ML18151A890

From kanterella
Jump to navigation Jump to search
SALP Repts 50-280/88-05 & 50-281/88-05 for Sept 1986 - Apr 1988
ML18151A890
Person / Time
Site: 05000000, Surry
Issue date: 07/26/1988
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18151A633 List:
References
50-280-88-05, 50-280-88-5, 50-281-88-05, 50-281-88-5, NUDOCS 8808100291
Download: ML18151A890 (45)


See also: IR 05000280/1988005

Text

  • .

4 .

ENCLOSURE 2

SALP BOARD REPORT

U.S. NUCLEAR REGULATORY COMMISSION

REGION I I

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

INSPECTION REPORT NUMBER

~gRs100291 aao726

G

ADOCK 05000280

PNU

50-280/88-05 AND 50-281/88-05

Virginia Electric and Power Company

Surry Plant Units 1 and 2

SEPTEMBER 1, 1986 - APRIL 30, 1988

r ** *---.,*-**,c ** o; ,* r~

... _*: :*. ',---,.: .. ".,

.

---

-

.

. . .

.-.*--*

. .

2

I.

INTRODUCTION

The Systematic Assessment of Licensee Performance ( SALP) program is an

integra~ed NRC staff effort to collect available observations and data on

a periodic basis and to evaluate licensee performance based on this

information.

The SALP program is supplemental to normal regulatory

processes used to determine compliance with NRC rules and regulations.

The SALP program is intended to be sufficiently diagnostic to provide a

rational basis for allocating NRC resources and to provide meaningful

guidance to licensee management in order to promote quality and safety of

plant construction and operation.

An NRC SALP Board, composed of the staff members listed below, met on

June 21, 1988, to review the collection of performance observations and

data to assess licensee performance in *accordance with guidance in NRC

Manual Chapter 0516, "Systematic Assessment of Licensee P~rformance

11 *

A

summary of the guidance and evaluation criteria is provided in Section II

of this report.

This report is the SALP Board's assessment of the licensee's safety and

management performance at Surry for the period September 1, 1986, through

April 30, 1988.

SALP Board for Surry:

C. Hehl, (Chairman) Deputy Director, Reactor* Projects Division (DRP)

H. Berkow, Director, Project Directorate II-2, Nuclear Reactor

Regulation (NRR)

E. Merschoff, Deputy Director, Reactor Safety Division

W. Cline, Acting Director, Radiation Safety and Safeguards Division

B. Wilson, Chief, Reactor Projects Branch 2, DRP

C. Patel, Projects Manager, NRR

W. Holland, Senior Resident Inspector, Surry, DRP

Attendees at SALP Board Meeting:

F. Cantrell, Chief, Reactor Projects Section 2A, DRP

K. Landis, Chief, Technical Support Section (TSS), DRP

S. Shaeffer, Technical Support*Engineer, DRP

M. Scott, Project Engineer, DRP *

T. MacArthur, Radiation Specialist, TSS, DRP

L. Nicholson, Resident Inspector, Surry, DRP

I I.

CRITERIA

Licensee performance is assessed in selected functional areas depending on

whether the facility has been in the construction, preoperational, or

operating phase during the SALP review period.

Each functional area

normally represents an area which is significant to.nuclear safety and the

environment, &nd which is a normal programmatic area.

Some functional

areas may not be assessed because of little or no licensee activity, or

,

  • .. , ...... ~*
  • -

. *"** ......

.

-~

'. ' .~

3

because of a lack. of meaningful NRC observations.

Special areas may be

added to highlight significant observations:

One or more of the following evaluation criteria was used to assess each

functional area; however, the SALP Board is not limited to these criteria

and others may have been used where appropriate.

A.

Management involvement in assuring quality

B.

Approach to the resolution of technical issues from a safety

standpoint

C.

Responsiveness to NRC initiatives

D.

Enforcement history

E.

Operational and construction events (including response to, analysis

of, and corrective actions for)

F.

Staffing (including management)

G.

Training and qualification effectiveness

Based upon the SALP Board assessment, each functional area evaluated is

classified into one of three performance categories.

The definitions of

these performance categories are:.

Category 1:

Reduced NRC attention may be appropriate.

Licensee

management attention and involvement are aggressive and oriented

toward nuclear safety; licensee resources are ample and effectively

used such that a high level of performance with respect to

operational safety or construction quality is being achieved.

Category 2:

NRC attention should be maintained at normal levels.

Licensee management attention and involvement are evident and are

concerned with nuclear safety; licensee resources are adequate and

are reasonably effective such that satisfactory performance with

respect to operational safety or construction quality is being

achieved.

Category 3:

Both NRC and 1 icensee. attention should be increased.

Licensee management attention or involvement is acceptable and

considers nuclear safety, but weaknesses are evident; 1 i censee

.resources appear to be strained or not effectively used such that

minimally satisfactory performance with respect to operational safety

or construction quality is being achieved.

The functional area being evaluated may have some ~ttributes that would

place _the evaluation in Category 1, and others that would place it in

either Category 2 or 3.

The final rating for each functional area is a

composite of the attributes tempered with the judgment of NRC management

as to the significance of individual items.

The SALP Board may also include an appraisal of the performance trend of a

functional area.

This performance trend will only be used when both a

definite trend of performance within the evaluation period is d1scernable

.. _, "".*~* * .n ** * ~

  • *

,>-'"';. * ...,. .... ,- ,., * ** ,* * *

      • * ** ,**~-,-..-,*-, *"'

-

~. v ... -- ** **


.-,.**-*p-****'

. *-*-- -*

----... --. -

4

and the Board believes that continuation of the trend may result in a

change of performance level.

The trend, if used, is defined as:

Improving:

Licensee performance was determined to be improving near the

close of the assessment period.

Declining:

Licensee performance was determined to be declining near the

close of the assessment period.

III. SUMMARY OF RESULTS

'

.......... *****' ~** .. .

A.

Overall Facility Performance

The Surry nuclear power station is staffed and managed by qualified

personnel with a broad background and many years of experience in the

nuclear operations area. Station management changes were made in the

Summer of 1987, due to normal company rotation policies. The station.

manager was transferred to the corporate office, the assistant

station manager for operations and maintenance was promoted to

station manager, the assistant station manager for nuclear l{censing

and safety was promoted to assistant station manager for operations

and maintenance, and the techn i ca 1 services superi n.tendent was

promoted to assistant station manager for nuclear licensing and

safety.

In .addition, new selections were made in the operations,

maintenance, and technical services superintendent positions* and in

the site quality assurance manager position during this assessment

period.

The changes were implemented with no adverse impact on

station operation. It should also be noted that all station senior

, management positions are presently filled with persons who held

Senior Reactor Operator licenses in previous positions with Virginia

Electric and Power Company (VEPCO) prior to reaching their present

management positions.

Corporate

senior management

involvement

in

plant performance

continues to be

!!Vi dent based on ongoing performance i ndi ca tor

monitoring, and the excellent manner in which the company handled the

Unit 2 feed pump suction piping rupture event, which occurred in

December, 1986.

A change in corporate management occurred 1 ate in

the SALP period due to r~organization of the company.

A new vice

president for nuclear operations was installed when the former vice

president was promoted to senior vice president in charge of all

power operation.

Also, the* corporate Quality Assurance Office

increased its effort in providing station management with a means to

review programmatic problem areas and provide appropriate feedback on

problem causes and recommendations for correciive actions.

This

effort has been evident in reviews by the inspectors of maintenance

and operations activities.

Dur.ing the SALP period, the Surry facility had high availability, with

th~ exception of outages on both units associated with inspection and

repair of the feedwater and condensate lines after the Unit 2

.* ._,... ... .t--*--.... -.. ~'"-"'
    • -*-,-... --:*-:--** ---** -- *..

. -- .-..... ---- ......

.. . .. ,. '.* **-" , . ....,,, .... ~.~ '~ ***-.

5

feedwater suction line rupture; and fewer than the industry average

of reactor trips.* During the period, Unit 1 had 5 total reactor

trips (3 automatic and 2 manual) and Unit 2 had 4 total reactor trips

(2 automatic and 2 manual).

This equates to 1.8 automatic reactor trips per year for Unit 1* and 1.2 automatic reactor trips per year

for Unit 2; and this is an improvement over the last SALP period.

In

addition, these automatic trip rates remain below the 1987 industry

average of 3.24 automatic reactor trips per year.

Of the five *

reactor trips for Unit 1, three of these trips were caused by

equipment failures, one was caused by human error, and one was caused

by a combination of human error and equipment failure.

In addition,

Unit 1 had to be shut down once because of high leakage of the

reactor coolant from a loop isolation valve, and once because of

leakage from a main steam trip valve. Of the four reactor trips for

Unit 2, two of these trips were caused by equipment failure, and two

trips were caused by human error.

Regarding

occupational* radiation exposure, data available for

calendar year 1987 inoicate that a total exposure of 712 person-rems

was received by personnel at the Surry station.

This represents a

substantial reduction in occupational exposure for the Surry units.

The

licensee

has

made

significant

improvement

in

reducing

occupational doses to the workers.

The licensee performed satisfactorily in all functio*nal areas as

indicated in the performance analysis of this report.

However,

during the latter part of the period, inadequate management attention

contributed to escalated enforcement actions relating to operability

of heat trace circuits in boric acid flowpaths, and a potential for

overexposure of personnel during maintenance on an i ncore flux

detector.

Referring to subparagraph B below, three functional areas

have changed category level since the last SALP period.

Plant

operations and fire protection have declined to level two, while

training and qualification effectiveness has risen to a level one.

The functional area of radiological controls remained a level two

with a declining trend.

As indicated in the operations section of

this report (IV.A), lack of attention to detail coupled with other

negative attributes accounted for the level change. The fire protec-

tion area (section IV.E) went to a level two based o~ 10 CFR 50, *

Appendix R, and fire fighting equipment problems identified during

the period. The training area was perceived to improve based on INPO

accreditation of all training programs, excellent operators' test

scores, and high marks on an NRC Balance of Plant inspection.

Radiological controls was rated as a level two, based on a generally

good performance over most of the SALP period.

However, due to

problems which occurred recently, *had the area been rated just for

the last three or four months, the rating may have been different.

In conclusion, the licensee is continuing with programs to implement*

new and innovative techniques to improve perf.ormance and quality 1n

the various disciplines involved in nuclear power plant operation .

--

6

These include an expansion of programs in which personnel from the

craft level in the maintenance areas, are being sent to observe

techniques employed by the French and Japanese at their nuclear

stations in order to improve performance at the licensee's s~ations.

Also, during this period, the licensee received full accreditation

from INPO for all of their trairiing programs.

8.

The performance categories for the current and previous SALP periods

in each functional area are as follows:

Functional Area

Plant Operations

Radiological Controls

Maintenance

Surveillance

Fire Protection

Emergency Preparedness

Security

Outages

Quality Programs and

Administrative Controls

Affecting Quality

Licensing Activities

Training and Qualification

Effectiveness

IV. PERFORMANCE ANALYSIS

A.

Plant Operations

1.

