ML18038B801

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Insp Repts 50-259/96-12,50-260/96-12 & 50-296/96-12 on 961013-1123.Violations Noted.Major Areas Inspected: Maintenance,Operations,Engineering & Plant Support
ML18038B801
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 12/20/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18038B799 List:
References
50-259-96-12, 50-260-96-12, 50-296-96-12, NUDOCS 9701150014
Download: ML18038B801 (42)


See also: IR 05000259/1996012

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION II

'Docket Nos:

'L'icense

Nos:

50-259,:50-260,

50-296

DPR-33,

DRP-52,

DPR-68

Report

No:

.

50-259/96-12,

50-260/96-12,

50-296/96-12

Licensee:

Tennessee

Valley Authority (TVA)

Facility:

Browns Ferry Nuclear Plant, Units 1, 2,

and

3

Location:

Cor ner of Shaw and Browns Ferry .Roads

Athens,

AL

35611

e

Dates:

Inspectors:

Approved by:

October .13

- November 23,

1996

H. Morgan, Acting Senior

Resident

Inspector

J. Star efos,

Resident Inspector

G. Walton, Reactor Engineer

(Paragraph

H1.1)

'S. Sparks,

Project Engineer

(Paragraphs

H4.1,

E8'.1,

M8.1, 02.4)

H. Lesser,

Chief

Reactor

Projects

Branch

6

'Division of Reactor

Projects

Enclosure

2

970ii500i4 9hi220

PDR

ADQCK 05000259

8

PDR

41

!I

EXECUTIVE SUMMARY

Browns Ferry Nuclear

Plant, Units 1,

2 5 3

NRC Inspection Report 50-259/96-12,

50-260/96-12,

50-296/96-12

This integrated inspection included aspects

of licensee

oper ations,

engineering,

maintenance,

and plant support.

The report covers

a six-week

period of resident inspection

and includes efforts of a regional project

engineer

and

a regional reactor engineer.

erations

On October 29, Unit 2 automatically

scrammed

due to problems with the main

generator excitation system.

The excitation system problem was caused

by a

failure in the alternator-exciter collector brush set/ring.

The licensee

addressed

the failure and responded

properly to the scram (Section 02.1).

~

'On 'November

6. Unit 3 Division I ECCS Inver ter power was lost due to a fuse

failure.

Repairs

were immediately performed,

the fuse was replaced,

the

inverter was subsequently

tested

and placed back into service.

An ECCS

backup power supply is scheduled for installation during the upcoming

Unit 3 outage.

The cause of the inverter failure was not fully determined.

Inspection Followup Item (IFI) 296/96-08-02

discussed

two previous failures

and remains

open.

(Section 02.2).

~

On November 19, during

a tour of the Unit 2 Emergency Diesel

Generator

. (EDG) Auxiliary Board Rooms,

inspectors

discovered that the two EDG

Auxiliary Boar d Room Exhaust

Fans were not running and their switches were

in the

OFF position.

Procedures

required operation of these

fans.

The

inspectors

concluded that licensee

personnel

had failed to follow

procedures

and

an existing procedu're

was inadequate.

A violation (VIO) .50-

296/96-12-01

was identified (Section 02.4).

Naintenance

~

During the inspection period,

a regional reactor engineer

performed

a long-

ter m.lay-up inspection of Unit l.

In-plant storage of equipment

was found

to 'be acceptable,

humidity controls were noted

as adequate

and housekeeping

was also acceptable.

Adequate lay-up control

was observed

(Section, Hl.1).

~

In December

1995,

and January

1996. dielectric pipe couplings failed and

this resulted in large volumes of non-radiological

water spills.

During

the inspection period inspectors revisited planned replacement activities

and noted that such replacements/repairs

were satisfactory

(Section H2.1).

~

During the previous inspection period inspectors identified an increase in

the number of EDG problems

and failures.

A review of some of these

items

was conducted to determine the adequacy of'he licensee's

cause

analyses.

The inspectors

concluded that the failures were isolated

and appeared

not

0

0

to have

a

common tie.

However, the inspectors

continued to review these

issues

and, therefore,

IFI 96-10-04 remains

open (Section H4.1).

~

On November

19 and 21, the inspectors

reviewed licensee

freeze protection

program activities.

The inspectors

found that the circulating water intake

structure

and

RHRSW room freeze protection program items were satisfactory.

Inspection of the freeze protection program continues

(Section H8.2).

En ineerin

~

Following a Unit 2 scram on October 29, the main steam relief valves failed

to operate at setpoint

due to a continuing generic problem of corrosion

bonding of the pilot disc and seat.

The licensee appropriately

removed all

relief valves

and recertified them.

The inspectors

reviewed various

documents related to the event

and valve rebuild, recertification and

testing specifics.

A Non-Cited Violation (NCV) was identified for failure

to evaluate out of tolerance lift reseat

data

(50-260/96-12-02)

(Section

E2.1) .

Plant

Su

ort

, ~

~

On October

19,

a calibration source

was found outside its

designated'torage

location.

This issue

was identified by the licensee

soon after it

had occurred.

Due to both source shielding configuration and its location

the radiological

hazard

was low.

Since the issue

was licensee-identified,

has not been

a prior problem and because it was immediately corrected it

was identified as

an

NCV 50-259,260,296/96-12-04

(Section R4.1).

~

On October

23, inspectors

observed portions of an emergency

preparedness

(EP) exercise.

The inspectors

found the exercise/drill to be challenging,

fast-paced

and positive (Section Pl ~ 1).

0

Summar

of Plant Status

Re rt Details

Unit 1 remained in a long-term lay-up condition with the reactor defueled.

Unit 3 operated at power for the report period.

