ML18152A023

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SALP Repts 50-280/89-16 & 50-281/89-16 for May 1988 - June 1989
ML18152A023
Person / Time
Site: Surry  Dominion icon.png
Issue date: 09/22/1989
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A024 List:
References
50-280-89-16, 50-281-89-16, CAL, NUDOCS 8910110225
Download: ML18152A023 (36)


See also: IR 05000280/1989016

Text

i*,'

ff9 tD I \\0 22-~

ENCLOSURE

SALP BOARD REPORT

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

INSPECTION REPORT NUMBER

50-280, 281/89-16

VIRGINIA ELECTRIC AND POWER COMPANY

SURRY UNITS 1 AND 2

MAY 1, 1988 THROUGH JUNE 30, 1989

TABLE OF CONTENTS

I. INTRODUCTION ............................ ~ ...... * .............. : ... l

A..

Licensee Activities ........................................ 1

B.

Direct Inspection and Review Activities .................... 3

I I. SUMMARY OF RESULTS .............................................. 4

I I I . C RITER I A . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . : . . . . . . . 7

IV. PERFORMANCE ANALYSIS ........... : ................................. 8

A.

Plant Operations ........................................... 8

B.

Radiological Controls ..................................... 12 *

C. -

Mai ntenance/Survei 11 ance .................................. 15

D.

Emergency Preparedness .................................... 20

E .

Sec u ri ty ........................................ * ........... 21

F.

Engineering/Technical Support ............................. 23

G.

Safety Assessment/Quality Verificition .................... 27

V. SUPPORTING DATA AND SUMMARIES .................................. 30

A.

Investigation Review ...................................... 30

B.

Escalated Enforcement Action .............................. 30

C*.

Management Conferences .................................... 32

D.

Confirmation of Action Letters ........................*... 33

E.

Review of Licensee Event Reports .......................... 33

F.

Licensing Activities ...................................... 33

.G.

Enforcement Activity ............................... * ....... 34

H.

Reactor Trips .................. ; .......................... 34

I. INTRODUCTION

The Systematic Assessment of Licensee Performance ( SALP) program is an

integrated NRC staff effort to collect available observations and data on

a periodic basis and to evaluate licensee performance on the basis of this

information.

The SALP program is supp 1 ementa 1 to norma 1 regulatory

process~s used to ensure compliance with NRC* rules and regulations. It is

intended to be sufficiently diagnostic to provide a rational basis for

allocation of NRC resources and to provide meaningful feedback to the

1 i censee

I s management regarding the NRC assessment of their facility I s

performance in each functibnal afea.

An

NRC SALP Board, composed of the staff members listed below, met on

August 30, 1989, to review the observations and data on performance and to

assess

licensee performance

in

accordance with Chapter

NRC-0516,

11Systemat i c Assessment of Licensee Performance.

11

The guidance and

evaluation criteria are summarized in Section III of this report.

The

Board

1 s findings and recommendations were forwarded to the NRC Regional

Administrator for approval and issuance.

This report is the NRC 1 s assessment of the licensee 1 s safety performance

at Surry for the period May 1, 1988, through June 30, 1989.

The SALP Board for Surry Units 1 and 2 was composed of:

L. Reyes, Director, Division of Reactor Projects (DRP), Region II

(RII) (Chairman)

E. Merschoff, Deputy Director, Division of Reactor Safety (DRS), RI!

J. Stohr, Director, Division of Radiation Safety and Safeguards

(DRSS), RI!

M. Sinkule, Chief, Reactor Projects Branch 2, DRP, RI!

H. Berkow, Director, Project Directorate II-2, Office of Nuclear

Reactor Regulation (NRR)

W. Holland, Senior Resident Inspector, Surry, *DRP, RI!

Attendees at SALP Board Meeting:

B. Grimes, Acting Deputy Regional Administrator, RI!

P. Fredrickson, Chief, *project Section 2A, DRP, RI!

S. Shaeffer, Project Engineer, Project Section 2A, DRP, RI!

G. Wiseman, Reactor Engineer, Technical Support Staff, DRP, RI!

W. Scott, Senior Operations Engineer, Performance and Quality

Evaluation Branch, NRR

D. Roberts, Intern, NRR

A.

Licensee Activities

Unit 1 began the assessment period in day 22 of. a scheduled refueling/

~aintenance outage.

The outage extended much longer than scheduled, and

2

the unit did not return to powef operation until the middle of duly 1988.

With the exception of one automatic reactor trip in A~gust 1988, the unit*

operated at power until the middle of September 1988, when ii was shut

down due to concerns about the operabi 1 i ty of the emergency di ese 1

generators. The outage lasted from September 14, 1988, thtough the end of*

the assessment period. However, Unit 1 was preparing to return to power

operation when the assessment period ended and was operating at power on

July 7, 1989.

Unit 2 began the assessment period at power.

The unit experienced an

automatic reactor trip in May 1988, and remained shut down for repairs for

the next five weeks, returning to ~ower operation in the latter part of

June'. 1988.

The unit operated at power until September 10, 1988 when,

  • during shutdown operations for a scheduled refue 1 i ng/maJ ntenance outage,

it tripped from approximately four percent power.

The refueling outag~

lasted longer than originally scheduled due to the parallel outage on Unit

1 and identification of significant safety issues which had to be resolved

for both units prior to restart. Uni£ 2 remained in cold shutdown at the

end of the assessment period while corrective actions that were required

prior to unit restart were being completed.

As indicated by the duration of the unit outages, significant safety

problems were identified whic;h required extensive corrective actions.

Some of the prob 1 ems re 1 ated to a 1 ack of procedura 1 guidance in the

performance

of operations, radiological controls, maintenance,, and

testing; lack of cleanliness affecting safety-r-elated systems; inadequate

identification and root cause resolution of significant conditions adverse

to quality; and a lack of proper planning and requiring accountability for

lower level supervision and craft in the performance of daily work.

After

significant safety issues associated with the original design of plant

systems became known, the *licensee augmented the station staff with

addi ti ona 1 management and engineering resources during the fa 11 of 1988.

Additional management changes and reorganizations continued to be made at

both the station and in the corporate offices well into the assessment

period.

Management and/or organization changes instituted by the licensee during

the assessment period included:

September 1988

November 1988

December 1988

January 1989

February 1989

New Vite President-Nuclear Operations

New Station Manager - Surry Plant

New Health Physics Superintendent - Surry Plant

Reorganization of the engineering organization.

New

Superintendent of Engineering position created and

assigned to both Surry and North Anna

New

Assistant

Station

Manager-Operations

and

Maint~nance - Surry Plant

B.

February 1989

March 1989

April 1989

June 1989

3

New Operations Superintendent - Surry Plant

Reorganization of the corporate org~nization to

specifically. focus

appro~riate

resources

on

the

nuclear program.

Changes included creation of a

Senior Vice

President-Nuclear position,* a

Vice

President-Nuclear Services position, a Vice President-

Nuclear Engineering pos*ition, and an Assistant Vice

President-Nuclear Operations.

These changes also

affected se~eral management positions in the corporate

offices including selection of a new Quality .Assurance

Manager.

New President and Chief Executive Officer

New Vice President-Nuclear Services (position created

in March 1989 restructure.)

Direct Inspection and Review Activiiies

During the assessment period, routine inspections were performed at the

- Surry facility by the resident and regional staffs.

From May* through

.December 1988,

36 inspections were conducted including an Augmented

Inspection Team (AIT) inspection of the reactor cavity seal leakage event

on Unit 1, a Safety System Functional Inspection (SSFI) of the service

water system in September 1988, and special inspections associated with

the

increased radiological

protection area monitoring,

which

was

instituted due to problems identified during the last assessment period.

From January through June 1989, 19 inspections were conducted.

Several of

these inspections were special inspections associated. with technical

problem areas i_dentified *during the licensee's Operational Readiness

Assurance Program (ORAP), which was implemented in January 1989.

Seven

management meetings,

fo~r technical meetings' and three Enforcement

Conferences were also conducted.

The-following is a listing of specific special inspections:

June 20-24, 1988; inspection to review environmental qualification

and Generic Letter 83-28 implementation.

September 1-3, 1988, AIT inspection to review the reactor cavity seal

leakage event.

September 12-16, 26-30, and November 14-18, 1988; SSFI inspection of

the service water and recirculation spray systems.

October 3-7 and 9-14, 1988; inspection to review reactor cavity seal

modifications and corrective actions .

4

.

.

January 23-27 a.nd February 1-2, 1989; inspections to followup on

mo~or operated valve (MOV) and electrical termination issues.

March 27 - April 4, 1989; inspection on motor operated valve (MOV)

issues.

April 10-14

and

May 10-12,

1989;

inspettion for fcillowup

on

electrical issues.

May 1-5, 1989; inspection for followup on SSFI issues.

June 5-9, 1989; in'spection for followup on MOV program implementa-

tion.

II.

SUMMARY OF RESULTS

Surry operated with mixed performance during the assessment period.

