ML18058A511

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Initial SALP II Rept 50-255/92-01 for Jan 1991 - Mar 1992. Area of Emergency Preparedness Rated as Category 2. Performance in Plant Operations Functional Area Declined
ML18058A511
Person / Time
Site: Palisades Entergy icon.png
Issue date: 06/08/1992
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18058A510 List:
References
50-255-92-01, 50-255-92-1, NUDOCS 9206160085
Download: ML18058A511 (19)


See also: IR 05000255/1992001

Text

INITIAL SALP REPORT

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

Inspection Report No. 50-255/92001

Consumers Power Company

Palisades Nuclear Generating Plant

January. 1, 1991, through March 31, 1992

9206160085 920608

PDR

ADOCK 05000255

G

PDR

SALP 11

CONTENTS*

I.

INTRODUCTION ****************************** * *************

Page

1

II.

SUMMARY OF RESULTS *************************************

2

JII. PERFORMANCE ANALYSIS *****...****** ~ **.********** ~......

3

A.

Plant Operations ***.**......**....*.**.***.****.**

3

B.

Radiological Controls ******** ~....................

5

C.

Maintenance/Surveillance ************ ~.............

7

D.

Emergency Preparedness *************r*******~******

9

E.

Security .......... *................................

10

F.

Engineering/Technical Support **** ~ ********* ~~.....

11

G.

Safety Assessment/Quality' Verificat.ion * * * * * ** * * * * *

13

IV.

SUPPORT! NG DATA AND SUMMAR I ES * * . * * *.* * * * * * * * * * * * * * * * * * * *

16

A.

Major Licehsee Activities ***.*********************

16

B.

~ajor Inspec~ion Activities ************ ~.*~******~

17

I.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) program is an

integrated U. S. Nuclear Regulatory Co1m1ission (NRC) staff effort to collect

av*ilable observations and data on a periodic basis and to evaluate licensee

performance on the basis of this information. The program is supplemental to

normal regulatory processes used to ensure compliance with NRC rules and

regulations. It is intended* to be sufficiently diagnostic to provide a

rational basis for allocating NRC resources and to provide meaningful feedback.

to the licensee's management regarding the.NRC's assessment of the facility's

performance in each functional area.

An NRC SALP Board, composed .of the staff members 1 i sted be 1 ow, met on May 13,

1992, to review the observations and data on performance, and to assess

licensee. performance in accordance with the guidance in NRC Manual

Chapter 0516, "Systematic Assessment of Licensee Performance."

This report is the NRC's assessment of the lic~nsee's safety performance at

Palisades for the period January 1, 1991, through March 31, 1992.

The SALP Board for Palis.ades was composed of the following individuals:

Board Chairman *

E. G. Greenman, Director, Division of Reactor Projects (DRP)

Board Members

H. J. Miller, Director, Division of Reactor Safety (DRS)

C. E. Norelius, Director~ Division of Radiatibn Safety and Safeguards (DRSS)

L. B. Marsh, Project Director, Project Directorate (PD) III-1, Office of

Nuclear Reactor Regulation (NRR)

B. L. Jorgensen, Chief, Section 2A, DRP

B. E. Holian, Senior Project Manager, PD IV-2, NRR

J. K. Heller, Senior Resident Inspector, Palisades

  • A. S. M~sciantonio, Project Manager, PD III-1, NRR
  • Non-voting member

Other Attendees at the SALP Board Meeting

C. E. Brown, Reactor Engineer, DRP

R. L. Bywater, Reactor Engineer, DRP

J. R~ Creed, Chief, Safeguards Section, DRSS

M. K. Gamberoni, Project Engineer, PD III-1, NRR

G. M. Hausman; Reactor Inspector, DRS

J. E. House, Senior Radiation Specialist, DRSS

F. J. Jab~onski, Chief, Maintenance and Outages Section, DRS

A. w. Markley, Senior Radiation Specialist, DRSS

F. A. Maura, Reactor Inspector, DRS

J. H. Neisler, Reactor Inspector, DRS

M. P. Phillips, Chief, Section 2B, DRP

T. J. Ploski, Senior Emergency Planning Specialist, DRSS

D. L. Schrum, Reactor Inspector, DRS

W. G. Snell, Chief, Radi~logical Controls Section, DRSS

II.

SUMMARY OF RESULTS

Overall performance at the Palisades Nuclear Power Plant was characterized by .

generally st.eady or improving results and showed a conservative and safe

operating philosophy.

The overall degree of management attention and

effectiveness was acceptable in all areas. However; regulatory compliance

problems indicated a need for increased emphasis in several functional areas~

Performance declined slightly in the area of Plant Operations. Several

unrelated shift management judgment errors occurred which were of some

rnnrPrn_

~nwPvPr_ ~trnnn nvPrall nPrfnrmanrP ann anmini~trativP nrnnram~

already in place,' combined with the actions taken to resolve the errors,

resulted in this area maintaining a Category 1 rating.

Radiologic~l Controls was again rated Category 2 *. Efforts to reduce personnel

dose.and personnel contaminations were commendable and. should be continued.

