ML18052B436

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Insp Rept 50-255/87-27 on 871026-30 & 1217.Violations Noted. Major Areas Inspected:Electrical & Mechanical Mods, Electrical & Mechanical Maint Activities,Operations & Sys Using Selected Portions of Modules
ML18052B436
Person / Time
Site: Palisades Entergy icon.png
Issue date: 12/23/1987
From: Cox T, Falevits Z, Jablonski F, Kropp W, Stasek S, Walker H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18052B434 List:
References
50-255-87-27, NUDOCS 8801060184
Download: ML18052B436 (16)


See also: IR 05000255/1987027

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION III*

Report No. 50-255/87027(DRS)

Docket No. 50-255

Licensee:

Consumers Power Company

212 West Michigan Avenue

Jackson, MI

49201

Facility Name:

Palisades Nuclear Generating Plant

Inspection At:

Covert, Michigan

Inspection Conducted:

October 26-30 and December 17, 1987

1-/)~b~l~'

Inspectors:* T.~o~

Qy~

Approved By:

~~

z. F~1rvi~

c;.~

S. Stasek

7- .9 ~ C)_~~<:;~ 'fui-*

H. J£1tM

1

1~/,t::,7,

W. Kropp

Team Leader

7-~I Q.ga.et~o~'

Frank J. lJa~nski, Ch1ef

Maintenance and Outage Section

Inspection Summary

License No. DPR-20

t2/2 3/g7

Date '

12/23/zz

Date ~ *

z/i
i/81

Date

/2-0 3187

Dat'e

t

1z/2:r/1ri

Date

/2/23/87

Dat'i

/

Inspection on October 26-30 and December 17, 1987 (Report No. 50-255/87027(DRS))

Areas Inspected:

Special, announced team inspection of licensee action on

previous inspection findings; electrical and mechanical modifications;

electrical and mechanical maintenance activities; operations and systems using

selected portions of Modules 37702, 62700, 62702 and 92720.

Results:

In the areas inspected, two violations were identified (lack of timely

corrective actions, (Paragraphs 2.d and 3.d(3)) and failure to follow procedures

in electrical maintenance (Paragraph 3.c(l)). Overall the team concluded that

licensee performance was continuing to improve in the maintenance and

modification programs; thereby, contributing to the continued improvement in the

material condition of the plant.

~~01060184 87!229

PDR

ADOCK 05000255

Q

DCD

1.

Persons Contacted

Consumers Power Company (CPCo)

D. Hoffman, Plant Manager

DETAILS*

R. Brazezinski, Instrument and Control Superintendent

R. Fenech, Operations Superintendent

D. Joos, Planning and Administrative Manager

R. Kasper, Electrical Maintenance Superintendent

  • C. Kozup, Technical Engineer

J. Lewis, Plant Technical Director

D. Malone, Nuclear Licensing Analyst

R. McCaleb, QA Director

R. Orosz, Engineering and Maintenance Manager

K. Osborne, Projects Superintendent

J. Palmisano, Systems Engineering Superintendent

R. Ricek, Operations Manager

H. Tauney, Mechanical Maintenance Superintendent

Nuclear Regulatory Commission (NRC)

B. Burgess, Section Chief, Projects Section 2A

F. Jablonski, Section Chief, Maintenance and Outage Section

T. Wambach, Licensing Project Manager

The above listed individuals attended the exit meeting on October 30,

1987.

Other licensee personnel were contacted as a matter of routine

during this inspection ..

  • Attended exit meeting via telephone on December 17, 1987.

2.

Licensee Actions on Previous Inspection Findings

a.

(Closed) Open Item (255/86035-01):

Commitment for preventive

maintenance (PM) on the fluid drive on Coolant Charging Pump P-55A.

The inspector reviewed documentation to substantiate that PM

activities were identified for the fluid drives.

These PM activities

pertained to changing the fluid-drive oil every year and rebuilding

the fluid drives every five years.

This matter is closed.

b.

(Closed) Open Item (255/86035-04):

Commitment for PM on condenser

hotwell cleaning.