  • Performance during the first half of the assessment period was poor

overall, but improved ~ignificantly toward the end of the period.

Major

weaknesses were identified in the areas of Plant Operations, Radiological

Controls, Maintenance/Surveillance, Emergency Preparedness and Safety

Assessment/Quality Verification.

A major strength was identiffed in the

Security area.

There was considerable activity in the Plant Operations area, though the

units operated for only a few months.

Operator inattention to detail, -

combined with inadequate management overview, contributed to several

events early in the assessment period.

Although management reaction was

evident for many of these events, root cause corrective action did not

occur until late in the assessment period.

A comprehensive ORAP was

developed for the restart of the units, but was initiated only after

several significant events necessitated some form of management action.

An additional problem, early in the period, was the tendency of operators

to tolerate equipment problems and work around them, rather than insisting

on repair or replacement.

Toward the end of the period, many of the

operations problems were in the process of being corrected.

Use of the

ORAP

provided effective means to identify,

evaluate and

correct

deficiencies.

Several plant management changes also contributed to

improvement late* in the assessment period; and, both management and the

operations staff d,sp l ayed an increased awareness toward attention to

detail, performance expectations and plant safety responsibilities.

The Radiological Controls functional area had not improved significantly

from the previous assessment period.

Early in the period,* an exposure-

related event occurred resulting in escalat~d enforcement action.

This

event and several other violations were directly attributed to inadequate

performance by the radiation protection staff.

During the last half of

the assessment period, the licensee began to more closely monitor work

activities for person-rem exposure and personnel contaminations.

The

s*

amount of contaminated area was reduced, but was still considered high.

Although the number of personnel contami.nations and the collective dose

were also high, a decreasing trend was noted in the number of personnel

contaminations toward the end of the assessment period.

Health physics

(HP) management changes and the development of a radiological engineering

capability resulted in improvement in this area.

Performance in the Mai ntenance/Survei 11 ance functi ona 1 area decreased

since the last assessment period.

A large maintenance back.log existed

during the period and

the preventive maintenance ( PM) program needed

improvement, as evidenced by several large-scale-equipment problems.

In

addition, the lack. of a formal check. valve maintenance program and an

ineffective maintenance root cause and trending program revea 1 ed a

deficiency in the abn ity to correct 1 ong-standi ng protil ems.

Procedures

were also a weakness in this functional area as was post-maintenance

testing. The deficient MDV maintenance program was an,example where all

of the specific: types of problems identified in this functional area

occurred, clearly indicating. a significant programmatic deficiency.

Toward the end of the assessment period, though, an aggressive MDV rework.

program was well underway.

Surveillances were generally performed in the

required time frame, but major problems involving emergency service water

pump

and control

room chiller surveillance testing revealed some

significant deficiencies.

A surveillance strength, though, was the

  • maintenance predictive analysis feedback. inio the surveillance program.

Weaknesses were observed in the Emergency Preparedniss (EP) area during

the 1988 annual emergency exercise and during NRC inspections.

Event

classification and the augmentation timeltness of personnel it emergency

response facilities were significant problem areas.

A remedial drill

corrected the classification problem, but an overall improvement in

augmentation timeliness was *not demonstrated.

Some EP program strengths

were noted during the last EP inspection conducted during the period.

As

a result of the problem*s ,observed in the EP area, the 1 icensee has

categorized specific areas for followup analysis and corrective action as

appropriate to improve the overall EP program.

With respect to the Security fun ct i ona 1 area, the 1 i cen see provided

exce 11 ent support within the requirements of its approved p 1 an.

_One

-

weakness was the timeliness of security equipment repair; a problem which

revealed that better coordination of activities between security and

maintenance was needed.

The security force had minimal turnover and was

well trained and supervised.

Procedures were clearly written and training

was thorou-gh.

Early in the assessment period, within the Engineering/Technical Support

functional area, poor performance was demonstrated by the engineering

department, through its failure to correctly determine the design basis

adequacy of the service water system.

Also early in the period,

engineering MOV reviews were inadequate, contributing to the significant

6

MDV problem.* An engineering self-assessment capability was lacking during

the assessment period, as evidenced by a large backlog of engineering

problems and the inadequate safety assessment of several

is~ues.

Engineering Work Request (EWR) problems revealed a deficiency with

training of ~he engineering staff and also deficiencies in EWR procedure

quality.

Engineering support to the equipment qualification (EQ) and

non~destructive examination (NOE) program was good.

Engineering involve-

ment in the ORAP, in a~ MDV task team, and in the initiation of a Design

Basis Documentation program represented a significant engineering effort

later in the assessment period.

In addition, the formation of a systems

engineering group and a design engineering group on site provides the

potential for improvement.

Training, overall, continued to be a strong

-area, with licensed operator training being very effective.

Training

facilities and high quality instructors were also positive assets,

especially during the latter part of the period.

Within the Safety Assessment/Quality Verification functional area, .the

1 icensee failed to take appropriate corrective actions in numerous

instances such as the reactor cavity seal leak event, foreign material/

cleanliness problems, potential gas binding of safety-related pumps, a

degraded ventilation system, and a leaking safety-related pump enclosure.

Early in the assessment period, the license_e did not demonstrate an

adequate safety assessment capability, which contributed to several

events.

Root cause analysis was a 1 so i dent i fi ed as being ineffective.

Other problems identified in this functional area involved not tracking

regulatory commitments and the independent review group not meeting its

regulatory review responsibilities.

The above noted deficiencies occurred

primarily during th~ first part of the asiessment period. Toward the end

of the period, management sensitivity increased and corrective action

became more thorough, safety assessment improved and the 1 icensee al so

began to improve the root cause analysis effort.

With respect to

licensing activities, submittals were of good quality and timely.

Although the mctjor problem areas were not identified through the quality

assurance (QA) program, the QA organization began to improve its problem

identification capability late in the assessment period.

Overview

Functional Area

Plant Operations

(Operations/Fire Protection)

Radiological Controls

Maintenance/Surveillance

Emergency Preparedness

Security

Engineering/Technical Support

(Engineering/Training/Outages)

Safety Assessment/

Quality Verification

(Quality Programs /Licensing)

NR - Not Rated

Rating Last

Period

2/2

2 Declining

2/2

2

2

NR/1/2

2/1

Rating This

Period

3 Improving

3 Improving

3

3

1

2

3 Improving

7

I I I. CRITERIA

Licensee performance is assessed in selected functional areas depending on

whether the facility is in the construction or operational phase.

Functional areas normally represent ar~as significant to nuclear safety

and the environment.

Some functional areas may not be assessed because of

little or no licensee activity*, or lack of meaningful observations.

Special areas may be added to highlight significant observations.

The following eval*uation criteria were used, ~s applicable, to assess each

functional area:

1.

Assurance of quality, including management *involvement and control;

2.

Approach to the resolution of technical issues from a safety

standpoint;

3.

Responsiveness to NRC initiatives;

4.

Enforcement hi story;

5.

Operational and construction events (including response to, analysis

of, reporting of, and corrective actions for);

6.

Staffing (including management); and

7.

Effectiveness of training and qualification program.

However, the NRC is not limited to these criteria and others may have been

used as appropriate.

On the ba-sis of the NRC assessment, each functional area evaluated is

rated according to one of three performance categories.

The definitions

of these performance categories is as follows:

1.

2.

C~tegory 1:

LiGensee management attention and

involvement are

readily evident and place *emphasis on superior performance of nuclear

safety or safeguards activities, with the resulting performance

substantially exceeding regulatory requirements.

Licensee resourses

are ample and effectively used so that a high level of plant and

personnel performance is being achieved.

Reduced NRC attention may

be appropriate.

Category 2:

Licensee management attention to and involvement in the

performance of nuclear safety or safeguards activities are good.

The

licensee has attained a level of performance above that needed to

meet regulatory requirements.

Licensee resources are adequate and

reasonably allocated so that good plant and personnel performance is

being achieved. - NRC attention may be maintained at normal levels .

3.

8

Category 3:

Licensee management attention to and involvement in the

performance of nuclear safety or safeguards activities are not

  • sufficient .. The 1*icensee 1 s performance does not sig~ifitantly exceed

that needed to meet minimal regulatory requirements.

Licensee

resources*. appear to be strained. or not effectively used.

NRC

attention should be increased above normal levels.

The SALP Board may also include an appraisal of the performance trend of a

functional area.

This performance trend will only be used when both a

definite trend of performance within the evaluation period is discernable

and th_e Board believes that c*ontinuation of the trend may result in a

change of performance level.

The trend, if used, is defined as:

Improving:

Licensee performance was determined to be improving near the

close of the assessment period.

Declining:

Licensee performance was determined to be declining near the

close of the assessment period and the licensee hftd not taken meaningful

steps to address this pattern.

IV.

PERFORMANCE ANALYSIS

A .

Plant Operations

1. *

Analysis

During the assessment period, inspections of plant operations were

performed by the resident and regi ona 1 staffs.

A 1 so, an AIT

inspection was conducted in September 1988, to review the event

associated with a. loss of reactor cavity water level during the

refueling of Unit 1 in May 1988. *

Performance in this functional area was mixed over the assessment

period.