-However, some events and programmatic problems were not effectively handled,

indicating that increased management attention is warranted. The Safety

Assessment/Quality Verification functional area was again rated Category 2.

The Board noted generally good performance in the support of self-improvement.

initiatives, event assessments, and inter-department communication and

coordination. However, continued emphasis is warranted in management oversight

of quality and corrective action followup.

Improved performance was noted.in the areas of Emergency Preparedness and

Engineering/Techn.ical Support.

Each area was rated Category 2. These areas

were previously rated Category 2 with a declining trend.

In the area of

Emergency Preparedness, improvements in training and staffing were noted by

the Board.

In the area of Engineering/Technical Support, the Board noted t.hat

the system engineering pr.ogram continued to be a strength. However, continued

emphasis is needed to resolve environmental qualifi~ation (EQ) problems and to

properly implement a program for procurement and dedication of commercial-grade

parts for safety-related applications.

Continued superior performance was noted in the areas of Security and

Maintenance/Surveillance, resulting in each area maintaining a Catego~y 1

rating.

The performance ratings during the previous assessment period and this

assessment period according to functional areas are given below:

Functional Area

Plant Operations

Radiological Cont~ols

Maintenance/Surveillance

Emergency Preparedness

Security

Engineering/Technical

Support

Safety Assessment/Quality

Verification

Rating Last

Period

1

2

. 1

2 Declining

1

2 Declining

2

2

Rating This

Period

1

2

.1

2

1

2

2

-

III. PERFORMANCE ANALYSIS

A.

Plant Opeiatirins

1.

Analysis

Evaluation of this functional area was based on 11 routine inspections by

the resident inspectof'.s, 2 licensed operator requalification examinations

and 2 inspections (a fire protection inspection and a special inspection) by

regional inspectors.

Enforcement history declined from the previous assessment period. One Severity

Level III violation was issued for an inoperable contain~ent spray pump *.

Corrective actions were prompt, ~ffective, and addressed the underlying

programmatic problem which the licensee identified with the restoration of

certain circuit breakers after an outage. A Severity Level IV violation was

issued for not complying with an applicable Technical Specification (TS).

The.

safety ~ignificance was minor, the violation was not repetitive arid the

corrective actions were prompt and effective.

Several licensee event reports (LERs) were issued that, applied to this

functional area. A couple of these events were attributed to personnel errors

that had a minor effect -0n safety. Others documented the three "at power"

reactor t~ips (discussed below) and the Severity Level III vicilation discussed

above.

The operators properly analyzed and initiated the appropriate response to the

three plant trips.

In addition,.they promptly and completely reported the

events. * Component aging was a root cause for the first reactor trip when t,rip

modules in the reactor protection system malfL!nctioned, actuating thehigh

pres~ure logic for the primary coolant system.

The initiating e~ent for the

second reactor trip was a decrease in turbine generator seJl oil pressure.

During the subsequent rapid power reduction, the operators manually tripped the

reactor upon observing high water level in the steam generators. The third

  • reactor trip followed a feedwater pump trip. The root cause analysi~ identified

an original plant design ~roblem that permitted an oil to electrical interfacing

short, circuit. This appeared to be the most likely root cause of the L!nexplained

plant trips' discussed in previous assessment periods.

In general, transient response procedures were appropriate; however, certain

off normal and emergency_ procedures did not clearly indicate the entry and

exit points for the procedures.

When one of these problems was identified

during a training session, the proced~re was not immediately revised.

However, the operators s~bseq~ently acted appropriately during a transient.

The assessment period began_and ended with the plant in startup activities

f~om two planned outages. During these activities, strong administrative

programs were in effect to control activities for heatups, cooldowns, reduced

water inventory operations, shutdown, and startup. A work control program

called "system windows~ was used to optimize scheduling of shutdown~related

activities. Prerequisites for refueling activities were planned and established

during the day shift to minimize the burden to back shift personnel. Although

these activities were planned* in advance, a few shift management judgment

3

I

I

errors occurred. These* included one containment integrity problem, a 5-minute

loss of shutdown cooling, and thebreaker problem that resulted in the Severity

Level III violation. These events were of concern to the NRC.

The operations department developed an effective program to determine the

trends of key plant parameters. In finding many of these trends, *the

operations staff evaluated the *system response and developed an overall

integrated view of performance. These trends were accessible to personnel

throughout the entire plant, which provided an important communication link

to the operating shifts. Examples were trending programs for leakage from

the service water and comoonent coolina water svstems.

ThP Pnd re~ult w~~

improved s~stem integrity~

-

- *

-

.

Management's effectiveness in ensuring quality was demonstrated by a

conservative* and safety-oriented operating philosophy as shown by the examples

above.

In addition, when proposed revisions to the TS. were submitted with more

restrictive out-of-service time and reporting requirements, they were

administratively implemented. Administrative programs were also i~plemented to

balance preventive maintenance, corrective maintenance, and limiting condi~ions

for operations to maximize component reliability and minimize out-of-service

time during "at power" operation.