The inspector reviewed documentation to

substantiate that a PM for condenser hotwell cleaning was identified

and scheduled for implementation.

This PM was tp be performed during

refueling outages.

This matter is clos~d .

2

c.

(Closed) Open Item (255/86035-05):

Commitment for PM on feedwater

recirculation valve inspection.

The inspector verified that a PM

activity had been identified for implementation during refueling

outages.

This matter is closed.

d.

(Closed) Open Item (255/86035-137):

The worst limiting accident

analysis for the charging pumps is the Main Steam Line Break (MSLB)

which requires 68 gpm to the core.

This flow is equivalent to two

charging pumps.

Palisades has three charging pumps; however, only

the

11A

11 and

11C

11 charging pumps wil 1 start from a Safety Injection

Signal.

The Palisades Technical Specification requires that two

e.

pumps be operable, but does not distinguish between the three pumps.

At the time of this inspection, the licensee's status of this item

was closed.

Information provided to the inspector to substantiate

this position consisted of a proposed revision to the FSAR that did

not address this open item.

Upon further review, the inspector

determined that the licensee had erroneously identified this item as

closed based on a proposed revision to the FSAR for another NRC issue.

As a result, inconsistencies in the operability requirements for the

charging pumps existed in the operating procedures, FSAR, and

Technical Specifications for several months.

This is an example of

not taking adequate and timely corrective action, and is considered

a violation of 10 CFR 50, Appendix 8, Criterion XVI .(255/87027-0la).

Therefore, the open it~m is closed but has been upgraded to a

violation.

In addition, the inspectors determined that the licensee did not have

an adequate system to track or keep status of issues identified by

the NRC.

Specifically, the licensee did not have:

An established method to verify acceptability of actions planned

and/or implemented to close issues identified by the NRC.

Ongoing knowledge of the specific steps and/or documentation

required to close issues identified by the NRC.

i

These weaknesses should be reviewed by the licensee to ensure that

  • timely closure of other NRC identified issues is accomplished.

This

is an open item (255/87027-02).

(Closed) Open Item (255/87023-01):

This item concerned the failure

of the mechanical maintenance organization to maintain the status of

replacement parts for maintenance work orders scheduled for work

during the outage.

Fourteen mechanical related work orders were on

hold for replacement parts and current procurement status was not

known.

During this inspection, the inspector noted that three of the

fourteen work orders were still on hold for parts. In addition to

these three, two more work orders had been added to the list due to

emergent work.

Mechanical maintenance personnel knew the current

status and were tracking the five procurements.

This matter is closed.

One violation was identified.

3

3.

Assessment of Maintenance and Modifications

This inspection was conducted to assess th~ licensee's progress regardin~

improvements in Palisades* maintenance and modification programs.

This

inspection was scheduled to coincide with a planned outage.

A previous

NRC inspection by Region III personnel assessed the licensee's planning

activities for this outage.

That inspection was conducted September 21-25,

1987, and documented in Inspection Report No. 50-255/87023.

Based on

results of this inspection, it appeared that the licensee's preoutage

planning activities were a success in further reducing the backlog of

maintenance work orders.

To assess the licensee's progress in improving the material condition of

the plant, the team evaluated specific areas of electrical/mechanical

maintenance and modification programs and system operations by review of

logbook entries, work orders, and modification packages, observation of

work and operations, and interviews.

Specific areas assessed included:

Threshold for placing equipment problems on maintenance work orders.

Corrective actions associated with equipment problems.

Progress towards the desired goal of approximately 50% of the

maintenance activities being classified as preventive maintenance.

Availability and accuracy of system design information.

Training of maintenance personnel.

Results of the inspection are documented in the following sections.

a.

Plant Personnel Perspectives

b.

The inspectors interviewed maintenance, operations, and QA personnel.

Those individuals interviewed were eight maintenance workers, two

maintenance.supervisors, three QA individuals, five control room

operators, and two shift supervisors.