Early

in

the

assessment period,

proper management

involvement and contro 1 at both the site and corporate l eve 1 s were

not evident.

Approach to resolution of technical issues from a

safety standpoint _was

inconsistent,

enforcement

hi story

was

indicative of programmatic problems, and operational events occurred

which ~ere poorly identified and marginally analyzed.

After

identification of several problem areas by both the NRC and the

licensee, a number of management changes were made at the station.

Duri*ng the assessment period, Unit 1 ciperated at power for two month~

and U~it 2 operated at power for three and one-half months with Unit -

1 experiencing one automatic reactor trip, and Unit 2 experiencing

two automatic reactor trips.

The three automatic trips in a six

month period of operation was considered high. All trips were caused

by equipment failures.

Both units* were

shut down

in early

September 1988; Unit 1 for a forced maintenance outage, and Unit 2

9

for a scheduled refueling outage. Neither unit had returned to power

operations py the end of the assessment period.

The long outages

were not attributable to the operations department* s performance;

however, the long downtime appeaied to have a detrimental eff~ct on

operator* a 1 ertness and attention to detail.

Ex amp 1 es of ope.rater

iMattention to detail during the outage included improper operation

of containment isolation valves, problems with valve alignments,

tagging problems, and improper pump(s) operation.

Early in the assessment period, the lack of proper management

overview resulted in an inadequate evaluation of the May 1988, Unit 1

reactor cavity seal event. Operator actions to recover cavity level

during this event were improper.

These deficiencies resulted in a

Severity Level III violation with a Civil Penalty.

Inadequate.

management overview was a 1 so noted during the return to power of

Unit 1 in July 1988, following an extended refueling outage.

That

occurrence involved initial. direction by station senior management \\o

continue with a plant heatup while the unit was in a Limiting

Condition for Operation (LCD) which required that the unit return to

cold shutdown.

Management* changes. made during the. assessment period incl 1,.1ded the

Station Manager (November 1988), the Assistant Station Manager for

Operations and Maintenance (February 1989), and the Operations

Superintendent (February 1989).

These changes resulted in improved

sensitivity to safety and a positive attitude towards the proper

conduct of nuclear power plant operations. This new sensitivity and

attitude were observed during safety committee meetings, Unit 1

readiness restart assessment meetings and restart action item

closeout meetings during the latter part of the assessment period.

In addition to the man~gement changes discussed previously, another

factor affecting the operation of the station after both units were

shut down was the lack of clear direction and appropriate scheduling

of corrective actions.

These actions were necessary to resolve

significant issues that had been identified which affected several

safety systems.

After identification of incorrectly wired (wrong

train) safety-related valves in December 1988, the licensee proposed

a comprehensive ORAP which provided for _an appropriate direction of

the activities needed to be accomplished prior to either units*

restart.

One of the positive actions taken was the implementation of a plant

status .log for each unit.

At the end of *the assessment period, the

initial indications were that this configuration control program had

a positive impact on the safe operation of each unit.

Some examples

were that the control boards were not cluttered with different tags

and information notes and the plant status logs provided a single

location for information relating to work requests, operator aid

notes and component tagout status .

1_0

Staffing levels were adequate. The op~rations department continued to

run with five operating shifts.

The operations department averaged

between 20 and '30 percent overtime, and early in the period some

backshifts were staffed with only two Senior Reactor Operators (SRO)

(minimum Technical Specifications (TS) requirement).

It should be

noted that, at the end of the assessment period, the -operating shifts

had a minimum of three SROs assigned to each shift which was

considered as an enhancement in technical and supervisory shift

capability.

At the end of the previous assessment period and conti~~ing into this

assessment period, operating procedures were identified as requiring

tmprovement.

During the early part of this assessment period, almost

every procedure in use by the operations department had one or more

temporary changes implemented.

This condition placed additional

burdens on the operators in the performance of their duties.

The

licensee acknowledged the poor condition of procedures and initiated

a program that involves the imp1ementation of a uniform method for

procedure writing (Procedures Writers Guide).

The licensee also

outlined a three-year schedule commencing

in

1989

which will

generally upgrade station technical procedures in the operations and

maintenance ar:eas to the new enhanced format.

At the end of the

assessment period, the licensee had

upgr~de~ approximately 50

procedures.

However, the procedur~s. which were used for the Unit 1

restart were not upgraded.

These procedures had been reviewed and

considered adequate for unit s*tartup.

Based on a population of

approximately 2500 procedures to be reviewed for upgrade program

completion, the three-year schedule appeared to be pptimistic.

During the early part of 1989, several operational errors occurred,

including

improper operation of containment isolation valves,

improper valve alignment resulting in flooding of the Unit 2 cavity

area, operati-on -of a charging pump without a suction flowpat_h, and

operation of a containment vacuum pump with the suction flowpath

blocked.

These errors resulted in a violation for failure to follow

- procedures and for inadequate procedures.

Another operational

occurrence that resulted in a violation was a loss of shutdown

cooling to Unit 1 in March 1989.

This problem again indicated

inadequate operator control of a required system.

Although each of

the occurrences resulted from either an inadequate procedure or a

failure of operations personnel to maintain cognizance of system

configuration, the more underlying cause was a 1 ack of persona 1

responsibility for attention to detail.

Management was involved

afte,r each event, providing direction to correct the problems.

However, management sensitivity towards proper operation of the

station and expectations regarding attention to detail and plant

ownership were not evident until the latter half of the assessment

period.

11

Early in the assessment period, the operations department tolerated

malfunctioning equipment and often took compensatory measures to work

around problems rather than have them corrected. This was evidenced

by the continuing problems associated with inadequate service water

to operating control room chillers and the acceptance and lack of *

repair of inoperable radiation monitoring equipment for long ~eriods

of time.

However, near the end of the assessment period, the

operations staff was requiring more accountability and performance of

the operations support departments with operators being

held

accountable for identification of problems affecting operational

readiness.

The licensee continued to upgrade the drawings which were needed *by

operations personriel in the performance of their daily duties and in

emergency conditions. Both units

1 flow diagrams were being converted

to the computer assisted drawing system (CADS) in order to ease

updating.

Several

NRC

reviews of the control

room drawings

identified few discrepancies which would affect the capability of the

operators to handle events.

Also, during conduct of the ORAP for

Unit 1, the flow drawings were used by the system engineers to walk

down the systems addressed in the emergency procedures for Unit 1.

D~ring these walkdowns, no significant problems were identified: At

the end of the period, the review process was still ongoing and the

licensee was continuing to update and correct minor discrepancies.

The operations department identified several discrepancies in the

program associated with establishing and maintaining isolation

tagouts over the 1 ong outages..

Although * add it i ona 1 management

attention was given -to this area, a comprehensive solution to

correction 6f identified problems was not evident. At the end of the

assessment period, the iicensee was in the process of converting to a

computerized tagout program to help improv~ this ~rea.

Based on a

limited review, implementation of this program should improve tagout

control.

The review of the fire protection program implementing procedures,

survei 11 ance procedures, test results, fire fighting equipment and

fire detection systems demonstrated that plant fire protection

features were in service and functional.

The control of combustibles

and general housekeeping in safety-related areas were found to be

training and drills for the fire brigade members met frequency

requirements specified by the fire protection program implementing

procedures.

The

effectiveness of fire brigade training was

demonstrated during an unannounced dri 11 observed by the NRC staff.

In addition,

NRC inspectors observed satisfactory fire brigade

performance during a response to two minor fire events.

The fires

were extinguished immediately and resulted- in no damage to plant

equipment or injury to plant personnel.

B.

2.

12

One Severity Level III violation and two additional violations were

identified during the assessment period.

Performance Rating

Category:

3

Trend:

Improving

3.

Board Recommendations

The procedures ~pgrad& program should be considered a high priority

issue and it's progress should be monitored .to assure timely

completion.

Management needs to assure that the operations staff

does not accept conduct of plant operations with poorly performing

equipment.

The Board recognizes that later in the assessment peribd,

past problems were. ~eing addressed.

The high level of inspection

effort should continue in this area.

Radiological Controls

1.

Analysis

During the assessment period, inspect i ans were performed by the

resident and regional staffs.

The inspections included six radiation

protection inspections and one radiological effluents and chemistry

inspection.

Radiation protection inspections were increased. as a

  • result of the previous assessment which concluded that Surry* s

radiation pfotectio~ program was degrading;

The licensee's radiatio*n protection, radwaste and chemistry staffing

levels were adequat~.

In the middle of the assessment period, a new

Radiation Protection Superintendent was named.

A 1 so, the 1 i cen see

recruited a radiological assessor to provide internal assessment of

the radiation protection program.

In response to below average

resol~tion of. technical issues reported in the previous assessment

report, and to remedy the weaknesses identified, the licensee

developed a radiological engineering.capability within the radiation

protection group by adding a staff of seven radiological engineers.*

The performance of the HP staff, in the early *part of the assessment

period, in support of routine and outage operations was poor.