With the exception of the

period of time noted in the following paragraph,

Unit 2 also operated at rated

power during the report period.

On October 29,

1996, at 3:38 p.m.,

an automatic reactor scram occurred

on

Unit 2 due to main turbine control valve fast closure.

The unit main

generator field collapsed

due to an exciter malfunction,

and the resultant

voltage and cur rent condition caused

generator

backup relays to operate.

The

associated

switchyard breakers

opened

and

a power load imbalance initiated

fast closure of the main turbine control valves.

This resulted in an

automatic reactor

scram.

The generator exciter was repaired,

reactor

criticality was achieved

on November 3.

1996,

and the unit was retur ned to

rated

power operations

on November 4,

1996.

On November 6,

1996, the Unit 3

ECCS Division I ATU Inverter failed and was

declared

inoperable.

Appropriate Technical Specification

(TS) Limiting

Condition for Operations

(LCOs) were entered

and on August 6, the licensee

notified the

NRC in accordance

with 10 CFR 50.72.

The inverter was repaired

and declared operable.

On November 8,

1996, Unit 3 power was reduced to 70

percent for control rod pattern adjustments

and condenser

waterbox cleaning

activities.

Unit 3 was returned to full rated

power

on November 9,

1996,

and

operated

at power for the remainder of the reporting period.

I. 0

rations

02

Operational

Status of Facilities and Equipment

02.1

Unit 2 Scram

Due to Hain Generator Exciter Problem

a.

Ins ection Sco

e

71707

93702

The inspectors verified that the licensee

took the appropriate

actions

in response to the Unit 2 automatic reactor scram on October 29,

1996.

b.

Observations

and Findin s

On October

29,

1996, Unit 2 automatically

scrammed

due to a problem with

the main generator excitation system.

The licensee

determined that the

opening of two switchyard breakers

which act as

a backup to the main

generator

breaker

caused

a fast closure of the main turbine control

valves which in turn resulted in the automatic reactor

scram.

The

licensee

determined that the system worked as designed;

however, they

planned to review the design to determine if the coordination

between

the backup (switchyard)

breakers

and the main generator

breaker

was in a

preferred condition.

0

0

The main generator excitation system problem was caused

by a failure ini5

the alternator-exciter collector brush set

and ring. The licensee

repaired the exciter collector ring and replaced the brushes.

Unit 3, "---';,

brushes

were also checked

and 3 brushes

were replaced.

The licensee

placed the Unit 2 mode switch to startup

on November 3,

1996 at

3:00 a.m.,

CST and took the reactor critical at 5:45 a.m.,

CST.

The licensee

determined that the loss of exciter output was caused

by '->

insufficient contact

between the brushes

and the positive collector

ring.

This was attributed to the correct

brush replacement criteria

having been inadvertently deleted

from the instruction in 1990 during

a

procedure consolidation project.

The licensee

changed

procedure

EPI-0-

047-TST-001

on October 30,

1996, to reflect the brush inspection/

replacement criteria recommended

by the vendor.

Conclusions

The licensee appropriately addressed

the failure of the exciter brush

set

and ring.

In addition, the licensee's

response to the Unit 2

automatic scram

was satisfactory.

Unit 3 Emer enc

Core Coolin

S stem

ECCS

Division I Inverter Failure

Ins ection Sco

e

71707

92700

93702

The inspectors

reviewed the actions taken by the licensee in response to

a Unit 3 Division I ECCS

ATU Inverter

power failure.

Observations

and Findin s

On November 6, 1996, the Unit 3 Division I ECCS ATU Inver ter power

was

lost due to

a fuse failure.

This inver ter supplies

power to 2 of 4

channels of drywell pressure

and the reactor water level sensors.

The

sensors

supply both divisions of initiation logic for RHR,

CS,

HPCI,

ADS, and the

EDGs.

Other sensors

for reactor pressure,

containment

and

RCIC are also supplied by this inverter

.

Since the other channels of instrumentation

are powered by the

Division II inverter, the logic of all

ECCS divisions would have been

initiated, if required.

With the exception of RCIC and the Division I

input into the Anticipated Transient Without Scram (ATWS)/Recirculation

Pump Trip (RPT) logic, all systems

would have performed their design

function.

Because this ATWS/RPT logic was inoperable

a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />

LCO (TS 3.2.L) was entered.

The Division II ATWS/RPT logic was operable

and

would have performed

as designed.

Approximately eight (8) hours after the inverter

was lost, the fuse was

repaired.

Inverter performance

was tested

and the inver ter performed

satisfactorily.

The

LCO was exited and the inver ter

was placed

back in

service.

All ECCS systems

were restored to pre-event conditions.

.L

r

'%~y

41

0

There have been recent Unit 3

ECCS inver ter failures (Reference

NRC IR

96-08, Section 02.2).

On July 17,

1996, the Unit 3 Division I Inverter

failed due to

a control board

and SCR/Diode failure.

On August 6, 1996,

the 3A inverter

again failed due to a similar circuitry problem.

Conclusions

Licensee analysis to determine the exact cause of these failures is on-

going.

The licensee is implementing

a backup source of uninterruptable

("DC-to-

DC") power to the circuitry.

The inspectors

reviewed

DCN T39853A which

documents installation of this power supply modification in the upcoming

February

1997 Unit 3 outage.

A similar DCN (T39852A) and modification

is being planned for Unit 2 installation during the Fall

1997 Unit 2

outage.

Because

a specific cause of these Unit 3 inverter failures has not yet

been determined

by the licensee,

this issue will remain open

and

continues to be addressed

as Inspection Followup Item (IFI) 296/96-

08-02,

Emergency Core Cooling System Inverter Failure.

