ML18101A778

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Monthly Operating Rept for May 1995 for Salem Unit 2.W/ 950614 Ltr
ML18101A778
Person / Time
Site: Salem PSEG icon.png
Issue date: 05/31/1995
From: Phillips R, Summers J
Public Service Enterprise Group
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
NUDOCS 9506200072
Download: ML18101A778 (7)


Text

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  • Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit June 14, 1995 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Attn.: Document Control Desk MONTHLY OPERATING REPORT SALEMNO. 2 DOCKET NO: 50-311 In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original copy of the monthly operating reports for the month of May are being sent to you.

John C. Summers General Manager -

Salem Operations RH:vls Enclosures C Mr. Thomas T. Martin Regional Administrator USNRC, Region I 631 Park Avenue King of Prussia, PA 19046 8-1-7.R4 9506200072 950531 PDR ADDCK 05000311 10~',

R PDR The power is in yow- hands.

95-2168 REV. 6/94

A~GE LEVE~

\ . DAILY UNIT POWER Docket No.: 50-311 Unit Name: Salem #2 Date: 05-10-95 Completed by: Robert Phillips Telephone: 339-2735 Month May 1995 Day Average Daily Power Level Day Average Daily Power Level (MWe-NET) (MWe-NET) 1 1085 17 1052 2 1105 18 1096 3 1065 19 1080 4 1069 20 1079 5 1083 21 1077 6 1083 22 1073 7 1018 23 1062 8 908 24 1067 9 812 25 890 10 800 26 932 11 994 27 1061 12 995 28 1078 13 995 29 1078 14 1021 30 1060 15 1064 31 1077 16 1060 P. 8.1-7 Rl

.OPERATING DATA REPORT Docket No:

Date:

50-311 06/10/95 Completed by: Robert Phillips Telephone: 339-2735 Operating Status

1. Unit Name Salem No. 2 Notes
2. Reporting Period MAY 1995
3. Licensed Thermal Power (MWt) 3411
4. Nameplate Rating (Gross MWe) 1170
5. Design Electrical Rating (Net MWe) 1115
6. Maximum Dependable Capacity(Gross MWe) 1149
7. Maximum Dependable Capacity (Net MWe) 1106
8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason_ _~N~A~-----------------------
9. Power Level to Which Restricted, if any (Net MWe) N/A
10. Reasons for Restrictions, if any N A This Month Year to Date Cumulative
11. Hours in Reporting Period 744 3623 119496
12. No. of Hrs. Rx. was Critical 744 2301.40 77916.62
13. Reactor Reserve Shutdown Hrs. 0 0 0
14. Hours Generator On-Line 744 2094.63 75062.55
15. Unit Reserve Shutdown Hours 0 0 0
16. Gross Thermal Energy Generated (MWH) 2443756.8 6278371.2 187252155.4 Gross Elec. Energy Generated (MWH) 797460 2023910 78473918
18. Net Elec. Energy Gen. (MWH) 765246 1896381 74619925
19. Unit Service Factor 100 57.8 62.8
20. Unit Availability Factor 100 57.8 62.8
21. Unit Capacity Factor (using MDC Net) 93.0 47.3 56.5
22. Unit Capacity Factor
  • (using DER Net) 92.2 46.9 56.0
23. Unit Forced Outage Rate 0 25.4 21.9
24. Shutdowns scheduled over next 6 months (type, date and duration of each)

None.

25. If shutdown at end of Report Period, Estimated Date of Startup:

N A.

8-l-7.R2

UNIT SHUTDOWN AND POWER REDUCTIONS REPORT MONTH MAY 1995 DOCKET NO. 50-311 ..

