspectors performed visual inspections of the

instrument nozzles and verified that no indication of leakage was

present.

Replace one recirculation spray heat exchanger MOV.

The licensee

replaced valve 2-SW-MOV-205A using DCP 96-006.

Develop procedure for controlling reactor vessel head vent valves .

The licensee developed procedure 2-0P-RC-013, Reactor Head Vent

8

And Standpipe Operations, revision 1, to control the reactor

vessel head vent valves.

This procedure was implemented prior to

commencing the Unit 2 RFO.

Resolve conflicting numbers between minimum time allowed for

defueling.

The licensee revised the UFSAR to resolve the

conflicting time requirements for core offload. The inspectors

verified that core offload did not commence prior to the most

conservative time referenced in the UFSAR prior to revision.

Expansion joint replacement.

The licensee replaced the Unit 2

circulating water expansion joints. This item is discussed

further in paragraph 3.8.

Control rod M-10 repairs.

The licensee replaced the CROM rod

travel housing.

This item is discussed further in paragraph 3.2.

Control rod testing.

The licensee performed rod drop time. testing

during the unit shutdown, and rod drag testing during the defueled

maintenance window.

This item is discussed further in paragraph

3.1.

2.11

Open Item Followup Review (Operations)

(Closed) EA 95-223: 01013, 01023 and 01033, RCS Draindown Event

Violations.

During the Fall 1995 Unit 1 RFO, several problems occurred during the

RCS draindown for removal of the reactor vessel head.

NRC Inspection

Report Nos. 50-280/95-20 and 50-281/95-20 documented this event and

escalated enforcement was taken.

The licensee's short term corrective

actions associated with this item included increased management

ovfrsight, station management meetings with operations personnel and

STAs to clarify and reinforce management expectations, additional

training of operators and STAi and procedure revisions to provide

additional control of shutdown activities. These corrective action

items were reviewed by the inspectors and were found to be acceptable.

Long term corrective actions included implementation of more detailed

operations standards, performance of an operations configuration control

assessment, implementation of an outage controlling procedure to

integrate and better control outage activities, and continued training

programs for operations personnel and STAs.

The inspectors reviewed the licensee long term corrective actions and

verified that they had been adequately accomplished to support the

Unit 2 refueling outage.

One violation was identified .

9

3.0

MAINTENANCE (61726, 62700, 627n1, 90712, 92902)

3.1

During the reporting period, the inspectors reviewed the following

maintenance and surveillance activities to assure compliance with the

appropriate procedures and TS requirements.

Review of Unit 2 Rod Testing to Satisfy NRC Bulletin 96-02

The inspectors reviewed the recorder traces for the as-found rod drop

testing that was committed to as part of the licensee's response to NRC

Bulletin 96-02.

The test was performed on May 3 after the unit shutdown

for refueling with the unit at NOT and NOP conditions.

Procedure 2-NPT-

RX-014, Hot Rod Drops by Bank, revision 2, was used to control testing.

The inspectors verified that rod drop times were within TS allowable

values.

The traces clearly indicated dashpot entry.

However, because

of equipment sensitivity and signal strength it was difficult to

determine ~ctual rod bottoming.

The inspectors along with the reactor

engineer did however note a slight trace disturbance following the

voltage decay after dashpot entry.

Per procedure 2-NPT-RX-014 this

disturbance is indicative of the rod bouncing on the bottom.

This

bouncing was verified on all rods except rod F-10 for which the

inspectors were unable to see the slight trace disturbance.

However,

two reactor engineers who routinely perform this type of testing

indicated, that although extremely difficult to observe, rod bouncing

did occur.

The inspectors accepted their position .

The second part of as-found rod testing was a rod drag test that was

performed in the spent fuel pool.

This testing was performed per

procedure STD-FP-1996-7751, Surry RCCA and Fuel Assembly Examination

Field Procedure, revision 0.

On May 31, the inspectors reviewed data

collected for the rod drag test. Westinghouse had performed the testing

under contract to Surry and the acceptance criteria was vendor supplied.

The inspectors' review of the data indicated that tw9 of the 48 rods

exhibited an upper guide tube drag force greater than the 40 lbs.

specified in the procedure.

Both assemblies had a burnup of

approximately 40,000 MWD/MTU and neither were planned to be reused for

future cycle core configurations.

The core locations where these two

assemblies had been discharged from were D-6 and H-10.

In addition to

the 48 RCCAs tested, Westinghouse used the dummy RCCA to drag test

several other high burnup assemblies that had been previously discharged

to the spent fuel pool.

Based on the inspectors' review of the data provided and in consultation

with the licensee's NAF personnel there appears to be a correlation

between fuel burnup and guide tube drag forces even in the 15Xl5 fuel

assemblies.

The final review and analysis of the licensee's data will

be conducted by NRR as part of Bulletin 96-02 review and closure

process.

On June 4, technicians performed 2-NPT-RX-014 to confirm Unit 2 RCCA

operability following the refueling outage.

The inspectors verified

that test prerequisites and reactor plant conditions including shutdown

10

margin were properly established. Communication repeatbacks between

technicians at the rod control cabinets and the test coordinator were

clear. All test connections were double verified prior to measuring rod

drop times.

The inspectors independently reviewed the recorded rod drop

traces. All control rod drop times were consistent and satisfied TS

requirements.

Each trace indicated bottom bounce which demonstrated

that the RCCA fully inserted and there was no indication of an unlatched

control rod.

The inspectors concluded that control rod testing was

performed in a professional manner and clearly demonstrated RCCA

operability prior to reactor startup from the refueling outage.

3.2

Replacement of Unit 2 Rod M-10 CROM Rod Travel Housing

During the Unit 2 RFO the licensee replaced the CROM Rod Travel Housing

for rod.M-10.