Analysis

Previous SALP

Dates

March 1, 1985

August 31, 1986

1

2

2

2

1

2

  • 2

2

2

1

2

Current SALP

Dates

September 1, 1986

April 30, 1988

2

2

2

2

2

2

2

2

2

1

1

During the assessment period, inspections of plant operations

were performed by the resident and regional inspection staffs.

Operations Summary:

s*oth units began the SALP period at full power operation and had

capacity/availability factors of 70.8/73.0 a.nd 64.3/67.5 percent

(Unit 1 and Unit 2, respectively) for the duration of the SALP

period.

Unit 1 entered a refueling/maintenance outage on

April 8, 1988, and Unit 2 completed a maintenance/refueling

outage during the period from October 4, 1986 to December 2,

1986.

Also, Unit 2 conducted a 16 day scheduled shutdown for

inspections and mairitenance in December 1987.

. .

. " .. *"" ..

- ....... ~ **:.-"""", ,**;** **,

.... .,.,.-r-,**. ,...

-.

  • . **** ***-?"*. ~ -~.-.

.

., I' (

  • -r--,* !~,,-

.*- ..

7

The

major

interruption to

power

operation occurred

on

December 9, 1986, when Unit 2 experienced the feedwater (FW)

pipe rupture (discussed below).

The uriit did not return to

operation for more than three months.

The licensee shut down

Unit 1 one day after the pipe rupture to conduct inspections and

repairs; the unit returned to operation about two months later.

On December 9, 1986, Surry Unit 2 experienced a major feedwater

pipe rupture accident which involved four fatalities. The event

was caused by erosion/corrosion phenomenon in carbon steel

piping containing a single phase fluid.

The licensee's initial

response and the follow-up actions were commendable.

The

licensee provided up-to-date information to the staff and the

media, and arranged for several presentations to provide the

information to the rest of the industry. Because of the generic

implication, the licensee elected to shut down Unit 1 from

December 10, 1986 to February 23, 1987 for inspection and

replacement of defective feedwater piping.

On June 23, 1987, Unit 1 experienced a primary coolant leakage

in excess of 40 gpm through a loop isolation valve.

The staff

was informed immediately and the unit was shut down manually in

an orderly fashion.

The licensee responded to the event in a

proper manner.

The operations summary indicates that with the exception of the

pipe break outage for both units, Unit 2 operated as planned

with only two unscheduled outages; one in the middle of the

period for main turbine balancing, and the other at the end of

the period for repair of an electrical component. *unit 1, on

the other hand, experienced one unscheduled outage early in the

period and nine unscheduled outages during the last eleven

months of the period. The Unit 1 outages lasted an average of 7

days each.

During this SALP period Surry Unit 1 experienced a tota 1 of

three automatic reactor trips and Unit 2 experienced a total of

two automatic reactor trips. This converts to an automatic trip

rate.of 0.28 per 1000 critiq.l hours for Unit 1 and 0.21 per

1000 critical hours for Unit 2.

These compare favorably with

the 1987 industry wide average rate of 0.43 trips per 1000

hours.

The Surry station continues to meet or exceed the

company goal of having no more than two automatic reactor trips

per unit per calendar year (two automatic for Unit 1, and one

automatic trip for Unit 2 during 1987) for the past two years.

Between September l, 1986 and April 30, 1988, Surry Units 1 and

2 experienced 5 and 4 reactor trips, respectively.

This

converts to a trip rate of 0.47 p~r 1000 critical hours (3.0 per

year) for Unit 1 and.0.39 per 1000 critical hours (2.4 per year)

'

  • ,-'""~ .... *. ,. ... ,,... .. :

' * ** * * ,-;-:"~' * - *,I*.,.

'*

--

. ... . -* .. , ... -............ -*.** .. .

8

for Unit 2.

These

rates are comparable

to the

1987

industry-wide average of 0.48 trips per 1000 critical hours (3.0

per year) for Westinghouse plants and are an improvement over

the previous SALP period.

Of the five reactor trips for Unit 1, three trips were automatic

and two trips were manual.

Three of these trips were caused by

equipment failures, one was caused by human error and one was

caused by a combination of human error and equipment failure.

In addition, Unit 1 had to be shut down once because of high

leakage of the reactor coolant from a loop isolation valve and

once because of leakage from a main steam trip valve.

Of the four reactor trips for Unit 2, three trips were automatic

and one was a manual trip. Three of these trips were caused by

equipment failure and one trip was caused by human error.

The Surry facility _has generally been adequately managed and

operated by the corporate office and plant staff during this

assessment period.

The operations staff was knowledgeable and

proficient in normal and emergency plant operations.

Their

response to the Unit 2 pipe rupture event in December 1986 was

excellent, and this performance carried over when required to

respond to transients and to the Unit 1 reactor trips in 1987.

However, lack of attention to detail during the -SALP period

which resulted in violations (b) through (e) of this section.

indicates that additional management attention is required to

minimize operator error during routine operation.

In addition,

violation (d) indicates a generic problem in the procedures area

with

regards

to

initial

conditions

identification

and

disposition of procedure changes.

When required, management

corrective actions are generally complete and technically sound

with appropriate effectiveness indicated.

The licensee's approach to resolution of technical issues from a

safety standpoint was demonstrated in the response to viola-

tion (d). The issues were understood by the licensee and timely

resolutions were provided with a technically sound and thorough

solution.

In addition, adequate training was provided to all

personnel involved in conducting evaluations for unreviewed

safety question determination; and positive results have been

observed during the last part of this period. However, near the

end of the rating period, a lack. of understanding of the boric

acid heat trace system* and management tolerance resulted in

que~tionable operability of the system for an extended period of

time, and resulted in a civil penalty violation that was issued

after the SALP period ended .

. A total of 79 Licensee Event Reports (LERs) were* submitted

during the SALP period.

These are addressed in Section V.H of

this report.

Of the LERs submitted,. four were ranked as

.

.-.*.

. . *. :*,* ; . .,.._._ ... , ... ~ .. ,~~* :" ...... ~. -*-: . . -. -.,---** ~ ........ .

' .

.

--

. . .

  • . ,..

.~ .. , .,.r*.

9

significant by the NRC screening process.

The most significant

event was the failure of a main feedwater pipe at Unit 2 due to

erosion/corrosion (This event has been repor~ed to Congress by

the NRC as an Abnormal Occurrence).

The licensee has submitted

an extensive re~ort (LER 281/86-020) and updates which provide

detailed descriptions of the event, causes and corrective

actions.

Two

of the significant LERs describe improperly

installed Raychem splices (LER 280/86-035 and 281/86-018).

The

fourth significant LER desctibes a loss of service water to the

charging pump service water subsystem which occurred due to a

leak in the blowdown line for the in-line service water strainer

(LER 280/86-029).

A large number (12) of LERs associated with the service water

system was observed, especially problems with control/relay room

chillers which were attributed*to low service water flow due to

clogged service water strainers. These events indicate that the

licensee had not taken action to correct the root causes of

these problems; however, additional actions are being taken

during the current Unit 1 refueling outage.

NRC review of the significant events which occurreQ during the

SALP period found that, in each cise, th- licensee had submitted

LERs which adequately addressed the reportable events.

Corporate interest in station activities continues at the

appropriate levels with the "Nuclear Performance Monitoring -

Management Information Report" continuing to provide appropriate

station management attention tq areas being reported.

Utility

policies were for the most part appropriately stated, dissem-

inated, and implemented; however, some weaknesses were noted in

the corrective action process for identification of deviations

(conditions adverse to quality).

The residents discussed the

site deviation threshold with station management and noted an

improvement during the second ha 1f of the SALP peri ad.

The

licensee was responsive to NRC concerns and requests, resulting

in proposals of acceptable resolutions.

During this evaluatio~ period, an inspection was conducted by

the regional staff to assess compliance with Generic Letter 81-21, Natural Circulation Cooldown.

This Generic. Letter

required the licensee. to establish and implement Emergency

Operating Procedures (EOPs)

and training relating to the

possible loss of the reactor coolant pumps during power

operations. Weaknesses were identified in th~ documentation of

differences from the Westinghouse Owners Group (WOG) Emergency

Response Guidelines (ERGs) for the natural circulation cooldown

EOPs.

This was identified by the NRC as a Deviation.

A viola-

tion was issued for inadequate EOPs when it was determined that

the quantitative cooldown curves used in the natural circulation

cooldown

EOPs

exceeded those specified in the Technical

.._, ." ....... _Jrr. r,**.

--

--

10

Specifications (TS).

No problems were identified concerning the

licensee's training in this specific area.

This inspection only

reviewed three of the 1 icensee' s 42 EOP' s and did not do a

programmatic assessment of the licensee's Procedure's Generation

Package (PGP).

The licensee, during this evaluation period, had the control

room operations personnel on a five shift rotation policy which

provided for adequate coverage whi 1 e a 11 owing for appropriate

training.

Three shifts were working eight hours each day, one

shift was off, and one shift was in training.

In addition, the

licensee usually had one extra licensed senior operator on

shifts which re qui red add it i ona 1 support (i.e., day shift).

Control room formality and behavior were maintained at a high

professional level.

Licensed operators performed their duti'es

in a professional manner which aids in safe and efficient

station operation.

Management involvement in day to day

operation was evident.

The new operations superintendent has

implemented a more formalized policy which should enhance the

operations program.

The human performance evaluation system and

check operator programs continue to improve operator efficiency

and help to. minimize recurrence of mistakes.

Operational

procedures, as indicated by violati.on (e), was one area which

  • needed improvement, and additional resources have been dedicated

to this area.

The licensee stressed the reduction of nuisance,

lit annunciators in the control rooms ("black board" concept)

that has result~d in less than 10 lit annunciators per control

room throughout the SALP period.

The licensee's operations

program continued to provide the necessary leadership and

professional attitude which has generally resulted in a high

level of operator performance while insuring safe operation of

the station.

During this assessment period, two Quality Assurance (QA)

Assessments related to operational activities were performed.

Areas

reviewed

included control

room activities, shift

turnovers, post reactor trip investigations, operating logs,

licensee

event

reports,

surveillance

procedures

and

documentation, the overall QA program, equipment labeling; and

opera ti ona 1 performance trending.

A 11 areas_ were assessed as

adequate; however, control room demeanor and post reactor trip

i nvesti gat ions

were

found

to

be

particularly

strong.

Additionally, management attention in the operations area was

especially noticeable as indicated by frequent management

presence in the control room and frequent plant tours. This QA

assessment, however, identified several problems related to an

event (Violation c of Section IV.I) in that the licensee did not

follow the Technical Specification requirement for inoperable

control rods and terminated an Unusual Event prior to corrective*

action being fully completed.

- .. -***.a*:*:_.,.._._,.,,..~.,.- ...... , "1

,-

~ *** ~....

"

11

The following violations were identified:

a.

Severity Level III violation for failure to maintain and

verify operability of heat trace circuitry for boric acid

flow path (88-04).

b.

Severity Level IV violation for failure to provide adequate

detailed instructions and failure to follow procedures

involving

residual

heat removal

pump

(87-05).

Also

discussed under the maintenance, surveillance, and outage

functional areas.)

C.

Severity level

IV violation for inadequate procedures

resulting in a degradation of containment integrity.

