ML18101A839

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Insp Repts 50-272/95-12 & 50-311/95-12 on 950515-0608. Violations Noted.Major Areas Inspected:Review of Maint Procedures,Breaker Reliability & Corrective Actions
ML18101A839
Person / Time
Site: Salem  PSEG icon.png
Issue date: 07/18/1995
From: Ruland W, Scholl L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18101A837 List:
References
50-272-95-12, 50-311-95-12, NUDOCS 9507260112
Download: ML18101A839 (10)


See also: IR 05000272/1995012

Text

DOCKET/REPORT NOS:

LICENSEE:

FACILITY:

DATES:

INSPECTOR:

APPROVED BY:

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

50-272/95-12

50-3'11/95-12

Public Service Electric and Gas Company

Salem Nuclear Generating Station, Units 1 and 2

Hancocks Bridge, N.J.

May 15 - June 8, 1995

Larry choll, Reactor Engineer

Electrical Section

Division of Reactor Safety

~Ur.kl.IL

Electrical Section

Division of Reactor Safety

7//o/9S-

Date

7/q/rr

Date

Areas Inspected:

The areas examined during this inspection included a review

of the operation and maintenance of the 4.16 kV and 230/460 volt air circuit

breakers.

The itispection included a review of established maintenance

procedures, breaker reliability, corrective actions taken for breaker failures

and actions taken in response -to industry and NRC information.

The inspector also performed a review of active operability determinations for

Salem Units 1 and 2 to evaluate the quality of these determinations and to

ensure that the evaluations had an adequate bases to support the conclusion

that the safety components were operable.

Results:

Refer to Executive Summary

9507260112 950718

PDR

ADOCK 05000272

Q

PDR

EXECUTIVE SUMMARY

Circuit Breaker Inspection

The inspectors found that preventive maintenance programs and procedures have

been established for the 4.16 kV and 230/460 volt air circuit breakers.

A good training course has been established to train the electricians on the

operation and maintenance of the various types of circuit breakers.

The

training facility was found to be excellent.

The 4.16 kV circuit breaker reliability has been generally good.

However, the

230/460 volt ITE circuit breakers have experienced numerous failures due to

hardened and/or dirty grease in the operating mechanisms.

The failure of

circuit breakers to operate properly can result -in the loss of safety systems.

Also, the slow closing of a circuit breaker could increase safety system

response times and change emergency diesel generator loading sequences.

The

licensee is presently attempting to resolve this problem.

Since this

condition has been allowed to exist for several years, a violation has been

cited for the failure of the licensee to take corrective action to prevent

repetitive failures.

The licensee review and disposition of industry information regarding circuit

breaker problems was found to be good.

Operability Determinations

The inspectors found the operability determinations to be of a variable

quality.

In some cases, the documented bases for the operability conclusions

were not complete, and it was necessary for the inspectors to obtain

additional information to assess the operability determination conclusion.

In

several cases, actions necessary to monitor degraded conditions to ensure

continued operability were not clearly specified.

PSE&G issued a new

procedure for the performance of operability determinations on May 25, 1995.

Unresolved Item 50-272/95-80-01;50-311/95-80-0l (regarding the adequacy of

operability determinations) will remain open pending NRC review of future

operability determinations performed using the new procedure .

ii

DETAILS

1.0

SCOPE/BACKGROUND (NRC INSPECTION PROCEDURE 62705)

The purpose of this inspection was to review the operation and maintenance of

the circuit breakers utilized in the 230, 460, and 4160 volt electrical

systems.

The inspection included a review of breaker reliability, preventive

maintenance (PM) program and procedures, corrective actions taken for breaker

deficiencies and failures and actions taken in response to industry

information associated with circuit breakers.

The inspector also interviewed

members of the -plant technical and maintenance departments involved in

activities associated with the circuit breakers.

The types of circuit breakers used at the Salem Units 1 & 2 plants are General

Electric (GE) Magne-Blast for the 4.16 kV buses and primarily ITE K-Series

breakers for the 230 and 460 volt buses.

The emphasis of this review was to identify possible problems associated with

the circuit breakers that could result in a common mode failure of more than

one breaker.

2.0

PREVENTIVE MAINTENANCE PROGRAM AND PROCEDURES

Preventive Maintenance Program

A PM program has been established for all safety and nonsafety breakers and

the frequency for each of the breakers was based on a reliability centered

maintenance study.

Preventive maintenance is performed on all of the circuit

breakers on a minimum frequency of every five years. Certain circuit breakers

had preventive maintenance performed on a more frequent bases.

For example,

the containment fan coil unit breakers have preventive maintenance performed

every 18 months since they are operated more frequently than other breakers.

