05000255/LER-1978-034-01, /01T-0 on 781026:during Surveillance of safety- Related Shock Suppressors,Snubbers S5 & S28 Found Inoper. Caused by Oil Leakage Past Failed O-ring in Both Snubbers. O-ring Failure Due to Age & High Temp Conditions

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/01T-0 on 781026:during Surveillance of safety- Related Shock Suppressors,Snubbers S5 & S28 Found Inoper. Caused by Oil Leakage Past Failed O-ring in Both Snubbers. O-ring Failure Due to Age & High Temp Conditions
ML18043A264
Person / Time
Site: Palisades 
Issue date: 11/09/1978
From:
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
Shared Package
ML18043A263 List:
References
LER-78-034-01T, LER-78-34-1T, NUDOCS 7811140228
Download: ML18043A264 (1)


LER-1978-034, /01T-0 on 781026:during Surveillance of safety- Related Shock Suppressors,Snubbers S5 & S28 Found Inoper. Caused by Oil Leakage Past Failed O-ring in Both Snubbers. O-ring Failure Due to Age & High Temp Conditions
Event date:
Report date:
2551978034R01 - NRC Website

text

PALISADES NRC FORM 366 (7-77)

U.S. NUCL'EAR REGULATORY COMMISSION LICENSEE EVENT REPORT CONTRO~ BLOCK: l l

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(?LEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

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(]J3].1 During routine s~rveillance o!-'sa£ety-related shock suppressors, snubbers1

[£]IJ 1 S5 and 828 (located on main steam and component cooling water lines)

[Q]I] I were found to be inoperable due to their oii levels being below the indicating range.

This condition exceeded the LCO of TS 3.20.

Snubbers

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were re~laced with rebuilt snubbers.

Snubber 85 had already been fIID I replaced when snubb~r 828 was determined to be inoperable.

LER 77-27

[§))] I reported a similar occurrence, Event had no ~dverse ef~ect on public

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44 47 [IIIJ I Low oil levels were caused by oil leakage past a failed 0-ring in both IJJJJ srn1bbers.

  • 0-ring failure has been attr.i buted to aging and high tempera-1 ITJ)) l ture service conditions.

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FACILITY 1'3()1 METHOD OF BO STATUS

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