text
...
lfflC--
IM31 LICENSEE EVENT REPORT (LER)
U.S. llUCLIAll lllCIULATOll'I' c:omt-
.-OVID Dll9 NO. J1111-010ol IXPlllll: I/JI..
'ACILIT'I' MAiia 111 I
DOCltlT-11121 I
r*~*,..,
P/\\T TQ/\\n"l<'Q l\\TTTl"'T 1"/\\P PT /11\\TrTI 0151010 IOb-1 51-5 1 loF Q*l4 TITLE l'I i<'ORRTCi-N Ml\\'FR::/TAT ON VllT,VH' RH'A'T' R1<~TTLmR TTIT 1 ~1rH-'" !ll"P.T.H' TC:::rH.ll'T'T()l\\T iTllT.iT-;<'
IVINT DATI Cll Liii N~lll Cll lllPOllT DATE 171 OTHlll,ACILITIU IWOLYIO 181 DOCKET NUMIElllSI NIA Ol'HATING
'ntll lllPOllT 11 IU.. ITTED l'UlllUANT TO THI lllOUllllMINTI 0' 10 C,11 §: lo.S:lt -
OI' -
of IN fel-..,J 1111 11---lllDD--l,..It-I _ __.rr...
11J -+~ ia.CZU1I 20.tmlel
~~ lo n 1-s--
7J.711al 71.71 lel a.a1a1111111 a.a1a1111111 I0.*1*1111 ll0.*1*1121
- .111111211.1 IO.nl91121fwll llt';ll=
a.a1a111111111 a.a11111111w1 tL
- 73111121181 I0.731111211HO
- 7149112llw1111AI I0.72lall21Cwlllllll
- .7Jlall21f*I O'TNlll 15-lftt in Ablftcr
>>IAI LICINllE CONT ACT,Dll THll Liii 1121 TELEPHONE NUMIER AlllA CDOI CSKozup_,. Technical Engineer, Palisades 6116 71614 l-181'.11113 COMl'LITI ONE LINI FOii IACH COMl'ONENT,AILUlll OllClllllO IN TH* lll_POllT 1131 CAUIE S'l'ITIM COMPONENT X
WID I II S IV Ml 112 I 0 NO I
I I
I I
I I
I I I I I
I I
I I
I I
I I
I IU"LIMINTAL lllPOllT IXPICTED IHI MONTH DAY
'!'~All n YES llf,.... _,_.,. llXHCTllO SU.II/SS/ON OATlll
~
NO EXPECTED IUIMISllON DATE 1151 I
I I
Abstract During the performance of Technical Specification (TS) Surveillance Test Q0-11, "Containment Isolation Check Valve Test 11 on December 2, 1988, inner containment isolation valve CV-1037 [WD;ISV] was discovered to be leaking by in excess of allowed TS limit, however, integrity of the outer containment isolation check valve CK-CRW408 was maintained.
TS 4.5.2 requires that the total leakage from all penetrations and isolation valves remain under 0.60La*
At 2216 when this condition was identified, the reactor was critical° with the Plant operating at 35.2 percent of rated power.
In attempting to identify the root cause of CV-1037's failure, it was flushed and cycled several times.
During this evolution, the valves stem was observed to be traveling further closed upon each cycle.
At this time mechanical binding of valve inte~nals was the suspected cause.
However, when the valve was disassembled, a small unidentifiable hardened green plastic object was found adhered to the valve's plug.
This plastic appeared to have been chipped away by cycling the valve such that_ acceptable seating was achieved prior to valve repair.