Unantici ated Unit 3 A and

B EHC Pressure

Re ulator

Swa

in

Problems

Ins ection Sco

e

71707

92700

The inspectors

reviewed the actions taken by the licensee in response to

two unexpected electrohydraulic control

(EHC) pressure

regulator

swapping events:

Observations

and Findin s

On November 4,

1996, at 10:10 p.m., the Unit 3 "A" Hain Turbine

EHC

pressure

regulator

unexpectedly

swapped-over to the "B" pressure

regulator.

At 11:34 p.m., the

B regulator shifted back to the A

regulator.

No system perturbations

were observed during either shifting

evolution.

The operations

group initiated BFPER961500

and work request

(WR) 270073,

was initiated.

On November 5,

1996,

management

tasked

licensee engineering with review of the problem and with determining the

root cause of the unanticipated shift.

No other unexpected shifts

occurred over the next eight days.

On November

12,

1996, at 11:08 p.m.,

a control board operator noticed

that the

B EHC pressure

regulator indicating light was blinking on the

main control panel.

Upon further examination of the problem, the Unit

Supervisor,

control board operator

and the Unit Hanager noticed that the

A EHC indicating light also remained energized.

This indicated that the

A and

B EHC pressure

regulators

were both intermittently regulating

EHC

pressure.

However,

as of November 4,

no system

per tur bations

were

observed.

WR f270073 was immediately, upgraded to a priority 2, "high-

risk," work order

(WO) 96-014296-000.

On November 13,

1996 at

6:00 a.m., the

B regulator

had completely taken over pressure

control

0

0

Cl

and the A regulator indicated

a backup control function.

Primary

EHC

pressure

control

had fully shifted over to the

B regulator.

Licensee

18C was contacted

and the drift between the A and the

B regulators

was

readjusted to maintain

a licensee-desired

1~r, psi bias between the

regulators.

At the end of the inspection period, licensee

engineering

continued to

investigate the problem and

had requested

and received vendor

assistance.

From November 13-21,

1996, the licensee operations

group

monitored and recorded the desired bias

on a daily basis.

The licensee

then intended to monitor and record this bias

on a weekly basis until

December 21,

1996. If the regulator drift was not excessive,

and if the

drift appeared

manageable,

the monitoring/recording of the bias is to be

performed

as

a quarter ly PH.

Conclusions

The licensee's

troubleshooting activities and increased

monitoring were

appropriate.

EDG Auxiliar

Boar d Room Exhaust

Fans

Ins ection Sco

e

71707

On several

occasions

during the report period, the inspectors

toured

accessible

plant areas in accordance

with guidance presented

in

IP 71707.

Observations

and Findin s

The inspectors

toured the Unit 3

EDG Auxiliary Board Rooms on

November 19,

1996,

and observed that

EDG auxiliary board

room exhaust

fan handswitches

3-HS-030-0243

and 3-HS-030-0244

wer e in the

OFF

position,

and the fans were not'running.

These exhaust

fans were for

rooms

3EA and 3EB, respectively.

The inspectors

noted that the room

temperatures

were not elevated.

The inspectors

questioned

the Unit

Hanager

about the correct position of the fans.

On November 20,

inspectors

toured the area again,

and identified that one fan handswitch

was in the

ON position and running, while the other fan handswitch

was

still in the

OFF position and not running.

The inspector s questioned

the Unit 3 Supervisor

on November 20, about why one was

ON and running

and one was in the

OFF position.

On November 22, the inspectors

followed up on the issue with the Unit 3 Reactor

Operator,

who stated

that both fans were in the

ON position and running.

The inspectors

reviewed licensee

procedure

O-OI-30F,

Common and

EDG

Building Ventilation, Revision 15.

The purpose of this procedure is to

provide precautions

and limitations, prestartup/standby

readiness

requirements

and procedural

steps for operations of the diesel

generator

and intake building ventilation.

Section 4.0 provides the standby

readiness

requirements for various ventilation systems,

including the

common building ventilation panel.

Section 4.1.2.4 requires that the

system lineup checklists

are current using Attachment

2AS,

Common

Building Ventilation Panel

Lineup Checklist, Unit 3.

Attachment

2A

states that the required position of the diesel Auxiliary Board

Room 3EA

and 3EB exhaust

fan handswitches

3-HS-030-0243

and 3-HS-030-244 is ON.

Note (1) to this requirement states that unless

maintenance is, being

performed,

these

fans should be kept in service to prevent excessive

temperatures

when the diesel

generator

480V auxiliary boards

are

energized.

In addition, this note references

LER 260/89022,

R1.

This

LER was issued

due to an inoperable

Standby

Gas Treatment

system,

due in

part because

the

EDG auxiliary board

room exhaust

fans were not

operating,

resulting in elevated

room temperatures

and causing the

relative humidity control heater circuit breakers to trip.

The licensee

provided corrective action in this

LER that appropriate plant

instructions will be prepared

addressing

the operation of the exhaust

fans for the Diesel Generator Auxiliary Board Room.

Based

on this

information, the inspectors

determined that the required position of

these fan handswitches

is in the

ON position, with the fans in service.

As such, the licensee failed to follow procedure

0-0I-30F.

The inspectors

learned that the handswitch positions for the Unit 2

exhaust

fans are currently verified on

a shiftly basis

as part of 0-GOI-

300-1, Operations

Routine Sheets,

dated

November 15,

1996.

However, the

Unit 3 handswitch positions are not on the routine sheets,

and thus are

not verified to be in the proper position.

The inspectors

consider this

to be the second

example of inadequate

and/or failure to follow

procedures.

On November

22, the licensee

changed

procedure

O-GOI-300-1,

Attachment 15.18, to include the verification of both Unit 3 diesel

auxiliary board

room exhaust

fans.

