ML18036B129

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Insp Repts 50-259/92-41,50-260/92-41 & 50-296/92-41 on 921114-1216.Violations Noted.Major Areas Inspected: Surveillance Observation,Maint Observation,Operational Safety Verification & Mods
ML18036B129
Person / Time
Site: Browns Ferry  
Issue date: 12/22/1992
From: Kellogg P, Patterson C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18036B127 List:
References
50-259-92-41, 50-260-92-41, 50-296-92-41, GL-88-14, NUDOCS 9301200125
Download: ML18036B129 (21)


See also: IR 05000259/1992041

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report Nos.:

50-259/92-41,

50-260/92-41,

and 50-296/92-41

Licensee:

Tennessee

Valley Authority

6N 38A Lookout Place

1101 Market Street

Chattanooga,

TN

37402-2801*

Docket Nos.:

50-259,

50-260,

and 50-296

License Nos.:

DPR-33,

DPR-52,

and

DPR-68

Facility Name:

Browns Ferry Units 1, 2,

and

3

Inspection at Browns Ferry Site near Decatur,

Alabama

Inspection

Conducted:

November

14

December

16,

1992

Inspector:

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nt

nspector

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ate

>

ne

Accompanied

by:

J.

Munday, Resident

Inspector

R. Musser,

Resident

Inspector

Approved by:

au

.

e

og

Rea to

c ion 4A

Division of Reactor Projects

SUMMARY

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ate

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Scope:

This routine resident

inspection

included surveillance

observation,

maintenance

observation,

operational

safety

verification, modifications, Unit 3 restart activities, reportable

occurrences,

action

on previous inspection findings,

and nuclear

safety review board.

One hour of backshift coverage

was routinely worked during the

work week.

Deep backshift inspections

were conducted

on November

22,

and

December

12,

1992.

A two week

NRC plant design

change

team inspection

was performed.

An exit meeting

was conducted

on December

4,

1992.

The team

V30i200i25 92i223

PDR

ADDCK 05000259

8

PDR

concluded that

an adequate

design control process

was in place.

A

concern

was raised

about operator action required to open drain

valves in the hardened

wetwell vent modification.

Resolution of

this item is being pursued

by the licensee.

The results of the

inspection will be in inspection report 93-201.

One deviation

was identified for not meeting

a commitment in reply

to Generic Letter 88-14,

Instrument Air Supply System

Problems

Affecting Safety-Related

Equipment,

paragraph

four.

The licensee

has failed to verify adequate

margin exits between

the ambient air

temperature

and

dew point range at dryer outlets.

Some vendor

recommendations

have not been followed and test results repeatedly

fail other criteria.

Unit 2 operated

at power coasting

down in power level

and

was

on-line for 77 days at 76 percent

power at the end of the period,

paragraph

four.

The licensee

continues to impose administrative

limits on recirculation

pump speed

due to vibration concerns with

small lines

on the recirculation

system.

Major pre-outage

modifications continue with significant scaffold installation in

the plant.

Plant modifications

has

implemented

a modifications performance

monitoring program,

paragraph five.

This consists of a checklist

that task managers

use to monitor in the field activities.

This

is an effective means to provide real-time feedback to management.

An inspector followup item was identified concerning the failure

of an environmentally qualified limit switch, paragraph

three.

The switch will be examined during the refueling outage

and

any

programmatic

issues

addressed.

Unit 3 activities continued

on

a limited scope,

paragraph

six.

A

reassessment

of the remaining engineering

work continues.

An

estimated

one-half of the design

change notices

have

been

completed.

,

Persons

Contacted

REPORT DETAILS

Licensee

Employees:

0. Zeringue,

Vice President

  • J. Scalice,

Plant Manager

J. Rupert,

Engineering

and Modifications Manager

D. Nye, Recovery

Manager

  • H. Herrell, Operations

Manager

J.

