ML18102A744

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Insp Repts 50-272/96-17 & 50-311/96-17 on 961113-1214. Violations Noted.Major Areas Inspected:Licensee Operation, Engineering, Maint & Plant Support
ML18102A744
Person / Time
Site: Salem  PSEG icon.png
Issue date: 01/08/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18102A742 List:
References
50-272-96-17, 50-311-96-17, NUDOCS 9701130122
Download: ML18102A744 (45)


See also: IR 05000272/1996017

Text

Docket Nos:

License Nos:

Report No.

Licensee:

Facility:

Location:

Dates:

~

Inspectors:

Approved by:

U. S. NUCLEAR REGULATORY COMMISSION

50-272, 50-311

DPR-70, DPR-75

REGION I

50-272/96-17, 50-311196-17

Public Service Electric and Gas Company

Salem Nuclear Generating Station, Units 1 & 2

P.O. Box 236

Hancocks Bridge, New Jersey 08038 .

November 3, 1996 - December 14, 1996

C. S. Marschall, Senior Resident Inspector

J. G. Schoppy, Resident Inspector

T. H. Fish, Resident Inspector

J. D. Noggle, Senior Radiation Specialist

E. H. Gray, Steam Generator Project Inspector

Larry E. Nicholson, Chief, Projects Branch 3

Division of Reactor Projects

9701130122 970108

PDR

ADOCK 05000272

G

PDR

EXECUTIVE SUMMARY

Salem Nuclear Generating Station

NRC Inspection Report 50-272/96-17, 50-311 /96-17

This integrated inspection included aspects of licensee operations, engineering,

maintenance, and plant support. The report covers a 6-week period of resident inspection;

in addition, it includes the results of inspections of radiological controls and steam

generator replacement by regional specialists.

Operations

During this inspection period, conservative decisions characterized operator performance.

Several of the decisions demonstrated the operators' high standards for equipment

availability prior to commencing core reload (Section 01 . 1). Operators demonstrated

improved performance in procedure adherence and inifa1ted- appropriate measures -to*

improve procedure quality. Senior reactor operators maintained good control over control

room evolutions and remained aware of equipment and safety system status (Section

03.1 ).

Before the start of refueling the unit 2 core, .inspectors confirmed that Salem

refueling. procedures insured compliance with the design basis and Technical Specification

requirements for fuel handling (Section 01.2). The Salem Senior Nuclear Shift Supervisors

maintained high standards for equipment and staff readiness in preparing for Salem Unit 2

refueling(Section 04.1) The operating shift demonstrated good safety focus in insisting

upon a procedure to control a total station air outage. The plant staff, however, did not

perform a 10 CFR 50.59 safety evaluation until prompted by the inspector. (Section 02.1 ) .

The plant staff made significant progress in addressing station air and control air reliability

concerns. The inspectors noted that plant staff continued to implement actions to improve

station and control air reliability. Although performance problems continued to occur with

the station and control air systems, the inspectors concluded that plant staff completed

adequate corrective actions to support plant startup (Section 02.2)

Maintenance

Inspectors observed improved maintenance performance during the inspection period. For

example, workers demonstrated ownership for their work by identifying additional small

jacket water leaks, a thermocouple that needed to be replaced, and demonstrated the

ability to effectively and safely diagnose and repair the EDG jacket water leak. During no.

23 service water strainer filter replacement, workers displayed familiarity with contents of

the procedures and the work package. They maintained current documentation of the

work and identified three items in the procedure that required clarification. The workers

took steps to obtain the clarification. The inspectors noted close supervision of the SW

work, and a good questioning attitude on the part of the workers (Section M 1. 1) In

response to learning that the Salem preventive maintenance (PM) program did not prevent

inappropriate lubrication of double-shielded bearings in the past, plant staff initiated

changes to the PM program in June 1996 that effectively controlled bearing lubrications

(Section M1 .2). Plant staff appropriately identified use of instruments with insufficient

accuracy during EDG surveillances, appropriately incorporated use of more accurate

ii

i.

instruments, and revised the EDG surveillance procedures to insure use of the new

instruments (Section M 1 .3)

Engineering

As a result of development and use of safety evaluation procedures and training, the safety

evaluations presented to the Station Operations Review Committee (SORC) showed

significant improvement in comparison with the quality of safety evaluations in early 1995.

They supplied comprehensive bases for concluding the changes did not constitute

unreviewed safety questions. In addition, the SORC reviews of safety evaluations also

improved (Section E1 .1 ). The engineering staff had not resolved the effect of operating

the penetration cooling system with air flows different than assumed design basis flows

(Section E1 .2).

The region-based steam generator replacement project (SGRP) Project Manager performed

inspections at the Salem site and the contractor's engineering office *:o cbtain an overview

of current and planned work, related procedures, documentation, quality inputs and

progress of the Salem Unit 1 SGRP. The inspector found generally high quality

performance in the areas inspected and identified no safety significant project deficiencies.

The inspector noted problems, however, with some first time evolutions that indicate a

potential deficiency in planning, work control, or full understanding of procedure

requirements by those performing work. The Salem SGRP management initiated corrective

and preventive actions to improve project performance (Section E1 .3).

The Salem staff implemented appropriate and timely corrective actions in response to

identification of improperly installed welds during implementation of the control room

ventilation modification (Section E1 .4).

Plant Support

The inspector determined that the licensee met and exceeded the planned radiation

protection (RP) staffing levels to support the steam generator replacement project (Section

R1 .2).

The additional remote surveillance capability of the RP command center was effectively

used to review work areas. The inspector observed conservative use of the remote

surveillance approach utilizing on-the-job RP technician resources to engage normal work

control situations. Also, the containment clean areas and radioactive material outside of

containment were effectively monitored and controlled during this inspection (Section

R1 .2).

An effective mockup training for installation of steam generator seal plates was performed.

Important sequencing of work details was established and an understanding of the scope

of work and radiological implications of the work were effectively discussed and

communicated to those present. However, the licensee had not established a requirement

that only those in attendance of the mockup training could perform the work and task

qualification controls had not been established for the seal plate installation work (Section

R1 .3).

iii

Contamination was well controlled and minimized. Through the use of temporary shielding

and filling of steam generators, radiation levels of principal work areas were maintained at

low levels without significant dose rate gradients. The inspector determined that excellent

radiological conditions were established for conducting the steam generator replacement

project (Section R2.1 ).

Although work packages were not all completed at the time of this inspection, general

work descriptions of all radiologically significant work had been researched and individual

RP job guidelines for each had been developed to provide some advance RP planning and

to communicate a level of RP technician job performance expectation. These RP job

guidelines provided a moderately effective vehicle for orienting and guiding the RP

technicians in preparation for radiologically significant project work evolutions (Section

R3.1).

The licensee had not dedicated specific quality assurance (QA) oversight review of the RP

program performance during the SGRP and only routine QA surveillance activities were*

being provided. In response to this finding, the licensee obtained an additional member of

the SGRP QA oversight group tasked with specific responsibility for radiation protection

oversight (Section R7).

The inspector identified overall effective radiological controls for Salem Station radiological

work activities, including preparation and transfer for disposal of the Unit 1 No. 14 steam

generator. Internal exposure controls, including contamination controls, were very good.

Augmentation of the staff was good with good training and qualification of personnel

noted. Self-identification of radiological concerns was very good. However, a noteworthy

weakness was identified in review and resolution of all issues identified in radiological

occurrence reports. Further, improvement in the identification and control of alternate

access paths to locked high radiation areas appeared warranted .

iv

TABLE OF CONTENTS

EXECUTIVE SUMMARY

ii

TABLE OF CONTENTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

v

I. Operations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

1

II. Maintenance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

9

Ill. Engineering

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

14

IV. Plant Support .... '. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .. . . . . . .. . . . 24

V. Management Meetings . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .. . 38

v

Report Details

Summary of Plant Status

Salem Unit 1 remained defueled throughout the inspection period. Late in the period,

workers removed the last of the four original steam generators from containment. The

plant managers expect to move the first replacement steam generator into containment in

early January 1997.

Salem Unit 2 staff neared completion of refueling preparations at the end of the inspection

period.

01

01.1

I. Operations

Conduct of Operations

General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations. In general, the conduct of operations was professional

and safety-conscious; specific events and noteworthy observations are detailed in

the sections below. The inspectors noted several examples of conservative

decisions by operators. Several of the decisions demonstrated the operators' high

standards for equipment availability prior to commencing core reload.

01.2 Preparations for Unit 2 Refueling

a.

Inspection Scope (60705)

The inspector reviewed procedures and administrative requirements for refueling

Salem, Unit 2.

b.

Observations and Findings

The inspector reviewed Salem refueling procedures to determine whether they met

the design basis of the plant as described in the Updated Final Safety Analysis

Report (UFSAR). For example, the UFSAR states that, prior to refueling, the reactor

is borated to refueling concentration. This requirement is captured in S2.0P-10.ZZ-

0009(Q), Defueled to Mode 6. The UFSAR also describes the capabilities and

safety features of the manipulator crane, such as bridge, trolley and hoist interlocks.

Maintenance procedure SC.MD-ST.CRN-0001 (Q), Fuel Handling Crane Periodic

Inspections, Operational Tests and limit Switch Adjustment, tests these features.

The inspector confirmed the refueling procedures adequately supported the Salem

facility as described in the UFSAR .

2

The inspector also reviewed refueling procedures to determine whether they

identified the Technical Specification requirements for entering Mode 6.

Attachment 2 of Integrated :Operating Procedure (IOP-) 9 lists the surveillance

requirements that demonstrate operability for equipment required by Technical

Specifications, including, for example, the emergency diesel generators, control

room ventilation, and the radiation monitoring system.

The inspector confirmed

refueling procedures insured compliance with the Technical Specification

requirements for entering Mode 6.

c.

Conclusions

Inspectors confirmed that Salem refueling procedures insure compliance with the

design basis and Technical Specification requirements for fuel handling.

02

Operational Status of Facilities and Equipment

02.1

Total Station Air Outage

a.

Inspection Scope (71707)

b.

The inspector observed operators' implementation and restoration of a total station

air outage.

Observations and Findings

On November 1 2, 1 996, Salem operations commenced a total station air (SA)

outage. When tagging instructions for the SA outage expanded to five pages, the

operators insisted that the staff develop a new procedure, TSC.OP-SO.CA-0101,

Maintaining Control Air System During Station Air System Manifold Replacement, to

control the work. The plan involved use of temporary station air compressors to

supply Unit 1 safety-related control air, the station blackout (SBO) air compressor to

supply Unit 2 safety-related control air, taking the safety-related emergency control

air compressors (ECAC) out of automatic control, and bypassing a check valve to

supply non safety-related control air from the safety-related piping. The inspector

found that operations staff did not consider these to be changes to the facility as

described in the safety analysis report. As a result, they did not perform a safety

evaluation as required by 10 CFR 50.59. (VIC 50-272&311196-17-01) In response,

operations management appropriately ensured safe plant configuration and

completed a thorough safety evaluation. The inspector determined that the safety

evaluation appropriately concluded that the changes did not result in an unreviewed

safety question (USQ).

