ML18059A559

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Forwards Insp Rept 50-255/93-24 on 930930-1115.No Violations Noted.Nrc Concerned Re Increased Potential for Personnel Contamination Events & Unnecessary Exposure
ML18059A559
Person / Time
Site: Palisades Entergy icon.png
Issue date: 12/06/1993
From: Kobetz T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To: Slade G
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
Shared Package
ML18059A560 List:
References
NUDOCS 9312130038
Download: ML18059A559 (56)


See also: IR 05000255/1993024

Text

Docket No. 50-255

Consumers Power Company

ATTN:

Gerald B. Slade

General Manager

Palisades Nuclear Generating Plant

27780 Blue Star Memorial Highway

Covert, MI

49043-9530

Dear Mr. Slade:

DEC o s 1993

SUBJECT:

ROUTINE RESIDENT INSPECTION AT PALISADES NUCLEAR PLANT

This refers to the inspection conducted by Messrs. M. E. Parker, D. G.

Passehl, D. J. Hartland, and J. A. Lennartz of this office, from September 30

through November 15, 1993.

The inspection included a review of authorized

activities for your Palisades Nuclear Generating Facility.

At the conclusion

of the inspection, the findings were discussed with those members of your

staff identified in the enclosed report .

Areas examined during the inspection are identified in the report.

Within

these areas, the inspection consisted of a selective examination of procedures

and representative records, interviews with personnel, and observation of

activities in progress.

The topics of the September 30 and October 21, 1993,

management meetings are also summarized.

A copy of your handouts presented at

'these management meetings are attached to the report.

The purpose of the.

inspection was to determine whether activities authorized by the license were

conduct~d safely and in accordance with NRC requirements.

During this inspection, housekeeping and material conditions were noled to

have deteriorated in various areas of the auxiliary building.

Most notable

was the excessive amount of cluttered and contaminated areas, and an increased

use of catchments to direct or contain leaks.

Some areas had work request

tags to improve these conditions that were several months to several years

old. This is of concern since there is an increased potential for personnel

. contamination events and unnecessary exposure.

We noted that you have begun

efforts to improve these areas and we will continue to monitor your progress.

Based on the results of this inspection, certain of your activities, involving

a procedure performance error during a safety injection surveillance test,

appeared to be in violation of NRC requirements.

However, as described in the

enclosed inspection report, you identified this violation. Therefore, the

violation will not be subject to enforcement action because your efforts in

identifying and correcting the violation met the criteria specified in Section

VII.B of the "General Statement of Policy and Procedure for NRC Enforcement

Actions," (Enforcement Policy, 10 CFR Part 2, Appendix C) .

9312130038 931206

PDR

ADOCK 05000255

G

PDR

-**-

Consumers Power Company

2

OEC o 6 1993

In accordance with 10 CFR 2.790 of the Corrunission's regulations, a copy of

this letter and the enclosed inspection report will'be placed in the NRC

Public Document Room.

We will gladly discuss any questions you have concerning this inspection.

Enclosures:

.1.

Inspection Report

No. 50-255/93024(DRP)

2.

Attachment 1

3.

Attachment 2

cc w/enelosure:

David P. Hoffman, Vice President

Nuclear Operations

David W. Rogers, Safety

and Licensing Director

~

OC/LFDCB

Resident Inspector, RIII

James R. Padgett, Michigan Public

Service Commission

Michigan Department of

Public Health'

Palisades, LPM, NRR

SRI, Big Rock Point

-<bee: . *PUBLIC .ILOl'"

Rl(le

!V

"

M-

RIII

Axe~n

Orsini

Burdi\\k

U-h/&J1

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(cover letter)

(para.6b'~

Sincerely,

Original sign~d by T.

Kobetz

T. Kobetz, Acting Chief

Reactor Projects Settion 2A

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RIII

~etz

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION Ill

799 ROOSEVELT ROAD

GLEN ELLYN. 11.UNQIS 60137-,5927

Docket No. 50-255

Consumers Power Company

ATTN:

Gerald B. Slade

General Manager

Palisades Nuclear Generating Plant

27780 Blue Star Memorial Highway

Covert, MI

49043-9530

Dear Mr. Slade:

o~c o s 1993

SUBJECT:

ROUTINE RESIDENT INSPECTION AT PALISADES NUCLEAR PLANT

This refers to the inspection conducted by Messrs. M. E. Parker, 0. G~

Passehl, D. J. Hartland, and J. A. Lennartz of this office, from September 30

through November 15, 1993.

The inspection included a review of authorized

activities for your Palisades Nuclear Generating Facility. At the conclusion

of the inspection, the findings were discussed with those members of your

staff identified in the enclosed report .

Areas examined during the inspection are identified in the report.

Within

these areas, the inspection consisted of a selective examination *of procedures

and representative records, interviews with personnel, and observation of

activities in progress.

The topics of the September 30 and October 21, 1993,

management meetings are also summarized.

A copy of your handouts presented at

these management meetings are attached to the report.

The purpose of the

inspection was to determine whether activities authorized by the license were

conducted safely and in accordance with NRC requirements.

During this inspection, housekeeping and material conditions were noted to

have deteriorated in various areas of the auxiliary building: Most notable

-was the excessive amount of cluttered and contaminated areas, and an increased

use of catchments to direct or contain leaks.

Some areas had work request

tags to improve these conditions that were several months to several years

old.

This is of concern since there is an increased potential for personnel

contamination events and unnecessary exposure.

We noted that you have begun

effo~ts to improve these areas and we will continue to monitor your progress.

Based on the results of this inspection, certain of your activities, involving

a procedure performance error during a safety injection surveillance test,

appeared to be in violation of NRC requirements.

However, as described in the

enclosed inspection report, you identified this violation.

Therefore, the

violation will not be subject to enforcement action because your efforts in

identifying and correcting the violation met the criteria specified in Section

VII.B of the "General Statement of Policy and Procedure for NRC Enforcement

Actions," (Enforcement Policy, 10 CFR Part 2, Appendix C).

-*

Consumers Power Company

2

In accordance with 10 CFR 2.790 of the Commission's regulations, a copy of

this letter and the enclosed inspection report will be placed in the NRC

Public Document Room.

We will gladly discuss any questions you have concerning this inspection.

Enclosures:

l.

Inspection Report

No. S0-255/93024(DRP)

2.

Attachment I

3.

Attachment 2

cc w/enclosure:

David P. Hoffman, Vice President

Nuclear Operations

David W. Rogers, Safety

and Licensing Director

OC/LFDCB

Resident Inspector, Rill

James R. Padgett, Michigan Public

Service Commission

Michigan Department of

Public Health

Palisades, LPM, NRR

SRI, Big Rock Point .

2A

-*

.,

U. S. NUCLEAR REGULATORY COMMISSION

REGION I I I

Report No. 50-255/93024{DRP)

Docket No. 50-255

Licensee: Consumers Power Company

212 West Michigan Avenue

Jackson, MI

49201

Facility Name:

Palisades Nuclear Generating Plant

Inspection At:

Palisades Site, Covert, Michigan

License No. DPR-20

Inspection Conducted:

September 30 through November 15, 1993

Inspectors:

Approved

Date

2A

Inspection Summary

Inspection from September 30, through November 15, 1993

(Report No. 50-255/93024(0RP))

Areas Inspected:

Routine, unannounced inspection by the resident and regional

inspectors of actions on previously identified items, licensee event report

followup, followup of events, operational safety verification, radiological

controls, maintenance, surveillance, engineering and technical support, and

management meetings.

No Safety Issues Management System {SIMS) items were

reviewed.

Results:

No cited violations or deviations were identified in any of the nine

areas inspected.

One noncited violation was identified and is described in.

paragr~ph 8.

'The strengths, weaknesses, and Inspection Followup Items are discussed in

paragraph l, "Management Interview."

9312130044 931206

PDR

ADOCK 05000255

G

PDR

-*-

1.

DETAILS

Management Interview (71707)

The inspectors met with licensee representatives (denoted in paragraph

11) on November 16, 1993, and informally throughout the inspection

period to summarize the scope and findings of the inspection activities.

The inspectors also discussed the likely informational content of the

inspection report including the attachments, with regard to document.s or

processes reviewed by the inspectors.

The licensee did not identify any

such documents or processes as proprietary.

Highlights of the exit interview are discussed below: *

a.

Strengths noted:

(1)

Performance of startup testing without incident.

This was

noted to be a significant improvement from the last

refueling outage.

(2)

Operator handling of a rapid power reduction that prevented

a reactor trip.

b.

Weaknesses noted:

(1)

Torque values for main turbine hydraulic fluid hose fittings

found not within specified values.