Corporate management visited the site regularly to a~sess a~tivities in the

control room and plant. Specifically, the Vice President of Nuclear Generation

performed monthly tours and the Chief Executive Officer performed quarterly

tours. Site managers remained cognizant of plant parameters by attending daily

meetings, making direct observations, and reviewing daily plant reports. Upper

and middle level plant managers were frequently observed in the control room*

and in the plant.

Management ensured the quality of the fire protection program by implementing

effective administrative controls for transient combustibles, by evaluating

the fire brigade, and by ensuring that the fire protection audits were

complete. Administrative controls for transient ~ombustibles were well written

and provided clear guidance to plant personnel. While performing fire drills,

the brigade demonstrated that it was well trained. Routine audits were

performed to ensure that equipment availability was maintained. Fire

protection problems from the previous assessment period did not reoccur.

Housekeeping and material condition in the auxiliary building were good.

Areas were well lighted; leaks of steam, water, or oil were minimized and

controlled; and the amount of contaminated area was small.

On the other

hand, housekeeping in the turbine building was inconsistent, varying at

times from good to.poor.

The approach to the resolution of technical issues from a safety standpoint

was routinely demonstrated by the conservative operating policy. Although not

required by TS, the plant was removed from service to correct a faulty level

indicator for a safety injection tank. The indicator did not directly affect

operability but indicated that an instrument problem may exist with the safety

injection tanks.

The turbine-driven auxiliary feedwater pump was conservatively

d~clared inoperable because the operators would not have had full response .

capability from the alternate steam supply line. This steam supply was not

4

required by the TS nor discussed in the final safety analysis report. The

operators demonstrated sensitivity to containment integrity when the back shift

operating crew, with su~port from ~ainte~ance and engineering personnel,

corrected a problem with minimum integrity risk.

Experience levels of managers and operations.personnel were excellent.

Staffing size was adequate.

Use of overtime during power operations and

outages was well managed.

The simulator was moved from a remote location to

the site~ Other simulator improvements included expanded computer capacity,

upgraded filming capabilities (used during student critiques), and instructor

control nanel enhan~ement~-

ThP trn;n;nn ftnn n11ftlifir~+inn nrnnr~mc woro

excelleni as evidenced by the 100 perceni pass 'rate f~r i~~ ~~~~~j{ii~;~ion

examination administered by the NRC.

2.

Performance Rating

Performance is rated Category 1 in this area. Performance was fated

Category 1 during the previous assessment period.

3.

Recommendations

None.

8.

Radiological Controls

1.

Analysis

Evaluation of this functional area was based on the results of routine resident

inspections and six inspections by regional inspectors.

Enforcement history declined somewhat during this assessment period. Five

violations (four Severity Level IV and one Severity Level V) were issued.

None

had major safety significance. Aspects of some violations are discussed below.

A single reportable event occurred which was assigned to this functional area,

relating to the circumstances involved in one of the violations.

Management's effectiveness in ensuring quality was mixed.

Management failed

to evaluate the safety significance of a change made in the processing and

storage of radioactive waste.

When discovered, a review led to the

identification of three similar failures* in earlier years.

On occasion,

management failed to ensure that various deficiencies were reported, adequately

evaluated, and corrective measures taken in a timely manner.

For example, a

hot particle exposure event was not reported in the plant's corr~ctive action

system, a comprehensive evaluation was not performed, and the corrective.action

was found to be inadequate. There was one instance of a transportation program

problem when a shipment of radioactive material left the plant with a leaking

package. Although this event had minimal safety significance, it created

public and ~ongressional concern that would have been avoided with proper

control over the activity. Evaluation found a programmatic weakness relating

to paperwork not providing drivers with an emergency point of contact.

5

[xamples of good management performance were the continued progress in

implementing the corrective actions from the health physics self-assessment,

strong support of the water quality program by installing new steam generator

blowdown demineralizers, and the significant upgrades of secondary plant

equipment which yielded much improved plant water qualjty. Managers also

significantly improved their support of ALARA (as-low as reasonably achievable)

philosophy by including ALARA criteria in the performance evaluations for

individuals and managers and broader support for ALARA ColTBTlittee efforts.

Progress was made to better integrate ALARA activities into all the plant

organizations, which was a problem area noted in the previous assessment period.

An effective. diverse source term reduction oroaram was continued. Audits were

generally accurate in assessing perf~rmance.

The approach to identifying and resolvin~ issues from a safety perspective was

good.

Good performance was noted with the effluents programs and radioactive

waste reduction. Improvements were noted in the use of electronic dosimetry,

ALARA planning, and records maintenance.

Health physics, ALARA, and chemistry

.organi~ations actively participated in daily, pre-outag~, and outage planning

meetings. Performance in nonradiological chemistry comparisons between the

licensee and the NRC was improved with all agreements in 26 comparisons.

Radiological confirmatory measurements results were also excellent with all

agreements in 49 comparisons.

The radiological env.ironmental monitoring

program was well implemented and equipment was well maintained.