Ele~en

of the fourteen violations of NRC regulations that occurred during

this assessment period could be attributed directly to inadequate

performance

by radiation protection department personnel.

Five

violations of NRC regulations involved requirements for controlling

personnel radiation exposure.

Four violations of NRC regulations

involved either the failure to follow approved procedures or

inadequate procedures.

In addition, the inability to adequately

control personnel exposure continued from the previous assessment

13

period.

Early in this assessment period, a person performing

cleaning and inspection of. the reactor vessel flange received

3.279 rem in one calendar quarter.

This overexposure resulted in

multiple violations characterized as a Severity Level III problem,

and the issuance of a Civil Penalty.

As a' result of the unsatisfactory performance during the early part

of the assessment period, the licensee performed an evaluation of

their radiation protection program and identified the following

corrective

actions

to

address

the

programmatic

weaknessei:

1) increased management involvement and control of pre-job prepara-

tions arid assessments; 2) management emphasis on accelerating the

implementation of the Corporate Radiation Profection Plan, including

issuing revised radio l ogi cal control procedures; 3) pro vis i ori for

additional experience in and proper management of the radiation

protection group, as we 11

as adequate radio l ogi cal

engineering

expertise onsite; 4) training and department meetings to review and

emphasize procedural compliance; and 5) a program to enhance overall

procedure quality.

The licensee presented a formal improvement program to the NRC in

July 1988.

New

initiatives for accountabiJity

of_ performance

implemented by the Pl ant Manager and the Radiation Protection

Superintendent .have resulted in imp roved performance by both* HP

supervisors and t.echni ci ans.

However, throughout and subsequent to

the end of the assessment period, problems were observed in station

workers' compliance with HP requirements.

Since identification of

the programmatic improvements, both units have been in extended

maintenance/refueling

outages.

During

these

outage

periods,

significant work requiring HP support was accomplished.

Although the

licensee did not achieve the reduction in person-rem exposure that

could be expected if both uni ts were operating' the licensee did

  • closely monitor each job for person-rem exposure and al so closely

monitored the personnel contaminations.

Reviews of the licensee's As

-Low ~s Reasonably Achievable (ALARA) program revealed that all items

identified as problems during a team inspection conducted in the

previous assessment period had been closed.

As a result of the

corrective actions taken by the licensee in response to the ALARA

team inspection, the most significant ALARA program improvement was

the management of collective dose at the station.

During the

previous assessment period, the licensee managed dose by utilizing a

daily collective dose average which was based on previous routine and

outage days.

The

licensee

improved the daily management of

- collective dose by basing the goals on specific ALARA reviews and

dose projections.

At the beginning of the assessment period, the licensee had 24,075

square feet (ft 2 )*of contaminated area, which represented 27 percent

of the radiologically c~ntrolled area of the plant.

By the end of

,.

14

the assessment period, this area was

reduced to 17,524 ft 2 ,

(19 percent), which was under the licensee's goal of 17,792 ft 2 for

1989. Although the reduction in contaminated area Js significant ~nd

can be attributed t6 increased management s~pport for decontaminatiqn

of controlled areas, and the recoating of large portions of the

controlled areas with epoxy, Surry's contaminated area was still

high.

During the assessment period, the licensee recorded 394 personnel

contamination events. This was a downward trend'and is attributed to

the decontamination effort and increased management attention in this

area.

The station's 1989 collective dose goal was established at 502

person-rem.

By the end of the assessment period, the licensee had

accumu1ated 435 person-rem towards this goal.

During this assessment

period, Unit 1 experienced 259 outage days while Unit 2 experienced

263 outage days.

The collective dose during this period was 1938

person-rem.

The cumulative exposure for the amount of outage time

was not considered to be excessive:

During the assessment period, the licensee began construction of a

new radwaste processing facility, which was designed using the latest

ALARA concepts and waste reduction technology.

In the past several assessment period, there continued to be a

significant decreasing trend in total curies released via the liquid

release pathway.

This was partially attributable to improvement in

radioactive waste processing and extended plant shutdowns during the

period.

Liquid and gaseous effluents for the period were within the

dose limits specified in 40 CFR 190, 10 CFR 50, Appendix I ALARA

Criteria, and the radioactive concentrations specified in 10 CFR 20.

No unplanned releases were reported during the assessment period.

J

In the liquid and gaseous effluent monitoring program, there has been

an apparent lack of management attention, in that the licensee has*

been in several continuous Technical Specification ACTION statements.

Examples of this are the inoperability of the component cooling water

effluent line monitor and the waste gas holdup system oxygen monitor.

Compliance has relied totally on compensatory measures.

At the end

of the assessment period, the licensee was actively pursuing redesign

of these monitors.

A radiological confirmatory measurements comparison continued to show

good agreement between NRC and licensee measurements.

One Severity Level III problem, composed of eight violations, and six

additional violations were identified during the assessment period .

2.

Performance Rating

Category:

3

Trend:

Improving

15

3.

Board Recommendations

Positive management initiatives are necessary to assure continued

reduction of cumulative exposure, to ensure that working level

pers6nnel understand the importance of adherence to HP proced~res and

to

expeditiously repair radiation. monitors

needed

for plant

operations.

The Board recognizes that the construction of a new

modern radwaste faci 1 i ty, a decrease in the number of personne 1

contamination events and a downward dose. trend are positive

indicators of your radiological control effort. Based on the overall

assessment, the Board recommends a continued high level of inspection

activity.

C.

Maintenance/Surveillance

1.

Analysis

During this assessment period, ~outine and special inspections were

  • performed by the NRC staff. Significant inspection findings in this

area were identified in an SSFI inspection of the service water

system, an AIT inspection of the reactor cavity seal event and

several MDV inspections*.

The maintenance staffing levels appeared adequate, with minimal

turnover rate.

The overtime rate was relatively high due to the

extended outages, even though a significant number of contractors

were used to augment the normal station staff.

The maintenance

department was expanded to include an engineering supervisor, who is

responsible for the predictive analysis group, the PM program, the

MDV coordinator, and the maintenance engineers.

The overall material condition of the plant improved during this

period, primarily due to identified problems driving a more thorough

maintenance approach.

For example, the main control room envelope

chillers and instrument air compressors wert ov~rhauled after being

allowed to degrade to a point where they would not have p~rformed as

required.

The licensee did not routinely use maintenance-specific performance

indicators to evaluate the effectiveness of the maintenance

department.

For example, the licensee did not identify and trend

rework and/or mean time to return equipment to service for management

review and evaluation.

The average age of corrective maintenance

work requests was approximately 200 days.

Although this figure was

16

elevated by a significant number of minor work requests, it did

indicate that a substant i a 1 amount of , back 1 og work remained.

Examples of these minor work requests were leakage reduction work

orders, valve packing. upgrades, and replacement of Grinnel valve

diaphragms due to the age of the material.

Management involvement

was evident regarding temporary modifications (i.e. jumpers, lifted

leads), with adequate emphasis placed on removal of those jumpers

necessary to return safety equipment to service.

PM comprised

approximately 25 percent of the. total maintenance effort.

The

deferral rate of scheduled PM work averaged approximately 20 percent.

~lthough this was an improvement over previous assessment periods,

continued improvement was needed, as evidenced by the extensive MDV

problems and the failure to implement PM requirements specified "for

the diesel driven emergency service water pumps.

The licensee was ineffective in implementing adequate programs to

correct long-standing problems.

For example, the PM program was

scattered throughout several disciplines, with no method to monitor

effe~tiveness.

Also, the licensee did not have a formal ch~ck valve

maintenance program in p 1 ace, even though a need for this type

program was identif_ied as a major weakness following the 1986

feedwater pipe rupture event.

In addition, at the end of the

assessment period, the licensee was developing a formal maintenance

root cause and trending program in respo'nse to numerous audit and NRC

concerns identified during the last assessment period. This program-

matic problem was discussed *in the last assessment period.

Manage-

ment was aware of this shortcoming and initiated efforts to improve.

A change in philosophy regarding program development and implemen-

tation occurred over the_ assessment period, turning away. from tasking

the statioh with developing programs and more to~ard turnkey program

deveiopment at the corporate level.

Training for the maintenance craft was found to be adequate.

The

trainin*g program maintained full accreditation with the National

Academy for Nuclear Training.

Construction was completed on a large

addition to the training center complex that contains additional

classrooms, laboratories-and offices._

Inadequacies. were

identified

regarding

the

identification,

procurement, and staging of parts. A previous failure to adequately

evaluate the suitability of non-qualified replacement parts, coupled

with an inadequate purge of these suspect parts_ from storage,

resulted in potentially unqualified replica parts being installed in

safety related components.

In addition, a problem was identified

regarding the failure to adequately identify and control materi~ls in

several safety-related work activities. At the end of the assessment

period,

the licensee was

implementing a program to increase

engineering involvement in the procurement process .

17

. Similar to the Plant Operations functional area, procedures also

continued to be a significant weakne~s in the maintenance area.

Changes to procedures were frequently required to enable work to.

proceed.