The breaker preventive maintenance is normally performed by PSE&G

electricians.

In addition to the preventive maintenance performed by PSE&G,

the 4 kV breakers are returned to the vendor (GE} every nine years to receive

a more comprehensive overhaul and refurbishment.

Maintenance Procedures

Maintenance procedures are in place to control work on each type of breaker

used at the Salem plants. The inspector reviewed portions of the procedures

and found that the vendor recommendations had been appropriately incorporated

into the procedures.

One procedural weakness that was identified was that the

circuit breaker lubrication recommendations were not clearly specified and

therefore the extent to which each breaker's moving parts were cleaned and

lubricated was left to the discretion of the particular electrician performing

the maintenance.

As discussed in Section 3.0 of this report, the lack of

proper lubrication has resulted in performance problems with the 230/460 volt

breakers .

2

Due to an unplanned Unit 1 outage, a planned PM activity on an ITE breaker was

canceled and the inspector did not have the opportunity to observe in-progress

circuit breaker maintenance.

The inspector interviewed two electricians and

found them to be very knowledgeable on the operation and maintenance of the

circuit breakers.

Training

The inspector toured the training facility and discussed the circuit breaker

training program with one of the electrical instructors. The inspector found

that a good training facility is utilized to provide thorough training on all

of the various circuit breakers utilized in the plant. The lesson plans are

detailed and a significant amount of time is dedicated to the circuit breaker

portion of the electrician training.

3.0

CIRCUIT BREAKER FAILURE HISTORY

4.16 kV Magne Blast Circuit Breakers

The 4.16 kV circuit breaker performance has been generally reliable and there

were no significant trends noted in a review of the breaker failure histories.

230/460 Volt ITE Circuit Breakers

A review of the failure histories for the ITE 230/460 volt breakers revealed

that numerous failures (failure of a breaker to close) were attributed to

hardened and/or dirty grease in the operating mechanism.

The licensee was

currently investigating a recent problem associated with a breaker failure

that was attributed* to hardened grease, but had not yet determined the root

cause or the corrective actions necessary to preclude repeat failures. The

inspector reviewed the problem with the circuit breaker lubrication in more

detail and determined the following:

The system engineer had reviewed the circuit breaker failure history and

found two similar failures in the recent data (approximately two years).

The inspector reviewed the failure reports for the past five years and

identified 13 cases where a safety-related circuit breaker failed to

close and the cause was attributed to hardened and/or dirty grease.

(The 13 included additional recent failures not yet added to the data

base reviewed by the system engineer.)

Plant operators, engineers, and maintenance personnel were aware of

instances where there was a delayed response to a breaker close signal.

One incident report stated that the delay could be as much as 30

seconds.

Corrective actions for the doc~mented breaker failures were to clean and

lubricate the particular circuit breaker, but the corrective actions did

not address generic implications .

3

The electricians that were interviewed were aware of the slow close

problem and had observed the slow close when doing as-found trip tests

of the breakers during the PM process. However, their experience was

that the breakers would always close and had not seen any breakers stay

open indefinitely.

The PM procedure had been revised in January 1992 to provide more

guidance as to what actions were specifically required to be performed

during a PM.

Previously, the procedure instructed the electrician to

inspect the breaker and perform cleaning and lubrication as necessary

but did not specify mandatory lubrication points.

A review of the current PM procedure showed that although there is more

specific guidance to the electricians, the specific roller that appears

to cause the slow and/or failure to close is not one of the specified

mandatory clean and lubrication points.

At the time of the inspection, the licensee had not performed any

documented safety assessment and/or operability determination to address

the implications of the breakers slow closing or failing to close.

An

operability evaluation was subsequently performed and addressed

considerations such as the effects of slow closure on system time

responses and emergency diesel generator load sequencing. Also, actions

were taken to ensure all circuit breakers were recently operated with

satisfactory results.

There did not appear to be a clear correlation between the timing of the

circuit breaker failures relative to when the breaker PM was last

performed or to whether or not it was last performed using the new

procedure.

The inspector found that the electrical systems engineer was developing a plan

to resolve the problem with the hardened grease and associated circuit breaker

failures. Actions included in this plan were:

Two tubes of the grease (Anderol 757) used to lubricate the breakers

were sent to the manufacturer for analyses.

One tube was from the

storeroom and the other was one that had been in use by the maintenance

department.

A sample of grease from an inservice circuit breaker will be sent to the

vendor for analysis.

The circuit breaker vendor (ABB) will be requested to review/observe the

PSE&G maintenance practices to assess their adequacy.

