05000255/LER-1979-029-03, /03L-0 on 790628:conductivity & Sodium Concentrations in a Steam Generator Increased in Excess of Tech Spec Limits.Caused by Leakage in Condenser Tube & Chemical Hideout Return as Result of Power Reduction

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/03L-0 on 790628:conductivity & Sodium Concentrations in a Steam Generator Increased in Excess of Tech Spec Limits.Caused by Leakage in Condenser Tube & Chemical Hideout Return as Result of Power Reduction
ML18043A878
Person / Time
Site: Palisades Entergy icon.png
Issue date: 07/26/1979
From:
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML18043A876 List:
References
LER-79-029-03L, LER-79-29-3L, NUDOCS 7908010508
Download: ML18043A878 (1)


LER-1979-029, /03L-0 on 790628:conductivity & Sodium Concentrations in a Steam Generator Increased in Excess of Tech Spec Limits.Caused by Leakage in Condenser Tube & Chemical Hideout Return as Result of Power Reduction
Event date:
Report date:
2551979029R03 - NRC Website

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PALISADES NRC FORM 366 (7-77)

U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT CONTROL BLOCK: I I 0 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6

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LICENSEE CODE 14

~5 LICENSE NUMBER 25 26

  • LICENSE TYPE 30 57 CAT 58 CON'T 0:2]

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~~~~~ L!:JG)I 01 51 o I 01 o I 21 515 101 o I 61 218 I 71 21@1o1.7 I 2 I 61 71 9 I© 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES @

I Following a power reduction in preparation for repairs of main condenser tube leaks, the conductivity and sodium concentrations in the A steam generator increased to 26.5 micro-mho/cm and 1.28 ppm respectively.

(B S/G conductivity - 25.0; sodium - 0.84.)

This was in excess of the limits of TS 3.18.1 Chemistry was returned to within s:vecifications (I]2J I within the time limits of TS 3.18.3 and 3.18.5.

No threat to public [II)) I health or safety existed.

Occurrence simi*J ar to LEE 79-02 8 and 79.;..027 I

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SYSTEM CODE IH IBI@

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LER/RO CVENTYEAR

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CAUSE

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CODE Io 121 9 i 1.....-1 I o I 31 23 24 26 27 28 29 COMP.

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30 VALVE SUB CODE LIJ@

20 l.=I 31 PRIME COMP.

REVISION NO.

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32 COMPONENT ACTION FUTURE EFFECT SHUTDOWN

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ATTACHMENT TAKEN ACTION ON PLANT METHOD HOURS SUBMl_TTED LxJ@l.ZJ@

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NPR0-4 FORM 5U8, SUPPLIER MANUFACTURER 33 34 35 36 37 40 41 Ur..l@>

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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @

43 44 47 ITITI I The out of SI?ecifi catj on condition resnl ted-_ "from a of

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condenser tube inleakage and chemical hideout return as a result of the power reduction.

The condition was corrected through S/G blowdown and plugging of leaking main condens.er tubes.

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9 FACILITY

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STATUS

% POWER OTHER STATUS ~

METHOD OF

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10 12 13 44 ACTIVITY CONTENT Cc\\

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10 11 44 45 46 80 80 45 LOCATION OF RELEASE @

NA PERSONNEL EXPOSURES

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NUMBER

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DESCRIPTION

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. PERSONNEL INJURIES Q

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9 11 12 80 LOSS o* OR DAMAGE TO FACILITY f'4:l\\

TYPE

DESCRIPTION

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