Maddox, Project Engineer

  • H. Bajestani,

Technical

Support

Manager

A. Sorrell, Special

Programs

Manager

C. Crane,

Maintenance

Manager

  • G. Pierce,

Acting Licensing Manager

R. Baron, Site guality Manager

  • J. Corey, Site Radiological

Control

Manager

A. Brittain, Site Security Manager

Other licensee

employees

or contractors

contacted

included licensed

reactor operators,

auxiliary operators,

craftsmen,

technicians,

and

public safety officers;

and quality assurance,

design,

and engineering

personnel.

NRC Personnel:

B. Wilson, Branch Chief

P. Kellogg, Section Chief

  • C. Patterson,

Senior Resident

Inspector

  • J. Hunday,

Resident

Inspector

R. Husser,

Resident

Inspector

A management

meeting

was conducted

on site

on November

19,

1992, to

review the project status.

NRC attendees

were S. Varga, Director

Reactor Projects I/II; G. Lanias, Assistant Director Region II Reactors;

T. Ross,

NRR; J. Williams,

NRR;

H. Thadani,

NRR;

P. Kellogg, Section

Chief, Region II.

  • Attended exit interview

2.

Acronyms

and initialisms used throughout this report are listed in the

last paragraph.

Surveillance Observation

(61726)

The inspectors

observed

and/or reviewed the performance of required SIs.

The inspections

included reviews of the SIs for technical

adequacy

and

conformance to TS, verification of test instrument calibration,

observa-

tions of the conduct of testing,

confirmation of proper removal

from

service

and return to service of systems,

and reviews of test data.

The

inspectors

also verified that

LCOs were met, testing

was accomplished

by

qualified personnel,

and the SIs were completed within the required

frequency.

The following SIs were reviewed during this reporting

period:

2-SI-4.3.c,

Scram Insertion Times

The licensee

conducted

a load reduction

on December

12,

1992, to

perform scram time testing

as

by required

TS and conduct control

rod drive insert

and withdrawal time testing

on 83 control rods.

The

CRD testing

was conducted

under 2-TI-20, Control

Rod Drive

System Testing

and scram time testing

under 2-SI-4.3.c.

Prior to

the test the inspector

reviewed the procedures

and identified that

2-TI-20 only addressed

testing

when the plant was not operating.

This item was discussed

with the licensee.

The licensee initiated

a procedure

change

on December ll, 1992, to allow the procedure to

be performed while the reactor is operating.

The TI is designated

a complex infrequently performed test that

must

be performed per

SSP 8. 1.

This requires

a test director and

pre-job briefing.

The inspector

attended

the 7:00 a.m., operation

shift turnover meeting

and these

upcoming evolutions were

discussed

and the test director identified.

The inspector

observed

portions of the scram time testing in the control

room

and auxiliary instrument

room.

Each rod was individual

scrammed

from the auxiliary instrument

room and then fully withdrawn from

the control

room.

Personnel

performing the test

used

good

communications.

No deficiencies

were identified.

No violations or deviations

were identified in the Surveillance

Observa-

tion area.

3.

Maintenance

Observation

(62703)

Plant maintenance activities were observed

and/or reviewed for selected

safety-related

systems

and components

to ascertain that they were

conducted

in accordance

with requirements.

The following items were

considered

during these

reviews:

LCOs maintained,

use of approved

procedures,

functional testing and/or calibrations

were performed prior

to returning components

or systems to service,

gC records maintained,

activities accomplished

by qualified personnel,

use of properly certi-

fied parts

and materials,

proper

use of clearance

procedures,

and

implementation of radiological controls

as required.

Work documentation

(HR,

WR,

and

WO) were reviewed to determine

the

status of outstanding

jobs

and to assure that priority was assigned

to

safety-related

equipment

maintenance

which might affect plant safety.

The inspectors

observed

the following maintenance activities during this

reporting period:

a.