NllC'"-*
Lr.I:\\ OOULL-LlUJ.19-431
NllC FM"' *A
'.ll-631 LICENSEE EVENT REPORT (LERI TEXT CONTINUATION U.I. NUCLEAll lllEGULATOlllY COMMIDI~
Al'l'ROVEO OMB NO 3150--0104 EXPIRES. 8/31185 OOCKET NU.. ER 121
~AGE Ill FACILITY NAME 111 LEiii N~Ell 111 Palisades Nuclear Plant TEXT I,,,,.,,,._..;,,,.,,.,nd, -
- - NlfC Fotm.m.4'111171 0 15 I 0 I 0 I 0 I 2 I s Is 8 18 -
o I 2 12 o p o I 2 o F o I 4 N"'C FORM 3e6.A
Description
During the performance of Technical Specification (TS) Surveillance Test Q0-11, "Containment Isolation Check Valve Test" on December 2, 1988, inner containment isolation valve CV-1037 [WD;ISV] was discovered to be leaking by in excess of allowed TS limit, however, integrity of the outer containment isolation check valve CK-CRW408-was maintained.
TS 4.5.2 requires that the total leakage from all penetrations and isolation valves remain under 0.60La*
At 2216 when this condition was identified, the reactor was critical with the Plant operating at 35.2 percent of rated power.
TS Surveillance Test Q0-11 is performed at three month intervals in accordance with TS 4.5_.2.d.2.
This test verifies the ability of containment isolation check valves to close in order to achieve their required safety position per ASME Section XI.
During test performance, a reverse pressure is applied across the check valve seat and flow is verified'to be secured by monitoring test pressure decay rates.
Containment isolation valve CV-1037 is associated with containment penetration 67* which services the clean waste receiver tank pump P-70 [WD;P] recirculation line. Penetration 67 is classified as a Palisades Final Safety Analysis Report (FSAR) class C2 penetration.
Penetrations in this class include systems that are not connected to either the containment atmosphere or to the primary coolant system and are normally
. open or may be opened during power operation.
- Pipe lines passing through the containment, associated with FSAR class C2 penetrations are required to have two automatic isolation valves in series.
Check valves are considered to be automatic.
Penetration 67 meets this requirement via CV-1037 and CK-CRW408 being in series, with CV-1037 receiving an automatic close signal upon actuation of the containment isolation system.
During the performance of Q0-11, CK-CRW408 is tested by applying 80 psia of air pressure between it and CV-1037.
A test fixture is attached at a test tap to monitor pressure decay.
When this test was performed on December 2, 1988, the acceptance criteria of maintaining greater than 69.7 psia of air pressure for five minutes was not met.
This determination was made at 2136.
At 2216, it was determined that CV-1037 and not CK-CRW408 was leaking by.
This was determined by opening an in-containment valve (CV-1018) upstream of CV-1037.
When the valve was opened, the test pressure rapidly dropped *off, thus confirming CV-1037 was leaking by.
At this time, Operations personnel entered TS 3.0.3 and initiated a series of line flushes and valve cycling operations in attempting to get CV-1037 to seat properly.
At 2316, it was determined that CV-1037 was functioning properly, so TS 3.0.3 was exited.
1e.eJ1 LER 88022-LIOl
NllC I A
19-631 LICENSE ENT REPORT (LERI TEXT CONTINUATION U.I. NUCLEAll llEGULATOllY COMMIDION A'PROVEO OMS NO. 3150~104 EX,.llES: 8/31 '115 FACILITY NAME 111 DOCKET NU.. ER 121 Liii NU..Ell 111 Palisades Nuclear Plant 0 15 I 0 I 0 I 0 I 2 I 51 5 8 18 o I 21 2 01 0 0 I 3 OF 0 14 T£XT (If,__ io '9qVftd, -
.-.W NltC Foml _.'*I 1171
Cause Of The Event
In attempting to identify the root cause of CV-1037's failure, it was flushed and cycled several times.
During this evolution, the valves stem was observed to be traveling further to closed upon each cycle.
At this time mechanical binding of valve internals was the suspected cause.
However, when the valve was disassembled, a small unidentifiable harden.ed* green plastic object was found adhered to the valve's plug.
