05000255/LER-1979-040-01, /01T-0:on 790927,ultrasonic & Radiographic Examinations Revealed Linear Cracklike Indications on 18- Inch Main Feedwater Lines Inside Containment.Cause Unknown. Approx 28 Inches of Main Feedwater Pipe Being Replaced

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/01T-0:on 790927,ultrasonic & Radiographic Examinations Revealed Linear Cracklike Indications on 18- Inch Main Feedwater Lines Inside Containment.Cause Unknown. Approx 28 Inches of Main Feedwater Pipe Being Replaced
ML18043B100
Person / Time
Site: Palisades Entergy icon.png
Issue date: 10/12/1979
From:
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML18043B099 List:
References
LER-79-040-01T, LER-79-40-1T, NUDOCS 7910190369
Download: ML18043B100 (1)


LER-1979-040, /01T-0:on 790927,ultrasonic & Radiographic Examinations Revealed Linear Cracklike Indications on 18- Inch Main Feedwater Lines Inside Containment.Cause Unknown. Approx 28 Inches of Main Feedwater Pipe Being Replaced
Event date:
Report date:
2551979040R01 - NRC Website

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I Ultrasonic and radiographic exa.!nfnations have revealed linear cr~ck-like

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