Feedwater

Leaks

On November

12,

1992, the inspector

observed

leakage

from the

reactor building ventilation duct on the

565

and

621 foot eleva-

tions in the reactor building as well as underneath

the torus.

The licensee

previously identified two steam or water leaks in the

main steam vault that they believed were being drawn

up into the

area ventilation exhaust

and then blown through the rest of the

vent duct work.

One leak appeared

to be

on the bonnet flange of

the 2-3-568, reactor feedwater

check valve and the other

a pres-

sure seal

leak on the 2-69-580,

RWCU return manual isolation

valve.

These

two leaks

account for about nine

gpm into the

reactor building floor drains.

The actual

source of the leaks in

the steam vault could not be verified due to the local radiation

field and the leak itself.

The inspector questioned

maintenance

personnel

about

when they were sure these

valves were in fact the

ones that were leaking.

The acting Maintenance

Manager

and the

inspector

viewed

a video tape previously made

by maintenance

personnel

that identified the leaks

coming from these

two valves.

The inspector

observed

the leaks

on November 23,

1992, to actually

be spraying

a steam

and water mixture onto other equipment in the

steam vault,

one of which is the outboard HSIV's.

During the

performance of 2-SI-4. 1.A-ll(II), Main Steam Isolation Valve

Closure Functional Test,

on November 28,

1992, the

D line outboard

HSIV, 2-FCV-1-52, failed to generate

a

RPS channel

B half-scram

when tested.

LCO 2-92-402-3. 1.A was entered

and the channel

was

placed in a tripped condition in accordance

with technical

specifications.

The failure was determined to be

a faulty valve

position limit switch that

may have

been

damaged

by this leak.

The switch is designed

to the environmental qualifications of 10 CFR 50.49

and therefore

should

be unaffected

by this type of

environment.

The licensee

intends to monitor the leaks until the

upcoming outage

when the leaks

and the HSIV limit switch will be

repaired.

The failure of the limit switch will be tracked

as IFI

260/92-41-01,

Failure of Environmentally gualified Limit Switch.

Equipment Drain

Sump Inleakage

The Reactor Building Equipment Drain sump is receiving approxi-

mately fifteen gpm inleakage,

eight of which is believed to be due

to hot water leaking past the seat

on the 2-69-577

and 2-69-578,

RWCU return line drain valves.

The inspectors

had previously

observed

steam rising from a drain in the

RHR Hx A room as well as

a four inch drain line that was hot to touch.

Following

investigation,

the licensee

determined

these

were tied to the

reactor building equipment drain

sump

and that the

sump was

actually steaming

back into these lines causing

them to heat.

On

November

12,

1992 the inspector

observed

the

2B Reactor building

equipment drain

sump

pump vibrating and making

a lot of noise.

The

pump was secured

by operations

and

a work order was generated.

The inspector

determined that since October,

1992, this

pump has

been

removed

from service for repair or rebuild three times.

The

licensee

believes

the increased

temperature

in the

sump is

contributing to the high failure rate.

A consultant is being

brought in to investigate

the problem further.

Currently, the

C.

d.

licensee

has

no plans to repair the leaking valves until the

upcoming outage.

Replacement

of Drywell Pressure

Transmitter

An inspector

observed

portions of licensee activities

on November

16,

1992,

associated

with

WO 91-29041-00,

which replaced

the

Drywell Pressure

Transmitter,

2-PT-64-0160B, with a refurbished

transmitter.

The replacement

was part of an on-going project in

response

to

NRC Bulletin 90-01,

Loss of Fill-Oil In Transmitters

Manufactured

By Rosemount.

The bulletin identified transmitters

from certain lots with model

number

1154

and manufactured prior to

July 11,

1989,

as needing replacement.

The old transmitter

was

a

model

1154 manufactured prior to July 1989, but was not from a lot

that was identified as exhibiting failure due to loss of fill-oil.

The licensee

had previously returned their old transmitters

from

stock to the manufacturer for refurbishment,

and

as

system

maintenance

allowed,

are replacing the old transmitters

with these

new ones.