(2)

Procedure performance error during a safety injection system

surveillance test.

(3)

Housekeeping and material condition in various

radiologically controlled areas of the auxiliary buiJding.

2.

Actions on Previously Identified Items (92701, 92702)

a~

(Closed} Inspection Followup Item 50-255/93010-0l(DRS}:

The-

licensee's technical specification required testing of the main

steam isolation valves did not accurately r~flect their ability to'

perform their safety function. The main steam isolation valves

were tested on power ascensions after they had already been

exercised, repaired, or conditioned.

Therefore, they did not

  • reflect the as-found condition.

The licensee revised General Operating Procedure 9 (GOP-9), "Plant

Cooldown from Hot Standby/Shutdown," Rev.13, to specify that the

subject testing be performed when the main steam isolation valves

are closed during a plant cooldown, which would reflect as-found

conditions and accurately demonstrate the main steam isolation

valves' ability to perform their safety function. This item is

closed.

2

b.

c.

(Closed) Notice Of Deviation 50-255/93010-02CDRS):

For a steam

line break inside containment concurre~t with a failure of the

main steam isolation valve to close on the unaffected steam

generator event, the licensee failed to meet their commitment

documented in a response dated April 28, 1986, with regard to the

following:

Go to once-through cooling (OTC).

Ensure maximum feed flow to at least one steam generator.

Maximize containment spray flow and place containment

coolers in emergency alignment.

Maximize service water and component cooling water flow.

The licensee identified where all of the above items would be

accomplished in the existing emergency operating procedures and

conducted a review of emergency operating procedure strategy with

respect. to initiation of OTC. The existing strategy allows

automatic initiatibn of feedwater, ensured by manual actions, with

acceptable cooling verified by steam generator level and primary

coolant system parameters. If continued use of the steam

generators for decay heat remo~al is not po~sible, OTC would be

initiated.

The current emergency operating procedure strategy was compared

with an alternative strategy of immediately initiating OTC upon

observing the symptoms of a steam line break concurrent with a

failure of the main steam isolation valve to fully close on the

unaffected steam generator. The licensee concluded that either

method would result in continued core cooling.*

. The licensee maintains that the current emergency operating

procedure strategy of using.OTC only if cooling using steam

generators cannot be verified is preferred to immediate initiation

of OTC. The current strategy reduces* the risk of losing the

abi] ity. to coo.l the core, does not further compound an -a 1 ready -. -

complicated event, and conforms to the approved guidance for

Combustion Engineering (CE) plant emergency operating procedures.

Based on the inspectors review of the licensee's response this

item *is closed.

(Closed) Inspection Followup Item 50-255/93010-03(0RS):

No

_operator training has been provided on a steam line break inside

containment concurrent with failure of the main steam isolation

valve to close on the unaffected steam generator event. This event

would result in simultaneous blowdown of both steam generators*

into containment. Additionally, no training has been provided on

determining operability of instrumentation which may be adversely

affected by this environment .

3

-*

d.

e.

The licensee has committed to complete classroom training prior to

th~ end of 1993 for this event. The training for the subject event

is to include discussions on the following:

How a blowdown of both steam generators could occur.

An explanation of why there are differences between safety

analyses and simulator modeling of some events.

Symptoms, expected plant response, emergency operating

procedure paths involved, and the potential for significant

error or failure of instrumentation located in the

containment.

J

Verification of instrument reading validity and use of

al~ernate instrumentation for this and other events which

degrade the containment environment.

Simulator training will also be provided once the necessary

simulator modeling changes are completed (Open item 50-255/93010-.

05(DRS)) and the emergency operating procedures associated with

this event are validated. Based on the licensee's commitm~nt to

provide. the described training, this item is closed.

(Closed) Inspection Followup Item 50-255/93010-04(0RS):

A-caution

in Emergency Operating Procedure 9.0 (EOP-9), "Functional Recovery

Procedure," Rev.3,

provided no useful information. The caution

statement at step 12 stated .the shift supervisor may deviate from

the procedure via 10 CFR 50.54X. This caution is unnecessary and

inappropriate.

Emergency Operating Procedure 6.0 (EOP-6), "Excess Steam Demand

Event," Rev.4, Attachment 2, contained graphs to account for

However, the attachment was not referenced in the body of the

procedure.

The licensee committed to delete the unnecessary caution from EOP-

9: o curing the current emergency operating procedure revision

effort. Additionally, the licensee identified that EOP 6.0,

Attachment 2, is referred to in several places within the EOPs,

such as step 6.a.l of Attachment 1 to EOP 6.0, and considers no

change necessary regarding this item. Based on a review of the

licensee's response this item is closed.

(Closed) Inspection Followup Item 50-255/93010-05(0RS):

The

simulator modeling of a main steam line break inside containment

concurrent with a failure of the main steam isolation valve to

close on the unaffected steam generator event was not accurate .

4

Simulator modeling of containment temperature and pressure

indicated lower value~ than those expected for the event based on

previous analyses.

The licensee is conducting a comparison between the simulator,

CPMAAP (an engineering analysis computer code), and safety

analysis calculations for containment response to the event to

determine correct simulator modeling. The corrections necessary

for proper simulator modeling are scheduled to be completed prior

to the end of 1993. This item is closed.

No violations, deviations, unresolved, or inspection followup items were

identified in this area.

3.

Licensee Event Report Followup (92700, 92720)

The inspectors reviewed the following Licensee Event Report (LER) by

means of direct observ~tion, discussions with licensee personnel, and

review of records.

The review addressed compliance to reporting

requirements and, as applicable, that immediate corrective action and

appropriate action to prevent recurrence had been accomplished.

a.

(Closed) LER 255/92009:

Inadvertent Actuation of the Control Room,

Heating, Ventilation. and Air Conditioning (HVAC) due to Damaged

Electrical Cable:

On February 13, 1992, the control room

ventilation system inadvertently switched to the emergency mode.

At the time of occurrence, the plant was in cold shutdown and the

primary coolant system was de-pressurized.

The control room

operators immediately verified that a valid containment high

pressure (CHP) or a containment high radiation (CHR) signal did

not exist. The licensee subsequently determined that electrical

maintenance personnel were replacing damaged flex conduit on the

CHR relay 5R-6 circuit~ When the wire on relay 5R-6, point 16,

was disconnected, the "A" train of control room HVAC automatically

switched to the emergency mode.

This event was caused by inadequate job planning and personnel

error. . The job p 1 an was inadequate -in that the work instructions

did not identify the electrical scheme as a "de-energize to

actuate" scheme.

Personnel erred by not referring to the approved

drawings prior to lifting wires.

The drawings clearly identify

the "de-energize to actuate" scheme.

The licensee's completed corrective actions were appropriate.

They include reiterating management's expectations through

training that the electrical and l&C staff review electrical

schematics against job plans prior to initiating work.

Proper job

planning requirements were also reviewed with the maintenance

planners. This LER is closed .

5

4.

b.

(Closed) LER 255/92015:

Noncomplying Movement of Heavy Loads due

to Procedure Error:

On August 24, 1989, the licensee discovered *

that a commitment for both the reactor engineer and the shift

supervisor to approve heavy load path deviations was inadvertently

removed from their heavy load procedures FHS~M-23, "Movement of

Heavy Loads in the Spent Fuel Pool Area," and FHS-M-24, "Movement

of Heavy Loads in the Containment Building Area."

A search commenced to determine if any deviations from safe load

paths, approved by only the shift supervisor, had occurred.

Such

a deviation from approved load paths had occurred on September 30,

1990.

The event was caused by the inappropriate procedure rev1s1on and

weaknesses in the commitment tracking system used in 1989.

Since

then the reactor engineer approval was re-instituted back into the

heavy load procedures and the commitment tracking system was

improved.

This LER is closed.

No violations, deviations, unresolved, or inspection followup items were

identified in this area.

Followup of Events (93702)

During the inspection period, the licensee experienced several events,

some of which required prompt notification of the NRC pursuant to 10 CFR

50.72.

The inspectors pursued the events onsite with licensee and/or

other NRC officials.

In each case, the inspectors *verified that the

notification was correct and timely, if appropriate; that activities

were conducted within regulatory requirements, and that corrective

actions would prevent future recurrence.

The specific events are as

follows:

October 9, 1993 -

October 12, 1993 -

November 5, 1993 -

November 6, 1993 -

November 12, 1993-

Unisolable through wall leak identified on

Pressurizer Temperature Element TE-0101.

Unisolable through wall leak identified on

Pressurizer Temperature.Element TE-0102.