This replacement was another step in the licensee

attempts to correct a rod position indication problem for rod M-10.

The

licensee along with their CROM and IRPI vendor had determined that

housing magnetism might have been the cause of previous indication

problems.

The inspectors reviewed the licensee CROM housing replacement

activities.

Work was performed by Westinghouse and was accomplished

while the reactor head was stored on its stand for refueling activities.

Work was controlled by WO 00335120-01.

Rod exercise and drop time

testing along with system pressure testing of the housing were performed

to verify rod operability.

The inspectors verified that the licensee's

corrective actions for control rod M-10 position indication problems

were satisfactorily completed.

3.3

Rod System Testing for DCP Verification

During the RFO the licensee implemented DCP 94-073 to modify and correct

a rod control system timing problem that occurred at another facility.

The licensee committed to modify the system in their response to NRC GL 93-04.

This modification involved re~sitioning diodes on the Slave

Cycler Decoder cards in the Rod Control System logic cabinets.

Rod

motion was controlled by procedure 2-NSP-RX-014, Rod Exercise Test,

revision 2.

This procedure referenced SNSOC approved Westinghouse

procedure O-NSD-EIS-95-047, CROM Timing Modification and Verification

Testing Vendor Procedure, revision 0, for sequencing and timing test of

the stationary, movable, and lift coils.

On June 2, the inspectors

monitored testing of CB A and C rods.

The recorder traces were reviewed

against a sample trace contained in the procedure.

The traces were

similar to the sample provided in the procedure.

The procedure allowed

variances between the actual and sample traces to account for electrical

noise and signal strength. Test results met procedural acceptance

criteria. During the test one !RPI failed and three of the eight step

counters did not exhibit good audible indication.

WOs and a DR were

written to track and correct the problems.

11

3.4

RWST Recirculation Pump Suction Valve Repairs

During the inspection period the inspectors observed corrective

maintenance activities associated with valve 2CS-27.

This valve is the

RWST recirculation pump suction header isolation valve.

The maintenance

activity consisted of establishing a freeze seal and replacing the valve

bonnet assembly due to problems with the spindle position indicator.

The work activity was accomplished in accordance with WO 00333229, RWP

96-2025, and procedure O-MCM-0402-01, Grinnell Diaphram Valve Removal,

Replacement, and Overhaul, revision 3.

The inspectors reviewed the WO,

RWP, system tagout, and monitored maintenance activities in progress.

The inspectors also verified that the freeze seal was properly*

established prior to commencing valve maintenance activity.

During the

installation of the replacement bonnet assembly the spindle separated.

The licensee installed a new diaphragm in the valve and reassembled the

valve using the old valve bonnet.

The work activity was accomplished in

accordance with the work package requirements and the maintenance

activity was well coordinated to minimize the time that the freeze seal

was required to provide isolatiQn for the work activity.

3.5

AAC Diesel Generator Testing

3.6

During the Unit 2 refueling outage the licensee completed the electrical

connection of the AAC diesel to Unit 2.

The AAC diesel generator

provides the power source for onsite electrical loads during SBO

conditions.

The inspectors observed the performance of Final Design

Test Procedure FDTP-92-052-3-9, AAC Diesel Generator Installation E

Transfer Bus Tie, revision 0.

This procedure coordinated and performed

the post modification testing to verify proper operation of the AAC

diesel generator after connection to the E transfer bus.

The procedure

verified proper phasing, governor and excitation controls during

parallel system operation, diesel auto start and proper breaker

operation during a SBO signal, proper bus voltage when a large motor

load was connected, and the ability to recover normal offsite power

following a SBO.

The inspectors reviewed the test procedure and verified that the test

acceptance criteria was met.

The test was performed in accordance with

the test procedure and good command and control was exhibited by the

operators conducting the procedure.

No problems were encountered during

the performance of the functional testing.

Unit 2 TDAFW Pump Operability Testing

Mechanics replaced the TDAFW pump governor stem and repaired the TDAFW

pump B steam supply isolation valve during the RFO.

The inspectors

observed TDAFW pump testing on June 6 to verify operability prior to the

reactor achieving 10 percent power.

Procedures 2-0PT-FW-003, TDAFW Pump

2-FW-P-2, revision 6-Pl, and 2-0PT-FW-007, TDAFW Pump Steam Supply Line

Check Valve Test, revision 3, were successfully completed to satisfy TS

and ISI program requirements.

The inspectors noted that operators were

familiar with the procedure and communicated clearly during the test.

.
.. *,.;,",

12

Check Valve Test, revision 3, were successfully completed to satisfy TS

and ISI program requirements.

The inspectors noted that operators were

familiar with the procedure and communicated clearly during the test.

Two equipment discrepancies were identified during the testing.

The

TDAFW pump failed to achieve rated speed on the first attempt.

Operators secured the turbine and determined that the governor speed

adjust control had been left at the low speed setpoint following outage

maintenance.

The speed adjust control was repositioned to the normal

full speed setpoint and the test was run successfully on the second

attempt.

The second discrepancy was that the B steam line supply

isolation valve (2-MS-120) stuck in the open position. Operators

subsequently freed the valve to complete the check valve 1ST.

The

inspectors discussed both discrepancies with the maintenance division

manager and verified that appropriate corrective action was initiated to

preclude recurrence.

3.7

Unit 2 MG-6 Relay Failures

During TS bus logic testing per procedure 2-0PT-ZZ-002, ESF Actuation

With Undervoltage And Degraded Voltage - 2J Bus, revision 6, several

MG-6 relays failed to perform properly.

