ML18101A611

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Insp Repts 50-272/95-03,50-311/95-03 & 50-354/95-02 on 950204-17.No Violations Noted.Major Areas Inspected:Review of Actions Taken in Response to Potential Loss of Automatic ESF Equipment Actuation Signal
ML18101A611
Person / Time
Site: Salem, Hope Creek  
Issue date: 03/24/1995
From: Calvert J, Rogge J, James Trapp
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18101A610 List:
References
50-272-95-03, 50-272-95-3, 50-311-95-03, 50-311-95-3, 50-354-95-02, 50-354-95-2, IEIN-95-010, IEIN-95-10, NUDOCS 9504030215
Download: ML18101A611 (19)


See also: IR 05000272/1995003

Text

  • .'

DOCKET/REPORT NOS:

LICENSEE:

FACILITIES:

DATES:

INSPECTORS:

APPROVED BY:

9504030215 950324

PDR

ADOCK 05000272

a

PDR

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

50-272/95-03

50-311/95-03

50-354/95-02

Public Service Electric and Gas Company

Salem Nuclear Generating Station,

Hope Creek Nuclear Generating Station, Units 1 and 2

Hancocks Bridge, N.J.

February 4-17, 1995

q~J1lti~4ff

J

Ca vert, Reactor Engineer

ectrical Section

ivision of Reactor Safety

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earn ea er

Division of Reactor Safety

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' Date

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- ' '

EXECUTIVE SUMMARY

The purpose of this inspection was divided into two separate activities.

One

activity was performed at the Salem Units 1 and 2, and the other performed at

the Hope Creek plant.

The first week of the inspection reviewed Salem's actions taken in response to

the potential loss of an automatic engineered safety features equipment

actuation signal and, the subsequent problems that occurred with the solid

state protection system (SSPS) power supplies when attempting to correct this

deficiency. The potential loss could occur as a result of a postulated main

steam line break or seismic event in the turbine building which could cause

electrical faults in some SSPS non-class lE input signals. The faults could

disable the power supplies in one or both of the SSPS trains. This could lead

to the loss of the ESF actuation signals.

(NRC Information Notice 95-10)

The second week of the inspection primarily focused on the Hope Creek

technical department, their program initiatives, implementation of the

temporary modification program, and performance in the resolution of technical

issues and problems.

The inspectors found that the Hope Creek technical department was adequately

staffed. Communications between the technical department and operations staff

were strong and effective. The experience level of the system engineers was

strong and the system engineers were knowledgeable of their assigned systems

and technical areas of expertise. The system engineering walkdown program was

a good initiative and was being effectively used to identify equipment

deficiencies. Technical department management was proactive in developing

initiatives, such as the system readiness and work around list to enhance

station performance.

The Hope Creek temporary modification program implementation was good.

Installed temporary modifications were installed in accordance with station

administrative procedures and safety evaluations were thorough.

The total

number of temporary modifications installed in safety-related systems was low.

The quality of Hope Creek root cause evaluations reviewed were inconsistent.

Some of the root cause evaluations reviewed were thorough, while others were

poorly documented and lacked technical rigor.

For example, a root cause

evaluation completed in 1993, regarding the failure of safety auxiliary

cooling system (SACS) room cooler valves, was narrowly focused and was

unsuccessful in preventing repeat valve failures.

The root cause evaluation

documentation provided for the most recent SACS valve failures was not

complete and root cause analysis (RCA) techniques required by procedures were

not rigorously used.

The management acceptance rate of root cause analyses

(RCA) done by the technical staff was low and management standards for RCA

were not clearly defined. Technical department management was aware of the

weaknesses in the RCAs, required for the corrective action program, and was in

the process of making significant changes to improve the program .

ii

The suitability of the Hope Creek reactor protection system {RPS) loads to

possible change in total harmonic distortion {THO) caused by the change in the

alternate supply transformer was not determined and is an unresolved item.

The licensee plans to measure the THO on the bus, while utilizing the

alternate supply, and will determine the suitability for the RPS loads.

{Unresolved Item 50-354/95-02-01)

The root causes for the Hope Creek plant trip caused by the faulty logic in

the overfill protection system of the digital feedwater control system were

well documented, reasonable, detailed, and valid.

The assessment of the performance associated with the Salem potential loss of

automatic ESF equipment actuation signal is given below.

1.

The E&PB engineering staff showed timely and appropriate defense of the

design basis by their research of the actual Salem design status when

information was given to them verbally by another utility. Management

acted promptly on the information presented to them by the engineers.*

This was an example of an appropriate safety-conscious decision process.

2.

Management involvement and direction was evident by the quick dispatch

of engineering specialists on a full 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> day coverage for

troubleshooting, analysis, and corrective action when the SSPS power

supply problems occurred.

3.

The troubleshooting work process was planned, controlled, and

documented.

The analysis of failures was accurate, detailed,

documented, and technically sound.