The transmitter replaced

by this

WO had exhibited

no

indications of fill-oilloss.

The inspector

observed

portions of

the actual

replacement

and reviewed the

WO.

The

WO provided

adequate

instructions

and approvals for the intended work.

Post-

maintenance

testing

was specified in accordance

with 2-SI-

4.2.F.21(B),

Drywell Pressure

Wide Range

(Div. II).

The inspector

did not identify any deficiencies during observation of this

activity.

3A DG Corrective Maintenance

On December

15,

1992, the inspector

observed

work associated

with

corrective maintenance

activities

on the 3A DG.

More

specifically,

damaged

teeth

on the bull gear were repaired

using

files and applicable

honing tools in accordance

with work order

92-66478.

The damage

occurred during the performance of

surveillance instruction 3-SI-4.9.A. l.a (3A), "Diesel Generator

3A

Monthly Operability Test,"

when

an

AUO apparently failed to remove

a manual turning tool from the engine prior to it being started.

The licensee

has initiated an incident investigation into the

matter

and the inspectors will review the results of that

investigation.

In conjunction with repairs to the bull gear,

the

licensee

replaced

two engine jacket water heat exchangers

due to

leaking tubes.

Following these repairs,

the engine

was tested

and

returned to service.

No violations or deviations

were identified in the Maintenance

Observation

area.

Operational

Safety Verification (71707)

The

NRC inspectors

followed the overall plant status

and any significant

safety matters related to plant operations.

Daily discussions

were held

with plant management

and various

members of the plant operating staff.

The inspectors

made routine visits to the control rooms.

Inspection

observations

included instrument readings,

setpoints

and recordings,

status of operating

systems,

status

and alignments of emergency

standby

systems,

verification of onsite

and offsite power supplies,

emergency

power sources

available for automatic operation,

the purpose of tempo-

rary tags

on equipment controls

and switches,

annunciator

alarm status,

adherence

to procedures,

adherence

to LCOs, nuclear instruments

opera-

bility, temporary alterations

in effect, daily journals

and logs, stack

monitor recorder traces,

and control

room manning.

This inspection

activity also included

numerous

informal discussions

with operators

and

supervisors.

General

plant tours were conducted.

Portions of the turbine buildings,

each reactor building,

and general

plant areas

were visited.

Observations

included valve position

and system alignment,

snubber

and

hanger conditions,

containment isolation alignments,

instrument

readings,

housekeeping,

power supply and breaker alignments,

radiation

and contaminated

area controls,

tag controls

on equipment,

work

activities in progress,

and radiological protection controls.

Informal

discussions

were held with selected

plant personnel

in their functional

areas

during these tours.

a ~

Unit Status

b.

Unit 2 operated

at power coasting

down in power level

and was

on-line for 77 days at 76 percent

power at the

end of the period.

The licensee

continues to impose administrative limits on

recirculation

pump speed

due to vibration concerns with small

lines

on the recirculation system.

Major pre-outage

modifications

continue with significant scaffold installation in the plant.

Drywell Control Air

The inspector

reviewed TVA's response

to Generic Letter 88-14,

Instrument Air Supply System

Problems Affecting Safety-Related

Equipment

as it pertained to the drywell control air system.

The

response

stated that the system is designed to supply compressed

air with a dew point of 30 degrees

Fahrenheit.

It also states

that the MSIVs and the

MSRVs require supply air with a dew point

of -40 degrees

F,

much less

than the system

can provide.

gDCN

f18984 was written requesting clarification of this requirement

and to determine if the current drywell control air system is

capable of attaining this lower dew point.

The resolution

concluded that the

SRV vendor document

has since deleted

the

requirement to maintain

a specified

dew point for its supply air

and that

a change to the MSIV vendor manual to either delete or

raise the

dew point requirement is being pursued.

It further

stated that the system

can only produce air with a dew point of 35

degrees

F and that this is acceptable.