The inspectors

discussed this issue with plant personnel

on the morning

of November 22,

and determined that no

PER had been initiated to review

this issue,

and the issue

was not logged in the main control

room logs.

Conclusions

The inspectors

concluded that the licensee failed to follow procedure

0-OI-30F in that the diesel auxiliary board

room exhaust

fans were not

in the required position.

This issue is identified as violation 50-

296/96-12-01,

Failure to Ensure Proper Position of EDG Aux Board

Room

Exhaust

Fans.

In addition, procedure

0-GOI-300-1 was found to be

inadequate

in that it did not require verification of the proper

position of the diesel Auxiliary Board

Room 3EA and

3EB exhaust

fans.

This is the second

example of violation 50-296/96-12-01.

In addition, the inspectors

concluded that the licensee did not

demonstrate

the appropriate sensitivity toward

a plant equipment

configuration control issue

when initially identified on November 19.

The inspectors

noted that no

PER was initiated until November 22.

The

licensee did not initially conduct

a thorough extent of condition

review, did not realize that both exhaust

fans were required to be in

the

ON position by procedure

O-OI-30F,

and did not identify that

procedure

0-GOI-300-1 was inadequate.

0

0

08

08.1

6

Hiscellaneous

Operations

Issues

(92901)

(Closed)

LER 50-296/96-005-00:

Reactor

Scram Required by Technical

Specification

Due to Trip of Reactor Recirculation Hotor Generator

Set

3A.

This Licensee

Event Report

(LER) was submitted, due to a plant

shutdown required by Technical Specifications.

Unit 3 experienced

a

trip of the,3A reactor recirculation

pump due to a fault in the

associated

motor-generator

set.

Based

upon the inspection

documented in

NRC IR 96-10, Section 04.1, this

LER is closed.

H1

Conduct of Maintenance

II. Maintenance

H1.1

a.

b.

Unit 1 Lon -Term La -u

Conditions

- Maintenance

Observations/Reviews

Ins ection Sco

e

92050

This portion of the inspection

was conducted to assess

the licensee's

preventative

maintenance

program, including long term lay-up conditions

on Unit 1 components

not required for Unit 2 or

3 operation.

The

inspector evaluated the adequacy of the program based

on the on-site

procedures.

The Unit 1 inspection effort consisted of field

inspections.

transfer controls for transferring equipment

from Unit 1 to

Unit 2,

3 or Sequoyah,

ongoing preventative

maintenance activities and

documentation.

Observations

and Findin s

The field inspections

were conducted in the reactor

building, auxiliary

building and included observation of the off-gas system,

steam jet air

ejector, stator cooling pump A, feedwater

heaters,

control rod drive

pump,

RHR pump, core spray

pump, lube oil cooler heat exchanger,

and

HPCI pump.

The applicable procedure

(SSP-12.52

Plant Lay-up and Preservation

Revision 5) that implemented the Unit 1 lay-up and preventative

maintenance

program

was reviewed.

Documentation of completed

PHs were

reviewed for adequacy

and included documents

1-HTR-068-0000A,

1-HTR-068-

0060B,

1-GEN-068-OOOOB. and 1-PHP-002-056.

The inspector also reviewed

Nuclear

Assurance

and Licensing Assessment

Report NA-BF-96-011, internal

memorandum

dated January

5,

1996, that deleted certain

PH tasks,

and

BFPER951039 that identified problems with the lay-up program.

The in-plant storage of equipment

was found acceptable.

Hotors were

observed to be adequately

covered

and heat

was being applied to the

motor windings.

Piping systems

were observed to be under

adequate

humidity controls for inside surfaces.

Housekeeping in the areas

reviewed were found acceptable.

0

III

The procedure

reviewed

was found acceptable

and implementation of the

preventative

maintenance

inspections

were found acceptable.

Conclusions

The in-plant storage of Unit 1 equipment

was observed to be adequately

controlled and consistent with long term storage

requirements.

The

records being generated

for the storage,

transfer,

and preventative

maintenance activities were adequate

and consistent with record

retention requirements.

Maintenance

and Material Condition of Facil.ities and Equipment

Unit 2 and 3 Dielectric Cou lin

Re airs

-

Re lacement Activit

U date

Ins ection Sco

e

62707

92902

The inspectors

reviewed repair activities associated

with replacement of

various Unit 2 and Unit 3 dielectric couplings.

The inspectors

assured

that activities were conducted in a manner that ensured reliable post-

maintenance

(post-coupling replacement)

operation of affected systems.

Observations

and Findin s

On January

24,

1996,

(Reference

NRC IR 96-03),

a 2-inch condensate

storage

and supply pipe broke spilling about 15.000 gallons of water in

the Unit 2 reactor building.

Operators identified the break to be

a

ipe coupling which. penetrated

the ceiling.

A similar coupling break

ad occurred in December

1995.

The couplings were embedded in concrete,

were made of a resin-type substance

(a dielectric)

and served

as

transition pieces

between existing stainless

steel

and aluminum piping.

Both of the couplings were replaced

and these

systems

were returned to

their normal alignments.

The inspectors

who reviewed these

events

determined that in both cases

no safety-related

equipment

had been

affected.

The inspectors

concluded that in both cases

licensee

responses

to the event were acceptable

considering the location of the

coupling failures and the relative obscurity of the piping.

Licensee

problem evaluation report

BFPER960151

was subsequently

initiated to,

1) identify additional couplings of this type,

2) to

determine if further actions were needed,

and 3) document

and track an

effective program of dielectric coupling repair .

II

0

c.

Conclusions

The inspectors

reviewed

an on-going program of dielectric coupling

replacement/repair

and noted the following:

~

Repairs/replacement

of both Unit 2 and Unit 3 couplings

have been

performed since

Hay 1996.