Hydraulic fluid leak found on main turbine

number 2 stop valve (CV-0571)

Erratic operation of main turbine number 1

governor valve (CV-0570)

Hydraulic fluid leak found on main turbine

number 2 intercept valve (CV-0548)

The following are brief summaries of the events.

The inspectors will

evaluate corrective actions for the events when the respective LERs are

reviewed .

6

a.

-*

  • '

b.

I

On October 9, 1993, during a reactor coolant system walkdown the

licensee identified water ieaking from a pressurizer head

penetration around the base of temperature element TE-0101.

This

element is used to determine the vapor phase temperature of the

pressurizer.

At the time the leak was identified, the reactor

plant was in cold shutdown with the plant pressurized to 250 psig.

The leak rate was estimated to be about one ounce per minute.

Shortly after this primary coolant system (PCS) leak was

identified, actions commenced to depressurize the system.

This pressurizer resistance temperature detector (RTD) well was

previously scheduled for a visual inspection during plant startup.

The RTD well

h~d not been worked on during the refueling outage;

however, moisture had been observed arouhd this penetration during

the power operated relief valve (PORV) line repairs some three

weeks earlier (see NRC Inspection Report 255/9302l(DRP)).

At the time the PORV leak was found the licensee was uncertain if

the moisture seen at TE-0101 was due to extensive wetting of the

pressurizer head area and surrounding insulation due to the PORV

leak, or due to an actual leak at the RTD nozzle.

Shortly

thereafter, the licensee performed a pressure drop test of the RTD

thermowell.

Although this test did not identify any concerns, the

licensee was unable to perform further evaluation until the PCS

was pressurized .

On October 12, 1993, a similar leak to that described above, was

found during a followup walkdown of the p~essurizer to inspect

additional nozzle penetrations.

The licensee identified moisture

and boric acid corrosion around pressurizer liquid phase

temperature element TE-0102.

This walkdown was performed with the

PCS depressurized and only a static head of water in the

pressurizer.

The leak was estimated at several drops per minute.

Based upon a review of industry experience and NRC Information

Notice 90-10, "Primary Water Stress Corrosion Cracking (PWSCC) of

Inconel 600," the licensee spe(:ulated that the leakage came froin.

between the inconel sleeve.and-the carbon steel shell of the

pressurizer.

On October 12, 1993, daily conference calls were established

between the licensee and the NRC.

In addition, on October 12 and

21, 1993, technical meetings were held with the licensee to

discuss PWSCC on the pressurizer.

The licensee obtained assistance from the Combustion Engineering

(CE) owners group to evaluate this problem.

Region III and NRR

specialists followed the results of additional PCS inspections in

addition to the PORV line repairs.

The licensee's repair efforts

of both TE-0101 and TE-0102 were satisfactory.

(See NRC

inspection report 50-255/93023(DRS) for further details.)

The licensee continued with startup preparations following

7

successful repairs to the leaking pressurizer PORV we)ds ~nd

pressurizer temperature elements.

No additional leaks were

observed during those repair efforts and during containment

closeout tours.

c.

On November 12, 1993, with the plant at 100 percent power~ the

plant experienced a transient when a steam supply valve to the "A"

low pressure turbine was closed due to a hydraulic fluid leak.

Operators performed a rapid down power maneuver on the primary

side to match the secondary side.

The leak occurred on CV-0548, the "A" low pressure turbine reheat

intercept valve.

Upon discovering the leak, the operators

isolated the fluid to the valve causing it to go closed.

The~

resultant pressure spike in moisture separator reheater E-9A

caused lifting of its relief valves.

The operators then isolated

the steam supply to moisture separator reheater E-9C.

This action

placed the main turbine steam system back into a configuration

covered by plant procedures, namely Standard Operating Procedure 8

(SOP-8), "Main Turbine and Generating Systems," Rev.26.

Operators handled the transient well with good coordination

betwee.n the primary side and secondary. side operators.

The quick

reaction by the plant operators and the action of the automatic

controllers in the steam generator water level control system

likely prevented a reactor trip.

The coordination between the

_ operators in the control room is considered a strength.

The hydraulic fluid leak was repaired and the unit was returned to

full power on November 14, 1993.

No violations, deviations, unresolved, or inspection followup items were

identified in this area.

5.

  • operational Safety Verification (71707, 71710, 42700)

Routine facility operating activities were observed as conducted in the

-plant and from-the,main control room. -Plant startup,*steady power*

operation, plant shutdown~ and system lineup and operation were observed

as applicable.

The performance of reactor operators and senior reactor operators, shift

engineers, and auxiliary equipment operators was observed and evaluated.

Included in the review were procedure use and adherence, records and

logs, communications, shift/duty turnover, and the degree of

professionalism of control room activities.

Evaluation, corrective action, and response for off normal conditions

were examined.

This included compliance to any reporting requirements.

Observations of the control room monitors, indicators, and recorders

were made to verify the operability of emergency systems,. radiation

8

.,

monitoring systems, and nuclear reactor protection systems.

Reviews of

surveillance, equipment condition, and tagout logs were conducted.

Proper return to service of selected components was verified.

Periodic verification of Engineered Safety Features status was conducted

by the inspectors.

Equipment alignment was verified against plant

procedures and drawings and detailed walkdowns selectively verified:

equipment labeling, the absence of leaks, housekeeping, calibration

dates, operability of support systems, breaker and switch alignment, as

appropriate.

a.

Genera 1

Plant operators brought the plant back on line on November 8,

1993, ending a 156 day refueling outage.

The plant began the

inspection period in cold shutdown with the primary coolant system

partially drained with preparations for leaving cold shutdown in

progress.

Some relevant dates are:

October 27, 1993 -

October 28, 1993 -

November 3, 1993 -

November 4, 1993 -

November 8, 1993 ~

Reactor left cold shutdown.

Reactor in hot shutdown.

Reactor critical at 10-

4 percent power.

Reactor enter~d power operations at

greater than 2 percent power.

Turbine Generator on line following

suq:essful overs peed testing

The inspectors followed various primary coolant system parameters

during and after plant startup. Primary coolant system leakage

was very low, with no observable trend in containment sump levels.

Primary coolant activity values were normal, at or below measured

values seen following previous refueling outages.

Dose equivalent

iodine averaged less than two percent of the technical

specification limit. Secondary side equipment operated well,

except for some hydraulic fluid leaks associated with the turbine

generator steam supply valves, as previously mentioned.

b.

The inspectors provided expanded site coverage beginning

immediately prior to criticality and extending through the start

of power escalation. Assistance from the D. C. Cook resident

inspector office was obtained. Coverage of all three shifts were

provided daily. Major activities observed were:

Approach to criticality

Reactor criticality

9

6.

Turbine Generator Overspeed trip testing

Synchronization of the turbine generator to the grid for

power ascension

c.

Criticality

The unit went critical at 11:09 a.m.(EST) on November 3, 1993.

This started the low power physics testing portion of the startup

program.

The estimated critical rod height and boron

concentration were within the predicted target band.

d.

Plant Tours

Tours of the control room were routinely made.

Staffing

requirements were met, operators were cognizant of changing plant

conditions, the equipment status and the limiting Condition for

Operation status boards were maintained up to date. *Portions of

the following startup activities were observed:

(1)

GOP-3, "Hot Shutdown to Critical in Hot Standby," Rev.12

(2)

T-191, "Startup Physics Test Program," Rev.4 *

(3)

SOP-8, "Mai~ Turbine and Generating Systems," Rev.27

No violations, deviations, unresolved, or inspection followup items were

identified in this area.

Radiological Controls (71707)

During routine tours of radiologically controlled plant facilities or

areas, the inspector observed occupational radiation safety practices by,

the radiation protection staff and other workers.

Effluent releases were routinely checked, including examination of on-

1 ine recorder traces and proper operation of automatic monitoring

equipment.

Independent surveys were performed in various radiologically

controlled areas.

a.

On one tour the inspector observed the entrance to the East

Engineering Safeguards Room was a posted high radiation area; this

area is typically only a radiation area.

Investigation found the.

reason was a 180 R/hr hot spot lodged in place near the suction of

the low pressure safety injection/shutdown cooling pump P-67A.

The hot spot was appropriately shielded. A gamma scan indicated

the hot spot to be a fuel particle, most likely due to the failed

fuel found earlier this outage and carried through the shutdown

cooling system while that system was operating .

10

-*--**

b.

The licensee's attempt to capture and f~rther char~cterize the

particle proved unsuccessful.

The original intention was to jog

P-67A while tracking the hot particle from the suction piping into

the pump casing.

Using a hot spot flush rig they would flush the

particle through a drain on the casing and capture it in the rig

for further analysis.