DRs S-96-0899 and S-96-0922

documented these failures. Three of the failed relays were reported to

be original equipment and failed because of unsatisfactory resistance

across the contacts. These three relays were replaced and subsequently

tested satisfactorily.

Two other relays that failed had been installed in 1993 and 1995.

Both

of the relays electrically energized to actuate but failed to latch

(i.e. mechanically hold in the correct position) during the test. These

relays were 2-SI-REL-SIA-B, the SI master relay, and 2-SI-REL-F2-B, a B

train feedwater isolation relay.

The relays were replaced and the logic

was successfully tested. These relay failures are discussed further in

paragraph 4.5.

The failure of 5 of 16 MG-6 relays during logic testing

was considered high.

3.8

Unit 2 CW REJ Replacements

3.9

Eight CW REJs were replaced due to reaching the end of their vendor

specified service life during the Unit 2 RFO.

This maintenance was

added to the outage work scope just prior to beginning the RFO.

The

inspectors verified that all eight CW REJ replacements were completed

and reviewed selected completed work packages.

The work packages were

comprehensive and included good consideration for turbine building

flooding precautions.

Maintenance Program Review

The inspectors conducted interviews with the Maintenance Superintendent,

his lead supervisor in maintenance engineering, and discipline

supervisors in mechanical, electrical, and instrumentation and controls .

Each of these interviews focussed on the background and training of each

13

individual, and general responsibilities in their current positions.

In

addition, the interview with the Mainte~ance Superintendent included a

review of the organization and staffing of the Maintenance Department,

and a review of the quality indicators used to track maintenance

performance.

During this interview, it was learned that the Maintenance

Department is currently staffed with approximately 200 people organized

into the three trade disciplines, maintenance engineering, and a support

group which performs the equipment predictive analysis .function.

Interviews with the discipline supervisors also included tours of each

work area, tool rooms and material storage areas.

The inspectors

observed that all of the work areas were clean and orderly. All

calibrated equipment observed by the inspectors in the work areas was

noted to be within the required calibration due date, and materials

stored in these areas was properly identified and protected.

The

following Quality Indicators involving maintenance performance were

reviewed by the inspectors during the inspection:

Quarterly Deviation Trend Reports for 3Q95, 4Q95, and 1Q96

April 1996 Work Process Production Indicators

Virginia Power Nuclear Business Plan Goal Performance (December

1995):

Total Work Order Backlog

Non-outage Corrective Maintenance Backlog

Work Order Rework

Work Orders Completed Not Closed

Actual/Planned Outage Schedule

Maintenance Rule SSCs in (a)(l)

Safety System Failures (Maintenance Related Issues)

EOG Reliability (Maintenance Related Issues)

EDG Unavailability (Maintenance Related Issues)

HHSI Unavailability (Maintenance Related Issues)

LHSI Unavailability (Maintenance Related Issues)

Containment/Quench Spray System Unavailability (Maintenance

Related Issues)

Recirculating Spray System Unavailability (Maintenance Related

Issues)

AFW System Unavailability (Maintenance Related Issues)

RHR System Unavailability (Maintenance Related Issues)

SALP Rating (Maintenance Related Issues)

Regulatory Performance Indicator (Maintenance Related Issues)

Licensee Event Reports (Maintenance Related Issues)

NRC Violations (Maintenance Related Issues)

Forced Outage Rate by Unit (Maintenance Related Issues)

Reactor Trips (Maintenance Related Issues)

The inspectors conducted a general plant tour and reviewed several key

administrative procedures which control the maintenance program.

The

plant tour included the control room, Turbine Building, and the

Auxiliary Building.

Areas observed by the inspector were noted to be in

excellent condition.

The procedures reviewed during the inspection were:

14

VPAP-0801, Maintenance Program, revision 5

VPAP-0802, Maintenance History Program, revision 2

VPAP-0803, Preventative Maintenance Program, revision 5

VPAP-0804, Safety and Relief Valve Program, revision 4

VPAP-0805, Motor Operated Valve Program, revision 5

VPAP-0812, Station Lubrication Program, revision 2

VPAP-2002, Work Requests and Work Order Tasks, revision 5

All areas reviewed during this inspection provided a favorable

impression of the overall maintenance program at Surry.

Personnel

appeared to be well qualified for their positions, work areas were

orderly and well maintained, the plant material condition was excellent,

and procedures were clear and concise.

No violations or deviations were identified.

4.0 * ENGINEERING REVIEW (37551, 37550)

4.1

Review of Safety and Oversight Committee Activities

The inspectors reviewed activities of two of the safety committees,

i.e., the on site SNSOC and the off site MSRC.

The inspectors attended the SNSOC meeting that involved a review of

SE 96-0084, revision 1, and JCO No. S2-96-002.

These documents

concerned the Unit 2 main control room annunciators being taken out of

service to replace the power supplies.

It was observed that the meeting

was well conducted and involved very extensive and detailed discussions

by the members involved.

The replacement of the power supplies was

successfully completed the week of June 3-7.

A review of all the meeting minutes for the MSRC was conducted for the

period January-May, 1996.

The inspectors observed that the committee

was successfully performing the functions delineated in the committee's

procedure.

4.2

Review of Engineering Documents

The inspectors reviewed four DRs, five SEs, two JCOs, and three

modification packages.

These documents covered activities dealing with

a leak in the RHR System, erosion/corrosion of a FW pipe, improper

installation of a valve, a relay problem, and a modification of

radiation monitoring equipment.

The inspectors examined the areas involving the repair and replacement

of the leaking RHR piping and the repair/replacement of a portion of the

15

FW p1p1ng due to erosion/corrosion. A through-wall leak in a Unit 2

six-inch diameter RHR pipe adjacent to a saddle weld for a support

resulted in a shutdown of the unit for repairs.