~

Of the 81 identified/scheduled

for repair,

57 have been replaced

(-701);

14 in the Unit 2 Reactor Building (RB); 42 in the Unit 3

Reactor Building (RB).

~

All Unit 3 RB couplings

have been replaced

and by the end of

January

1997 all Unit 2 couplings are scheduled to be replaced.

~

Two Unit 3

EDG couplings are scheduled for replacement

in February

1997.

This replacement will complete the scheduled

program of

dielectric coupling repair.

The inspectors

have noted, during routine tours of the facility that

associated

repair activities have been performed in a satisfactory

manner.

The inspectors

have also noted that on-going repair activities

are proceeding

as scheduled.

t

M4

Maintenance Staff Knowledge and Performance

H4.1

EDG Material Condition Concerns

a.

Ins ection Sco

e

62707

During the previous inspection period, the inspectors identified an

increase in the number of EDG problems

and failures (IFI 50-259,260,296/

96-10-04).

A review of'ome of these

items was performed to determine

the adequacy of the licensee's

cause

analyses.

b.

Observations

and Findin s

The inspectors

reviewed the following issues identified in IFI 96-10-04:

August 30,

1996,

3B EDG air pressure

in header

low-alarm received

without either

air

compressor

star ting.

Discussions with the system engineer

indicated that this failure

could most likely be attributed to painters.

WRs have

been

written to replace all flex hoses

(hydraulic/air ) on Unit 3.

Unit 1 and 2 EDGs do not have these flex hoses.

Replacement

is

planned for completion by the end of 1997.

September

1, 1996.

3C

EDG overspeed trip relay actuated to trip

EDG output breaker; identified during routine surveillance.

0

0

This overspeed trip relay consists of a limit switch which was out

of adjustment

due to vibration.

Licensee corrective action

consisted of relay replacement.

The inspector

reviewed failure

and surveillance test history of EDG overspeed trip relay limit

switches during the past two years,

and noted that there were no

other failures of these switches.

~

September

4,

1996, the 2A EDG oil circulating pump was discovered

to have

a broken coupling.

This was identified by an Assistant

Unit Operator

(AUO) when it was noted that oil temperatures

were

lower than normal.

The inspector

reviewed the failure and surveillance history of the

EDG oil circulating pumps for the previous

2 year period,

and

noted

no similar failures.

~

October

11,

1996,

2A EDG problem identified with start circuit 2

pinion aux relay; identified while the diesel

was inoperable for

two-year maintenance.

The inspector

reviewed the failure history of these relays,

and

determined that the licensee

had previously identified a failure

trend in December

1995

(BFPER951830).

In addition,

BFPER951828

and BFPER951360

were initiated to document increased

failures with

this relay.

The failure mechanism

was due to dried grease

on the

plunger of the timer, resulting in slow response.

In response,

the licensee

conducts

a visual examination of the relays

(approximately

12 per

EDG) during the 2 year

PHs,

and replaces

any

which have excess

accumulation's of grease

on the plunger.

In

addition, solid state relays

have been

used for replacement of

some relays.

The licensee's

review determined that the

October ll, failure was not due to dried grease.

The inspectors

consider

the licensee's

identification of a negative failure trend

for this issue to be good;

c. Conclusions

Of the above

EDG problems originally identified in IFI 96-10-04, the

failures appear to be isolated examples

and do not have

a

common tie.

The licensee's

cause analysis

was adequate

for the above issues,

and

appropriate corrective actions

have been taken or planned in the four

cases

reviewed.

The inspectors will continue to review additional

examples of recent

EDG problems,

and as such this IFI will remain open.

H8

Hiscellaneous

Haintenance

Issues

(92902,

71714,

62707,

40500)

H8.1

(Closed) IFI 50-259,260,296/95-64-11:

Thread Lubricant Effects on

Torque Values.

This issue

concerned

an apparent

discrepancy

between

engineering

guidance

used by maintenance

personnel

in determination of

torque values

when thread lubricant is (and is not) used.

In response,

the licensee

issued

BFPER951122 to review this issue.

The licensee

issued

a revision to HSI-O-OOO-PR0017,

General

Torquing Guide, which

II

0

10

deleted the requirement for utilizing table multiplication factors,

such

as multiplying table values

by 0.9 when fastener

threads

are lubricated.

In addition. the procedure

was revised

such that when there is

a concern

of adequacy or component

damage resulting from the use of the listed

torque value, the table torque value can be increased

or decreased

by 10

percent or torque can be calculated.

The inspectors

consider

licensee

actions for this issue to be appropriate

and this issue is closed.

Im lementation of the Freeze Protection

Pro ram

Ins ection Sco

e

71714

92902

The inspectors

reviewed activities related to implementation of the

licensee's

freeze protection program.

The inspectors

assured that such

activities were conducted in a manner

consistent with procedure

0-GOI-

200-1 Freeze Protection Inspection

and W(596009582000,

Annual Inspection

5 Preventative

Haintenance of Freeze Protection

Systems.

Observations

and Findin s

On November

19 and 21,

1996, the inspectors

toured the residual

heat

removal service water

(RHRSW) building and circulating water intake

structures

and inspected

freeze protection systems.

In the

RHRSW areas

the inspectors

noted that portable heaters

were staged;

however, they

were not yet plugged into their associated

220VAC power supplies.

Operations

and,maintenance

management

personnel told the inspectors that

they would be energizing the space

heaters

when sustained

temperatures

of twenty-five (25) degrees

F or below were being met.

Twenty-nine (29)

degree

F temperatures

were the lowest outside temperatures

experienced

during the inspection period.

