ML18057A787

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SALP 10 Rept 50-255/91-01 for Sept 1989 - Dec 1990
ML18057A787
Person / Time
Site: Palisades Entergy icon.png
Issue date: 03/07/1991
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18057A786 List:
References
50-255-91-01, 50-255-91-1, NUDOCS 9103180049
Download: ML18057A787 (22)


See also: IR 05000255/1991001

Text

INITIAL SALP REPORT

REGION III

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

Inspection Report No. 50-255/91001

Consumers Power Company

Palisades

September 1, 1989 through December 31, 1990

049 91fl307

CJ103180

. 05000255

PDR

ADOCK

PDR

Q

SALP 10

TABLE OF CONTENTS

Page No.

I.

INTRODUCTION ....................... *. . . . . . . . . . . . . . . . . . . .

1

II.

SUMMARY OF RESULTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .. . . . . .

2

Overview . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

2

III. PERFORMANCE ANALYSIS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

3

A.

Pl ant Ope rat i ans ................................. .

B.

Radiological Controls ............................ .

C.

Maintenance/Surveillance ......................... .

D.

Emergency Preparedness ........................... .

E.

Security ......................................... .

F.

Engineering/Technical Support .................... .

G.

Safety Assessment/Quality Verification ........... .

3 - 5

5 - 8

8 -

10

10 - 11

12 - 13

13 - 16

16 - 18

IV.

SUPPORTING DATA AND SUMMARIES ..........................

18

A.

Licensee Activities .............................. .

B.

Inspection Activities ............................ .

C.

Escalated Enforcement Actions ..................... .

  • D.

Confirmatory Action Letters (CALs) ................ .

E.

Licensee Event Reports ............................ .

18 - 19

19 - 20

20

20

20

I.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) program is an integrated

NRC staff effort to collect available observations and.data on a periodic basis

and to evaluate licensee performance on the basis of this information.

The

program is supplemental to normal regulatory processes used to ensure compliance

with NRC rules and regulations. It is intended to be sufficiently diagnostic

to provide a rational basis for allocating NRC resources and to provide

meaningful feedback to the licensee

1 s management regarding the NRC 1 s assessment

of the facility 1s performance in each functional area.

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February 13 and 21, and on March 4, 1991, to review the observations and

data on performance, and to assess licensee performance in accordance with

the guidance in NRC Manual Chapter 0516,

11Systematic Assessment of Licensee

Performance.

11

This report is the NRC 1s assessment of the licensee 1 s safety performance at

Palisades for the period September 1, 1989, through December 31, 1990.

The SALP Board for Palisades was composed of the following individuals:

Board Chairman

T. 0. Martin, Director, Division of Reactor Safety

Board Members

H. J. Miller, Director, Division of Reactor Projects

W. L. Axelson, Deputy Director, Division of Radiation Safety and

Safeguards

L. B. Marsh, Director, Project Directorate III-1

H. B. Clayton, Chief, Projects Branch 2

B. E. Holian, Licensing Project Manager

J. K. Heller, Senior Resident Inspector

Other Attendees at the SALP Board Meeting

A. B. Davis, Regional Administrator

W. G. Snell, Chief, Radiological Controls and Emergency Preparedness

Section

D. H. *Danielson, Chief, Materials and Processes Section

B. L. Jorgensen, Chief, Projects Section 2A

E. R. Schweibinz, Senior Project Engineer

C. F. Gill, Senior Reactor Programs Specialist

J. A. Gavula, Reactor Inspector

J. R. Kniceley, Security Specialist

A. W. Markley, Radiation Protection Specialist

D. M. Barss, Emergency Planning Specialist

T. J. Kozak, Radiation Specialist

R. L. Bywater, Jr., Reactor Engineer

II.

SUMMARY OF RESULTS

Overview

The liceniee 1 s overall performance level during this assessment period was

acceptable in all areas.

The degree of management attention and effectiveness

ranged from commendable in some areas to needing attention in others. Overall,

the conduct of activities was appropriately directed to assurance of safety.

Management appeared proactive and effective in demonstrating a conservative

operat~ng phil~sophy an~ esta~~~shing hi~h standards ~f ~erforman~e in

opera"t;1ons, ma1n"t;enam:;e1surve111anc;e, anu sec;ur1"t;y.

r-er1un11a11c;e 11111.a*uveu i;.u

C1

Category 1 level in the former two areas. While some significant problems were

identified by the licensee with its fitness-for-duty program, performance in

the security area was strong enough overall to maintain a Category 1 rating.

Declining performance was noted in areas of emergency preparedness and

engineering/technical support.

Emergency preparedness was downgraded from

a Category 1 to a Category 2 with a declining trend.

Significant among the

weaknesses identified in this area was the failure of the licensee to ensure

that trained individuals were available to fill critical emergency preparedness

positions.

Engineering/technical support was rated a Category 2 as it was last

assessment period but with a declining trend. Significant weaknesses were

noted in design control and technical oversight of contractors.

Some strengths

were noted in engineering activities in support of maintenance.

However,

increased management attention is suggested in the engineering/technical

support functional area, especially since design control problems were identified

in the last assessment period and licensee actions to address these were not

fully effective.

Strong involvement in radiation protection for the steam generator replacement

project was observed.

It is suggested that lessons learned from the replacement

project be reviewed for incorporation in the routine radiation protection

program.

Material and personnel resources were generally adequate in all areas.

The performance ratings during the previous assessment period and

this assessment period according to functional areas are given below:

Functional Area

Plant Operations

Radiological Controls

Maintenance/Surveillance

Emergency Preparedness

Security

Engineering/Technical Support

Safety Assessment/Quality

Verification

Rating Last

Period

2 Improving

2

2 Improving

1

1

2

2

2

Rating This

  • Period

1

2

1

2 Declining

1

2 Declining

2

III. PERFORMANCE ANALYSIS

A.

Operations

1.

Ana,Ysis

Evaluation of this functional area was primarily based on the results of 11

routine inspections by the resident inspector. A total of 1,323 inspection

hours were expended in this functional area, comprising 20.4 percent of the

total inspection hours.

