05000220/LER-1979-008-03, /03L-0 on 790510:during Refueling Outage, Containment Spray Heat Exchangers 112 & 121 Failed Leak Rate Test.Caused by Tube Leaks.Tubes Plugged

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/03L-0 on 790510:during Refueling Outage, Containment Spray Heat Exchangers 112 & 121 Failed Leak Rate Test.Caused by Tube Leaks.Tubes Plugged
ML18037A172
Person / Time
Site: Nine Mile Point 
Issue date: 05/31/1979
From: Duda E
NIAGARA MOHAWK POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18037A171 List:
References
LER-79-008-03L, LER-79-8-3L, NUDOCS 7906110181
Download: ML18037A172 (2)


LER-1979-008, /03L-0 on 790510:during Refueling Outage, Containment Spray Heat Exchangers 112 & 121 Failed Leak Rate Test.Caused by Tube Leaks.Tubes Plugged
Event date:
Report date:
2201979008R03 - NRC Website

text

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