ML18095A486

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Insp Repts 50-272/90-20 & 50-311/90-20 on 900629-0815.One Noncited Violation Noted.Major Areas Inspected:Review of Circumstances Surrounding & Licensee Response to Reactor Trip on 900628
ML18095A486
Person / Time
Site: Salem  
Issue date: 08/29/1990
From: Swetland P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18095A484 List:
References
50-272-90-20, 50-311-90-20, NUDOCS 9009250150
Download: ML18095A486 (16)


See also: IR 05000272/1990020

Text

I*

Report No.

License

Licensee:

Facility:

Dates:

Inspector.s:

Approved:

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

50-272/90-20

50-311/90-20*

DPR-70

DPR-75

Public Service Electric and Gas Company

P. 0. Box 236

Hancocks Bridge, New Jersey 08038

Salem Nuclear Generating Station - Units 1 and 2

June 28 - August 15, 1990

Thomas P. Johnson, Senior Resident Inspector

Stephen M.

P~ndale, Resident Inspector

Stephen T. Barr, Resident Inspector

Harold I. Gregg, Senior Reactor Engineer

Reactor Projects Section 2A tt?<t:ta_,_90

~

Inspection Summary: Inspection 50-272/90-20; 311/90-20 on June 28 - August 15, 1990

Areas Inspected:

Special inspection to review the circumstances surrounding,

and the licensee response to, the reactor trip of June 28, 1990 and the sub-

sequent identification of deficiencies in the main steam isolation circuitry

and potential deficiencies in the main steam isolation valves.

Results:

The inspectors identified one non-cited deviation concerning the

failure of the main steam isolation circuit to meet all the requirements of

IEEE Standard 279-1971 as committed to in the Salem Updated Final Safety Analysis

Report.

The inspectors also identified weaknesses in the licensee 1 s initial

knowledge of MSIV performance characteristics, in the preventive maintenance of

the valves, in the licensee 1 s tolerance of degrading valve conditions, and in

the lack of proper review by the licensee of the first attempt at fixing the

circuit deficiency.

The inspectors noted that Salem system engineering responded

well in defining the MSIV problem and in developing maintenance and surveillance

techniques to correct those problems.

Additional strengths were exhibited by

licensee engineering and management in the conservative postulation, analysis

and solutions of the various problems encountered with the MSIVs and their

isolation circuitry.

PSE&G was recognized as being open and thorough in their

communications with the NRC concerning the MSIV problems and their resolutions.

TABLE OF CONTENTS

PAGE

  • 1.

Overview.............................................................

1

2.

Main Steam Isolation Valve Description and Operation.................

2

3.

Main Steam Isolation Valves (MSIVs) Circuit Design...................

3

4.

Regulatory Requirements..... . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

4

5.

Sequence of Events..................................... . . . . . . . . . . . . . .

4

6.

Licensee Activities and Corrective Actions...........................

5

7.

NRC Inspection Activities and Results ................................ 10

8.

NRC Conclusions ........................................................ 13

  • 9.

Exit Inte.rview ........................................ 1 ***************

14

..

1.

DETAILS

Overview

On June 28, 1990 at 12:32 a.m., Unit 2 automatically tripped from 75% power

following a loss of feedwater flow.

The event began with a failure of

non-vital 4kV/460V transformer No. 2F, which resulted in the loss of the

operating lubricating oil (LO) pump on each of the two operating steam

generator feed pumps (SGFPs).

The turbine governor controls for the No. 22

SGFP were also powered from the affected 460 volt bus.

The No. 21 SGFP backup LO pump automatically started following the loss of

the operating LO pump.

It did not, however, effectively restore LO system

pressure to prevent the automatic low LO pressure SGFP trip from occurring.

The No. 22 SGFP was also immediately lost, due to both the loss of the

operating LO pump and loss of turbine governor control.

The reactor auto-

matically tripped due to steam flow/feed flow mism~tch coincident with low

steam generator water level.

All three auxiliary feedwater (AFW) system

pumps, two motor driven and one turbine driven, automatically started fol~

lowing the trip as designed.

While responding to the reactor trip per emergency ope~ating procedures,

plant operators experienced one significant abnormality.

Approximately

eleven minutes following the trip, a control room operator attempted to

manually initiate a fast main steam line (MSL) isolati"on by depressing the

MSL isolation control panel pushbuttons in order to reduce the primary

system cooldown per emergency procedure direction.

Only two of the four

main steam isolation valves (MSIVs) indicated closed.

A slow MSIV closure

was then initiated, but no immediate results were noted.

About seven

minutes following the initial fast MSIV closure attempt, a second attempt

was made.

This time, the MSL isolation pushbuttons were maintained de-

pressed for several seconds and the control room console closed indications

lit for the remaining two MSIVs.

The unit was subsequently stabilized in

Mode 3 (Hot Standby).