This plastic appeared to have been chipped away by cycling the valve such that acceptable seating was achieved prior to valve repair.
The source.of the hardened gree.n plastic object is not known, however, it is felt to be an i.solated occurrence resulting from maintenance activities.
Corrective Action
NlllC FORM 3e8A 19-1131 CV-1037 was disassembled, inspected and repaired.
During this repair, the valve packing was upgraded by installation of graphite packing to minimize mechanical binding.
Valve operability was confirmed by the satisfactory performance of the Local Leak Rate Test R0-32-367.
During this event, Operations personnel noted that Q0-11 prescribed actions for test results not meeting a.cceptance criteria entailed retesting, initiating corrective action documents and initiating applicable local leak rate tests during the next cold shutdown condition.
However, no reference was made to potentially applicable TS Limiting Conditions of Operation.
Therefore, actions prescribed within Q0-11 are being evaiuated to assure proper actions are taken to preclude potential TS violations regarding containment integrity.
Procedures regarding cleanliness control have recently been upgraded to aide in precluding foreign materials and tools from entering Plant system.
Analysis Of The Event
During the one hour period when CV-1037 was declared inoperable, the integrity of the outer most containment isolation valve CV-CRW408 was maintained.
Therefore, at no time was there leakage from the Containment Building in excess of Plant TS.
TS 3.6 requires that containment integrity be maintained unless the reactor is in the cold shutdown condition.
TS 1.4, as it applies to automatic isolation valves, is defined to exist when "all automatic containment isolation valves are operable or are locked closed".
In that CV-1037 was not operable and was not locked closed, this event is being reported per 10CFRS0.73(a){2){ii) as an operational condition prohibited by Plant TS.
LER 88022-LIOl
NRC *****'..
A 19-831 LICENSEE ENT REPORT (LERI TEXT CONTINUATI U.I. NUCLEAI! lliGULATOll'I' COMMlalON A"ROVEO OMD NO. 3150~104 EX,IRES 81311115 FACILITY NAME (11 DOCKET N..,...EI! 121 YEAfllt SEQUENTIAL.::::.<* llllEVrllON NUM Ell!
'Palisades Nuclear Plant 0500025 588-02 2-0 00 TEXT l/f-- *--* --NltC -.-...*111171
Additional Information
Containment isolation valve, CV-1037 is a Masoneilan Division model number 38-20571 control valve.
For additional information regarding inoperable containment isolation valves, reference Licensee Event Reports87-005, 87-026,85-029, 83-059,83-066 and 81-036.
NJllC FOllllM 38eA (9-!131 LER 88022-LIO 1 (I
OF 0 4
PDWERINli MICHlliAN'S PROGRESS General Offices: 1S45 West Parnell Road, Jack_son, Ml 49201 * (517) 788-0550 December 28, 1988 Nuclear-Regulatory Commission Document Control Desk Washington, DC 20555 DOCKET 50-255 - LICENSE DPR PALISADES PLANT -
LICENSEE EVENT-REPORT 88-022 - FOREIGN MATERIAL ON VALVE SEAT RESULTS IN-INOPERABLE ISOLATION VALVE Licensee Event Report (LER)88-022 (Foreign Material on Valve Seat Results in Inoperable Isolation Valve) is attached.
This event is reportable to the NRG per 10CFR50.73(a)(2)(ii).