The metallurgical failure analysis of the piping and the repair and

replacement activities displayed a through understanding of this

engineering discipline. Another example of this continuing strength

(had been noticed in previous inspections in this area) was the repair

and subsequent replacement of a section of the FW piping.

The SEs, dispositions of DRs, and JCOs reviewed by the inspectors were

good.

A continuing strength exists in the area of

materials/metallurgical solutions to corrosion, erosion problems

identified at the site.

4.3

Engineering Interface With Other Groups

4.4

The inspectors attended several meetings and had discussions with

engineering personnel to determine the extent of interfacing with other

groups.

The inspectors attended a safety committee meeting, a Unit 2 outage

meeting, and a daily meeting of the engineering group.

The engineering

group participated well with the other groups and readily accepted

requests for additional assistance. A member from operations attended

and participated in the daily engineering meeting.

Discussions with the

engineering manager revealed that he assigned one of the two system

engineering managers to attend the daily maintenance meeting to

determine if additional engineering assistance was needed on any

maintenance project.

The inspectors concluded that there was an

excellent interface between engineering and the groups they supported.

Problems with Safety-Related Batteries

In 1989, the licensee and the NRC became aware that the safety-related

vital batteries were experiencing problems that appeared to be the

result of manufacturing defects.

These batteries were manufactured by

Exide, and the cell design was designated as 2GN-23.

They were flooded

cell type with lead calcium plates.

The 2 prefix indicated that two

cells were in one jar.

The inspection scope was to review the specific

circumstances and resolving corrective actions.

Inspection activities

included:

Discussions with the system engineer for the batteries.

Review of laboratory analysis reports on failed or weak cells.

Examination of the installed batteries .

16

Review of an engineering study ET NO. CEE-94-063, Evaluation of

Cell Jumpering, dated October 27, 1994.

Review of capacity tests results for the batteries.

The Train B batteries for both units were installed in 1986.

The date

code stamp affixed to the cells were 8603R and 8607R.

These batteries

have not experienced a problem except for cells 51 and 52 (same jar) in

the 2B battery which had voltage at the low end of the acceptable range.

The jar was replaced in January 1989 and again in May 1991.

Currently,

the voltage of those cells remains the lowest in the lineup, but is not

trending down.

The inspectors found the Train B batteries to be in good

condition during a detailed walkdown type inspection.

Records of tests

showed that the capacity of these batteries was at least 100 percent of

rated.

A number of cells in the Train A batteries, which were installed in

1988, had heavy sedimentation due to disintegration of the plates.

The

same cells also had decaying voltage and specific gravity. Six cells

(three jars) in the IA battery were replaced in December 1994.

Eighteen

cells (nine jars) were replaced in the 2A battery in November 1994.

The

replacement of cells did not resolve the problems, since voltage and

specific gravity of the new cells trended down.

At least one cell

failed and was jumpered out.

An analysis was performed to show that the

battery could meet the design basis with 59 cells rather than the

original 60.

The inspectors reviewed this analysis and found it to be

acceptable.

An entire new IA battery of the same design (2GN-23) was

installed in September 1995, and a new 2A battery was installed in May

1996.

In the past, equalizing charges were done at 138 V or 2.3 volts per

ce~l. which was lower than recommended by the manufacturer, due to

equipment rating limitations. This was seen as contributing to the

problems, although the basic problem was manufacturing defects.

Currently, the licensee uses single cell charging at 2.6 V when

necessary during normal unit operation.

After capacity testing, which

is performed during the unit outage period, freshening charges are

applied at 2.5 V to replace the expended energy.

The freshening charge

is supplied with a portable charger to a battery which has been isolated

from the rest of the system.

The inspectors concluded that, at the time of the inspection, there were

no concerns with the batteries.

The new Train A batteries and the 1986

Train B batteries were performing well.

In addition, the

inspectorsconcluded that at no time during the past period of problems

were the batteries not able to perform their intended function while the

respective unit was at power .

17

4.5

Problems with Safety-Related Reiays - Type MG-6

During TS surveillance testing of the ESF logic conducted during the

Spring 1996 Unit 2 refueling outage, several relay failures occurred.

The relays that failed were manufactured by Westinghouse Electric

Corporation and Asea Brown Boveri and were type MG-6 relays.

The

particular relays that failed were electrically reset latching relays.

A total of 16 of these relays were installed in safety-related

applications.

Five of the 16 failed.

For three relays, the failure

mode was high contact resistance in two or more of the contacts.

These

contacts were in the trip circuit of the feedwater pumps.

Two relays

failed to latch.

In addition, relays drawn from the warehouse as

replacements also failed to latch during the replacement and checkout

process.

The original relays were manufactured by Westinghouse Electric

Corporation.

At some point, the relay manufacturing plant was bought by

Asea Brown Boveri.

After the takeover, ABB did not offer the MG-6 relay

as safety-related.

The licensee purchased MG-6 relays from Westinghouse

who procured them from ABB and performed commercial grade dedication.

Of the original 16 installed relays, one had been replaced in August

1993 and one had been replaced in February 1995.

This fact was

determined by the licensee by checking the date codes on all the

installed MG-6 relays.

These were the two relays that failed to latch

in the Spring 1996 surveillance test.

The ABB representative, who came to the site to help determine the cause

of the failures, stated that the relays that failed to latch had date

codes putting them in the group of relays known to have some defect

causing the latching problem.

As related to the inspectors by the

licensee, the ABB engineer stated that any relays having date codes from

1991 to 1994 (first quarter) were suspect of having the failure to latch

problem.

The licensee stated they had not received any service bulletin

or other communication from ABB or Westinghouse about this problem.