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high standard established during the previous assessment period.

Inspectors

identified one Severity Level V violation for failure to maintain control of

flammable liquids. Its safety significance was minor, it did not indicate a

programmatic breakdown, and no similar violation was identified during the

previous assessment period.

Several licensee event reports (LERs) issued during this assessment period were

applicable to this functional area. A few LERs were attributed to various

personnel errors, but the effect of these errors on safety was minimal.

The

other LERs documented power reactor trips. One was a manual trip following a

main feedwater pump trip and the other was a variable high power trip during a

transient initiated by a main feedwater pump trip.

The operators' response to the two reactor trips and to the significant

depressurization event demonstrated their ability to respond to.plant transients.

Operators manually initiated the first trip (a conservative action) after the

operating main feedwater pump tripped.

For the second trip, the operators

properly responded to the initiating event (loss of a main feedwater pump) by

rapidly reducing plant power to a level at which sufficient steam generator

feedwater could be supplied by the operating pump.

Following the power

reduction, the increase of feedwater resulted in a power rebound to a variable

power trip setting.

The operators could have manually reset the trip setting,

but appropriately chose not to, because conditions were_still transient.

Because of preparations to replace the steam generators and the beginning of

the replacement outage, the unit was cycled for three preplanned outages.

Each of these shutdowns and startups was performed without incident.

Handling

the heatups and cooldowns also demonstrated evidence of consis~ent planning and

assignment of priorities. The department's procedures for conduct of activities

were well stated, controlled, and explicit.

In addition to the two reactor

trips previously discussed, other transients included the failure of a.

pressurizer heater transformer that de-energized half of the pressurizer

heaters, a trip of all cooling tower fans, an actuation of a main steam

atmospheric relief valve, and a number of minor transients.

Loss of the

pressurizer heater transformer placed the plant in a limiting condition for

operation (LCO) that required a shutdown.

The licensee's conservative operating

policy resulted in a controlled shutdown well within the LCO time limit.

Appropriate planning of the repairs revealed that they could not be completed

without exceeding the LCO time limit for cold shutdown.

This planning was

instrumental in establishing early communication with the NRC to permit use of

the temporary waiver of compliance policy and prevented an unnecessary

3

temperature transient on the plant.

Proper onshift response to the cooling

tower transient resulted in a controlled power reduction and reestablishing

cooling tower operation before a plant trip occurred.

During past assessment

periods, a cooling tower trip resulted in a reactor trip. Actuation of a main

steam atmospheric relief valve had been an occasional problem under certain

plant conditions during a startup.

During this period, a startup was halted to

permit trouble shooting and root-cause analysis.

Management involvement and control of quality consistent.ly demonstrated a

conservative and safety-oriented operating philosophy as noted in the previous

examples.

Licensee control during plant manipulations was routinely demonstrated

wit.ii usua11y exce11ent, result.s.

1ne t'1ant. iyianay~r duu uµ~rdl;,iuu~ i*idudy~r

routinely visited the control room during normal and off-normal plant operation.

In addition, the Operations Superintendent relocated his office to the control

room complex and was routinely observed in the control room during all phases

of plant operation.

Operations management i nvo*l vement and control in ensuring quality were

acceptable, as shown by the active role that was taken during administration of

requalification examinations.

Operations management personnel, who were part

of the examination team, provided valuable technical expertise and clear

expectations for operator performance.

Corporate managers routinely visited the site to provide direct assessment of

control room and plant activities.

The Vice Presidents (Nuclear and Special

Projects) both performed weekly plant tours.

The Chief Executive Officer and

Senior Vice President conducted tours of the site at least quarterly.

Licensee

managers (both plant and corporate) kept cognizant of plant parameters by

attending daily meetings (morning and afternoon), directly observing activities,

  • and reviewing daily plant reports and monthly trend graphs.

The licensee's approach to resolving potential safety issues was routinely

demonstrated by the gains made in plant material condition. Painting and floor

recoating projects were nearly complete.

The coating improved postmaintenance

cleanup activities and decontamination efforts.

However, one drawback to the

coating is that the color and gloss have a tendency to hide potentially

contaminated wet spots.

During the previous assessment period, inspectors

noted a weakness involving containment cleanliness following outages.

The

licensee established a chain of responsibility for cleanup and postoutage

inspection.

These actions resulted in continuing improvement in the postoutage

cleanliness of the containment.

The fire protection program was challenged at the start of the steam generator

replacement outage.

Several minor fires occurred early in the outage due to

improper control of work.

The licensee recognized that these fires could be a

precursor to more serious fires because of the scope of the outage and the size

of the contractor work force.

Measures implemented were re-education of work

force, re-evaluation of procedures, use of stop work orders, and assignment of

fire protection specialists to provide 24-hour coverage.

The Operations Department had a strong program for tracking and analyzing

various plant parameters for determining trends and for implementing early

corrective action.

For example, trends for safety injection tank levels

4

revealed the need for corrective maintenance and the need to increase the

sampling frequency to prevent a tank being rendered inoperable as a result of

its low concentration or level. Another example involved leakage of chargi~g

pump seals and the ability to predict degraded seals.

Thus, repairs for these

seals were scheduled on a preventive basis, versus waiting until the seal

failed.

The staffing and experience levels of the operations department personnel

exceeded Technical Specification requirements.

A 5-shift rotation was utilized

that allowed for proper support of the operator requalification training

program without excessive overtime.

The remote location of the simulator was discussed during the last assessment

period.

At that time, the licensee acknowledged the NRC observations and

stated that the simulator would be moved to the Palisades site after to the

steam generator replacement outage;

The building that will house the simulator

has been built, and the move is expected to occur during the next SALP assessment

period.

2.

Performance Rating.

The licensee's performance is rated Category 1 in this area.

The licensee's

performance was rated Category 2 and improving during the previous two

assessment periods.

3.

Recommendations

None.

8.

  • Radiol6gical Controls

1.