Testing in accordance

with

TI-34, Monthly Control Air System Dryer Dew point Test

and

Purge

Control, indicates that the 35 degree

F requirement

has not been

maintained.

The inspector

reviewed the tests

performed

on

6

February

21,

1992,

Harch 12,

1992, April 13,

1992,

and April 16,

1992,

and noted that the

2B drywell control air dryer failed to

meet the acceptance

criteria three times

and the

2A dryer once.

Engineering

has determined that the current temperature

switches

require replacement

due to improper deadband

and following

replacement

believe the 35 degree

F dew point can

be achieved.

In

TVA's response

to the

GL, they committed to revising TI-34 to

verify that adequate

margin is maintained

between

the ambient air

temperature

and

dew point range at air dryer outlets.

Contrary to

this, TI-34 was not revised to verify adequate

margin is

maintained for all components

supplied

by the system,

namely the

,

HSIVs.

This is

a deviation from the commitment

made in response

to

GL 88-14.

This item is identified as

DEV 260/92-41-02,

Drywell

Control Air Dew point.

c.

Unit

1 Hain Battery

During

a routine tour of the control

bay on December

7,

1992, the

inspector toured the Unit

1 main battery board room.

The

inspector questioned

the seismic mounting of the battery because

of styrofoam spacers

between

the battery cells.

Other batteries

in the plant use plywood spacers

that are firmer.

Also, several

of the unistrut locking devices

were secured

and not aligned in

the locknut grooves.

These

items were discussed

with SOS

and

system engineer.

A work request

was written to align the locking

devices correctly.

The vendor was contacted.

The vendor sent

a

letter to the licensee stating the styrofoam spacers

were supplied

with the battery

and rack and were acceptable

for seismic

protection.

These actions resolved the questions

regarding

seismic mounting of the Unit

1 battery.

One deviation

was identified in the operational

safety verification

area.

Hodifications

(37700,

37828)

The inspectors

maintained

cognizance of modification activities to

support the restart of Unit 2.

This included reviews of scheduling

and

work control, routine meetings,

and observations

of field activities.

Throughout the observation of modifications being performed in the field

gC inspectors

were observed monitoring and documented verification at

work activities.

The licensee

has developed

a program to assess

contractor compliance

with plant requirements for major maintenance

and modifications work.

In the past, this work had

been performed

by utility personnel.

The

modifications group for Unit 2 developed this program.

Key elements of

this program are task managers

and task manager

rounds.

A task manager

was assigned

to each design

change.

The task manager

remains in contact

with the design

change until the system is returned to service.

During

implementation of the design,

the task manager

makes daily rounds of all

projects

assigned

to them.

A field implementation checklist

was

developed to aid the task managers

and provide consistency.

The

checklist requires

review of proper work authorization

and permits,

work

documents

on site,

housekeeping,

productivity, craftsmanship,

safety

practices,

alarm,

and other items.

This data is compiled

and management

reports generated.

The inspector

reviewed several

reports

and program organization.

This

program provides

an effective means to provide real-time feedback to

management

on plant modifications.

This program is being extended to

Unit 3 recovery activities.

No violations or deviations

were identified in the modification area.

Unit 3 Restart Activities

(30702)

The inspector

reviewed

and observed

the licensee's

activities involved

with the Unit 3 restart.

This included reviews of procedures,

post-job

activities,

and completed field work; observation of pre-job field work,

in-progress field work,

and

gA/gC activities;

attendance

at restart

craft level, progress

meetings,

restart

program meetings,

and management

meetings;

and periodic discussions

with both

TVA and contractor

personnel,

skilled craftsmen,

supervisors,

managers

and executives.

a ~

Unit 3 Engineering

On December

9,

1992, the inspector

met with the Site Engineering

and HodificatIons Manager at the Bechtel

engineering offices in

Athens,

Alabama.