(87-26)

d.

Severity Level

IV violation for failure to conduct an

evaluation for a unreviewed safety question determination.

(87-21)

e.

Severity Level IV violation for failure to follow procedure

during performance of a surveillance test.

(88-01)

f.

Severity Level

IV

violation for inadequate emergency

operating procedures for natural circulation cooldown:

coo 1 down curves exceed those in the Techn i ca 1 Speci fi ca-

tions.

(87-32)

g.

Deviation for failure to follow procedures generation

package commitments

in generating emergency operating

procedures for natural circulation cooldown.

(87-32)

2.

Conclusion

Category:

2,

3.

Board Recommendations

The board noted that the effectiveness of the licensee's reactor

trip reduction program continued to provide positive results.

However, the board concluded that an overall lack of attention

to _detai 1 in the plant operations area in conjunction with a

rising industry standard for excellence resulted in a lower

evaluation in this area.

No changes to the* NRC inspection

resources recommended.

B.

Radiological Controls

1.

Analysis

. ; -:---*****-~** ... -.-.**:*****--- .,

12

During the assessment period, inspections were performed by the

resident and regional

inspection staffs.

The

inspe~tions*

included three radiation protection inspections, and five

radiological effluents and chemistry inspections which included

confirmatory measurements using the Region II mobile laboratory.

Also conducted was a special appraisal of the licensee's program

for maintaining radiation exposures as low as reasonably achiev-

able (ALARA) and one inspection to review an event having a

significant potential for personnel exposures in excess of NRC

limits.

The licensee's health physics, radwaste, and chemistry staffing

levels were appropriate and compared well to other utilities

having a facility of similar size.

An adequate number of ANSI

qualified licensee and contract health physics (HP) technicians

and qualified chemistry technicians were available to support

routine and outage operations.

The 1 i censee ut i 1 i zes some

contract HP support during non-outage periods.

During outages,

the licensee supplements the HP staff with additional ANSI

qualified health physics technicians and decontamination support

personnel. During outages, the contract technicians who work at

the plant during non-outage situations become coordinators of

the supplemental contractor technicians, resulting in improved

plant interfac~s between contract technicians and the permanent

plant staff.

The knowledge and experience level of the site health physics

and chemistry staffs are good.

The staff has a low turnover

rate and an effective training program which has received INPO

accreditation. The licensee had only three staff members leave

or retire during the assessment period.

During the assessment period, the licensee's radiation protec-

tion organizational structure remained unchanged.

However, the

licensee permanently filled the Supervisor of Health Physics

Technical Services position for the first time since it was

created in 1984.

Key positions in the radwaste management_

program and environmental surveillance programs were also filled

with qualified staff.

The performance of the HP staff in support of routine operations

and outages was adequate.

However,

procedural compliance

appeared to be a program weakness.

At least four procedura 1

compliance violations were identified during ttie assessment

period, two with multiple examples.

The licensee began development of a plan to upgrade the radia-

tion protection program in 1983 to correct a breakdown in the

program identified by the NRC.

In 1985, the licensee formally

issued the Radiation Protection Plan (RPP) which established

policies and responsibilities for upgrading the radiation

-

. ,* .... * .*. < ... *. ~- -, ..

13

protection program.

The licensee issued an implementation plan

with the RPP in 1985, which established the schedule for

upgrades in specified program areas such as external dosimetry

and ALARA.

The plan has lead to significant improvements in

radiation protection facilities at the station.

Although the

development and implementation of the RPP has been in progress

for nearly five years. at the end of the assessment period, the

licensee had fully implemented only two out of nine major

elements of the program.

The delays in implementing the* RPP are

due, in part, to a lack of strong direction and leadership from

the corporate health physics staff.

The licensee's schedule

calls for the RPP to be fully implemented with upgraded

procedures in place by July 1989.

Near the end of the assessment period, there was an event

involving maintenance on

an

incore detector which had a

significant potent i a 1 for an overexposure of personne 1.

Two

instrument and control (I&C) technicians and one HP technician

~ntered the subatmospheric Unit 2 containment with the plant at

100 percent power to free a stuck i ncore detector.

During

efforts to free the incore detector, approximately 100 feet of

cable attached to the detector were pulled through the polar

  • crane wa11* into the work area.

As a result of pulling

approximately three f_eet of activated cable in to the work area,

radiation levels ~n excess of 1000 Rem per hour were measured.

The workers evacuated the work area.

Although radiation doses

to the workers were less than NRC limits, there was a signifi-

cant potential for the workers to receive exposures in excess of

NRC limits.

The civil penalty violations resulting from this

event involved failure of the licensee to evaluate the radiation

hazards present during the work, inadequate procedures for

freeing the detector, and inadequate briefing of all personnel

involved in the work.

This event represented a breakdown in the

facility's management and control systems, in that station

management failed to perform an adequate pre-job assessment of

the potential hazards* involved in the work. A weakness in the

licensee's radiation work permit (RWP) program was evidenced by

this event in that a standing RWP written for minor maintenance

and inspections was used to free the stuck incore detector

discussed above,

rather than a more specific and more

restrictive special RWP.

After the event, the licensee was slow

to initiate an investigation of the event.

t,iowever, once

initiated, technical support from corporate staff was excellent,

as evidenced by

a comprehensive

and technically

strong

evaluation of the workers' doses after the event.

Resolutions of technical issues has been below average, as

evidenced by:

(a) the operation of the demineral izer-based

radioactive waste systems until breakthrough rather than *

maintaining

optimum

water

quality;

(b) strong management

attention has not been placed on vendor personnel to repair the

--

14

filter tape drive mechanism on the new containment air sampling

and monitoring system; and (c) timely resolution of the long-

term problem of buildup of internal radioactive contamination in

the liquid radioactive effluent detection chambers.

At the end of 1986, the licensee had 29,000 square feet (ft2) of

contaminated

area which

represented

32 percent

of

the

radiologically controlled area (RCA) of the plant, not including

the containment buildings.

By the end of the assessment period,

the licensee had reduced. the size of the contaminated area down

to 24,000 ft 2 or 26 percent of the RCA.

Although the total area

contaminated is significantly above that of a good performer in

Region II, the licensee has made excellent progress in reducing

the total area of the plant maintained as contaminated.

In 1987, the personnel contamination reports decreased 340

percent to a total of 465, which included 161 skin contamination

events.

This reduction in skin contamination was partly

influenced by the fact that there was no refueling outage in

1987.

At the end of the assessment period for 1988; the

1 icensee had documented 237 cases of personnel contamination

which included 138 skin contamination events.

The licensee's

corporate

hea 1th

physics *staff eva 1 uated the personne 1

contamination events and has made recommendations to reduce the

nu~ber of events and to improve per~onnel contamination

monitoring and control programs.

The 1986 collective radiation dose was 1178 person-rem per unit,*

which was

approximately 3 times the national average of

397 person-rem per pressurized water reactor (PWR).

From 1983

through 1986, the station's collective dose was significantly

above the national average.

In 1987, the station's collective

radiation dose was 356 person-rem per unit which compares

favorably with the national average of 368 person-rem per PWR

unit.

However, there was no refueling outage in 1987. * The

licensee has established a 1988 goal of 734 person-rem per unit,

which is likely to be significantly greater than the national

average due to the fact that both units will be.in refueling

outages this year~ The licensee has established a long range

goal to be at or be 1 ow the national average for co 11 ect i ve

occupational radiation dose by 1991.

During the assessment period, the NRC performed a special

assessment

of

the

licensee's

program

for

maintaining

occupational radiation dose as low as reasonably achievable

(ALARA).

Although the necessary elements of an effective ALARA.

program were in place, the 9verall effectiveness of the program

Jn reducing the station's collective radiation dose is yet to be

demonstrated.

Management support and involvement in matters

relating to the ALARA program improved during the assessment

period.

Licensee plant and corporate management are routinely

--

15

involved in setting program goals.

The licensee's senior vice

president persona1iy monitors collective dose trends and reviews

instances where dose goals are exceeded.** Management had

dedicated significant attention and resources to collective dose

reduction.

During 1987, management of the 1 icensee 1 s ALARA program was

observed by the !'"esident inspectors on a daily basis.

The

licensee established a goal of 719 person-rem total station

exposure for the ca 1 endar year.

Goa 1 s were es tab 1 i shed and

results displayed daily on the station internal television

system so that each emp 1 oyee could monitor progress in their

departments.

Daily discussions involving the past days

person-rem exposures were held by station management in the plan

of the day meetings.

High expenditure jobs were specifically

discussed including the specific departments using most of the

expenditure for the day.

Results of this management effort

included the station bettering its goal by expending only 712

person-rem in 1987.

The licensee has taken a number of actions to reduce exposures,

including additional training to improve the staff's awareness

of ALARA concepts; procurement of video equipment to provide for

remote monitoring of equipment, area~ and jobs; procurement of a

computerized Visual Information Management System which will

display* approximately 90 percent of the plant for pre-job

planning; allocation of significant resources to reduce the size

of the contaminated area of the plant; removal of. snubbers in

high dose rate areas; installation of fuel with zircalloy grids,

rather than inconel to reduce the source of cobalt; installation

of extended life light bulbs to reduce dose received on light

bulb replacement; and reduction of the exposure rates in the

Auxiliary Building by cleaning out sumps, drains and tanks.

These actions should result in collective dose reductions in the

long-term.

A number of other initiatives (e.g., source term

reductions) in the licensee's ALARA Action Plan have not been

completed and do not have completion dates assigned.

In 1986, the licensee shipped for burial 22,562 cubic feet (ft3 )

of solid radioactive waste containing 1156 curies.

In 1987, 'the

licensee shipped for burial 18,169 ft 3 of solid radioactive

waste containing 29,370 curies.

The majority of the 1987

radioactivity, 28,800 curies, came from irradiated hardware.

The licensee shipped 229 ft 3 of solid irradiated stainless

steel, borosilicate glass, and deposited metal oxides (thimble

plugs and burnable poison rod assemblies in cut up form).

By

the end of the assessment period, the licensee had shipped in

1988 2,942 ft 3 of solid radioactive waste having 156 curies.

During the assessment period the licensee* began shipping dry

active waste to a vendor for volume reduction.

This offsite

  • -~'* :, .** '**** ,*f ~ **

,.

.

16

compactor gives a volume reduction twice the capability of the

onsite box compactor.*

Plant discharges of liquid effluents contained 8.77 curies of

mixed fission products in 1986 and 5.17 curies in 1987.

While

this was an improvement over the plants prior liquid release

history (examples:

14.5 curies in 1983 and 65.5 curies in

1977), releases of IT'ixed fission products in 1987 in liquid

effluents, as in every year since 1980, have been higher than

any. other plant in Region

II.

The principal reason for this

appears to be the plant policy of operating the demineralizer-

based radioactive waste systems to the point of break.through

(onset of high conductivity in the processed water) rather than '

maintaining optimum water quality.

Such operation meets ALARA

limits under the criteria of Appendix I to 10 CFR Part 50, so

long as doses to the public meet the 40 CFR 190 limits.

Releases have consistently been well

below these limits.