Analysis

Evaluation of this functional area was based on the results of seven inspections

performed by region-based inspectors and observations made by resident

inspectors.

A total of 843 inspection hours were expended in this functional

area, comprising 13 percent of the total inspection hours.

Enforcement-related performan4e in this functional area was adequate; two

violations were identified.

An enforcement conference was held to discuss

access controls for high-radiation areas and record falsifications in the

general employee training and chemistry quality control programs.

This

enforcement conference resulted in one Severity Level IV violation for the

willful violation of access-control requirements for high-radiation areas. A

second Severity Level IV violation of high radiation area access control

requirements was also identified during this assessment period.

Although no

violations associated with the record falsification issues were cited - in

part, because they were licensee identified - they represented a concern

because the NRC must be able to reasonably rely on the integrity of licensee

personnel.

5

Staffing levels and qualifications were adequate to implement the radiation

protection, radwaste, chemistry,*and radiological environmental monitoring

programs.

Replacement of the Radiological Services Manager during this

assessment period did not have a discernable effect on .program implementation

or performance.

Laboratory supervisors appointed during this assessment period

were knowledgeable and committed to implementing needed improvements in the

quality assurance and quality control (QA/QC) program.

The licensee contracted

additional management and technical staff to handle the demands of the steam

generator replacement project (SGRP).

The licensee developed a parallel

radiation protection organization with distinct responsibilities and established

lines of authority for the SGRP.

The licensee employed a consultant to promote

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org*nizations. This effort was successful in promoting effective communications

between the two organizations.

The effectiveness of training and qualification programs was adequate.

In

general, the licensee's staff was adequately trained and qualified to perform

assigned duties.

Proficiency and continuity continued to improve.

However,

as-low-as-is-reasonably-achievable (ALARA) concepts were not fully incorporated

into the training program, including lesson plans and procedures for general

workers and radiological safety technicians.

The licensee's radiation protection

(RP) and ALARA supervisors and professional staff maintained proficiency by

attending numerous professional workshops and seminars.

The licensee's

ut1lization of mock-up training for major SGRP activities was excellent.

Management's involvement and control in ensuring quality was inconsistent

during this assessment period, particularly in the area of ALARA.

ALARA

considerations for non-SGRP activities were not well integrated into work

planning. Administrative controls in the ALARA area were weak and indicative

of a lack of a firm ALARA commitment.

With some exceptions, an attitude

existed that ALARA activities and concerns were solely the responsibility of

the Radiological Services Department.

In contrast, management support was very

good for ALARA initiatives for the SGRP activities.

The radiation source term *

reduction program also received inconsistent management support.

Positive

aspects of the program included implementation of a hot-spot reduction program

and a coordinated lithium-boron chemistry pH control system.

Also, the licensee

implemented primary coolant system hydrogen peroxide additions to reduce

incore and some excore cobalt-58 and cobalt-60 levels.

However, little progress

was made in reducing the incore and excore inventory of high cobalt-bearing

materials.

Management support for chemistry QA/QC and water quality programs

remained generally strong; although, the licensee was somewhat slow to implement

the QA/QC program.

This was evidenced by the continuing poor performance in

the nonradiological confirmatory measurements program.

The licensee took

corrective actions to improve technicians performance (following the data

falsification incident) and installed a reverse osmosis system for purification

of steam generator makeup water. Additionally, the licensee's water quality

program was consistent with industry guidelines.

One significant management initiative was an extensive self-assessment review

of the radiation protection program, including ALARA implementation.

Near the

end of this assessment period, the licensee drafted a series ~f action plans to

resolve issues identified by the self-assessment.

6

The licensee's approach to identifying and resolving technical issues from a

safety standpoint was also inconsistent.

Inspectors noted good performance in

the resolution of issues fdentified regarding the Safety Injection and Refueling

Water (SIRW) tank.

Other good practices or initiatives included the

implementation of electronic dosimetry, creative uses of video and communication

equipment, bilingual radiological postings, shielding, and pipe-end

decontamination.

However, the licensee experienced recurrent problems with

access control to high-radiation areas.

The work practices of workers and some

radiological safety technicians for contamination control were poor during the

early stages of the SGRP.

Inspectors also noted that an unusually high number

~f con~amination event~ oc~~rred_in area~ ~ot d~siQna~ed a~ bein~ contamina~ed.

~on~am1na~1on even~s s1gn1r1can~1y exceeaea goa1s aur1ng ~ne ear1y s~ages or

the SGRP; however, the licensee was able to reduce the rate of contaminations

as the outage progressed.

The licensee continued to reduce its gaseous radwaste

effluents.

Liquid radwaste effluents remained well within Technical Specification

limits.

By recognizing that lack of progress on an in-state radwaste disposal

site could affect station operations, the licensee proceeded to minimize the

solid radwaste stored at the site.

No radwaste transportation incidents were

identified.

The licensee's ALARA program was significantly challenged during this assessment

period.

In addition to the maintenance outages during the fall of 1989 and

spring of 1990, the licensee performed an SGRP as well as a routine refueling

outage from September through the end of this assessment period.

The licensee

emphasized the regulatory and exposure performance responsibilities of the

contractor with a system of fee programs and financial incentives.

The 1989

radiation dose total was approximately 314 person-rem.

The estimated 1990

radiation dose total for plant activities, excluding SGRP, was approximately

337 person-rem.

This total for the plant represented adequa~e performance.

The 1990 radiation dose total for the SGRP was approximately 397 person-rem.

This included the major portion of the SGRP, and projected dose totals reflected

good planning and performance.

The licensee's ALARA performance compared

favorable with previous industry SGRP projects. Although the licensee's ALARA

performance for non-SGRP activities improved somewhat during this assessment

period, greater management support for SGRP ALARA initiatives resulted in a

better dose reduction program for SGRP activities than for non-SGRP activities.

Performance in the nonradiological confirmatory measurements program was poor,

achieving 19 agreements out of 30 comparisons initially.

Following instrument

recalibration, the licensee achieved 28 agreements out of 30 comparisons.

The

licensee maintained trend charts for water chemistry parameters.