Approximately 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> following the reactor trip, the licensee concluded

that two of the four MSIVs had not fully closed in response to the i~itial

manual MSL isolation attempt.

Followup investigation revealed an anomaly

within the MSIV circuitry by which, under specific conditions, both the

manual and automatic MSL isolation signals will not seal-in and thereby

not complete MSIV closure unless the signal (demand) remained until the

valves fully closed.

The licensee notified the NRC Operations Center of the reactor trip and

the subsequent findings in accordance with 10 CFR 50.72 reporting require-

ments .

2.

2

Main Steam Isolation Valve Description and Operation

Salem Units 1 and 2 each utilize four MSIVs manufactured by Hopkinsons

Limited of England (distributed in the U.S. by Atwood & Morrill).

The

valves are 27 inch parallel slide (double circular discs), reverse acting

gate valves, with two integral operating pistons and cylinders.

The bottom

of the gate holds the double circular discs and the gate has a 24-inch

diameter through-hole located above the discs.

When the gate is in the

full down position, the through-hole is aligned with inlet and outlet ports

and the valve is full open.

In this position, the bottom of the gate and

the double discs are in a lower body chamber below the valve through-port.

Closing the valve is accomplished by moving the gate to the full upward

position and the double circular discs are aligned with the i~let and outlet

ports, and through-flow is prevented.

The valve stem has a piston and cylinder arrangement within the valve bonnet;

system steam pressure above and below the piston balances the gate in its

full open and detent latched position, or in full closed and detent latched

position.

The detent mechanism of the valve is contained in a yoke assembly

attached to the valve stem. The yoke holds four spring and roller assemblies

that, wh~n the valve is in the full open or closed pos:it*ion, engage detents

in four lugs attached to the valve body (two lugs in the full closed posi-

tion and .two in the full open position). The force th~t the spring ex~rts

to keep the roller in the detent assists in keeping the* valve in the full

open or full closed position. The piston has a small equalizing orifice

and a small condensate drain pipe attachment.

During normal

operatio~,

the steam cylinder has equal steam pressure in each of the two chambers

because of the equalizing orifice.

Each MSIV has two air operated vent valves connected to the upper steam

chamber of the steam cylinder.

Vent valve position is controlled by a

solenoid valve, located in the air supply line to each valve.

The solenoid

valves allow air pressure to hold the vent valve in the closed position

unless an MSIV emergency fast closure signal is received.

Upon receipt of

an MSIV fast closure signal, steam evacuates from the upper chamber through

the two vent valves.

The resulting pressure inbalance provides the motive

power to move the piston and gate out of the detents and to the full upward

(valve closed) position.

The valves were required to fast close within

five seconds per Technical Specification requirements and design basis

assumptions.

An eight second closure time had been recently approved for

one operating cycle.

In order to improve MSIV closing times, the licensee

plans to implement a modification which would facilitate condensate drainage

from the top of the piston in the steam cylinder.

A hydraulic cylinder (utilizing hydraulic oil) and pump motor assembly

attached to the upper end of the stem is the only means to open the valve

and is an alternate means to close the valve.

It also acts as a hydraulic

snubber during fast closure.

The MSIV slow hydraulic stroke takes about

five minutes .

    • .

3.

3

The MSIVs are designed to provide protection in the following cases:

For a MSL break inside containment, the MSIVs serve to isolate reverse

flow to limit the containment building pressure rise.

For a MSL break outside containment, the MSIVs serve as isolation to

prevent the uncontrolled blowdown of more than one steam generator.

To minimize the positive reactivity effects of the reactor coolant

system associated with an excessive primary system cooldown.

The MSIVs receive an automatic fast closure signal from the MSL isolation

actuation circuitry, which is generated by either high-high containment

pressure, or high MSL flow coincident with either low-low Tave or low MSL

pressure.

The only other U.S. nuclear plant with Hopkinsons MSIVs is D.C. Cook.

Main Steam Isolation Valves (MSIVs) Circuit Design

The MSIVs are manually operated by various means.

They are individually

slow-closed or slow-opened from the control room panels (bezels).

Fast-

closure is accomplished via individual MSIV fast-close bezels or through

individual MSL isolation bezels.

There are two safety-grade trains associ-

ated with the MSL isolation function, consisting of four pushbuttons per

train (two per MSIV).

The MSL isolation circuitry closes the MSIVs, the

MSI.V bypass valves, and the main steam line. drain valves.

Only the MSIVs

are normally open during power operation.

The automatic MSIV closure occurs

as a result of an MSL automatic isolation signal.

The MSL isolation circuitry was such that an open limit switch permissive

was required to allow a short duration isolation signal to fully close the

valves.

That is, if an MSIV was not fully open (with its open limit switches

not satisfied), the valves would close in response to both a manual and

automatic isolation signal only as long as the signal was present.

The

MSIVs are required to close within five seconds.