Brian D Johnson Staff Licensing Engineer CC Administrator, Region III, USNRC NRC Resident Inspector - Palisades Attachment OC1288-0248-NL04
,,,_ )**
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000255/LER-1988-001-01, :on 880123,discovered That Pressure Level on Primary Coolant Sys Exceeded 55% Level Required by SOP-1. Caused by Personnel Failing to Maintain Low Temp Overpressure Protection Sys |
- on 880123,discovered That Pressure Level on Primary Coolant Sys Exceeded 55% Level Required by SOP-1. Caused by Personnel Failing to Maintain Low Temp Overpressure Protection Sys
| | | 05000255/LER-1988-002, Forwards Corrected Semiannual Effluent Release & Waste Disposal Rept for Period Jan-June 1988,including LER 88-002 Inadvertently Omitted from Original 880831 Submittal & Supplemental Jul-Dec 1987 Rept | Forwards Corrected Semiannual Effluent Release & Waste Disposal Rept for Period Jan-June 1988,including LER 88-002 Inadvertently Omitted from Original 880831 Submittal & Supplemental Jul-Dec 1987 Rept | | | 05000255/LER-1988-002-01, :on 880209,inservice Waste Gas Decay Tank Lost Approx 26 Psi.Caused by Failure to Hold Gaseous Radwaste for Min of 15 Days Per Tech Specs.Pressure Drop Isolated & Air Samples Taken by Health Physics Personnel |
- on 880209,inservice Waste Gas Decay Tank Lost Approx 26 Psi.Caused by Failure to Hold Gaseous Radwaste for Min of 15 Days Per Tech Specs.Pressure Drop Isolated & Air Samples Taken by Health Physics Personnel
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1988-003-01, :on 880221,23 & 24,secondary Side Contents of Steam Generators E-50A & E-50B Discharged to Lake Michigan as Continuous Release.Samples Disposed of Prior to Required Analyses.Caused by Procedure Deficiency |
- on 880221,23 & 24,secondary Side Contents of Steam Generators E-50A & E-50B Discharged to Lake Michigan as Continuous Release.Samples Disposed of Prior to Required Analyses.Caused by Procedure Deficiency
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1988-004, :on 880303,required Dissolved Oxygen Analysis Not Completed.Caused by Personnel Error.Data Sheets Revised to Clearly Identify Analyses Required by Tech Specs & Required Time to Be Completed |
- on 880303,required Dissolved Oxygen Analysis Not Completed.Caused by Personnel Error.Data Sheets Revised to Clearly Identify Analyses Required by Tech Specs & Required Time to Be Completed
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1988-005, :on 880304,stroking of Svc Water Containment Isolation Valves Occurred During Prohibited Conditions. Caused by Procedural Deficiencies.Administrative Procedure 9.21 Revised & Tech Spec Tests Reviewed |
- on 880304,stroking of Svc Water Containment Isolation Valves Occurred During Prohibited Conditions. Caused by Procedural Deficiencies.Administrative Procedure 9.21 Revised & Tech Spec Tests Reviewed
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1988-006, :on 880327,auxiliary Feedwater Pump Inadvertently Started When Auxiliary Feedwater Actuation Sys Manually Actuated.Caused by Insufficient Guidance Available in Alarm/Response Procedures.Training Provided |
- on 880327,auxiliary Feedwater Pump Inadvertently Started When Auxiliary Feedwater Actuation Sys Manually Actuated.Caused by Insufficient Guidance Available in Alarm/Response Procedures.Training Provided
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1988-007, :on 880429,auxiliary Feedwater Actuation Sys Actuated.Caused by Surveillance Procedure RO-21 Inadequacy That Permitted Input of Test Signal to Result in Quick Open Signal Generation.Procedure Corrected & Tested |
- on 880429,auxiliary Feedwater Actuation Sys Actuated.Caused by Surveillance Procedure RO-21 Inadequacy That Permitted Input of Test Signal to Result in Quick Open Signal Generation.Procedure Corrected & Tested
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1988-008, :on 880512,containment Penetration Declared Inoperable Due to Failure to Complete Required Local Leak Rate Test within Prescribed Time Limitation.Caused by Data Entry Error.Test Schedule Verified |