The inspectors ascertained

that there was good morale, an attitude to perform activities right

the first time, continued improvement in communications between plant

departments, continued commitment by plant management to improve the

maintenance program, and continu~d commitment to improve the material

condition of the plant; however, management should continue to be

actively involved in plant activities to ensure continued improvement

in the material condition of the plant.

Design Control

The inspectors reviewed design change packages and modifications-*

performed by the licensee's on-site engineering organization to

determine technical adequacy and conformance to regulatory

4

requirements and industry standards.

Work associated with the* design

change packages and modifftations was examined .in the field. The work

examined was of acceptable quality and the work areas were clean and

organized.

During the review of the design change packages, the

inspectors focused specifically on 10 CFR 50.59 reviews, procedural

compliance, and the need for preventive maintenance.

( 1)

E'l ectrica l

  • The inspectors selected the following electrical Facility Change

(FC) and Specification Change (SC} packages for review.

In

addition, the inspectors examined the field work associated with

these packages:

FC-687

SC-87-14

Addition of Local/Remote Transfer Switch to

Breaker, 152-106.

Addition of diodes to annunciator circuitry for

High Pressure Safety Injection (HPSI) motor .

operator valves (MOV) to eliminate signal feedback.

At the time of this inspection, the modification associated

with package FC-687 had been installed and tested while package

SC-87-14 was in the initial stages of design .

In regards to FC-687, the inspectors performed a detailed

document review and a visual inspection of the field installed

modification.

The facility change package contained documents

that pertained to: design reviews; 10 CFR 50.59 evaluations;

QA/QC requirements; testing requirements; and methods for

.installing the modifications. The licensee's review of this

package determined that the modification was adequately designed,

reviewed, and implemented; however, the inspectors determined

that Schematic Diagram E-5, Sheet 15, Revision 5 had not been

revised to incorporate modification FC-687.

The NRC previously

identified a violation in Inspection Report No. 50-255/86028

that identified electrical drawing as-built inaccuracies. The

  • licensee's corrective action ta that violation included

establishment of a Configuration Control Project (CCP) to resolve

the electrical drawing inaccuracies. Effectiveness,of the CCP

could be adversely affected if management attention is not given

to future modifications. This matter is an unresolved item

(255/87027-03).

An associated concern not affected by FC-687, pertained to

Schematic Diagram E-129, Sheet 1, Revision C, which did not have

a switch development for local control switth 52/CS-L and did

not depict the field installed overcurrent relays test swffi:hes.

This concern should be resolved during the implementation of the

electrical walkdown portion of the CCP.

5

-

Another concern pertained* to resolutions of* an engineer's

comments on a document review sheet that were not included in ,

the resolution column; however, the resolutions did not have ari

adverse effect on FC-687.

The matter of assuring that

resolutions to comments are documented was discussed with the

licensee.

In regards to Specification Change SC-87-14, the inspectors

reviewed the preliminary design for technical adequacy.

SC-87-14

was initiated as a result of a system functional evaluation test.

While performing this test, the licensee temporarily installed an

electrical jumper to simulate an electrical overload condition

on one motor operated valve (MOV).

Instead of activating an

alarm indicating one MOV overload, the control room operators

received alarms indicating two MOV overloads.

The licensee

determined that there was a feedback signal which caused the

erroneous alarms and diodes will be added in the annunciator

control circuitry to correct the problem.

The inspectors

reviewed the preliminary design associated with SC-87-14 that

appeared to resolve the feedback problem; however, it was unclear

to the inspectors why post modification testing, performed five

years ago for the original alarm i.nstallation, did not identify

the feedback problem. The licensee should determine why original

post modification tests did not identify the feedback problem and

apply any lessons learned to future modifications. This is an

open item (255/87027-04).

In conclusion, the inspectors determined that the licensee's

electrical design control process for modifications had

continuqd to improve and a positive attitude was noted during

discussions with field engineers. The inspectors determined

that the 10 CFR 50.59 evaluations were adequate .. Except for.

the concerns identified by the inspectors, procedural compliance

was acceptable.

.

(2) Mechanical

During this inspection*, the following mechanical FCs and SCs

were reviewed by the inspectors. Included was an inspection of

. field work associated with these design changes.