On the.other

hand, the nonradiological environmental program did not adequately reflect

applicable TS. -There were some examples in which efforts reflecting

performance in the identification and resolution of issues from a safety

perspective were somewhat narrowly focused. These included problems with

radioactive source control and timely.communicati9n of radiological survey

information.

Performance in controlling personnel contaminations was good, even though the

licensee's goal -for the 1992 refueling outage was not met.

The total amounts

of personnel exposure reflected improving performance.

Exposure for the early

part of the period was expectedly higher because of the Steam Generator

Replacement Project (SGRP).

ALARA efforts have matured significantly over

this assessment period with good performance in this area.

-

Staffing levels and qualifications of the radiation protection, radwaste

management, and chemistry programs were good.

Verification of contract

radiation protection technician experience and qualifications improved markedly

during this assessment period. The training programs were effective~ The

staff was appropriately trained and qualified to perform assigned duties.

2.

Performance Rating

Perforinance is rated Category 2 in this_ area. Performance was rated Category

2 during the previous assessment period.

3.

Recommendations

None.

6

C. *Maintenance/Surveillance

1.

Analysis

Evaluation of this functional area was based on the results of 10 routine

inspections by the resident inspectors, a special inspection performed by

headquarters inspectors and 3 inspections performed by regional inspectors.

Enforcement history was excellent. There was one Severity Level IV violation *.

The safety significance was minor and the violation was not programmatic or

r~n~titivi:o_

There were several LERs applicable to this functional area, comparable in

frequency to the previous assessment period.

One pertained to an inadequate

surveillance procedure that caused a reactor trip signal during cold shutdown

conditions. Another discussed an inadequate work instruction that.resulted in

an inadvertent left-chann~l containment isolation. Both events resulted from

the use of plant schematics that did not reflect the correct system configuration~

Plant ~ocument accuracy issues are being actively pursued by th~ Configuration

Control Project. The other events did not indi~ate repetitive, generic, or

programmatic problems.

None of the events had major safety significance.

The survei 11 ance program was successfully managed and implemented, with tests

routinely completed on time.

The extension of surveillance intervals to permit

use of the "grace period" was minimized by appropriate management controls.

Surveillance procedures were controlled, revised, and maintained by the plant

organization most knowledgeable and responsible for the equipment.

Eac~

procedure had a supporting basis document that explained the assumptions,

defined the calculations, and amplified the justification for the acceptance

criteria.

-

Plant personnel consistently used the procedures at the job site, and discussed

unexpected equipment responses with plant management.

Problems were

appropriately resolved in the corrective action program. Several problems

were encountered when infrequently performed test procedures were used during

outage startup activities. This resulted in a number of events reportable

under 10 CFR 50.72. *These problems did not result in safety problems or

inoperable equipment; however, they indicated that the challenge of

infrequently performed tests observed early in the period had not been

resolved. A special review group was formed to evaluate this challenge

and its evaluations were still in progress at the end of the period.

The post-maintenance test program was good with responsibility assigned to the

appropr1ate maintenance superintendent and system *engineer to determine the

appropriate post-maintenance test. Operations personnel ensured that the

tests were properly authorized, performed, reviewed, and documented before

returning the equipment to service. However, a maintenance personnel error

resulted in a loss of shutdown cooling for approximately 5 minutes.

The predictive maintenance program effectively used vibration monitoring,

lube oil analysis and infrared thermography to trend equipment performance.

Examples included the identification of an impending service water pump bearing

.7

failure, a resonant frequency problem on a service water pump, and alignment

problems between.the pump and motor which resulted in improved alignment

techniques.

Management effectiveness in ensuring quality remained a strength. Personnel

were effectively utilized for planning *and scheduling of. work activities,

including arranging for pre-staging of parts, and routine visits t~ the job

site by supervisors. A violation assigned to the Safety Assessment/Quality .

Verification functional area, however, documented a problem with the control

of vendor manuals when planning and performing work *. This did not result

in inoperable equipment but did identify that personnel did not appreciate the

administrative program for control of vendor manuals. A computerized work

order system permitted easy reference to historical information. The value of

, detailed work order summaries was observed as indicated by the presence and use

of previous work order.summaries at the job site.

There were two planned outages performed during this p~riod: Outage

. management maintained the global overview required to ensure the safety of the

plant.and safety of personnel involved in various activities. The outages were

weJl planned and used a 24-hour rotating shift manager position to ensure that

proper attention was directed to the outage work path and that new work was

properly evaluated .and categorized. For example, multi-disciplinary work

groups were established to recover a fuel bundle which became stuck to the

upper.guide structure, and a dropped fuel pin in the spent fuel pool.

The approach to the identification and resolution of technical issues with a

view to safety remained strong. Maintenance activities were closely followed*

by both the system engineer and first line supervjsor. Examples included.

repairs to a feedwater heater d~ain valve, noise within the governor 6f a .

feedwater pump turbine, and turbine generator lube oil problems.

Each day,

upper level managers were informed of current work.

Meetings included

discussion of problems encountered and usually resulted in prompt evaluation

and effective resdlutions as discussed above ..