- on 880512,containment Penetration Declared Inoperable Due to Failure to Complete Required Local Leak Rate Test within Prescribed Time Limitation.Caused by Data Entry Error.Test Schedule Verified
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1988-009, :on 880516,failure to Maintain Continuous Fire Watch as Required by Tech Spec 3.22.3 Occurred.Caused by Poor Performance of Security Officer.Review Conducted,Only to Determine Problem as Being Isolated |
- on 880516,failure to Maintain Continuous Fire Watch as Required by Tech Spec 3.22.3 Occurred.Caused by Poor Performance of Security Officer.Review Conducted,Only to Determine Problem as Being Isolated
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1988-010, :on 880609,discrepancy Identified in Radiological Consequence Analysis of Plant Fsar,Section 14.22.No Cause Can Be Readily Identified for Failure to Follow Plant Mod Procedures.Analysis Initiated |
- on 880609,discrepancy Identified in Radiological Consequence Analysis of Plant Fsar,Section 14.22.No Cause Can Be Readily Identified for Failure to Follow Plant Mod Procedures.Analysis Initiated
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000255/LER-1988-011, :on 880624,determined That Single Failure Criteria Not Met for All Ac Instrument Bus Alignments. Caused by Personnel Error.Evaluation Performed to Determine Feasibility of Performing Design Mods |
- on 880624,determined That Single Failure Criteria Not Met for All Ac Instrument Bus Alignments. Caused by Personnel Error.Evaluation Performed to Determine Feasibility of Performing Design Mods
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000255/LER-1988-012, :on 880808 & 1205,unusual Event Declared Due to Plant Chemistry Notifying Shift Supervisor of Secondary Leak Rate at 0.31 Gpm.Caused by Damaged Tube Due to Either Plate Stress,Plate Growth or Tube Denting |
- on 880808 & 1205,unusual Event Declared Due to Plant Chemistry Notifying Shift Supervisor of Secondary Leak Rate at 0.31 Gpm.Caused by Damaged Tube Due to Either Plate Stress,Plate Growth or Tube Denting
| | | 05000255/LER-1988-013, :on 880822,control Room HVAC Sys Declared Inoperable for Failing to Meet Tech Spec Criteria.Caused by Open Electrical Penetrations in Control Room Floor.Tech Spec Test RO-28 Revised to Correct Fan line-up |
- on 880822,control Room HVAC Sys Declared Inoperable for Failing to Meet Tech Spec Criteria.Caused by Open Electrical Penetrations in Control Room Floor.Tech Spec Test RO-28 Revised to Correct Fan line-up
| 10 CFR 50.73(a)(2)(vi) 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000255/LER-1988-014, :on 880903,area Radiation Monitor Inadvertently Struck,Resulting in Automatic Actuation of Containment Isolation Sys.Caused by Workmen Performing Activities from Reactor Cavity Deck.Monitor Reset |
- on 880903,area Radiation Monitor Inadvertently Struck,Resulting in Automatic Actuation of Containment Isolation Sys.Caused by Workmen Performing Activities from Reactor Cavity Deck.Monitor Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1988-015, :on 880903,fuel Bundle Observed Hanging from Bottom of Upper Guide Structure.Caused by Bundle Adhering to Guide Pins.Remainder of Fuel Bundles in Core Visually Inspected |
- on 880903,fuel Bundle Observed Hanging from Bottom of Upper Guide Structure.Caused by Bundle Adhering to Guide Pins.Remainder of Fuel Bundles in Core Visually Inspected
| | | 05000255/LER-1988-016, :on 880911,inadvertent Containment Isolation Signal Received When Temporary Filter Element Carried by Radiation Monitor RIA-231.Caused by Temporary Filter Element Being Removed from Containment.Monitor Reset |