FC-725

Fc,...773

SC-87-141

SC-87-203

SC-87-306

Replacement of Atmospheric Steam Dump Valves.

Electro-Hydraulic Control (EHC) System

Modification

Replacement of Drain Valves for a Feedwater

Heater .

Snubber Reduction Programs.

Change MV-3232, Containment Spray Pump

Recirculation Valve, from Velan to a Vogt.

6

The documents in these packages were generally consistent with

the plant procedures used to control *and manage design*changes~

Some inconsistencies with current plant procedures were noted,

individually not serious, but collectively indicated that

additional attention to detail was required during the review

process.

The inspectors identified concerns with Safety

Evaluations (SE) (10 CFR 50.59); however, during a previous

inspection, Inspection Report 50-255/86035, concerns were

identified with the SE process and resulted in the issuance of

a violation (255/86035-152) that is still open.

At the time of

the inspection, the licensee had not revised Administrative

Procedure 3.07, "Safety Evaluation,

11 to resolve the violation.

Inspection Report 50-255/87018 also identified concerns with the

SE process.

During a meeting prior to the exit, the licensee

committed to revise Procedure 3.07 prior to January 1, 1988.

This commitment will be tracked with violation 255/86035-152.

The following concerns, not related to the SE process, were

identified:

(a) Preventive Maintenance (PM) requirements were not adequately

addressed for FC-725.

The Design Document Checklist

stipulated that maintenance requirements were applicable;

however, the PM procedures were not identified.

Also, there

was no objective evidence in the FC package that indicated a

review was conducted of the PM procedures for the

Atmospheric Dump Valves to determine applicability for the

new Masoneilan valves.

The existing PM procedures were

written for the originally installed Copes-Vulcan valves.

Pending further review, this is an open item (255/87027-05).

(b) The Design Input Checklist, Design Document Checklist, and

the Design Review Checklist in the package for FC-773 did

not specify any PM activity for the modified EHC components.

Although non-safety related, the EHC system's function is

important and lack of reliability could lead to spurious

plant trips.

Discussion with the Project Engineer

determined that PM was planned.

Pending further review of

the PM program for the EHC system, this is an open item

(255/87027-06).

(c) Section 15 of the Design Input Checklist for the EHC

modification did not identify any 11additional QA/QC

requirements;

11 however, an excerpt from Section 15 of the

checklist stipulated

11for certain jobs or special processes

not covered by the codes, additional QA/QC requirements may

be desired.

The case of a non-Q (non-safety-related) job

with high reliability aspects and a desire for QC is .. an *

example. 11

The inspectors expected QC involvement since the EHC system

requires high reliability to preclude unnecessary challenges

7

to the reactor systems, and previous Palisades experience

included reactor trips due to the EHC component problems ..

There was no evidence that personnel were involved in QC *

activities.

Future modifications of high reliability

systems with previous experience of causing reactor system

challenges will be evaluated for appropriate QC involvement

in a future NRC inspection.

This is an open item

(255/87027-07).

In conclusion, the inspectors determined that mechanical design

packages were generally acceptable for control of a facility

change or specification.

As previously stated, inconsistencies

with current plant procedures were noted that indicate additional

attention to detail in the design review process was required.

c.

Maintenance

The inspectors interviewed maintenance personnel to ascertain the

threshold for identifying equipment problems on maintenance work

requests and to determine the effectiveness of maintenance activities.

The inspectors reviewed:

Completed work orders

Maintenance procedures

Craft training

Status of corrective and preventive maintenance (PM) activities *

Control room logbooks

Licensee corrective action documents

Ongoing maintenance activities

Computer printouts of outstanding PM and Corrective Maintenance

Work Requests.

(1) Electrical Maintenance

The inspectors reviewed eleven work ord~rs of which five

pertained to ongoing maintenance activities.

The inspectors

verified that maintenance activities had been adequately

preplanned and correctly prioritized by the review and

observation of field implemented work orders.

Instructions were

appropriately detailed and applicable proce9ures were included in

the work order packages.