The.work order backlog was routinely evaluated and managed by a program that

considered available person-hours and crew size. Additional, non-site

resources were available to control backlog size, resulting in a well managed

backlog. At the beginning of 1992, only 90 non-outage work requests wereover

12 weeks old, indicating that maintenance was timely and long-standing

equipment problems were mini~ized. Work orders scheduled to be completed

during the outages required senior management approval to be deferred, and the

nu~ber actually deferred was minimal (approximately 2 percent of the 1992

. refueling outage work orders).

The maintenance program had a defined policy for finding, evaluating, and

implementing corrective action for repeat maintenance.

The computerized work

order program and database were useful for evaluating equipment history.

Preventive maintenance programs were effective as evidenced' by the equipment

availability and the material condition of the pl ant. A valve improvement

program implemented during a previous assessment period proved beneficial

as indicated. by the absence of containment boundary valve failures during local

leak rate testing.

.8

Staffing in this functional area continued to be a strength. This was

  • attributed to the low turnover rate of both.workers and supervisors. Programs.

remained in place to provide temporary upgrades of maintenance. workers to staff

positions for use as planners.

In *addition, support engineers continued to be

rotated into licensing classes. Rotations wefe controlled arid did not affect

  • quality; rather, quality was enhanced by improved communication and

coordinatfon between wotk groups~ *

2.

Performance Rating

during the previous assessment period.

3.

Recommendations

None.

D.

Emergency Preparedness

1.

Analysis

Evaluation of this functional area was based on the r~sults of two inspectio~s.

Enforcement history was excellent with. no violations identified.

No

reportable events occufred which were assigned to this functional area.

Management's effectiveness in ensuring qualitj~as good.

Corrective actions

to eliminate training program inadequacies, identified at the end of the

previous assessment period, became effective in mid~l991. The emergency

.

preparedness coordiriato.r (EPC) position became a full-time assignment late iii

the period~ Emergency resp.onse facilities were good and *well maintained, with

. several .equipment upgrades either complete or nearly complete.

Working

relationships with State and county officials were very good.

.

.

The identification and resolution of technical issues with a view to safety

generally remained good.

Actual emergency plan activations were *correct and

timely, including making the conservative unusual event declaration in February

1992 upon experiencing a fuel handling problem.* Response to thi$ problem

included a partial activation of the technical support center (TSC) by management,

  • health physics, and communications personnel. State, county, and NRC officials

were notified of actual emergency decl~rations in an accurate and timely

manner.

The licensee thoroughly evaluated its records associated with actual

emergency declJrations.

In contrast, during followup of an NRC~jdentified

issue in 1991', the licensee identified a significant limitation in the

telecomputers used to notify *1ts emergency response organization (ERO) during

off hours.

Efforts remained in progress at the end of the assessment period to

overcome this equipment limitation, so that th~re would be reasonable assurance

that *onshift personnel would be sufficiently augmented in a timely manner

during off hours.

Overall performance during the 1991 exercise was good, with improvements

evident within the emergency operations facility. All emergency clas~ification

decisions and associated offsit~ notifications were correct and timely.

9

Although performance improved during the 1991 exercise, a previously noted

problem relating to the coordination and tracking of inplant teams by supervisors

in the control room and several response facilities had not been corrected.

Corrective actions were incomplete at the end of the assessment period. The

effectiveness of completed or planned ch-anges to the layout, equipment, staffing,

and procedures of response facilities has not been demonstrated during an

exercise.

The EP groups from the plant and the corporate office were adequately staffed

by well qualified persons. Late in the assessment period, the EPC was relieved

ur ~~~ ca11~t~~~~ ~~~~:: :: t~:i~~~; ~==~1i~~t~~. ~~i~h h~rl rnn~um~d about

30 percent of his time. This allowed him to dedicate his efforts full time to

_the EP area.

The EPC was supported by two part-time assistants, a part-time

training instructor, and several corporate personnel. The ERO's staffing

level improved and is now very good to ensure 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> staffing capability for

key and support positions with currently qualified personnel.

The-EP training program improved and became well organized during the

assessment period.

In response to violations identified during the previous

period, administrative controls and practices were established by the EPC a*nd

training department staff to ensure that only currently trained personnel were

on the ERO's call out list. The maintenance and overall quality of EP lesson

plans improved and was very good.

All required drills were conducted and

critiqued *.

2.

Performance Rating

Performance is rated Category 2 in this area. Performance was rated Category 2

with a declining trend during the previous assessment period.

3.

Recommendations

None.

E.

Security

1.

Analysis

Evaluation of this functional area was based on the results of two inspections

and routine resident inspector observations.

Enforcement tiistory improved and was excellent; no violations were identified.

Management's effectiveness in ensuring the qua1ity of the security program

remained excellent. Senior managers supported security initiatives by

encouraging the contract security supervisors to attend licensee-sponsored

management development classes. Management's dedication to improving security

was demonstrated through the continued reduction in personnel errors and

improved implementation by plant personnel of security requirements.

The

managers maintained good oversight of the daily implementation of the program.

The approach to the identification and resolution of technical issues was

excellent.

One initiative-involved appointment of an operations liaison to

10

work with the security department in identifying pertinent information on -

protecting vital equipment to improve tactical response capabilities.