Included in the five

seconds is a 1.5 second time delay to allow for a shuttle v~lve in the

hydraulic system to reposition prior to MSIV movement.

Only the manual

and automatic MSL isolation functions were affected by this anomaly. The

manually initiated individual MSIV fast-closure actuation function (from a

separate bezel) was not affected.

The result of this anomaly was that

MSIVs that did not have open limit switches satisfied would not have fully

closed in response to a momentary (manual) pushbutton MSL isolation or for

an automatic MSL isolation signal of short duration (less than five seconds).

At the time of the event, the Salem operators had not been trained in this

peculiarity of the isolation circuit and, consequently, were not aware

that the isolation pushbutton would have to be held depressed until the

valve was closed for any valve that was off its full open seat .

..

4

The licensee had preliminarily concluded that this circuit design may be a*

generic NSSS vendor (Westinghouse) design.* The licensee had been in com-

munication with the vendor since June 29, 1990, in order to evaluate the

design basis of the circuit. It was determined that the logic design and

requirements were developed by Westinghouse, but the circuit design de-

velopment was left to the individual plant's architect and engineering

firm, which in this case was PSE&G themselves.

4.

Regulatory Requirements

The Salem Updated Final Safety Analysis Report (UFSAR) Section 7.3.1.1.6,

"Main Steam Isolation", states that the automatic actuation system is de-

signed to meet the requirements for protective systems as described in

UFSAR Section 7.2.1.

UFSAR Section 7.2.1.3, "Principles of Design", states that the reactor

trip system is designed in accordance with IEEE Standard 279-1971, "Cri-

teria for Protective Systems for Nuclear Power Generating Stations".

IEEE Standard 279-1971, Section 4.16, "Completion of Protective Actio_n

Once It Ls Initiated, states that the protective system shall be so de-

signed that, once initiated, a protective action at th~ system level ~hall

go to completion.

Return to operation shall require s~bsequent delib~rate

operator action.

UFSAR Section 10.3.2.2, "Main Steam Stop Valves", states that the MSIVs

are capable of closure as long as main steam pressure is in 100 psig.

Salem Unit 1 and Unit 2 Technical Specifications 3.7.1.5, "Main Steam Line

Isolation Valves", require that each main steam line isolation valve shall

be operable while in Modes 1, 2 and 3.

5.

Sequence of Events

Prior to the reactor trip on June 28, 1990, Unit 2 was holding power at

approximately 75% for reactor physics data collection, and was in a power

ascension status following completion of its recent fifth refueling outage.

The trip occurred at 12:32 a.m.

During the response to the trip, emergency

procedures directed the plant operators to initiate a MSL isolation to

prevent an excessive cooldown (Tave was less than 530 degrees F).

Prior

to manually initiating the MSL isolation, the senior reactor operator (SRO)

noted that the open limit indicator as displayed on the control room con-

sole was not illuminated for two MSIVs (21MS167 and 24MS167).

The reactor operator (RO) subsequently initiated the MSL isolation (fast

closure) at about 12:43 a.m. by momentarily depressing the MSL isolation

Train A and Train B pushbuttons (four per train).

The operators observed

that a closed indication was received on only two MSIVs (22MS167 and

23MS167).

The position of the remaining two MSIVs was not known.

Neither

the open nor the closed limit indicators were lit for those valves, which

6.

5

is the expected indication when the MSIVs are not full open and not full

closed.

The RO then attempted a slow closure for 21MS167 and 24MS167 which

appeared to be functioning properly, however, the slow closure from fully

open to fully closed takes approximately five minutes.

At about 12:50

a.m., the SRO directed the RO to attempt a fast closure of the two MSIVs

from the same MSL isolation pushbuttons by maintaining the pushbuttons

depressed for several seconds.

This time, closure indication was received

on two separate console valve position indications.

At 12:50 a.m., seven

minutes following the first closure attempt, 21MS167 and 24MS167 valves

were closed.

Following the trip, Tave reached a value of 520 degrees F.

The primary

system cooldown was attributed to high AFW system flow rates, *the low decay

heat load associated with a reload core, and the roughly ten minutes it

typically takes to reach the procedural step which requires operators to

verify the value of primary system average temperature.

The unit was sub-

sequently stabilized in Mode 3 (Hot Standby), and the appropriate 10 CFR

50.72 notifications were made.

Licensee Activities and Corrective Actions

Following the reactor trip, the licensee performed a post-trip review, in

accordance with Administrative Directive No. 16,

11 Post Reactor Trip/Safety

Injection Review.

11

Also, in order to fulfill the PSE&G Nuclear Department

commitment to perform an independent review of each reactor trip, the Salem

General Manager convened a Significant Event Response Team (SERT), per

Nuclear Administrative Procedure NC.NA-AP.ZZ-0061(Q),

11Significant Event

Response Team Management.