Discharges of tritium in liquid effluents averaged approximately

400 curies per year per unit, which is typical of large PWRs.

Radioactive gaseous effluents were lower in 1987, than at any

time since the plant went into commercial operation. Average

releases in the 1980-1986 time period were comparable to other

2-unit plants in Region II.

Annual effluent release summaries

for 1985 - 1987 can *be found in section V.L of this report.

Ope rational expertise with process and effluent monitoring

systems was generally satisfactory.

The licensee resolved a

long-term problem with the liquid radioactive effluent monitors

caused by a buildup of radioactive contamination internally in

the detecti~n chamber and a check source which was too small to

result in a measurable meter deflection upon source check

activation.

This resulted in a violation.

Environmental monitoring activities were adequate. Samples were

changed regularly by well trained personnel. The environmental

samples

were

analyz_ed

by

a contract

laboratory

which

participated in .a cross-chec~ program with the EPA and NRC.

During the assessment period, it was noted that the licensee

fa 11 ed to conduct an eva 1 uat ion to determine if radioactive

materials were contained in licensee-generated sanitary sewage

sludge.

Samples taken by the licensee after this finding showed

2 to 3 pCi/g of activity in the dried sludge, principally Cs-137

and Co-60.

This resulted in a violation.

As part of the confirmatory measurements inspection, the

1 icensee was requested to analyze four. simulated waste or

reactor coolant samples on each of three detectors. Out of the

twelve analyses, the results of one were not in agreement. The

disagreement was resolved on a recount.

17

The licensee was observed to have given increased attention to

corrosion and erosion control.

Good chemistry control was

maintained throughout 1987 and was attributed to the following

factors:

relatively stable plant operation of both the plants;

increased surveillance of condenser tube integrity; improved

efficiency of producing

makeup

water;

operation

of the

condensate cleanup systems;

adherence to contra 1 criteria

recommended by the Steam Generators Owners Group; increased

resources (physical facilities, manpower,

inline analytical

instrumentation) for the chemistry staff; an9 support being

provided by Westinghouse through a maintenance agreement.

Weak

points were observed in the reliability of water treatment plant

and on the continua 1 transport of corrosion products to the

steam generators.

Nine violations were identified:

a.

Severity Level III violation for failure to adequately

evaluate the radiation hazards present during work on an

i ncore detector, inadequate procedures for freeing the

incore detector and for briefing those involved in the

work, and failure to conduct operations in accordance with

  • approved procedures (88-10).

b.

Severity Level IV violation for failure to control radio-

active- material in accordance with 1 icensee procedures

(87-35).

c.

Severity Level IV violation for failure to comply with a

low level radioactive waste disposal facilities Agreement

State's licensee conditions (87-03).

d.

Severity Level IV violation for failure to comply with

Department of Transportation regulations for transporting

radioactive material (87-03).

e.

Severity Level

IV violation for failure to adequately

source check an effluent monitor (87-22).

f.

Severity Level IV violation for failure to evaluate the

concentrations of radioactive material in sanitary sludge

(87_-22).

g.

Severity Leve 1 V violation for failure to adhere to

radiation control procedures addressing whole body counter

quality control checks (87-24).

h.

Severity Level V violation for failure to adhere to

radiation control* procedures addressing .Low Level Waste

Storage Faci 1 i ty inventories and surveys, and failure to

.

. . -..-.~-,,-~--.... **-

--

18

condu.ct

performance

checks

for

PCM-IA

personne~

contamination monitors (87-03).

i.

Severity *Level V violation for failure to provide adequate

procedures for the filling of waste disposal cans to 85%

capacity (86-21).

2.

Conclusion

Category:

Trend:

2

Declining

3.

Board Recommendation

The Board notes a declini~g trend at the end of the SALP period

and further notes a continued decline after the end of the SALP

period, including several violations identified during a outage

inspection

and

an

overexposure.

Based

on

this

recent

performance, the Board notes that a more current SALP category

would be a 3.

This, coupled with the lack of identification of

the root cause of the incore detector exposure event, causes the

Board to recommend comprehensive high level management attention

to implementation of radiological .controls by all organizational

components at Surry.

In addition,

the Board

recommends

increased NRC inspection.

C.

Maintenance

.. 1.

An al y s i s

During the assessment period,

maintenance were performed by

inspections staffs.

inspections in the area of

the resident and

regional

While not a regulatory requirement, a special inspection of the

secondary systems, and maintenance in the balance of plant

systems was inspected and found to be satisfactory.

Upper

management involvement was evident by their participation in

plant sta*rtups and shutdowns, daily production meetings, and

post trip reviews for both balance of plant (BOP)

and

safety-related systems matters.

The

licensee takes a sound viable approach* in resolving

technical issues.

For example, many improvements have been

initiated to increase the feedwater control system's reliability

and to reduce challenges to the safety systems. A *self imposed

requirement to test feedwater regulating valves at shutdown and

prior to startups has been instituted to avoid unforeseen

problems.

The licensee has also establi*shed a Predictive

Analysis Group to prevent future problems (see section IV.D).

However, specifically for the BOP/feedwater system, a formal,

,. .. '*-* ... *.

~. -..... *--

--

19

we 11 defined program for root cause analysis, documentation,

trending and utilization of information from. the station has not

been established. A review of BOP related events, that are

maintenance related, shows a lack of consistency in establishing

relationships to previous BOP events.

During the evaluation period, an inspection was performed in the

areas of electrical and instrument *maintenance practices,

planning and schedulin~, plant engineeririg interfaces, trending,

and information review programs.

No violations or deviations

were identified.

A weakness was identified involving .the

effectiveness of the licensee's program for trending equipment

failures.

The quarterly trending reports issued by Plant

Engineering do not provide a useful trending analysis of

repetitive problems or determination of root causes.

This

concern was also expressed by the licensee 1 s staff.

The maintenance program continues to be a high priority with

both the station and corporate management.

T~e specific daily

activities are discussed in frequent management meetings with

the assigned priorities displayed on

television monitors

throu*ghout the station.

Added emphasis has been pl aced on

pre-job and post-job briefings and the need to adequately

document the work performed.

As discussed previously (section

IV.B), the failure to perform an

adequate pre-job brief

contributed to

the potential

for an

overexposure while

performing maintenance on the incore detector. The availability

of technically sound and thorough maintenance procedures and the

strict adherence to these procedures continues to be a weakness

in the maintenance program.

Specific maintenance tasks are

sometimes performed using general procedures. This condition

resulted in the improper assembly of a main steam trip valve

(identified in violation (a)), and fa.ilure

_to

adhere to

procedures that resulted in subsequent degradation and rework of

a residual heat removal pump (identified in violation (b) of

section IV.A of the report). In addition, a QA inspection

conducted early in the period resulted in numerous maintenance

procedural deficiencies which resulted in a* violation which is

identified in section IV.I of this report.

The resolution of technical issues as they arise during main-

tenance appears to demon.strate a generally sound and thorough

approach with adequate understanding of the issues.

Senior

station and corporate management have acknowledged that a solid

programmatic approach to obtaining the root cause of problems

has been a weakness in the maintenance program and were taking

steps to enhance this area at the end of this SALP period.

A

major improvement was noted when the maintenance engineering

group was formed early in _the period.

This group of engineers

worked alongside the mechanics to resolve problems and ensure an

adequate failure analysis.

Late in the period, it was decided

. .

', --. -,:--,-.. ~*--:-. '

. -..:,.

~ .

!. *-*.*-* .. *.*

- . --

- . -

.. ~. -*--**-~.

20

that additional engineers would be added to the station staff to

supplement the work being accomplisli*ed by the maintenance

engineers.

These new engineers would become system engineers.

and thereby could provide immediate involvement in resolution of

problems

associated

with

systems

for

which

they

were

responsible. This program was in the implementation stages when

the SALP period ended.

Management response to NRC initiatives was v1able and sound with

acceptable resolutions generally proposed.

The

licensee's

evaluation and resolution of NRC IE Notices have generally been

both timely and thorough.

Each IE Notice sampled was placed on

the commitment tracking *system for reso 1 ut ion with firm commit-

ment dates established.

Overdue commitments are brought to

management's attention. A formal check valve PM program has not

been.implemented in spite of the identification of industry and

site check valve problems; however, a study of check valve

applications has been completed, and work is in progress to

develop such a program.

An improvement in the overa 11 performance of the maintenance

department is noted by the relatively low number of transients

during this . SALP period and 247 days of continuous power

operation on Unit 2. Although Unit 1 experienced several forced

outages, only two were directly attributable to improper

maintenance; and others relating to equipment failure resulted

in licensee corrective actions to prevent recurrence.

The

licensee is progressing with the development of the Quality

Maintenance Team (QMT) concept with all electricians, mechanics,

and welders receiving additional training in health physics, QA,

and nondestructive testing.

Station management consistently

demonstrated a commitment to this approach in the daily

scheduling of maintenance activities and attribute the improved

equipment availability to this program.

A weakness was identi-

fied (violation b) with the control of substitute material in

safety-related components when a field fabricated part in a

valve actuator contributed to it's failure to perform as

desired; however, this substitution did occur prior to the QMT

concept.

Staffing continues to improve with the key positions identified

and the responsibilities adequately defined. The use of previ-

ously 1 icensed reactor operators as maintenance coo-rdinators,

and maintenance foremen as planners, aids in both communications

and

effectiveness.

The

establishment of a

maintenance

engineering staff greatly enhances the capability of the

maihtenance department to adequately evaluate and correct

problems in the field as they arise.

During this assessment period, two QA Assessments related to

maintenance activities were performed.

The

licensee has

... *.*.* .... ,. .*---~ ,.-,** .

.

.. -: ',

.

., , f ** -Y.*.**~i-. * . .

.'

. . *

  • . . . '

...... _ ~ *' --- ~.

. **-* ._-, ....... --.. -- -*--

.. **----~. *--- ,-~.-

21

strengthened

their maintenance

tagout system,

and

also

increased their usage of a computer system (WPTS) for scheduling

and tracking maintenance activities. The licensee has increased

their attention to using predictive analysis programs for better

overall equipment reliability.

Weaknesses were

identified

relative to the Station Nuclear Safety and Operating Committee

(SNSOC) timely reviews of maintenance procedure and other

procedure changes.

Storage of maintenance related spare parts

was not always adequate in that level A and B required materials

were .found in the same lay down area during one inspection.

This problem was immediately corrected by the licensee.

A problem was

identified related to failure to follow

established controls for maintenance work orders (in section

IV.I, violation a). The apparent root cause is. the failure of

personnel to follow procedures. Multiple examples of incorrect

work orders were i dent i fi ed even though these work orders

received final closeout by maintenance, supervisory, and QA

personnel.

The following violations were identified:

a.

Severity Level IV violation for failure to provide.detailed

instructions in maintenance procedures for safety-related

equipment (main s*team trip valve).

(86-42) Unit 2 only.

b.

Severity Level V violation for failure to provide adequate

control and evaluation of the substitution of replacement

parts in safety-related components.

(88-01)

2.

Conclusion

Category:

2

3.

Board Recommendation

None

D.

Surveillance

1.