The inspectors

also noted that

RHRSW

sample station area thermostats

were properly set for weather conditions

(ON at 40 degrees

F) and they noted that

RWRSW pump motor

space

heaters

and intake piping heat trace

power supplies'ere

energized.

Conclusions

Initial inspector review of freeze protection procedures

and field

activities revealed that the licensee's

current efforts are adequate to

provide necessary

protection to guar d against cold weather conditions.

The inspectors will continue review during the next inspection report

period.

Third-Part

INPO

Assessment

of Plant Haintenance Activities

40500

The inspectors

reviewed

an October

24,

1996 Institute of Nuclear Plant

Operations

(INPO) to Site Vice President letter pertaining to an

October

8 to 10,

1996 assessment

of licensee

maintenance activities.

In

general

the results

were not inconsistent with NRC assessments

in this

area.

0

0

III. En ineerin

Engineering Support of Facilities and Equipment

SRV Failed to 0 crate at Set oint

Ins ection Sco

e

37551

71707

Following the October 29, Unit 2 scram,

the licensee identified that the

main steam safety valves should have lifted and failed to do so.

The

inspectors

reviewed licensee

data

(see attachment)

for the

13 SRVs

removed from Unit 2 after the scram.

The inspector s also reviewed

portions of the Safety Parameter

Display System

(SPDS) reactor pressure

data which indicated that reactor pressure

wide range point 3-54 reached

1131 psig -during the event.

The inspectors

reviewed portions of

surveillance instruction O-SI-4.6.D.1,

Bench Test Relief Valves,

Revision 8,

and the associated

urgent intent change

(UIC-10).

Observations

and Findin s

During the Unit 2 Scram on October

29,

1996, reactor

pressure

wide range

instr.ument,point

3-54 indicated

1131 psig.

The licensee

determined that

this pressure, exceeded

the main steam safety/relief valve

(SRV)

setpoints

on 8 of the 13 valves.

Technical Specification

(TS) Safety

Limit 1.2 requires that the pressure

at the lowest point of the reactor

vessel

shall not exceed

1375 psig whenever irradiated fuel is in the

reactor vessel.

TS Limiting Safety System Setting

(LSSS) 2.2 applies to

trip settings of the instruments

and devices

which are provided to

prevent the reactor

system safety limits from being exceeded.

The LSSSs

for the SRVs are as follows:

1105 psig s 11psi

(4 valves)

[1094-1116 psig]

1115 psig s 11psi

(4 valves)

[1104-1126 psig]

1125 psig a 11psi

(5 valves)

[1114-1136 psig]

The licensee

entered cold shutdown conditions

on October

31,

1996, at

2:12 a.m.

[CST].

The licensee

removed all of the 13 SRVs and tested

them at an off-.site contract test facility.

Licensee data

showed that 3

of the

13 SRVs removed from the vessel fell within their acceptable

LSSS

range.

The licensee's

safety evaluation concluded that the failures

would not have resulted in exceeding the Safety Limit for any abnormal

transient

(LER 96-08).

This is

a well known generic problem that the

licensee

continues to experience.

The licensee

has

documented

the issue

in several

LER's and continues to pursue resolution through the

BWR

Owners Group.

The licensee attributed the setpoint drift of the

remaining valves to corrosion bonding of the

SRV pilot disc and seat.

The inspectors

reviewed the surveillance instruction and verified that

the as-left setpoint for the 13 SRVs were within their specific

LSSS

range.

While discussing the procedure with engineering

personnel

following restart of Unit 2, it was brought to the inspectors attention

that

a por tion of the procedure

had not yet been completed.

The

0

0

0

C.

12

procedure

addresses

certain guidelines which needed to be met. If not

met, it required either

a Technical Operability Evaluation

(TOE) to be

completed

or required the valve to be rebuilt and recertified.

Four of

the valves,

which had been returned to service,

did not meet the

procedural

guideline for percent reseat

and the licensee

had not written

a TOE or rebuilt and recertified the valves prior to installation of the

pilot valve as required by the procedure.

The licensee

subsequently

implemented

UIC-10 on the procedure

which

eliminated the requirement

discussed

previously.

It instead required

that the system engineer

determine acceptability for installation.

In

addition, the acceptance criteria portion of the procedure

was changed

to require that reseat

values outside the approved guideline limits will

be evaluated

by the System Engineer for installation acceptability

and

the evaluation documentation will be included with the SI.

The System Engineering Evaluation that addressed

the four valves which

were outside the reseat

guidance specified in the procedure,

determined

that the margin to reseat is acceptable

from a performance standpoint.

In addition, it appear s that TVA Engineering

was aware that the percent

reseat

values were outside of the acceptance

range

and that it was

determined to be acceptable.

This was noted

on the test data

page that

was supplied to the licensee

by the contr act test facility.

This failure to conduct

a TOE as required by procedure constitutes

a

violation of minor significance

and is being treated

as

a Non-Cited

Violation, consistent with Section IV of the

NRC Enforcement Policy

(NCV 50-260/96-12-02).

Conclusions

E8

E8.1

E8.2

The inspectors

determined that the licensee's

actions, to'bring Unit 2

to cold shutdown,

and remove

and test the 13 SRVs, were appropriate.

Miscellaneous

Engineering Issues

(92902)

(Closed)

LER 296/94-02:

A Deficiency Regarding

Raychem Tubing Used for

Environmental

Qualification Applications.

The licensee

issued this as

a

voluntary LER.

The licensee

reviewed the use of Raychem tubing, type

WCSF-070N, Lot No. N15057,

used to insulate the splice connection of

Conax

ECSA conductors to the conductors of their respective field cables

for Unit 3.

The licensee identified two uses of Lot No. N15057 in

Unit 3,

and no uses

for Unit 2.