Management also began program planning for replacing the card reader and

computer portion of the access control system.

-

Security staffing was good.

The experience level of the guard force was high-

as a result of low turnover. - A close and effective liaison existed between

local law enforcement agencies and licensee security managers. During this

assessment period, the security managers continued to routinely keep both

resident inspectors and regional personnel fully informed of site security

issues. Security operational events were orooerlv identified~ analvzed. and

documented. Security-related records and logs were complete, well maintained,

and readily retrievable.- A timely program was implemented to heighten security

awareness during the Persian Gulf conflict.

The training and qualification program for the_ security force was good.

In the

middle ~art of the assessment period, an outside contractor with tactical training

expertise was hired. This action helped correct the weakness identified in the

previous period regarding the need for additional and more effective tactical

response training. Security personnel were competent in executing their

duties.

2.

Pe~formarice Rating

Performance is rated Category 1 in this area~ Performance w~s rated

Category- 1 during the previous assessment period.

3.

Recommendations -

None.

F.

Engineering/Technical Support

1.

Analysis

Evaluation of this functional area was based on the results of 14 routine

inspections, an electrical distribution system functional inspection (EDSFI),

a modified operational safety team inspection (OSTI-) ,_ 3 operator 1 icensing

examinations, and interactio-ns among the licensee and NRR staffs.

Enforcement history was weak.

One Severity Level III violation was issued for

a programmatic breakdown in the area of piping and pipe support design.

However, much of the inspection jnformation which resulted in this violation

was discussed in the previous SALP.

This violation was similar in nature to

the Level III violation issued in the previous assessment period. Subsequent

corrective actions and root cause evaluations were adequate and appeared to

be comprehensive.

Two Severity Level IV violations were also issued.

One

of these was in electrical design control, for which a design change in 1986

was not implemented *. The other violation was in the area of corrective action.

This was the second time within the last three SALP periods that the licensee

had failed to take the corrective action .stated in its response to a previously

'issued Notice of Violation.

11

.

-

Several LERs were attributed to this functional area. Approximately half of

the LERs discussed failure to meet EQ commitments associated with Regulatory

Guide (RG) 1.97. Many of these resulted from the licensee's review of the .*.

contractor report discussed below.

The remaining. LERs were issued for

inadequate design controls. Most of the LERs were th~ result of activities in

previous assessment periods.

Management effectiveness in ensuring quality remained mixed.

On the positive

side, the system engineering program, established in the mid-1980s, was well

implemented *. System engineers were involved in the daily operation and

performance of assiQned systems and supported olant maintenance in identifyino

trends in system performance, identifying equipment problems, and planning

maintenance activities. The configuration control project continued to make

good progress. For example, several original plant electric design

deficiencies were identified. Relocation of corporate engineering resources

to the site significantly improved engineering support o~ the plant.

The EDSFI found design develop~ent and implementation for the electric~l

distribution* system were satisfactory. For the most part, design attributes

were retrievable and verifiable, although some modification documentation, such

as for the unbolted diesel silencers, was not retrievable. Engineering

calculations were technically sound, although some nonconservative assumptions

were identified in cable sizing and design calculations. Most of these

problems were associated with initial design.

Improvement in design control

was noted for recent design activities. This had been an area of concern

during the previou~ assessment.

Management's effectiveness in the area of operator requalification and initial

operator examinations improved from the previous assessment period partly a.s a

result of the additional personnel assigned to the training staff. The

  • relocation of the training simulator to the plant training building had a

positive impact due to increased accessibility.

On the negative side, management's effectiveness in controlling the EQ program

was poor. Although the licensee hired a contractor to study the EQ program,

it did not provide sufficient staff and attention to review the problems

  • identified in a report by the contractor and to take corrective action. A

detailed review of the report was not completed until a year after it was

received. Similarly, management involvement and control of the RG 1.97 program

was not effective. Program requirements were not completed and commitments

made in response t6 a Notice of Violation were not performed. Managers ~lso

failed to apply the necessary attention and resources in the program for

procuring and dedicating commercial grade components for safety-related

applications. Finally, weaknesses were identified by the EDSFI team in

post-modification testing.

The approach to the identification and resolution of technical issues from a

safety standpoint was mixed.

On the positive side, system engineers prepared

-quarterly system performance monitoring reports on all systems in which

selected system performance indicators were trended.

The reports identified

adverse component trends and were an effective predictive maintenance tool.

The system engineers also routinely demonstrated a conservative approach in

12

r~solving problems.

Examples included the handling of a problem with the

alternate steam supply valve for the turbine-driven auxiliary feedwater pump,

the response to reactor trips initiat~d by a loss of feedwater due to a short

circuit caused by oil leaking in a control cabinet for the main feedwater

. pumps, and the use of vibration analysis beyond normal- inservice testing

requirements to diagnose serv,ice water pump problems. Root cause analyses were

routinely performed by engineers following acceptable guidelines. Corrective

actions to resolve.significant problems identified in the configuration control

and design bases review programs continued to be well prioritized.