The failure to imp 1 ement adequate procedura 1 control

resulted in a programmatic weakness regarding * foreign materi a 1

exclusion.

This weakness was highlighted by the discovery of debris

that had accumulated for several years inside the poorly maintained

screens of both- containment

sumps.

Further examples of poor

procedures were identified involving the failure to incorporate

reactor cavity seal design requirements into maintenance procedures,

improper orientation. of flow *orifices, the poor reinstallation of

Appendix R cable tray covers, and the improper torquing of system

closure fasteners.

The licensee acknowledged the poor condition of

th~ procedures and initiated* a three-year procedure upgrade program

as discussed in the Plant Operations area.

Significant and numerous problems were identified regarding the

. maintenance of MOVs.

The MOV deficiencies indicated weaknesses in

the technical content of implementing procedures, little involvement

from management and f i rst-1 i ne supervisors and a 1 ack of a we 11 *

structured, comprehensive MOV program.

Resolutions to correct MOV

defici~ncies were often not thorough and in some cases not aahered

to.

During the latter half of the assessment period, the licensee

instituted a major rework program involvi_ng virtually all the safety

system MOVs, after it became apparent that the MOV failure rate was

unacceptable.

A task group consisting of. corporate engineering

staff, plant system engineers and operations personnel

had been

assigned to develop and implement a comprehensive MOV program.

The

implementation of the riew MOV program was well underway toward the

end of the assessment period.

The local leak rate test program implementing procedures and controls

were well executed and had improved since the previous assessment

period.

System features necessary to ensure containment integrity

were found to be adequately maintained.

Post-maintenance testing was identified as a weakness, as evidenced

by the fact that the licensee did not have in place a comprehensiv~

program that addressed post-maintenance testing.

The program that

was es tab 1 i shed to imp 1 ement * the testing requirements of American

Society of Mechanical Engineers (ASME)Section XI was informally

adapted to specify post-maintenance testing of components not covered

by the ASME Code.

Several

examples were identified where the

maintenance scope increased, yet the post-maintenance test require-

ments were not reviewed for adequacy.

In addition, an example was

identified involving the failure to perform adequate post-maintenance

18

testing following a major repair to a safety~related pressure control

valve.

The ASME Section XI 'inservice ~nspection (ISI) test program wis fou~d

to be generally sound,

although two examples were identified

regarding failure to adequately perform required testing.

Midway

through the as*sessment period the licensee issued a revised ISI

manual

that included both new and revised administrative and

non-destructive examination (NOE) procedures.

The admi ni strati ve

procedures established a more comprehensive control of ISI activities

and the NOE procedures, and in most cases, were an improvement over

previously used procedures.

NRC initiatives were well received by

the licensee**as evidenced by the establishment of guidelines

  • pertaining to second independent interpretations of radiograph film

and additional radiography being conducted when earlier results were

questionable.

Also, an extensive NOE program to identify erosion-

and corrosion-affected components within suspect piping systems was

impiemented.

Post-refueling startup test activities were reviewed for Unit 1,

cycle 10, which occurred early in the assessment period.

The

assessment of core physics data collected during the startup agreed

well with the predicted p~rformance criteria. The licensee continued

to maintain a sound approach to post-refueling startup activities.

The licensee responded positively to an NRC request for additional

engineering evaluations and testing to confirm power supplies to

plant equipment and train independence, and to conduct additional

load sequencing tests for the emergency diesel generators (EOG).

These requests were in response to SSFI inspections, feactor cavity

seal in~pections and licensee's identified items in areas of system

design control, system configuration control and system maintenance

practices. The licensee's s*taff demonstrated adequate technical and

operational skills in the preparation and performance of complex and

,integrated plant

system testing.

However,

deficiencies were

identified in testing of electrical emergency buses.

An example of

poor coordination and com~unication was noted during performance of

special* testing on the Unit 1 H bus.

In addition, an example of

failure to establish adequate initial plant conditi~ns for electrical

testing of the Unit 1 J bus was identified.

Management was actively

involved in correcting these problems. -

Surveillante tests were generally performed within the allowable time.

interval.

The licensee continued to integrate the data collected

from the predictive analysis group into the official surveillance

program.

A significant problem was identified, however, regarding

the failure to adequately test the capacity of the emergency service

water pumps and their* associated diesel start batteries. The pumps

were in fact found to be incapable of supplying an adequate makeup to

the ultimate heat sink following a design basis accident.

Inadequate

2.

19

surveillance testing was also identified regarding the verification

that the main control room envelope chillers were operating within an

acceptable performance envelope.

The above i terns contributed to

several Severity Level III violations with Civil Penalties.

Although not issued within the assessment period, a deviation was

identified during the SSFI for not including vendor 1 s equipment

maintenance recommendations into site procedures.

These vendor

recommendations pertained to operation of various MOVs, emergency

service water diesels and the recirculation spray heat exchangers.

The possibility existed that these problems could have been avoided

if full implementation of NRC Generic Letter 83-28, Required Actions

Based on Gener*ic Imp*lication~ of Salem ATWS Events,

had been

instituted by the licensee.-

The implementation of the secondary chemistry control program was

successful in maintaining water purity generally within the accepted

guidelines.*

However,

minimal

success in slowing the rate of

corrosion of the secondary system was achieved.

Corrosion products

continued to be transported to the steam generators (SGs) of both

units.* As. a result, large amounts of solid corrosion products were

removed from the SGs during the spring and ,fall of *1988 for Units 1

and 2, respectively. This provided evidence of pipewall thinning and

  • the formation of conditions within the SGs known to be conducive to

the corrosion and cracking of SG tubes.

The licensee had installed

an

on-1 ine monitoring system for principal secondary chemistry

parameters.

This system would a 11 ow corit i nuous monitoring and

trending of steam cycle chemistry along with computerized data

logging.

The low turnover rates and the resultant continuity of the

chemistry staff, backed up by a commendable training program and

adequate management sup~~rt, were licensee strengths.

Two Severity L~vel III violations, ten additional violations and one

deviation were identified during the assessment period.

Performance Rating

Category:

3

3.

Board Recommendations

The Board recognizes good performance in the areas of maintenance

training, leak rate testing, the ASME Section XI

ISI program,

post-refueling startup test activities and secondary plant chemistry

control. However, management attention is needed to assure improve-

ment of the PM program, the procurement of spa re and replacement

parts and the implementation of post-maintenance testing.

The Board

recommends a continued high level of inspection activity in this

area .

-.*

D.

20

Emergency Preparedness

1.

Analysis

During the assessment period, inspections were performed by regional

and resident staffs. Two routine inspections and two evaluations of

EP exercises were conducted.

The first routine inspection focused on the Emergency Pl an and

implementing procedures; emergency facilities; equipment, instrumenta-

tion, and supplies; organization and management control; training;

and the independent reviews of the ,EP program.

No violations were

identified during the inspection; however,

an off-hours callout

drill, which was requested by the NRC inspector, identified a problem

with augmenting the emergency organization.

The ca 11 out dri 11

consisted of the licensee calling individuals li*sted in the Emergency

Personnel Notification List and obtaining an estimate of the time

. required to respond to the site.

The callout drill did not clearly

demonstrate that the emergency organization could be fully staffed

within

the

required

times.

Also,

the

Emergency

Personnel.

Notification List that sec4rity personnel were going to use was.

several revisions out of date; this was corrected pri'or to the

callout drill.

Although the. liten~ee committed to take c6rrective

actions in this area, the timenness. of the augmentation staffing

continued to be a prob 1 em.

For ex amp 1 e, during the off-;-hour annual

emergency exercise, conducted on November 1, *1988, the excessive time

to activate the Technical Support Center (TSC), *ego* minutes), *and:

Local Emergency Operations Facility (LEOF), (150 minutes), with the

standard being 60 and 90 minutes, respectively, was a problem noted

by the licensee and the NRC.

Later, during the second routine

inspection of the* assessment period, the failure to meet the

Emergency Plan 1s augmentation staffing requirements within the times

set forth was identified as a violation.

The

annua 1 emergency exercise al so

i dent i fi ed the fa i 1 ure to

recognize and classify a Site Area Emergency as a significant

exercise weakness.

The classification was not made in a timely

manner and had to be prompted by the controllers. As a result of the

inability to classify the event, the licensee committed to conduct

retraining in needed areas and redo the exer~ise within approximately

90 days.

An additional problem area identified in the exercise was

the failure to provide accurate arid updated messages to the State and

local response organizations.

Although 1 icensee management appeared responsive in their concern

over the less than satisfactory exercise by committing to redo the

exercise, the remedial exercise that followed did not reflect the

increased management attention and involvement that the situation

2.

21

required.

Observations supporting this statement included the

minimally challenging scenario, the identification of a new exercise

weakness ad_dress i ng the fa i 1 ute to ma i nt_a in contamination access

control to the emergency response facilities, and a* repeat of the

excessive activation times for the TSC and LEOF.