- on 880911,inadvertent Containment Isolation Signal Received When Temporary Filter Element Carried by Radiation Monitor RIA-231.Caused by Temporary Filter Element Being Removed from Containment.Monitor Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1988-017, :on 880911,inadvertent Containment Isolation Signals Received.Caused by Electrical Noise Generated from Starting & Stopping Motor for Temporary Pump Which Seized. Logic Reset & Failed Pump Replaced |
- on 880911,inadvertent Containment Isolation Signals Received.Caused by Electrical Noise Generated from Starting & Stopping Motor for Temporary Pump Which Seized. Logic Reset & Failed Pump Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1988-018, :on 881027,inadvertent Containment Isolation Signal Received.Caused by Personnel Error & Inadequate Communication.Administrative Procedures 9.05 & 4.03 Revised |
- on 881027,inadvertent Containment Isolation Signal Received.Caused by Personnel Error & Inadequate Communication.Administrative Procedures 9.05 & 4.03 Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1988-019-01, :on 881001,inadvertent Containment Isolation Actuation Signal Received During Performance of post-mod Test to Verify Proper Reinstallation of Left Channel Containment High Radiation Initiate Switch |
- on 881001,inadvertent Containment Isolation Actuation Signal Received During Performance of post-mod Test to Verify Proper Reinstallation of Left Channel Containment High Radiation Initiate Switch
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000255/LER-1988-020, :on 881027,as-found Lift Pressure of Pressurizer Safety Valve RV-1039 Exceeded Tech Spec Limits. Cause Unknown & Under investigation.RV-1039 Disassembled, Inspected & Adjusted & Valve Disc Replaced |
- on 881027,as-found Lift Pressure of Pressurizer Safety Valve RV-1039 Exceeded Tech Spec Limits. Cause Unknown & Under investigation.RV-1039 Disassembled, Inspected & Adjusted & Valve Disc Replaced
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1988-021, :on 881104,several Spurious Unexplained Svc Water Pump Trips Occurred.Caused by Original Relay Settings Which Did Not Account for Motor Svc Factor Rating.Protective Relays Reviewed |
- on 881104,several Spurious Unexplained Svc Water Pump Trips Occurred.Caused by Original Relay Settings Which Did Not Account for Motor Svc Factor Rating.Protective Relays Reviewed
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000255/LER-1988-022, :on 881202,foreign Matl on Valve Seat Resulted in Inoperable Isolation Valve.Valve CV-1037 Disassembled, Inspected & Repair & Procedures Re Cleanliness Control Upgraded |
- on 881202,foreign Matl on Valve Seat Resulted in Inoperable Isolation Valve.Valve CV-1037 Disassembled, Inspected & Repair & Procedures Re Cleanliness Control Upgraded
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000255/LER-1988-023, :on 881117,component Cooling Water Room Radwaste Drain Line Isolation Valve MV-RW118 Found Not Fully Closed.Caused by Inadequate post-mod Testing of Installed Chain Operator.Valve Operator Modified |
- on 881117,component Cooling Water Room Radwaste Drain Line Isolation Valve MV-RW118 Found Not Fully Closed.Caused by Inadequate post-mod Testing of Installed Chain Operator.Valve Operator Modified
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000255/LER-1988-024, :on 881224,14% of Contents of Waste Gas Decay Tank T-68A Released Contrary to Plant Tech Spec 3.24.6. Caused by Operator Error.Sop 18A, Radwaste Sys - Gaseous Revised |
- on 881224,14% of Contents of Waste Gas Decay Tank T-68A Released Contrary to Plant Tech Spec 3.24.6. Caused by Operator Error.Sop 18A, Radwaste Sys - Gaseous Revised
| 10 CFR 50.73(a)(2)(i) | | 05000255/LER-1988-025, :on 881226,reactor Regulating Rod Group 3 Not Fully Withdrawn While Rod Group 4 Withdrawal Continued. Caused by Personnel Error.Event Reviewed w/on-shift Personnel by Operations Superintendent |
- on 881226,reactor Regulating Rod Group 3 Not Fully Withdrawn While Rod Group 4 Withdrawal Continued. Caused by Personnel Error.Event Reviewed w/on-shift Personnel by Operations Superintendent
| 10 CFR 50.73(a)(2)(i) |
|