These

parameters were generally below action levels and were reviewed by laboratory

management daily.

Overall water quality was good.

The chemistry

self-assessment program continued on schedule.

Deficiencies occurred in the

conduct of the Radiological Environmental Monitoring Program.

Flow meters for

two air samplers were operated after their calibration period expired, and air

in-leakage was evident in many of the air samplers.

2.

Performance Rating

The licensee's performance is rated Category 2 in this area.

The licensee's

performance was rated Category 2 in the previous assessment period.

7

3.

Recommendations

None.

C.

Maintenance/Surveillance

1.

Analysis

Evaluation ot this tunct1ona1 area was based on ~he resu1~s u1 ii ruu~1r1~

inspections, 1 special inspection performed by the resident inspectors and

3 routine inspections by regional inspectors. A total of 1,588 inspection

hours were expended in this functional area, comprising 24.5 percent of the

total inspection hours.

Two Severity Level IV violations and one deviation were issued during this

assessment period.

Five Severity Level IV violations were issued during the

previous assessment period.

The two level IV violations were identified at the

beginning of the assessment period and pertained to improper maintenance and

surveillance of a containment penetration and associated piping.

Post-discovery

surveillance activities mitigated the safety signfficance.

However, the

violations did indicate that the plant maintenance staff and engineers were not

appropriately aware of containment integrity requirements and that biennial

review of these procedures did not identify this problem.

Two violations

relating to containment testing occurred during the previous assessment period.

Violations involving failure to follow procedures were noted during the previous

assessment period, but none were identified during the current period.

The

deviation was for failure to implement commitments from a previous violation

and perform additional verification of cold leg tube plugging patterns in the

steam generators.

Several LERs issued during this assessment period were applicable to this

functional area, but the number decreased (approximately half) from the number

issued last period, including the occurrence of personnel errors which caused

reportable events.

None of the LERs had major safety significance.

One

pertained to the violations discussed in the previous paragraph, one pertained

to a personnel error that caused an inadvertent actuation of auxiliary feedwater,

and one pertained to a maintenance activity where the inoperability of boric

acid heat tracing was not communicated to the operations department to permit

proper classification of a Technical Specification time limit.

The remaining

few were less important, were not repetitive, and lacked generic or programmatic

implications.

The licensee continued to manage and successfully implement the Technical

Specification surveillance program with surveillances routinely completed on

time.

The extension of surveillance intervals and permitting use of the "grace

periods" was controlled and documented by the appropriate level of management.

The surveillance procedures were controlled, revised, and maintained by the

engineering, maintenance, or operations group responsible for and most

knowledgeable about the equipment.

This good practice allowed the surveillance

procedures to not only check parameters stated in the Technical Specification

but provide a tool for developing equipment trends and evaluations to determine

long-range maintenance and modification needs.

For example, when an inspector

8

questioned the operability of the air start system for the diesel generator,

the system engineer produced graphs indicating that starting times were slowly

increasing and stated that additional preventive actions were being planned.

The administrative policies for preparing new surveillance procedures were

well stated, disseminated, and apparently understood.

These policies produced

surveillance procedures that were consistent in format, structure, and content

and that had a supporting basis document to explain the assumptions, define the

calculations, and justify the acceptance criteria.

Procedures were routinely

in evidence at the job site. Unexpected equipment responses were immediately

brought to the appropriate level of management and resolved using the corrective

action program.

The only negative observation in this regard concerned the

-

-

-

v101a~1on re1a~1ng ~o con~ainmen~ pene~ra~ion ~es~ing.

Management involvement in ensuring quality remained strong. Efficient use of

planners permitted effective planning of work activities, proper scheduling,

prestaging of parts, and routine visits to the job site by supervisors.

The

licensee used a computerized work order system that permitted easy access to

work order history.

Workers demonstrated the value of detailed work order

summaries by using previous work order summaries at the job site as an aide in

both pre-job briefings and preparing work orders.

This represented improving

performance compared to the previous assessment period. Outages performed

during this assessment were well planned.

During the outages the licensee

utilized onsite Shift Managers.

This was a round-the-clock position staffed by

senior managers or senior plant engineers.

The Shift Manager ensured that

proper attention was directed to the outage work path and that emergent work

was properly evaluated and categorized.

One example of positive management

control was the use of a multi-disciplinary organization, which had a defined.

charter and contingency plans to resolve the injection valves flow path problem

in the hot leg.

Plant management's approach to identifying and resolving technical issues

remained *good.

Both the system engineer and the first line supervisor closely

followed maintenance activities and informed upper management of work progress

on a daily basis.

During these daily meetings, the staff identified any

problems encountered, including unexpected equipment conditions, parts or

personnel shortages, coordination issues, etc. These were usually promptly

evaluated and effectively resolved as previously discussed. However, a defective

component in the boric acid heat tracing system was not promptly evaluated for

compliance with Technical Specification time limits.

The work order backlog, corrective work orders, and preventive maintenance

program were routinely evaluated and adequately controlled.

Preventive

maintenance work orders were normally implemented as scheduled, rarely

deferred or missed.

The licensee established a rework maintenance policy that:

(1) defined 11 repeat 11 maintenance, (2) established a mechanism for identifying

11 repeat 11 maintenance, and (3) established a board of managers and superintendents

to evaluate corrective action for

11repeat

11 maintenance.

Rework did not appear

to be an issue or a problem.

The plant's computerized work order program and

database were very useful for ascertaining equipment history.

The quality of

work performed by the maintenance department was good_, and was confirmed by

challenging post-maintenance testing.

The causes of equipment problems were

usually identified and addressed.

An exception was the unexplained trips of

the main feedwater pump that preceded the reactor trips.

A root-cause could

not be determined.

The inservice inspection program was also considered

adequate.

9

Staffing in this functional area continued to be a licensee strength.

This was*

largely attributed to the low turnover rate in both the worker and supervisory

ranks.

The licensee continued to implement programs to provide temporary

placement of maintenance workers in staff positions for use as planners or QC

inspectors.

