05000255/LER-1979-023-03, /03L-0 on 790518:leak in Regenerative Heat Exchanger (E-56) Shell Side Vent Line Resulted in Degradation of Chemical & Vol Control Sys.Caused by High Porosity in Weld.Weld Ground Out & Repaired

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/03L-0 on 790518:leak in Regenerative Heat Exchanger (E-56) Shell Side Vent Line Resulted in Degradation of Chemical & Vol Control Sys.Caused by High Porosity in Weld.Weld Ground Out & Repaired
ML18043A750
Person / Time
Site: Palisades Entergy icon.png
Issue date: 06/18/1979
From:
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML18043A748 List:
References
LER-79-023-03L, LER-79-23-3L, NUDOCS 7906220269
Download: ML18043A750 (1)


LER-1979-023, /03L-0 on 790518:leak in Regenerative Heat Exchanger (E-56) Shell Side Vent Line Resulted in Degradation of Chemical & Vol Control Sys.Caused by High Porosity in Weld.Weld Ground Out & Repaired
Event date:
Report date:
2551979023R03 - NRC Website

text

l PALISADES NRC FORM366 (7-77)

U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT CONTROL BLOCK: I I G)

(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6

[ili] IMII"IPI AILP. 1010101-1°1°101°1°1-1°1°101411111111101 I 1© 7

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LICENSEE CODE 14

,5 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T [iliJ 7

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EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRiPTION AND PROBABLE CONSEQUENCES@

[]JIJ I During preparations for start.11p, a 1 eak in the regeueratiJTe heat exchanger I 1II2J I (E-56) shell side vent line resulted in degradation of the CVCS.

The leak I

!IE] I was through a weld in the 3/4-inch vent line.

This occurrence is report-

[QJIJ able per TS 6.9.2.b.4.

No threat to public health or safety existed.

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REPORT I 7 I 91 NUMBER 21 22 11 12 13 18 19 SEQUENTIAL OCCURRENCE REPORT REPORT NO.

CODE TYPE I I Io I 2 I 31 Ld I o I 3J LJJ 23 24 26 27 28 29 30 20 1=:J 31 ACTION FUTURE EFFECT SHUTDOWN r::;::.,

ATTACHMENT NPRD-4 TAKEN ACTION ON PLANT METHOD HOURS -

SUBMITTED FOAM :;us..

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44 47, I The leak resulted from high porosity in the weld.

The weld was ground out 1J]J] I and rep.aired.

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STATUS

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NUMBER

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9 11 12 13 PERSONNEL INJURIES c::;.,

NUMBER DESCRIPTION~

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