Circuit breaker operating times will be checked before and after

maintenance to evaluate the effectiveness of the preventive and/or

corrective maintenance .

4

The system engineer was also in the process of reviewing an incident report

developed by the operations department that documents numerous failures of the

circuit breakers for the primary water pumps.

During this review, the system

engineer found that a significant number (approximately 40%) of the

maint~nance work orders listed the cause of the failure as "unknown".

The

system engineer issued Engineering Memo #95-150 to the operations engineers to

ensure that the plant operators were aware of the hardened grease problem and

to request that the operators initiate actions to troubleshoot breaker

problems before any actions are taken that may disturb the conditions at the

time of malfunction.

For example, breakers should not be racked out of the

operate position before as-found data is documented and any possible

troubleshooting has been performed.

Although the licensee is currently investigating the breaker failures caused

by hardened grease, the failure to identify the cause of the problem that has

existed for several years and the failure to take corrective actions to

prevent repetitive failures is a violation of 10 CFR 50, Appendix B, Criteria

XVI corrective action requirements.

(50-272/95-12-01; 50-311/95-12-01)

4.0

PSE&G REVIEW AND RESPONSE TO INDUSTRY INFORMATION

The inspector reviewed the actions taken by PSE&G in response to the following

NRC Information Notices (INs):

'

IN 84-29

IN 85-64

IN 89-29

IN 91-55

IN 94-02

General Electric Magne-Blast Circuit Breaker Problems

BBC Brown Boveri Low-Voltage K-Line Circuit Breakers with

Deficient Overcurrent Trip Devices

Potential Failure of ASEA Brown Boveri Circuit Breakers

During Seismic Event

Failures Caused By An Improperly Adjusted Test Link in 4.16

kV General Electric Switchgear

Inoperablity of General Electric Magne-Blast Breaker Because

of Misalignment of Close-Latch Spring

The inspector found that PSE&G had appropriately evaluated the above

information and had implemented hardware and/or procedure changes to address

the applicable issues.

5.0

WALKDOWN OF SWITCHGEAR AND MAINTENANCE AREA

The electrical equipment was found to be in good condition during a walkdown

of the switchgear areas. Housekeeping was very good in the switchgear areas

and th~re were not an excessive number of equipment trouble tags.

The

deficiencies identified on trouble tags were minor .

5

6.0

MANAGEMENT OVERSIGHT AND SELF-ASSESSMENT

Following the initial inspection activities and NRC identification of concerns

with the lack of timely resolution of the circuit breaker lubrication issue, a

quality assurance (QA) audit report was provided to the inspector that had

identified concerns with the failure of the containment fan coil unit (CFCU)

circuit breakers.

The QA audit identified that there were repeat failures of

the CFCU circuit breakers and that an adequate cause determination or actions

to prevent recurrence had not been established.

The report also noted that

the generic implications of the failure had not been addressed nor was there a

documented safety evaluation to assess the effects of a slow start during an

event.

The inspector found the QA audit findings to be excellent. However, the

maintenance department was allowed the routine time of 30 days to respond to

the findings.

The inspector concluded that a more timely safety assessment

would have been appropriate to ensure that the problems with the circuit

breakers did not affect the operability of safety equipment.

7.0

OPERABILITY DETERMINATION (OD) REVIEWS (NRC INSPECTION PROCEDURE 71707)

(UPDATE UNRESOLVED ITEM 50-272/95-80-01; 50-311/95-80-01)

During a special NRC team inspection conducted April 26 - May 12, 1995, the

inspectors identified nine examples where the station had been operated with

degraded equipment for which operability determinations had been prepared.

The technical bases for the operability determinations were found to be

deficient and inappropriately justified operability based upon equipment

redundancy, the lack of technical specification or Updated Final Safety

Analysis Report documentation, the lack of effect on the reactor protection

system, and fail safe positioning. Subsequent to the departure of the

inspection team from the site, PSE&G committed to completing a review of all

active ODs by May 19, 1995.

The results of the PSE&G review were forwarded to

the NRC during the week of May 22, 1995.

The inspectors reviewed the adequacy of the bases for the active ODs during

this inspection and found that the quality of the ODs was variable and in

several cases the inspectors required additional information to reach a

conclusion regarding equipment operability.

Some of the ODs clearly stated

what the safety functions of the components and systems were and others only

listed reference documents that described the safety functions.

The higher

quality ODs clearly listed the safety functions and then addressed the effects

of the degraded condition against each of the safety functions. Another

weakness was that the bases for operability did not clearly specify what

periodic inspections, measurements and/or tests were necessary* to ensure

continued operability. The inspector also noted that several of the ODs

provided addressed conditions that had already been resolved by component

replacement and as such were not active ODs.