Rotations of this type appeared to increase interaction between

work groups.

Overtime was controlled and the licensee administrative procedures

amplified the requirements of their technical specifications, to include plant

and contractor personnel.

A few cases were identified in which the limitations

were exceeded without obtaining proper approval.

The licensee took prompt

corrective action to resolve this issue.

complied with the applicable codes.

The coordination of work and the working

relationship between the security and maintenance departments were excellent.*

The overall effectiveness of the security-related equipment was attributed to

diligent and competent maintenance support.

2.

Performance Rating

The licensee's performance is rated Category 1 in this area.

The licensee's

performance was rated Category 2 improving in the previous assessment period.

3.

Recommendations

None.

D.

Emergency Preparedness

1.

Analysis

Evaluation of this functional area was based on the results of two inspections

performed by region-based inspectors and observations made by resident

inspectors.

A total of 132 inspection hours were expended in this functional

area, comprising 2 percent of the total inspection hours.

Enforcement-related performance was relatively weak.

Two Severity Level IV

violations were identified during this assessment period, which appeared to

have programmatic implications, as discussed in the following paragraphs.

No

violations were identified during the previous period.

Management was not adequately involved in ensuring.quality in this area during

this assessment period, as indicated by two violations identified near the end

of the assessment period.

Both violations concerned weaknesses identified in

the licensee's staffing and training of the emergency response organization

(ERO).

Management had not effectively monitored the status of ERO qualifications

nor provided sufficient support for the emergency preparedness (EP) training

program.

The licensee's identification and resolution of technical issues from a safety

standpoint were good.

In response to Emergency Plan activations, the licensee

conducted post-activation reviews for each event to identify areas that could

be improved.

Items identified through these reviews of real events, critiques

10

of drills and exercises, internal and external audits, and NRC inspections were *

tracked and resolved in a timely*manner.

The licensee volu.ntarily participated

in the.implementation of the emergencx response data system (EROS).

The

licensee was the first utility in Region III to have an operational EROS.

The licensee's response to operational events was good.

Two events were

classified and reported pursuant to 10 CFR 50.72 as Emergency Plan activations

during this assessment period.

Both of these events were classified as Unusual

Events.

Each event was correctly classified in a timely-manner.

The licensee

appropriately notified the State, counties, and the NRC within the required

time limit for each event.

Staffing of the ERO was inadequate, at times, during this assessment period.

Because of lapsed training, the licensee would have been unable to continuously

staff several ERO positions with trained and qualified personnel.

The licensee

cross-trained many individuals for multiple ERO positions.

Utilizing individuals

who had been cross-trained helped to mitigate the shortages of qualified

individuals.

The emergency plan training program was ineffective because it received

inadequate management oversight.

Numerous ERO members were not fully qualified

for their designated positions because they had not completed required retraining

within allowed time requirements. Although the licensee had a program for

tracking ERO qualification and training needs, and the required training courses

were made available, the courses were poorly attended. Also, the licensee's EP

training matrix was lacking a required course for the position of HP support

group leader.

Due to an administrative error, this course was omitted during a

program revision.

Also, some lesson plans were not reviewed or revised in a

timely manner.

Although the qualification program in general was not effectively

implemented, the licensee did utilize problem sets to provide good practical

exercises for individuals as part of the program.

Performance during the annual EP exercise was generally good.

The scenario,

which involved a tube rupture in the steam generator and a non-isolable break

in the main steam line, was adequate to challenge and involved most of the ERO.

Problems were observed with command and control of the Operations Support

Center and Maintenance Support Center, and the Emergency Operations Facility

was not activated in a timely manner .. Both facilities successfully fulfilled

their respective emergency response roles.

2.

Performance Rating

Licensee performance is rated a Category 2 and declining in this area.

The

licensee was rated a Category 1 during the previous assessment period.

3.

Recommendations

None.

11

E.

Security

1.

Analysis

Evaluation of this functional area was based on the results of three routine

security inspections and two Fitness-For-Duty (FFD) ins*pections by regional

inspectors and observations made by resident inspectors. A total of 186

inspection hours were expended in this- functional area, comprising 2.9 percent

of the total inspection hours.

Enforcement-related performance in the security area was good.

Inspectors

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of some access control search equipment and appeared to be an isolated

occurrence.

The licensee identified FFD problems that were cumulatively

treated as a Severity Level III violation. This violation involved a

significant breakdown in several basic elements of the licensee's FFD program

which was implemented by corporate personnel through the Human Resources

Department.

Once the problems were identified, licensee management initiated

aggressive and effective corrective actions.

Management involvement in ensuring the quality of the security program was

good.

Management support was demonstrated through continual upgrades to the

security program during the SGRP.

These upgrades included additions to the

security staff and security building modifications.

Inspectors considered

management oversight, planning and extensive compensatory measures for the

SGRP, and routine daily security activities a program strength. Security

management was re5porisive to all findings that could strengthen the overall

security program.

Licensee action for these findings was comprehensive and

utilized the coordinated talents of security and contractor personnel.

During

this assessment period, security managers kept both resident inspectors and

regional personnel fully informed of site security issues.

The licensee's approach to identifying and resolving issues was good .. The

licensee demons~rated a cl~ar understanding of the issues throughout the

planning and implementation of security requirements associated with the SGRP.

The implementation included extensive long-term, in-depth compensatory measures;

protected and vital area barrier modifications; .and extensive security plan

revisions.

This 11defense-in-depth 11 philosophy assured the licensee that

in-attentive guards or equipment failure would not become a *Security issue.

The

licensee's program for required reporting of security events was excellent.

Required reports and logs were accurate and timely.

In general, security-related

records were complete, well maintained, and readily available.

Licensee staff resources dedicated to-the security organization were ample

during this assessment period.

The licensee increased the number of security

officers to meet requirements for support of the SGRP and associated activities.

The security resources were effectively utilized and a high level of security

awareness was evident.

The close and effective liaison established among local

law enforcement agencies, the security contractor site management, and licensee

security management was a program strength.