On the

. negative side, deficiencies associated with design work performed for the SGRP

were not resolved in a timel.Y manner because manaaement failed to rPr.noni7i:o

their significance. Resolution of these deficiencies was only underta~en

after lengthy discussions with the NRC and a second inspection of the area

during this assessment period confirmed the previous findings.

The licensee

identified significant problems when it performed a re-analysis to address

these deficiencies.

One finding resulted in having to.re-modify the main -

steam system.

Engineering and technical support staffing was sufficient in siie to adequately

address most technical issues. The system engineers were experienced and well

motivated.

In response to concerns identified in the previous assessment

period, a design ehgineering reorganization took place which elevated the

position of Manager of Nuclear Engineering to report directly to the Vice

Presiderit of Nuclear GeneratiOn.

The design change program was strengthened*

considerably by relocating corporate engineers to the site, resulting in a

sense of "own~rship" for the design of specific projects. The engineers who

performed design ba~is*documentation (DBD) developm~nt and safety system design

configuration (SSDC) activities were knowledgeable in system design and

operations. The staffing problems in the training department, identified

during the last assessment period, were corrected. The EQ program was

understaffed and due to the high turnover experienced over the years, the

engineers wer~ wotking mainly on their backlog rather than dealing ~ith

emerging issues.

The effectiveness of the initial operator and requalification program was

excellent as evidenced by the 100 percent passing rate during the assessment

period. A formal training program existed for system engineers and included

root cauie analysis.

2.

Performance Rating

Performance is rated Category 2 in this area. Performance was rated

Category 2 with a declining trend during the previous assessment period.

3.

Recommendations

None.

G.

Safety Assessment/Quality Verification

1.

Analysis

Evaluation of this functional area was based on the results of routine

inspections by resident, regional, and NRR inspectors and special team

13

inspections.

In addition, requests for amendments, exemptions or relief,

responses to NRC generic communications, and other interactions with the NRC

staff were considered.

During this assessment period four Severity Level IV v.iolations were issued.

The violations covered a variety of areas, and were neither*programnatic nor

repet~tive. In addition, enforce~ent action was pending at the conclusion of

the assessment period for a significant failure of the corrective action

program, relating to EQ problems recently identified, but which occurred in

previous periods.

une LER was attributed to this functional area. A TS change was approved and

implemented without a .full understanding of the programmatic changes caused by

the revised TS.

Although this was an isolated event, it indicated a weakn~ss in

the process for reviewing TS changes. Additionally, two LERs (assigned

to other functional areas) indicated that proper onsit~ revie~s of

documentation provided by offsite organizations were not conduC:ted.

The LERs

submitted during this assessment period were,* in general~ clearly written a.nd.

comprehensive.

Management involvement and control to ensure quality were generally good.

Site-wide

11teamwork

11 and good interdepartment convnunications were generally

evident.

Manager~ continued to support various self-improvement initiatives,

several 'of which began during the previous assessment period and are scheduled

to continue into the next period. These initiatives included the configuration

control project and critical self assessments, such as the independent EQ

evaluation, to help corporate and plant management improve work activities.

When items were entered into the formal corrective action program, the program

provided a timelj classification and proper segregation of items for review by

the appropriate plant and corporate managers.

The staff and managers

discussed, clearly defined, and documented courses of action.

The initial

screening process, however, did not always prompt a retrospective operability

review~ This was the case in the containment spray pump inoperability issue

which prompted the NRC to take escalated enforcement action.

However,

adequate operability reviews have been performed in recent situations arising

from the corrective action program.

Responsibility for re.solution of corrective action documents was assigned to

specific indi~iduals. This established accountability and ownership. Most

corrective actions demonstrated sufficient evaluations of the problem and

associated system, and usually addressed the root causes. The plant licensing

dep~rtment tracked corrective action documents.which ensured timeliness and

minimized overdue actions~

Management follow-up of corrective actions in several areas, however, was

considered poor.

As indicated in the Engineering/Technical Support section,

corrective actions were not always adequate or timely for EQ, design work for

the SGRP, and DBD discrepancies related to cable routing problems.

The hiring

of a contractor to perform twQ EQ assessments was considered a very positive

action. Although one assessment report was adequately evaluated upon receipt,

the initial review for the second report was not sufficiently comprehensive to

14

ensure that items having potential impact on operability were promptly

addressed.

Upon a more comprehensive review of the second report, the licensee

determined (among other things) that the main steam isolation valves could be

rendered inoperable by a steam line break outside containment. The cause of

the delayed review appears to be either a 'lack of deta-iled knowledge about EQ

requirements on the part of the reviewer, or excessive workloads associated

with the steam generator replacement project. Additionally, no formal tracking

of the contractor report was performed to ensure management's awareness of the

report and timely completion of the detailed review.

Management strenQthened its support and overview of the confiQuratioh control

project. The categorization and closing of findings from DBD development and

SSDC activities were timely and effective. The DBD Writer's Guide, although

modified to adequately cover technical areas and.provide sufficient

instruction, was not used to update relevant design, operation, maintenance,

and regulatory documents.