Also, the inspector verified that:

Applicable Technical Specification and plant conditions were

noted;

Special safety and QC requireme!1ts were noted;

8

(2)

Operability test requirements were specified;

Provisions to summarize work performed were made; and

Required administrative reviews were completed prior to

declaring the system operable.

The maintenance staff had a positive attitude and appeared to be

knowledgeable of assigned tasks.

The inspectors did identify an

anomaly in the issuance of a work order 24500885 for maintenance

of the diesel generator crankcase exhaust motor.

This work order

was originally planned and written in April 1985; however, the

work order was issued in October 1987, without a current review

by the work planner or maintenance supervisor.

As a result, the

work order package did not contain or reference two procedures

that were applicable in October 1987, but not in April 1985.

These two procedures were:

SPS-E-7, which delineated

requirements for electrical resistance tests; and MSE-E-12, which

delineated the requirements for electrical terminations~ The

crankcase exhaust motor was not resistance tested prior to

disassembly and QC was not notified to witness the test as

required by procedure SPS-E-7.

Failure to review Work Order 24500885 prior to issuance for work is an example of an

improperly planned maintenance activity.

Licensee Administrative

Procedure 5.01, "Processing Work Requests/Work Order" requires a

review of work orders by the Work Planner, Maintenance Supervisor,

and others to ensure that all necessary documents and

instructions were identified.

Failure to review Work Order 24500885 for the diesel generator crankcase exhaust motor prior

to issuance is an example of a violation of Technical

Specification, Section 6.8.1.a. (255/87027-08).

Mechanical

The inspectors reviewed four work orders for which work had

been completed in the field.

These work orders were identified

as

11open

11 pending completion of operability testing.

The

inspectors reviewed the documentation in these work packages.

Based on these reviews, no problems were identified with the

maintenance activities; however, a problem was identified in

one of the work orders that was not directly related to

maintenance activities.

Work Order 24706014, involved the

disassembly and inspection of an auxiliary feedwater motor

operated valve (M0-0743) due to excessive cycling.

The valve

cycled open and then closed continuously for at least 22 hours2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br />,

which exceeded the designed operations for some of the Limitorque

valve operator components.

Failure to remove a jumper, which had

been placed in the valve operator circuitry during MOVATS *testing,

caused the excessive cycling.

Failure to remove the jumper was

documented on Deviation Report (DR) No. D-PAL-87-1424, which was

issued on October 10, 1987.

The action described to prevent

9

d .

recurrence appeared to be adequate; however, during the

inspection three other problems pertaining to lifted leads and.

jumpers were identified.

See Paragraph 3.d:(3) of this report

for further details.

The inspectors also reviewed three work order packages that were

ready for work.

The work orders had the appropriate approvals,

contained adequate work instructions, applicable procedures, and

the necessary design information to perform the maintenance

activity.

The work was of acceptable quality and performed in

accordance with the work order packages.

The inspectors also

witnessed-maintenance associated with five work orders.

Maintenance personnel appeared to be knowledgeable of the work

and job instructions in the packages.

The packages contained the

necessary documents and informatfon, and no problems were noted.

The inspectors reviewed training requirements for maintenance

personnel classified as repairman A, repairman B, and welders.

Training records for five mechanical maintenance personnel were

selected for review.

During discussions with licensee personnel,

the inspectors were informed that due to union contracts,

upgrading of repairman levels to other classification levels was

based on length of service rather than training.

In some cases,

repairmen may not have completed the designated course for a

specific classification level.

To ensure that only qualified

personnel performed maintenance work, the licensee established a

qualifications system based on tasks. -During a review of a list

identifying qualified repairmen, the inspectors noted that 42 of

the*56 repairmen listed were qualified to perform more than

two-thirds of the listed task based solely on past experience.

There was insufficient time for the inspectors to review the

methods used for qualifying maintenance personnel by tasks.

This is an open item (255/87027-09).