The Salem system engineers provided

accurate analysis in the operability determinations of the SSPS.

iii

DETAILS

1.0

PURPOSE AND SCOPE (IP 37550)

The purpose of this inspection was divided into two separate inspection

activities. The first week of the inspection reviewed Salem's actions taken

in response to the potential loss of an automatic engineered safety features

(ESF) actuation (NRC Information Notice 95-10) and the subsequent problems

that occurred with the solid state protection system (SSPS) when attempting to

correct this deficiency (NRC Information Notice 95-10, Supplement 1). The

second week of the inspection primarily focused on the Hope Creek technical

department, including their program initiatives, implementation of the

temporary modification program, and performance in resolution of technical

issues and problems.

The inspectors also reviewed two Hope Creek plant

modifications.

2.0

HOPE CREEK TECHNICAL DEPARTMENT

2.1

Organization and Responsibilities

The Hope Creek Technical Department organization is comprised of a technical

manager, 6 technical engineers (supervisory level engineers), 32 system

engineers (SEs), 4 reactor engineers, and an administrative and technical

support staff. The function of the technical department is to provide

technical support to station personnel through the system engineers who serve

as system experts. These activities include system performance evaluation,

procedure development and review, initiation of corrective actions, project

team members for modifications, development of temporary modifications, and

the performance of root cause analyses and safety evaluations. The SEs also

provide assistance to operations department on equipment and system

operability determinations. At the time of the inspection, the administrative

and the engineering positions were fully staffed with the exception of 3

system engineers positions in the balance of plant area.

The inspectors

concluded that the technical department is adequately staffed at this time.

The system engineers that were interviewed were cognizant of their assigned

responsibilities. All of the system engineers interviewed had extensive

nuclear experience, including many with previous experience with reactor

vendors or architectural engineering firms. Several system engineers were

observed in attendance at the plant morning status meetings where they

provided information regarding the system for which they were responsible.

Licensed operations personnel were cognizant of system engineer assigned

responsibilities. The operations personnel interviewed stated that the system

engineers provided strong support of plant operator issues and concerns.

System engineers were observed in the control room and in the plant when

issues such as LCO maintenance on their assigned systems was being performed.

Specifically, strong communication was observed between the reactor core

isolation cooling system engineer and operations personnel during RCIC

maintenance activities. The inspectors concluded that the system engineers

communications with other station personnel were strong and effective .

2

2.2

Techn;cal Department Programs

Three programs implemented by the system engineers were reviewed to assess the

quality. The programs reviewed were the system engineers walkdown program,

operations work-around elimination program, and the system readiness rev;ews.

The inspectors accompanied a system engineer on a routine monthly walkdown of

the system engineer's assigned systems.

The systems walked down were balance

of plant system located in the turbine building. The system engineer was very

knowledgeable of the system performance. Crit;cal system performance

parameters were recorded and the system engineer was cognizant of past

performance trends.

The system engineer frequently commun;cated with

operat;ons personnel during the walkdown to gather additional ;nformation

regarding system performance.

The walkdown program expectations are

documented in a technical department d;rective. Documented findings of other

system engineer walkdowns were reviewed and were found to provide good

feedback on system performance issues. The inspectors concluded that the

system engineering walkdown program was a good initiative and was being

effectively used to identify equipment deficiencies.

The Hope Creek Technical Department has recently developed a operations work-

around elimination program.

The program administration guidelines are

described in Station Directive SA-SD.ZZ-27.

The program is designed to

enhance the timeliness of resolution of issues that could complicate operator

response to plant transients that distract control room personnel from normal

duties. The plant operators are responsible to identify those deficiencies to

be included in the work-around program.

The issues are tracked using the

performance improvement request system (PIRS).

The technical department

engineers evaluate the work-arounds and initiate corrective actions. This

program was recently initiated and the effectiveness of the implementation of

the program was not reviewed.

However, the inspectors concluded that this

program is a positive effort by the technical department management to provide

enhanced support for operator concerns.

The Hope Creek technical department has recently developed a system readiness

review of important systems. A system readiness report includes several

important parameters including corrective maintenance work orders, incident

reports, temporary modifications, and engineering concerns.

The reports are

computer generated and provide a sound bases for establishing the readiness of

the system.

Five systems readiness reports have been generated.

The system

engineers and technical department management demonstrated a commitment to

completing the system readiness reports for other key systems.

The system walkdown program was being implemented in a quality manner.

The

work-around and system readiness programs were good initiates. The inspectors

concluded that the implementation of these initiatives demonstrated the

Technical Department management's strong commitment to enhancing department

performance .

3

3.0

TEMPORARY MODIFICATIONS

The temporary modification {TM) process was reviewed to verify that the

installed temporary modifications do not degrade the function of plant safety

systems.

The inspectors reviewed TM administrative controls, the detailed

design information, and conducted field observation of several installed TMs.

The engineering management attention to address long-standing design

deficiencies, temporarily resolved by installing TMs, was also reviewed.

The TMs are administratively controlled in accordance with administrative

procedure NC.NA-AP.ZZ-0013(Q) "Control of Temporary Modifications." The

procedures provided detailed instructions and designated the responsible

individuals for TM installation. Station Operations Review Committee (SORC)

review is required of all safety-related TMs prior to installation. The

administrative guidance provided for TM installation was detailed with a

particular strength noted in the design criteria specifications.