In particular, the

TSC activation time was approximately 25 minutes greater than in the

previous exercise where the licensee had identified the excessive

times to activate as a deficiency requiring corrective action.

The

remedial exercise was successful for demonstrating the required

corrective action of properly classifying a radiological release and

adequately

providing

messages

to

state

and

local

response

organizations; however, a significantly improved overall level of

emergency response effectiveness was not demonstrated.

During April 1989, an inspection conducted noted that the licensee

had effectively ut i 1 i zed a computerized system to track emergency

response training; that. tbe early warning siren system had been

upgraded; and that the knowledge of classification procedures was

noted as a program strength.

The licensee, through a root cause

analysis approach, has categorized the outstanding EP deficiencies.

Corrective actions for these deficiencies commenced subsequent to the

end of the assessment period .

One violation was identified during the assessment period.

Performance Rating

Category:

3

3.

Board Recommendations

Observations during the assessment period indicated that- although

management expressed their awareness of a need for increased attention

to the EP program, only limited program improvements were actually

observed by the end of the assessment period.

Management attention

is needed to complete the actions the licensee identified necessary

to improve the EP program.

An increased NRC inspection effort is

warranted to monitor and asses~.program improvement.

E.

Security

1.

Analysis

During the assessment period, inspections were performed by the

resident and regional inspection staffs. The evaluation was based on

three routine inspections conducted by the NRC regional staff, in

which no violations were cited;* however, one licensee identified

violation was identified relative to the reliability of the vital

area door locks .

22

The . 1 icensee provided eJ<cel lent security* i_n. accordance with the

requirements of its . NRC""approved

Physi d.l -security . Pl an.

The

licensee retained a some'v/hat unique security organization in that the

site. security force, a *propri-efary force, reports directly to the*

off-s.ite Corporate Director._o.f Nuclear Security, and indirectly

i hterfaces with the on-s_ite Pl ant Manager.

These two management

chains provided very goo~ daily operational support.

The daily performance of the security force and its on-site

supervisor and management was the single greatest strength of the

licensee's program for site security.

Day-to-'day operations of the

security shifts continually met and exceeded NRC criteria and the

1 icensee

committed TS

requirements.

In spite of hardware and

equipment deficiencies, the security force performed at superior

levels.

The 1 i censee I s corporate security department performed numerous

audits o.f the contractor's personnel screening programs, including

the adm1nistration of psychological tests.

At the corporate QA

1 eve 1, * the 1 i cen see continued to experience aggressive annua 1 audits

of its security program:

During the licensee's annual 1988 security

audit, a negative finding was reported relative to the time needed to

complete repairs of degraded security equipment.

A repair time of 11

days versus the 1 icensee' s goal of 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> was considered to be

excessive.

There were multi-examples of this deficiency.

While

station outages could have explained some of this delay,_ the NRC

concurred with the auditor's findings and considered this to be an

area where plant support could be improved.

A review of the negative

findings

found

in security inspections (vital area door lock

maintenance, upkeep of the isolation zone; and upkeep of safeguards

cabinets) supported the conclusion that a more effective working

relationship between the security and maintenance organization was

needed.

The proprietary- security force had a minimal t_urnover rate, overtime

did not appear excessive, and the. shifts appeared extremely wel 1

supervi sect and staffed'.

Procedures were very clearly written, and

other documentation was readily available for regulatory tracking

purposes.

Training and requalification continued to be a strong

  • point.

Contingency tactical drills appeared realistic and were run

frequently such that each shift was exercised.

Close liaison with

off-site response authorities was also noted.

The licensee's security staff implemented a personalized briefing of

persons who were badged for unescorted access to the station.

This

special briefing addressed required duties and responsibilities

associated _with *being granted unescorted access.

The NRC considered

that this new briefing concept at the time of badging was a positive

F.

2.

23

training attribute with regard to implementation of personnel

awareness of security requirements at the station.

The licensee's use of continuously manned stationary defensive

positions (bullet resistant towers) has assured rapid and accurate

assessment and resolution of protected area perimeter alarms.

Compensatory measures were adequately implemented at the perimeter

barrier through the use of officers in defensive positions.

Five

changes to security plans were

submitted pursuant to

10 CFR 50.54(p).

Licensee changes to the security plan met the

reporting requirements of 10 CFR 50.54(p) with respect to timely

notification; however, the changes were not always consistent with

the provisions of the regulation regarding decreases in plan

effectiveness.' There was one request for which the 1 icensee 1 s

processing of changes could have been enhanced by more communication

with the NRC staff prio~ to the submittal.

The explanations which

were included with the submittal did not always provide an adequate

synopsis of the actual

rev1s1ons.

For example, changes were

evaluated by the licensee and considered editorial or minor, while,

in fact they were more substantive and related to access authori-

zation, materials search and equipment

No violations were identified during the assessment period.

Performance Rating

Category:

1

3.

Board Recommendations

The excellent quality of personnel, procedures and training are

recognized by the Board.

The special security briefing is also- a

strength.

Timeliness

of equipment

repairs

needs

management

attention.

Reduced inspection effort should be considered.

Engineering/Technical Support

1.

Analysis

Evaluation of the Engineering/Technical Support functional area was

based on routine and special inspections conducted by the NRC in this

and other functional areas.

Special inspections conducted were an

SSFI on service water and an AIT inspection of the reactor cavity

seal event.

This area addresses the adequacy of technical and

engineering support for all plant activities.

The area includes

licensee activities associated with plant modifications, technical

support - provided

for

operations,

maintenance,

testing

and

surveillance, training, and configuration management.

24

Poor performance of the engineering department was demonstrated by

the calculations produced to support operability of the service water

system and recirculation spray heat exchanger.

This issue resulted

in a Severity Level III violation with a Civil Penalty .. The

evaluations used to determine if the service water system met design

requirements lacked detail and,did not include an in-depth review of

critical data.

The calculations also utilized invalid assumptions.

The evaluation focused on verifying a conclusion that the design

basis requirements were met rather than providing a review of all

pertinent aspects of system performance.

The errors in the service

water system calculations, which were accomplished early in the

assessment period, demonstrated that the engineering department did

not fully util*ize existing regulatory guidance relative io the design

and review process.

Consequently, the licensee failed to reach

adequate conclusions on the operability of the service water systems.

Recirculation heat exchanger calculations utilized inaccurate and

nonconservative design assumptions and inputs.

Environmental effects

on safety related components and control of mechanical specifications

were also elements of weakness in the recirculation heat exchanger

calculations.

Calculations for reactor coolant leakage surveillance employed

incorrect values for constants which provided the potential for

underestimating RCS leakage.

The error in RCS leakage calculations

could have resulted in acceptince of unidentified leakage in excess

of TS limits.

A violation was issued concerning the use of the

incorrect constants.

During the first portion of the assessment period, engineering

involvement was minimal in evaluation and resolution of significant

problems with MOVs.

Engineering did not review MOV actuator test

results in order to evaluate ~efic~encies and determine corrective

actions.

Deficiencies written on MOVs were not evaluated for root

causes, and MOV engineering sketches were inadequate.

The lack of

engineering review of MOV problems resulted in a violation for

failure to properly identify and correct MOV deficiencies.

As a

result of the above discrepancies, a task team was established in the

latter portion of the assessment period and provic:led a positive

impact on the resolution 6f MOV deficiencies.

Early in the assessment period, the engineering organization had not

demonstrated an adequate self-assessment capability.

A specific

example was the lack of administrative control for the backlog of

potential problem reports which were generated i ri the corporate

offices.

Incorrect assessment of safety significance of outstanding

issues was identified as a problem area.

This condition became

obvious when

significant safety issues (i.e., emergency diesel

generator

sequencing

problems

and

control

room

envelope air

conditioning/ventilation problems) were first addressed in the

licensee 1 s corrective action program approximately two years after

25

they were identified.

Also, during review of outstanding station

EWRs for appropriate disposition as a part of the restart ~ffort,

severa 1 of the o 1 der EWRs were .di sc:overed to be i ncomp 1 ete and not

properly closed out.

These conditions indicated that the programs

for proper disposition and ~l oseout of engi neeri n_g documentation

appeared to be ineffective.

Tech~ical support weaknesses were also evident in plant EWR procedure

quality.

Examples of these weaknesses were identified as violations

for failure to ensure that proper technical reviews were being

completed prior to returning safety-related components to service,

and failure to provide ~dequate instructions in EWRs relating to

safety-related activities.

In addition, the* technical staff was

using the EWR process to perform plant modifications, which resulted

in inadequate technical reviews for addition of heat lbads to plant

air conditioning/ventilation systems and improper modification of the

reactor cavity seal backup air supply system without implementating

fequired *drawing revisions.

The above problems were also indicative

of a lack of adequate training of engineering personnel.

The issues identified by the SSFI and AIT resulted in management 1s

recognition of existing *deficiencies in engineering and technical

support.

Improvements

initiated included increased resources,

engineering

improvement

programs,

and

reorganization of the *

engineering department.

A Design Basis Documentation (DBD) Project

which encompasses 80 plant systems was initiated.