11

The corrective actions recommended by the

post-trip review included resolution of the cause of the loss of the 2F

4kV/460V transformer, and of the problem with

11 closed

11 indication for the

21MS167 and 24MS167 valves.

The initial direction taken by the SERT also

centered around the 2F 4kV/460V transformer, along with the normal in-

dependent trip follow up.

On June 29, 1990, the licensee ~onfirmed that the 21MS167 and 24MS167 had

not fully closed following the reactor trip.

The licensee concluded that

only the manual circuit was affected.

A Station Operations Review Committee

(SORC) meeting was conducted on June 29, 1990.

During the meeting, it was

questioned whether the automatic MSL isolation logic was affected, however,

the presenter stated that the automatic circuit was not similarly affected.

The General Manager subsequently authorized the unit to escalate from Mode

3 to Mode 2 in order to perform the MSIV closure surveillance test to

verify the valve position indications and to conduct circuitry testing to

verify the manual MSL isolation design anomaly theory.

Prior to escalating

modes, the licensee participated in a telephone conference call with NRC

Headquarters and NRC Region I personnel to discuss the trip response and

the intended testing plan.

During the call, it was determined that a

11 spike 11 signal received in the automatic MSL isolation circuitry, with any

MSIVs off their full open limit, also would result in those affected valves

not fully closing. This caused the NRC to question the Salem commitment to

  • '

..

6

IEEE 279-1971, which requires that a protective system be so designed that,

once initiated, a protection actfon at the* system level shall go to com-

pletion.

With this concern raised about the manual and automatic MSL

isolation actuation logic, the licensee suspended their plans for Mode 2

testing and convened a team of engineers from the Engineering and Plant

Betterment (E&PB) Department to determine whether the MSL isolation circuit

was in compliance with IEEE 279-1971.

The engineering team concluded that

the MSL isolation circuit did not comply with the IEEE 279 requirement any

time an isolation was actuated with a MSIV off of its full open seat.

This condition exists any time a MSIV has drifted off its open seat during

normal plant operation, as had been the case on June 28, 1990 or any time

a MSIV is being opened from the closed position, as is the case during a

plant startup.

Once the concerns were raised in regard to MSIV full closure, the licensee

determined that Unit 1 was similarly affected and implemented compensatory

measures at that unit, which was operating at power.

Among these measures

were briefings of all oncoming operating crews to inform them of the pos-

sibi~ity of an MSIV not going fully closed under specific conditions and

developing an operating log to verify a.nd document that all MSIVs indica*ted

fully open.

Salem Unit 2 was taken to Mode 4 (Hot Shutdown) on June 30,

1990 in order to accomplish a system engineering inspe~tion and maintenance

plan for .the MSIVs, including the valve instrumentation and actuating: de-

vices.

The plant remained in Mode 4 while the E&PB engineering team con-

tacted Westinghouse and developed the necessary modification to the M'SL

isolation manual and automatic actuation logic.

The E&PB engineering team eventually determined that the cause of the

failure of the MSIVs to close was a defect in the MSL isolation logic.

The seal-in function that ensures that the valve goes fully closed was

µrecluded from functioning due to the reset loop in the circuit overriding

the operate loop in the manual and automatic actuation modes if the MSIV

was not initially fully open.

The licensee corrected the problem by re-

versing the position of the operate and reset coils in the isolation cir-

cuitry.

The modification ensured that the actuation signal is sealed in

and the MSIV will go full closed, even if the valve was not fully opened

at the initiation of the isolation signal.

The modification was approved

by a SORC meeting on July 3, 1990 and subsequently installed on July 4,

1990.

Continuity and logic functional tests were completed on the new

circuit on July 5, 1990, while the plant was in Mode 4.

These tests showed

the modification to be successful in closing the valve regardless of in-

itial MSIV position.

However, reversing the reset and operating coils was

found to prevent the automatic reset of the isolation circuit.

The circuit

not resetting prevented any subsequent reopening of the valve due to the

close signal remaining sealed in, which precluded any hydraulic operation

of the valves.

E&PB engineering proposed that this problem could be re-

solved by manually resetting the circuit subsequent to any manual or auto-

matic MSL isolation signal. This proposal was satisfactorily tested,

approved by SORC and implemented into all necessary procedures.

E&PB was

tasked to study the relevant circuitry and determine if a more suitable

7

long-term solution was available.

In addition, E&PB engineering stated

that an in-depth analysis of this and other similar logic circuits would

be undertaken in order to determine if any other undetected flaws might

exist. Subsequent to the circuit modification and procedure revision, the

licensee participated in a telephone conference call on July 6,1990, to

inform the NRC of their corrective actions and their intention to proceed

with a Unit 2 startup over that weekend.

During the forced outage, the licensee had measured and visually inspected

all Unit 2 detent mechanism positions.