The inspector noted that the procedure unnecessarily limited operators to use of

only two of the three available temporary air compressors. The unnecessary

restriction made operators more vulnerable to station air equipment problems. The

Senior Reactor Operator (SRO) initiated an on-the-spot-change to correct this

3

deficiency. Operators subsequently needed the third temporary air compressor

when one of the other temporary air compressors could not handle the load.

On November 15, the operating shift experienced several problems with station and

control air components that delayed system restoration until November 20. These

problems included: (1) no. 1 ECAC trip on start demand, (2) no. 1 station air

compressor (SAC) would not stay latched in auto, (3) no. 2 SAC would not start,

then experienced excessive amp swings, (4) no. 3 SAC lube oil reservoir heater

controller malfunctioned, and (5) a temporary air compressor could not handle the

load. The system manager initiated corrective action for each of the above

deficiencies.

c.

Conclusions

The operating shift demonstrated a good safety focus in insisting upon a procedure

to control a total station air outage. The plant staff, however, did not perform a 10

CFR 50.59 safety evaluation until questioned by the inspector.

02.2 Reliability of Control Air (NRC Restart Issue 11.2) (Closed)

a.

b.

Inspection Scope (71707)

The reliability of the control air system, the control air dryers, and the service air

system compressors that supply the control air system has been a long standing

concern at Salem. Distractions caused by degraded control air conditions have

frequently challenged operators. The NRC documented control air reliability

concerns in NRC Inspection Reports 50-272, 311/94-19, 94-24, and 94-34.

PSE&G initiated design changes, conducted refurbishment and performed preventive

maintenance activities to address these long standing issues. Plant staff

documented these actions in the Control Air System Reliability closure package,

dated November 6, 1996. The inspector reviewed the closure package as well as

related work documents, design change packages, test results, operating

procedures, calculations, and Performance Improvement Requests (PIRs). In

addition, the inspector conducted field observations to evaluate the material

condition of portions of the service and control air systems.

Observations and Findings

From the review of the closure package, the inspector found that Salem staff

identified the following issues as contributi~g to the control air reliability concerns:

Control Air D~yers - Air header pressure decreases during dryer maintenance,

resulting in auto start of the ECACs and low pressure alarms in the power operated

relief valve (PORV) accumulators.

PORV Accumulators - Low pressure alarm resulted in operators closing the PORV

block valves.

4

Station air compressors (SACs) - Numerous high vibration trips and other problems

resulted in concerns with SACs availability and reliability.

Plant staff completed the following actions:

To address the overall reliability of the control air system, plant staff completed the

air dryer pre-filter PMs on schedule. Delaying this activity in the past compounded

the effects on the control air system because the other pre-filter degraded during

the delay. Subsequent removal of the first pre-filter from service for cleaning

caused increased air flow through the remaining air dryer, resulting in an increased

differential pressure across the air dryer, further degrading the control air header

pressure. Prompt pre-filter maintenance will ensure control air pressure is

maintained within acceptable limits during maintenance. In addition, plant staff

refurbished the dryer skids, inspected and/or replaced the desiccant, rebuilt the

switching valves, and replaced the control solenoid poppits. Maintenance staff

issued a repetitive task PM for the control solenoid poppits to require annual

inspection or rebuild.

The actions taken for the control air dryers will also preclude having to close PORV

block valves as a result of degraded control air header pressure. In addition, plant

staff discovered a problem with the PORV alarm and solenoid setpoints on Unit 2.

They implemented DCP 2EC-3416 to correct this condition.

To address high vibration tripping of the SACs, Salem staff installed a design

change (DCP 1 EE-0324) to eliminate vibration trips as a result of displacement

during compressor startup.

Workers had not completed implementation of SAC design change package DCP

1 EC-3651 at the close of the inspection period. Installation of this DCP will address.

the following SAC issues, to further improve the reliability of the station air system,

and thus the control air system:

Condensate removal problems with the coolers and moisture separators will

be corrected by installation of automatic drain valves. This condition has

resulted in two (2).compressor trips due to high moisture levels in the

moisture separators

Rust in the discharge piping between the compressor and the aftercooler

contributes to pre-filter clogging resulting in increased maintenance on the

control air dryer skids. Plant staff will replace the degraded piping.

The blowoff valves are too far from the compressor. The location has

resulted in compressor surge conditions, reducing compressor overall. Plant

staff will replace and relocate the blowoff valves.

The SACs remain susceptible to vibration trips during load carrying

conditions due to the cyclic loading and unloading of the compressors.

Engineers expect installation of a constant pressure control option to provide

5

compressor stability during operation by significantly reducing the cycles

imposed on the valves, relays, and switches.

During the review of the closure package, the inspector identified questions about

past operation of the containment penetration cooling system. These are

documented in section E1 .2 of this report.

c.

Conclusion

The inspectors concluded that plant staff made significant progress in addressing

station air and control air reliability concerns. The inspectors noted that plant staff

continued to implement actions to further improve station and control air reliability.

For example, plant staff continued installation of DCP 1 EE-0324 to convert the

compressors to constant pressure operation, further reducing station air compressor

trips. Although performance problems continued to occur with the station and

control air systems (see section 02.1 ), the inspectors concluded that plant staff

completed corrective actions and the measures to insure prompt air dryer

maintenance were adequate to support plant startup.

03

Operations Procedures and Documentation

03.1

Procedure Use and Quality

The inspector observed control room operator use and adherence to implementing

procedures. During the inspection period, operators demonstrated consistent

attention to procedure compliance. Operators made a conscientious effort to use

procedures to control activities whenever possible. Operators insisted upon new

procedure development when required to perform complex evolutions that did not

have adequate guidance. An example of this behavior was operations' staff

development of TSC.OP-SO.CA-0101 to control an abnormal station air outage (see

section 02.1 ). In addition, the operating shift, including the test engineers, stopped

control room activities to implement procedure improvements. The inspector noted

that the operating shift repeatedly sacrificed productivity to ensure the procedure

was correct and appropriate. This was evident in "B" vital bus testing as the

operating shift implemented no fewer then seven on-the-spot-changes. The

inspector observed detailed shift briefings prior to complex evolutions and

significant SRO involvement in all control room activities. The inspector concluded

that operators demonstrated improved performance in procedure adherence and

initiated appropriate measures to improve procedure quality. Senior reactor

operators maintained good control over control room evolutions and remained aware

of equipment and safety system status .

04

04.1

a.

b.

07

07.1

6

Operator Knowledge and Performance

Operator Standards for Plant Equipment

Observations and Findings (71707)

During the inspection period, operators demonstrated high standards for equipment

acceptability on a number of occasions. For example, they identified generic

aspects of a failure of the operator for the service water inlet valve to the no. 28

EOG lube oil cooler. They insisted on acceptable resolution prior to entering mode

6. When they learned about a hinge pin corrosion problem in an EOG service water

check valve, they declared the associated EOG inoperable. In a meeting with the

Management Review Committee, the Senior Nuclear Shift Supervisors (SNSSs) from

the fm~r crews slated to restart Salem Unit 2 identified several issues that required

resolution prior to reloading the core. The issues included repair of the no. 28 EOG

jacket water leak, complete review of the Technical Specification Limiting Condition

for Operation (LCO) tracking log by each SNSS, and completion of training for the

design change packages (DCPs) required for mode 6. In order to determine operator

readiness for mode 6, the SNSS for each crew assessed the readiness of each

member of their crew through interviews and observation. In addition, each SNSS

reviewed surveillance results, outstanding operator workarounds, temporary

modifications, and degraded control room indicators for equipment required for

mode 6. In this manner, the SNSS for each crew determined the readiness to begin

refueling operations.

Conclusions

The Salem Senior Nuclear Shift Supervisors maintained high standards for

equipment and staff readiness in preparing for Salem Unit 2 refueling.

Quality Assurance in Operations

(Closed) Violation 50-272&311 /96-12-01: failure to take adequate actions for a

significant condition adverse to quality to preclude repetition. Inadequate

procedures allowed operators to enter Mode 6 without ensuring that they met the

reactivity requirements of TS 3.9.1. Although an operator identified and

documented the failure to meet TS 3.9.1 requirements, the licensee failed to take

adequate corrective actions. In response to the violation, operations staff revised

the integrated operating procedure for Mode. 6 to require proper boron concentration

sampling. Operations staff revised the reactor cavity fill procedure, S2.0P-SO.SF-

0003, and issued the violation response to the Operations and Licensing

Departments as required reading. The inspector verified the S2.0P-SO.SF-0003

procedure revision and the required reading material.

The inspector noted that the response did not discuss the licensee's Quality

Assurance (QA) program practices and procedures. The licensee did not review QA

oversight practices to determine if QA should have identified the violation and what,

08

08.1

7

if any, measure need be taken to strengthen the QA program. The *inspector

observed that an inadequate procedure and inappropriate condition resolution (CR)

corrective actions contributed to the violation. The inspector reviewed the QA

Monthly Reports from December 1995 to August 1996 and noted limited QA

oversight of procedure adequacy and corrective action thoroughness. During

discussions with the inspector, QA managers stated that they had implemented

measures to adjust the QA program based on observed weaknesses in plant staff

and equipment performance. They also stated that they planned to continue to

improve adjustments to QA program focus.

The inspectors concluded that the licensee implemented adequate corrective action

for-entering mode 6 without insuring compliance with TS 3.9.1. The inspectors will

continue to monitor the QA adjustment to performance problems as part of normal

inspector follC1wup of violation responses.

Miscellaneous Operations Issue

(Closed) Violation 27 2&311 /94-24-03

During a Salem Unit 2 shutdown in October 1994, plant staff failed to perform a

daily heat balance calibration of the power range neutron flux functional unit. The

plant staff determined that operators incorrectly interpreted daily as meaning once

per day, as opposed to once per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. In response, plant staff revised the shift

routine procedure, SC.OD-DD.ZZ-OD40, to clarify the surveillance frequency and

separate actions required by Technical Specifications from actions required for other

reasons. In addition, the operators received training specific to the missed heat

balance calibration. The inspector verified implementation of the corrective* actions

and considered them adequate to prevent recurrence.

08.2 (Closed) Violation 50-272&311 /94-24-05

In October 1994, a security guard permitted two persons to enter the Salem Unit 2

no. 2C emergency diesel generator (EDG) room without verifying proper

authorization prior to granting access. Security staff attributed the violation to

personnel error. In response, they immediately relieved the guard, retrained and

certified the guard in performance of control access in an emergency or on a

compensatory post, and discussed the incident with guard force personnel during

shift briefings. The inspectors considered the corrective actions adequate to

address the cause of the violation. Inspectors and plant staff identified broader

security performance weaknesses during routine inspection in August 1996. The

NRC documented the broader issues separately and proposed escalated

enforcement. The NRC will assess the effectiveness of corrective actions for those

problems during subsequent inspection .