The inspectors reviewed the following temporary modifications:

1.

TM 94-039 "Disabling the EOC/RPT Al arm"

2.

TM 94-026 "MSIV Seal System Draining"

3.

TM 94-027 "Adjustment of Reset Point on IEG-FSL-2544D."

The inspectors verified that the temporary modifications reviewed were

installed in accordance with the installation instructions. The design of the

temporary modifications reviewed were technically sound and did not degrade

the function of plant safety systems.

The safety evaluations were thorough

and provided adequate bases to determine that the temporary modification did

not involve an unreviewed safety question. Control room drawings were revised

to indicate configuration changes as required by the administrative procedure.

The total number of installed TMs was 27.

The total number of TMs has

remained relatively constant over the past six months.

The majority of the

TMs were not installed on safety-related systems.-

The inspectors concluded

that the TM program implementation by the technical department was good.

4.0

ROOT CAUSE ANALYSES {RCA)

4.1

Incident Report Reviews

Incident reports (IRs) document degradation and anomalous responses of plant

systems and equipment.

They are used by the licensee to investigate and

resolve these and other types of problems.

Procedure NC.NA-AP.ZZ-0006(Q)

(NAP-6), "Incident Report/Reportable Event Program and Quality/Safety Concerns

Reporting System," specifies the requirements for IR initiation,

documentation, and resolution.

IR resolution requires the use of a predefined

root cause methodology.

Specifically, Step 5.2.2 of this procedure requires

the use of one type of root cause methodology, causal factor, and barrier

. .

4

analysis or change analysis for every IR.

The inspectors reviewed selected

open and closed IRs to assess the quality and effectiveness of the licensee's

root cause methodology for both in-process and completed IRs.

The findings

were identified as written below.

4.2

Diesel Room Cooler Safety Auxiliary Cooling System (SACS) Valves

Stick;ng Closed (IR 93-087)

The root cause evaluation conducted following the failure of two emergency

diesel generator (EOG) room cooler valves to open was reviewed to determine

the quality of the root cause determination. A description of this failure,

including the apparent cause and corrective actions were documented in

Licensee Event Report 93-006.

There are 32 SACS supply valves that provide isolation for EDG and emergency

core cooling system (ECCS) pump room coolers.

Each room is provided with two

redundant coolers from independent SACS loops.

The cooling water isolation

valves are Anchor/Darling flex wedge gate valves with Hiller pneumatic

actuators. The Anchor/Darling gate valves used are 3-inch, 4-inch and 6-inch

depending on the cooler design.

The Hiller pneumatic operators use air

pressure to close the valves and springs return the valves to the open

position. The valves are designed to fail open on a loss of air or electrical

power to the solenoid actuator valve.

The valves receive an automatic open

signal following a loss of coolant accident (LOCA) or high room temperature

signal. The valves are in the inservice test program and are stroke time

tested quarterly.

On S~ptember 6, 1993, an operator identified that the "D" EDG room cooler fan

was running, but the SACS valve (EGHV2398D) had failed to open as expected.

The valve was.mechanically agitated and it opened.

The operator then

attempted to open the redundant EDG room cooler SACS valve (EGHV2398H), which

also failed to open.

One SACS EDG room cooler valve in each EDG room was

failed open to assure adequate room cooling, and a RCA was initiated.

The RCA was documented in a memorandum from the system engineer to the

technical manager dated September 30, 1993.

The evaluation stated that a

search of the work order history indicated that 12 of the 32 SACS cooler

valves had failed since 1987, with 2 valves failing twice.

On average, one of

the 32 valves was disassembled every six months.

The failed valves were of

different sizes and were located in several different locations. The RCA

concluded that the gates were binding in the valve body.

The binding was due

to excessive thrust when closing the valves.

The excessive thrust was the

result of a 19~9 design change that replaced the original Crane asbestos valve

packing with Chesterton graphite packing. The Chesterton packing thrust

loading was less than that of the original packing and design packing load.

The reduction in packing load resulted in more thrust being imparted to the

valve stem and disc seating. The additional stem thrust caused the valve disc

to become wedged in the valve seat and the spring force was unable to overcome

the static friction to open the valve.

To reduce the stem thrust, the air

pressure to the Hiller actuator was reduced from 80 psig to 60 psig. This

reduced the closing thrust of the valve by approximately 25% (1000-1500 psig)

5

to compensate for the estimated reduction in packing load thrust (800 psig).

The valves were tested using a Fisher Controls (FlowScanner) to measure the

reduction in unseating thrust (450 psig) required following the reduction in

air pressure.

Changes were also made to the stroke time surveillance duration following the

valve failure. All the SACS cooler valves were stroked weekly. After the

reduction of actuator air pressure, 15 of the 32 valves were put back on the

quarterly surveillance schedule. This test schedule was continued, with no

valve failures, until April 1994 when the valves were placed back on the

quarterly surveillance schedule.