The program

consists of. six phases, from document collection to approval and

final issuance of the final DBD.

For the first seven systems, phases

one and two have been completed.

The third phase,

i nvo 1 vi ng

component design basis, was on schedule.

Identification by the licensee of an actual configuration problem in

the middle of the assessment period resulted in a program to verify

the integrity of the Unit 1 plant configuration in accordance with

emergency

procedures.

The

ORAP

represented

a

considerable

engineering commitment of resources to ensure that actual plant

configuration was in accordance with approved pl ant drawings and

procedures and also ensured that divisional power supplies to

safet~-related compo~ents were correct.

During the assessment period, the licensee realized that the

engineering staff was not focusing appropriate resources to the needs

of the station.

In order to correct this condition, the licensee

reorganized the engineering department and established a larger

engineering staff at each nuclear station. The formation of a system

engineering group and a design engineering group provided a major

improvement potential.

A reorganization of technical resources

provided consolidation of nuclear support resources on the corporate

  • level arid a stronger on-site engineering presence.

This reorgani-

zation appeared to .be a strength, in that during the latter part of

2.

3.

26

the assessment period,* increased systems and design engineering

capabilities on-site allowed for more timely resolution of Unit 1

restart technical issues.

Technical support related to EQ was good.

The engineering staff was

kn owl edge ab 1 e of . EQ issues and NRC-i dent i fi ed defi ci enci es were

resolved.

Operator training, as evidenced by the performance on the replacement

examination, was effe-ct i ve.

A 11

12 candidates passed both the

operating and written portions of the examination.

Reference

material sent to the NRC for exam preparation was well organized and

detailed.

The quality of the reference ~aterial and a review effort

by the licensee prior to the exam contributed to it's high quality.

'

.

Training facilities and instructor quality continued to be one of the

strengths.

This was particularly evident during the latter part of

the assessment period.

During this timeframe, additional training

was conducted with regard to new system modificati6ns and operating

requirements.

In addition, special refresher training was provided

to operators for Unit 1 restart and was conducted in an excellent

manner.

Training* for the maintenance craft was found to be adequate.

The training pregram maintained full accreditation with the National*

Academy for Nuclear Training. Also, all programs at the* station have

received

accreditation

from

the Institute of Nuclear

Power

Operations.

Construction was completed on a large addition to the training center

complex.

The new structure includes nine additional classrooms, new

instructor offices,

five

laboratories

(mechanical,

electrical,

chemistry, HP, and instrumentation and control), a technical library,

and a practical factors area for general employee training.

This

modern training addition provides facilities for the station to

properly train personnel in all requisite areas and is expected to

increase plant proficiency in -the future.

One Severity Level III problem, composed of four violations, one

additional violation and one deviation were identified during the

assessment period.

Performance Rating

Category:

2

Board,Recommendations

Management needs to continue the improvement of engineering support

to the station and to closely monitor the engineering organization

for effectiveness.

The reorganization of the engineering organi-

zation, the initiation of the Design Basis Documentation effort and

)

27

the conduct of the ORAP provided indication that *this area was

improving.

Based on the mixed performance in this area, the Board

had difficulty in determining the .final performance rating. A high

level of inspection effort should be maintained.

G.

Safety Assessment/Quality Verification

1.

Analysis

During the. assessment period, inspections were performed _by the

resident and regional inspection staffs and licensing reviews were

conducted by the NRR staff.

Inspections evaluated the licensee 1s

corrective action

program,

performance

of appropriate

safety

evaluations, root cause analysis of plant events, the corporate

offsite independent review group 1 s functions, the licensee 1 s on-site

safety committee functions, and the quality function as used in the

monitoring of the overall performance of the plant.

During the early part of the assessment period, significant

weaknesses in plant and corporate management leaderihip and skills

resulted_ in lower than desired expectations and accountability.

These weaknesses were illustrated by multiple examples dealing with

the failure to take aaequate corrective actions, and the failure to

conduct appropriate safety and root cause evaluations._ These problem

areas resulted in several. Severity Level III violations with Civil

Penalties.

Numerous examples of management 1s failure to take adequate corrective

actions, as exemplified in the last assessment period by the failure

to verify boric acid heat tracing operability, _continued to be

identified in this assessment period.

These examples were as follows:

the Unit 1 reactor cavity seal failure event, where management failed

to take necessary corrective action due to not understanding the

event, as .discussed in the Plant Operations section; the failure to

identify and correct a longstanding adverse condition involving

inadequate housekeeping and improper maintenance of the containment

sumps, as discussed in the Maintenance/Surveillance section; the

failure of the licensee 1s corrective action program to identify a

potential for gas binding of safety-related pumps;. the failure to

promptly identify a degraded condition of the control room and*

emergency switchgear ventilation system; the failure to promptly

correct leakage of water around safety-related pump room roof plugs

until prompted by the NRC; and failure to completely resolve a

non-original

equipment

manufactured parts

problem

when

first

discovered several years ago.

-

The preceding examples of failure to take adequate corrective actions

were mostly identified in the first half of the assessment period.

After identification of the programmatic deficiencies, licensee

management took action to change the threshold for identification of

28

conditions adverse to quality.

During the latter part of the

assessment period, licensee-identified station deviation reports

increased by a factor of lO over previous numbers and problem

identification sensitivity of the station staff was improving.

Weaknesses with regards to proper safety reviews were identified in

the last assessment period, as exemplified by a failure to properly

evaluate the consequences of an event which involved a worker 1 s

unnecessary exposure to an extremely high radiation field.

This type

of problem continued to be identified during this assessment period.

Four previously discussed examples highlighted this continuing

weakness.

In addition, the lack of management sensitivity to safety evaluations

of degraded conditions at the beginning of the assessment period was

evident.

An example was during the restart of Unit 1 in July 1988,

when senior station management indicated to licensed operators that

Un.it 1 heatup should continue even though the operators had indi-

cation of containment boundary leakage which required the unit to

retur~ to cold shutdown.

The

preceding examples

of failure to conduct proper safety

evaluations were mostly identified in the first half of the

assessment period. After identification of the programmatic problem,

licensee management

1 s attitude and sensitivity to the conduct of

proper safety evaluations and reviews improved. During the latter

part of the assessment period, frequent monitoring of the station

safety committee meetings and other event reviews indicated an

improvement in this area.

Another problem area that was identified. during the previous

assessment period and continued into this assessment period was

inadeq~ate root cause analysis of events, failures, and/or condition5

adverse to quality.

-

The licensee recognized in the latter part of the assessment period,

that root cause evaluations were not being accomplished.

After

identification of the problem, the licensee implemented a root cause

analysis procedure at the station focusing on system engineer

eva 1 uat ions.

However, a forma 1 corporate root cause eva 1 uat ion

program was not initiated until near the end of the assessment

period.

A weakness was also identified with the licensee 1 s capability to

properly track regulatory commitments and ensure that measures were

in place to prevent their deletion from a procedure without proper

review.

An example of this problem occurred when abnormal procedures

were revised in response to an NRC Bulletin commitment.

Due to a

lack of proper tracking, this commitment was deleted in a later

procedure revision, contributing to inadequate operator response

during the cavity se~l leak event.

This problem was indicative of a

29

significant weakness with regards to ensuring compliance with

commitments.

During the latter part of the assessment period, an evaluation of the

1 i censee I s self assessment capability was cdnducted.

The assessment

concluded that the on-site review committee was performing an

adequate review as required by TS.

However, a major weakness was

observed during the review of the corporate independent review group.

The review, which resulted in a violation, concluded that this group

was not complying with TS because they were not conducting the

required reviews of all safety evaluations, violations, reportable

events, and on-site safety review committ~e actions. The review also

concluded that this TS function had not been complied with for an

extended period of time.

Based on these observations of the off-site

review function it appeared that corporate management did not

effectively use self-assessment to assure quality in activities.

The licensee's initial approach to the resolution of technical issues

from a safety standpoint contained in NRC Bulletin 85-03, MDV Common

Mode Failure~ During Plant Transients Due

to Improper Switch

Setting~, was neither conservative nor thorough.

The MDV Task Team's

subsequent design review identified deficiencies that should have

been identified during the bulletin review.

Also, numerous station

deviati~ns were written on valves covered by the bulletih after the

1 i cen see reported comp 1 et ion of the program.

The same type of

inadequate review was cor:iducted of NRC Bul 1 et in 84-03, Refue 1 i ng

Cavity Water Seal, and was noted as part of the cause of the cavity

seal event discussed earlier in this functional area.

Licensee submittals such as amendment requests and relief requests

were of good quality and submitted in a timely manner.

The licensing

staff was professional and thorough and 1n most instances scrutinized

their submittals for both technical content and conformance with

regulatory requirements.

Increased use of technical personnel on audit activities resulted in

audit findings of greater technical substance than in the previous

assessment period.

The method for closing audit findings, including

the recurrent ones, was changed in August 1988.

This new method

involved evaluating the corrective action for an audit finding, on

more than one occasion and then presenting the decision to close a

finding for approva 1 by the manager of the audit group.