.*

8

08.3 (Closed) Violation 50-272&311/95-10-01

Jn June 1995, a technician failed to unlatch the no. 2R cylinder fuel pump rack on

the no. 1 C EOG. As a result, plant staff operated the EOG during a surveillance

without fuel supplied to the affected cylinder. The EOG did not suffer damage as a

result. Plant staff concluded that personnel error caused the violation. In response,

maintenance managers counseled the technician, reviewed the applicable

maintenance procedure for adequacy, and revised the procedure to add independent

verification that the fuel racks are unlatched. The inspector reviewed the

procedure, SC.MO-ST.OG-0003(0) to ensure the procedure required independent

verification that technicians unlatched all fuel pump racks.

In May 1995, inspectors discovered that operators had not ensured the no. 2C EOG

fuel rack linkage remair.arl ~n the open position after completion of a surveillance.

Plant staff determined that personnel error was the most probable cause. They also

determined that EOG design features automatically positioned the fuel racks to

supply full fuel on an EOG start. As a result, plant staff concluded the procedure

requirement for operators to reposition the fuel racks was not required for proper

EOG operation. In response, the plant staff deleted the procedure requirements to

manually position the fuel racks .. In addition, operations staff reviewed department

procedures to insure that the procedures included appropriate measures for

independent verification. The inspectors verified that the operations staff deleted

the requirement for manual fuel rack positioning from the applicable procedures and

that the procedures contained appropriate requirements for independent verification.

08.4 (Closed) Violation 50-272&311/95-10-02

In May 1995, the licensee completed a shutdown of Salem Unit 1, and did not

report the shutdown within 30 days as required. The Salem staff determined that

inadequate focus on reporting requirements, lack of follow up by plant staff on a

known commitment, lack of ownership and accountability for the Licensee Event

Report (LER) process, and a flawed submittal strategy contributed to the failure. In

response, the licensee completed and submitted all overdue LERs, counseled plant

staff concerning ownership and accountability, and modified the LER process to

include timely scoping meetings. In addition plant staff initiated a report to identify

the status of LERs in process to insure proper management attention to completing

LERs. The inspector verified the use of the reporting system, including the

Licensing LER Performance Indicators. In addition, the inspector noted discussion of

the status of LERs at the Salem General Manager's staff meeting with appropriate

attention to insuring timely submission of the reports .

.*

9

II. Maintenance

M 1

Conduct of Maintenance

M 1 . 1 General Comments

a.

Inspection Scope (62707)

The inspectors observed all or portions of the following work activities:

WO 961206309, procedure SC.MD-CM.DG-0002(0), Emergency Diesel

Generator Cylinder Head Replacement, Rev. 0, dated 1 /28/91, and procedure

SC.MD-PT.DG-0002(0), Post Maintenance Diesel Engine Break-in Run, Rev.

0, dtd 12/13/96

WO 961202133, procedure SC.MD-PM.SW-0003(0), Service Water

Automatic Strainer Adjustment, Inspection, Repair, and Replacement,

Revision 13 dtd 1 2/5/96

While running the no. 28 EOG for testing, Salem operators observed a slow

decrease in level in the jacket water expansion tank. Maintenance staff determined

that jacket water leaked into the no. 1 R cylinder at about 25 cc/min. They

determined that the cylinder head had developed a small leak, and decided to

replace the cylinder head and liner. Although the EOG had performed within

acceptance criteria in recent tests, and although industry experience indicated that

the EOG would continue to operate reliably for months with the minor leak, they

decided to replace the cylinder head. After removing the head, the maintenance

staff found that jacket water leaking into the cylinder had apparently caused

polishing of the cylinder liner. Although they did not consider the liner significantly

degraded, they replaced the liner also. During the replacement of the EOG cylinder

head, inspectors noted that the workers had the work package on site and in use.

Although maintenance staff concluded that the cylinder head and liner met design

requirements for continued use, they conservatively decided to replace the liner and

head. Workers demonstrated ownership for their work, as demonstrated by

identifying additional small jacket water leaks, a thermocouple that needed to be

replaced, etc. As a result of their efforts, the maintenance staff demonstrated the

ability to effectively and safely diagnose and repair the EOG jacket water leak.

Inspectors also observed technicians replacing the filter elements in the no. 23 SW

strainer. During discussions with the inspector, workers demonstrated familiarity

with contents of the procedure and the work package. The workers maintained

current documentation of the work and identified three items in the procedure that

required clarification. The workers took steps to obtain the clarification. The

inspectors noted close supervision of the work, and a good questioning attitude on

the part of the workers.

.*

b.

10

Inspection Scope (61726)

The inspectors observed all or portions of the following surveillances:

52.0P-ST.FHV-0001:

S2.0P-ST.RM-0001:

S2.0P-ST.SSP-0002:

S2.0P-ST.RHR-0004:

52.0P-ST.SSP-0004:

52.0P-ST.DG-0002:

52.0P-ST.DG-0014:

52.0P-ST.DG-0021:

SC.MD-ST.CRN-0002:

refueling operations - fuel handling building

ventilation

radiation monitors - check sources

engineered safety features manual safety

injection 2A vital bus

in service testing - residual heat removal valves

engineered safety features manual safety

injection 2C vital bus

2B diesel generator surveillance test

2C dieseJ g<;nerator endurance tun

2C diesel generator hot restart test

manipulator crane periodic inspections and

operational tests

The inspectors observed that plant staff did the surveillance safely, effectively

proving operability of the associated system.

M1 .2 Double-shielded Bearing Inspection

a.

Inspection Scope (62707)

The inspector reviewed lubrication preventive maintenance (PM) tasks for selected

safety related motors that contain double-shielded bearings.

b.

Observations

The inspector audited the lubrication PMs for the switchgear penetration area

ventilation (SPAV) fan motors, the boric acid transfer (BAT) pump motors and the

fuel handling ventilation (FHV) fan motors to determine whether technicians were

performing the appropriate PM for the type of motor bearing . The bearing type --

double shielded, single shielded, or open -- determines the PM task. In particular,

the PM program directs technicians not to lubricate double shielded bearings

because this activity could pressurize the grease cavity, causing grease to inject

into the motor. (NRC Information Notice 94-51, Inappropriate Greasing of Double

Shielded Motor Bearings, of July 15, 1994 has additional details.) The inspector

reviewed the PM history for SPAV, FHV, and BAT motors and found that, prior to

improvements in the PM program, technicians inappropriately lubricated the double

shielded bearings in nos. 11 and 12 BAT pumps (September, 1994, and January,

1995). Maintenance engineers inspected these bearings and did not find degraded

conditions. Motor vibration data was also acceptable .

.*

11

In June, 1996, Salem Maintenance staff wrote an Action Request (AR 960618077)

that identified the PM schedule inadequately controlled bearing lubrication tasks.

Subsequently, maintenance engineers identified the types of bearings for motors

installed in both units, including the BAT pump motors, SPAV and FHV fan motors,

and revised the lubrication tasks where applicable to clearly reflect that technicians

are not to lubricate double shielded bearings.

Failure of Salem staff to identify and correct lubrication deficiencies in a timely

fashion is a violation of the requirements in 10 CFR 50 Appendix B, Criterion XVI,

Corrective Action. Since the NRC has taken significant enforcement action for

Salem's failure to identify and correct conditions adverse to quality, and since

PSE&G voluntarily maintained both Salem units shut down to address equipment

and enforcement deficiencies, the NRC will not take additional enforcement action

in this case.

c.

Conclusions

Although the Salem preventive maintenance program did not prevent inappropriate *

lubrication of double-shielded bearings, the inspector found that changes to the PM

program initiated in June 1996 effectively controlled lubrication of bearings.

M1 .3 Emergency Diesel Generator !EDG) Surveillance

a.

Inspection Scope (617261

The inspector reviewed the engineering staff response to an operations department

identified concern regarding the adequacy of using an installed watt meter to

perform EDG surveillance testing (ST).

b.

Observations and Findings

The operators, in accordance with pre-existing surveillance procedures, utilized an

installed watt meter to satisfy several EDG technical specification (TS) surveillance

requirements (SRs) including: monthly load testing (SR 4.8.1.1.2.a.2), semi-annual

load testing (SR 4.8.1.1.2.c), 18 month load testing (SR 4.8.1 .1.2.d.7) and hot

restart testing (SR 4.8.1.1.2.f). The above SRs required the operators to maintain

EDG loading between 2500 and 2600 KW. The installed watt meter, however, had

an accuracy range of approximately +I- 65 KW. As a result, an indication of 2550

KW would indicate actual power somewhere within the range 2485 KW to 2615 *

KW. Operators, therefore, could not certify that the EDG had developed rated load

during the surveillance.

The inspector reviewed the 2C EDG 18 month endurance run test procedure

(S2.0P-ST.DG-0014(0)) and noted that the test procedure had been revised on

November 26, 1996 to incorporate the use of higher accuracy instrumentation. The

operators utilized the revised procedure to perform testing on all three Unit 2 EDGs.

The inspector observed portions of the 28 and 2C EDG testing and noted that the

operators maintained the EDG output within the required band.

.*

12

The operators subsequently revised remaining EOG test procedures to require the

use of the high accuracy load instrumentation in order to satisfy the other SRs listed

above. The operators performed the EOG tests in accordance with the revised

procedures.

During the 2C EOG 18 month endurance testing, the system manager compared the

load indicated by the installed watt meter to the load indicated by the high accuracy

test instrumentation to better quantify the accuracy of the installed watt meter.

The system manager determined, based on this comparison, that the previous 2C

EOG endurance test run had exceeded the required TS range. The inspector

independently reviewed the applicable test data and agreed with this conclusion.

The EOG test load restrictions had been incorporated into TSs by amendments 148 *

and 126 in November 1993. The inspector noted that TS ami:mrlment and the **

applicable EOG test procedures had not been properly reviewed at that time to

insure that the TS load requirements would be satisfied during testing.

Previously performing surveillances with inadequate instruments had minor safety

consequence, since, based on use of the less accurate instruments, the EDGs* had

been loaded during testing to within 2.5% of the required limits. This licensee

identified and corrected issue meets the criteria specified in Section Vll.b of the

NRC Enforcement Manual and is considered a Non-Cited Violation.

c.

Conclusions

Plant staff appropriately identified use of instruments with insufficient accuracy

during EOG surveillances. They appropriately incorporated use of more accurate

instruments, and revised the EOG surveillance procedures to insure use of the new

instruments.

MS

Miscellaneous Maintenance Issues

M8.1 NRC Restart Issue 11.36 - Safety Injection (SI) Relief Valves Performance History of

Leakage and Lifting !Closed - Unit 2. Open - Unit 1)

a. Inspection Scope

The inspector reviewed the corrective actions which were taken to resolve a

problem regarding repetitive Safety Injection system relief valve leakage. The

inspector reviewed the Restart Issue T-36 Closure Package. The package included

the closure summary, the root cause analysis for the probiem, and PIR Nos.

,

950901391 and 960321090. The inspector also reviewed a design change package

for Salem Unit 2 which increased the relief valve set points (DCP 2EC3582), and

procedures which provided direction for setting and testing them. The design

change package for the Salem Unit 1 change was not yet available.

13

b. Observations and Findings

The root cause analysis specified corrective action to reduce the risk of safety relief

valve failures. One corrective action was to increase the relief valve set point. This

was necessary because during safety injection pump startup, the pressure spike

would at times be sufficient to lift the relief valve causing unnecessary wear. The

inspector reviewed the design change engineering analysis and found it adequate.