The use of diagnostic test equipment to validate assumptions and the failure

history search were positive attributes of the RCA following the valve

failure.

However, it's not apparent that the root cause techniques described

in NAP 6 were used.

The root cause evaluation information documented on NAP

6, Form NC.NA-AP.ZZ-0006-1,Section IV was not complete.

The failure to use

the RCA techniques narrowed the scope of the potential failure modes

evaluated.

For example, the valve packing issue, that was later identified as

a potential cause following the most recent valve failure in 1994, was not

thoroughly evaluated. The corrective actions implemented following the

completion of the RCA were not successful in preventing repeat valve failures.

4.3

SACS (Hiller) Valves Failed to Operate During OP-15.EG-0102Q (IR 94-185)

On October 22, 1994, two SACS supply valves to the "B" EDG (6-inch valve

1EGHV-2398F) and "D" residual heat removal room coolers (3-inch valve

EGHV-2290H) failed to open during the conduct of the routine quarterly

surveillance test.

The valves opened following mechanical agitation. The

valves were returned to a weekly stroke schedule until corrective actions

could be implemented.

The air pressure supplied to the actuators was checked

and found to be appropriate. A description of the valve failures was

documented in LER 94-017.

A review of the design adequacy of the valve actuators was conducted.

The

valve and actuator vendors assisted the licensee in making this determination.

Calculations were performed to determine the required thrust to unseat or seat

the valves using a disc friction coefficient of 0.5. The margin between

required and available thrust varied between a minimum of approximately 369

psig for the 3-inch valves to approximately 700 psig for the 4-inch and 6-inch

valves. It appears from these calculations that the currently installed

actuators are adequately sized.

A review of the valve packing configuration as a potential cause for the

failure was also conducted.

The original Crane valve packing was replaced

with Chesterton Graphfoil packing in 1988.

In most cases, the rings of Crane

packing were replaced one-for-one with the Chesterton packing.

However, the

control of the number of packing rings installed and the torque values used

6

for the packing gland were not well controlled. This resulted in a variety of

different packing/torque combinations used for the SACS valves. The current

industry practice for graphite packing is to use 4 or 5 packing rings. The

reduction in the number packing rings by half (10 to 5), could reduce the

calculated packing load by approximately 50%.

The RCA stated that industry experience indicates that graphite packing tends

to stick to the valve stem in valves that remain in stationary positions for

long periods of time. Sticking of the packing can substantially increase the

force required to unseat the valves. The sticking can be reduced by improving

the finish on the valve stem.

The root cause evaluation concluded that the valve packing was the most likely

cause of the failure. The corrective actions are to establish configuration

control of the valve packing and repack the valves with the standard 5 rings

of Chesterton packing.

The licensee's cognizant engineers stated that a

thorough inspection of each valve would be conducted to establish a baseline

condition of critical components.

While the corrective actions appear appropriate, the RCA evaluation conducted

for the failure of these valves was not thoroughly documented.

The RCA

consisted of several E-Mail letters that described a chronology of actions

taken to investigate the cause of the failure.

The results of testing and

physical inspection were frequently not included in the RCA documentation .

For example, the information on the number of packing rings and type of

packing removed from the failed valves was not included in the documentation.

Since the conclusion was that packing was the cause of the failure this

information was important to support this conclusion. It was not apparent

that the RCA techniques described in NAP 6 were used.

Nor was it apparent

that a detailed plan to evaluate the failures had been developed.

The

additional documentation to support the conclusion of the RCA was being added

to the RCA at the conclusion of this inspection.

4.4

80° Emergency Diesel Generator Room Cooler Supply Valve 1EGHV2398F

Failed to Stroke Open

On October 29, 1994, during the first weekly stroking of the SACS cooler

valves following the October 22, 1994 failures, one of the diesel room cooler

supply valves failed to open (1EGHV-2398H).

The operators proceeded to fail

the valve open pending an evaluation by engineering.

The investigation of the failure determined that the air pressure being

supplied to the actuator was 85 psig rather than the design pressure of 60

psig. The increase pressure was caused by a faulty air regulator. The

regulator was replaced and the valve was returned to service.

The documented root cause evaluation was not thorough.

The RCA techniques and

forms provided in NAP-6 to conduct the RCA were not used.

The root cause

evaluation documentation consisted of an E-Mail letter that was primarily a

chronology of events.

The cause for the air regulator failure was not

documented.

The fact that a similar valve failed one week earlier that had

the proper air pressure was not discussed.

In addition, prior to 1993 the

  • ..

7

SACS cooler valves air pressure was normally set in the 80 psig range, with

infrequent valve failures; therefore, it's not apparent that the additional

air pressure was the cause of this failure. Since the corrective action taken

in 1993 to reduce the air pressure to the actuators had not been completely

s~ccessful, it was not clear that the current reduction would correct this

problem.

The root cause evaluation did not evaluate packing loads or other

potential causes for this failure.

4.5

Conclusions

The RCAs reviewed regarding the failures of the SACS room cooler supply valves

were weak.

The inspectors requested that the licensee provide some recent

examples of thorough RCA.