These activities found the valves

out of the detent open position in varying amounts for three of the four

Unit 2 MSIVs (21MS167 out by 3/8 inch, 22MS167 out by 1/4 inch, and 24MS167

out by 3/4 inch).

Also, one detent had a damaged roller (21MS167) and one

detent was jammed open (24MS167).

Subsequent to finding the damaged roller

and detent mechanisms, the licensee mechanically locked open the four MSIVs

and removed all eight roller assemblies in order to examine their internals.

Two damaged assemblies were replaced, and the other six were regreased and

checked for the proper spring constant (

11 K

11 ).

After the roller assemblies

were reinstalled, the licensee checked and adjusted the limit switch ~osi

tions on each MSIV. The limit switches were adjusted to ensure the valve

hydraulic motor was run long enough to allow definite latching by the

rollers and detents, and to ensure positive indication of valve full open

and full closed position was received by the isolation circuitry and dis-

played in the control room .

A similar Unit 1 MSIV inspection was also conducted which found one valve

(14MS167) slightly off (1/4 inch) its open detent position.

The detents

were not removed and refurbished because the unit was at power.

The in-

spector was advised that the proper detent positioning was made on all

MSIVs and that specific maintenance instructions were being developed to

define the detent position requirements.

In order to maintain Unit 1 at power, the licensee conducted an evaluation

to justify the continued operation of Unit 1 without implementing the con-

trol circuitry modification.

The evaluation concluded that Unit 1 could

be safely operated due to the recent history of Unit 1 MSIVs not drifting off

their open seat and due to the adequacy of the compensatory measures taken

at the unit.

The evaluation also concluded that the logic circuitry should

be modified at the next Unit 1 outage in order to enhance the fault tolerance

of the circuitry should a valve drift off its open seat.

The justification

for continued operation was accepted by Salem management at a SORC meeting

on July 3, 1990.

During plant startup on the morning of July 9, 1990 in Mode 2, the MSIVs

were fast closure tested while in Mode 2 (Startup), and all the MSIVs closed

within Technical Specification time limits, and the new procedures were

correctly performed by the operating crews.

An additional problem was

identified, however, during the startup and MSIV fast closure testing.

During the fast closure testing of the MSIVs, the licensee stationed an

operator in the vicinity of the MS169 and MS171 MSIV vent valves to verify

.,

8

that steam exhausted from both vent valves when the MSIVs are fast closed.

The operator noted that steam continued to exhaust from the vents even

after the MSIV had gone closed.

Previously, the vent valves reclosed upon

MSIV closure, preventing any further steam release.

This abnormal condi-

tion was investigated by station engineering, and it was determined that

the vent valves staying open was another result of the logic circuit not

automatically resetting after the MSIV closed.

It was further determined

that the vent valves did close when the maintenance technician manually

reset the circuit per the new procedures.

This was the second time that

the recent circuit modification had produced a result that could have been

predicted but was not. Consequently, the licensee decided to return the

plant to Mode 4 while an engineering team was convened to fully analyze

the MSIV isolation circuit, the modification that had been made, all possible

consequences of the modification, and any new changes that might be required.

The engineering team conferred with the vendor, Westinghouse, and concluded

that, with certain procedure revisions, continued operation of Salem Unit

2 could be safely justified.

Plant management, however, was concerned with the additional actions now

requ~red of the plant operators to restore the MSIVs to normal following a

MSL isolation.

Of particular concern was the steam generator tube rupture

accident scenario.

With Unit 2 modified as it was, a radiological release

path would exist from the affected steam generator through its vent valves

until the circuit was manually reset and the vent valves could close.

The

licensee weighed this concern against the initial concern of an isolation

signal occurring with one or more of the MSIVs having drifted off its open

seat and the signal not lasting long enough to drive that valve fully shut.

Plant management concluded, on the basis that Unit 2 MSIVs had been mech-

anically reworked such that drifting should not be as frequent and that

any accident requiring MSIV closure would generate a signal long enough to

fully close any drifted valve, that the original circuit design of Unit 1

was more conservative than the modified circuit at Unit 2.

As a result of

this conclusion, the licensee decided to return the Unit 2 MSL isolation

circuitry to its original configuration and develop a justification for

continued operation (JCO) that would cover both Salem units.

Realizing

that the original circuit design still did not meet IEEE 279 requirements,

' E&PB engineering remained tasked to redesign the circuit so that it will

meet all IEEE 279 requirements while still maintaining the automatic fea-

tures of the present circuit.

On July 13,1990, the licensee presented the

proposed circuit resolution to SORC and subsequently to the NRC in a tele-

phone conference call involving Region I and NRR.

With SORC approval and

NRC concurrence, the licensee proceeded with a new design change package

(DCP) to remove the modifications made to the Unit 2 circuit and the pre-

paration of the required JCO.