The change package also contained satisfactory documentation of setting and

installation of the relief valves and documentation of satisfactory test results of the

post installation functional testing. The inspector learned from discussions with the

system engineer that there was no evidence of valve leakage during testing.

The root cause analysis also attributed a faulty test stand filter as a contributing

cause. The filter was not well maintained and as a result, particleTtsand and rust)

would be introduced into relief valves and cause seat wear. The inspector verified

that the filter was being periodically maintained as evidenced by work order

documentation.

Another corrective action was a procedure change to require leak testing before and

after set point verification on the test stand. This would provide evidence of the as

found condition and assurance that the valve was leak tight prior to installation.

Although the long term effectiveness of corrective actions taken has not yet been

determined, the inspector did verify that PIR No. 960321090 contained an action

item to verify the effectiveness by periodically reviewing relief valve lift and leak

test data.

c. Conclusions

From his review, the inspector was able to conclude that it was reasonable to

expect that implementation of the corrective actions would resolve the long term

problem of leaking relief valves. This item is closed for Salem Unit 2 but will remain

open for Unit 1 pending implementation of the design change and subsequent

testing and installation.

M8.2 (Closed) LER 272/96-027-00: This LER described the use of the installed EOG watt

meter to perform EOG testing as discussed in Section M 1 .3 of this report. No new

issues were identified by the LER.

.*

E1

E1 .1

E1 .2

a.

14

Ill. Engineering

Conduct of Engineering

Safety Evaluations*

Observations and Finding

During the inspection period, plant staff prepared several safety evaluations required

by 10 CFR 50.59, and presented them for SORC review. The safety evaluations

included:

DCP 1 EC-3453, package 1 of 3, Unit 1 EDG Fuel Oil Day Tank Setpoint

Change.

Minor modification S-96-023, Removal of 22123 CCW Pump Room Door.

UFSAR change notice 96-169, Change Temperature Range in UFSAR for

SPA V System.

The safety evaluations, prepared using procedure NC.NA-AP.ZZ-0059 (Q), 10 CFR

50.59 Safety Evaluation, included references to Technical Specification and UFSAR

sections reviewed for applicability, and other documents referenced by the

evaluator. The evaluations also listed plant procedures, affected parameters and

systems, and credible failure modes associated with the change.

The inspectors reviewed the safety evaluations and observed their presentation at

SORC. As a result of training and use of procedure NC.NA-AP.ZZ-0059 (Q), the

preparers developed consistently thorough safety evaluations that included broad

consideration of the. effects of the proposed change on plant operation. In addition,

the inspector observed that the SORC obtained a reasonable basis for approving the

safety evaluations through review of the package and questioning the presenters.

Conclusions

The inspector concluded that the safety evaluations supplied reasonably

comprehensive bases for concluding the changes did not constitute unreviewed

safety questions. In addition, the inspector observed that, as a result of the safety

evaluation procedures and training, the quality of safety evaluations and SORC

reviews has increased significantly in comparison with that observed by NRC

inspectors in early 1995.

Containment Penetration Cooler Issues

Inspection Scope (37551)

  • The inspector reviewed design calculations, test data, system descriptions, work

orders, UFSAR Section 9.1 (Compressed Air Systems), and Configuration Baseline

15

Documentation (CBD), to assess the material condition of the containment

penetration cooling system.

b.

Observations and Findings

UFSAR Section 3.8.1.6.5, Containment Penetrations and Openings, states in part:

"Cooling, by both free and forced convection, is provided where necessary to

maintain concrete temperatures adjacent to hot pipe penetrations below 1 50

degrees F. The potential heat transfer [for radial conduction] ... can be significant.

The heat is removed by compressed air flow in plate type heat exchangers (coolers)

installed within the penetration sleeves. It has been shown that for constant

exposure of concrete to temperatures up to 150 degrees F, the loss in strenyth is

quite small; and for temperatures as high as 500 to 600 degrees F, the deterioration

in structural properties is tolerable. Considering the redundancy in air supply lines,

the only cause of loss of penetration cooling would be complete loss of the station

air compressors, a condition which would not be permitted to persist long enough

to cause significant localized concrete deterioration."

During an NRC inspection of Salem's licensing basis in May, 1996, the NRC

requested the licensee provide the basis for the minimum penetration cooler throttle

valve positioning to ensure the proper flow of compressed air to the penetration

coolers .

PSE&G located a calculation that provided the basis for the throttle valve positions,

but determined that the calculation was not reproducible and was not officially part

of the CBD. The basis was re-developed in calculation S-C-PC-MDC-1657,

Penetration Cooling Valves Adjustment, Revision 0. The inspector reviewed the

calculation and determined that the minimum throttle valve positions for the

penetration coolers had been determined. The calculation also documented the

actual position of the penetration cooler throttle valves in the field. In all cases the

documented field throttle valve positions were at least the minimum specified in the

calculation.

Based on concerns the inspector had with the number of penetrations equipped with

forced air cooling, the inspector reviewed the following documents to determine

how the penetration cooling air flow rates were accounted for in the station air

consumption calculations.

UFSAR Section 9.3.1, Compressed Air Systems

CBD DE-CB.CA-0014(0), Configuration Baseline Documentation for Control

Air and Station Air Systems, Revision 3;

Calculation S-C-CA-MDC-1639, Integrated Air Load Management Program

Update, Revision 0;

Calculation S-C-SA-MDC-0525, Station Air System Load Study, Revision O;

16

Calculation S-C-CA-MDC-0549, Station Air and Control Air Systems

Analytical Flow Model and Test, Revision O;

System Description SD-M946, Containment Penetration Cooling, Revision O;

and,

Data Acquisition DCP 1 SX-2286, Determination of Air Consumption Rates

and Operating Pressures for CA and SA Systems, Revision 0.

Based on these reviews, the inspector made the following observations:

1.

The Integrated Air Load Management Program Update calculation provided

documentation that a single station air compressors (SAC) capacity was

4232 scfm and the worst case load demand was 4439 scfm. A note

contained in this calculation stated: "The total load of 4439 scfm, exceeds

the capacity of a single SAC (4232 scfm) by 207 scfm or 5%. This is well

within the conservative margin inherent in the development of the individual

loads as discussed in Section 5.1 and 5.2 of Reference 11 [Station Air

System Load Study calculation). Therefore, based on the results of this

evaluation, it is concluded that a single SAC is capable of supporting the

worst case continuous and intermittent loads."

To account for the penetration cooling system contribution to the SAC air

load, PSE&G uses an air consumption value of 636.8 scfm per Unit (1273.6

scfm total) based on the penetration cooling throttle valves being positioned

at their minimum throttle setting. The minimum required throttle valve

positions were listed in the original Containment Penetration Cooling system

description. Further, the inspector determined that the penetration cooling

air consumption value of 636.8 scfm per Unit (1273.6 scfm total) was based

on air flow through a total of 20 penetration coolers per Unit and did not

account for penetrations No. 30, 36, 54, and 55. The documented field

position for the additional throttle valves (eight per Unit) for these

penetrations were "full open". The inspector estimated that the additional air

consumption due to air flow through these open throttle valves would be

300 - 400 scfm per Unit (600 - 800 scfm total), which would exacerbate the

worst case air load consumption values used in the Integrated Air

Management Program calculation. Based on ~his estimate, the total worst

case air load would exceed a single SAC by 1J! - 24% as compared with the

~% stated in the calculation (discussed above). The inspector's estimate

was based on information- contained in the original Penetration Cooling

system descrrption and the Penetration Cooling Needle Valve Adjustment

calculation.

Salem UFSAR, Section 9.3.1, Compressed Air Systems, Paragraph

9.3.1.2.2, states: "The dual station service air headers are fed by three 100

percent capacity air compressors, any one of which can supply the total

service and control air requirements for both units." Based on the

inspector's observation, the accuracy of this UFSAR statement is in

2.

3.

4.

17

question, which may impact the operation and maintenance practices with

regard to the station air compressors.

The Station Air System Load Study calculation was performed on September

18, 1990. Section 5.2.4 of this calculation contained information that

reflected Unit 1 "as found" penetration cooling air flow measurements

significantly below the stated design flow rate (250 scfm versus 636.8

scfm). Engineering's actions documented in response to this condition was a

recommendation that the throttle valve settings be checked, and where

necessary, adjusted to the design position. At the conclusion of the

inspection period, PSE&G personnel were unable to provide a documented

engineering evaluation to show that the reduced flow through the Unit 1

penetration cooling system had not adversely degraded the containment

concrete surrounding these penetrations as a result of the reduced air cooling

flow, and whether operations had found the throttle valves out of position,

thus requiring repositioning or further flow evaluation.

The Station Air System Load Study calculation also contained information

that reflected Unit 2 as found penetration cooling air flow operating at flow

rates in excess of their design capacity. The magnitude of the air

consumption could not be established because the measuring instrument

was damaged by the excess flow. Again, engineering's recommendation

was to check the throttle valve settings, and where necessary, adjusted to

the design position.

Based on discussion with the operations staff, the inspector determined that

the operation of the pressure regulators that supply the penetration cooler air

headers are not contained in operating procedures. Valves associated with

the station air and penetration cooling systems are included in the Tagging

Request Inquiry System (TRIS) which requests the performance of system

valve alignments on a rolling 3 year basis. According to PSE&G, the Unit 2

penetration cooling regulators and the penetration cooling valves had last

been aligned by TRIS lineup in May of 1993. The operations staff does not

require routine monitoring of the penetration air regulator outlet pressure to

ensure they are operating properly, nor are there any routine PM tasks

conducted on the air regulators.

During a search of the corrective action data base the inspector found three

(3) corrective maintenance work orders (WOs) that had been written on

August 8, 1996 to correct problems .with the penetration cooler air regulating

valves for Units 1 & 2. Specifically, the normal and backup air regulator for

Unit 1 and the backup air regulator for Unit 2 were found to be maintaining

1.§ psig to the penetration coolers instead of the required 75 psig. The 75

psig setting requirement was included as part of the assumptions in the air

load calculations to ensure the proper amount of air flow to the penetration

coolers. After the inspector questioned the commonality of the three (3)

WOs, PSE&G personnel initiated a Condition Report to document the failures.

At the close of the inspection period, the WOs were still open. After

18

questioning by the inspector, the Unit 2 WO was changed from "post restart

required" to "restart required".

The inspector noted, that while the Action Request Process did not

specifically require the improper regulator settings to be identified as a

condition report, the fact that all three regulators were identified in the same

condition on the same day should have been questioned and result in the

issuance of a condition report. This missed opportunity to identify a

Condition Report issue represents a continued weakness in the corrective

action process.

c.

Conclusions

Based on the above observations, the inspector concluded that there are unresolved

questions associated with the penetration cooling system, including:

1.

The affects of the additional air consumption on the UFSAR and the CBD,

including the Integrated Air Load Management and the Station Air Load

calculations.

2.

The affects the additional air consumption has on plant operations and

maintenance activities.