QA audits of the security program

by contractor personnel as well as corporate QA personnel contributed to the.

security organization's overall good performance.

The audits were aggressive,

detailed, broad in scope, and well documented.

Aggressive management/employee

relations programs are partially responsible for a low turnover rate of only

about 3 percent for 1990.

12

The training and qualification program for the security organization was good.

The program was effectively implemented.

Security personnel were competent in

th~ execution of their duties.

The licensee's security organization identified

the need for additional and more effective tactical response training.

However,

due to SGRP support requirements, very little of this training was performed

this assessment period.

During this as~essment period, NRC inspectors reviewed the licensee's FFD

program required by 10 CFR Part 26.

This review indicated that, initially,

portions of the rule either were not addressed or were implemented contrary to

NRC regulations.

The licensee's QA staff identified these problems during an

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was later held and the root causes of the Severity Level III violation appeared

to be inadequate management oversight and too much reliance* on the FFD program,

which was already in place before the implementation of 10 CFR Part 26.

The

licensee took immediate and extensive corrective actions to correct all the

problems once they were identified, and the licensee's FFD program thereafter

appeared to meet the objectives of 10 CFR Part 26.

2.

Performance Rating

The licensee's performance is rated a Category 1 in this area. The licensee's

performance was rated Category 1 in the previous SALP assessment period.

3.

Recommendations

None.

F.

Engineering/Technical Support

1.

Analysis

Evaluation of this functional area was based on one team, one special, and two

routine inspections by regional inspectors; one enforcement conference, one

requalification, and one initia] examination by operator licensing examiners;

several inspections by resident inspectors; and interactions between the

licensee and the staff of NRR.

Overall, 882 inspection hours were expended in**

this functional area, comprising 13.6 p.ercent of the total inspection hours.

Enforcement history included one Severity Level III violation for a programmatic

breakdown in the areas of design control, adherence to procedures, and

corrective action for engineering activities that involved piping and pipe-

support analyses.

These problems occurred prior to the appraisal period.

In

addition, two Severity Level IV violations, one in the area of test control and

the other in the area of environmental qualification of electrical equipment

were identified.

Of the several LERs attributable to this area, all except two were the result

of original design or design change errors performed during prior assessment

periods.

These errors were found by the configuration control project (CCP).

One current LER was the result of an improper work practice and the other

pertained to a design error during a modification.

13

Management involvement in ensuring quality continued to be inconsistent this

period.

On the positive side, the engineering staff was actively involved in

maintenance and operational activities.

In addition, engineering support

personnel continued to be rotated into operator licensing classes.

The CCP,

started during an earlier assessment period, continued to progress well and

disclosed a number of design problems.

A critical self-review of the design

change program was completed, with results confirming the need to strengthen

control of activities in this area.

The licensee modified the requirements of

various service contractors to provide monetary incentives (bonuses and penalties)

for regulatory and safety performance including compliance with fire protection

and security programs and meeting ALARA goals.

The licensee upgraded the

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and enhanced the controlling administrative procedure for facility changes in

order to attain a more consistent approach in technical methodology and

documentation.

However, the effectiveness of these efforts was reduced by the

implementation of a different administrative procedure and project specific

design criteria for the SGRP contractor.

Management involvement in the planning

and assignment of priorities for the SGRP was also evident.*

On the other hand, technical evaluation and oversight for the hydrostatic

pressure testing of plant systems by the HAFA Company was poor.

Management

lacked control of this technical contractor as exemplified by the inadequate

technical review of the implementing procedures, the use of improperly certified

personnel, and the incompleteness of test data and related records.

When the

NRC pointed out the deviations from the NRC-approved concept, the licensee

continued to maintain that the tests were valid, even though they lacked a

technical basis.

Further, management was not aggressive in purs.uing a number

of other engineering or t.echnical issues.

Examples of this include the licensee's

attempt to resolve a welding issue for four branch connections using

circumstantial justification instead of addressing the issue using positive

verification in accordance with their commitments.

Also, for a socket weld

issue, the licensee's initial evaluation of dimensional weld data used an

approach that did not adequately bound the potential significance of the issue.

Engineering activities associated with piping and structural analyses continued

to show weaknesses with design verification. Management's efforts to achieve

programmatic improvements and to communicate quality standards in the area of

design verification, while worthy of mention, were not fully effective.

Reviews of calculations performed near the end of the assessment period continued

to disclose a lack of attention to detail similar to that found during earlier

inspections.

In one case, a piping component in the auxiliary feedwater steam

supply system was changed without considering the impact of the change on the

piping stress analysis.

In another case, an incorrect analytical approach,

noted by the NRC, resulted in the modification of a pipe support in the

containment sump drain system.

These examples demonstrate that the significant

design control deficiencies, which led to the escalated enforcement early in the

period, had not been completely resolved.

The design change program was reviewed with mixed results. Modifications to the

ATWS system, the refueling machine, the pressurizer power operated relief

valves (PORV), and the closure logic to the feedwater valves were reviewed.

Most were performed with satisfactory results, however, the PORV modification

resulted in a design change that was implemented without fully understanding

14


-------

the system configuration and the operating characteristics of the PORV.

This

implementation led to the uncontrolled opening of the PORV during post

modification testing, causing a reactor coolant system pressure transient. A

number of _design changes pertaining to the SGRP were also reviewed.

These

included replacement of feedwater heaters, replacement of steam generators,

replacement of the condenser, addition of steam piping, modification of blowdown

piping, and establishment of the containment construction opening.

These

design changes were generally well planned and effectively implemented.

The

post modification testing was in progress at the conclusion of this assessment

period.

safety standpoint was considered mixed.

Numerous problems with design activities

and calculations, particularly with respect to certain SGRP piping analyses,

were identified during onsite engineering reviews and quality assurance audits.

However, management did not aggressively correct the cause of these problems.

On *the other hand, in the case of the unexpected operation of the atmospheric

dump valves as a result of electrical noise, the engineering staff demonstrated

its ability to resolve a problem once it was identified. Also, the licensee

responded vigorously to investigate and resolve the issues associated with the

uncontrolled opening of the PORV, including close monitoring and control of

the involved technical contractor.