Discussions

were held with the

new Bechtel

project manager,

David Brannen

and

new Bechtel

engineering

manager

Rick Jackson.

The overall status of Unit 3 recovery

and Unit 2

Cycle

6 outage

were discussed.

DCN production

was reviewed.

For

Unit 3 and multi-unit DCN's about half of 500 total

DCNs are

complete.

This was accomplished

in the preceding year or year

and

a half.

A complete review of these

DCN's by the licensee

as part

of the transition to a single organization

was performed.

Consultants

were being

used to promote team building.

Some

88

DCN's were eliminated or determined

not needed.

The screening

criteria used

was that all commitments or commitment related

work

would be performed.

Also, uniformity would be maintained

between

Unit 2 and Unit 3.

The remaining

DCNs were being reviewed to see

if they could be completed

by the end of the Unit 2 Cycle

6 outage

consistent with productivity rates.

The current Bechtel staff had

been

reduced

from 1480 to 800-850 personnel.

All the

DCNs for the

Unit 2 Cycle

6 outage

were complete

except for CREVs

modifications.

A POD meeting is conducted

each

day at noon.

The inspector

attended

the meeting

on December

10,

1992

and December

15,

1992.

The meeting is conducted

by TVA management

with the Bechtel

engineering

manager

in attendance.

Emphasis

was placed

on meeting

the scheduled

DCN production for the week.

The inspector will continue to monitor the

new organization

and

attend

POD meetings.

The initial assessment

is that

TVA managers

have

assumed

the lead responsibility for Unit 3 engineering

recovery with emphasis

on working together with the contractor.

SPOC Walkdown of Cooling Towers

On December

7,

1992, the inspector

accompanied

the licensee

on

portions of the

Phase

I SPOC walkdown of the cooling towers, lift

pump stations,

and associated

4kV switchgear.

The walkdown team,

included persons

from TVA technical

support,

operations,

electrical

maintenance,

and the work control group,

conducted

the

walkdown in accordance

with OSIL number 64,

"System

Pre-Operability Checklist Walkdowns."

The operations

walkdown was

performed to satisfy the requirements

of step VI.3. of Appendix

C

in SSP-12.

In addition, four evaluators

from the Site guality

Audits and Assessments

organization

took part in the walkdown to

evaluate

the performance.and

adequacy of the

SPOC for the cooling

towers.

During the

SPOC,

each cooling tower cell was entered

and

inspected.

Emphasis

was placed

on the cooling tower fans

and

associated

electrical cabling.

The lift pump stations

were

examined for damage/defects

through

a visual walkdown.

The 4kV

switchgear

rooms were walked

down in a similar fashion.

Discrepancies

identified were recorded in Attachment

2 of OSIL

number 64.

Each discrepancy

was assigned

a work request

number

for dispositioning.

After the walkdown, the

SRO determined

in which phase of the

program each matter would have to be completed,

in order to

satisfy the

SPOC.

Items identified during the walkdown included:

Inadequate

sealing of power cables to the cooling tower fans

General

housekeeping

deficiencies

Loose or missing bolts in the fan stacks

Supports missing from cables

and small tubing

Loose ground cabling

Hissing tags

(a few)

A breaker

door that would not latch

Improper oil level for two cooling tower fans

Based

on the inspectors

observations,

the walkdown was adequate

and satisfied

the applicable portion

(Phase

I) of the

SPOC.

JTG Meeting

On December

10,

1992, the inspectors

attended

JTG meeting

92-005

in the plant engineering building.

The first item of discussion

was the approval of the previous

JTG meeting minutes.

The minutes

were approved

as proposed to the group.

Following discussion of

the meeting minutes,

a change to test procedure

3-RTP-027C,

"Condenser Circulating Water Test,"

was presented

to the JTG.

The

change deleted existing procedure

steps for the performance of

cooling tower

5 and

6 pump discharge

flow control valve

and bypass

valve interlock test.

These

items were previously performed

during the post modification test.