3.

The adequacy of the operational configuration control of the penetration

cooling system, including throttle valve positions, air regulator status, and

system air flows.

4.

  • The material condition of the containment concrete surrounding the affected

penetration due to potential long term overheating as a result of measured air

flows lower than design (250 scfm versus 636.8 scfm) and/or pressure

regulators maintaining pressure less than design (15 psig vetsus 75 psig).

This inspectors will review resolution of this issue in the next inspection period. (IFI

50-272&311/96-17-02)

E1 .3

Steam Generator Replacement Project CSGRP)

a.

Scope (37001, 50001)

Inspections were performed by the Region-based SGRP Project Manager to obtain

an overview of current and planned work, related procedures, documentation,

quality inputs and progress of the Salem Unit 1 steam generator replacement project

(SGRP). The site inspection included observations of work in progress at the

replacement steam generator (RSG) staging area, welding preparations, lifting and

rigging oversight; work packages and procedures; identified problems and corrective

actions; independent review of the site SG haul path; discussions with the

responsible engineers and observation of conditions and activities inside the

containment building.

19

An offsite inspection was conducted of SGRP engineering a.t the Framatome office

in Lynchburg to review the engineering task scopes, calculation methods, results

and documentation to confirm that acceptable engineering practices were applied in

development of information for safety evaluations required by the 1 OCFR 50.59

process.

b.

Findings

By December 14, 1996, one original steam generator (OSG) had been shipped

offsite by barge, two were in the preparation area for shipping and the fourth was

outside the containment building prior to movement to the shipment preparation

area. A significant portion of the pre-installation work on the RSGs was complete.

The movement of the OSGs by Chem Nuclear and Bigge transporters on the

designated haul paths was done per the planning without incident. Preparation for

the shipment of the first OSG was observed to be well planned and executed.

Work in the RSG staging area and preparations for lifting in the containment building

were observed to be generally proceeding in an orderly manner with appropriate

supervision and work control packages.

However, *the licensee has identified several problems during the progress of the

SGRP and has initiated root cause analysis, developed corrective actions and

selectively stopped work. The more significant problems were not nuclear safety-

related, but included a failure to field verify the orientation of the OSG support feet

which delayed the down ending of the first OSG, welding of T1 steel with a vertical

up technique not shown in the welding procedure, limiting only craft workers to

signing the Work Package logs of one contractor and not fully following the

procedure (WCP-2) in storing coated weld electrode in a rod heating oven. The root

cause analysis determined that problems were mostly associated with first time

activities. Corrective and preventive actions emphasized additional independent

review of first time sequences, increased PSE&G specialty oversight, and improved

pre-job briefings.

Engineering

A major portion of the engineering evaluations to determine the effect of differences

between the OSGs (Model 51) and RSGs (Model Fl on Unit 1 plant performance are

being performed by the project contractor, Framatome (FTI), with parts of the work

being done by Westinghouse and PSE&G. Inspection of a sample of SGRP

engineering work recently completed at FTI was initiated to confirm that reasonable

inputs were being developed for the safety evaluations required under the 50.59

process.

The inspector reviewed the FTI method and extent of engineering for the SGRP in

the 50.59 area. The engineering and related licensing scope are discussed in the

SGRP Work Scope Description dated August 15, 1996, and the SGRP Conduct of

Operation Plan, PSBP 322391, dated September 13, 1996. Included in the

engineering work scope is a review of the FSAR Chapter 1 5 Safety Analysis and

other Safety Analysis where the steam generators are involved; SG performance

b.

20

calculations; deadweight, thermal, seismic and high energy line break loads and

structural stress analysis; review and update of the affected parts of the FSAR,

Technical specifications and SER's; and operator training support.

The engineering process includes a Salem Unit 1 set of Analysis Input Data, an

Analytical Input Summary for each engineering task, the specific calculation

packages and guidelines for preparation and processing of calculations. The

inspector reviewed these and portions of the calculations on Low Temperature Over

Pressure Protection, SG performance and SG structural supports.

Engineering evaluations and design changes associated with steam generator (SG)

replacement reviewed during this inspection were found to be done in conformance

with requirements in the facility license, the applicable codes and standards,

licen-~ir;g commitments, and the regulations. Some minor issues were identified.

These included a lack of clarity on identification of some data curves in calculation

51-1258559-00 for design transients and the Analysis Inputs Data not having been

compared against the findings of the PSE&G FSAR project applicable to steam

generators. The licensee acknowledged both issues and proposed to review these

for appropriate action.

Conclusions

Inspections were performed at the Salem site and at the contractor's engineering

office by the Region-based SGRP Project Man~ger to obtain an overview of current

and planned work, related procedures, documentation, quality inputs and progress

of the Salem Unit 1 steam generator replacement project (SGRP). The inspections

found a generally high level of project performance in the areas inspected and

identified no safety significant project deficiencies. However, problems were noted

with some first time evolutions at the site that indicate a potential deficiency in

planning, work control or full understanding of procedural requirements by those

performing work. The Salem SGRP management initiated corrective and preventive

actions to improve project performance.

In the area of engineering activity that provides input to the required 1 OCFR 50.59 *

safety evaluations within the FTI work scope, the calculation process was found to

be well organized, significant factors were considered and no items of regulatory

concern were identified.

E1 .4

Modifications to Control Room Ventilation

As a result of a concern about the implementation of the control room ventilation

modification, the Salem staff inspected 1 00 percent of the welds completed during

installation of modification 1 EC-3505. The staff identified a number of welds that

workers had not installed in accordance with the final modification drawings. In

addition, they found that workers had used uncontrolled drawings to install portions

of the modification. Salem managers took disciplinary action with the contractor,

and resolved the incorrect welds through analysis and removing and replacing

welds. In addition, the Salem staff inspected a sample of welds for other ventilation

21

system modifications completed during the outage, and found no additional

examples of incorrectly completed welds. The inspectors concluded that the Salem

staff responded appropriately to the concern.

E2

Engineering Support of Facilities and Equipment

E2.1

(Closed) Inspector Follow-up Item 50-311194-24-02: Auxiliary Feedwater Pump

Trip Evaluation

This issue pertains to two trips of the turbine driven auxiliary feedwater pump. The

operators determined that in each case, the trip latch was not properly engaged and

vibration on pump startup caused the trip valve to operate. The inspector

conducted .:a r.eyiew of the licensee's actions to address this issue. The inspector

found that Salem staff made changes to procedure S1 /S2.0P-SO.AF-0001 (0),

Auxiliary Feedwater System Operation, to provide clear instructions to set and

verify proper trip latch engagement. The inspector also verified by a review of

corrective action data base that there have been no recurrences of this failure mode.

This item is closed.

E2.2

NRC Restart Issue 11.42 - Auxiliary Feedwater (AFW) Performance and Reliability

(Update)

a. Inspection Scope

The inspector reviewed the closure package for this issue as well as related work

documents, design change packages, surveillance test results and the AFW

operating procedure. The inspector held discussions with system engineering

personnel and inquired about recent AFW performance and state of readiness .. The

inspector also reviewed the system readiness exception list and performed a field

walkdown of the AFW pump rooms.

  • b. Observations and Findings

From the review of the closure package, the inspector found that Salem staff

attributed most of the problems regarding AFW reliability to turbine driven pumps;

specifically, they were attributed to the turbine governor. The following factors

were identified as having caused failures of the turbine driven pumps:

Poor control of oil quality

Incorrect oil use

Governor valve stem corrosion

Governor internal *configuration incorrect

...

/

~

The inspector verified that corrective action had been taken to resolve each of those

problems. Salem has implemented a control oil sample program to ensure

satisfactory oil quality.

A minor modification has been made at the governor cooler

to ease governor removal and reduce the risk of water being introduced into the

22

governor during the removal process. A recurring maintenance task has been

initiated to periodically inspect the governor valve stem for' corrosion. Measures

have also been taken to control the governor control oil inventory and Salem

management has formally delegated responsibility to maintenance for administration

of the oil control program.

Salem staff attributed the governor internal configuration problem to parts being

installed which were not identical to those being replaced. The vendor had made

these replacements without PSE&G knowledge. (The issue of configuration control,

in general, is being addressed under NRC Restart Issue 111.2, Configuration Control.)

The corrective action for the turbine governor problem included sending the units

back to the vendor to have them inspected and, if required, rebuilt to assure their

configuration was in accordance with the Salem design specification. The inspector

verified by field inspectiQn and document review that the units had been returned to

the Salem site and, for Unit 2, had been reinstalled.

The inspector obtained a copy of the "AFW System Unit 2, System Readiness

Review Final Affirmation," dated November 13, 1996. This document had been

approved by the system manager and identified approximately 60 incomplete items

most of which were tests to demonstrate acceptability of components which had

been repaired or modified. Examples include a manual trip of the turbine driven

pump to demonstrate operation of the trip and throttle valve, flow instrumentation

operational check, valve indication verification, check valve operational check, and

an evaluation of potential over pressurization damage to the actuator of valve

2MS132 (Isolation valve for steam to the turbine). The inspector determined that all

of the system readiness items were a restraint to entering Mode 3 or Mode 4.

c. Conclusions

The inspector concluded from his inspection that the actions taken by the licensee

to improve AFW performance and reliability should be effective. However, because

of the large number of outstanding items which remain to be tested, this Restart

Item will remain open until satisfactory AFW performance has been demonstrated.

E2.3

(Closed) LER 50-272/96-015: inadequate Containment Fan Coil Unit (CFCU) heat

removal capability due to bio-fouling. During the first quarter of 1993, the

individual CFCUs had been tested and noted to be performing at less than the

acceptance criteria. However, the combined effect of poor performance of three

units was not addressed. The total heat removal capability requirement is 250.8

million BTU/hr. In July 1996, an engineering review determined that the actual

capability during the first quarter of 1993 was 201.2 million BTU/hr for Salem Unit

1 and 209.6 million BTU/hr for Unit 2. The LER documented that there was no

safety consequences because under worst case accident scenarios, the containment

spray pump would be available to provide sufficient additional heat removal

capability .

E2.4

23

PSE&G has determined that one cause of the CFCU performance degradation was

bio-fouling as a result of the service water chlorination system being inoperable

between June 1991 to at least June 1993. PSE&G has also determined that lack of

organizational and management sensitivity to the maintenance and operation of the

chlorination system was also a cause of this event. Additionally, the absence of

controlled and accurate test acceptance criteria in the test procedure was a cause.

The inspector reviewed the corrective action identified for this event. The

corrective action includes implementation of a CFCU monitoring plan, procedure

revisions to emphasize the importance of maintaining the service water chlorination

system, and procedure revisions to ensure the chlorination system is in service prior

to placing the Service Water System in service. In addition, training was developed

to stress the importance of maintaining the service water chlorination system in

service. The inspector confirm.ad that the procedure revisions are complete, training

has been conducted, and the CFCU performance monitoring program is being

developed with an expected completion scheduled for December 1996.