Activities in this functional area reflected, in general, a proper emphasis

on safety in resolving technical issues. Initiatives were proactive in .

identifying deficiencies in design control and operations. The audit program,

independent design reviews, and configuration control project identified

problems and specified appropriate corrective actions for many deficiencies in

the plant electrical system.

On the negative side, although the plant had a

history of EQ problems, only one quality assurance audit had been performed in

this area since 1985. This audit, conducted in March 1991, was very limited in

scope.

During this assessment period, three plant events.highlighted the licens~e*s

strengths and weaknesses in clearly and concisely _communicating with the NR~ *.

The first pertained to a temporary waiver of compliance (TWOC) for unqualified

main steam isolation valve control citcuits. The second pertained to a fuel

bundle that stuck to the bottom of the upper guide structure when it was lifted

for defueling. For these two events, the oral communications demonstrated a

thorough understanding of the problem and accurately conveyed that the licensee

was properly managing the situations. Also, the written documentation

demonstrated a*comprehensive working knowledge of the NRC TWOC administrative

procedure.

The third event pertained to a configuration control project finding relating

to inconsistencies in cable routing drawings and data.

In contrast to the

other two events, information presented to the NRC during various conference

calls was not always consistent. These communication difficulties contributed

to the impression that cable routi11g inconsistencies were *not aggressively

pursued.

A new director of safety an~ licensing was assigned during this assessment

period. The new director brought a valuable knowledge of probabilistic risk

assessment, which was incorporated when evaluating items to determine

appropriate corrective actions and to determine the schedule for implementation.

For example, it was determined that a fast transfer circuit problem existed for

the emergency diesel generators. The licensee properly evaluated the problem

and initiated discussion with the NRC to effect a resolution.

In addition,

relocafion of the licensing staff to the site improved communications, both

internally and externally.

15

I I

The onsite Plant Review Committee (PRC)' was properly staffed and functioned*

well. A subcommittee was established to manage the workload of the PRC and

determine which issues require formal co11111ittee review.

The 10 CFR 50.59 *

  • evaluations were generally well documented and comprehensive.

Most licensing submittals were of good quality and showed improvement over

the previous assessment period.* The licensee routinely demonstrated that it

properly understood technical issues and that ma~agement effectiveness was

good.

However, a number of submittals did not provide sufficient information,

or required revision prior to final acceptance by the NRC staff. This was

discussed with the licensee midway through the assessment period, and

Noteworthy responses were made on two significant licensing issues.

The first

issue involved an unreviewed safety question relating to the potential for

radioactive water inleakage into the safety injection and refueling water tank

following a loss of. cool ant accident *. Pl ant management ident_ified this concern

and initiated discussion with the *NRC staff.

An Information Notice was

subsequently issued by the NRC staff to all pressurized water reactor licensees.

The second issue related to the generic issue of reactor vessel pressurized*

thermal shock. Although initially slow in aggressively pursuing this issue,

the licensee formed an effective plant task force, with excellent management

guidance and oversight~ later in the assessment period.

The task force

compiled and evaluated a large data base of information on the reactor vessel *.

Ma,nagers expertly responded to NRC staff technical questions during several

meetings and in follow-up correspondence.

2.

Performance Rating *

Performance is rated Category 2 in this area. Performance was rated Catego*ry 2

during the previous assessment period.

3~

Recommen.dations

  • None.

IV.

SUPPORTING DATA AND SUMMARIES

A.

  • Major Licensee Activities

Significant outages and events are described below~

The unit began the period in a refueling and steam generator replacement

outage that ended on March 10, 1991~

On March 24, 1991, the unit was shut down to repair a failed level float

switch for a safety injection tank.

The unit was returned to service on

March 25, 1991.

On July 3, 1991, the unit tripped because of a failure of two relays in the

reactor prot~ction system *. The uriit was returned to service on July 8, 1991.

16

On July 12, 1991, the unit tripped because of a loss of a main feedwater

pump.

The unit was returned to service on July 13, 1991.

On December 9, 1991, the unit tripped during an emergency power reduction

necessitated by a turbine-generator seal oil system failure.

The unit was

returned to service on December 15, 1991.

On. February 6, 1992, the unit was removed from service for a refueling and

maintenance outage.

B.

Major Insp~ction Activities

1.

Inspection Data

The inspection reports discussed in the SALP are listed below:

Docket No. 50-255

Inspection Reports: 90025, 90039, 91002 through 91024, 91026, 91201, 91202,

and 92002 through 92011.

2.

Special Inspection Summary

a.

From September 19, 1990, through April 18, 1991, the NRC conducted an

engineering team inspection (IR 90025).

b.

From June 10 through 21, 1991, the NRC conducted an engineering and

design control inspection (IR 91202).

c.

From September 10 through 20, 1991, the NRC conducted a special safety

inspection (IR 91017).

d.

From November 4 through December 13, 1991, the NRC conducted an

electrical distribution system functional inspection (IR 91019).

e.

From January 6 through 10, 1992, the NRC conducted a modified operational

safety team inspection (IR 92003).

17

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I