The engineering and technical support staff continued to be relatively stable

and the licensee maintained a strong commitment to the system engineer program.

The level of staffing appeared to be sufficient to handle the engineering

workload, however, as mentioned above, the licensee did not exhibit sufficient

technical oversight of some of its contractors.

Rotations among the engineering

department and other plant departments were accomplished which encouraged a

team concept among plant personnel.

Overall, management performance in the areas of operator requalification and

replacement operator examinations declined from the. previous assessment period.

Inspectors identified deficiencies in the written examination question bank for

requalification examinations similar to those found in the previous assessment

period. The training department did not effectively support the requalification

examinations.

Licensee representatives dedicated to the examination team were

required to participate in collateral activities. This reduced their time

available for examination development and resulted in poor quality of the

written examinations submitted to the NRG for approval, particularly the most

recent examination.

In addition, deficiencies in the written examination

bank, similar to those identified in 1989, were indicative of an inability to

maintain the requalification material.

Improvements were noted during the

requalification retake examination late in the assessment period.

The

licensee's proposed plan to upgrade the quality of their reference material was

comprehensive and well presented.

Performance during requalification examinations was judged satisfactory,

however, the effectiveness of training decreased as exemplified by the fact

that the passing rate for NRG-administered initial and requalification

examinations declined.

One of two licensed operators who failed the

requalification examination also failed the NRG-administered requalification

retake examination, indicating that remedial training was not effective.

15

. 2.

Performance Rating

The licensee's performance is rated Category 2 and declining in this area.

The

licensee's performance was rated Category 2 in the previous assessment period.

3.

Recommendations

None.

G.

Safety Assessment/Quality Verification

1. Analysis

Evaluation of this functional area was based on the results of 11 routine

inspections by the resident inspectors, several routine inspections by regional

inspectors, and a team inspection to review 10 CFR 50.59 evaluations of the

steam generator replacement.

In addition, the NRC considered its staff's

review of licensee submittals and requests for amendments to the operating

licenses. A total of 1,525 inspection hours were expended in this functional

area, comprising 23.6 percent of the total inspection hours.

The enforcement history in this functional area included three Severity Level IV

violations.

The first was for failure to request a Technical Specification

change following a design change.

Compensating maintenance and surveillance

requirements, however, were implemented at the time of the change.

The second

violation involved a change to a procedure that altered the original intent,

yet no safety evaluation was performed.

The third violation involved failure

to take adequate corrective action for a previous violation in the equipment

qualification area.

The violations did not share a common root cause, were not

representative of programmatic breakdowns, and were not the same as any of the

three Severity Level IV violations issued during the last assessment period.

The single LER issued during this assessment period that was attributed to this

functional area was for a personnel error in configuration control that occurred

while verifying wiring.

The error caused an electrical short and a right

channel containment isolation while the plant was in cold shutdown.

This LER

did not indicate a programmatic weakness.

Management involvement in ensuring quality was inconsistent.

Management

conti~ued to support various programs, several of which had begun before and

will continue past this assessment period. These included the configuration

control project (CCP) and the performance of critical self-assessments as a

tool for corporate and plant management to improve work activities. The

self-assessments each involved an assessment team and generated some long term

corrective actions.

To ensure continuity, the team leader is tasked with

tracking and trending all the team items through ultimate closure.

The CCP

consists of retrieving and reconstituting design basis documentation and

confirming safety system design.

Inspectors considered licensee implementation

extensive in both scope and detail. However, the lack of a writer's guide

before beginning the review of the design basis documentation resulted in

16

scheduling delays for completing the CCP.

In addition, the licensee chose to

let the contractor manage overtime, which resulted in some critical personnel

working to the point of exhaustion.

One such individual ev.entually resigned.

Evaluation of his work determined that quality had not been compromised.

During the CCP, the licensee identified numerous technical issues and potential

safety concerns.

Each received a timely evaluation and no immediate safety

concerns were identified. The actions and schedule to correct the many

electri~al design and wiring diagram discrepancies were reasonable, however,

the schedule for resolving other discrepancies has not been determined.

The licensee provided additional resources to disposition all the CCP findings.

The licensee continued to operate a large-volume, low-threshold corrective

action program, focused on timely classification and segregation of significant

items for review by the appropriate level of plant and corporate management.

The corrective action program provided for daily meetings chaired by one of the

managers.

Responsibility for maintaining and resolving discrepancies among

corrective action documents was assigned to individuals instead of a group or

section, which established direct accountability for the end product.

Processing

of corrective actions was generally characterized by proper technical and

safety focus, effective root-cause and trend evaluations, and timeliness.

One notable exception involved a failure to meet a commitment.

The quality of the licensee's evaluations associated with ongoing licensing

actions was generally good.

However, on several occasions, the NRC had to

request additional information in order to properly evaluate a licensing issue.

These requests were responded to in a timely manner, however, th~ number of

such requests indicated a weakness in the licensee's ability to ensure that.

consistent, high-quality evaluations were prepared and reviewed.

NRC questions

about licensing submittals were not always factored into the licensee's planning

process.

The licensee's approach to identifying and resolving technical issues from a

safety standpoint was typified by the general thoroughness of the 10 CFR 50.59

evaluations performed for the SGRP.

These evaluations identified and adequately

addressed the safety issues related to the SGRP.

The only deficiencies were

failures to identify that certain minor Technical Specification changes were

required before startup.

However, during this assessment period, the licensee

submitted its final evaluations regarding TMI Action Plan Item II.D.1,

"Performance Testing of Relief and Safety Valves,

11

for which a number of

concerns had been identified during the previous assessment period.

The

content of the submittals during this assessment period, coupled with

discussions with the licensee's staff, indicated that significant attention and

thorough evaluation were given to the remaining outstanding items for this TMI

issue.

The licensee was proactive in conducting public meetings with local residents

to discuss topics of interest.

Public meetings, pertaining to steam generator

replacement and dry storage of spent fuel, were attended by the resident inspector.

