05000255/LER-1980-018-03, /03L-0:on 800522,during Routine Testing of Hydraulic Snubbers,Oil Level in Snubber 2 Was Found to Be Less than Zero & Was Declared Inoperable.Apparently Caused by Seal Degradation

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/03L-0:on 800522,during Routine Testing of Hydraulic Snubbers,Oil Level in Snubber 2 Was Found to Be Less than Zero & Was Declared Inoperable.Apparently Caused by Seal Degradation
ML18045A273
Person / Time
Site: Palisades Entergy icon.png
Issue date: 06/19/1980
From:
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML18045A272 List:
References
LER-80-018-03L, LER-80-18-3L, NUDOCS 8006240513
Download: ML18045A273 (1)


LER-1980-018, /03L-0:on 800522,during Routine Testing of Hydraulic Snubbers,Oil Level in Snubber 2 Was Found to Be Less than Zero & Was Declared Inoperable.Apparently Caused by Seal Degradation
Event date:
Report date:
2551980018R03 - NRC Website

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I During routine testing of hydraulic snubbers, the oil level in. snubber -

CITIJ I No. 2 was fou..1'ld to be less than zero, and the. snubber was declared r::I:EJ inoperable.

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