Instead, the licensee attempted to flush the hot spot with only

the head of water from the hot spot flush rig, without jogging P-

67A, due to other ongoing testing.

The hot spot did not move

during this attempt.

Later during hot shutdown surveillance

testing of this system, the particle became dislodged and was

flushed out of the piping.

The licensee checked all accessible

piping within the system and concluded the particle is probably

residing in the safety injection and refueling water tank.

There has been no indication of abnormal or excessive radiation

doses received by any individuals nor have any anomalous trends

been noted.

The licensee has an acceptable monitoring program in

place to locate and shield the particle should it reappear in the

system:

Housekeeping and material condition was noted to have deteriorated

in various auxiliary building areas as observed during an NRC

management tour just prior to the end of the current refueling

outage.

Of note was the excessive amount of contaminated area in*

the east and west safeguards pump rooms.

Additionally, throughout

the plant an increased use of catchments to direct or contain

leaks was observed.

Some areas had work request tags to repair

valve and pump leaks and improve material condition that were

several months to several years old.

This item is of concern since there is an increased potential for

personne 1 contamination events a_nd unnecessary exposure.

These observations were discussed with the licensee, who has

commenced aggressive action to reclaim and clean up contaminated

areas. *The inspectors-will continue to monitor the licensee's

progress in this area.

No violations, deviations, unresolved, or inspection followup items were

identified in this area.

7.

Maintenance (62703, 42700)

Maintenance activities i~ the plant were routinely inspected, including

.both corrective maintenance (repairs) and preventive maintenance.

Mechanical, electrical, and instrument and control group maintenance

activities were included, as available.

The focus of the inspection was to assure the maintenance activities

reviewed were conducted in accordance with approved procedures,

11

-*--

  • 8,

regulatory guides and industry codes or standards, and in conformance

with Technical Specifications.

The following items were considered

during this review: the Limiting Conditions for Operation were met while

components or systems were removed from service; approvals were obtained

prior to initiating the work; activities were accomplished using

approved procedures; and post maintenance testing was performed as

applicable.

The following maintenance activities were observed:

(1)

Repairs to the pressurizer PORV weld and temperature element

nozzles

(2)

Troubleshooting of an inoperable subcooled monitoring channel

(3)

Containment Air Cooler VHX-2 service water leak repair

(4)

Troubleshooting of the hydraulic fluid leak found on main turbine

number 2 stop valve (CV-0571)

(5)

Troubleshooting of the erratic operation of main turbine number 1

governor valve (CV-0570)

(6)

Troubleshooting of the hydraulic fluid leak found on main turbine

number 2 intercept valve (CV-0548)

No violations, deviations; unresolved, or inspe~tion followup items were

identified in this area.

Surveillance (61726, 42700)

The inspector reviewed technical specifications required surveillance

testing as described below, and verified that testing was performed in

accordance with adequate procedures.

Additionally, test instrumentation

was calibrated, limiting conditions for operation were met, removal and

restoration of the affected components were properly accomplished, and

test results conformed with technical specifications and procedure

-requirements.

The results were reviewed by personnel other than the

individual directing the test, and deficiencies identified during the

testing were properly reviewed and resolved by appropriate management

personnel.

The following surveillance tests were observed:

a.

b.

c.

RI-47, "Rod Withdrawal Prohibit Interlock Matrix Check," Rev.7

Ml-SA, "Containment High Pressure Test," Rev.O

Q0-1, "Safety Injection System," Rev.34

The licensee issued a deficiency report after testing the left

channel of safety injection when the operators performing the test

12

missed a procedure step to place the control switch for certain

valves in their required positions. Step 5.2.5.b required the

operator to position the control switch for each of eight valves

to the "as-left" position.

However, the operators only visually

verified the valve positions without manipulating the control

switches.

Step 5.2.4 of the procedure requires the operator to push and hold

the safety injection actuation signal (SIAS) push button until

step 5.2.7.

Releasing the SIAS button in step 5.2.7 removes the

S1AS test signal.

When step 5.2.5.a was performed with the SIAS button pressed, the

operators properly verified that the eight valves, two of which

were CV-0913 and CV-0950, changed to their required test

positions.

CV-0913 and CV-0950 supply seal cooling water to the *

high and low pressure safety injection pumps.

Both valves

properly went to the "open" test position.

The following step 5.2.5.b required the operator to position the

control switches for CV-0913 and CV-0950 to the "as-left (in this

case the "open") position.

However, the operators only visually

verified the valves were open without t~rning the control switch

to the "open" position.

The intent of using the control switch

was to leave a standing open signal to CV-0913 and CV-0950, so

that after the SIAS button was released the valves would not

reclose with the high and low pressure safety injection pumps

still running.

As a result, the left train of high and low pressure safety

injection pumps (P-668 and P-678, respectively) ran for about

fifteen minutes without cooling flow to the seals and bearings,

until an operator discovered the condition.

Technical Specification 6.8.1.a requires, in part, that written

procedures be established, implemented, and maintained covering

the applicable procedures recommended in Appendix A of Regulatory

Guide J.33, Revision 2 (February 1978), -Quality Assurance Program

  • Requirements, as endorsed by CPC-2A, Quality Program Description.

The Quality Program Description in CPC-2A endorses Emergency Core

Cooling System Tests in Appendix A of Regulatory Guide 1.33,

section 8.b.(j).

The inspector considers the failure to implement procedure step

5.2.5.b to be a violation of the above requirement.

The cause of

the failure was personnel error, although the instructions at this

section of the procedure could be clearer.

The safety significan~e of running P-668 without seal and bearing

cooling flow for this short time was minimal.

Component cooling

water flows in parallel to cool the pump bearings, stuffing boxes,

and the seal flushing water cooler.

Final Safety Analysis Report

13

{FSAR) section 6.1.2.2.3 states that the seals are designed for

300°F and are provided with cooling to extend seal life. Si nee

the seal cooling was 60°F water from the Safety Injection and

Refueling Water {SIRW) Tank, little if any seal degradation

occurred. Additionally, correspondence from the pump manufacturer

stated that bearing cooling is not needed for the high pressure

safety injection pumps below 250°F.

A similar argument can be made for P-678.

FSAR section 6.1.2.2.2

states that the seals are designed for 325°F and since the seal

cooling was 60°F water from the SIRW tank, little if any seal

degradation occurred. Also, no significant temperature trends

developed during a 1989 test to track performance of the seals,

bearings, and stuffing boxes without cooling water flow during a

45 minute period.

Although the operators made a procedure error, there were several

positive observations.

The prejob briefing went extremely well.

The operator in charge of the test read through the entire

procedure with the rest of the crew and expectations were laid

out.

The ~ystem engineer was

involv~d at the onset of the prejob

brief until the test was completed and provided some good

comments.

There was good discussion on contingency actions should

problems arise during the test, such as an unforeseen loss of

noncritical service water.

Additionally, there was good involvement by the Nuclear Plant

Assessment Department (NPAD) observer present for the test.

Upon

discovering the loss of seal cooling to the pumps the NPAP

observer suggested that someone be sent to the safeguards rooms to

check on the condition of the pumps.

Therefore, the violation will not be cited since the licensee

discussed the problem and quickly performed appropriate recovery

actions and since the criteria specified in Section VII.B.2 of the

"General Statement of Policy and Procedures for NRC Enforcement

Actions," (Enforcement Policy, 10 CFR P~rt 2, Appendix C), were

satisfied.

No violations, deviations, unresolved, or inspection followup items were

identified in this area.

9.

Engineering and Technical Support (37700,92705)

The inspector monitored engineering and technical support activities at

the site and, on occasion, as provided to the site from the corporate

office. The purpose was to assess the adequacy of these functions in

contributing properly to other functions such as operations,

maintenance, testing, training, fire protection, and configuration

management .

14

a.

Various portions of the startup testing program were observed.

Hot shutdown testing, low power physics testing, and power

escalation proceeded relatively smoothly as a result of being

conducted in a well coordinated fashion.

Unlike similar testing

performed at the conclusion of the previous refueling outage, the

startup program was performed without any unplanned engineered

safety feature actuations.

This is a significant improvement from

the last refueling outage and is considered a strength.

b.

The licensee's investigation into the hydraulic fluid leaks on the

main turbine steam supply valves was followed.

The causes of the

two hydraulic fluid leaks were totally separate.

The cause of the

November 5, 1993, leak on main turbine stop valve CV-0571 Was that

one of the hydraulic fluid hose fittings had been insufficiently

torqued.

The cause of the November 15, 1993, hydraulic fluid leak

on main turbine intercept valve CV-0548 was due to a failed a-ring

in a test solenoid valve that supplies the hydraulic fluid.