The

licensee stated they were reviewing the failures for potential

reportability pursuant to 10 CFR 21.

The licensee stated they were in the process of determining the failure

mechanism for the relays at their corporate laboratory, at least the

cause of the high contact resistance.

4.6

125 VDC System Ground Detection Equipment

During the walkdown inspection of the batteries discussed in Section

4.4, the inspectors also looked at the battery chargers to confirm that

the voltage was normal and that the parallel chargers were sharing

loadequally.

At that time, the inspectors noted there was no system

ground fault indicators on the chargers, so the inspectors inquired

about the ground detection capability.

18

The ground detection equipment for the 125 voe Vital Safety-Related

System consisted of two 2800 ohm indicating lamps wired in series

between the positive and negative buses.

The center point (between the

lamps) was solidly grounded.

In the case where no ground faults existed on the system, the voltage

. across each lamp was one-half of full system voltage or about 62.5 voe.

The lamps can detect grounds as follows.

If a ground fault is present

on the system, the resistance of the ground fault itself would be in

parallel with one of the 2800 ohm lamps.

In this case, the equivalent

resistance of the lamp/ground fault combination is different than the

resistance of the lamp on the other side of the center point.

Therefore, the voltage across the two lamps is unequal.

The operator

would see a difference in brightness between the two lamps which is

indicative of a ground.

In the extreme case of a zero resistance ground

fault, one lamp will be dark and the other will be full brightness.

The lamps were located in the control room on the vertical control

board.

They are checked at shift turnover and at other times at the

discretion of the operators.

As stated in the licensee's Technical Report No. EE-060, "DC Ground

Detection," revision 0, dated June 29, 1990, the highest resistance

ground fault detectable with the lamp system described above was 6,760

ohms.

Determination of this value took into consideration the

subjectivity inherent in visual detection of differences in lamp

intensity. This report also calculated values called the minimum

allowable resistance to ground.

This was the threshold resistance value

that could cause a relay circuit to mis-operate if the ground were

located on the positive bus side of the relay coil.

The minimum

allowable resistances associated with a HFA relay and a HGA relay were

53,680 ohms and 102,550 ohms respectively.

Both these values were well

above the highest detectable resistance.

Therefore, the ground

detection equipment at Surry had a design weakness in that a ground of a

certain ohmic value could exist on the system which could cause a

safety-related circuit to mis-operate, and that ground could not be

detected by the ground detection equipment.

Another weakness of the ground detection equipment was that it did not

include continuous monitoring and annunciation.

A ground existing at an

end device that was operated for brief periods of time during normal

plant operation or surveillance testing would have had a low probability

of detection even though it was in the detectable range (6760 ohms or

less).

The reason for this is that the operator would have had to be

looking at the ground indicating lamps during the brief operating

period.

The installed DC ground detection equipment was consistent with that

described in the current version of the UFSAR text and diagrams.

Therefore, the inspectors concluded that the design was considered

acceptable at the time of initial plant licensing.

Since that time,

however, operational experience at other plants throughout the industry

19

has highlighted the weaknesses described above.

The licensee stated

they had no plans to upgrade the ground detection equipment.

The

inspectors concluded that the current design weaknesses require further

review by the NRC.

The matter will be tracked via Inspection Followup

Item 96-05-02, Adequacy of DC Ground Detection Equipment Under Review by

the NRC.

4.7

480 VAC Ground Detection Equipment

During plant walkdowns conducted in relation to review of engineering

activities, the inspectors noted that there were ground indicating lamps

on each of the 4160 - 480 V load centers.

The inspectors noted a

difference in brightness among the three ground fault indicating lamps

at load center 2-EP-LCC-2H.

The center {phase B) lamp was dimmer than

the other two lamps (phases A & C).

The inspectors followed up this

observation with a design review of the ground detection equipment for

the 480 VAC Distribution System.

The 4160 - 480 V transformers were connected in delta configuration on

both the high- and low-voltage sides. Therefore, it was an ungrounded

system.

At each of the load centers, a 480 V system neutral was derived

through the connection of potential transformers and a resistor. Three

480 - 120 V potential transformers were connected in wye configuration

on the high-voltage side and the neutral point was grounded through an

800 ohm resistor. Three ground indicating lamps were connected on the

low-voltage side of the potential transformers in a grounded wye

configuration. Should a ground fault occur on one phase of the system,

the voltage seen by the voltage transformer connected to that phase

would collapse and the lamp on the secondary side would become dark.

It

was not clear to the inspectors what conditions could cause the lamp of

one phase to dim to some intermediate brightness as observed during the

walkdown.

However, the licensee stated that, based on their experience

with the system,' the difference in brightness observed by the inspectors

was too small a difference to indicate a ground.

Nevertheless, the

licensee stated they would evaluate this condition, and if necessary,

make voltage measurements to ascertain the true voltages.

Regardless of whether or not a ground existed on the system at the time

of the inspection, the fact that there was no system ground annunciator

installed represented a design weakness.

A ground existing at an end

device (such as a valve motor) that was operated from the control room

for brief periods of time during normal plant operation or surveillance

testing would have a low probability of detection since there would be

no indication of a ground in the control room.

Circuit breakers would

not trip because the ground fault current for the single-line-to ground

fault is negligible in an ungrounded system.

However, an undetected

ground is a concern, because it could result in a double-line-to-ground

fault should a second ground appear on the system.

The ground detection

equipment for the 480 VAC Distribution System was not described in the

current version of the UFSAR.

The inspectors concluded that the lack of

a system ground detector and the inability to detect a possible ground

20

require further review by the NRC.

This matter will be tracked via

Inspection Followup Item 96-05-03, Adequacy of 480 V Ground Detection

Equipment Under Review by the NRC.

