05000255/LER-1979-039-03, /03L-0:on 790829,pH of Steam Generator a Dropped to 8.08 Following Change in Condensate Demineralizers.Caused by Increase in Demin Resin Level to Correct High Condenser Tube Leakage.Corrective Action Under Evaluation

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/03L-0:on 790829,pH of Steam Generator a Dropped to 8.08 Following Change in Condensate Demineralizers.Caused by Increase in Demin Resin Level to Correct High Condenser Tube Leakage.Corrective Action Under Evaluation
ML18043B069
Person / Time
Site: Palisades Entergy icon.png
Issue date: 09/28/1979
From:
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML18043B068 List:
References
LER-79-039-03L, LER-79-39-3L, NUDOCS 7910030391
Download: ML18043B069 (1)


LER-1979-039, /03L-0:on 790829,pH of Steam Generator a Dropped to 8.08 Following Change in Condensate Demineralizers.Caused by Increase in Demin Resin Level to Correct High Condenser Tube Leakage.Corrective Action Under Evaluation
Event date:
Report date:
2551979039R03 - NRC Website

text

PALISADES PL.A.NT NRC FORM366 f7*77)

U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT CONTROL BLOCK:.._!-'---'--"---'--'---'--CD 1

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ITifl I Follom.ng. a change: in condensate d~neralizers, the pH of the 'At steam generator dropped to 8.08.

Morpholine additions to bo~h S/G's resored pH I

to TS limits within the time allowed by TS 3.18.3.

Occurrence similar to [D}J 1 LER 79-032.

No threat to public health or safety existed.

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selectively remove ammonia and morpholine before sodium, a drop in pH IT))] I resulted.

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