The inadequate procedures constitute a violation of 10 CFR 50, Appendix B,

Criterion V, "Instructions, Procedures, and Drawings." The inadequate test

procedure constitutes a violation of 10 CFR 50, Appendix B, Criterion XI, "Test

Control". The failure to adequately maintain the service water chlorination system

constitutes a violation of 10 CFR 50, Appendix B, Criterion XVI, "Corrective

Action." In light of the fact that these problems are licensee-identified and

corrected and in recognition of the ongoing PSE&G efforts to address the generic

issues of management effectiveness, procedural shortcomings, and maintenance

problems as part of the Salem Unit 1 & 2 restart effort, these violations are being

treated as Non-Cited Violations, consistent with Section Vll.B.I of the NRC

Enforcement Policy.

(Closed) LER 50-272/96-012: potential loss of residual heat removal capability due

to inadequate valve design. The maintenance history for the residual heat removal

(RHR) flow control valves provided evidence that there have been seven

key/keyway failures since 1993. PSE&G engineering determined that the original

design provided little or no design margin. For reasons not known at the present

time, the original Westinghouse specification and data sheet did not specify any

flows or pressure drop across these valves.

PSE&G determined that these RHR valves wouJd need to be replaced prior to

entering Mode 6 for Salem Units 1 & 2. Also, a review was made to determine if

any other valves of the type installed at Salem had similar problems. That review

lead to the conclusion that adequate margin existed for other valves in use at Salem

and there was no record of the key/keyway failure mode for these valves.

The inspector verified that the Salem Unit 2 RHR flow control valves have been

replaced and a design change package is being prepared to replace those in Unit 1 .

The inadequate design is considered a violation of 10 CFR 50, Appendix B, "Design

Control." This violation is considered a Non-Cited Violation, consistent with Section

Vll.B.1 of the NRC Enforcement Policy.

- - -

-

24

IV. Plant Support

R1

Radiological Protection and Chemistry (RP&C) Controls

R1 .1

Exposure Goal/Status

The licensee's annual exposure goal for 1996 was 208. 745 person-rem and was

based, in part, on the restart of both Units 1 and 2. The goal however, did not

anticipate the Unit 1 steam generator replacement project. Not including the steam

generator replacement project, total Salem exposures for 1 996 through

December 12, 1996 was 202.408 person-rem. The steam generator replacement

project was originally estimated at 166. 733 person-rem with a project goal set at

158.253 person-rem. The SGRP estimata was revised on November 11, 1996, to

add an additional 31.529 person-rem resulting in a new project estimate of 198.262

person-rem. The reasons for the additional exposure included: additional detailed

planning was completed for the new steam generator structural support

modifications indicating significantly more work was required; the steam generator

downending ring required significant repair due to insufficient field verification prior

to fabrication; and overall project schedule delays have extended the SGRP an

additional 6 weeks. As of December 12, 1996, the SGRP had accrued 110.595

person-rem versus an estimated 178.444 person-rem to date. Total Salem Station

personnel exposures for 1996 through December 12, 1996 was 313 person-rem .

R1 .2

Radiological Work Controls

a. Inspection Scope

During inspection from 10/28 until 11 /4 of the Salem Unit 1 SGRP outage, the

inspector observed work control practices, interviewed workers and RP staff, and

reviewed licensee procedures. The inspector observed licensee postings, use of

contamination controls, and locked high radiation areas.

b. Observations and Findings

During the inspection period, all areas reviewed were properly posted,

contamination areas were controlled, and locked high radiation areas were found to

be locked as required.

Appropriate RP/worker interfaces were established during entry through the

temporary access facility (T AF) and upon entry to containment; and at the refueling

floor satellite RP control point and upon entry into the bioshield wall in the

basement of containment. The T AF provided dress out facilities, RWP sign-in,

cellular phone issue, and dosimetry issue. Once inside containment, cellular .phone

contact was made by each work party with the RP remote command center located

in the TAF. The TAF RP command center consisted of three remote monitoring

stations; one for the refueling floor, and one for each pair of steam generator

platforms. The RP monitoring stations consisted of remote video monitors of their

25

respective areas. During the inspection, approximately 9 different camera views

were simultaneously displayed at each RP monitoring station. The RP command

center RP technicians controlled the remote camera pan, tilt, and zoom functions

and could call the work parties and associated RP technicians in the areas of their

responsibility to provide additional RP oversight, and potential remote constant RP

coverage capability. During the inspection, no remote constant coverage use of the

RP command center was observed.

The licensee had identified four project tasks that would require continuous RP

coverage: pipe end decontamination, seal plate installation, pipe severance and

steam generator removal. The inspector questioned the positive control aspect of

the remote setup when audio communications relies on recognition of the worker

and dialing the applicable cellular phone number to establish contact to provide

direction to the workers. The inspector quest~~-':'ie,d the RP technicians ability.to

recognize the workers in containment (especially due to the uniform protective

clothing dress). The licensee resolved this concern by requiring each individual

carrying a cellular phone into containment to label the last two digits of the phone

number on their hard hat cover. This provided the visual reference needed during

remote surveillance to establish audio communications when necessary.

The inspector observed effective setup and controls associated with the clean area

side operations. The refueling floor inside containment consisted of a partial clean

area that extended out through the equipment hatch. The inspector noted that

appropriate contamination monitoring equipment and dedicated RP technician

resources were devoted to these clean areas to ensure personnel and radioactive

material control were maintained .. The clean areas mentioned and the "yard" areas

outside were effectively monitored and controlled during this inspection.

c. Conclusions

The inspector determined that the majority of the project work activities would be

conducted without the need to establish high radiation areas and associated

requirements. Sufficient RP technician resources were provided inside containment

to provide the surveying and radioactive material control aspects of the project.

The additional remote surveillance capability of the RP command center provided

another level of review of the work areas and was being considered for possible

applications involving remote surveillance of high exposure jobs. Also, the

containment clean areas and control of radioactive material outside of containment

were effectively monitored and controlled during this inspection. No discrepancies

or violations of any radiological work control requirements were identified.

R1 .3

Mockup Training

a. Inspection Scope

During inspection from 10/28 until 11 /4 the inspector observed mockup training for

installation of steam generator RCS seal plates and for RCS pipe end

26

decontamination. The inspector also interviewed applicable licensee personnel and

reviewed RP job guideline documentation.

b. Observations and Findings

Prior to removing the old steam generators, after severing the reactor coolant

piping, a steel plate is welded to the steam generator end of the reactor coolant

piping to provide a contamination boundary. Prior to performing this work

evolution, mockup training was performed. The mockup training involved 3-4

ALARA personnel, 3-4 pipefitters and 2 construction supervisors. The mockup

training session involved a good test of the planned work technique. The mockup

facility was full-scale as were the seal plate and welding *equipment. No protective

clothing or steam generator platforms were modeled and no communications

equipment were utilized as the actual work performance env.ironn:tent would entail.

Attendance was taken of the training participants for archival purposes only. The

inspector observed that no quality assurance personnel attended the seal plate

installation mockup training. Several days later, the RCS pipe end decontamination

mockup training was also performed. This training was conducted inside a

contaminated area inside the fuel handling building with appropriate RP, FTI,

ALARA, pipefitter, and quality assurance personnel in attendance.

c. Conclusions

An effective mockup training for installation of steam generator seal plates was

performed. Important sequencing of work details was established and an

understanding of the scope of work and radiological implications of the work were

effectively discussed and communicated to those present. The inspector noted that

important details of the work method that incorporated the radiological work

hazards were established during the mockup training.

Although the mockup

training was performed in street clothes and was unencumbered by protective

clothing, platform restrictions, and communication system usage, the inspector

determined that the most important aspects of the training were met. However, the

licensee had not established a requirement that only those in attendance of the

mockup training could perform the work. Task qualification controls had not been

established for the seal plate installation work. The lack of quality assurance

personnel in attendance was noted.

The licensee responded to this NRC identified weakness by delineating that the

responsibility for worker qualifications was with the work contractor (principally

Raytheon Nuclear Incorporated (RNI), and FTI). In response to this concern, RNI

included a worker qualification matrix into applicable work packages with a work

package step requiring review of personnel qualifications prior to commencement of

the mockup specific work. FTI had previously included their personnel* qualification

records in the applicable task deployment letter (work package) for review.

Approximately 12 local pipefitters' qualifications were not originally included in the

documentation packages. Late in the inspection, RNI and FTI mockup qualification

27

documentation records were completed and reviewed and verified by the inspector.

Later performance of pipe end decontamination mockup training incorporated these

enhancements.

R 1 .4 Pipe End Decontamination Controls

a. Scope (83750)

During inspection from 12/9 until 12/13, the inspector observed the setup,

implementation, and RP coverage controls associated with sponge-media blast

decontamination of RCS pipe ends of steam generator No. 12.

b. Observations and Findings

The inspector observed effective contamination controls and confirmation of

negative ventilation of the operating equipment before beginning the

decontamination work. The decontamination equipment was remotely operated

from a low dose rate area of containment by reference to closed circuit television

cameras inside the RCS pipe. Excellent air sampling was provided at several

locations on the steam generator platform and two CAMs were provided to allow

for the rapid detection of airborne radioactivity.

The inspector noted that the effectiveness of the pipe end decontamination dose

rates was monitored outside of the RCA in the temporary access facility RP

Command Center. A remote readout of dose rates was provided to the RP

technician providing oversight of the area. In order to understand decontamination

goals and hold points, the inspector asked the RP technician and an ALARA

radiological engineer where the dose rate detector was located and how the dose

rate information was used to determine when the decontamination operation was

completed. The inspector noted that such information was important in

understanding when decontamination was complete to the maximum extent

possible to avoid unnecessary personnel exposure. Both individuals did not know

where the dose rate detector was located and indicated that the vendor would

determine when the decontamination was completed. The inspector noted that the

dose rate detector configuration was accurately described in the applicable RP Job

Guideline that was available to the staff in the RP Command Center. In response to

this concern, the licensee implemented a read and sign order to ensure the

applicable RP technicians were knowledgeable of the decontamination monitoring

configuration. The inspector noted that the pipe end decon RP job guideline

provided only marginal guidance* on acceptance criterion for the decontamination

and also noted that the RP Job Guidelines were not station-approved procedures

and did not appear appropriate for control of work. The licensee responded by

modifying the pipe end decon work package to include an RP hold point before

completion of the decontamination work evolution .

28

c. Conclusions

RP surveying and monitoring of the pipe end decontamination operation were

effective and exposures were minimized. However, the control of decontamination

to maximize effectiveness was not well established. The licensee added an

appropriate RP holdpoint to the pipe end decontamination work package in response

to this concern.

R1 .5 * Internal Exposure Assessments

a. Scope (83750)

During inspection from 12/9 until 12/13, the inspector reviewed the investigational

whole body counts for 1996 and reviewed and verified calculations of internal

exposures recorded for 1996.

b. Observations and Findings

The inspector's review indicated that approximately 50 whole body counts (WBCs)

were performed during 1996 for investigational purposes as possible internal

exposures. Of these, 41 WBCs were determined to be below procedural action

levels. Several others represented low level contaminations that fell below

procedural action levels after a day later recount. Only two individuals indicated

detectable internal contamination. Both individuals were associated with steam

generator eddy current inspection work at Salem in June 1 996. One individual was

assessed a CEDE of 7 mrem as a result of the internal contamination. The 7 mrem

was below the 10 mrem level of recording. The other individual was assessed an

internal exposure of 32 mrem CEDE which was assigned to his personnel exposure

record.