No violations or deviations were identified.

5.0

PLANT SUPPORT (71750, 83750)

The inspectors conducted facility tours, work activity observations,

personnel interviews, and documentation reviews to determine whether

license programs met regulatory requirements in the areas of

radiological protection, security and fire protection.

5.1

Occupation Radiation Exposure Control Program Changes

Changes in the Radiation Protection program, since the last inspection

in October 1995, were reviewed to determine whether program changes met

applicable program requirements and to assess their impact on the

effective implementation of the RP program.

The review included interviews with the RP Manager and staff,

observations and selected review of licensee procedures.

The licensee recently established an oversight program and organization

for the purpose of improving overall site performance.

The Supervisor

of Radiological Engineering from the RP department was selected for the

Plant Support position in the oversight organization.

As a result,

several personnel moves within the RP organization were made.

The

inspectors determined that all personnel were sufficiently qualified to

fill newly assigned positions within the RP organization.

The licensee eliminated the requirement for an annual Whole Body Count.

The capabilities of the Radiation Control Area exit whole body friskers

to detect low levels of radioactive contamination and the relatively low

incidence of personnel receiving measurable intakes of radioactivity

were considerations in the licensee's decision.

The licensee was using

the whole body friskers as passive whole body monitors (paragraph 5.2).

The licensee increased the outage work week for plant HP staff from

approximately 50 hour5.787037e-4 days <br />0.0139 hours <br />8.267196e-5 weeks <br />1.9025e-5 months <br />s/week to 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />s/week.

The change permitted the

licensee to assign plant staff responsibilities for specific work

locations for improved RP control and accountability.

The licensee removed the requirement to issue a TLD for all personnel

entering the RCA.

The licensee removed TLDs for certain persons

typically having less than 100 mrem annual dose.

However, the licensee

21

still used the electronic dosimeter to monitor the radiation exposures

for those personnel when they entered the RCA and TLDs were required for

work in high radiation areas.

The inspectors did not identify any concerns with any of the reviewed

program changes.

No violations or deviations were identified.

5.2

External and Internal Exposure Controls

This program area was reviewed to evaluate the adequacy of the

licensee's RP controls for internal and external radiation hazards and

to verify individual radiation doses did not exceed regulatory limits.

The inspectors reviewed individual personnel exposure records, Radiation

Work Permits and survey documents.

Direct observations of radiological

controls were made during tours of the facilities and during the

performance of on-going work activities within the RCA.

The maximum individual doses (Rems) for calendar year 1995 is.shown

below.

The 1996 values are from TLD measurements through March 31,

1996.

Maximum Individual Radiation Doses

Year

TEDE

Skin

Extremity

Lens-Eye

1995

2.817

3.674

3.674

2.850

1996

0.451

0.451

0.451

0.451

Limits

Part 20

5.000

50.000

50.000

15.000

Adm.

4.000

40.000

40.000

12.000

The highest individual internal exposures for 1995 was approximately

0.1 rem CEDE and the licensee had not made any CEDE dose assignments for

1996.

All external and internal exposures were well within the

regulatory limits.

No concerns with the individual radiation exposures

were identified.

The inspectors reviewed a few personnel radiation dose records to verify

that the licensee was maintaining records of radiation exposures.

One

of the records indicated a radiation worker had ended his work

assignment at Surry without an exit WBC.

The worker was an escorted

contractor employee on site during the period from February through

April 1993.

The inspectors determined that the worker was dismissed

from the site without processing through the dosimetry department prior

to his exit.

The staff reported that while it was desirable to obtain

an exit WBC for all personnel leaving the site it was not a requirement.

The licensee's procedures recommended but did not require an exit WBC .

22

Whole body friskers were being used as passive internal contamination

monitors.

The inspectors reviewed a technical evaluation report which

documented the whole body friskers' ability to detect approximately one

percent ALI.

Since all personnel routinely exit the RCA through the

whole body friskers the licensee concluded the whole body friskers

provided internal monitoring capabilities for each RCA exit.

Personnel

clearing whole body friskers were unlikely to have any measurable

intakes.

Personnel having one percent ALI could cause an alarm on the

whole body friskers prompting an investigation to determine whether the

contamination was internal or external.

Persons suspected of internal

contaminations could receive a quantitative assessment of suspected

intakes with WBC equipment and sampling as needed.

This was part of the

justification for eliminating routine annual WBCs.

The licensee had

utilized the whole body friskers at the Surry RCA exits for

approximately six years.

During tours of the facility, the inspectors verified radiological

postings were appropriate for the radiological hazard, radiation

monitoring equipment was operational and used appropriately, high

radiation areas were properly controlled and independent radiation

surveys agreed with the licensee's surveys.

The inspectors observed

good use of process and engineering controls to limit exposures to

airborne radioactivity.

No discrepancies were identified during those

tours.

The inspectors concluded the licensee was implementing adequate RP

controls and monitoring individual occupational radiation exposures in

accordance with the requirements and that all individual doses reported

were within 10 CFR Part 20 limits.

No violations or deviations were

i dent ifi ed.

5.3

Control of Radioactive Materials and Contamination, Surveys and

Monitoring

This area was reviewed to evaluate the licensee's control of radioactive

and contaminated material.

The review focused on observations made during plant tours and the

review of applicable procedures for the control of radioactive

contamination or radioactive material.

Housekeeping in the Auxiliary Building was generally good.

No

uncontrolled containers of radioactive material or contamination were

identified during tours of the licensee's facilities .

