05000255/LER-1980-026-03, /03L-0:on 800719,during Refilling of Safety Injection tanks,FT-0313 Found Inoperable.Caused by Failure to Close Instrument Equalizing Valve During Recent Calibr

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/03L-0:on 800719,during Refilling of Safety Injection tanks,FT-0313 Found Inoperable.Caused by Failure to Close Instrument Equalizing Valve During Recent Calibr
ML18045A523
Person / Time
Site: Palisades Entergy icon.png
Issue date: 08/18/1980
From:
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML18045A521 List:
References
LER-80-026-03L, LER-80-26-3L, NUDOCS 8008220236
Download: ML18045A523 (1)


LER-1980-026, /03L-0:on 800719,during Refilling of Safety Injection tanks,FT-0313 Found Inoperable.Caused by Failure to Close Instrument Equalizing Valve During Recent Calibr
Event date:
Report date:
2551980026R03 - NRC Website

text

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[]JI} I During refilling of Safety Injection tanks following sampling, it was

())!J I observed that FT-0313 (HSPI flow to loop 2B) was inoperable.

Instrument

((II] I was restored to operable status within time required by LCO of TS 3.17.

((IT] I (See LER 80-13. )

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