On July 18,1990, the DCP that would remove the modification and restore

the previously installed Unit 2 isolation circuit to its original configu-

ration was presented to the SORC, who recommended approval.

During the

preparation of the 10 CFR 50.59 Safety Evaluation and the JCO, however, an

E&PB mechanical and electrical engineering review identified a new problem,

9

in which both the Unit 1 and Unit 2 MSIVs may not meet design basis closure

requirements.

The design basis for the MSIVs, as stated in FSAR Section

10.3.2.2, is that the valves will close within the Technical Specification

required fast closure times as long as main steam pressure is in excess of

100 psig.

While studying MSIV performance in order to justify plant opera-

tions with the original isolation circuit, the licensee preliminarily con-

cluded that a higher steam pressure (approximately 250 psig) is actually

required to ensure valve fast closure.

Postulated steam line break accidents

are assumed to reach pressures less than 250 psig before the MSIVs would

be fully closed.

Due to this determination, Unit 1 was shutdown on July 22, 1990 and reached

Mode 4 on July 23, 1990.

Both plants were maintained in Mode 4 while the

licensee further evaluated the preliminary conclusions and investigated

corrective actions.

On July 23, 1990, PSE&G participated in a telephone

conference call with NRC Headquarters and Region I personnel to inform

them of the current plant status and of the steps that were being taken to

resolve the MSIV problems.

For the next two and one half weeks, PSE&G mechanical engineering analy~ed

all steam line break models to determine the resultant steam line pressures.

At the same time, PSE&G worked with Hopkinsons and Atwood & Morrill to

determine more accurately the steam pressure required to close the *MSIVs.

On July 30, 1990 a ~onference call was conducted to inform the NRC of the

progress being made.

Within a week of that call, PSE&G determined that

the steam pressure required to initiate MSIV closure was approximately 100

psig and that all MSIVs would close for all main steam line breaks analyzed.

While the mechanical engineering group was analyzing actual valve perform-

ance, the Instrumentation & Controls engineering group developed a new

modification for the MSL isolation circuit.

The new modification involved

replacing the open limit switch* relay in the circuit reset loop with a

closed limit switch relay.

This change prevents a valve that has drifted

off of its open seat from initiating a circuit reset and preventing valve

closure.

The new change also provides a seal-in function in the circuit

because the reset loop now cannot be energized until the MSIV has gone

fully closed.

This modification was presented to a Salem SORC on July 31,

1990 and subsequently installed in both units.

With all modifications and analyses completed and approved by SORC, PSE&G

made a conference call to NRC Headquarters and Region I on August 10, 1990

to present their findings and conclusions on the MSIV issue and their plans

for plant restart.

Subsequently, the licensee made preparations for a

parallel startup of Units 1 and 2.

Plant heatup had already been started,

and both units were in Mode 3 by August 13, 1990.

Both units developed

problems apart from the MSIVs during power ascension.

Each unit

eventually reached Mode 2, and each unit's MSIVs performed satisfactorily

during the fast closure testing in that mode.

At the conclusion of the

10

inspection period, Salem Unit 2 was at power and operating satisfactorily,

and Unit 1 had returned to and was remaining in Mode 5 awaiting reactor

coolant pump motor replacement.

7.

NRC Inspection Activities and Results

The inspectors reviewed the applicable regulatory requirements and licensee

commitments, operator logs, post-trip review data and plant drawings.

Discussions were held with licensee technical, maintenance and operating

personnel involved with the events.

On June 29, 1990, the inspectors par-

ticipated in the telephone conference call held between NRC and licensee

personnel to discuss issues related to the events.

In addition, the in-

spector performed several walkdowns to observe the MSIVs and vent valves

located in the Unit 1 and Unit 2 penetration areas, and the vent valve

discharge piping located on the roof.

Following the reactor trip, the licensee pursued the MSIV problem, although

it had been characterized by personnel on the day shift as an indication

prob~em.

Information relative to the two MSIVs drifting off the open limit

switches was apparently not communicated to the appropriate day shift per-

sonnel.

As discussed previously, a control room operator observed that

the MSIVs that did not close after the trip had drifted off the full open

position immediately following the trip and prior to the MSL isolation.

A

separate incident report was written which reflected the observed.drift

conditions.

This report was apparently not reviewed by personnel reviewing

the trip response.

The lack of this knowledge resulted in the MSIV problem

being perceived to be an indication-only problem and therefore, not aggres-

sively pursued.

This lack of knowledge of the event details also apparently

delayed the involvement of the system engineers.

About 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> following

the trip, system engineering concluded that the valves had not fully closed,

utilizing information relative to valve position prior to the MS~ initiation

and by review of circuit drawings.

During the June 29 conference call, the inspector questioned the numerous

Unit 2 control room operator log entries relative to MSIV drifting and

manual reopening, however, licensee personnel involved in the conference

were unaware of the entries. The inspector identified that on June 24,

1990, 23MS167 and 24MS167 drifted off the open limit and was manually re-

opened by plant operators from the control room.