Analysis

During the _assessment period, inspections were performed by the

resident and regional

inspection staffs in the areas of

periodic surveillance testing, containment local. and integrated

leak rate testing (ILRT),

and

inser.vice i_nspection (ISI)

programs.

Manag.ement involvement in the scheduling and performance was

adequate as evidenced by the routine reviews of tests being

performed in the daily meetings.

Test records were generally

.. " .. -.....

.

L_

22

found to be complete and available.

A weakness was noted,

however, in the formal identification and evaluation of testing

discrepancies.

The inspectors performed~ comprehensive audit

of the integrated safeguards tests performed during the last

  • refueling outages and found, as identified by violation (b)

below, that the records were not complete and the review and

evaluation of discrepancies inadequate.

Decision making was

solely by the operation superintendent performing the test w~th

no overview or technical evaiuation evident.

Retest, after

equipment repairs, was performed using special tests that did

not receive adequate review and approval.

The normal process of

eva1uating discrepancies appeared to have been bypassed for this

rather complex test.

Technical Specification (TS) required surveillances were, with

few exceptions, completed*in a timely manner.

The licensee's

program to track survei 11 ance intervals and identify overdue

tests to key

individuals appears to be effective.

The

inspectors did identify a required TS surveillance, included in

violation (b) below, that had not- been added to the .testing

program after it was added to the TS several years earlier. The

requirement involved the testing of emergency bus undervoltage

and degraded voltage circuitry and was previously identified as

an omission to the testing program with no subsequent corrective

actions performed.

During the evaluation period, inspections were conducted by

regional inspectors of the snubber survei 11 ance program,. post-

refueling

and

zero-power

startup

tests*,

RCS

1 eak.age

measurements, and integrated 1 eak rate testing.

The snubber

surveillance program showed evidence of prior planning through

well

defined

procedures.

Records

were

complete,

well-maintained, retrievable, and legible.

Staffing and training

of personnel involved in the snubber surveillance program were

adequate.

The

approach to problems

encountered due

to

functional test failure was timely, technically sound, and

thorough.

Decision making was usually at a level which ensured

adequate management review .

. Unit 2 post-refueling, zero-power startup tests were witnessed

in December 1986.

The tests performed and the procedures used

to perform them were acceptable.

The personnel performing the

test were familiar with test requirements.

The onsite personnel

function primarily as data takers since technical analysis is

performed by corporate office personnel.

Independent analysis by the NRC inspection of thermal power

calculations and RCS *1eakage measurements was performed in

concert with rev.i ews of 1 i-censee procedures.

The differences

between results calculated by the licensee and the inspector

were acceptable. However, the licensee's procedure for leakage

-* **
  • -*:** ~-****-.. 1 **:*.*,* * ** -
. ** **.;-*-*
  • .

- . .

'* r** ~>**,**"*"' ***

._,-,--,. ~ ..... , ..

--.-,

'

-

~,,.

'

> ,**

-

'"

-

23

measurement needed improvement, which management readily agre~d

to perform.

The

integrated

leak rate test on

Unit 2,

performed in

November 1986, was witnessed by

NRC inspectors.

Management

interest and involvement in leak rate surveillance testing are

indicated by the development of a detailed test procedure which

controls test preparations, activities, acceptance criteria and

system

restoration.

Also,

staffing

and

training

were

satisfactory for conduct of the test.

Management involvement and conservative resolution of technical

issues were observed in the licensee

1 s actions \\aken to correct

the sump pump discharge isolation valve leakage problem.

These

valves had exhibited recurring leakage problems, and the licensee

conducted a thorough investigation to determine the cause. The

results were to change the valve design, modify operating and

test procedures, and perform a number of 1 oca l tests on the

modified system.

The licensee had taken responsible, conserva-

tive action to achieve a quality performance.

Inspections of

the ILRT revealed several technical issues that are indicative

of a non-conservative approach toward resolution.

These

involved data averaging, assumption-of water seals, and status

of' liner weld leak chase.

The latter two issues have not been

resolved and are currently under review by NRC.

While the

issues are not of a nature to indicate a significant breakdown

of management control and quality assurance programs, they do

i~dicate a need for increased management attention to achieve a

high quality test performance.

The licensee generally demonstrated a clear understanding of

technical

issues and was responsive to

NRC concerns.

A

significant weakness in the licensee program for testing heat

tracing circuits on boric acid flowpaths was identified as part

of a civil penalty violation late in the period; the violation

(a, section IV.A) was not issued until after the SALP period

ended.

These circuits, required by technical specifications,

had not been adequately tested since original installation. The

licensee took prompt corrective actions to research and correct

the problems which appeared to indicate a failure to properly

review the applicable procedures, as well as a general lack of

understanding

regarding the heat tracing circuits.

The

reporting and analysis of surveillance events was in most cases

prompt and thorough, although a weakness was identified in

~iolation (d) of section IV.A which is listed in the Operations

functional area, regarding the failure to report special tests

as required by 10 CFR 50.59.

A strong management commitment to the use of extensive

predictive analysis during surveillance testing was evident

during the reporting period.

The licensee utilized equipment

  • _.

"'_*. __

24

monitoring techniques that greatly exceed the basic testing

requirements.

This additional testing was often performed even

though it constituted an additional constraint on both resources

and schedules.

The following violations were identified:

a.

Apparent violation for failure to properly position valve

for penetrations for a Type A test (86-36, Unit 2 only);

this issue has not been resolved.

The NRC did not consider

the issue during this SALP evaluation.

b.

Severity Level IV violation for inadequate procedure and

failure to follow procedure in testing of safety injection

system. ( 87-21)

c.

Apparent violation for failure to follow nondestructive

test and ANSI procedures involving radiographic testing has

not been resolved .. It was not considered during this SALP

evaluation.

2.

Conclusion

Category:

2

3.

Board Recommendation

None

E.

Fire Protection

1.

Analysis

During this assessment period, inspections were conducted by the

regional inspection staff of the licensee's fire protection and

fire prevention program including a review of the implementation

of the safe shutdown and related fire protection requirements of

10 CFR 50, Appendix R.

On May 4-8, 1987, an NRC team conducted an

II Appendix R" in spec-

ti on to determine if the protection features provided for

structures, systems, and components important to safe shutdown

were in compliance with 10 CFR 50, Appendix R, Sections III.G.,

III.J., III.L., and III.O. This inspection determined, through

a random sampling of cable routes and components associated with

safe shutdown and alternate shutdown capability, that the fire

protection features provide adequate protection to ensure one

train of equipment is available to perform plant shutdown or

alternate shutdown.

Fire protection. features met the require-

ments of Appendix Rand applicable industry codes, or exemption

request and/or engineering evaluations have been provided

.

. ... ,~ ... -. *. *.~-.. *

- . .

"

.

'

. . .* .. "**,*: *:**- *;- ~-*.* . . .

  • . ",: , ,. ' ..

.-.*: ** - .... ~.

,._.., .y-_.,-.-,

25

justifying the deviations.

The licensee adequately acdressed

associated circuits and breaker coordination, and emergency

shutdown procedures are available for use in the event of a

fire.

Prior to the Appendix R inspection, it was determined that the

power and contra l cables for a 11

on site emergency ci ese l

generators were routed through Fi re Area 2.

Therefore. it is

possible for a fire in this area to result in a loss of charging

pumps for both units (violation (a) below).

The licensee had identifiep this cable interaction discrepancy

and a Special Report, No. 87-10, was submitted to the NRC.

The

licensee initiated prompt corrective action by establishing a

fire wa*tch in the area and initiating a design change to reroute

the Diesel Generator No. 3 cables out of the are*a.

The design

modification package was completed promptly.

Two

inspections of the routine fire protection/prevention

program were also conducted during the assessment period.

The

licensee had issued procedures for the contra 1 of fire hazards

within the plant, surveillance and maintenance of the fire

protection systems and equipment, and organization and training

of the fire brigade.

These procedures were found to meet the

NRC requirements and guidelines. The staff inspection reviewed

the licensee's implementation of the fire protection and

administrative controls.

General housekeeping and con~rol of

combustible and flammable materials were satisfactory.

The fire protection extinguishing systems, detection systems and

fire barriers, and fire barrier penetrations were found to be in

service, or the appropriate limiting condition for operation

requirements of the Technical Specifications had been implemented

except as noted below.

Surveillance inspection, tests, and

maintenance of the fire protection system and features were

satisfactory.

Organization and staffing of the plant fire brigade met the NRC

guidelines.

Fire protection staff positions were identified and

authorities and responsibilities were clearly defined.

The

training and drills for the brigade members met the frequency

specified by the procedures and the NRC guidelines.

Personnel

were well qualified for their duties.

A violation was identified during one of these routine inspec-

tions.due to the licensee's failure to maintain emergency fire

fighting equipment available exclusively for fire fighting use.

In reviewing plant Technical Specification surveillance results

it was found that on numerous occasions-over the one year period

reviewed, that emergency fire fighting equipment was routinely

being

removed

from storage locations specified in plant

  • ,*.**** *;*-~*-** v.-.-*. : .***.

..

.. - .. _.,, ............ ,., ............ -.... .

26

procedures.

At the time of the ins~ection, three storage areas

were found to be missing necessary equipment. The equipment was

found being used for non-fire fighting uses by the pl ant

operations department.

Licensee management took immediate

corrective action to replace the r.iissing equipment and also

issued a memo to all plant personnel emphasizing the importance

of this equipment and stating this equipment is to be used for

fire fighting purposes only.

Additionally, the licensee had

established a unique marking sys~em for fire fighting equipment

which identifies it as emergency equipment.

Except for the violations identified, the management involvement

and control in assuring quality of the fire protection program

is evident based upon their involvement in the site fire

protection program to ensure the program complies with NRC

requirements and the prompt resofot ion of nonconformances.

The

licensee's approach to resolution of technical fire protection

issues indicates an apparent understanding of issues.

The

responsiveness to NRC initiatives are technically sound and

thorough.

The following violations were identified:

a.

Severity Level III violation for failure to assure that one

redunda*nt train of equipment, cabling and associated

circuits necessary to achieve and maintain hot shutdown

remains free of fire damage pursuant to the requirements of

10 CFR Part *50, Appendix R, including specifically Section

Capability

(87-07).

b.

Severity Level IV (Supplement I) violation for failure to

comply with the requirements of Technical Specification 6.4.J and Fire Protection Program procedure 3.5.1 which

requires that fire protection systems shall not be used for

reasons

other

than

the

prevention,

detection

or

extinguishing of fires, or to perform scheduled testing or

training un.less specifically approved in writing by the

loss prevention coordinator. (88-07).

2.

Conclusion

Category:

2

3.

Board Recommendation

Licensee management attention and

involvement

should be

increased to prevent the relatively few but significant

deficiencies noted above.

F.

Emergency Preparedness

  • . :**~:-*,::.*:* -,-- 0.-*--*-*-.,*;****

I

-

-***:* **~-.--..-...**: r

' .. -

..

' '.._ __ ._* __ ~-*-/ ,;

  • ,

-~--

'

  • *

.

J **

,,

,*

,,

-.*,_;

,

  • * --:.~ _;,; -*~**. **
  • .
  • '

., *** ,'*', *.\\.<. ~7r" *

--

27

1.