The inspector reviewed the applicable bioassay measurement data and

independently performed an internal exposure assessment for the latter individual.

The inspector calculated 29 mrem CEDE, which agreed well with the licensee's

result.

c. Conclusions

There were few internal exposure incidents identified at the Salem and Hope Creek

Stations in 1996. One internal exposure of 32 mrem CEDE was recorded. This is

indicative of very good contamination controls at both Stations .

29

R2

Status of RP&C Facilities and Equipment

  • R2.1 *Unit 1 Radiological Conditions

a. Inspection Scope

During inspection from 10/28 until 11 /4 the inspector toured the principal

radiological work areas of Salem Unit 1 during the steam generator replacement

project. Independent survey measurements were made, licensee surveys and log

book documentation were reviewed in order to assess the radiological hazards

presented to the workforce.

b. Observations and Findings

The Unit 1 containment radiological conditions were determined as follows.

Refueling floor: general area dose rates were < 1 mR/hr in most areas with areas

over the reactor head on the cavity deck grating of 1-6 mR/hr. Inside the upper

biological shields surrounding each steam generator were dose rates from

1-20 mR/hr. The refueling floor contamination levels were maintained to

approximately 1,000 dpm/100 cm 2 (the station clean area limit). Log entries

indicated that some structural steel was contaminated from 6,000-20,000 dpm/100

cm2* The steel was wiped down controlled to maintain area contamination levels to

approximately 1,000 dpm/100 cm 2*

Basement floor, inside the bioshield area (with steam generators full): general area

dose rates of 1-15 mR/hr were found, with steam generator platform dose rates of

5-15 mR/hr and reactor coolant pump catwalk dose rates of 5-15 mR/hr. The

reactor coolant piping averaged 30 mR/hr contact. Contamination levels in the

lower levels of containment were maintained between 1,000 to 2,000 dpm/100

cm

2

, although log entries documented occasional occurrences of contamination

excursions up to 350,000 dprn/100 cm 2* These were promptly decontaminated and

maintained at the low contamination levels, previously stated. *

Although, the containment was posted as a high radiation area, the principal work

areas were less than 1 5 mR/hr and contamination levels were maintained at very

low levels.

Shielding

The licensee provided approximately 70,000 pounds of temporary lead shielding to

provide the excellent dose rate environment previously mentioned. *Areas that were

shielded included: reactor head, pressurizer surge line, regenerative heat exchanger,

pressurizer spray line, safety injection lines, residual heat removal piping,

intermediate RCS loops, steam generator platforms, reactor coolant pump platforms,

and pressurizer relief tank .

30

c. Conclusions

Contamination was maintained at near clean levels, and through the use of

temporary shielding and filling of steam generators, radiation levels of principal work

areas were maintained at low levels without significant dose rate gradients. The

inspector determined that excellent radiological conditions were established for

conducting the steam generator replacement project.

R2.2

Unit 2 Radiological Conditions

a. Scope (83750)

The inspector toured the principal radiological work areas of Salem Units 1 and 2

during extended outage conditions. Independent survey measurements were made

and licensee surveys were reviewed.

b. Observations and Findings

During inspection tours of the Unit 2 containment from 12/9 until 12/13, the

inspector noted a variety of protective clothing dress by workers in the same areas.

The variations ranged from only shoe covers and gloves; to lab coats, shoe covers

and gloves; to full protective clothing dress. The licensee indicated that during the

extended outage period, both containments had been decontaminated in many areas

to below the clean area contamination limit. Survey documentation of floor areas

confirmed the low contamination levels. Survey documentation of the walls and

low hanging interferences in these areas were not well documented, although the

licensee believed these surfaces were also decontaminated and represented a low

risk to the workers. The inspector performed gross masslin wipedowns of the

easily accessible wall surfaces and low hanging overhead surfaces to evaluate the

contamination hazards. None of the inspectors' gross contamination samples

indicated any detectable contamination, confirming the licensee's understanding

that resulted in the reduced protective clothing dress practices in containment.

During a tour of the Unit 2 Auxiliary Building, the inspector noticed a posted locked

high radiation area at the entrance to the No. 21 waste holdup tank (WHT) room.

Entry to the room is obtained by climbing a 6-foot vertical ladder over a weir wall

and then down another ladder into the room. Access_ was prevented by a ladder

lock which covered the rungs of the ladder and successfully prevented access by

way of the ladder. The inspector noted an adjoining mezzanine platform at the

same level as the top of the weir wall that could allow a worker to circumvent the

ladder lock and gain access to the room from the mezzanine. A current survey of

the room indicated a maximum dose rate of 700 mR/hr at 30 centimeters, which did

not meet the Technical Specification requirement for locking to prevent

unauthorized access. In addition, there was no indication that any unauthorized

entries had been made into the room. The licensee immediately locked a gate

preventing access to this area and was evaluating a means to prevent access to the

No. 21 WHT room from the adjoining mezzanine. No violations were identified in

this area.

  • '

31

c. Conclusions

R3

R3.1

a.

b.

c.

The inspector concluded that radiological controlled areas at the Salem Station were

properly posted. Further, locked high radiation areas were properly controlled.

However, a possible access path to the No. 21 WHT room was identified. The

licensee maintained contamination within the reactor containment to low levels.

This was a very good initiative.

RP&C Procedures and Documentation

RP Job Guidelines

Inspection Scope

During inspection from 10/28 until 11 /4 the inspector found that the licensee was

conducting the SGRP with very limited advance planning. The work package review

process was continuing during this inspection for work yet to be performed. It was

during this review that the ALARA and RP control requirements are specified in the

work package. In order to facilitate timely communication of expected RP job

performance during radiologically significant work evolutions, RP Job Guidelines

were often written for RP staff use before the work package was completed. The

inspector reviewed these documents to determine if adequate RP precautions and

considerations had been planned.

Observations and Findings

The RP job guidelines reviewed provided a good description of each job. The

guidelines included some RP setup requirements and specified some RP

requirements for surveying, monitoring, and air sampling. The RP job guidelines

provided clear definition of work steps that predicate changes of radiological

conditions. The inspector noted that there was no discussion of dosimetry

placement when working inside or in close proximity of open reactor coolant piping.

Also, no radiological contingency planning was built into the RP job guidelines.

Instead, there were occasional work control restrictions that caused work be

stopped for evaluation of conditions and controls.

During tours of the plant, the inspector noted that the RP job guidelines were only

available in the RP command center. RP technicians in the field were not provided

with this information. Later during the inspection, the licensee distributed the RP

job guidelines to all containment satellite RP *stations.

Conclusions

Although work packages were not all completed and detailed work requirements

were therefore not available for RP planning purposes, general work descriptions of

all radiologically significant work had been researched and individual RP job

guidelines for each had been developed to provide some advance RP planning and

32

to communicate a level of RP technician job performance expectation. These RP job

guidelines provided a moderately effective vehicle for orienting and guiding the RP

technicians in preparation for radiologically significant project work evolutions.

R3.2

Transportation Shipment of Old Steam Generator

a. Scope (86750)

On December 6, 1996, the inspector reviewed the licensee's shipping records and

preparations for shipment of the first Unit 1 steam generator to be shipped to the

Barnwell Low Level Radioactive Waste Disposal Facility. The shipment review was

made with respect to DOT regulations including specific DOT Exemption No. 11745

requirements.

b. Observations and Findings

In preparation for shipment, the licensee decontaminated Steam Generator No. 14

to below Station release limits. All exterior penetrations were sealed and the. RCS

pipe nozzles, in addition to being seal welded, had three-inch thick shield covers

welded in place. The generator was also painted. The lifting trunions were

defeated by welded gussets at each 90-degree location. The steam generator was

secured to a special flatbed trailer transporter that included steel plate shielding

around three sides covering approximately the lower 2/3 of the steam generator.

The inspector observed the licensee performing final survey measurements of the

shielded transport vehicle and the inspector performed independent dose rate

measurements. All contamination and dose rate measurements were within

regulatory requirements. The shipment was properly marked with the specific DOT

exemption number of the shipment as well as the shipping classification,

Radioactive-Surface Contaminated Object, and other required markings.

The inspector reviewed the shipping manifest (No.96-218) and noted that the

licensee accounted for the internal solid metal oxides residues and accounted for

any liquid remaining in the plugged steam generator tubes. All required information

was included and no discrepancies with regulatory requirements were identified.

c. Conclusions

The licensee properly prepared the No. 14 steam generator for shipment. Shipping

records were complete and met all regulatory requirements.

RS

Staff Training and Qualification in RP&C

a. Scope (83750)

During inspection from 12/9 until 12/13, the inspector reviewed applicable

procedures and lessons plans associated with contractor RP technician training and

qualification. The inspector also conducted interviews with the training staff.

.;

l

R6

33

b. Observations and Findings

The inspector determined that contractor senior RP technician candidates were

required to pass a generic RP technician screening examination within the past 3

years followed by station specific procedure training and testing. The contractor RP

technicians were also subjected to a practical evaluation performed by permanent

RP staff to complete the qualification process. The inspector reviewed the lesson

plan materials for the station specific procedure training and determined that they

were of good quality. The inspector also reviewed the station specific procedure

examination and noted that it had been upgraded since previously inspected.

c. Conclusions

The licensee maintained a good training and qualification program for contractor RP

technicians. No discrepancies were identified.

RP&C Organization and Administration

R6.1

Unit 1 SGRP Radiation Protection Organization

a .

b.

Inspection Scope

During inspection from 10/28 until 11 /4, the inspector reviewed the licensee's RP

staffing organization in support of the steam generator replacement project. The

review consisted of organization documentation review and observations of program

implementation during the project.

Observations and Findings

The original staffing plan called for 58 contractor senior RP Technicians and 24

contractor junior/decon RP technicians making use of 10 permanent station senior

RP technicians. The actual RP organization staffing utilized a total of 75 contractor

senior RP technicians and 24 contractor junior/decon RP technicians. An additional

7 radiological engineers were provided by RNI and FTI. The licensee utilized

existing PSE&G RP personnel in overall RP operations supervision capacities to

oversee all ALARA and RP operations functions. All major radiological work areas

were observed to be well staffed with cognizant RP staff.

c.

Conclusions

The inspector determined that the licensee met and exceeded the planned RP

staffing levels to support the steam generator replacement project. Through

observation, the inspector determined that very good RP staff resources were

available to provide the radiological survey and job coverage needs of the project .

-.

