ML18043A824

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IE Insp Rept 50-255/79-07 on 790430-0504 & 09-11.No Noncompliance Noted.Major Areas Inspected:Licensee Response to IE Bulletin 79-06B Re Operability & Availability of Engineered Safety Features & Operator Training Procedures
ML18043A824
Person / Time
Site: Palisades Entergy icon.png
Issue date: 05/17/1979
From: Jorgensen B, Warnick R, Wright G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18043A823 List:
References
50-255-79-07, 50-255-79-7, NUDOCS 7907180411
Download: ML18043A824 (10)


See also: IR 05000255/1979007

Text

U.S. NUCLEAR REGULATORY COMMISSION

OFFICE OF INSPECTION AND ENFORCEMENT

REGION III

Report No. 50-255/79-07

Docket No. 50-255

License No. DPR-20

Licensee:

Consumers Power Company

212 West Michigan Avenue

Jackson, MI

49201

Facility Name:

Palisades Nuclear Generating Plant

Inspection At:

Palisades Site, Covert, MI

Inspection Conducted:

April 30-May 4 and May 9-11, 1979

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Inspectors: {""" B. L. Jorgensea_)

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r1'- G. C. Wright

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Approved Byi~R. F. Warnick, Chief

Reactor Projects Section 2

Inspection Summary

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Inspection on April 30-May 4 and May 9-11, 1979 (Report No.

50-255/79-07)

Areas Inspected:

Special, announced inspection of licensee activ-

ities in response to IE Bulletin 79-06B including operability and

availability of engineered safety features (ESF); administrative

control of ESF; ESF status at the time of inspection; operator

training; operating procedures; and licensee response to other

miscellaneous Bulletin items.

The inspection involved 122

inspector-hours onsite by two NRC inspectors.

Results:

No items of noncompliance or deviations were identified in

any of the areas inspected.

One unresolved item was identified

(Paragraph 4) relating to the necessity of obtaining both flowrate

and discharge pressure on inservice inspection of ESF pumps .

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1.

DETAILS

Persons Contacted

  • J. Lewis, Plant Superintendent
    • H. Keiser, Operations and Maintenance Superintendent
    • K. Berry, Technical Superintendent
  • R. McCaleb, Quality Assurance Superintendent
    • B. Shaner, Operations Supervisor
  • B. Harshe, Senior Engineer
  • G. Petitjean, General Engineer
    • R. Mieras, Shift Supervisor
  • D. Langschwager, Shift Supervisor

A. Brookhouse, Shift Supervisor

S. Ghidotti, Shift Supervisor

W. Thompson, Shift Supervisor

D. Kaupa, Shift Supervisor

K. Villermain, Control Operator

G. Cheeseman, Control Operator I

J. Ford, Control Operator I

G. Pothoff, Control Operator II

W. Stearns, Control Operator II

J. Liddell, Training Supervisor

C. Bills, Engineering Analyst

Some discussions were also held with eight additional oper-

ations staff personnel; control operators and auxiliary

operators.

  • present at inspection status meeting on May 4, 1979.
    • present at May 4 status meeting and at final exit inter-

view May 11, 1979.

2.

General

This inspection was conducted to review licensee activities in

response to IE Bulletin 79-06B "Review of Operational Errors

and System Misalignments Identified During the Three Mile

Island Incident." This review included verification of licensee

activities as identified in his initial written response to the

Bulletin and examination of other related activities.

This inspection also included an independent review by the

inspectors of records, procedures and equipment to determine

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3.

the continuous availability and operability of safety-related

systems and components as required.

During this inspection, direct training discussions were con-

ducted on May 2, 1979, with six members of the Palisades Plant

operating staff concerning the sequence of events at the Three

Mile Island Nuclear Station Unit 2 during and following the

loss of feedwater incident on March 28, 1979.

Sections of IE

Bulletin 79-06B were also discussed.

These training discussions

were provided for operating staff personnel not present during

previous presentations by an IE and NRR task group on April 19,

1979.

Thus, as of May 2, 1979, every member of the plant operating

staff had attended a direct training discussion on these subjects

provided by NRC.

Engineered Safety Features Availability/Operability

This inspection included a review of engineered safety systems

alignment procedures against current piping and instrument

diagrams and single-line diagrams to verify the alignments do

not compromise the availability or operability of safety-related

components.

Valve, breaker, and/or switch alignments were

examined for the following systems:

a.

High Pressure Safety Injection

b.

Low Pressure Safety Injection

c.

Charging Pumps

d.

Component Cooling Water

e.

Auxiliary Feed Water

f.

Service Water (emergency services portions)

g.

Containment Isolation Systems

h.

Emergency Diesel Generators

i.

Safety Injection Tanks

j.

Containment Spray

k.

Containment Fan Coolers

The reactor protection and safeguards actuation circuitry were

also reviewed briefly, as were portions of the primary coolant

system.

Lineups are provided, for the most part, by checklist.

The

same checklist for proper lineup may be referenced by various

procedures.

Where checklists were so referenced, they were

utilized for the inspection.

For some operations surveillance

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tests, return-to-service lineups are specified within the test

procedure.

All such lineups were also examined to verify

systems are properly returned to an operable condition.

The review of system lineup and surveillance test procedures

did not identify any instances of improper lineup control, such

that the operability or availability of safety systems would be

compromised.

A number of inconsistencies, contradictory or

confusing instructions, apparent typographical errors and

outdated references were noted.

None of these were considered

significant from the standpoint of affecting safety-related

systems, but a compilation of such items was provided to the

licensee for his followup.

Licensee activities in performance of the same type of system

operability and availability review were examined during this

inspection and discussions were held with cognizant licensee

personnel.

The licensee has concentrated on valve lineups

specified by procedure or checklist, and has included deter-

minations that lineup control is complete and that valve

failure modes do not compromise engineered safety features

operation.

By May 11, 1979, only the review of the emergency

services portions of the service water system remained to be

completed.

Licensee personnel stated no items had been iden-

tified which could compromise the operability or availability

of required engineered safety features.

No items of noncompliance or deviations were identified.

4.

Engineered Safety Features Administrative Control

Licensee administrative controls to assure proper return to

service of safety-related systems and components following

maintenance activities and at the conclusion of extended

outages are and have been subject to continuing review by the

NRC inspector.

These areas were reviewed during this inspec-

tion only to ascertain management controls have not been changed

so as to reduce their effectiveness.

Based on this determination,

administrative controls continue to be considered adequate to

assure proper return to service.

Discussions were also conducted with licensee personnel con-

cerning independent verification of system lineups.

The

licensee utilizes independent verification of component oper-

ability and valve positioning prior to return to power oper-

ations from any cold shutdown, in accordance with plant

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procedures.

This constitutes a verification by licensed per-

sonnel of proper return to service by maintenance personnel

and/or auxiliary operators.

Additional independent verifi-

cation is occasionally performed by duty shift supervisors in

accordance with other selected procedures, at the direction of

the Operations Supervisor, or at the shift supervisor's own

initiative.

Licensee tagging practice and procedures, to provide control

operator cognizance of equipment status, was reviewed during

control room tours conducted during this inspection.

The

purpose of this review was to ascertain the potential for tags

to obscure position indicators, meters or alarms.

Plant oper-

ators may use either of two types of tags in the control room;

one a small adhesive sticker and the other a larger hanging

tag.

Discussions with operating staff and examination of tags

currently in place indicate very little liklihood that meters

or alarms have been or will be obscured.

A few hanging tags

were noted, however, primarily on vertical panels, which were

at least partially obscuring various indicator lights.

None of

these involved safety-related equipment.

Results of the most recent surveillance testing of safety-related

components were examined during this inspection to verify

conformance to acceptance criteria. Technical Specification 4.6.3 describes acceptable pump performance as achieving rated

shutoff head at minimum recirculation flow.

This implies both

pump discharge pressure and flowrate must be verified.

The

Palisades Nuclear Generating Plant does not have and has never

had instrumentation installed to provide containment spray pump

discharge pressure indication. Further, though flow instrumen-

tation is available and is used for the testing of high-pressure

and low-pressure safety injection pumps, no acceptance criteria

for pump flowrate have been established.

This matter will be

brought to the attention of the NRC Off ice of Nuclear Reactor

Regulation for a determination on the adequacy of current

practice. Until such determination, this item will be considered

an unresolved item.

No items of noncompliance or deviations were identified.

S.

Current Engineered Safety Features Status

During this inspection licensee valve lineup procedures and

current piping and instrument diagrams were also used in a

comparison against actual conditions (plant in cold shut-down)

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and against required positions for power operations as verified

by physical inspection of all accessible components in engineered

safety systems.

Complete system flowpath walkdowns, except

inside the containment building, were completed for the following:

a.

High Pressure Safety Injection

b.

Low Pressure Safety Injection

c.

Component Cooling Water (emergency services portions)

d.

Service Water (emergency services portions)

e.

Auxiliary Feedwater

f.

Containment Spray

Extensive walkdowns, limited slightly by accessibility con-

siderations, were also performed on the charging and concen-

trated boric acid systems.

Among those systems aligned as they would be as required for

power operations, no valves were identified as mis-positioned.

Positive position control was questionable on three valves,

which were identified to the licensee for his followup.

Three

instances were noted in which the current piping and instrument

diagram did not reflect the "as built" configuration correctly.

These were also identified to the licensee.

None of the iden-

tified inconsistencies were considered to threaten availability

or operability of required systems, though one item requires

further review.

This item concerns the fact that the service

water return isolation valve from the containment fan coolers

(CV-0824) has been relocated significantly from its original

position near the containment penetration in the component

cooling water pump room.

The valve is now located an estimated

50 feet from its original position, downstream of a flow instru-

ment, in the west .safeguards room.

Although it is believed the

valve was relocated as many as 8 to 10 years ago, neither

system checklists nor current drawings reflect the correct

valve location.

Several members of the operations staff,

including the last individual documented to have checked this

valve, were questioned, with each person indicating a belief

the valve is located in the CCW pump room.

The licensee stated

a review would be performed to determine the affect, if any, of

the repositioning of valve CV-0824 on system function.

This

review will specifically include a verification that the seismic

qualification of the involved piping runs is not compromised.

This item will be reviewed during a subsequent inspection .

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Normal and standby power supplies for safeguards components in

the above systems were also examined during this inspection.

This examination included the 2400v. safeguards buses 1-C and

1-D; 480v. load centers 11 and 12; 480v. motor control centers

1, 2, 7 and 8; and 120v. preferred a.c. buses Y-10, Y-20, Y-30

and Y-40 including chargers, battery banks, and inverters.

During this review, charging pump P-55C was determined to be

the available pump, while the "Safeguards Equipment Status"

board in the control room erroneously indicated P-55A to be the

available pump.

The status board was immediately corrected.

It was noted the power supply indications on the control panel

were correct.

Particular attention was directed to the examination of valve

and switch or breaker positions for the auxiliary feedwater

system.

The walkdown of this system on May 3, 1979, included a

verification that all valves identified by the licensee as

requiring positive position control were actually locked in the

required position.

No items of noncompliance or deviations were identified.

6.

Operations Staff Training

Licensee activities to provide an appropriate review of the

loss of feedwater incident at Three Mile Island Unit 2 for his

operations staff personnel were examined during this inspection.

This effort has taken three forms as follows:

a.

An early, undocumented review focused on conditions leading

to fuel damage and offsite releases of radioactivity.

b.

Operations Department memoranda addressing reset of SIS,

maintenance of 50°F subcooling, and the licensee's written

response to IE Bulletin 79-06B.

c.

A longer term incorporation of TMI-related considerations

as they affect operating practice at Palisades, into the

routine formal operator requalification training program.

At the time of this inspection considerable effort had been

expended in reviewing the TMI incident as it might relate to

the Palisades nuclear plant.

Though not yet well documented,

interviews with training staff and with plant operations staff

indicate the discussions have been comprehensive with respect

to items identified for review in IE Bulletin 79-06B.

Further

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discussions and training, for which documentation will be more

extensive, are planned for the 5-week training cycle beginning

May 21, 1979.

No items of noncompliance or deviations were identified.

7.

Operating Procedures Review

Licensee review of operating, off-normal and emergency pro-

cedures pursuant to matters identified in IE Bulletin 79-06B

was discussed with licensee personnel during this inspection.

These activities have been as described in the licensee's

response to the subject Bulletin dated April 27, 1979.

Specific attention was directed to manual initiation of

auxiliary feedwater since this system is not automatically

initiated at Palisades.

Discussions were_ held with plant

operators and data derived from plant trips from high power

level were reviewed.

Manual initiation is a relatively simple

evolution, in which plant operators are well experienced,

normally accomplished from the control room but with backup

control locally in the plant.

The discussions and review

indicate auxiliary feedwater can be and has been established

within seconds.

This is seldom necessary, however, since one

of two main feedpumps usually remains available.

These pumps

do not trip on reactor or turbine trip but instead ramp down to

5% output in 60 seconds.

It was determined the licensee does not have procedures pre-

pared for feeding a dry steam generator.

In fact, existing

procedures caution against such unless absolutely necessary.

The Palisades Plant steam generators are sized such as to

provide about 16 minutes of decay heat removal after loss of

all feedwater from full power.

Other procedure revisions contemplated, relating to continuance

of forced circulation flow and HPSI flow, had not been made at

the time of the inspection.

Some modification of plant systems

will be required to enable such operation for those cases where

the conditions initiating SIS clear almost immediately or the

SIS is otherwise unnecessary.

No items of noncompliance or deviations were identified .

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8.

Other Bulletin Items

Two additional items from IE Bulletin 79-06B, relating to

isolation of containment on SIS and to assuring the pressurizer

power-operated relief valves do not malfunction, were reviewed

and discussed during this inspection.

As noted in the licensee's submittal of April 27, 1979, the SIS

signal at Palisades performs some isolation functions but not a

complete containment isolation.

However, there may be little

or no benefit from complete isolation on SIS, considering plant

design and operating requirements, and the effect of a complete

isolation on continued availability of the primary coolant

pumps may be deleterious.

The licensee has no plans to modify

the existing containment isolation signals to include SIS.

The pressurizer power-operated relief valves (PORV's) at

Palisades are isolated during normal power operations, being

used only to provide overpressure protection below 300°F

primary coolant system temperature.

The several indications

that a PORV is open have been identified to plant operators.

No items of noncompliance or deviations were identified.

9.

Unresolved Items

Unresolved items are items about which more information is

required in order to ascertain whether they are acceptable

items, items of noncompliance, or deviations.

An unresolved

item disclosed during the inspection is discussed in Paragraph

4.

10.

Management Interviews

Management interviews (attended as shown in Paragraph 1) were

conducted on May 4, 1979, and at the conclusion of the inspec-

tion on May 11, 1979.

The inspectors discussed the scope and

findings of the inspection.

The following were specifically

discussed, with licensee responses as noted.

a.

The inspectors advised the licensee that the independent

review of ESF systems, lineups and administrative controls

performed by the inspectors had identified no conditions

threatening ESF operability or availability .

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b.

The inspectors stated the unresolved item relating to

surveillance testing acceptability criteria for ESF pumps.

The licensee stated submittals for change of the existing

technical specifications had been made, requesting confor-

mance to ASME Section 11 on inservice inspection.

The

licensee further noted ASME Section 11 does not require

acceptance criteria for both pump flowrate and discharge

pressure.

c.

Summary notes relating to inconsistencies, dated references,

apparent inaccuracies and other comments from the inspectors'

reviews were provided to the licensee.

d.

Modification of the Palisades Plant as may be considered

appropriate in view of IE Bulletin 79-06B was discussed.

The inspectors stressed the necessity, and the licensee

concurred, that very careful evaluation precede any modi-

fication with the potential to affect safety-related

systems, no matter the time frame.

e.

The relocation of valve CV-0824 (service water return

isolation from the containment fan coolers) was discussed.

The licensee stated the effect of the repositioning, if

any, would be evaluated, including verification that the

seismic qualification of the piping run is not compromised .

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