UNIT NAME Salem #2 '

DATE 6-10-95 COMPLETED BY Robert Phil Li OS TELEPHONE 609-339-2735 w METHOD OF SHUTTING LICENSE DURATION DOWN EVENT SYSTEM COMPONENT CAUSE AND CORRECTIVE ACTION NO. DATE TYPE 1 (HOURS) REASON 2 REACTOR REPORT # CODE 4 CciDE 5 TO PREVENT RECURRENCE 2579 5-8-95 1 53.8 A 5 ----------- HF PUMPXX CIRCULATING WATER PUMPS 2647 5-26-95 1 26.7 A 5 ----------- HF PUMP XX CIRCULATING WATER PUMPS 1 2 3 4 5 F: Forced Reason Method: Exhibit G - Instructions Exhibit 1 - Same S: Scheduled A-Equipment Failure (explain) 1-Manual for Preparation of Data Source B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refuel ing 3-Automatic Scram Event Report CLER) File D-Requlatory Restriction 4-Continuation of (NUREG-0161)

E-Operator Training & License Examination Previous Outage F-Administrative 5-Load Reduction G-Operational Error (Explain) 9-0ther H-Other (Explain)

  • DOCKET NO:
  • 50-311 MONTH: MAY 1995 UNIT NAME: SALEM2 DATE: 06/10/95 COMPLETED BY: R.HELLER TELEPHONE: 609-339-5162 The following items were evaluated in accordance with the provisions of the Code of Federal Regulations 10CFR50.59. The Station Operations Review Committee has reviewed and concurs with these evaluations.
1. Design Change Packages (DCP) 2EC-3224, Pkg. 1 * "Reracking of Spent Fuel Pool for Increased Storage Capacity Rev. I - This DCP removes existing Exxon racks and replaces them with maximum density Holtec racks.

This revision to the DCP is being made to: I) incorporate lessons learned during the installation of Unit 1 reracking, and 2) incorporate existing Unit 2 MCRs. This revision involves neither .the addition, deletion or modification of any equipment designed to monitor or control plant systems or components. There is no reduction in the margin of safety as defined in the basis for any technical specification.

(SORC 95-053)

2. Temporary Modifications (T-Mods)95-034 "Temporary Leak Repair of23SC109" Rev. 0 - On 23 Circulating Water Traveling Screen B outlet header, a reinforced thermo setting resin pipe (RTRP) flanged spool piece is to be replaced on a temporary basis with a carbon steel flanged spool piece which will be coated for corrosion resistance. Fit, form and function will be identical to the original. All design parameters of the CW system are maintained and no new operating configurations are being introduced. There is no reduction in the margin of safety as defined in the basis for any technical specification.

(SORC 95-043)

,1 REFUELING INFORMATION

  • DOCKET NO:
  • 50-311 MONTH: MAY 1995 UNIT NAME: SALEM2 DATE: 06/10/95 COMPLETED BY: R.HELLER TELEPHONE: 609-339-5162 MONTH: MAY 1995
1. Refueling information has changed from last month: YES_NO X
2. Scheduled date for next refueling: April 6. 1996 Scheduled date for restart following refueling: June 5. 1996
3. a. Will Technical Specification changes or other license amendments be required?

YES~NO NOT DETERMINED TO DATE X

b. Has the reload fuel design been reviewed by the Station Operating Review Committee?

YES NO X If no, when is it scheduled? April 1996

5. Scheduled date(s) for submitting proposed licensing action: _ _ ____rN~/"-=-A.::;___ __
6. Important licensing considerations associated with refueling:
7. Number of Fuel Assemblies:
a. Incore 193
b. In Spent Fuel Storage 556
8. Present licensed spent fuel storage capacity: 1632 Future spent fuel storage capacity: 1632
9. Date of last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity: March2012 8-1-7.R4

SALEM GENERATING STATION MONTHLY OPERATING

SUMMARY

- UNIT 2 MAY 1995 SALEM UNIT NO. 2 The Unit began the period operating at 100% power and continued to operate at that level until 5/8 when load was reduced to 88% due to moisture separator reheater drain tank level control and circulator screen problems. Power was increased to 100% on 5/15 following the return of the circulator. The Unit continued operating at 100% power until 5/26, when load was reduced to 85%, due to two circulators being out of service to repair traveling screens. Power was increased to 100% on 5/27, and remained at 100%

throughout the rest of the period.