34

R6.2

Unit 2 Outage RP Organization

R7

a. Scope (83750)

During inspection from 12/9 until 12/13, the inspector reviewed the licensee's RP

outage organization responsible for support of Unit 2 restart outage activities and

Unit 1 steam generator replacement project activities. The review consisted of

review of organizational documents and observations of work area coverage during

the inspection.

b. Observations and Findings

The RP Department had increased the staffing of 36 permanent plant senior RP

technicians to include the contracted services of 86 senior RP technicians and 26

junior RP technicians. Approximately 30 contracted senior RP technicians were

utilized for radiological coverage of Unit 2 and the Unit 1 non-containment RCA

areas. The SGRP RP organization utilized the balance of the contracted RP

technicians to provide all Unit 1 containment RP support. Inspection tours of both

Unit 1 and 2 containments and Units 1 and 2 Auxiliary Buildings, the Solid

Radwaste Building and the "yard" RCA areas, indicated that all areas were

effectively monitored by radiological controls personnel.

c. Conclusions

Appropriate RP staffing levels were obtained and used to support the outage

activities of both Salem. Units 1 and 2.

Quality Assurance in RP&C Activities

R7. 1

QA Oversight of RP

a.

Inspection Scope

b.

During inspection from 1 0/28 until 11 /4, the inspector reviewed the resources

dedicated to providing oversight of the radiation protection program implementation

during the steam generator project. Applicable quality assurance documents were

reviewed and interviews with cognizant personnel were conducted.

Observations and Findings

The licensee provided a Quality Assurance (QA) steam generator replacement

project (SGRP) oversight plan, that provided for the identification of high risk events

and plans for assessing the adequacy of the contractor's QA controls over the high

risk planned activities. Four individuals were contracted by PSE&G for performing

this QA oversight work, each having had recent steam generator replacement

experience. Each major contractor (RNI, FTI) was required by contract to provide

their own QA monitoring and controls. The inspector noted that the SGRP did not

35

contract the RP function, that this function was supplied directly by PSE&G. No

additional QA oversight had been specifically planned to cover the RP area. One

PSE&G individual having normal responsibility for reviewing the RP and Chemistry

areas was involved due to normal job performance. Limited SGRP QA surveillance

observations had been documented by this individual during the project. Two days

of observations were documented during the project. These included observations

of RP command center remote monitoring of RCS pipe cutting of old steam

generator no. 12 and the review of one radiological occurrence report. No

discrepancies . .were recorded by the QA inspector. Also, a limited SGRP RP

preparation review was performed by an outside RP consultant, however the review

indicated that a comprehensive RP preparation audit should be conducted prior to

project commencement, which was not performed. The inspector questioned the

adequacy of QA oversight of the SGRP RP program. In response to this inspection

concern.**the licensee added a fifth member to the QA oversight group with specific

responsibility for radiation protection oversight.

c.

Conclusions

The inspector determined that the licensee had not dedicated specific QA oversight

review of the RP program performance during the SGRP and only routine QA

surveillance activities were being provided. In response to this finding, the licensee

obtained an additional member of the SGRP QA oversight group tasked with specific

responsibility for radiation protection oversight.

R7.2

Radiological Occurrence Reports (RORs)

. a. Scope (83750)

During inspection from 12/9 until 12/13, the inspector reviewed the licensee's

program for identifying, investigating, and correcting radiological occurrences at

Salem Station. The inspector reviewed selected RORs for 1996 to assess the

licensee's performance in this area. The inspector also conducted interviews with

applicable RP staff.

b. Observations and Findings

During 1996, the licensee recorded 154 level 1 RORs, 40 level 2 RORs, and 8 level

3 RORs (level 1 ROR indicates least significant and level 3 ROR the most

significant). The inspector observed that the level 1 RORs were predominantly

personnel contaminations. The inspector reviewed in detail selected level 3 and

  • 1evel 2 RORs. Based on this review, the inspector noted that most of the

radiological occurrences were of low exposure consequence and that there was a

good low threshold for reporting radiological incidents. Also, the investigations of

the level 2 and 3 RORs were thorough and detailed. However, corrective action

resolution of the level 2 and 3 RORs frequently did not address all of the issues

identified in the investigations and the corrective actions were often limited to

counseling of the involved individual and informing the staff. The following two

examples are provided for illustration.

.J

36

ROR No.96-123 was written in response to a series of work control errors

associated with a valve repair that took place inside the unit 2 regenerative heat

exchanger room. The ROR identified that l&C technicians had entered the room to

perform work and were stopped due to a system tagging conflict. Mechanical

maintenance made several unnecessary entries into the room due to a failure to

drain the piping system, failure to bring valve parts, and rework of the valve repair

caused by failure to remove the old gasket before installing a replacement. The

ROR captured the various planning deficiencies. The one exception was the ALARA

prejob planning meeting that serves to ensure a radiologically significant job is

adequately prepared. In this case, an ALARA meeting was held and did not identify

the planning inadequacies prior to the start of the job. This was not captured by

the ROR. The *HOR assigned l&C and Mechanical Maintenance with corrective

action resolution. This consisted of holding departmental review meetings to

communicate this. incident tQ their respective staffs. The ROR corrective actions

were subsequently approved by the RPM. Planning and departmental interfaces

with operations and ALARA were not reviewed or evaluated to improve

maintenance practices.

ROR No.96-168 was written in response to a worker entering a high radiation area

(Unit 1 containment bioshield) without being monitored by a TLD (although his

exposure was monitored by EPD). The ROR investigation determined that when the

individual entered the security guardhouse, he was issued his security badge

without his TLD attached. The individual failed to notice the missing TLD and was

later admitted inside the bioshield of Unit 1 containment by an RP technician and

allowed to work. The ROR identified that the security guard, the individual, and the

RP technician, were inattentive to the missing TLD and the ROR also identified that

the security badge clasp or snap that held the TLD badge to the security badge was

weak and had failed. The ROR corrective actions consisted of counseling the

individual on the applicable RP procedures and receiving disciplinary action from his

supervisor. Also, the incident was a topic of discussion during a safety meeting.

The inspector determined that the ROR had identified several failure mechanisms

but had only pursued one. The inspector noted that the individual was issued his

security badge improperly since the TLD was found in the applicable security badge

slot. The slots are too small for the security/TLD badge assembly which cause the

badges to be folded and twisted into the badge slots. Repeated cycling apparently

caused the snap to fail. This was not addressed in the ROR. Also, entry into the

containment bioshield area requires RP technician permission to gain access. Plant

policy allows dosimetry to be placed inside or outside of protective clothing and

when dosimetry is placed inside of protective clothing, RP technicians cannot verify

that workers are in compliance with requirements prior to allowing access to certain

high radiation areas. Review and evaluation of this plant practice was also not

reviewed in the ROR.

c. Conclusions

The inspector concluded that; radiological occurrences were of low exposure

consequence, that there was a good low threshold for reporting radiological

-.

RS

RB.1

37

incidents; and that the investigations of level 2 and 3 RORs were thorough.

Corrective action resolution of the level 2 and 3 RORs frequently did not address all

of the issues identified in the investigations and the corrective actions were often

. limited. Additional attention in this area was warranted.

Miscellaneous RP&C Issues

(Closed) Violation 50-311196-01.-05:

During late 1995, the licensee reported several instances of entering the RCA

without electronic dosimetry monitoring and other related access control procedure

violations. The repetitive nature of these procedure violations resulted in issuance

of a violation against 10 CFR 50 Appendix B, Criteria XVI, failure to provide

effective corrective actions to prevent recurrence.

The inspector determined that establishing the electronic locking turnstiles at the

RCA entrance provided substantial positive control over workers accessing the RCA

to ensure each worker's exposure is monitored by an electronic dosimeter. Two

software system modifications were made that served to enhance worker

performance during RCA entry procedures. This violation is closed.

RB.2

(Closed) Unresolved Item 50-272/96-12-04:

Since June 25, 1996, until early November 1996, the Salem Radiation Protection

Manager (RPM) was assigned to a temporary position in the Salem Unit 2 Outage

Management group. The RPM designated the Senior ALARA Supervisor as the

acting RPM in his absence. During the previous inspection, sufficient information

was not available to determine if the individual met the applicable regulatory

requirements, specifically 5 years of professional radiation protection experience.

During this inspection, the licensee provided a breakdown of RP supervisory

experience for the acting individual that, in aggregate, equated to 5.5 years of

professional experience. As a result, the subject individual was found to meet the

regulatory requirements for the RPM position. This item is closed.

RB.3

Updated Final Safety Analysis Report (UFSAR)

The inspector reviewed current Salem Station practices with respect to Section

12.1.5 of the UFSAR. This section describes the semi-annual leak checks, control

and storage of radioactive sources. The inspector verified the source- inventory and-

reviewed documentation indicating successful completion of the semi-annual leak

checks. All sources were controlled in locked storage cabinets with keys controlled

by RP or RP instrumentation personnel. The inspector determined that the UFSAR

wording was consistent with the observed plant practices and procedures.

38

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at the

conclusion of the inspection on December 24, 1996. The licensee acknowledged the

findings presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary. No proprietary information was identified .

Opened

50-272&311/96-17-01

50-272&311 /96-17-02

Closed

50-272/96-12-04

50-311194-24-02

50-311196-01-05

50-272&311/95-10-01

50-272&311/96-10-02

50-272&311/96-12-01

50-272&311 /96-24-03

50-272&311 /96-24-05

50-272/96-012

50-272/96-015

50-272/96-027

ITEMS OPENED, CLOSED, AND DISCUSSED

VIO

UNR

UNR

IFI

VIO

VIO

VIO

VIO

VIO

VIO

LER

LER

LER

failure to perform required safety analysis report

possible degradation of containment penetrations

radiation protection manager qualification

auxiliary feedwater pump trip evaluation

repetitive RCA access control procedure violations

failure to relatch EDG fuel rack

failure to report shutdown required by Technical

Specification

failure to take ad<:;(j-uate actions for'"a significant

condition adverse to quality to preclude repetition

missed heat balance

inadequate access control

potential loss of RHR capability due to inadequate valve

design

inadequate CFCU heat removal capability due to bio-

fouling

diesel watt meter inaccuracies not accounted for in

surveillance testing

!

...

AFW

A LARA

BAT

CFCU

CR

ECAC

EDG

FHV

FTI

NRC

PDR

PIR

PM

.PORV

PSE&G

QA

RCA

RCS

RHR

RNI

RP

RP&C

SA

SAC

SBO

SGRP

SI

SPAV

SRO

SRs

ST

TAF

TS

UFSAR

USO

LIST OF ACRONYMS USED

Auxiliary Feedwater

As Low As Is Reasonably Achievable

Boric Acid Transfer

Containment Fan Coil Unit

Condition Resolution

Emergency Control Air Compressor

Emergency Diesel Generator

Fuel Handling Ventilation

Framatome Technologies Incorporated

Nuclear Regulatory Commission

Public Document Room

Performance Improvement Request

Preventive Maintenance

Power Operated Relief Valve

Public Service Electric and Gas

Quality Assurance

Radiological Controlled Area

Reactor Coolant System

Residual Heat Removal

Raytheon Nuclear Incorporated

Radiation Protection

Radiological Protection and Chemistry

Station Air

Station Air Compressor

Station Blackout

Steam Generator Replacement Project

Safety Injection

Switchgear Penetration Area Ventilation

Senior Reactor Operator

Surveillance Requirements

Surveillance Testing

Temporary Access Facility

Technical Specification

Updated Final Safety Analysis Report

Unreviewed Safety Question