The Unit 3 applications

were well

within the revised allowable use range

as specified by the vendor.

The

inspectors

consider

licensee

actions for this issue to be satisfactory

by (1) reviewing if the particular

Lot number of Raychem splices

was

used in Unit 3,

(2) evaluating whether the application was consistent

with vendor

recommendations.

This

LER is closed.

(Closed)

EEI 260/96-05-01:

RCIC Inoperability Following Replacement of

Turbine Exhaust

Check valve.

A predecisional

enforcement

conference

was

held on July 11,

1996.

A Notice of Violation was issued in

0

0

0

13

correspondence

dated August 1, 1996.

Followup to the violation is being

tracked under

NOV ID No. 01013.

E8.3

(Closed)

EEI 260/96-05-02:

Failure to Comply with IST Procedures

for

Testing

RCIC and HPCI Following Turbine Exhaust

Check Valve Replacement.

A predecisional

enforcement

conference

was held on July 11,

1996.

A

Notice of Violation was issued in correspondence

dated August 1.

1996.

Followup to the violation is being tracked

under

NOV ID No. 02014.

E8.4

(Closed)

URI 260/96-04-03:

Shutdown Cooling Low Level Isolation

Bypassed Prior To Cavity Flood-up.

This URI was opened

as the result of

questions

raised by the inspectors

during the Spring 1996 Unit 2

refueling outage.

In a November Office of Nuclear Reactor Regulation

(NRR) letter to the licensee staff,

NRR stated that they had reviewed IR

50-259,260,296/96-04

and that they had also reexamined the following:

~

TVA's 10 CFR 50.59 safety evaluation

and assessment

performed to

support bypassing the isolation function.

~

NUNRC 91-06,

"Guidelines for Industry Actions to Assess

Shutdown

Hanagement".

~

IR 50-259,260,296

which described

an inadvertent loss of reactor

vessel

inventory just prior to Unit 3 restart in November

1995.

~

IR 50-259.260,296/96-300,

documenting initial reactor operator

license examination results

where most candidates

gave incorrect

responses

to a question

on shutdown cooling valve interlocks.

~

A September

6,

1996 TVA submittal requesting

implementation of

improved standard technical specifications

based

upon NUREG-1433,

"Standard Technical Specifications

General Electric Plants

BWR/4".

~

An April 19,

1994 safety evaluation supporting

a TS amendment

which revised

LP coolant injection oper ability requirements

in

shutdown

modes.

Based

upon the review the

NRR staff concluded that TVA's actions to

bypass the isolation, while permissible with existing the TS was

inconsistent with overall industry practice

and

NRC standards.

As a

result of discussions

between

NRR and TVA, TVA submitted

a letter

dated

October 22,

1996,

and committed to revise procedures.

The isolation

function would no longer

be bypassed.

TVA also stated that they would

revise their improved standard technical specification

(ISTS) submittal

to,be consistent with NUREG-1433 requirements for isolation oper ability

in shutdown

modes.

Based

upon this letter

and completion of

commitments,

URI 96-04-03 is closed.

li

0

R4

R4.1

a.

14

IV. Plant Su

rt

Staff Knowledge and Performance in ROC

Co-60 Calibration Source

Found Outside Its Desi nated Stora

e Location

Ins ection Sco

e

71750

b.

C.

The inspectors

reviewed licensee

actions regarding misplacement of a Co-

60 calibration source.

The review included follow-up observation of

areas

near the licensee-designated

radioactive source storage cabinet,

examination of a licensee-initiated

BFPER961412,

review of an October

21,

1996, radiological control

(RADCON) memo and discussions

with RADCON

management

and the Region II RADCON specialist.

Observations

and Findin s

On October 19,

1996,

a Co-60 Area Radiation Honitor (ARH) calibration

source

was found outside its designated

storage location.

A RADCON

technician discovered the source (located inside its own individual

case)

on the floor approximately 2 feet away from its locked source

storage

cabinet location.

The source's

case

was properly labeled

and

the sour ce itself was appropriately tagged

and contained inside of the

shielded

case.

Haximum case contact

dose readings

(from the -150pCu

source)

measured -2.5 mrem/hr.

In a discussion with the inspectors,

RADCON management

indicated that

a

member of their staff had removed the source,

and its source

case,

from

the cabinet in order to get to another

source

case.

The technician did

this in order,to record data listed on the other case.

The technician,

later in his shift, found that he needed

more data from the other

source

case.

After the second

check the technician forgot to place the 150pCu

source

back into its designated

storage locker as

he had done during his

first check.

This event was identified soon after it had occurred,

and due to both

source configuration

and location, the radiological

hazard

was low.

Conclusions

The cause of the event was

a lack of attention detail.

As noted by the

licensee,

handling of'y-product materials

requires strict adherence

to

criteria specified in licensee

procedure

SSP-5.3,

Controlling Byproduct

8 Source Haterial Sources.

As part of the licensee's

corrective actions

in a memorandum

dated October

21,

1996 event details were presented to

all licensee

RADCON staff and management

personnel.

Licensee

management

corrective actions included individual counseling.

This licensee-identified

and corrected violation is being treated

as

a

Non-Cited Violation, consistent with Section VII.B.1 of the

NRC

Enforcement Policy (260,296/96-12-03)

~

0

15

Pl

Conduct of Emergency Preparedness

(EP) Activities

P1.1

EP Trainin

Exercise/Drill

Observations

and Findin s

71750

On October 23,

1996, the inspectors

observed portions of the emergency

preparedness

training drill/exercise.

Through the inspectors'eview of the drill scenario

and observations

in

the Technical

Support Center

(TSC), it was determined that the drill was

challenging

due to the fast pace of the scenario.