Analysis

During the assessment period, inspections were performed by the

resident and

regional

staffs in the area of emergency

preparedness.

These inspections included the annual emergency

preparedness exercises in October 1986 and October 1987, and a

routine emergency preparedness inspection in May 1987.

The routine inspection disclosed that the licensee had an

adequate emergency preparedness program for emergency detection

and classification, protective action decision-making, notifica-

tions and communications, changes to the emergency preparedness

program, dose calculation and assessment, licensee audits,

coordination with offsite agencies, and emergency facilities and

equipment.

Emergency preparedness and implementation of the

Emergency Plan was adequatel~ demonstrated during the feedwa~er

pipe rupture event of December 10, 1986.

One violation and four exercise weaknesses were noted during the

three inspections.

The one violation identified during* the

routine inspection was for failure to provide training to

various members of the emergency organization in accordance with

the Emergency Plan.

In reviewing the training for approximately

20 individuals, it was determined that eight personnel. had not

received the initial training or bi-annual emergency response

retraining required by the Emergency Plan.

The exercise weaknesses addressed a number of different aspe~ts

of the emergency response program.

The October 1986 exercise

findings noted a lack of contingency messages for the scenario.

This resulted in confusion and

inconsistencies for both

controllers and

players as

11 0n

the spot" freeplay was

interjected that would

have

impacted other players and

contra 11 ers who were unaware of the new events.

Another

weakness* concerned

the

making

of

protective

action

reconvnendations

(PAR)

by

the Recovery Manager

when

the

responsibility for the same had not been assumed from the

Station Emergency

Manager.

This

responsibility was

ndt

specifically controlled to ensure that only one coordinated PAR

was provided by the licensee to offsite authorities. The other

exercise weakness

from

the 1986

exercise addressed the

untimeliness of communication of .core assessment and plant

status data to the Local Emergency Operations Facility and the

Corporate Emergency Response Center.

In one case, the data

available was more than one hour old. Timely data is needed by

the offsite response facilities to provide effective support to

the onsite emergency facilities.

The 1987 exercise demonstrated that corrective action for the

latter two weaknesses had been taken but minor problems with

message preparation in the scenario were noted.

Another

- ******-..

.

. ..

.

.

,, . *""

... *.t;"*.-:*--r;**.-*

. *.

28

exercise weakness was noted regarding the failure to coordinate

press releases with the State spokesperson.

On one occasion it

was noted that the State spokesperson was summoned to the

microphone in the 1 oca 1 Emergency News Center with no prior

knowledge of what the licensee's statements would be.

This

could result in the State spokesperson needing to address an

issue withou: sufficient time to consult with required parties.

The following violation was identified:

Severity Level IV violation for failure to provide training

to members of the emergency organization in accordance with

the Emergency Plan (87-12).

2. * Conclusion

Category:

2

3.

Board Recommendation

None

G.

Safeguards (Security/Material Control and Accountability)

--

  • ,,-*.--*~-:--***--*.**:.**w-*;,":** - ~

1.

Analysis

Security

During the inspection period, routine inspections were performed

by the resident and regional inspection staffs.

The

licensee's performance in this area has improved in

comparison with the previous SALP rating period.

The two

violations identified were relatively minor and

are

not

considered to reflect a deficient security program.

The 1 i cen see has deve 1 oped and imp 1 emented a security audit

capability covering all aspects of the security program.

Included in the audit are.alarm exercises, safety implication

assessment, alarm station duties, and event management.

The

licensee's annual

audit (#87-05) reflected an aggressive

approach and resulted in findings being addressed at the

appropriate corporate and site management levels.

The security organization's performance during the December 9,

1986 pipe rupture event was noteworthy.

The security shift

faci 1 itated the response of off site emergency personnel and

equipment, and was instrumental in the initial offsite emergency

reactionary brigade to the accident.

An

11after-action

11 report

was generated by the security force in an attempt to critique

  • :

j

_::_

_

c'_~- _ * .

,

r .*: * .. *

.

-*-~. ::" . ":'

'

, -..

- ..... ------

I

I

--

'-. -.., .,

~ .-,~.

,._ ... _.- -; ..

2.

29

--its commendable performance and many of its recommendations*have

been implemented.

Corporate and site management's support continue to have a

positive

impact.

Daily

close

superv1s1on,

simplified

procedures, realistic training and a continued sensitivity to

requirements

are

the

characteri sties

of

the

security

organization.

Training and qualification effectiveness were evident as demon-

strated during this evaluation period when backshift security

personnel observed that a 1 icensed operator may not have been

fit for duty when he was entering the station. This information

was reported to the operator's supervisor and appropriate action

was taken.

Materials Control and Accountability (MC&A)

During the assessment period, one regional based inspection was

conducted in the area of MC&A at the Surry site. The inspector

determined that the licensee had established, maintained and

followed written MC&A procedures for controlling and accounting

. for new and spent fue 1 receiving, storing, shipment, inventory

burn-up

calculations,

recordk.eeping

and

reporting.

The

licensee, however, was not aware of the requirement to account

for a 11 non-fue 1 ( i ncore detectors) Special Nucl ea*r Materials

(SNM) as required by the regulations.

A new procedure was

written to ensure that all SNM (fuel a*nd non-fuel) undergo a

semi-annua 1 phys i ca 1 inventory.

Vi o 1 ati on ( c) was issued for

failure to establish and maintain an adequate MC&A procedure

which resulted in a failure to conduct a physical inventory of

all non-fuel on inventory.

The implementation of the new

inventory procedure has not yet been examined by an on-site

inspection.

The following safeguards violations were identified:

a.

Severity Level IV for failure to escort a visitor (86-30).

b.

Severity Level. IV for failure to install an adequate

locking device (87-?3).

c.

Severity Level IV for failure to establish and maintain an

adequate material control and accountability procedure

(87-10).

Conclusion

Category:

2

3.

Board Recommendation

None

30

H.

Outages

1.

Analysis

During the assessment period.

operations were

performed

by

inspections staffs.

inspections of plant outage

the resident and

regional

Unit 2 conducted a refueling outage from October 4, 1986 to

December 2, 1986.

The refueling activities on the unit were

adequately preplanned with realistic assignment of priorities

and contra l of activities.

Refueling procedures were adequate

to accomplish the associated task; however, violation (b) under

the Operations functional area indicated a lack of ap~ropriate

engineering review/documentation for deviation of a maintenance

procedure involved in the rework of a residual heat removal

pump.

Adequate levels of management attention were observed

during refueling; however, violation (a) listed below did

identify a weakness in management overview of the inservice

inspection effort.

Refueling crew staffing and staff training

were observed to be adequate.

Post refue 1 i ng startup test

records were adequate and showed that the testing was conducted

in an acceptable manner.

During the months of December 1986, and January through March,

1987, both units experienced outages due to pipe degradation in

the condensate and feed systems.

These outages were not

scheduled and received additional attention from outside parties

due to the sensitivity of the failure of the piping.

However,

with minimal preplanning, the licensee put in place an effective

outage organization which accomplished the piping inspection and

replacement tasks with minimal delay.

Management attention to

this effort was excellent.

In addition to performing the

physical work,

the licensee evaluated the piping failure

mechanism promptly and provided this information to*the NRC and

the industry as quickly as information was available.

The

licensee also provided a complete report on the event entitled

"Surry Unit 2 Reactor Trip and Feedwater Pipe failure Report".

This report discussed aspects of the event as wel 1 as the

recovery actions tak.en for unit(s) restart, and was presented in

meetings in six different locations in the country to provide

information relative to the failure mechanism

to other

utilities.

Corporate management was involved in site activity

and recovery actions, and decision making was at a level that

ensured adequate management review.

Regional inspectors reviewed the Inservice lnspection/Inservice

Testing (ISI/IST) program

and

procedures,

observed work

activities, and

reviewed selected quality records.

The

31

inspectors found that the ISI/IST program was procedurally well

deiineated.

Training,

qualification and certification of

IS!/IST personnel

has

contributed to good

adherence to

procedures, with only a minimum of personnel errors as evidenced

by violations (a) below and (c) of Section IV.I.

Records were

complete, well maintained, and available.

During this assessment period,

licensee management placed

additional emphasis on reducing the number of outstanding

maintenance backlog items.

During the two week outage in

December 1987 for Unit 2, over 400 outage work orders were

completed.

This work reduced the outstanding work order outage

list by 50 percent.

The licensee has also reduced the total

outstanding work order backlog.

During 1986 and 1987, this

backlog was reduced from approximately 5400 to approximately

2000.

.

During the last month of the assessment period, Unit 1 began a

refueling/maintenance outage.

The outage scope of work was

adequately planned; however, when the SALP period ended, the

licensee was having difficulty maintaining the schedule due in

part to jobs which had never been accomplished in past outages.

Management attention to work i,n progress was evident.

Daily

meetings were held to insure senior management was aware of all

aspects of the work in progress.

Schedules were revised on a

frequent basis to address slippage of work activities and to

redefine priorities based on identification* of new work and

material status.

Technical i terns were appropriately addressed

as they were identified, and engineering involvement was evident

in daily work items.

A QA Assessment inspection related to design control activities

was also performed during this assessment period.

This inspec-

tion reviewed various plant performance data pertaining to plant

events caused by design errors, station deviations reports based

on design control or configuration problems, field changes

issued for eight design packages, design change backlog,

temporary modification control, and construction trouble reports

issued during design change installation.

Addi_tionally, all

aspects of a design change package were reviewed.

These

activities were well controlled. The licensee's design control

program has improved significantly since the last assessment

period. Although several minor problems were identified, these

were caused by lack of attention to detail as opposed to

programmatic problems.

The following violation was identified:

Severity Level

IV violation for failure to provide

appropriate

inservice

inspection

drawings

for

the

--

32

examination of safety related welds on the pressurizer

(86-34).

2.

Conclusion

Category:

2

3.

Board Recommendation

None

I.

Quality Programs and Administrative Controls Affecting Quality

1.

Analysis

During the assessment period, inspections were performed by the

resident and regional inspection staff in the areas of quality

programs and administrative controls affecting quality.

For the

purposes of this assessment, this functional area is defined as

the ability of the licensee to identify and correct their own

problems.

It encompasses all plant activities, al'l

plant

personnel, as well as those corporate functions and personnel

that provide service to the plant.

T~e plant ~nd corporate QA

staff have responsibility for verifying quality. The rating in

this area speci fi cal ly denotes results achieved by various

groups in the facility as well as th~ QA staff in verifying that

quality.

A QA Effectiveness inspection was conducted in March and April

1987.

This

inspection

reviewed

licensee self-identified

trending indicators and management actions when these trending

indicators were not meeting established goals.

The inspection

reviewed

operations

and

surveillance,

design

control,

maintenance and procurement, and quality assurance. Another QA

inspection was conducted in March and April

1988.

This

inspection

reviewed

operations,

maintenance

and

quality

assurance.

These inspection results are discussed in the

various sections of this report.

All QA auditors were adequately trained through a combination of

previous industry experience, on-the-job training, or both.* Few

auditors had technical degrees.