Specific

QA/QC problems were identified, though, during conduct of the SSFI in

the middle of the assessment period. A violation was noted in which

QC identified work orders containing design change deviations and

nonconformances that were not addressed in the corrective action

program.

In addition, effective maintenance activity corrective

actions had not been taken as evidenced by recurrent QA audit

findings.

After identification of these QA/QC problems, the QA

v.

A.

2.

30

department t,ook appropriate actions.

All of the significant defi-

ciencies discussed in this functional area were not aggressively

identified and pursued through the use of the licensee's QA program.

Late in the assessment period, though, the QA organization demon-

strated an improved capability to identify problems in safety-related

plant activities.

This conclusion was based on monthly discussions

between the resident inspector and QA management.

During the latter part of the assessment period, some of the

aforementioned changes did provide an indication that problems

attri butab 1 e in pa'rt to an inappropriate management attitude and

significant weaknesses in plant and corporate management leadership

and ski 11 s * were changing. Past management practices which had

resulted in lower than.desired expectations' and accountability were

also improvtng. A positive change with regards to sensitivity and a

lack of attention to detail was also noted.

The licensee's ORAP,

which was instituted in January 1989, and the management restart

readiness confirmation which was conducted prior to Untt 1 re~tart

were indicative that past programmatic problems were being addressed.

Three Severity Level III problems, composed of eight violations, one

Severity Level III violation and one additional violation were

identified during the assessment period.

Performance Rating

Category:

3

Trend:

Improving

3.

Board Recommendations

Management needs to continue the imp 1 ementat ion of the corrective

action, safety assessment and root cause analys-i s programs that

successfully- improved the performance in the latter part of the

assessment period. The Board recognizes that late~ in the assessment

period management was demonstrating an improved sensitivity toward

safety issues.

Inspection effort in this area should remain high.

SUPPORTING DATA AND SUMMARIES

Investigation Review

None.

B.

Escalated Enforcement Action

1.

Violations

Severity Level III violation issued on June 13, 1988 for failure to

31

verify operability of re qui red boric acid heat trace circuitry as

required by TS

(CP -

$50,000).

This violation occurred in the

pre~ious assessment period, but was issued during this period.

Severity Level III violation issued on June 13, 1988 for failure to

adequately evaluate radiation hazards, have adequate procedures, and

follow procedures while working on a stuck incore detector.

(CP -

$100,000).

This violation occurred in the previous assessment

period, but was issued during this period.

Severity Level III problem, composed of eight violations, issued on

August 25, 1988 for failure to control an individual 1 s occupational

radiation dose to less that 3 rems per calendar quarter and to meet

other 10 CFR 20 occupational dose requirements.

(CP - $100,000).

Severity Level III violation issued on November 10, 1988 for failure

to have adequate procedures to ensure that system cleanliness and/or

foreign material exclusion was being maintained on safety-related

systems.

(CP - $50,000).

Severity Level III violation issued on May 18, 1989 for failure to

provide adequate procedures for operation and testing of the

  • inflatable seal portion of the reactor cavity seal. (CP - $100,000).

Severity Level III problem, composed of two violations, issued on May

18, 1989 for failure to conduct an adequate 10 CFR 50.59 evaluation

of the reactor cavity seal design and failure to conduct an adequate

evaluation of the cavity seal failure event.

(CP - $100,000).

Severity Level III vi.ohtion issued on May 18, 1989 for failure to

promptly identify and correct a significant condition adverse to

quality involving potential gas binding of the high pressure safety

injection pumps.

(CP - $75,000).

Severity Level III problem, composed of two violations, issued on

M~y 18, 1989 for failure to promptly identify and correct significant

conditions adverse to qua 1 i ty i nvo l vi ng

inadequate capacity of

control

room

chillers

and

degraded

condition

of

control

room/emergency switchgear room ventilation system.

(CP - $50,000).

Severity Level III problem, composed of four violations, issued on

May 18, 1989 for failure to promptly identify and correct significant -

conditions adverse to quality with regard to the use of non-qualified

replacement

parts

for

safety related

components,

wetting

of

safety-related electrical components, and lack of implementation of

an effective component failure trending and root-cause analysis

program.

(CP - $50,000).

Severity Level III problem, composed of four violations, issued on

C.

32

May 18, 1989 for failure to correctly translate into specificitions,

drawings and procedures the design bases for operabi 1 i ty of the

recirculation spray heat exchangers and the emergency service water

pump house equipment; the effects of added loads on the-125 VDC vital

bus batteries; and the effects of minimum wa 11 thickness for a

component cooling water heat exchinger.

(CP - $25,000).

Severity Level I II. vi o 1 at ion issued on May 18, 1989 for failure to

comply with TS requirements re 1 ated to fl owrate operability of the

emergency service water pumps.

(CP - $100,000).

2.

Orders

None.

Management Conferences

1.

June 8, 1988

2.

July 6, 1988

Technical meeting at Region II to discuss issues

on recirculation spray heat exchangers.

Enforcement Conference at Region II to discuss

the Radiation Protection Program.

3.

September 16, 1988

Enforcement

Conference

at

Region

I I

on

4.

October 26, 1988

safety-related sump cleanliness issues.

Management meeting at NRC Headquarters on the

cavity seal event,

service water SSFI,

and

restart issues.

5.

November 17, 1988 _ Management meeting at the station to review the

status of the Radiation Protection Program.

6.*

December 8, 1988

Technical meeting at NRC Headquarters to discuss

EOG sequencing issues.

7.

December 22, 1988

Technical meeting at NRC Headquarters to discuss

8.

January 5, 1989

9.

January 26, 1989

restart issues.

Management meeting at Region II to discuss

restart issues.

Enforcement Conference at Region II on design

control and corrective action problems affecting

v~rious plant systems.

10.

February 28, 1989

Management meeting at the station on current

issues,

configuration management,

ORAP,

and

restart issues .

11.

March 30, 1989

12.

April 19, 1989

13.

April 26, 1989

14.

May* 22, 1989

33

Technical/Management meeting at NRC Headquarters

on restart issues.

Techriical meeting at NRC Headquarters to discuss

fo~lowup on masonry wall design.

Management meeting at Region II ori the overall

improvement action plan.

Management meeting at the station to discuss the

status of restart issues.

D.

Confirmation of Action Letters

E.

F.

1.

September 6, 1988

Refueling cavity seal leakage.

2.

November 2, 1988 *

Surry res ta rt issues

3.

March 9, 1989

Surry restart issues

Review of Licensee Event Reports (LERs)

During the assessment period 67 LERs for Unit 1 and 2 were analyzed.

The

distribution of these events by cause,. as determined by the NRC staff, was

as fo 11 ows:

Cause

Unit 1

Unit 2

Total

Component Failure

20

10

30

Design

10

0

10

Construction, Fabrication,

1

1

2

or Installation

Personnel

- Operating Activity

9

1

10

- Maintenance Activity

1

2

3

- Test/Calibration Activity

7

2

9

- Other

0

0

0

Other

2

1

3

Total

50

17

67

Licensing Activities

In support of licensing actions, frequent meetings were held with the

licensee to address licensing and other technical issues.* During this

assessment period there were 50 licensing actions completed, i.e., 22

amendments, 8 reliefs, 12 Multi-Plant Actions (MPA), 2 exemptions, and 6

other licensing actions .

G.

H.

34

Enforcement Activity

ENFORCEMENT ACTIVITY

FUNCTIONAL

NO.- OF VIOLATIONS/PROBLEMS IN SEVERITY LEVEL

AREA

Dev.

V

IV

III

II

I

Plant Operations

0

0

2

1*

0

0

Radiological Controls

0

1

5

1

0

0

Maintenance/Surveillance

1

1

9

2

0

0

Emergency Preparedness

0

0

1

0

0

0

Security

0

0

0

0

0

0

Engineering/Technical

1

0

1

1

0

0

Support

Safety Assessment/

0

0

1

4

o*

0

Quality Verification

TOTAL

2

2

19

9

0

0

Reactor Trips

a.

Unit 2 on May 16, 1988, from 100% power. * Event was due to an

undetermined fa i 1 ure of the e 1 ectro-hydraul i c contra 1 system which

caused the main turbine governor va 1 ves to close resulting in a

low-low level SG automatic reactor trip.

b.

Unit 1 on August 15, 1988, from 100% power.

Event was caused by a

spurious

actuation

of the

11A

11-train-Hi

consequence

limiting

safeguards relay during the performance of a normal surveillance test

procedure resulting in the automatic reactor trip.

c.

Unit 2 on September 10, 1988, from approximately'4% power.

Event was

caused by erratic operatfon of a governor valve controller which

caused the first stage impulse pressure to increase greater that 15%.

When impulse pressure increased greater than 15%, with the generator

output breakers open, a turbine trip signal tripped the main turbine.

The impulse pressure increase also caused permissive P-7 to reinstate

(P-7 indicates reactor power greater than 10%)~

An automatic reacto~

trip was then initiated due to the turbine trip with permissive P-7

reinstated.