23

The following m1n1mum and maximum contaminated floor space during non-

outage periods was reported:

Plant Contaminated Areas (ft

2

)

Year

Total Area

Areas Contaminated

Minimum

Maximum

Goal

1994

    • 137,127

0

11,000

250

1995

137,127

0

6,400

250

1996

137,127

0

2,544

750

The quantity of contaminated plant area was low and the maximum area

contaminated at any one point in time continued to decline.* The

licensee had recently raised the non-outage contaminated area goal from

250 to 750 ft 2 in 1996 in the interest of ALARA.

The inspectors reviewed recent PCE information for adyerse trends.

The

licensee documented PCEs at a low threshold of 100 cpm above background,

when measured with a thin window GM detector.

The numbers of PCEs

remained fairly constant in last_two years as shown below .

Personnel Contamination Events

Year

Actual

Goal

Skin

Outage Days

1994

199

NA

125

114

1995

198

NA

97

81

1996

47

NA

-

11*

  • Through May 14, 1996

The licensee had seen an increase in numbers of hot particle

contaminations during the Unit 2 RFO.

A few of the particles resulted

in small individual skin exposures that were significantly less than

regulatory limits.

The inspectors reviewed the licensee's dose

assessments associated with the particles and did not identify any

concerns with the licensee's assessments.

The highest particle skin

exposure was approximately 2.5 rem.

The licensee increased monitoring

and cleanup frequencies in areas affected with hot particles.

Overall, the licensee appeared to have a good contamination control

program.

No specific concerns with the program were identified during

the inspection and no violations or deviations were identified .

5.4

-~~ ---* -

24

Maintaining Occupational Exposures ALARA

This program area was reviewed to determine the status and effectiveness

of ALARA program initiatives in reducing site collective dose.

The inspectors reviewed the licensee's annual and outage collective dose

goals and the status of ALARA initiatives with ALARA staff.

A summary of recent collective dose and goals for the site is shown

below.

Collective Personnel Exposures {Person-Rem)

Annual Dose

Outage Dose

Year

Actual Goal

Title

Actual

Goal

Days

1994

378

642

Ul RF0

1

233

312

64

U2 SG

29

20

22

Cleaning

Ul SG

29

22

28

Cleaninq

1995

406

460

U2 RFO,

158

164

47

Ul RFO

197

191

44

1996

66 2

209

U2 RFO

-

164

-

1-10 Year ISI Outage

2-1996 dose information through 05/13/96.

The primary reason for exceeding the Unit 1 RFO exposure goal in 1995

was expanded SG work and equipment problems.

The collective dose

exceeded the estimated 20 person-rem by approximately 13 person-rem.

The licensee took steps to prevent a similar performance on Unit 2 by

taking measures to improve SG planning and training.

The scope of SG

work on Unit 2 was significantly less and the actual person-rem was

approximately equal to the 10 person-rem project dose.

The 1996 annual collective dose goal was challenging considering

previous collective exposure history.

The licensee's 1996 collective

dose during non-outages was greater than anticipated by approximately 6

person-rem primarily from Unit 2 RCP work activities at power, failed

fuel on Unit 1 and continued permanent shielding on the Charging Pump

System.

The 1996 outage collective dose was approximately equal to the

estimated dose.

Overall, the licensee was approximately 4 person-rem

5.5

25

over the projected annual dose during the inspection.

The inspectors

concluded the licensee was utilizing ALARA techniques, developing

challenging ALARA goals and making progress in reducing collective doses

for the staff.

No concerns with the licensee's ALARA program were identified during the

inspection and no violations or deviations were identified.

UFSAR Review in the Radiation Protection Area

The licensee's RP program for Surry was not described in the licensee's

UFSAR.

Therefore, no comparison with the actual RP program could be

made.

However, the inspectors reviewed the status of the Area Radiation

Monitors (ARMs) with the UFSAR descriptions in section 11.3.4, Area

Radiation Monitoring System.

The inspectors verified that the

licensee's system was operating as described.

The inspectors reviewed

the ARM System operability, maintenance activities and design changes.

The licensee was in the process of completing significant modifications

to the plant radiation monitoring systems.

The amount of effort in

maintaining certain process monitors and problems with obtaining parts

for the aging equipment were the primary reasons for implementing the

modification.

While the ARMs had performed well the system was modified

to take advantage of better signal capabilities with detectors having

local pre-amps.

The modifications did not change the general

description of the monitors in the UFSAR and the licensee did not plan

to amend it.

No concerns with the ARM System or UFSAR descriptions were identified.

5.6

Open Item Followup

6.0

(Closed) LER 50-281/96-002, Inoperable EOG Fire Suppression System Due

to Personnel Error.

This LER discussed the inoperability of the EOG number 2 carbon dioxide

fire suppression system due to the rear exit door being left open.

This

item was discussed in NRC Inspection Report Nos. 50-280/96-03 and

50-281/96-03 and resulted in a violation being issued for failure to

establish a fire watch as required by TS.

The inspectors reviewed the

LER and the associated corrective actions to prevent recurrence.

The

inspectors determined that the corrective actions should be adequate to

prevent recurrence.

No violations or deviations were identified.

Review of UFSAR Commitments

A recent discovery of a licensee operating their facility in a manner

contrary to the UFSAR description highlighted the need for a special

focused review that compares plant practices, procedures and/or

parameters to the UFSAR descriptions.

While performing the inspections

26

discussed in this report, the inspectors reviewed the applicable

portions of the UFSAR that related to the areas inspected.

No

discrepancies were identified during this review.

No violations or deviations were identified.

7.0

OTHER NRC PERSONNEL ON SITE

On May 13 and 14, the new NRR Project Manager, Gordon Edison, was onsite

to tour the facility and meet with licensee personnel.

8.0

EXIT

The inspection scope and findings were summarized on June 19, 1996, by

M. Branch with those persons indicated in paragraph 1.

Interim exits

were conducted on May 17 and 24, 1996.

