LER-1979-008, /03L-0 on 790126: Tank Vent Valve (CV-3051) Opened Simultaneously w/N2 Fill Valve;Tank Pressure Dropped Below Tech Specs Limit. Caused by Electrical Short Between Wires for Fill & Vent Valves |
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| 2551979008R03 - NRC Website |
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Palisades NRC FORM366 17:111 U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT CONTROL BLOCK: I I G)
(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6
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LICENSEE CODE 14
~5 LICENSE NUMBER
~5 26 LICENSE TYPE 30 57 CAT 58 CON'T WI]
7 8
- ~~~~lkJ©IOl5 IOl.01 921 5151G)!O!l!2161719l@!Ol2121ll719JG) 50 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@
l]J]J I During an attempt ~o raise the pressure in safety injection tank T-82D,
[]JI} 1 the tank vent valve (CV-3051) opened simultaneously with the N2 fill valve 1
((IIJ causing the tank pres sure to drop be low the limit of TS 3. 3. lb.
The vent
!)))) valve has been disabled to the closed position in* order to perm.it use of the N2 fill valve.
The low pressure condition lasted for 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.
l:IIZJ I No threat to public health or safety existed.
CIT[]
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SYSTEM
CAUSE
CAUSE CODE CODE SUBCOCE COMPONENT CODE 1s1F1@ L!J@ w 1v1A.111v1E1x1e COMP.
VALVE SUBCODE SUB CODE l!J@) ~@
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9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REPORT NA.
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T.YPE L=.l 1°1°1ti1
~ 1°151
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23 24 26 27 28 29 30 LER/RO LVENTYEAR REPORT (7 19 I NUMBER 21 22 L=J 31 ACTION FUTURE EFFECT SHUTDOWN r.;:::-,
ATTACHMENT NPRD-4 PRIME COMP.
SUPPLIER REVISION*
.COMPONENT MANUF-"'CTlJRER 80 TAKEN ACTION ON PLANT METHOD HOURS ~ SUBMITTED FORM ~UB.
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43 44 47 CAUSE DESCRIPTION AND CORREC"rlVE ACTIONS @
I Valve malf'unction appears to have been caused by an electrical short betwe;n [I]J] I the wires for the fill and vent valves for T-82D.
Both valves are on the same electrical scheme, and their wires share a common connector at the IIIIJ '--~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~--'
containment electrical penetration.
When plant conditions permit, the o::ID ~'~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~~--'
ITilJ I fault will be located and corrected.
1 a 9 FACILITY IJQ\\
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% POWER I OTHER STATUS I.:;::;
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AMOUNT OF ACTIVITY~
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46 80 N/A LOCATIOlll OF RELEASE @
44 45 80 PERSONNEL EXPOSURES
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9 11 12 13 PERSONNEL INJURIES
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80 NUMBER DESCRIPTION~
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11 12 LOSS. OF OR DAMAGE TO FACILITY (,jJ\\
TYPE
DESCRIPTION
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ISSUEDC,;\\ DESCRIPTION~
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I I I I I I I I I I I I I NRC USE ONLY a s 10 68 69 80
consumers Power company General Offices: 212 West Michigan Avenue, Jackson, Michigan 49201
- Area Code 517 788-0550 February 21, 1979
~..r James G Keppler Office of Inspection and Enforcement Region III US*Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 DOCKET 50-255 - LICENSE DPR PALISADES PLANT - LER 79-008 On the reverse side is Licensee Event Report 79-0o8 which is reportable under Technical Specification 6.9.2.b.(2).
~lJ, p
~-.;;;;;D'avid P Hoff:man tJ
- Assistant Nuclear Licensing Administrator CC:
Director, Office of Nuclear Reactor Regulation Director, Office of Inspection and Enforcement
~g 2 3 1979
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| 05000255/LER-1979-001, Forwards LER 79-001/03X-1 | Forwards LER 79-001/03X-1 | | | 05000255/LER-1979-001-03, /03L-0 on 790102:reactor Protection Sys Power Range Channels NI05,06 & 07 Bypassed W/O First Tripping NI08.Caused by Failure to Use Administrative Controls | /03L-0 on 790102:reactor Protection Sys Power Range Channels NI05,06 & 07 Bypassed W/O First Tripping NI08.Caused by Failure to Use Administrative Controls | | | 05000255/LER-1979-002-03, /03L-0 on 790103:steam Generator Specific Conductivity Increased to 7.65 micro-mho Per Cm.Steam Generator Rate Increased & Morpholine/Hydrazine Feed Rate Decreased.Caused by Air in Leakage to Main Condenser | /03L-0 on 790103:steam Generator Specific Conductivity Increased to 7.65 micro-mho Per Cm.Steam Generator Rate Increased & Morpholine/Hydrazine Feed Rate Decreased.Caused by Air in Leakage to Main Condenser | | | 05000255/LER-1979-003-01, /01T-0 on 790117:fitting in Fire Protection Piping for a Cooling Tower Broke.Resulting Leakage Could Not Be Isolated;Fire Pumps Placed in Manual.Break Caused by Freezing Weather Conditions | /01T-0 on 790117:fitting in Fire Protection Piping for a Cooling Tower Broke.Resulting Leakage Could Not Be Isolated;Fire Pumps Placed in Manual.Break Caused by Freezing Weather Conditions | | | 05000255/LER-1979-004-01, /01T-0 on 790117:svc Water Pump P-7B Taken out-of- Service W/O Prior Test of Diesel Generator 1-2.Caused by Combination of Poor Judgment & Lack of Awareness of Tech Spec Requirements by Shift Operating Personnel | /01T-0 on 790117:svc Water Pump P-7B Taken out-of- Service W/O Prior Test of Diesel Generator 1-2.Caused by Combination of Poor Judgment & Lack of Awareness of Tech Spec Requirements by Shift Operating Personnel | | | 05000255/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000255/LER-1979-005-03, /03L-0 on 790103:1/4-inch Drain Line in Diesel Generator Fuel Sys Broke,Spraying 100-150 Gal of Fuel Oil Onto Engine.Caused by Vibration | /03L-0 on 790103:1/4-inch Drain Line in Diesel Generator Fuel Sys Broke,Spraying 100-150 Gal of Fuel Oil Onto Engine.Caused by Vibration | | | 05000255/LER-1979-006-01, /01T-0 on 790125:during Preparation for Leak Testing Personnel Air Lock,Found Pressure Gauge Normally Mounted on Outer Door of Air Lock Was Missing.Caused by Procedures Not Specifying Gauge Replacement After Removal | /01T-0 on 790125:during Preparation for Leak Testing Personnel Air Lock,Found Pressure Gauge Normally Mounted on Outer Door of Air Lock Was Missing.Caused by Procedures Not Specifying Gauge Replacement After Removal | | | 05000255/LER-1979-006, Forwards LER 79-006/01T-0 | Forwards LER 79-006/01T-0 | | | 05000255/LER-1979-007-03, /03L-0 on 790115:primary Computer Stopped.Caused by Computer Program Failure.Computer Reprogrammed to Restore Operability | /03L-0 on 790115:primary Computer Stopped.Caused by Computer Program Failure.Computer Reprogrammed to Restore Operability | | | 05000255/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000255/LER-1979-008-03, /03L-0 on 790126: Tank Vent Valve (CV-3051) Opened Simultaneously w/N2 Fill Valve;Tank Pressure Dropped Below Tech Specs Limit. Caused by Electrical Short Between Wires for Fill & Vent Valves | /03L-0 on 790126: Tank Vent Valve (CV-3051) Opened Simultaneously w/N2 Fill Valve;Tank Pressure Dropped Below Tech Specs Limit. Caused by Electrical Short Between Wires for Fill & Vent Valves | | | 05000255/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000255/LER-1979-009-01, /01X-1 on 790220:design Review Indicated Butterfly Valves May Not Close Under Accident Conditions.Caused by Vague Purchase Specs Which Did Not Include Requirements for Closing Against Pressure | /01X-1 on 790220:design Review Indicated Butterfly Valves May Not Close Under Accident Conditions.Caused by Vague Purchase Specs Which Did Not Include Requirements for Closing Against Pressure | | | 05000255/LER-1979-009, Forwards LER 79-009/01X-1 | Forwards LER 79-009/01X-1 | | | 05000255/LER-1979-010-03, /03L-0 on 790207:during Resin Sluicing Operations, Manual Isolation Valve (MV-CVC502) Was Left Open,Resulting in 17 Gpm Leak to Radwaste Sys.Caused by Broken Valve Stop. Valve Stop Will Be Replaced | /03L-0 on 790207:during Resin Sluicing Operations, Manual Isolation Valve (MV-CVC502) Was Left Open,Resulting in 17 Gpm Leak to Radwaste Sys.Caused by Broken Valve Stop. Valve Stop Will Be Replaced | | | 05000255/LER-1979-011-03, /03L-0 on 790227:primary Data Logger Was Inoperable.Caused by Multiplexer Failure at Computer Input/ Output.Faulty Relays Replaced | /03L-0 on 790227:primary Data Logger Was Inoperable.Caused by Multiplexer Failure at Computer Input/ Output.Faulty Relays Replaced | | | 05000255/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000255/LER-1979-012-03, /03L-0 on 790201:during Normal Plant Operation, Primary Coolant Pump Inadvertantly Stopped.Reactor Immediately Tripped.Shutdown Margin Was Less than Specified in Tech Specs.Power Conversion Sys Was Emergency Borated | /03L-0 on 790201:during Normal Plant Operation, Primary Coolant Pump Inadvertantly Stopped.Reactor Immediately Tripped.Shutdown Margin Was Less than Specified in Tech Specs.Power Conversion Sys Was Emergency Borated | | | 05000255/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000255/LER-1979-013-01, /01X-1 on 790327:level in T-82C Safety Injection Tank Decreased While Draining D Tank to Permit Increase in Boron Concentration.Caused by Seal Leakage.Cv 3004 Drain Valve Will Be Repaired During Next Refueling Outage | /01X-1 on 790327:level in T-82C Safety Injection Tank Decreased While Draining D Tank to Permit Increase in Boron Concentration.Caused by Seal Leakage.Cv 3004 Drain Valve Will Be Repaired During Next Refueling Outage | | | 05000255/LER-1979-013, Forwards LER 79-013/01X-1 | Forwards LER 79-013/01X-1 | | | 05000255/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000255/LER-1979-014-03, /03L-0 on 790315:during Normal Plant Operation, Primary Computer Stopped,Due to Computer Program Failure. Computer Reprogrammed & Restored to Operability | /03L-0 on 790315:during Normal Plant Operation, Primary Computer Stopped,Due to Computer Program Failure. Computer Reprogrammed & Restored to Operability | | | 05000255/LER-1979-015-01, /01T-0 on 790409:refer to from Dp Hoffman to Dl Ziemann Re Pipe Supports | /01T-0 on 790409:refer to from Dp Hoffman to Dl Ziemann Re Pipe Supports | | | 05000255/LER-1979-015, Forwards LER 79-015/01T-0 | Forwards LER 79-015/01T-0 | | | 05000255/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | | | 05000255/LER-1979-016-03, /03L-0 on 790406:diesel Generator Output Breaker Has Potential to Lockout Open.Caused by Failure of Contact on Shutdown Sequencer to Operate.Sequencer Repaired | /03L-0 on 790406:diesel Generator Output Breaker Has Potential to Lockout Open.Caused by Failure of Contact on Shutdown Sequencer to Operate.Sequencer Repaired | | | 05000255/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000255/LER-1979-017-03, /03L-0 on 790404:while Taking Battery Voltage Readings,Two Cells in Station Battery 2 Burst Due to Explosion of Hydrogen Inside Cells.Battery Taken Out of Svc. Two Replacement Cells Ordered | /03L-0 on 790404:while Taking Battery Voltage Readings,Two Cells in Station Battery 2 Burst Due to Explosion of Hydrogen Inside Cells.Battery Taken Out of Svc. Two Replacement Cells Ordered | | | 05000255/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000255/LER-1979-018-03, /03L-0 on 790409:reactor Made Critical W/O Conducting Flow Test of Lines.Caused by Misinterpretation of Tech Specs.Personnel Instructed to Exercise Care When Reviewing Operability Requirements | /03L-0 on 790409:reactor Made Critical W/O Conducting Flow Test of Lines.Caused by Misinterpretation of Tech Specs.Personnel Instructed to Exercise Care When Reviewing Operability Requirements | | | 05000255/LER-1979-019-03, /03L-0 on 790331:sump Drained to Auxiliary Bldg Floor Drains Through Test Connection Located Between Containment Bldg Isolation Valves.Caused by Communication Failure.Corrective Action Still Being Evaluated | /03L-0 on 790331:sump Drained to Auxiliary Bldg Floor Drains Through Test Connection Located Between Containment Bldg Isolation Valves.Caused by Communication Failure.Corrective Action Still Being Evaluated | | | 05000255/LER-1979-019, Forwards LER 79-019/03L-0 | Forwards LER 79-019/03L-0 | | | 05000255/LER-1979-020-01, /01T-0 on 790501:restraints for Piping Between Power Conversion Sys Safety Injection Tanks B & D Not Adequate.Caused by Program Error Used by Consultant to Determine Hanger Placement | /01T-0 on 790501:restraints for Piping Between Power Conversion Sys Safety Injection Tanks B & D Not Adequate.Caused by Program Error Used by Consultant to Determine Hanger Placement | | | 05000255/LER-1979-020, Forwards LER 79-020/01T-0 | Forwards LER 79-020/01T-0 | | | 05000255/LER-1979-021-03, /03L-0 on 790427:during Routine Surveillance of safety-related snubbers,S-44 (LPIS Pump Discharge) Had No Visible Oil Level.Oil Leakage from Snubber Caused by Failed O-ring,attributed to Ald Age.Ring Replaced | /03L-0 on 790427:during Routine Surveillance of safety-related snubbers,S-44 (LPIS Pump Discharge) Had No Visible Oil Level.Oil Leakage from Snubber Caused by Failed O-ring,attributed to Ald Age.Ring Replaced | | | 05000255/LER-1979-022-03, /03L-0 on 790426:during Routine Surveillance of safety-related snubber,S-9 (Main Steam Line) Had No Visible Oil Level.Oil Leakage from Snubber Caused by Failed O-ring,attributed to Old Age.Ring Replaced | /03L-0 on 790426:during Routine Surveillance of safety-related snubber,S-9 (Main Steam Line) Had No Visible Oil Level.Oil Leakage from Snubber Caused by Failed O-ring,attributed to Old Age.Ring Replaced | | | 05000255/LER-1979-023, Forwards LER 79-023/03L-0 | Forwards LER 79-023/03L-0 | | | 05000255/LER-1979-023-03, /03L-0 on 790518:leak in Regenerative Heat Exchanger (E-56) Shell Side Vent Line Resulted in Degradation of Chemical & Vol Control Sys.Caused by High Porosity in Weld.Weld Ground Out & Repaired | /03L-0 on 790518:leak in Regenerative Heat Exchanger (E-56) Shell Side Vent Line Resulted in Degradation of Chemical & Vol Control Sys.Caused by High Porosity in Weld.Weld Ground Out & Repaired | | | 05000255/LER-1979-024-03, /03L-0 on 790608:level in Safety Injection Tank Fell Below Tech Spec Limit.Caused by Annunciation of Independent Level Switch.Switch Adjusted | /03L-0 on 790608:level in Safety Injection Tank Fell Below Tech Spec Limit.Caused by Annunciation of Independent Level Switch.Switch Adjusted | | | 05000255/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | | | 05000255/LER-1979-025-01, /01X-1 on 790619:heat Transfer Coefficients of Component Cooling Water Heat Exchanger Were Less than Required.Caused by Fouled Tube Sides.Tubes Will Be Cleaned More Frequently | /01X-1 on 790619:heat Transfer Coefficients of Component Cooling Water Heat Exchanger Were Less than Required.Caused by Fouled Tube Sides.Tubes Will Be Cleaned More Frequently | | | 05000255/LER-1979-025, Forwards LER 79-025/01T-0 | Forwards LER 79-025/01T-0 | | | 05000255/LER-1979-026-03, /03L-0 on 790604:steam Generator Chemistry Ph Dropped Below Tech Spec Min When Condensate Polishers Placed in Svc.Caused by Resin Leakage from Polishers Due to Defective Septums.Resin Mixture Changed;Chemical Feed Ended | /03L-0 on 790604:steam Generator Chemistry Ph Dropped Below Tech Spec Min When Condensate Polishers Placed in Svc.Caused by Resin Leakage from Polishers Due to Defective Septums.Resin Mixture Changed;Chemical Feed Ended | | | 05000255/LER-1979-026, Forwards LER 79-026/03L-0 | Forwards LER 79-026/03L-0 | | | 05000255/LER-1979-027-03, /03L-0 on 790614:during Normal Power Operation, Conductivity of B Steam Generator Increased to 7.65 Micro/Mhos Per Cm Beyond Tech Spec Limit.Caused by Condenser in Leakage | /03L-0 on 790614:during Normal Power Operation, Conductivity of B Steam Generator Increased to 7.65 Micro/Mhos Per Cm Beyond Tech Spec Limit.Caused by Condenser in Leakage | | | 05000255/LER-1979-027, Forwards LER 79-027/03L-0 | Forwards LER 79-027/03L-0 | | | 05000255/LER-1979-028-03, /03L-0 on 790623:conductivity & Sodium Concentration in Steam Generator a Exceeded Tech Spec Limits.Caused by Combination of Condenser Tube in Leakage & Chemical Hideout Return as Result of Power Reduction | /03L-0 on 790623:conductivity & Sodium Concentration in Steam Generator a Exceeded Tech Spec Limits.Caused by Combination of Condenser Tube in Leakage & Chemical Hideout Return as Result of Power Reduction | | | 05000255/LER-1979-028, Forwards LER 79-028/03L-0 | Forwards LER 79-028/03L-0 | |
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