The quality of the RCAs provided were excellent.

The inspectors concluded that the quality of the RCAs varied considerably and

the standards for RCA were not clearly defined.

The cognizant technical staff

stated that while the quality of RCA documentation was improving, the

rejection rate of RCA documentation was recently as high as 75%.

Based on the

three RCAs reviewed in detail, it did not appear that station supervisors

provided clear expectations or oversight of RCA completed by their staff. In

addition, the guidance provided in the administrative procedures did not.

clearly establish expectations and was often not followed.

The current

administrative procedures required the same level of RCA be performed for

every IR regardless of safety significance or failure history. This approach

appeared to overburden the capability of conducting quality RCA and did not

focus staff efforts on the more safety significant issues. The technical

department staff and management responsible for the RCA program were aware of

the weaknesses in this program.

Efforts were in progress to make significant

revisions to the program to improve the overall quality of RCA and corrective

action program.

5.0

PLANT MODIFICATIONS

5.1

Reactor Protection System (RPS) Alternate Power Supply Transformer

Replacement (Hope Creek 4EC-0032)

This modification involved the replacement of the RPS alternate power supply

transformers (1AX432, 1BX432) with ferroresonant voltage regulation

transformers.

The RPS alternate power supply is mainly used for maintenance

purposes.

The reason for the change was that the two series connected RPS electrical

protection assemblies (EPAs) were tripping on undervoltage when large pump

motors or combinations of motors were started. Each EPA contains a breaker

that is controlled by solid-state electronics. They provide protection for

the RPS loads against overvoltage, undervoltage, and underfrequency.

The design intent of the modification was to reduce the voltage dips caused by

the starting of the large motor loads on the input side of the transformers,

and hence any unnecessary trips caused by the EPA's .

. '

8

Rev;ew - Unresolved Item 50-354/95-02-01

The inspectors reviewed for:

(1) the performance changes in the voltage

regulation; and (2) the suitability of voltage waveform harmonic distortion

with EPA calibration and RPS loads.

The licensee performed tests to determine the voltage levels under conditions

of high and low input voltage under load conditions.

The inspectors reviewed

the test data for the starting of fan motors {lAVH-404 lBVH-105.)

The data

showed good voltage regulation, but the waveform was quite distorted.

The inspector asked what the total harmonic distortion (THO) specification was

for the RPS bus.

The licensee stated that there was no THO specification for

the RPS bus in the documentation on site, and would contact the NSSS vendor

for confirmation.

The vendor stated that the MG sets, which supply power to

the RPS buses, did specify an allowance for 5% THO in the purchase

specifications. The vendor added, however, that there was no design

requirement, for the Hope Creek plant, in the RPS design specifications as it

relates to the system, its components, or the power buses.

The licensee said that the THO on the RPS busses would be measured when plant

conditions permit.

The determination of the THO on the RPS buses when

connected to the alternate power supply and the suitability of the measured

THO value for the connected loads is an unresolved item.

The licensee plans

to measure the THO on the bus, while utilizing the alternate supply, and will

determine the suitability for the RPS loads.

{Unresolved Item

50-354/95-02-01)

The inspectors reviewed the design analysis for the calibration of the EPAs

when used with the distorted waveform.

The licensee had information from

another utility that had used ferroresonant transformers for this application.

The information was that the EPAs compute the average value of the rectified

waveform, not the root-mean-square (RMS) value of the waveform.

The

requirements for overvoltage and undervoltage protection for the RPS bus loads

are given in terms of RMS voltage for a sine wave, not the average value

voltage for a sine wave.

The licensee recognized that a different method of calibrating the EPAs had to

be implemented for the case using a harmonically distorted waveform.

They saw

from plant testing, during the design stages for the modification, that there

was no noticeable change in the shape of the ferroresonant transformer voltage

waveform throughout the load range of 0 to 70 amps.

They conducted tests to

determine the RMS value of the distorted wave at which the EPAs tripped. They

knew where the overvoltage and undervoltage setpoints were set for the RMS

sine wave case from calibration data.

The licensee then used a graphical method and mathematical spreadsheet formula

to determine the average and RMS value of the distorted wave.

The calculated

values correlated correctly with the test data. Then they calculated the

amplitude ratio of the distorted wave case to the sine wave case.

. .

9

The amplitude ratio was used to calculate and set the RMS sine wave

calibration of the EPAs for the distorted waveform case. This allowed the

licensee to use a standardized EPA calibration method, but account for the

distorted waveform case by setting the trip points to values determined by a

formula.

The inspectors reviewed the derivation of the amplitude factors and the

resulting overvoltage and undervoltage set points for the EPAs.

The graphical

method used in the derivation considered enough points of the waveform to be

valid. The design analysis was clear, showed reasons for the options chosen,

and was reasonable.

The inspectors walked down the installation of the ferroresonant transformers

in the MG set room and found the material condition excellent.

Conclusion

The modification appropriately considered the influence of harmonic distortion

on the calibration of the EPAs for the alternate RPS supply.

The engineering

design analysis of the waveforms for calibration standardization was

noteworthy.