However, provisions have been

made to use technical experts on audit teams when required.

Many audits being performed are compliance oriented, although

the licensee is changing their auditing techniques to be more

performance oriented.

Based on reviewing audit schedules,

schedule- adherence, and auditor qualifications, the audit

program is being satisfactorily managed.

Reviewing followups to

audit findings identified a weakness in that full implementation

of c.orrect i ve action for some audit findings was not always

verified.

However, overall corrective actions for audit

'

.'f-** , *,,' ~--*- '~, .<

., ~.

. /

.r ... '

33

findings were being adequately followed up and proper management

attention resulted in appropriate corrective action resolution.

Procurement activities were generally satisfactory except for

issues identified and discussed in the maintenance area of this

report.

Additionally, a weakness was identified regarding a

lack of a feedback mechanism from receipt inspections to the

approved vendor list.

Neither corporate nor site QA*personnel

developed a system to track vendor performance, vendor reject

rate, and vendor deficiencies found during receipt inspections.

Consequently, action was not being taken to modify purchase

order requirements based on vendor performance.

A review was performed on all SALP sections in an attempt to

capture perceived strengths and weaknesses related to management

controls affecting quality.

The

following are some perceived strengths in management

controls affecting quality:

The licensee has demonstrated the ability to correct problems

relating to the thinning of the feedwater pipe identified

following the pipe rupture in December 1986.

The

fo 11 owing are some perceived weaknesses in management

controls affecting quality:

The 1 icensee has not demonstrated the abi 1 ity to correct

recurring problems related to; lack of attention to detail

regarding operator errors during routine operation, poor timely

resolution related to the boric acid heat trace system

deficiencies, and programmatic deficie.ncies including multiple

examples of procedural noncompliance relating the radiological

control program.

The following violations were identified:

a.

Severity Level IV violation for failure to follow main-

tenance procedures involving eight examples dealing with

site work orders (87-06).

b.

Severity Level IV violation for not adequately implementing

the emergency plan (88-11).

c.

Severity Level IV violation for having inoperable control

rod banks while the unit remained critical (88-11).

d.

Severity Level V violation for failure to follow document

control procedures (87-30).

--

  • 2.

Conclusion

Category:

2

3.

Board Recommendation

None

J.

Licensing Activities

1.

Analysis

34

During the SALP period, the licensee continued to show an active

i nvo 1 vement of. management in assuring the qua 1 i ty of submi tta 1 s

for licensing actions.

The management is alert to issues

involving plant safety and public health and safety.

The

management takes an active part in resolution of any problems in

the normal licensing reviews.

Decision making is consistently

at a level that ensures adequate management review.

The

licensee's

submittals

in

most

cases

are

timely* and

well-prepared. Most applications submitted by the licensee

during this SALP period were wel 1 written with the safety

analysis fully supporting the requested action.

Also, the

corporate management is frequently involved in site activities.

There were some i so 1 ated cases where addi ti ona 1 management

involvement was

desirable.

For

example,

the licensee's

submittal for the Technical Specification change related to main

steam trip valve stroke time was not submitted in a timely

manner to avoid unnecessary p 1 ant shutdown.

However,

the

management response to the problem was excellent after the staff

highlighted the situation.

The licensee's request for an

administrative change to the NA-1&2 and Surry TS regarding the

licensee's corporate reogranization (April 1, 1988) was not

submitted in a timely manner even though the NRC was advised of

the scheduled change.

Overall,

the

licensee's management

has

continued to be

consis.tently involved in licensing activities and has demon-

strated excellent control in a number of situations, including

the main feedwater pipe* rupture accident at Unit. 2.

The licensee demonstrates clear understanding of the technical

issues involved in licensing activities.

The

licensee's

evaluations for no significant hazards considerations are

thorough and clear in most cases. The licensee keeps abreast of

industry approaches to the resolution of general plant ~afety

issues. Management participates in many group~ representing the

nuclear industry.

The licensee takes a conservative approach

when there is an

issue which may *have potential safety

significance for plant safety. For example, the responsiveness

..

35

in resolving technical issues was demonstrated by a design

modification for the inside containment recirculatior. spray

system to faci 1 i tate fl ow testing of the pumps as req~i red by

the ASME Code.

The licensee was very responsive to the staff's

concern that these pumps should be flow tested.

Also, the.

response to the feedwater line break in Unit 2 was exemplary.

The licensee evaluated the cause of the accident ar:d took

appropriate corrective actions in.an expeditious manner.

The licensee has been very responsive to NRC's initiatives in

almost all cases.

VEPCO maintains a system which tracks the

commitments for responding to NRC' s requests for information.

Commitments generally are met unless adequate justification is

provided in advance and agreed upon by the staff for extension.

The licensee resolves technical issues in a timely manner and

has cooperated in providing the resources when requested by the

staff on a voluntary basis.

For example, the licensee provided

support during several visits to the Surry site by NRC staff and

the contractors in efforts related to NUREG-1150 studies.

In

addition,

the

licensee supported the efforts related to

risk-based performance indicators and other studies.

There was one instance where the licensee was not ful Ty

responsive to the staff's request:

This relates to the

Technical Specification change for Inservice Inspection and

Testing.

The licensee's response to the staff's request was

considerably late.

The Project Manager discussed this problem

with the licensee's staff and has been assured that problems in

this area will be corrected in the future.

The NRR Project Manager attended several Enforcement Conferences

in Region II offices.

In most conferences the licensee was

well-prepared to discuss the issues and they were well received

by the staff. The staff has identified several instances where

the licensee's 50.59 reviews were not adequately performed or

documented.

The 1 icensee has made some changes in the 50.59

review process and it is expected that licensee's performance in

this area will improve.

The licensee continues to maintain adequate staff for licensing

activities. The licensing group exhibits a high degree profes-

sionalism and cooperation with the staff.

The licensing staff

is intimately familiar with the NRC regulatory framework, and

also has good knowledge of plant operation.

The licensee main-

tains a staff at the site which interfaces with the licensing

staff at the headquarters in licensing activities.

The person

in charge for the staff at the site has in-depth knowledge of

plant operation and has been very helpful in assisting the PM

during plant visits and for providing quick information during

transients.

Also, the licensee's operations staff is very

cooperative with the NRC staff.

.

.*

2.

Conclusion

Category:

1

3. . Boa rd Recommendation

36

Although the Board assigned a category 1 rating in the

functional area of licensing, it should be noted that there were

several instances, as discussed in the evaluation, where the

responsiveness of the licensee's submittals fell short of the

category 1 criteria. The licensee should strive for improvement

in this area during the next rating period to e 1 i mi nate

deficiencies of this type.

No change in NRC staff resources is

recommended.

K.

Training and Qualification Effectiveness

1.

Analysis

During this inspection period, a training inspection was

performed by* regional inspection staff.

The review of the licensee's training program involved licensed

operator training, licensed operator requalification training,

non-licensed operator training, exam bank security, simulator

procedure review, emergency pre pa redness, security force, and

ISI/IST program (see section IV.H).

The requalification training program, based on record reviews

and interviews, is well developed and implemented. Staffing was*

thin in the past but appears to be adequate now.

Management is

actively involved in the program evolution.

The program is

fully accredited by INPO with no outstanding items.

The licensee has corporate staff dedicated to the evaluation of

the

training

program.

The

program

includes evaluation

i ndi ca tors and criteria for determining the adequacy of each

training area.

A schedule is maintained that evaluates each

area on a monthly, quarterly, semi-annual, or annual basis.

A

discrepancy report is written when an indicator does not mee~

its acceptable level.

The* discrepancy report requires the

person responsible for the indicator to sign and attach an

action plan if necessary. Management is then required to review

the discrepancy report and sign off. The inspectors found this

audit capacity of the training program to be very good.

One

violation was identified (section IV.F) in the emergency

preparedness area.

Operator training in BOP areas also has changed as necessary to

address identified problems.

For example, additional simulator

training in feedwater controls during startups and shutdowns has

-

  • -****.--*

-

~,-*,.* *****

  • ....

.I

    • .
    • ::~~ .. -.,

.,_, .......

.

--

37

been implemented* due to experienced feedwater control problems.

The frequency of these problems has reduced.

The check operator program continues to provide good feedback to

the Operations training group.

The check operator has been

observed by

inspectors to be monitoring

actual

operator

responses to transients~ The check operator feedback appears to

be one of the-reasons that operator response to emergencies has

been good.

Two sets of replacement operator license examinations were

administered during this SALP period.

The operating and written

examinations administered in February 1987 resulted in 3 of 3

Senior Reactor Operator (SRO) candidates and 2 of 2 Reactor

Operator (RO) candidates passing.

The operating and written

examinations administered in March 1988 resulted in 2 of 2 SRO

candidates and 2 of 2 RO candidates passing. The requalifica-

tion program was not evaluated during this SALP period.

The replacement examination passing rate was 100~~. which is

considerably higher than industry average.

2.

Conclusion

Category:

1

3.

Board Recommendation

None

V.

SUPPORTING DATA AND SUMMARIES

A.

Licensee Activities

Unit 1 began the assessment period at power.

The unit experienced

one forced maintenance outage in September 1986, prior to shutting

down for extensive feedwater and condensate system piping repairs in

December 1986.

The unit returned to power operation in late

February 1987, and operated at power until the middle of May 1987,

when the unit was tripped from full power due to failure of a loop

isolation valve stem.

From the middle of May 1987, until the unit

entered its scheduled refueling/maintenance outage in April 1988,

Unit 1 experienced nine unscheduled outages lasting an average of

seven days each. At the end of the evaluation period, Unit 1 was in

day 21 of a scheduled 62 day outage.

Unit 2 began the assessment period at power.

The unit operated at

power until early October 1986, when it entered a scheduled refueling

outage.

The unit comp 1 eted the refue 1 i ng outage and returned to

power operation in early December 1986. Approximately one week after

returning to power operation, Unit 2 experienced an automatic reactor

.,

,

_>

',.'

  • *** > ~-' :*,. *

i-.*---.-~-*****,-,*.-,*-~*-******:***--.,-,--

38

trip followed by a main feedwater pump suction line rupture.

The

unit was brought to cold shutdown and extensive repairs to the feed-

water and condensate piping systems were accomp 1 i shed.

The unit

returned to power operation in late March.1987, *and with the

exception of one forced outage in early April to balance the main

turbine, Unit 2 operated at power (247 days) until the unit was shut

down in December 1987, for a scheduled snubber inspection/maintenance

outage.

The unit returned to power operation in late December 1987,

and operated at power for the remainder of the evaluation period with

the exception of one forced outage in March 1987, to repair a vital

bus power supply.

B.

Inspection Activities

During the assessment period, routine inspections were performed at

the Surry facility by the resident and regional inspection staffs.

From September to December 1986, 15 inspections were conducted

including the special inspection associated with the Unit 2 pipe

break event.

During 1987, 35 inspections were conducted including a

special

inspection associated with

10

CFR

50,

Appendix

R

requirements.

From January through April 1988, 13 i nsp_ect ions were

conducted including a special team inspection for balance of plant

maintenance and a special inspection associated with the incore

detector withdrawal event in March 1988.