On June 25, 1990, 21MS167

drifted and was reopened.

MSIVs have historically drifted off their open seat, especially at Unit 2.

Position drifting had previously been attributed to vent valve leakage

problems.

Prior to the March 30, 1990 shutdown for the refueling outage,

two Unit 2 MS!Vs were drifting off their full open position, as observed

in the control room, roughly three times a day.

Excessive leakage was

then observed at the vent valves and roof vents.

After the June 25, 1990

startup from the outage (after all vent valves were repaired), all MSIVs

drifted at least once during the short time prior to the June 28, 1990

trip.

There have also been recent condensate buildup problems which have

11

resulied in a Technical Specification change to increase the allowed valve

closing stroke times.

The inspector found* that the recent valve drifts

were not communicated to the system engineer by operations, nor did the

system engineer become aware of the problems by independent log review.

This is an example of licensee personnel accepting potentially significant

off-normal conditions without further question because the problems had

. existed for a long period of time and had become an accepted discrepancy.

On June 29, 1990, the inspector observed the MSIVs and vent valves in the

outer penetration of Unit 1.

Unit 2 valves 22MS167 and 24MS167 were in

the closed position and the stem indicator pointers were on the shut scale

mark.

The detent posts were observed to be protruding through the stop

bar, but the detent could not be verified to be in the latched position.

Through discussions with the system engineers, latch position verification

is performed by observing that the detent post protrudes through the stop

bar, but no measurements or alignment to any mark was made or was required

by procedure.

The four vent valves associated with the MSIVs in the same area were ob-

served to be leaking, as ~videnced from the water discharge from the drilled

leak orifices in the vent pipe downstream of the valve5.

These valve~ had

just undergone an overhaul, and the inspector noted that leak testing; is

not a requirement for these va 1 ves fo 11 owing such an activity.* The i'n-

spector also expressed concerns that this type of valve may not be the

most leak tight, and its actuator force in the closed position may not be

large enough to limit the leakage to an acceptable amount (less than the

piston orifice flow).

Observations of the roof vents were also made and

there was no evidence of vapor from these valves.

Similar walkdown observations were made of the Unit 1 outer penetration

MSIVs and vent valves.

Again, the vent valve5 were observed to be leaking

and two of the roof vent pipes had substantial vapor flows.

The inspector questioned whether specific detailed procedures were his-

torically used to adjust the MSIV limit switches and/or detents.

The lic-

ensee stated that they had not used any procedure while setting the limit

switches/detents, and that those activities were assumed to be within the

knowledge of the technicians.

The inspector, however, expressed concern

that the MSIVs are unique valves, using several limit switches (two open,

two closed) which must be set and coordinated with detent position.

The

inspector found that detent position was not specifically considered during

limit switch adjustments.

The inspector also found that the detent mechanisms have not been maintained.

During an inspection of the Unit 2 detents, the licensee found that the

detent mechanisms' internal oil had burned off and allowed the internal

detent components to degrade.

The licensee subsequently determined that

the oil temperature rating was insufficient relative to the operating tem-

peratures in the MSIV penetration rooms.

Also, there were only two spare

.

'

12

detent mechanisms in stock (there are four detent mechanisms per MSIV).

The licensee also found detent mechanism iTiternal 0-rings to be brittle.

New 0-rings were not in stock, however, the licensee was able to procure

new replacement a-rings.

The inspector determined through discussions with the system engineers

that the MSIVs had never been disassembled.

Further, the detent mechanisms

had never been disassembled or maintained via a preventive maintenance

program.

The inspector found that the bottom of the lower body cavity was

removed on several valves in the early 1980 1 s to view the disc seats, but

no work was performed.

Also, one hydraulic actuator was removed from a

valve in the same time frame.

During the past outage, all Unit 2 vent

valves were overhauled.

The solenoid valves, check valves, and relief

valves on the hydraulic units were also rebuilt at the same time.

The

inspector noted that the vent valves have no leakage test requirements

following repair.

Also, there had been no surveillance or maintenance

process to verify the precise detent latch position location.

Based on observations of the valves and review of the assembly drawings,

the Hopkinsons MSIVs appear to be sturdy and well constructed valves.

Since the valves have never been disassembled, there i~ little knowledge

of the internal wear of the seats, the condition of the piston orifice and

drain tube, and other important internal parts.

The v~lves have unde~gone

numerous actuations due to trips and several surveillance fast-closure

strokes with generally favorable results, except for those related to; the

noted vent valve leakage and condensate problems that required the valve

closing times to be increased.

It was only subsequent to this event that the licensee in fact took many

of the above mentioned measures, such as a more precise setting of the

MSIV limit switches, int2rnal examination of the roller mechanisms, the

use of a temperature resistant grease in the rollers, and verification of

proper roller-detent alignment. The licensee also performed these measures

on the Unit 1 MSIVs during the Unit 1 outage, while the engineering analyses

were being performed. System engineering has been tasked with implementing

the preventive maintenance measures into station surveillance procedures

and making them recurring tasks in order to optimize future valve perform-

ance.

The inspectors monitored the development of the procedures and wit-

nessed the initial implementation of many of them during the restoration

of Units 1 and 2.

Coincident with the maintenance and evaluation of the MSIVs, system and

E&PB engineering pursued the resolution of the MSL isolation circuit de-

ficiencies.

The resident inspectors participated in the initial telephone

conference calls which raised the concerns about the MSL isolation circuit

and followed the licensee's first attempt at modifying the circuit.

An

8.

13

inspector was present during the July 9, 1990 startup attempt and witnessed

the plant operators' and system engineer 1 s recognition of the abnormal

event when the MS169 and MS171 vent valves remained open.

From this point

on the resolution of the MSIV problem centered on PSE&G and vendor engi-

neering analysis of valve performance, circuit design and potential accident

scenarios.

The resident inspectors closely monitored the licensee 1s pro-

gress in arriving at the eventual solution to the MSIV and associated cir-

cuit problems, and at least one inspector was present at every NRC con-

ference call and Salem SORC meeting previously noted in Section 6.0 above.

An inspector was also present to witness the final successful fast closure

testing of MSIVs at the end of the inspection period.

The inspectors noted

that the licensee was open and forthright in keeping the NRC

inspectors informed of both the progress and setbacks experienced

during the resolution of the problem.

NRC Conclusions

The majority of the problems and concerns with the MSIVs and associated

isol~tion circuit discussed in this report were discovered subsequent to

the Salem Unit 2 reactor trip of June 28, 1990.

Through the testing,

operating experience and engineering analysis described in section 6.0 of

the report, the licensee achieved a satisfactory resolution of the problems.

Although initial identification of the problem and the first attempt*at

fixing it were faulty, the licensee's thoroughness and conservative approach

thereafter produced an acceptable solution.

Weaknesses were noted in the licensee 1 s prior knowledge of MSIV charac-

teristics, their effect on valve performance, and in the inadequacy of

relevant maintenance and surveillance procedures to assure proper valve

operation.

This lack of a thorough understanding of the MSIVs and of

~roper valve maintenance contributed to another identified weakness, the

licensee

1 s tolerance of degraded MSIV performance, as evidenced by the

recurrent valve drifting events.

Following the discovery of the circuit

deficiency, the engineering team again displayed an insufficient

understanding of how the MSIVs and the circuit function by recommending

the reversal of the operating and reset loop coils.

This modification was

made too hastily, without the proper engineering review and verification,

and resulted in the introduction of more complex and potentially more

severe concerns.

PSE&G was also slow in understanding the requirements of IEEE 279 as they

pertained to the MSL isolation circuit.

The fact that the MSIVs were not

assured of going completely shut if a valve was not initially fully open

when an isolation signal was initiated was a failure to comply with IEEE

Standard 279-1971, Section 4.16, which was committed to in the Salem UFSAR.

However; due to the licensee's self-identification of the non-compliance

and their timely and considerate correction of the deficiency, this failure

to meet a commitment is classified as a non-cited deviation.

(NON 272/90-20-01).

9.

14

~nee the MSIV problems were identified and better appreciated, Salem system

engineering responded well by conducting the proper testing and evaluation

of actual MSIV performance and by developing the new maintenance and sur-

veillance procedures needed to deter future drifting and position indication

problems.

Also noteworthy was the plant operators* post-trip performance

in recognizing and overcoming the failure of the 2 MSIVs to close and the

assistance they provided to engineering in defining what actually had

occurred on June 28, 1990.

After the initial circuit modification was

found to be unsatisfactory, the licensee's engineering effort to resolve

the matter was more deliberate and thorough, as indicated by the in-depth

analysis of all pertinent accident scenarios and by engineering's question-

ing attitude which initiated the full review of actual MSIV performance.

While the engineering team was pursuing these tasks, PSE&G management dis-

played a conservative and safety conscious attitude by shutting down Unit

1 and maintaining both units shut down until a complete and proper resolu-

tion to all problems had been achieved.

The inspectors also noted that

the licensee, both management and staff, was open and cooperative with the

NRC resident staff and Headquarter personnel in the communication and re-

solution of the issue.

Exit Interview

An exit meeting with members of Salem plant management and staff was con-

ducted on August 22, 1990.

The inspectors discussed the inspection and

presented its findings and conclusions to the licensee.

The licensee had

no major questions and expressed their appreciation for the NRC 1 s coopera-

tion throughout the inspection period.

Based on Region I review and discussions with PSE&G, it was determined

that this report does not contain information subject to 10 CFR 2 restric-

tions.