The suitability of the RPS loads to possible change in total harmonic

distortion caused by the ferroresonant transformer was not determined and is

an unresolved item.

The licensee plans to measure the THO on the bus, while

utilizing the alternate supply, and will determine the suitability for the RPS

loads.

(Unresolved Item 50-354/95-02-01)

5.2

Overfill Protection System (OPS) Logic Correction (Hope Creek 4HE-163)

This modification was a result of an unexpected trip of the main turbine

generator with consequent reactor trip. This event occurred on

October 2, 1994.

The cause of the trip was traced to a design deficiency in

the digital feedwater control system (DFCS).

The design requirement was to require two series contacts for high reactor

vessel water level to cause a main turbine trip. The system was actually

configured such that the contacts were wired in parallel.

The reactor vessel water high water level for OPS is sensed in three channels,

which are separate from the feedwater level channels. These OPS channels are

combined to produce a normally energized two-out-of-three logic in two

separate trains.

Each train drives one contact. The train contacts should

have been connected in series to the energize-to-trip turbine trip relay. The

licensee believed that one of the train contacts was intermittent, but was

unable to confirm this with follow-up testing.

Review

The inspectors reviewed the modification package and verified that the wiring

diagrams actually showed the two sets of contacts in series.

10

The inspectors reviewed the licensee design review of the DFCS, dated

November 28, 1994. Three root causes were determined:

(1) the schematic was

not available during the development of the wiring diagrams, installation

instructions, or testing requirements, so that correctness could not be

determined; (2) the design process had many elements in parallel, so that the

flow from requirements to the schematic and to the wiring diagrams was

uncoordinated; and (3) the design outputs were not reviewed for correctness

with the design analysis.

The inspectors interviewed the design engineer and determined that the root

causes were valid. The design analysis was performed at the same time that

the wiring diagrams were being developed. The design engineer noted the

problem with the OPS output to the turbine trip circuit.

He verbally informed

the proper people of the necessity for a design change.

The proper action did

not take place, and the engineer was preoccupied with other issues, so he

forgot to follow up.

A very strong factor that negatively influenced the

design cycle was aggressive scheduling. This was typified by the fact that

some of the plant level power tests were not done as originally scheduled.

Conclusion

The licensee's review of the design process accurately depicted the factors

and actions that caused this small, readily understood, flawed design detail

to develop into a challenge of the plant safety systems.

The root causes were

well documented, reasonable, detailed, and valid.

6.0

QUALITY ASSURANCE (QA) AUDIT REPORTS

The inspectors reviewed two audit reports and one surveillance report

conducted by the licensee's QA organization. The reports were assessments of

Hope Creek technical department activities. The reports were reviewed by the

inspectors to assess the quality of the independent oversight provided by the

QA organization.

The two QA audit reports reviewed were 94-133, "Technical Support Nuclear

Department,

11 and 94-133-3, "Reactor Engineering & Nuclear Fuel Design.

11

A

Quality Assurance surveillance 94-0315, "Control of Temporary Modifications,

11

was* also reviewed.

The inspectors concluded that the QA oversight of the technical department was

good.

This conclusion was based on the scope and number of recent audits and

surveillances conducted of technical department activities. However, the

inspectors observed that the summary section of the audit reports described

specific technical issues and did not provide an overall assessment of the

issues or the activities of organization audited.

An overall assessment as to

the quality of the activities or organization reviewed would be useful to

assist plant management in assessing performance .

11

7.0

POTENTIAL FOR LOSS OF AUTOMATIC ENGINEERED SAFETY EQUIPMENT ACTUATION

SIGNAL

The licensee was alerted to a potential loss of automatic engineered safety

(ESF) equipment actuation signal under certain circumstances by a phone call

from another utility that had a solid state protection system (SSPS) similar

to the Salem plants. The design engineers in Engineering and Plant Betterment

(E&PB) immediately researched the design basis drawings to see if a similar

problem did in fact exist at the Salem plants. They discovered that a

postulated seismic event or steam line break in the turbine building could

render both trains of SSPS inoperable or susceptible to a single failure.

Either one of the postulated design basis events could potentially lead to the

loss of ESF actuation signal because of certain wiring and fusing

configurations that existed.

The wiring for the non-Class IE turbine stop valve limit switch contacts, the

auto-stop oil relay contacts, and the reactor coolant pump (RCP) breaker open

contacts pass through termination boxes which are located in the turbine

building. The turbine building is a non-seismic structure and is susceptible

to the harsh environment that could be caused by a steam line break.

The scenario assumed a postulated failure that could cause a short to ground

of the non-Class IE wiring that would consequently cause loss of the 15 and 48

Vdc power supplies in one or both trains. The resulting impact could be

either a partial or total loss of the ESF actuation function of the SSPS, but

the reactor would trip.

NRC Information Notice 95-10 was issued to alert licensees to the to the

potential for loss of the ESF actuation function according to the above

scenarios.

The licensee reviewed the Hope Creek design basis (Letter ELE-95-0031,

February 3, 1995), and found that the plant did not have the same

vulnerability because the individual circuits were fused as well as interposed

with relays prior to going to the RPS trip circuits.