Furthermore,

steps

were

added

to the procedure to verify and review the post maintenance

test

records

and to attach

a copy of the records to the procedure.

Two

additional

steps

were

added to the procedure to verify that flow

was established

to the cold water channel

through the cooling

tower bypass

valve.

The safety

assessment

for the change

was also

presented

to the group.

The changes

were approved

and forwarded

to the plant manager for his approval.

During the meeting,

the

JTG chairman discussed

a Notice of

Violation issued

at Watts Bar in NRC Inspection

Report 390,

391/92-30.

The violation stated that contrary to the Watts Bar

JTG charter,

agenda material

was not being distributed prior to

the meeting.

The Browns Ferry JTG chairman stated that

no such

requirement existed at

BFNP,

however it was standard

practice to

distribute

agenda material prior to scheduled

meetings.

He

further stated that if a special

JTG meeting

was required,

ample

review time during the meeting would be provided for each group

member.

Reportable

Occurrences

(92700)

The

LERs listed below were reviewed to determine if the information

provided met

NRC requirements.

The determinations

included the

verification of compliance with TS and regulatory requirements,

and

addressed

the adequacy of the event description,

the corrective actions

taken,

the existence of potential generic problems,

compliance with

reporting requirements,

and the relative safety significance of each

event.

Additional in-plant reviews

and discussions

with plant

personnel,

as appropriate,

were conducted.

(CLOSED)

LER 260/92-006,

Reactor

Scram

on Indicated

High Reactor

Water

Level

Caused

by Signal

Spike During Feedwater

Level Control

System

Troubleshooting

On July 28,

1992, during troubleshooting of the Unit 2

FWLC System,

a

main turbine trip and reactor

scram occurred.

Engineered

safety feature

actuations

including PCIS groups

2, 3, 6,

and

8 occurred

as well as

initiation of Standby

Gas Treatment

and

CREV.

The trip occurred

due to

an unexpected

level spike induced during the replacement

of a relay in

the

FWLC system.

The licensee

determined

the root cause of the event to

be due to an inaccurate

evaluation

and diagnosis of prior feedwater

system trouble symptoms,

and failure to anticipate the

FWLC circuit

response

to the relay replacement.

The licensee

revised Electrical

Generic Troubleshooting

Instruction EII-0-000-TCC106

and I

5.

C Generic

Troubleshooting Instruction SII-O-XX-00-3014, to include

a requirement

10

that activities involving high risk troubleshooting

receive

an

independent

technical

review.

Additionally this event

was reviewed with

technical

support,

maintenance,

and operations

personnel

and included

emphasizing that work involving the breaking of current loops must

be

evaluated for signal spiking during re-establishment

of the loop.

The

inspector determined that adequate

licensee

actions

have occurred to

preclude

a recurrence

of this event.

Action on Previous

Inspection

Findings

(92701,

92702)

a ~

(CLOSED) VIO 259,

260, 296/92-03-01,

Failure to Follow Procedure

for Diesel

Generator Surveillance

and Spent

Fuel

Pool Transfer

Canal Operation.

In the first example during the performance of a SI,

an

inadvertent

DG start occurred.

This was caused

by a communication

problem between

maintenance

and operations

personnel

during

altering of the hold order boundary for the

DG start circuit.

The

corrective actions for this violation were revision of the

equipment clearance

training program to include the circumstances

of this event, training of appropriate

personnel,

and revision of

the SI to include specific instructions

on equipment

alignment.

The inspector reviewed the licensee's

response,

supplemental

response,

and closure

package for this example.

The documentation

provided indicated the corrective actions

were completed

and

addressed

the cause of the violation.

The second

example

was for transferring material

through the spent

fuel transfer canal without utilizing an approved

procedure.

This

violation was caused

by inadequate training.

The corrective

actions taken included review of the event,

counseling of

personnel,

and revision of two other plant procedures

to reference

the procedure for the transfer canal.