The licensee has inspected.the other main turbine steam valves and

stated that no other fittings were found to be under-torqued, but

some were found with a higher than specified torque value. All

the fittings found outside the specified torque range were

corrected.

Further analysis has begun to show that. the as-found

values were acceptable from an engineering standpoint, although

they were outside the licensee's internally specified values.

The

licensee's evaluation of this issue is still in progress .

The licensee has inspected other solenoid valves for signs of o-

ring failure with no immediate concerns identified. Their

investigation into this problem is also still in progress and will

continue to be followed.

No violations, deviations, unresolved, or inspection followup items were

identified i.n this area.

10.

Management Meeting (30702)

A ma,nagement meet.ing was held on September -30; 1993, between 0. P

~ *

Hoffman, Vice President Consumers Power Company, and H.J. Miller, Deputy

Regional Administrator, Riii, and their respective staffs. The purpose

of the meeting was to discuss significant events which have occurred

during the current refueling outage and the short and long-term

initiatives Palisades plans to implement for corrective action.

Attachment 1 is a copy of the material presented by the licensee.

A second meeting was held on October 21,* 1993, to discuss events and

corrective actions associated with primary water stress corrosion

cracking (PWSCC) at Palisades. Attachment 2 to this report is a copy of

the licensee's handout from this meeting .

15

11.

Persons Contacted

Consumers Power Company

  1. D. P. Hoffman, Vice President, Nuclear Operations
  • G. B. Slade, Plant General Manager
    • R. D. Orosz, Nuclear Engineering & Construction Manager
  • R. M. Rice, Director, NPAD

T. J. Palmisano, Plant Operations Manager

      • D. W. Rogers, Safety & Licensing Director
  • K. M. Haas, Radiological Services Manager

J. L. Hanson, Operations Superintendent

R. B. Kasper, Maintenance Manager

  • *K. E. Osborne, System Engineering Manager
  • C. R. Ritt, Administrative Manager
  • J. C. Griggs, Human Resource Director
  • H. A. Heavin, Controller
  • D. J. Fitzgibbon, Shift Supervisor
  • G. J. Daggett, Material Management Superintendent

.

  • G. B. Szczotka, Staff Engineer, Nuclear Training Department

Nuclear Regulatory Commission (NRC}

  1. J. B. Martin, Regional Administrator
  1. H. J. Miller, Deputy Regional Administrator

G. E. Grant, Director Designate, Division of Reactor Safety

W. M. Dean, Acting Director, Project Directorate, 111-1, NRR

  • A. H. Hsi a, Project Manager, NRR

.

  • B. L. Jorgensen, Acting Chief, Reactor Projects Branch 2
  • T. J. Kobetz, Acting Chief Reactor Projects Section 2A
    • C. N. Orsini, Reactor Engineer, Reactor Projects Section 2A
  1. *M. E. Parker, Senior Resident Inspector
  • D. G. Passehl, Resident Irtspector
  1. Denotes those present at the management meeting on September 30, 1993.
  • Denotes those present at the management meeting on October 21, 1993.
  • Denotes those present at the exit meeting on November.16, 1993

Other members of the plant staff, and several members of the contract

security force, were also contacted during the inspection period .

16

I

SI'RATEGIES TO PRODUCE lisISI'ENT, IDGH PERFORMANCE *

PERFORMANCE ISSU~ .

  • ACKNOWLEDGE CHALLENGE - BY

EVERYONE (including DPHoffman and

stafO.

'

Driving Force: Our human perfonnance is

1101 allowing us lo achieve the standards and

goals set in our Business Plan.

AN EXCESSIVE COOI...DOWN RATE OF

THE PRIMARY COOLANT SYSTEM

OCCURRED. WE MUST LEARN ALL WE

CAN FROM THIS AND Pl{EVENT THIS

KINO OF PEIU'Ol{MANCE ERl{01{

FROM HAPPENING IN THE FUTURE.

NOD MANAGEMENT HAS A

RESPONSIBILITY TO ASSURE THAT

THE APPLICATION OF DESIGN

AUTHORITY IS ROHUST AND

EFFECTIVE.

STRATEGY

Senior NOD management will conununicate to ~II

NOD employees the significance of inconsistent

pcrfonnance. Gain acceptance by all NOD

employees that perfonnance needs to be

improved.

l~oot cause assessment of this event will he

performed. The implkat ions for senior NOD

management action will he assessed prior to

.. slm1up. The NRC will he brief eel re~ardin~ tlu.*

aclions rclalcd lo lhe cooldow11 t*vcnl.

A review of rccenl design cngi11ccl'ing relalcd

plant evenls will he cond11ctecl, i11cl11cli11g lhc

inoperable safeguards room cooler fans.

Necessary corrcclive aclions will he clcterr11i11ecl.

l111111ediak co1Tcclivc aclio11s will he co111pkll'd

prior lo slnr1iap.

I RESPONSIBILITY I

TPllagan -

Prior to Critical

GBSladc - Prior to

II ea I 11 p

Rl>Orosz - Prior to

Power Operations

u------------------------------*--------------*-*---**** *----*-***-*------

1-ialis.ad('S Nuclear Planl

St*ph*ml>c~r 29, I 99;\\

Page I

--..

I

I

. STRATEGIES TO PRODUCE,NSISTENT, IIIGH l'EIU<'ORMANCE *

PERFORMANCE ISSUFS

RECENTLY, PLANT EQUIPMENT WAS

CHANGED WITHOUT INVOKING THE

'MODIFICATION PROCESS~ I

A PIUMAR\\' OB.IECTIVE OF NOO IS TO

MAINTAIN THE MATEIUAL CONDITION

OF TllE PLANT WITlllN ITS DESIGN

HASIS. RECENTLY, A PRESSUIUZER

NOZZLE TO PIPING WELD CltACJ<

l>EVELOl'EL> TO BECOME A TllROUGll

WALL CRACK. THE IMPLICATIONS OF

TlllS EVl~NT MUST HE ADDRESSED.

l~1li'>.lult~ Nuclcnr lttlrnt

September 29, 1993

~*-----------*

STRATEGY

RESPONSIBILITY

Plant administrative processes will be reviewed to

RDOrosz - Prior to

determine if .they allow 'changes' to the plant

Power Operations

outside the approved Design Basis without

adequate review. Procedure and organizational

responsibilities will he changed as necessary to

prevent this.

A plant specific c11gi11ecri11g cval11alio11 of lhe

primnry wntc~r .'ltl'l'SS COl'l'OSiOll Cl'lldd11g ('OIH'C'l'll

\\viii he pcrforuwd 1111<1 will he <

00111plel eel pl'ior Io

plant star1up. A strategy will he clcvclopcd to

dent with Industry co11<'l'1*11s rdall*cl ,,, pri111ar.Y

mater stress col'l'oslon c1*acld11g. Palisades issues

will he 11sscsscd 11 ncl <1<'11 It with 1a.11 11 gc*11c*ric.

concern relevant to the i11cl11stry.

All adio11s

required to assure safe operation in lhc m*xl

operating cycle will he complelcd prior to

startup.

IU>Orosz - f>rio1; lo

I lc*al ll11

STRATEGIBS TO PRODUCE CONSISTENT, IIlGII PERFORMANCE

PERFORMANCE ISSU~

NOD MANAGEMENT RECOGNIZES ITS

NEED TO BECOME MORE EFFECTIVE

IN CREATING THE CONDITIONS AND

CAPABILITIES WHICH WILL PRODUCE

MORE EFFECTIVE PERFORMANCE. IT

WILL SEEK CANDID AND OBJECTIVE

FEEDBACK ABOUT ITS PERFORMANCE

AND WILL CONTINUOUSLY WORK TO

IMPROVE.

MANY VERBAL COMMITMENTS HA VE

UEEN MADE IN PUHi.JC AND NRC

MEETINGS. NOD TAKES THESE

COMMITMENTS SEIUOUSLY.

TllE SAFETY SIGNIFICANCE OF

DISCREPANCIES IDENTIFIED BY CCP

REVIEW NEEDS TO BE QUANTIFIED.

P*.tlisade-; Nuclear Plant

~~ptcmh<~r 29, 1993

STRATEGY

An assessment will be performed to review

management's current approach to the challenges

we face and will provide information to

corporate management about the effectiveness of

our managemerit process and proposed actions.

An independent consultant (Tencra) will be

utilized to support this assess.ment.

Corporate ma11agc111e11t will he briefed 011 IN PO

field notes and the information obtained fro111 the

site debrief.

Public meetings and enforcement conference

meeting 111in11h.*s will he reviewed to c11s111*t* all

commitments have heen met.

The CCP discrcp1111cy list will he reviewed to

ensure the Plant Review Committee has been

made aware of any signific:1nt iss1u.*s. Any new

issues wlll be dispositioned prior to plant star111p.

Page 3

RESPONSIBILITY

RM.Rice - Prior to

Critical

I> 1'11 off man - Prior

to Power

Ope rat ions

CBSladl' - Prior

lo Crit iral

IU>Orosz - Prior to

I feat up

STRATEGlliS TO PRODUCE CONSISTENT IUGH PERJ:i"'ORMANCE

.

.

'

PERFORMANCE ISSUES

PROCEDURAL PROBLEMS RELATEO

TO TEST ANO SURVmLLANCE

ACTIVITIES HA VE BEEN PREVIOUSLY

IDENTIFIED AND MUST RE RESOLVED.

THE INDETERMINATE STATUS OF

NODS HAS BEEN A SIGNIFICANT

CONTRIBUTOR TO AMBIGUITY. SOME

NODS llA VE NOT BEEN CANCELLED AS

PLANNED; AND SHOULD BE.

HUMAN PERFORMANCE l~OOT CAUSE

EVALUATIONS PROVIDE IMPORTANT

INFORMATION FOR NOD

MANAGEMENT.

NOD MANAGEMENT RECOGNIZES ITS

RESPONSIBILITY AS A NUCLEAR

LICENSEE TO KEEP THE NRC

INFORMED.

l~1li..ad~ Nuclear Pta'nt

September 29, 19'J3

STRATEGY

A 111111fi-cli.c;dpli11nry h*n111 n*vil'w will he

conducled of all new or previously prolJlcmalic

special tests and si1rvcillancc procedures llrnl will

he implcmcnlcd prior lo startup. The review

and any procedural revisions will be performed

prior to their use during plant sta1111p.

An SMSC Meeting will he conducted to cancel

NODS which arc ready for cancellation.

RESPONSIBILITY

CBSlaclt* - All

mill's! ones (as

procedure is

rcq 11 ired)

.J.J Fremeau - Prior

to Critical

Pnlisndcs llPES Coordinalor will review 1993

CBSlade - Prior to

Human Performance Event/Deviation Repo11s lo

Critical

determine if there arc any common causal facl ors

which have not been addressed. The results for

Palisades will be reviewed pri01' lo planl startup

at n Plant Review Commiltce mccling which will

include the NOD Senior M:rnagemcnl tea111.

A. co1111nunication slratcgy lo l<c<.*p NRC i11for111t'cl

of significanl (~V('

1

a1ls will IH* dcv(*lopt*cl. l<t*.v

conlacls, frequency of meetings, and

con11111111ication loots will be developecl.

Page 4

l'M Do1111clly - Prior

to ll1*al11p

PROCESS FOR LONG-TERM HUMAN PERFORMANCE IMPROVEMENT

BUSINESS PLANNING MEETING -

OCTOBER 14

Accelerated Human Performance Action Plan

Long-Term Human Performance ~ctio~ ?lans

Status of Short-Term Human Perforwar.ce Action Plans

NRC UPDATE MEETING -

LATE OCTOBER

TENERA DIAGNOSTIC ASSESSMENT -

OCTOBER 29

Root Cause of Human Perf orrnance Problems

Cultural/In.stitutional Issues

Recommendations for Improvement

BUSINESS PLANNING MEETING

-

NOVEMBER 10

TENERA Diagnostic Recommendations

"Performing on the Job" Strategy

Review of Performance Against Business Plan Targets

Status and Update of Business Plan Action Plans

The outcome of this meeting will be an update to the

Business Plan for 1994.

NRC UPDATE MEETING -

LATE NOVEMBER

BUSINESS PLAN MEETING -

EARLY JANUARY

1994 Goals and Objectives (Reflecting the Updated

Business Plan) .

NRC UPDATE MEETING -

LATE JANUARY

1994 BUSINESS PLAN MEETINGS TO BE SCHEDULED

.

.

--*-*

.

"!'.

  • .

.

.::

.*Non** NOW

.News of immediate interest to employees of NOD September 27, 1993

PALISADES MONITORING PROGRAM UPDATE

This year a number of issues and events arose involving human performance at

Palisades. These issues and events have impacted our continued success as an

organization and as such, demands all of our attentio_n to improve.

Over the past several weeks, the Palisades Management Team has been

collectively meeting to create a plan of action to help us understand and address these

human performance issues. The first step of.the plan involves systematic monitoring

of individual and group performance through field observation as well as Corrective

Action and Human Performance Enhancement System (HPES) trending. The field

.onitoring of performance will be conducted as an addition to the periodic reviews

organizational performance, equipment performance, and material condition that

have been on-going to determine the need for action in these areas.

The principal concept of the program is to observe the general environment

  • .employees work in: the procedures. the processes, and the barriers that employees

cope with to accomplish their work. Then we will work to break down those barriers.

Field notes will be used by the Management observers, similartoan INPO Field Team,

  • to permU recall and follow-up. Each manager will conduct two observations monthly.

We will then meet to compare notes and define actions and additional areas to

monitor the next month.

In addition, within the coming week, Vice President, Nuclear Operations, David

Hoffman, will be issuing an all-employee communication detailing an Action Plan for

the NOD Management Team to address Human Performance improvement for both

the short- and long-term future .

  • -*

I.

PALISADES MONITORING PROGRAM

  • Revis ion 0

PURPOSE

To systematically monitor organizational performance issues thro~gh

field observation, corrective action and HPES trending, NPAO monitoring.

and NOD management monitoring.

II. CONCEPT

Palisades Plant Management will establish a focused monitoring pian

which incorporates direct field observations, reviews of results of

existing management systems, and outside observation activities by NPAD

and others.

A periodic review of the current level of organizational

performance, equipment performance, and material condition will be held

to determine the need for additional action.

II I. PLAN

A.

Palisades Plant Management staff shall meet and identify specific

topics or areas to be monitored for next quarter.

The purpose of

this discussion is to focus monitoring efforts so that consistent

data is obtained for further review.

8.

A monitoring schedule shall be established imonthly identifying

topics.or activities to be monitored and specific individuals

assigned to monitor.

C.

Monitoring shall be performed as assigned.

Written summary of

observations should be submitted within 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> of monitoring.

D.

Monthly review meeting shall be held with Palisades Management

Staff to review results of following, as apprqpriat_e:

1.

Field monitoring.

2.

HPES reviews.

3.

Corrective Action trending.

4.

Departmental monitoring systems (RDR's, rework monitoring,

etc.}.

5.

NOD management visit program.

6.

NPAD monitoring results .

7.

Internal and External audit report results.

Page Two

Monthly review meeting should have a set format.

Specific topics

which should be covered include:

1.

Human Performance.

2.

Work Process performance.

3.

Equipment performance.

4.

Effectiveness of previous actions.

5.

Topics for future field monitoring.

  • D.

Action assignments shall be made based on the results of the

review meeting.

E.

Quarterly, the Plant General Manager should report the results of

this monitoring program with the VP Nuclear Operations.

IV.

RESPONSIBILITIES

A.

B.

The Plant General Manager is responsible for the impler.iEntation of

this program.

He is also responsible for quarterly reporting of

results to the VP Nuclear Operations .

The Operations Manager is responsible for the scheduling of

monthly review meetings, including written documentation of the

results of the meeting.

C.

Various Management personnel are responsible for perfon:iing

monitoring activities as assigned.

V.

RECORD REQUIREHENTS

A,

The only records required to b~ retained ~re the minutes of the

monthly Management Review Meeting.

These records shall be filed

in DCC.

VI.

PROGRAM CHANGES

The program may be changed with the approval of the Plant General

Manager.

Changes to the program shall be docU11Dented as revisions to the

program .

Plant General Manager

  • ----

1.

FIELD OBSERVATION GUIDANCE

Observe as many aspects of the activity as is practical including the pre-job

briefing and the follow-up documentation.

2.

  • Observe - don't supervise. You are there to observe not consult

(Unless, of course, you need to intervene to prevent personal injury or equipment

damage.) It is okay to ask questions but do not provide direction_

3.

Log TIME on the Field Notes periodically.

(If something unusual occurs you may want to increase the frequency of your

timing notes. For example: if they are interrupted by the page and it would help

your evaluation to know how long it took them to get back on track.)

4.

lndude every factual observation and interaction that occurs.

5.

Try to withhold judgement while taking Field Notes. Record facts not opinions_

6.

Evaluate the Field Note facts using the Field Observation Checklist

7.

Conduct a feedback session with the workers and supervisor. If a problem or

deviation occurred, determine if a corrective action document is warranted.

8.

Forward all documentation to Debbie Beach .

OBSERVATION FIELD NOTES

Workers Involved

Dateffime

Supervisor

Location

Observer

Activity

I TIME I

oss=RVATION FACTS

I EVALUATION

jj

I .

'

!

I

l

ij

-

--*-

  • I TIME I

.

"-

OBSERVATION FIELD NOTES

(Continuation Sheet)

OBSERVATION FACTS

I

Page _of_

EVALUATION l

--*

FIELD OBSERVATION JOB AID

Workers Involved

Supervisor

  • Observer

Datemme

Location

Activity

PREPARATION

Individuals are trained and qualified to perform the task

Prejob briefing conducted IAW prejob briefing job aid

.Prerequisites were completed and verified

Procedures, precautions, and limitations were reviewed

Tools/materials were available and ready

Job was properly planned and scheduled

PERFORMANCE EVALUATION

Crew successfully completed the task

Written instructions were used and adhered to and were adequate

Crew{s) worked together as a team to complete the task

Industrial safety standards were rr.et

Radiation safety standards were met

Initiative and innovation were demonstrated in completing the job

Decisions made were conservative

Supervision kept appraised of job status and problem5

Communications IAW departmental communications policies

REMEDIAL ACTIVITIES .

Effective proper feedback provided to workers

Appropriate corrective action documents generated

Procedures changed as required

  • CLEANUP/DOCUMENTATION

lessons learned captured in historical file

Tools and equipment returned to the originaVproper condition

Documents/records-were- completed correctly

Work area returned to the originaVproper condition

SAT

NII

NOTES/COMMENTS (Include comments for all.needs improvement {NII) items and for any exceptional

performance)

N/O

I

To

From

Date

Subject

cc

MA£ngle, Palisades

BAFarnworth, Palisades

OLBeach, Palisades

September 8, 1993

PALISADES PLANT:

MANAGERS MEETINGS.

CSmith, Palisades

CONSUMERS

POWER

COMPANY

Internal

Correspondence

Below is a list of upcoming managers' meetings,:: be held in the Managers Conference

Room from 1100-1300, including dates and tJpic(s) fer discussion.

DATE

TOP!C(S)

September 14

STANDARDS AHO EXPECTATIONS

16

Development

21

Corrcunicate

24

Monitor

28

Accountability

October 6

HONITORIHG

8

Review Program

14

MANAGING CHANGE

Identification

Assessrnient

Pi ann ing

Imp l e-:nenta ti on

Priorities

October 19

COHHUHICATIOH

27

Content

29

Tools

Feedback

November

3

LEADERSHIP ANO MAHAGE11EHT SKILLS

9

Coaching

--

- .

--

17

Counseling

24

Feedback

30

Development Haves

Department Head Alianment

December 9

PERFORMANCE RECOGNITION

.

~

.

OPERATIONS PERSONNEL AVOIDABLE OCCURRENCES

20

..

CJ)

  • (AS DETERMINED BY ER'S AND DR'S)

1993 YEAR TO DATE

Both D/Gs Out Of Service.

Misaligned !so-Phase Bus Cooling.

CV-0521 Mispositioning.

Tagging Error On C-903A.

Improper Lineup For Q0-1.

CROM 20 & 31 Excercizcd In Error.

SFHM Unclerload Bypassed .

w

(.)

I

  • ' ' ' * t ''' ' ''''' '* '''

SID Cooling Temperature <70° F.

Failure To Uncouple Control Rod

Failure To Close MV-PCI094A During

R0-65

z

w

a: 15

a:

>

(.)

(.)

0

w

_J

co 10

<(

0

0 >

<(

LL

0

5

a:

w

co

~

J

z

..................

  • .:.:.:.* .. ".:*.:*,:*.:*.:*.:*.

.*::::::*:::::::::::::::::::*:::::.:.::::::::::::.

.:*. **. **.:* ........ **.:*. ",:*.:*.:

0-----...

1989

1990 :

........................

                                                • .

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.. .. ** ........... " .

. .. .. ,. , ............. .

.. , ....... , ........... .

......................

.. .. " ................ .

, ... , ............. ..

..................

1991

1992

1993 (YTD)

. 935090 PCS HEA TlJp I COOLDOWN

PORV LINE CRACKED WELD LOCATED IN HOT SHUTDOWN

550 ------------------------*------*---*---*-----.

500

450

400

350

300

250

200

150

100

SDC RETURN_;>-

TEMP

50

,~.--.---.---.---.-..---..----.--..--..---..---.--.-..---.--.---.----.-,-r--1--r--1-r--r--*-1--*1--*1-- -.--r-,-,-

12:00 AM

12:00 PM

12:00 AM

12:00 PM

12:00 AM

12:00 PM

12:00 AM

Sepl5,'93

Sepl6,

193

Sepl7,'93

Sepl8,'93

935090 PCS COOLDOWN

PCS COOLDOWN AFTER PORV LINE CRACKED WELD FOUND IN HOT SHUTDOWN

500

450

400

350

300

op

250

200

SOC RETURN

TEMP

>

150

100

50 ~--..--.--.---.-~-.---.--r--,.---,i--..--,

-,--,--.--.-.--.--.--,-,---,-r::-i--,--r--r-r-r-,*-r-r-1--y*-1-T-!-T-T-.-...---.---I

6:00 PM

9:00 PM

12:00 AM

3:00 AM

6:00AM *

9:00AM

i2:00 PM

3:00 PM

6:00 PM

Sep 16,

193

Sep 17,

193

2 MINUTECFMS DATA

. ' .

Attachment 2

.-

CONSU1\\.1ERS PO\\VER CO:\\lPAl'\\i'Y l\\1EETING \\'1TH J\\1RC

INCO~L 600 ISSlJES

INDUSTRY AA"'D PALISADES EXPERIENCE

OCTOBER 21, 1993

AGENDA

1. Introduction

RD Orosz

2 . Industry Inconel 600 Experience

PD Fitton

- Failures and Corrective Actions

- Safety Assessments

3. Palisades. Experience

DJVandeWalle

- Failures and Corrective Actions

- Safety Assessments

--

4. Cause of the Relief Valve Nozzle

RBJenkins

Safe-End Crack

5.

Palisades Inconel 600 Program

DABemis

6. Long Term Corrective Actions

RDOrosz

INDUSTRY INCONEL 600 EXPERIENCE

CEOG formed an lnconel 600 Working Group in late 1989. This

group was formed to investigate the Primary Water Stress Corrosion

Cracking (PWSCC) leaks at:

Calvert Cliffs

San Onofre Unit 3 (1986)

St Lucie Unit 2 (1987)

EdF * (7 Units) (1989) (France)

AN0-1 (B&W) (1990)

GOALS:

1. Determine root cause and contributors

2. Evaluate susceptibility to PWSCC at other CE plants

3. Determine safety consequences if a leak were to occur

4.

~ ~~tablish methods and frequency of inspection

5. Develop repair methodologies

--*

INDUSTRYINCONEL600EXPERIENCE

IN Silltfl\\iARY WE LEARNED:

1.

For Primary Water Stress Corrosion Cracking (PWSCC) to occur

we must have:

A.

Susceptible material

B.

High temperature

C.

High tensile stresses

,,

I

I.

I !

I

!

INDUSTRYINCONEL600EXPERIENCE

  • OUR PRELIMINARY EVALUATION CONCLUDED:

1. The pressurizer is by for the most susceptible location due to

normal operating temperatu'res.

2.

High strength material was most susceptible because it could

retain higher

levels of residual stress without yielding, and

  • hence limiting the stress.

3. . PWSCC in inconel 600 penetrations is an economic issue, not a

safety issue. This conclusion was based on work demonstrating:

A. We expect axial cracks with J weld configurations

I . Field data

2. Analytical modeling

3. Mockup measurement of residual stresses

B. Leakage could occur for several fuel cycles without

compromising the integrity of the PCS pressure boundary.

4. Leakage is most likely to occur in the pressurizer vapor space .

INDUSTRYINCONEL600EXPERIENCE

PRESSURIZER LEVEL TAPS

1.

Unique Butt weld safe end

2. Contracted CE to measure residual stresses in mockup

3. Conclusion: No significant residual tensile stresses are not

produced by this configuration. (Reference 91-ESP-77 A)

CONTROL ROD DRIVE MECHANISM REACTOR HEAD

PENETRATIONS

1.- Goals same as pressurizer

2. Palisades is participating in these activities

3. Work to date has supported conclusion that PWSCC does not

. Jeopardize PCS integrity for these penetrations ..