7.1

Solid-State Protection System (SSPS) Modification (lEC-3403, 2EC-3351)

The licensee developed a modification for the Salem SSPS to reconfigure the

input bay wiring such that the logic power supplies will not be affected by a

postulated short to ground of the input wiring that comes from contacts in the

turbine building.

The licensee declared both trains of the SSPS inoperable

for Salem 1 and 2.

They applied for and received NRC enforcement discretion

to implement the modification.

The new configuration moved the 120 Vac power feed for the logic power

supplies, which are individually fused, upstream of the existing 15 amp fuses.

This left the fuse in a position to provide the proper protection for the

input bay wiring.

In addition, the 15 amp fuses were replaced with 5 amp

fuses that coordinated properly with the upstream breaker.

' '

12

The licensee stated that they performed a modification pre~installation

rehearsal on identical equipment not housed in the plant. This allowed them

to refine the installation procedure without the risk of a plant trip.

SSPS Power Supply Failures

During the implementation of the design change that addressed isolation of

non-safety inputs from safety-related power, the licensee experienced some

SSPS power supply (PS) problems in Salem 1. The NRC enforcement discretion

was rescinded because the power supply problems changed the conditions under

which the discretion was granted.

The licensee shut down Salem 1 and 2 in

accordance with the Technical Specifications.

There are two independent power supply chassis for each train.

Each chassis

and contains one 15 Vdc section and one 48 Vdc section.

Each chassis has a

model number, which indicates the incorporation of certain vendor internal

power supply design changes.

Each section uses a switching regulation

technique and has overvoltage and overcurrent protection. The respective

sections from each power supply are diode coupled to form a single 15 Vdc

supply and a single 48 Vdc supply for each train.

The initial SSPS power supply problem was found during the power-down sequence

prior to actually starting the modification.

When the breaker for train A,

PSI 15 volt section, was manually tripped, the breaker for PS2 15 volt section

would trip.

In the course of troubleshooting this malfunction, the licensee

became aware of other anomalies in the power supplies and decided to bench

test all the SSPS power supplies for Salem 1 and 2.

The wiring and fuse

changes for the modification proceeded in parallel with the power supply bench

testing.

The four power supplies (three model 101, one model 100) for the SSPS of Salem

1 were removed, bench tested in the I&C shop, and did not meet specifications.

The four power supplies (two model 103, one model 101, one model 100) from

Salem 2 SSPS were tested and all but one (model 101) were acceptable.

The

three acceptable Salem 2 power supplies were then installed in Salem 1 SSPS.

One power supply (model 103), that was a spare from another utility, was also

bench tested and installed in Salem 1.

The SSPS for Unit 1 was then returned

to service, the post-modification testing was performed and passed.

One spare power supply from the warehouse (model 100) was bench tested,

installed in Salem 2, but failed, and was removed from service. Three spare

power supplies (all model 103) from other utilities, along with one spare

(model 103) from the PSE&G warehouse, were bench tested and installed in Salem

2.

The SSPS for Unit 2 was then returned to service and the post-modification

testing was performed and passed .

c

13

Rev;ew

The inspectors reviewed the design change package (DCP), "SSPS Interface to

Turbine Building," for wiring changes, fuse coo rd i nation, fuse commercial

dedication, fuse seismic qualification, and post-modification testing, and

found them adequate.

The post-modification test procedures for the SSPS were

based on the same as used in the plant functional test.

The inspectors determined by interviews that the output supply volta~es are

verified on a regular basis, but the output ripple voltage is not measured or

verified.

The inspectors audited the testing of the modification, the bench testing, and

the troubleshooting of the power supplies. The Salem plant manager requested

assistance from E&PB management, and engineering specialists were dispatched

around-the-clock to provide in-depth technical analysis for the

troubleshooting tasks. Plans were developed for the in-situ testing of the

supplies. Plans were developed for inspection and bench testing of the

removed power supplies. The power supplies were visually inspected and

cleaned.

The bench test covered overvoltage function, overcurrent function,

output ripple measurements, and output voltage regulation. Test data was

recorded and compared to vendor specifications for acceptance. Associated

system indications, consequent equipment conditions, and annunciators were

examined and probable causes documented by the Salem system engineers .

The original problem was found to be a single component failure in Salem 1,

train A, PS2 15Vdc section. A short in the regulator circuit was caused by a

wire being grounded to a heat sink, which most likely degraded the regulation

of the PS2 15 volt section. The presumed scenario was that when the redundant

supply was tripped, the increased load on PS2 caused overshoot of the output

due to degraded regulation, and the overvoltage protection circuit tripped the

supply.

The troubleshooting showed that several probable causes were responsible for

five of the original eight and one PSE&G spare power supplies specification

malfunctions. Table 1 shows the distribution of the malfunction categories.

The malfunctions can be categorized as random component failures stemming from

latent manufacturing defects and age degradation of electrolytic filter

capacitors.