The inspectors described the

areas inspected and discussed in detail the inspection results. A

listing of inspection findings is provided.

Proprietary information is

not contained in this report.

Dissenting comments were not received

from the licensee.

I:i.JIB.

Item Number

Status

VIO

50-280, 281/96-05-01

Open

IFI

50-280, 281/96-05-02

Open

IFI

50-280, 281/96-05-03

Open

EA

95-223: 01013, 01023

Closed

and 01032

LER

50-281/96-002

Closed

9.0

ACRONYMS

ABB

AC

AAC

AFW

AHU

ASEA BROWN BOVERI

ALTERNATING CURRENT

ALTERNATE ALTERNATING CURRENT

AUXILIARY FEEDWATER

AIR HANDLING UNIT

Description and Reference

Inadequate System Isolation

(paragraph 2.3).

Adequacy of DC Ground

Detection Equipment Under

Review by the NRC (paragraph

4. 6).

Adequacy of 480 V Ground

Detection Equipment Under

Review by the NRC (paragraph

4. 7) .

RCS Draindown Event Violations

(paragraph 2.11).

Inoperable EOG Fire

Suppression System Due to

Personnel Error (paragraph

5. 6).

ALARA

ALI

ARM

BRT

CB

CEDE

CR

CFR

cpm

CROM

cw

DC

DCP

DP

DR

EA

ECCS

EOG

ESF

FW

GL

GM

GOP

HHSI

HVAC

I&C

IFI

IRPI

IST

JCO

LER

LHSI

MER

MOV

mrem

MSRC

MTU

MWD

NAF

NOP

NOT

NRC

NRR

PCE

PDR

POTT

PM

PPB

psi

PZR

RCA

RCCA

27

AS LOW AS REASONABLY ACHIEVABLE

ANNUAL LIMIT INTAKE

AREA RADIATION MONITOR

BORON RECOVERY TANK

CONTROL BANK

COMMITTED EFFECTIVE DOSE EQUIVALENT

CONTROL ROOM

CODE OF FEDERAL REGULATIONS

COUNTS PER MINUTE

CONTROL ROD DRIVE MECHANISM

CIRCULATING WATER

DIRECT CURRENT

DESIGN CHANGE PACKAGE

DELTA PRESSURE

DEVIATION REPORT

ENFORCEMENT ACTION

EMERGENCY CORE COOLING SYSTEM

EMERGENCY DIESEL GENERATOR

ENGINEERED SAFETY FEATURE

FEEDWATER

GENERIC LETTER

GEIGER MULLER

GENERAL OPERATING PROCEDURE

HIGH HEAD SAFETY INJECTION

HEATING VENTILATION AND AIR CONDITIONING

INSTRUMENTATION AND CALIBRATION

INSPECTION FOLLOWUP ITEM

INDIVIDUAL ROD POSITION INDICATOR

INSERVICE TESTING

JUSTIFICATION FOR CONTINUED OPERATION

LICENSEE EVENT REPORT

LOW HEAD SAFETY INJECTION

MECHANICAL EQUIPMENT ROOM

MOTOR OPERATED VALVE

MILLIREM

MANAGEMENT SAFETY REVIEW COMMITTEE

METRIC TON-URANIUM

MEGAWATT DAYS

NUCLEAR ANALYSIS AND FUEL

NORMAL OPERATING PRESSURE

NORMAL OPERATING PRESSURE

NUCLEAR REGULATORY COMMISSION

NUCLEAR REACTOR REGULATION

PERSONNEL CONTAMINATION EVENT

PUBLIC DOCUMENT ROOM

PRIMARY DRAIN TRANSFER TANK

PREVENTIVE MAINTENANCE

PARTS PER BILLION

POUNDS PER SQUARE INCH

PRESSURIZER

RADIATION CONTROLLED AREA

ROD CLUSTER CONTROL ASSEMBLY

  • ,

,_

RCE

RCP

RCS

REJ

REM

RFD

RHR

RP

RPS

RSHX

RWP

RVLIS

RWST

SALP

SBO

SE

SG

SI

SNSOC

SRO

SSC

STA

SW

TDAFW

TEDE

TLD

TS

UFSAR

V

VAC

VDC

VIO

VPAP

WBC

WO 28

!.
  • ~.-:-.

ROOT CAUSE EVALUATION

REACTOR COOLANT PUMP

REACTOR COOLANT SYSTEM

RUBBER EXPANSION JOINT

ROENTGEN EQUIVALENT MAN

REFUELING OUTAGE

RESIDUAL HEAT REMOVAL

RADIATION PROTECTION

REACTOR PROTECTION SYSTEM

RECIRCULATION SPRAY HEAT EXCHANGER

RADIATION WORK PERMIT

REACTOR VESSEL LEVEL INDICATION SYSTEM

REFUELING WATER STORAGE TANK

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

STATION BLACKOUT

SAFETY EVALUATION

STEAM GENERATOR

SAFETY INJECTION

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

SENIOR REACTOR OPERATOR

STRUCTURES, SYSTEMS AND COMPONENTS

SHIFT TECHNICAL ADVISOR

SERVICE WATER

TURBINE DRIVEN AUXILIARY FEEDWATER PUMP

TOTAL EFFECTIVE DOSE EQUIVALENT

THERMOLUMINESCENT DOSIMETER

TECHNICAL SPECIFICATION

UPDATED FINAL SAFETY ANALYSIS REPORT

VOLTS

VOLTS ALTERNATING CURRENT

VOLTS DIRECT CURRENT

VIOLATION

VIRGINIA POWER ADMINISTRATIVE PROCEDURE

WHOLE BODY COUNT

WORK ORDER