In conclusion, the inspectors determined that corrective and

preventive maintenance activities appeared to be properly controlled:

The inspectors reviewed a report entitled

11WO Report - Count of Open

Work Order by Status,

11 dated October 28, 1987.

This report included

1,942.open maintenance work orders.

This number included 530 work

orders that were field complete, but were classified as

11 open

11 pending

completion of operability testing.

This left 1,412 open work orders

that field work had not been completed, which reflected a substantial

reduction in the number of open work orders from previous months.

In

addition, the inspectors determined that the licensee continued to

progress toward a maintenance program goal of approximately 50%

preventive maintenance.

Based on this inspection, the inspectors

concluded that maintenance activities were effectively implemented.

Operations and Systems

To assess the level of involvement by operations in maintenance, the

inspectors observed control room activities, reviewed appropriate

logbooks and status boards maintained by.the Operations Department,

10

and conducted interviews involving two shifts of operators and shift

supervisors.

System/Component inspections of the 1-1 and 1-2 Diesel

Generators (DIG) were conducted to ascertain the material condition

and to verify that appropriate work requests had been initiated to

maintain the systems operable.

The inspectors also reviewed a recent

event, loss of shutdown cooling, which occurred on October 15, 1987.

Reviews to assess the adequacy of post maintenance/modification

testing were performed for several Facility Changes, Specification

Changes, and Work Orders.

(1) Control Room Activities

(2)

The inspectors reviewed control room and shift supervisor's

logbooks, switching and tagging order logbook, current LCO status

board entries, and current equipment status board entries to

verify proper implementation of administrative procedures that

controlled removal and restoration of equipment.

The inspectors

also reviewed Administrative Procedures 4.01, "Shift Operations,

11

4.03, "Equipment Control,

11 and 5.01;

11 Processing Work Requests/

Work Orders,

11 and interviewed several plant operators and shift

supervisors to assess levels of familiarity with the requirements

contained within those procedures.

During review of the control room logbooks, the inspectors noted

that some entries appeared to be incomplete or missing.

There

were entries that documented equipment returned to an operable

status without a corresponding prior logbook entry which

documented removal of the equipment from service.

Also, there

were entries that identified the initiation of surveillance

activities, but no subsequent entries showing completion.

It

was determined that the missing entries from the control room

logbooks had been included in the shift supervisor 1s logbook,

Palisades Nuclear Plant Administrative Procedure 4.01,

11Shif;t

Operations,

11 delineates the types of entries required in each

logbook.

The control room logbook entries noted as incomplete

were required in the control room logbooks and the shift

supervisor's logbook.

This indicated an apparent weakness on the

part of plant operators to properly implement that portion of

Administrative Procedure 4.01 which addresses control room

logbooks.

The quality of logbook keeping is considered an

unresolved item (255/87027-10).

The inspectors did determine

that equipment problems noted in the control room logbooks had

been identified on work orders.

System Walkdown

The inspectors conducted a walkdown inspection of the 1-1 and

1-2 DGs to ascertain the material condition.

The inspectors were

primarily interested in fluid leaks and operability of individual

components.

The inspectors verified that all conditions

identifiable as potentially degradable to the DGs continued

11

operability had been identifie~ by plant personnel and tagged

with Component Problem Identification Tags (CPITs) .. The *1-1 OG

had 16 CPITs and the 1-2 OG had 13 CPITs on individual components

at the time of the walkdown.

The inspectors verified that each

CPIT was directly traceable to a work request initiated to

correct the particular problem and was properly prioritized.

The material condition of the OGs was determined to be acceptable.

(3) Maintenance Related Events

The inspectors reviewed several events that occurred over an

eight day period which culminated in loss of shutdown cooling on

October 15, 1987.

The following is the sequence of these events:

(a)

(b)

On October 7, 1987, while MOVATS, Inc. personnel* were

performing diagnostic tests of valve M0-0798 (Auxiliary

Feedwater to Steam Generator ESOB Isolation), an electrical

jumper was inadvertently installed in the circuitry involved

with M0-0760,

This problem was detected during the test

when M0-0798 could not be locally closed at the step

required by the procedure.