In addition, the

initial conditions of. the scenario

had the unit in a refueling outage

which was

a positive exercise for the staff considering Unit 3 will

begin

a refueling outage in February 1997.

X1

Exit Meeting Summary

V. Mana ement Meetin s

The resident inspectors

presented

overall inspection period results to

licensee

management

on November 22,

1996.

The licensee

acknowledged the

findings presented

and the inspectors

asked the licensee

whether

materials

examined during the inspection should be considered

proprietary.

No proprietary information was identified.

Licensee

'PARTIAL LIST OF PERSONS

CONTACTED

T. Abney, Licensing Manager

J. Brazell, Site Security Manager

G. Bugg, Acting Manager,

Radiological Control

and Chemistry

R. Coleman, Acting Radiological Control Hanager

C. Crane, Acting Plant Hanager

J.

Johnson,

Site Quality Assur ance

Hanager

R. Jones,

Operations

Hanager

G. Little, Operations

Superintendent

R. Hachon, Site Vice President,

Br owns Ferry

G. Pier ce,

System Engineering

Hanager

T. Shriver,

Nuclear

Assurance

and Licensing Hanager

K. Singer,

Maintenance

Hanager

H. Williams, Engineering

and Haterials

Hanager

NRC

J. Williams, Browns Ferry Project Hanager

0

16

IP 37551:

IP 62707:

IP 71707:

IP 71750:

IP 92050:

IP 92700:

IP 92901:

IP 92902:

IP 93702:

INSPECTION PROCEDURES

USED

Onsite Engineering

Maintenance

Observations

Plant Operations

Plant Support Activities

Review of Quality Assurance f'r Extended Constrauction

Delays

Onsite Followup of Written Reports of Nonroutine Events at Power

Reactor Facilities

Followup-Plant Operations

Followup-Maintenance

Prompt Onsite Response to Events at Operating

Power Reactors

Opened

ITEMS OPENED

CLOSED

AND DISCUSSED

T~

Item 'Number

Status

VIO

50-296/96-12-'Ol

Open

Descri tion and Reference

Failure to Ensure Proper Position of EDG

Aux Board

Room Exhaust

Fans

(Section 02.4)

NOV

01013

NOV

02014

Closed

Open

Open

RCIC Inoperability Following Replacement

of Turbine Exhaust

Check Valve (Section

E8.2)

Failure to Comply with IST Procedures

for

RCIC and

HPCI (Section E8.3)

~T

Item Number

'Status

NCV

50-260/96-12-02

Closed

NCV

50-259,260,296/

Closed

96-12-03

LER

50-296/94-002-00

Closed

LER

50-296/96-005-00

Closed

Descr i tion and Reference

SRV Bench Test Procedure

Not Followed

(Section E2.1)

Uncontrolled Radiological

Source

(Section R4.1)

A Deficiency Regarding

Raychem Tubing Used

for Environmental Qualification

Applications (Section

E8. 1)

Reactor

Scram Required by Technical

Specifications

Due to Trip of Reactor

Recirculation Hotor Generator

Set

3A

(Section 08.1)

0

0

0

IFI

50-.259,260,296/

95-64-11

Closed

17

Thread Lubricant Effects on Torque

Values (Section H8.1)

EEI

50-260/96-05-01

Closed

EEI

50-260/96-05-02

Closed

URI

50-260/96-04-03

Closed

Discussed

~T

Item Number

Status

IFI

50-296/96-08-02

Open

IFI

50-259,260,296/

Open

'96-10-04

RCIC Inoperability Following Replacement

of Turbine Exhaust

Check Valve

(Section E8.3)

Failure to Comply With IST Procedures

for

Testing, RCIC and HPCI Following Exhaust

Check Valve Replacement

(Section E8.3)

SDC Low Level Isolation Bypassed Prior To

Cavity Flood-up (Section E8.4)

Descr i tion and Reference

Emergency Core Cooling System Inverter

Failure (Section 02.2)

EDG Haterial Condition Concerns

(Section H4.1)

0

0

0

Valve

Position

Setpoint

Serial Number

1st

2nd

Setpoint (psig)

3rd

4th

5th

6th

Setpoint

Deviation

Pilot Leakage

( ml / 5 min )

Pre-Leak

Post-Leak

Notes

2-PCV-01-004

1125

1078

1135

1134

1135

0.89

ND

ND

2-P CV-01-005

1115

1017

1240

1161

1121

1120

11.21

ND

ND

2-PCV-01-018

1115

1079

1147

1127

1123

1126

1121

2.87

ND

ND

2-PCV-01-019

1105

1072

1183

1106

1104

1104

1103

1112

7.06

ND

ND

7th: 1098

2-PC V-01-022

1115

1232

1129

1120

1110

1101

1110

1.26

ND

ND

2-PCV-01-023

1105

1084

1169

1115

1112

1110

5.79

ND

ND

2-PCV-01-030

1115

1061

1131

1121

1122

1126

1.43

ND

2-PCV-01-031

1105

1031

1141

1128

1119

1117

3.26

ND

ND

2-PCV-01-034

1105

1060

1163

1108

1105

1105

5.25

ND

ND

2-P CV-01-041

1125

1015

1183

1135

1134

1130

1135

1133

5.16

ND

ND

2-PCV-01-042

1125

1032

1160

1136

1136

1131

3.11

ND

ND

2-P CV-01-179

2-PCV-01-180

1125

1125

1064

1071

1136

1136

1124

1117

1116

1126

1122

1114

1125

0.98

0.98

ND

ND

ND

ND

7th: 1127,

8th: 1122,

9th: 1119

ND - data is not currently available. Willbe obtained from Wyle test report.

Attachment

e

0

'