')

6

Examples of these findings:

The OD associated with bolt failures on the emergency diesel generator

(EOG) fuel inlet block stated that "the risk of additional bolt failures

was low due to *the large number of bolts for all six engines and their

large number of operating hours".

The OD did not contain a discussion

on how the number of operating hours correlated to the observed bolt

failures. Data provided to the inspector indicated that the bolt

failures had occurred on the Unit 2 EDGs that had approximately 1300

operating hours while the Unit 1 EDGs had approximately 800 operating

hours. This data could suggest that the Unit 1 EDGs would experience

bolt failures when additional operating hours accumulate on the EDGs.

The documentation provided in the OD did not indicate that the root

cause of the failures had been identified and corrected.

During followup discussions with the system engineer and maintenance

personnel, the inspector obtained additional information regarding the

suspected cause of the bolt failures and corrective actions taken.

The

root cause of the failures was believed to be a deficiency in the

machining of the fuel pump inlet counterbore area. This deficiency

resulted in some of the mounting bolts bottoming out in the mounting

hole and caused insufficient bolting forces on one side of the fuel pump

inlet face. This condition caused higher forces to act on the other

bolt and resulted in fatigue failure of the bolt. Dimensional checks

have been made on the counterbore area and bolt holes to verify that all

bolts are fully seated during torquing and where necessary the bolt

holes have been tapped to provide full bolt seating.

Based on the

additional information provided, the inspector concluded that

operability concerns had been appropriately addressed.

The operability determination for a battery cell that had a portion of

scavenger post-seal lead broken loose from the positive post-seal did

not address the long term effects of the missing scavenging lead. The

purpose of the scavenger lead is to protect the current carrying lead

post from corrosion. The operability determination only addressed the

effects of the piece of lead having landed on the top of adjacent plate

separators. Since the affected cell was subsequently replaced, this was

not an active OD; however, this is an example of an OD that lacked a

thorough technical bases.

The OD for battery cells that experienced copper contamination did not

address the long term effects of this condition. The contamination may

have been the result of copper being displaced from the current carrying

insert in the battery post and the time dependent effects of this copper

displacement was not addressed.

The affected cells have been replaced

and therefore this is no longer an active OD.

However, it is an example

where the bases did not adequately address how long the condition could

exist without impacting operability or what inspections, measurements

and tests were necessary to ensure continued operability .

_!

v

7

The inspector noted that on May 24, 1995, Procedure SC.OP-DD.ZZ-OD02(Q) -

Revision O, "Operability Determination," was issued.

The purpose of this new

procedure is to provide guidance to the station personnel for conducting

operability determinations of structures, systems, and components and

documenting the results of the review.

Conclusions

The inspectors did not identify any examples where component operability could

not be justified, although process weaknesses were identified as discussed

above.

The effectiveness of the new procedure could not be assessed at this

time due to the recent issuance and lack of a significant number of

operability determinations that were performed under this procedure. This

unresolved item remains open pending additional NRC review of the adequacy of

operability determination performed utilizing the new procedure.

8.0

EXIT MEETING

Exit meetings were held on May 24 and June 8, 1995, with members of the

licensee's staff noted in Attachment 1.

The inspector discussed the scope and

findings of the inspection. The licensee had no disagreements with the

findings.

Proprietary information was reviewed during this inspection;

however, no proprietary information is contained in this inspection report.

Attachment:

Exit Meeting Attendees

-~

'

ATTACHMENT 1

EXIT MEETING ATTENDEES

MAY 24, 1995

Public Service Electric and Gas

R. Chranowski, Technical Department

B. O'Grady, Operations Department

L. Hayos, Nuclear Engineering Department

G. Madsen, Technical Department

R. Malone, Licensing Department

M. Morroni, Maintenance Department

D. Tauber, Quality Assurance Department

Atlantic Electric

M. Sesok, Site Representative

J. Janocha, Lead Engineer

Public Service Electric and Gas

C. Bersak, Staff Engineer

R. Brown, Strategic Planning

E. Harkness, Planning Department

JUNE 8, 1995

M. Metcalf Sr., Maintenance Department

P. Moeller, Licensing Department

J. Morrison, Corrective Actions

B. Preston, Engineering Department

J. Ranalli, Technical Department

P. Steinhauer, Technical Department

J. Summers, General Manager, Salem Operations

D. Tauber, Quality Assurance Department

Atlantic Electric

M. Sesok, Site R~presentative

PECO Energy

R. Kankus, Joint Owners Affairs

Delmarva Power

P. Duca, Site Representative