The licensee subsequently

determined that the improperly installed jumper was a

result of MOVATS testing personnel being unfamiliar with

Palisades electrical drawing schemes.

To preclude

. recurrence, the licensee assigned an electrical engineer

to augment the MOVATS team and increase involvement in

MOVATS testing activities.

Upon identification of thfs

problem, plant personnel took steps to correct the

situation; however, no Deviation Report was.initiated in

accordance with Palisades Administrative Procedure 3.03,

11Corrective Action.

11

On October 8, 1987, upon completion of MOVATS diagnostic

tests, valve M0-0743 (Auxiliary Feedwater isolation

va1ve) was reenergized with an electrical jumper still

installed.

As a result, and not known to operations

personnel, valve M0-0743 cycled open and closed for 22

hours.

M0-0743 was deenergized and work orders initiated

to disassemble and inspect both the valve and operator.

Deviation Report (OR), D-PAL-87-142, was issued to document

.this event.

This OR described the event in regard to the

jumper not being removed, which resulted in the cycling of

valve M0-0743; however, the DR described the cycling as

11an extended period of time

11 instead of specifically

stating 22 hours2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br />.

The DR did not address the reason the

cycling of the valve was not identified by operations

personnel.

The inspector was concerned since valve position indicating

lights for M0-0743 operated correctly in the control room

during the approximately 2000 complete cycles from open to

close.

12

(c)

On October 9, 1987, during tests of valve M0-3080 (High

Pressure Safety Injection Mode Selection Valve) MOVATS

personnel identified that lifted leads had not been logged

by the previous shift as required by procedures.

Upon

identification, the MOVATS personnel verified that the

proper leads were lifted and documented the condition on

the

11Jumper/Lifted Wire Data Sheet;

11 however, a DR was not

issued to document the failure as required by Palisades

Administrative Procedure 3.03,*

11Corrective Actions.

11

(d)

On October 15, 1987, during diagnostic tests, an electrical

jumper was inadvertently installed in the circuitry of valve

M0-3008 (Low Pressure Safety Injection Cold Leg Isolation).

The jumper caused valve M0-3008 to begin cycling with a

resultant effect on Safety Injection pump

11A

11 discharge

pressure.

Because of a concern for pump cavitation,

operations personnel secured the pump and deenergized

M0-3008.

As a result, shutdown cooling was termin~ted for

approximately 26 minutes that resulted in an increase of

37 degrees in reactor coolant temperature.

The events described above all occurred during the diagnostic

testing of valves by a site contractor, MOVATS, Inc.

In response,

the licensee took steps to correct the specific problem(s)

identified in each case; however, corrective actions to raise

the overall level of licensee control of this contractor's

activities were untimely as shown by the continued events.

This

failure to take timely corrective action to preclude repetition

is considered an example of a violation of 10 CFR 50, Appendix B,

Criterion XVI (255/87027-018).

During review of the above events,

the inspectors identified the following concerns that should be

included in the licensee's corrective actions:

Site contractor's activities need to be strengthened,

especially in the area of preplanning.

There is a weakness in implementation of the

11 jumper

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program by plant personnel; licensee personnel were directly

participating with MOVATS personnel in the placing of

electrical jumpers, yet serious performance problems

occurred ..

An in-depth evaluation of the DR process should be

performed by the licensee since three of the events

identified above were either not documented or were

inadequately described on ORs.

With respect to the October 8 event, an apparent weakness ~xisted

with operator awareness of plant systems status since valve

M0-0743 cycled for approximately 22 hours2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br /> without the cognizance

of operations personnel.

A contributing factor appeared to be

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the absence of any direct means to aid the operator_ in

ascertaining system/component status from the panels.

Currently,

to determine equipment status, operators must review logbooks and

status boards.

If some means had existed to directly identify

the status of M0-0743 at the panel, the cycling of the valve may

have been detected sooner than 22 hours2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br />.

The licensee agreed to

evaluate the inspector's concern in this area.

This is an open

item (255/87027-11).