Informal feedback from participants indicated the meetings were helpful in

determining the level of public interest.

Plant and corporate use of QA audits and QC verifications were evident by the

findings made and corrective actions taken.

Positive contributions to good

17

I.

programmatic performance were evitient in the security area.

Early

identification and correction of problems to prevent more significant

deficiencies from developing occurred in the fire protection and FFD programs.

On the other hand, QA audits did not identify training.and qualification

problems that existed in the emergency planning area.

Auditors and inspectors were qualified and technically competent.

The scope

and quality of the audits and inspections met or exceeded requirements and

usually emphasized performance as well as compliance.

Findings were usually

responded to in a thorough, timely, and technically sound manner.

The Onsit~ R~viPw rnmmi++ee wes prop9rly st:ff:d :~d funet1onad wa11.

The

licensee decentralized its licensing function, assigning the duties of a staff

of approximately 10 licensing engineers from the headquarters to the respective

plants.

The transition went smoothly and served to improve licensing staff

access to plant technical staff and hardware.

2.

Performance Rating

The licensee's performance is rated Category 2 in this area.

The licensee's

performance was rated Category 2 in the previous assessment period.

3.

Recommendations

None.

IV.

SUPPORTING DATA AND SUMMARIES

A.

Licensee Activities

Palisades Nuclear Generating Plant operated at the administratively imposed

power level limitation of 80 percent during this SALP assessment period.

The

limitation was imposed by the licensee during the previous assessment period to

resolve NRC questions pertaining to the integrity of steam generator tubes.

The unit was removed from service for three preplanned outages.

Two outages

prepared the unit for the steam generator replacement outage.

The third was

the steam generator replacement and refueling outage that was continuing at the

completion of this assessment period.

In addition, two forced outages occurred.

One pertained to replacement of a faulted pressurizer heater transformer and

the second was a continuation of a preplanned outage when a PORV failed to

function properly.

Palisades experienced eight engineered safety feature (ESF) actuations and four

reactor trips.

Two trips occurred while operating at .greater than 15 percent

power and two occurred with control rods already inserted.

Both power trips

were preceded by inadvertent trips of main feedwater pumps.

The other two did

not involve co.ntrol rod movement--one was caused by implementation of a design

modification that did not consider plant operating characteristics and the

other was due to an incorrect test procedure.

18

f

Significant outages and events that occurred during the assessment period are

summarized below.

  • 1.

On 10/01/89, the plant was shut down to prepare for the steam generator

replacement.

This shutdown became a forced outage on 11/26/89 when a PORV

and block valve failed to function as intended.

The outage was extended

to 12/20/89 at which time the plant was returned to service.

2.

During 01/08-10/90, the plant reduced power for main condenser maintenance.

On 01/09/90, the plant was manually tripped from 35 percent power when the

11A

11 main feedwater pump tripped for unknown reasons.

The plant was

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On 02/28/90, an inadvertent loss of the 118

11 main feedwater pump occurred

when the plant was at 80 percent power.

During recovery actions, the

plant tripped from approximately 59 percent power because of a variable

high power trip. The plant was returned to power operations on 03/03/90.

4.

On 09/15/90, the unit was removed from service for a planned 150-day

refueling and steam generator replacement outage. This outage extended

through the end of the assessment period.

B.

Inspection Activities

Forty-one inspection reports are discussed in this SALP (09/01/89-12/31/90) and

are listed below.

Significant inspection activities are listed in Paragraph 2 .

. 1.

Inspection Data

Facility Name:

Palisades Nuclear Power Plant Docket No.:

50-255

Inspection Reports:

89024, 89026 through 89034, 90002 through 90006, 90008

through 90019, 90021 through 90025, 90027 through 90031, 90034, 90035, 90037

and 90038.

2.

Special Inspection Summary

a.

During 08/14-12/08/89, a special.safety inspection was conducted of the

licensee's snubber reduction program.

This inspection resulted in an

enforcement conference and a civil penalty pertaining to a programmatic

breakdown in the control of design activities, compliance with procedures,

and corrective action.

(Inspection Report 255/89024 and 255/90002).

b.

During 07/19-09/05/89, a special inspection was conducted pertaining to

containment integrity and reportable events.

(Inspection Report 255/89027).

c.

During 11/23-12/15/89, a special team inspection was conducted to evaluate

the inadvertent depressurization event on 11/21/89 (Inspection Report

255/89033).

19

'

d.

During 05/21-25/90 the annual EP exercise was conducted (Inspection

Report 255/90011).

e.

During 05/13-31/90, a special assessment of the ALARA program was conducted

(Inspection Report 255/90013).

f.

During 07/30-08/03/90, a special team inspection was conducted to evaluate

the 10 CFR 50.59 review process for the SGRP (Inspection Report 255/90017).

g.

During 08/13-09/19/90, a special safety inspection was conducted of

circumstances associated with falsification of training records by an

instructor and fal,ifir::itinn 0-F

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This inspection resulted in an enforcement conference.

(Inspection

Reports 255/90019, 255/90028, 255/90030 and 255/90035).

h.

During 10/15-19/90, a special safety inspection was conducted of the

licensee's FFD program.

This inspection resulted in an enforcement

conference and a civil penalty (Inspection Report 255/90027).

C.

Escalated Enforcement Actions

1.

A Severity Level III Notice of Violation and a proposed $75,000 civil

penalty were issued on 02/20/90 for a programmatic breakdown in the

control of design activities, compliance with procedures, and corrective

actions.

(Enforcement Action EA 89-251 and Inspection Report 255/90002).

2.

A Severity Level III Notice of Violation (with no civil penalty) was

issued on 12/14/90.

This action was based on problems associated wit~ the

licensee's FFD program.

(Enforcement Action EA 90-189 and Inspection

Report 255/90027).

D.

Confirmatory Action Letters

None.

E.

Licensee Event Reports

LERs 89021 through 89025 and 90001 through 90021 (including "voluntary"

LER 89022) were issued during this assessment period.

20