No malfunctions were noted in the model 103 series power

supplies. The theory was that they were manufactured later than the other

series, had internal design changes incorporated, and had newer electrolytic

capacitors. The six supplies found out of specifications were in the I&C

shop, tagged as defective .

'

L

14

TABLE 1: NUMBER OF POWER SUPPLY MALFUNCTIONS BY TYPE AND MODEL

PERFORMANCE

Model 100

Model 101

Model 103

AREA & PS

SECTION

High Ripple

(note 1)

48 Vdc

1

2

15 Vdc

2

Regulation

48 Vdc

1

2 (note 2)

15 Vdc

1 (note 4)

2 {note 3)

TABLE 1 NOTES:

(1)

Suspect aged electrolytic capacitors.

(2)

One section, transistor shorted/overheating.

(3)

One section, wire was shorted to heat sink.

One section, suspect faulty electrolytic capacitors.

(4)

Unauthorized use of metallic standoffs caused regulator

failure by creating a shorting path. Spare from PSE&G

warehouse.

Through the visual inspection and troubleshooting tasks, the licensee

uncovered some design issues that were resolved as described below.

1.

The general warning alarm for the SSPS, that provides local and control

room warning, was discovered to not alarm if the power supply voltages

levels were degraded, but not completely lost. This meant that if a

supply failed and the redundant supply had an undetected failure of the

output regulation, then an alarm would not happen.

The vendor stated

that the general alarm was only designed to detect a complete loss of

voltage, not a degraded voltage condition. This could lead to failure

within a train, but the redundant train would be available, and the SSPS

would still meet the design basis. The licensee stated that they will

pursue a design change with the vendor to improve the detection

capability of the general warning alarm.

2.

The design problem discovered by another utility was confirmed. A

resistor in the overvoltage protection circuitry of the 48 Vdc section

of a supply was the incorrect wattage rating in the 100 and 101 models.

The resistor could dissipate up to twice the rated wattage.

If failure

3.

15

of the resistor occurred, the vendor stated that the overvoltage

setpoint could drift up to 10%.

For the one model 100 supply installed

in Salem 1, the licensee checked the resistor for proper value after

bench testing. The particular model 100 supply was previously installed

in Salem 2 SSPS since plant start-up, and the resistor had not failed or

caused output voltage problems.

The E&PB engineering staff has

recommended that the resistor be replaced at the next outage to the

value and wattage as recommended by the vendor.

The licensee noticed that the output breaker identification markings

were different in the supplies. The identification difference concerned

a time delay feature of the breakers. The licensee contacted the

vendors involved and the breaker suppliers to determine if the breakers

were identical. The review of the information indicated that the

breakers were all of the correct type.

At the end of the inspection, the licensee had not yet finished the formal

root cause analysis of the SSPS power supply failures.

The E&PB engineering

staff stated that preventive maintenance procedures to measure the output

voltage ripple, measure the output voltage regulation, and replace the

electrolytic filter capacitors on.some age-related basis would be examined.

7.2

Conclusions

The E&PB engineering staff showed appropriate defense of the design basis by

their research of the actual Salem design status when information was given to

them from another utility. The engineers received the information verbally

and acted in a timely manner.

Management acted promptly on the information

presented to them by the engineers. This was an example of an appropriate

safety-conscious decision process.

Management involvement and direction was evident by the quick dispatch of

engineering specialists on a full 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> day coverage for troubleshooting,

analysis, and corrective action when the SSPS power supply problems occurred.

The troubleshooting work process was planned, controlled, and documented.

The

analysis of failures was accurate, detailed, documented, and technically

sound.

The Salem system engineers provided accurate analysis in the

operability determinations of the SSPS.

The design issues were put in the perspecti~e of plant safety. There was

evidence of effective communication with the engineering vendors and suppliers

involved.

8.0

EXIT MEETING

An exit meeting was held on February 17, 1995, with members of the licensee's

staff noted in Attachment 1.

The inspectors discussed the scope and findings

of the inspection. The licensee had no disagreements with the findings.

The

inspectors received and reviewed proprietary material during the inspection

and used the material only for technical reference.

No part of the material

was knowingly disclosed in this inspection report.

I - *"

ATTACHMENT 1

EXIT MEETING ATTENDEES

Public Service Electric and Gas

P. Bernini, Principal Engineer - QA Programs

J. Benjamin, Director QA/NSR

M. Bursztein, Nuclear Electrical Engineering Manager

J. Clancy, Technical Manager - Hope Creek

J. Defebo, Hope Creek - Quality Assessment

W. Denardi, Sr. Projects Engineer

B. Diaz, Hope Creek Projects

G. Englert, Civil Structural and Programs Manager

S. La Bruna, Vice President Nuclear Engineering

C. Manges, Station Licensing Engineer - Hope Creek

C. Nentwig, Nuclear Engineer Design

J. Priest, Engineer Licensing and Regulation

D. Smith, Principal Engineer Nuclear Licensing

F. Thomson, Manager Licensing and Regulation

U. S. Nuclear Regulatory Commission

R. Summers, Senior Resident Inspector - Hope Creek