(4) Post Modification/Maintenance Testing

The following FCs, SCs, and Work Orders (W.O.s) were reviewed

to determine if the specified post modification/maintenance

testing was adequate to ensure equipment operability.

FC-87-001

Installation of Remote/Local Transfer Switch

and Associated Fused for Breaker 152-106.

FC-725

Replacement of Atmospheric Steam Dump Valves.

'FC-773

Upgrade of EHC System Hydraulic Tubing and

Associate Fittings.

SC-87-141

Replacement of MV-FW501 and MV-FW501A Vogt

Globe Valyes with Vogt Gate Valves.

SC-87-306

Replacement of MV-3232 2 inch Velan Valve

with a 2-inch Vogt Valve.

W.O. 24704920

Investigate/Correct Stroke Time Increase on

CV-04388.

W.O. 24704922

Investigate/Correct Stroke Time Increase on

CV-0437B.

W.O. 24705607

PM for P64A (North Hotwell Sample Pump).

The inspectors determined that the post modification/maintenance

testing associated with the above FCs, SCc, and W.O.s appeared

adequate to ensure operability of the affected equipment.

One violation and an example of another violation were identified.

e.

Canel usi ons

Based on inspection activities described in this report, the

inspection team concluded:

The threshold for placing equipment problems on maintenance work

orders was sufficient to maintai'n the material condition of the

plant at an acceptable level.

This conclusion was based on

interviews, walkdown of both diesel generators, review of control

room logbooks, and review of work o~der computer printouts.

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Corrective actions for equipment problems appeared adequate and

focused towards the root. *cause.

This conclusion was based on ,

review of various corrective actions documents, cohtr61 room

logbooks, and Component Problem Identification*Tags (CPIT) for

the diesel generators.

Interviews with personnel did not

disclose any instances where rework was excessive.

Preventive Maintenance (PM) was progressing towards the desired

goal of approximately 50% of the maintenance activities; This

conclusion was based on a review of computer listing of PMs, an

interview with the Mechanical Maintenance Supervisor and a review

of a computer listing of overdue PMs.

Availability and accuracy of mechanical design documents were

generally acceptable to support the processing of mechanical

modification packages; however, management attention is

required to ensure that electrical drawings are revised to

reflect future modifications.

Additional management involvement

is necessary in this area.

Except .for this particular weakness,

the team concluded that the electrical modification activities

had improved since the last NRC inspection in this area.

The training program for maintenance personnel appeared to be

effectively implemented.

This conclusion was based on reviewing

training records for maintenance personnel and the absence of

problems while witnessing maintenance activities.

The

maintenance training program was recently accredited by INPO.

Prior planning and assignment of priorities in maintenance

activities was evident in resolving equipment problems.

Management's involvement has resulted in improving maintenance

and modification activities, thus improving the material

  • condition of the plant.

Management involvement with contractor work activities needs

improvement in the area of orientation and training.

Management attention should be directed towards establishing a

more viable system for tracking and status of NRC identified

problems.

Management involvement needs improvement in the area of timely

corrective actions.

This was evident in the events preceding

the loss of shutdown cooling on October 15, 1987.

One violation and an example of another violation was identified.

4.

Open Items

Open items are matters that have been discussed with the licensee, which

will be reviewed, further, and involve some action on the part of the NRC

_or licensee or both.

Open items identified during the inspection are

discussed in Paragraphs 3.b(l), 3.b(2), 3.c(2l, and 3.d(3).

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5.

Unresolved Items

Unresolved .items are matters about which more information is required in

order to ascertain whether they are acceptable items, violations, or

deviations.

Unresolved items disclosed during this inspection are included

in Paragraphs 3.b(l) and 3.d(l).

6.

Exit Interviews

The inspectors met with licensee representatives (denoted in Paragraph 1)

on October 30, 1987, at the Palisades Plant and discussed by telephone on

December 17, 1987, and summarized the purpose (scope) and findings of the

inspection.

The inspectors discussed the likely informational content of

the inspection report with regard to document or processes reviewed by the

inspectors during the inspection.

The licensee did not identify any such

documents or processes as proprietary.

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