The inspector

reviewed the

closure

package for this item and the procedure revision.

The

actions

addressed

the violation.

b.

(CLOSED) VIO 259,260,296/92-11-01,

Failure to Perform Independent

Verification.

The first example occurred during the performance of Surveillance

Instruction 0-SI-4. 11.B.2.a,

Diesel Driven Fire

Pump Operability

Test.

On April 15,

1992,

an

NRC inspector

observed that

independent verification steps

in the body of the instruction wer e

not performed "step

by step"

as required

by SSP-12. 1, Conduct of

Operations.

Six steps

in the SI required

IV following performance

of the step

and prior to continuing with the next step.

The

verification steps

were performed

upon completion of the test.

TVA reevaluated its program for IV and determined that SIs with IV

steps

located in the body of the procedure

cannot

have the

IV

performed

as required

by SSP-12.6,

Verification Program,

"step

by

step", without negatively impacting the performance of the

procedure.

To do this would require constant

stopping,

performing

11

the IV, and then recommencing

the SI.

Therefore,

TVA reviewed all

SIs to re-verify the need for IV and

remove if unnecessary,

and to

relocate

IV steps that are not necessary

to prevent detrimental

equipment operation to the end of the SI.

Two-hundred sixty-five

procedures

were revised

based

on this review.

Following these

revisions the Site guality organization

performed

a review of ten

percent to independently verify their accuracy.

No discrepancies

were identified.

The inspector reviewed the following revised

procedures

and found no discrepancies:

2-SI-4.2.A.22

Rev 5,

Group I PCIS Logic

2-SI-4.4.A.2

Rev 12,

SLC System Functional

Test

2-SI-4.5.B.l.a(I)

Rev 6,

Loop I

RHR Simulated Automatic

Actuation Test

2-SI-4.7.F. 1

Rev 3, Primary Containment

Purge

System Filter

Pressure

Drop Test

O-SI-4.11.B.l.c

Rev 12, High Pressure

Fire Protection

System

Flushes

0-SI-4. 11.8.2.a

Rev 10, Diesel

Driven Fire

Pump Operability

Test

2-SI-4.5.G

Rev 6, Automatic Depressurization

System

Simulated

Auto Actuation Test

2-SI-4.2.B-27

Rev 8, High Pressure

Coolant Injection Sup-

pression

Chamber

High Level Instrumentation Calibration

2-SI-4.2.B-24FT(II)

Rev 1,

Core Spray Sparger to Reactor

Pressure

Vessel Differential Pressure

Functional

Test

2-SI-3.2. 10.F

Rev 5, Verification of Remote Position Indica-

tors for Reactor

Core Isolation Cooling

2-SI-4.7.A.2.g-3/3b2

Rev 4, Primary Containment

Local

Leak

Rate Test Reactor

Feedwater

Line B: Penetration

X-9B

2-SI-4.7.A.2.g-3/32a

Rev 6, Primary Containment

Local Leak

Rate Test Control Air: Penetration

X-48

The second

example occurred

on February

25,

1992 during the

performance of Surveillance Instruction 2-SI-4.2.C-8FT

when

a step

requiring IV was not performed properly.

The individual

performing the IV relied on the observed

actions of another

individual rather than performing

a physical

hands

on check

himself.

This resulted in a pressure

transmitter isolation valve

for turbine first stage

pressure,

remaining closed for six days

following completion of the surveillance.

This individual

received

personnel

corrective action in accordance

with TVA

personnel

policy.

Based

on the above,

the inspector determined that adequate

licensee

actions

have

been taken to preclude recurrence

of this

event.

12

Nuclear Safety

Review Board

(40500)

On November 20,

1992, the inspector

met with the

NSRB Chairman at the

corporate office.

The organizational

structure,

membership,

and

use of

outside advisors

were reviewed.

The

NSRB Chairman functions

as both the

NSRB Chairman. reporting to the

Senior V.P. Nuclear

Power

and

as General

Manager; