/03X-1 on 781031:with Diesel Generator 1-2 Out of Svc,Pwr Supply for Alternate Changing Pumps Was Shifted to D/G 1-1 Before Charging Pump P-55c Was Removed from Svc. Caused by Personnel Error| ML18043A344 |
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| Site: |
Palisades  |
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| Issue date: |
12/14/1978 |
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| From: |
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.) |
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| To: |
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| Shared Package |
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| ML18043A343 |
List: |
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| References |
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| LER-78-037-03X, LER-78-37-3X, NUDOCS 7812220107 |
| Download: ML18043A344 (1) |
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LER-1978-037, /03X-1 on 781031:with Diesel Generator 1-2 Out of Svc,Pwr Supply for Alternate Changing Pumps Was Shifted to D/G 1-1 Before Charging Pump P-55c Was Removed from Svc. Caused by Personnel Error |
| Event date: |
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| Report date: |
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| 2551978037R03 - NRC Website |
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text
(
PREVIGlJS RE.PORT DA-TE il/30/78 PALISADES PLANT NRC FORM366 (7-77)
U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT CONTROL BLOCK:~!
~..__....___.l~-___.~...__,lG)
(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
!IE] I M I I I P I A IL I l l@l~O__.l_O_._I __._I *_o...,I =O'=I 0,...,..1..,..,0.,,.,,_1,,....o_._I __._I O__._I O-:dl01 4 I l I 1 I l I 11 G)I I I 0 7
8
- 9.
LICENSEE CODE 14
'ls L.ICENSE NUMBER 25 26 LICENSE TYPE JO S7 CAT 58 CON'T
-~
7 8
- ~:~~~ ~I o I 5 I o I o I o I 2 I 5 I 5 (VI 1 I o 1 3 11 I 71 8 011 12 I 1 I 4 I 7 I 8 10) 60 61 DOCKET NUMBER 68 63 EVENT DATE 74 75 REPORT DATE 80 EVENT OESCRIPTION ANO PROBABLE CONSEQUENCES (,Ci) 1During normal plant operation, Cifesel generator No. 1-2 was taken out
((]I) I of service to permit repairs to its. pre-lube oil numo.
W~th the 1-2 D/G
((II] I still out of service, charging pump P-55c was also taken out of service, C§:[IJ I because of leaking seals. :Prior to removing P-55c charging pump from
[]JI] 1 service, the power supply (load ctr. 12) for the alternate charging pumps
((ill I was shifted to diesel generator l;-i.* This event reportable ner TS 6.9.
a:n::l I 2.b.3. Upon discovery *of this condition, D/G 1-2 was returned to service. 1 7
8 9 80 SYSTEM CODE
CAUSE
CAUSE COMP.
VALVE [ill]
. COOE SUSCOOE COMPONENT COOE SUBCOOE SUBCOOE l.!J@ L!J@ 1z1z1z1zrz1z1@ LB@ L~@:
IEIBI@
9 10 7
8 11 12 13
. 18 19 20 SEQUENTIAL OCCURRENCE REPORT r.::,,
LERIRO CVENT Y~A REPORT NO.
cooE TYPE *
'..::,) REPORT I 7 -I ~,
I I 10 I 3 I 7 I 1......-1 10 I 3 I
~ I I NUMBER
- 26 27 28 29 JO 31 ACTION FUTURE EFFECT SHUTDOWN
~ ATTACHMENT NPRQ.4 PRIME COMP.
TAKEN ACTION ON PLANT METHOD HOURS SUBMITTED FOAM ~us.
SUPPLIER
~@L!J@ ~(§) L!J I o Io Io I I L!J@
L!.J@)
~@
JJ 34 35 36 37 40 41 42 43 CAUSE OESCRIPTION ANO CORREC-rlVE ACTIONS @
REVISION t!1 J2 COMPONENT MANUFACTURER 1z 1919191@
44 47
!JI§] I Su~ervisory personnel made the decision to cross-connect the 11 and 12 1
ITIIJ 1load centers (thereby placing both load ctrs on the same D/G) w/o realizing [JJ]J 1that this action could potentially lead to an exces~ive load on the o~erab~e [JJJJ !D/G.
To prevent recurrence, event has been reviewed with licensed shi~. I OE 1personnel.
7 8
9 FACILliY 13Q\\
ST A TUS
.,. POWER
/ OTHER STATUS ~-
IIIT1 L!J@ 111010 I@! N,A 8
9
.10 12 13 4'
ACTIVITY CONTENT
~
RELEASED OF REI.EASE
!-Mt'JUNT OF ACTIVITY ~.
[ill] UJ@ ~@I* N~
I 7
8 9
10 11 4'
80 METHOD OF r.:;:;..
OISCQllERY '
Op t
~(El1.*~~e_r_a~1_n_g~~-o_g~rt_e_vi~_ew~-~*~~~~--
~s 46 80 N/A
~OCATION OF RELEASE 80 PERSONNEi.. EXPOSURES Q...
NUMBER r.;:;... TYPE r:;;;-,. DESCRIPJlON [J]1J I O I O I o l~~.....__N.._;A ________________________ ____.
8 9
11 12 13 80 PERSONNEL INJURIES
/,;'.;\\
NUMBER OESCRIPT7N6 lili) IOIOIOl~~I ~N~c~A~~~~~~~~~...,.....,.--~~~~~~~~~~~~
8 9
12 LOSS o~ OR OAMAGC: TO FACILITY t4JI D::I:!] ITYZ[<!V_D~-S-CR_l_PN_l/A_A~~-~-'..;::;:,J~~~~~~~~~~~~~~~~~~~~~~~~~------~~~~--
__ J.
80 7
8 9
10 PUBL.ICITY
~
ISSUED(,";\\ DESCRIPTION::
ITI.§J L!Jeil N _
7 8
9 10 80.
NRC USE ONLY I I I I I I I I I I I I I !
68 69 80 781222D{ 07
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| 05000255/LER-1978-000, License Event Report LER-78-000-00 Re Out-of-Sequence Rod Withdrawal | License Event Report LER-78-000-00 Re Out-of-Sequence Rod Withdrawal | | | 05000255/LER-1978-004, Two Updated License Event Reports, LER-78-004 & LER-78-006 | Two Updated License Event Reports, LER-78-004 & LER-78-006 | | | 05000255/LER-1978-007-01, /01T-0:on 780313,during Sealing of Electrical Connectors Located Inside Containment,Sockets &/Or Sealing Plugs Were Discovered Missing from Connectors.Caused by Connector Holes Not Being Filled During Wiring | /01T-0:on 780313,during Sealing of Electrical Connectors Located Inside Containment,Sockets &/Or Sealing Plugs Were Discovered Missing from Connectors.Caused by Connector Holes Not Being Filled During Wiring | | | 05000255/LER-1978-013, Forwards LER 78-013/01X-1 | Forwards LER 78-013/01X-1 | | | 05000255/LER-1978-013-01, /01X-1 on 780421:containment Bldg Air Valve Was Opened During Hot Shutdown Resulting in a Breach of Containment Integrity,Caused by Personnel Error.Notice Posted & Personnel Instructed Re Proper Procedures | /01X-1 on 780421:containment Bldg Air Valve Was Opened During Hot Shutdown Resulting in a Breach of Containment Integrity,Caused by Personnel Error.Notice Posted & Personnel Instructed Re Proper Procedures | | | 05000255/LER-1978-030, Forwards LER 78-030/01T on 780828 | Forwards LER 78-030/01T on 780828 | | | 05000255/LER-1978-030-01, /01T on 780828:During Cooldown of the Reactor,The Containment Bldg Was Ventilated Thru the Purge Supply & Exhaust Valves.Improper Tagging Caused Valves to Be Open & Containment Integrity Not Met. (Encl to 7809190170) | /01T on 780828:During Cooldown of the Reactor,The Containment Bldg Was Ventilated Thru the Purge Supply & Exhaust Valves.Improper Tagging Caused Valves to Be Open & Containment Integrity Not Met. (Encl to 7809190170) | | | 05000255/LER-1978-031, Forwards LER 78-031/01T-0 | Forwards LER 78-031/01T-0 | | | 05000255/LER-1978-032-01, /01T-0:on 781019,during Monthly Sampling of SI Tanks,Boron Concentrations in Tanks B & D Were 1,703 & 1655 Ppm,Respectively.Caused by Dilution of SI Tank Contents from Water Left in Shutdown Cooling Lines After Shutdown | /01T-0:on 781019,during Monthly Sampling of SI Tanks,Boron Concentrations in Tanks B & D Were 1,703 & 1655 Ppm,Respectively.Caused by Dilution of SI Tank Contents from Water Left in Shutdown Cooling Lines After Shutdown | | | 05000255/LER-1978-032, Forwards LER 78-032/01T-0 | Forwards LER 78-032/01T-0 | | | 05000255/LER-1978-033-01, /01T-0:on 781025,during 15-day Isolation of Waste Gas Decay Tank,Part of Tank Contents Leaked Out.Caused by Faulty Pressure Instrumentation.Instrumentation Recalibr | /01T-0:on 781025,during 15-day Isolation of Waste Gas Decay Tank,Part of Tank Contents Leaked Out.Caused by Faulty Pressure Instrumentation.Instrumentation Recalibr | | | 05000255/LER-1978-033, Forwards LER 78-033/01T-0 | Forwards LER 78-033/01T-0 | | | 05000255/LER-1978-034, Forwards LER 78-034/01T-0 | Forwards LER 78-034/01T-0 | | | 05000255/LER-1978-034-01, /01T-0 on 781026:during Surveillance of safety- Related Shock Suppressors,Snubbers S5 & S28 Found Inoper. Caused by Oil Leakage Past Failed O-ring in Both Snubbers. O-ring Failure Due to Age & High Temp Conditions | /01T-0 on 781026:during Surveillance of safety- Related Shock Suppressors,Snubbers S5 & S28 Found Inoper. Caused by Oil Leakage Past Failed O-ring in Both Snubbers. O-ring Failure Due to Age & High Temp Conditions | | | 05000255/LER-1978-035, Forwards LER 78-035/03L-0 & 78-036/03L-0 | Forwards LER 78-035/03L-0 & 78-036/03L-0 | | | 05000255/LER-1978-035-03, /03L-0 on 781020:channel D Pressure Instru pt-0102D Found to Be Out of Calibr.Caused by Zero Shift. Calibr Frequency Changed from Annually to semi-annually | /03L-0 on 781020:channel D Pressure Instru pt-0102D Found to Be Out of Calibr.Caused by Zero Shift. Calibr Frequency Changed from Annually to semi-annually | | | 05000255/LER-1978-036-03, /03X-1 on 781021:during Monthly Surveillance of Fire Hose Stations,Hose Station 11 Was Found to Have 50-foot Hose Instead of Required 74-foot Hose.Caused by Personnel Error | /03X-1 on 781021:during Monthly Surveillance of Fire Hose Stations,Hose Station 11 Was Found to Have 50-foot Hose Instead of Required 74-foot Hose.Caused by Personnel Error | | | 05000255/LER-1978-036, Forwards LER 78-036/03X-1 | Forwards LER 78-036/03X-1 | | | 05000255/LER-1978-037-03, /03X-1 on 781031:with Diesel Generator 1-2 Out of Svc,Pwr Supply for Alternate Changing Pumps Was Shifted to D/G 1-1 Before Charging Pump P-55c Was Removed from Svc. Caused by Personnel Error | /03X-1 on 781031:with Diesel Generator 1-2 Out of Svc,Pwr Supply for Alternate Changing Pumps Was Shifted to D/G 1-1 Before Charging Pump P-55c Was Removed from Svc. Caused by Personnel Error | | | 05000255/LER-1978-037, Forwards LER 78-037/03X-1 | Forwards LER 78-037/03X-1 | | | 05000255/LER-1978-038, Forwards LER 78-038/03L-0 | Forwards LER 78-038/03L-0 | | | 05000255/LER-1978-038-03, /03L-0 on 781106:during Constr activities,2 Elec Penetration Fire Barriers Opened to Permit Cable Routing W/O Fire Tour Being Established.Caused by Failure of Contractor Personnel to Comply W/Plant Procedures | /03L-0 on 781106:during Constr activities,2 Elec Penetration Fire Barriers Opened to Permit Cable Routing W/O Fire Tour Being Established.Caused by Failure of Contractor Personnel to Comply W/Plant Procedures | | | 05000255/LER-1978-039, Forwards LER 78-039/03L-0 | Forwards LER 78-039/03L-0 | | | 05000255/LER-1978-039-03, /03L-0:on 781110:during Normal Operation,Steam Generator Ph & Conductivity Exceeded Tech Spec steady-state Limits.Caused by Inadvertent Addition of Morpholine to Condensate Sys Thru Leaking Drain Valve | /03L-0:on 781110:during Normal Operation,Steam Generator Ph & Conductivity Exceeded Tech Spec steady-state Limits.Caused by Inadvertent Addition of Morpholine to Condensate Sys Thru Leaking Drain Valve | | | 05000255/LER-1978-040, Forwards LER 78-040/01X-2 | Forwards LER 78-040/01X-2 | | | 05000255/LER-1978-040-01, /01X-1:on 781128,during Venting of Waste Gas Surge Tank,Leakage Resulted in Gaseous Release W/O 15-day Holdup Time.Cause Under Evaluation.Rept Will Be Issued by 790105, Not 780105 as Previously Reported | /01X-1:on 781128,during Venting of Waste Gas Surge Tank,Leakage Resulted in Gaseous Release W/O 15-day Holdup Time.Cause Under Evaluation.Rept Will Be Issued by 790105, Not 780105 as Previously Reported | | | 05000255/LER-1978-041, Forwards LER 78-041/01T-01 | Forwards LER 78-041/01T-01 | | | 05000255/LER-1978-041-01, /01T:on 781214,dtermined That Insufficient High Pressure Safety Injection Flow Would Be Delivered to Core in Event of Small Break Loca.Caused by Redundant High Pressure Safety Injection Header Being Valved Out of Svc | /01T:on 781214,dtermined That Insufficient High Pressure Safety Injection Flow Would Be Delivered to Core in Event of Small Break Loca.Caused by Redundant High Pressure Safety Injection Header Being Valved Out of Svc | | | 05000255/LER-1978-042-03, /03L-1 on 781209:reactor Was Taken Critical After Repairs to Boric Acid Gravity Flow Feed Line But Prior to Obtaining Equipment Outage Request (Eor) Signatures.To Prevent Recurrence,Startup Checklist Will Include Eor | /03L-1 on 781209:reactor Was Taken Critical After Repairs to Boric Acid Gravity Flow Feed Line But Prior to Obtaining Equipment Outage Request (Eor) Signatures.To Prevent Recurrence,Startup Checklist Will Include Eor | | | 05000255/LER-1978-042, Forwards LER 78-042/03L-1 | Forwards LER 78-042/03L-1 | | | 05000255/LER-1978-043-01, /01T-0 on 781231:during Control Rod Drive Mechanism Exercising,Rod 29 Was Driven Too Far,Resulting in Misalignment Greater than 8 Inches from Remaining Rods in Group.Caused by Diversion of Operators Attention | /01T-0 on 781231:during Control Rod Drive Mechanism Exercising,Rod 29 Was Driven Too Far,Resulting in Misalignment Greater than 8 Inches from Remaining Rods in Group.Caused by Diversion of Operators Attention | | | 05000255/LER-1978-043, Forwards LER 78-043/01T-0 | Forwards LER 78-043/01T-0 | | | 05000255/LER-1978-044, Forwards LER 78-044/04L-0 | Forwards LER 78-044/04L-0 | | | 05000255/LER-1978-044-04, /04L-0 on 781219:during Power Ascension Following Plant Startup,Thermal Discharges to Lake Caused 6 F Increase Above Ambient Temp of Receiving Water.Caused by Damaged Wier Stop Logs | /04L-0 on 781219:during Power Ascension Following Plant Startup,Thermal Discharges to Lake Caused 6 F Increase Above Ambient Temp of Receiving Water.Caused by Damaged Wier Stop Logs | |
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