-.

PALISADES INCONEL 600 EXPERIENCE

Pressurizer relief valve nozzle safe-end crack .

circumferentially oriented crack in heat affected zone of

safe-end-to-pipe welq

repaired weld with like design

Pressurizer temperature instrumentation nozzle leaks .

axially oriented cracks in nozzle near structural "J" weld to

pressurizer vessel

temporary modification involving installation of exterior weld

"pad" addition and severing of Inconel sleeve between "pad"

and "J" welds

3"

Relief

Valve

~zzte

3"

Safety

Valve

Nozzle

l"

l"

Level

~le

TOQ View

Level

Nozzle-.4-"--..,.

Bottom View

Manw~

3"

Safety

Valve

~zzle

Relief

v at\\'t

Noz::zle

I

L

... ----121f co :Ret----

Su~rt

Skirt

I

llO ii' 0 IA II nsido Cladding1

Heater

Su~e

Noz:z e

, ..

!

T!~O

~.;ozzie

I

130f' 00

Elevation

r/6UR£ 1

PRESSURIZER SHED

. -

.

GENERALEQUIP:MENTLAYOUT

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PflESSUR I Z ER ____.

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. .

. - -

.-

. --

... LONGITUD*INAL *SECTION *SHOWING WEL.D ,-- CRACK I

WELD RE.PAIR .

TE-0101 MODIFICATION

,... ,.... SA.-- -

.......

~.::::>.

rt :.N:_*

INCONC:L

NOZZL~

PRJ 0 n~~n ~xT~~roo

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WE:.....O "PAD" ADDITION

C.S. PRESSURIZE=:

INTERNAL

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-'*-*

LP..: 0!.NG

T- 72 PRESSURIZER

-*

PALISADES INCONEL 600 EXPERIENCE

Safety Assessment

Pressurizer relief valve nozzle safe-end crack

Evaluated other pressurizer and PCS nozzles with Inconel 600

for susceptibility *

Examined susceptible nozzles on the pressurizer

Evaluated lifetime of repaired pressurizer relief valve nozzle.

Repair is considered temporary with a lifetime of one refueling

cycle. A permanent repair will be implemented during the 1995

refueling shutdown .

Evaluated margin-to-failure of cracked pressurizer relief .valve

nozzle and concluded that nozzle had sufficient strength to

withstand normal and faulted conditions

Evaluated primary coolant system leakage detection system and

concluded that similar cracks would be detectable. This .leak

detection capability was demonstrated during the pressurizer

. relief valve nozzle leak .

  • --

PALISADES PRESSURIZER SAFE-END CRACK

Cause of the Safe-End Crack

For primar*y water stress corrosion cracking (PWSCC), there

are three required factors. These are:

A metallurgical condition

An aggressive steam/water environment

A threshold stress value

The safe-end was made of a material with a high yield stress

which made it vulnerable to PWSCC. These vulnerabilities are

refl~cted by:

A high hardness HRC-22

A high yield stress of 77KSI

An assumed low (1600-1700°F) post"'.forging heat treatment

The safe-end was exposed to stagnant steam at approximately

640°F. The material would be highly sensitive to cracking at

this temp~rature.

  • *

Although externally applied piping system loads induced by

pressure, weight and thermal expansion meet design

.

requirements and are relatively low, significant local stresses

. appear to exist at the Inconel/stainless steel safe-end weld.,

These stresses are due to:

The field welding process

The mismatch in pipe/safe-end sizes

The materials mismat.ch thermal effects

To add insight into the load assessment, analysis of dissimilar .

metal effects and temperature stratification were conducted.

These evaluations led to the conclusion that these loadings

along with the external piping loads, as induced by the piping

support system, were not the driving forces for the crack. The

local pipe/safe-end configuration and fabrication process are

judged to be as the primary romributors.

,:i

PALISADES PRESSURIZER SAFE-END CRACK

Repair of the Pressurizer Safe-End

The heat affected zone of the inconel material was removed and

the weld prep machined to assure that the new heat affected

zone does not have intergranular penetration or discontinuities

that could act as stress risers.

The fit-up between the safe-end and stainless steel pipe was

improved.

The inner surface of the weld was ground s~ooth .

There were no repair weld deposits made, to the inner surface _

of the weld .

All of these improvements and changes will extend potential

crack initiation time significantly, resulting in increased lifetime

for the repaired weld as compared with the original weld.

Very conservative crack propagation calculations indicate more

than 20 months at temperature and pressure (640°F, 2060 psia)

would be required for a crack to grow through wall. For the

. 15 month fuel cycle, an initial 0.039in semi-elliptical crack of a

6: 1 aspect ratio would just grow through-wall.

Time to crack initiation in the heat affected zone of the new

safe-end should be comparable with that of the original safe-end

heat affected zone. No credit is taken for this in the calculation

of time to through wall cracking.

Therefore, the lifetime of the new weld will exceed one

operating cycle.

    • '

...

PALISADES INCONEL 600 EXPERIENCE

Safety Assessment

Pressurizer temperature instrumentation nozzle leaks

Confirmed that cracking is similar (i.e. axial orientation) to that

experienced in other industry instrument nozzles

Evaluated other pressurizer and PCS nozzles for susceptibility

Examined susceptible nozzles on pressurizer and PCS loop

Evaluated lifetime of temporary modification~ Modification is

considered temporary with a lifetime of one refueling cycle .

Combustion Engineering Owners Group generic safety

evaluation applies

, .

PALISADES INSPECTIONS/LEAKAGE MONITORING

Palisades outage/startup inspections

l. ASME Section XI ISI inspections

2. PCS boric acid walkdowns

3*.

System Engineering inspection of pressurizer heater sleeves

4. PCS walkdown at 2150 psia after each refueling outage.

On line leakage monitoring

1. Daily PCS leakage calculation

2..

Monitoring containment parameters

Sump level

Containment temperature

Containment humidity

Radiological conditions

Biweekly containment. tour of lower elevation

PALISADES INCONEL 600 PROGRAl\\1

I.

BEFORE 1995 REFOUT

A.

Plan for replacement or justification of continued operation

of temporary Inconei 600 penetration repairs.

B.

Implement comprehensive PCS penetration inspection

program, based upon industry and Palisades experience:

1 .

Maintain list of PCS penetrations prioritized for

inspection and maintenance, including the following

considerations:

a.

Material types.

b.

Postulated mode(s) of failure.

c.

Potential safety and economic impacts from

failure.

d.

. Expected reliable life (Reliable life ends when

continued use or repairs are not justifiable for

safety, reliability, exposure, or economic

reasons).

e.

Conditions required for inspection, repair, and

replacement.

2.

Establish enhanced inspection program for PCS

penetrations approaching end of expected reliable life.

3.

Develop plan to improve or replace penetrations prior

to expected end of reliable life.

-

4. . Ensure that inspecJion program effectively bounds

conditions under which cracking is found.

5.

Evaluate and qualify non-destructive examination

techniques for detection of PWSCC .

C.

Develop remediation plan for cracked and leaking Inconel

600 penetrations.

PALISADES INCONEL 600 PROGRAM

.. II.

1995 REFOUT

A.

Replace:

l.

Temporarily repaired penetrations that are not

justified for continued operation past one cycle.

2.

Other penetrations identified for replacement with

improved materials or designs.

B.

Inspect old, removed penetration components for:

1.

Adequacy of previously performed repairs.

2.

Evidence of aging as compared to expected rate.

3.

Verification of conformance to expected failure

modes.

,.

c.

Inspect penetrations in accordance with PCS penetration

inspection program.

D.

Based upon inspection results, expand inspection scope as

needed to bound cracked penetrations.

E.

Remedy found cracked and leaking penetrations in

accordance with remediation plan.

III.

SUBSEQUENT TO 1995 REFOUT

A.

Adapt penetration inspection program and remediation plan

after each Refout, based upon updated industry and

Palisades experience.

B.

Execute penetration inspection program and remediation

plan during each Refout .

  • .

PALISADES INCONEL 600 EXPERIENCE

Long Term Corrective Actions

Evaluate design of pressurizer relief valve nozzle and PORV line

and perform modifications necessary to assure a suitable nozzle

lifetime.

Perform permanent modification to pressurizer temperature

instrumentation nozzles.

Develop comprehensive program to deal with Inconel 600 issues at

Palisades. Program to include:

Evaluation and qualification of non-destructive examination*

techniques for detection of PWSCC .

Development of an augmented inspection program for

Inconel 600, including temperature nozzles, safe-ends and

control* rod drive nozzles.

Planning for replacement of Inconel 600.

Contingency planning for inspections/repairs of any future leaks .