C.

Investigation and Allegation Review

No significant investigations or allegations occurred during this

SALP period.

D.

Escalated Enforcement Actions

1.

Civil Penalties

a.

A severity level III violation for failure to implement

fire protection requirements of 10 CFR Appendix R with no

civil pena 1 ty.

b.

A severity level III violation for failure to maintain and

verify operability of heat trace ci~cuitry for boric acid

flow path ($50,000 civil penalty).

c.

A severity level III violation for failure to adequately

evaluate the radiation hazards, having adequate procedures,

and following approved procedures while working on a stuck

incore detector ($100,000 civil penalty).

2.

Orders

None

"'~- ................... '.

-* *.* *-. . ** *"" v,* , ....... * ,

... *:," .

. .**

39

E.

Licensee Conferences Held During Appraisal Period

Management Meeting held on April 13, 1987, to discuss implementation

of the Fire Protection Issues.

Enforcement confer*ence held on May 19, 1987, to discuss the failure

to meet the requirements of 10 CFR 50, Appendix R, with respect to

the independence of cabling associated with alternative safe shutdown

equipment.

Enforcement conference held on August 26,

1987, to discuss a

violation of containment integrity.

Enforcement conference held on

September 24,

1987,

to discuss

deleting the turbine valve freedom testing without performing a 10

CFR 50.59 safety evaluation and failure to perform a Technical

Specification required surveillance.

Management Meeting held on January 13, 1988, to discuss circulating

and service water repairs.

Enforcement conference held on March 28, 1988, to discuss inoperable

heat tracing on certain safety-related boric acid lines.

Enforcement conference. he 1 d on Apri 1 21, 1988, to discuss the

findings of the investigative task force formed to review the incore

detector maintenance radiation exposure event of March 3, 1988, and

subsequent corrective actions.

F.

Confirmation of Action Letters

No Confirmation of Action letters were issued in this period.

G.

Discretionary Enforcement

October 13, 1987, Unit 1 main steam line trip valves

March 30, 1988, Unit 1 nuclear service water system repairs

April 1, 1988, both units, organizational changes

Above dates refer to NRC letter issuances.

H.

Review of licensee Event Reports

During the assessment period there were 79 LERs reported.

The

distribution of these events _by cause, as determined by the ~RC

staff, was as follow:

..... -.-r:.,- ... * ...

,"., l*

-

  • .**.:*
  • *

r-

,. *- ~***

I.

--

I L . . . . ---. *-. . . *----- .. ". --

40

Component Failure

Design

Construction, Fabrication, or

Installation

Personnel

Operating Activity

Maintenance Activity

Test/Calibration Activity

Other

Out of Calibration

Other

Total

Licensing Activity

1.

NRR/Licensee Meetings

SALP Meeting

Management Briefing Meeting

Unit 1

17

13

4

10

6

5

1

3

2

--

61

ISI/IST Program and Recirculation Spray Pumps

Steam Gene~ator Tube Rupture Analysis

!ST Program Review Meeting

2.

Commission Briefings

Unit 2 Feedwater Line Rupture

3.

Schedular Extension Granted

None

4.

Reliefs Granted

Reactor Vessel Nozzle Surface Examination

Relief from first 10-year inspection interval

Relief from inservice testing requirements

Relief for component cooling water and

. *... . ...... , ... ' . , .... ~.

*
  • ~ ' .. --: *- ... --._

Unit 2

6

1

1

4

l

3

0

2 a

18

Total

23

14 s

14

7

8

1

5

2

79

Dates

3/12/87

4/7/87

11/9/87

12/23/87

3/29/88

2/25/87

10/29/86

4/15/87

1/6/88

2/25/88

5.

41

Recirculation spray heat exchangers

Exemptions Granted

Appendi x-R, 10 CFR 50

6.

License Amendments Issued

Titles

Amendment Nos.

Organizational changes

Deletes inservice inspection

requirements for reactor vessel

closure head cladding

Extension of OL to 40 years

Revises frequency of audit of

security program

Transfer of canal door over

spent fuel pool

MSIV closing time TS

FQ(Z) and accumulator water

volume TS affected by revised

LOCA analysis

New improved fuel, control rod

insertion limit and fully

withdrawn position

TS changes in Section 3.7 and

4.1 which included 83-28

item 4.3 and WCAP 10271 changes

Core exit thermocouple and

smoke detector Tech. Spec.

Organizational changes

(Generic Letter 88-06)

109

110

111

112

113

114

115

116

117

118

119

7.

Emergency Technical Specification Issues

None

8.

Orders Issued

None

109

110

111

112

113

114

115

116

117

118

119

2/25/88

Dates

9/9/86

11/21/86

12/31/86

2/3/87

3/10/87

11/17 /87

12/10/87

1/6/88

2/17/88

3/15/88

4/28/88

', --... --*-. .---:-*.-- . *-

~ .. '

. .

. *_' '*

J.

42

Enforcement Activity

UNIT SUMMARY

FUNCTIONAL

NO. OF DEVIATIONS AND VIOLATIONS IN EACH

AREA

SEVERITY LEVEL (SL)

D

V

IV

III II

I

UNIT NO. 1/2 1/2

1/2 1/2 1/2

1/2

Plant Operations

1/1

5/5

t:.

Radiological Controls

3/3

5/5

t:.

Maintenance

1/1

0/1

Surveillance

1/1"'

Fire Protection

1/1 1/1

Emergency Preparedness

1/1

Security

3/3

Outages

1/1"'

Quality Programs and

Administrative Controls

1/1

1/3$

Affecting Qual~ty

Licensing Activities

Trainin

TOTAL

1/1

5/5

18/21 3/3

Notes t:.

88-04 and 88-10; two Severity level III violations with

civil penalties issued after SALP period ended and are

counted here.

"'

$

86-36 (Severity level IV, Unit 2 only, outages) and 87-21

(~L V, surveillance) both are under NRC review, not counted

here.

88-11, two Severity level IV violations , Unit 2 only, are

counted here, but the report was issued after the SALP

period.

K.

Reactor Trips

a.

Unit 1 on September 19, 1986, from 20: power.

Event was due to

indication of second dropped control rod requiring manual reactor trip in accordance with procedure.

b.

Unit 2 on December 9, 1986, from 10~ power.

Event was due to

closure of C steam generator main steam trip valve resulting in

steam generator Clow low level trip signal.

c.

Unit 2 on March 16, 1987, from 0% power.

Event was due to

personne 1 error 1 n performance of a periodic test during

preparation for startup.

~ ,. ..

- *:

'

.

.

'

'

.*

. -.

. -- ._ .. ,*-:-;*

'** -.. _.--** .

--

43

d.

Unit 2 on April 4, 1987, from 11~~ power.

Event was due to

generator anti-motoring turbine trip due to governor valve

leakage resulting in turbine trip/reactor* trip.

e.

Unit 1 on May 16, 1987, from 100~~ power.

Event was due to

partial loss of flow in A reactor coolant loop due to failure of

A hot leg loop stop valve allowing valve to partially shut

blocking loop flow and resulting in low flow trip.

f.

Unit 1 on August 7, 1987, from 100~~ power.

Event was due to

failure of* the cooling capability of the 18 main transformer

resulting in operator action to manually trip the unit.

g.

Unit 1 on September 20, 1987, from 100% power.

Event was due to

trip of B reactor coolant pump breaker due to a phase to ground

fault in the B phase at the electrical connection on the pump

resulting in B reactor coolant pump breaker open unit trip.

h.

Unit 1 on February 16, 1988, from 100!'~ power.

Event was due to

personnel error during performance of surve i 11 ance testing of

the reactor protection logic.

i.

Unit 2 on March 27, 1988, from 100~~ power.

Event was due to

failure of power supply to vital bus III which resulted in loss

of cooling flow to A Reactor Coolant Pump and required manuil

reactor trip in accordance with procedure.

L.

Effluent Summary for Surry

Activity Released (curies)

1.

Gaseous Effluents

Fission & Activation

Products

Iodines and Particulates

2.

Li gui d Effluents

Fission & Activation

Products

Tritium

.. -~-* -* ~-- --- -~--.~-.-* -.

1985

2.07E+3

2.67E-2

8.52EO

1.09E+3

1986

1987

1. 99E+3

3.08E+2

2.09E-2

2.09E-2

8.77EO

5.17EO

8.73E+2

8.15E+2

. '

~ ....... \\

.. , . :* -**::--... -,:;*;*.

.. __ .* ..

. . **:

.* .

. . ,""

-

List of Acronyms

BOP

CRO

CTS

cw

OR

EDO

HPES

HP

ISC

IEB

IEN

IFI

INPO

LER

MOVAT

MSIV

MWO

NOOPS

NODS

NPROS

NRC

NSE

OER

OJT

O&M

OMC

OP

OPA

PM

PMT

POD

PORV

PT

QA

QAOIN

QAOPS

QAOS

QC

QCAR

QMT

QS

RCP

RHR

RS

RWP

SALP

--~ ~-~*: .... ' ,. ___ .. --* -

ENCLOSURE 3

'

I

Balance of Plant

Control Room Operator

Commitment Tracking System

Circulating Water System

Deviation Report

Executive Director for Operations

Human Performance Evaluation System

Health Physics

Instrumentation and Controls

Inspection and Enforcement Bulletin

Inspection and Enforcement Notice

Inspector Followup Item

Institute of Nu~lear Power Operations

Licensee Event Report

Motor Opeta-ted Valve Analysis and Testing

Maintenance Work Order

Nuclear Operations Department Policy Statement

Nuclear Operations Department Standard

Nuclear Plant Reliability Data System

Nuclear Regulatory Commission

Nuclear Safety Engineering

Operational Experience Review

On The Job Training

Operation and Maintenance

Operations Maintenance Coordinator

Operating Procedure

Operational Performance Assessment

Preventive Maintenance

Post Maintenance Test

Plan Of The Day

Power Operated Relief Valve

Performance Test

Quality Assurance

Quality Assurance Department Instruction Nuclear

Quality Assurance Organization Policy Statement

Quality Assurance Organization Standard

Quality Control

Quality Control Activity Report

Quality Maintenance Team

Quench Spray

Reactor Coolant Pump

Residual Heat Removal

Recirculation Spray

Radiation Work Permit

Systematic Assessment of Licensee Performance

... , -.--.-** ..... .

. --- *-;** --.* *: .

. -- --,~:---,,,.._-- ' - ' . *.** - ***,-*-;- . -- ... :*

.*.

-

. -

~- .

. -'.,. . .

.

~-

.. ,. ..

,. .

-'* _, ' ... *,_ .. -*--**** .. -..

SRO

ss

STA

TS

TSC

URI

WGOT

WO

WR

. . .

,. - . -**- - -:~,.-. -

( .. ,-..

2

Senior Reactor Operator

Sh1f\\- Supervisor

Shift Technical Advisor

Technical Specification

Technical Support Center

Unresolved Item

.

Waste Gas Decay Tank

Work Order

Work Request

... *- . ~--. . .*. -***.~- _: .. , . ; .:** :~*:.._-~--* ::*,:::. --_";" .*

. ".-.:-*-;* --.**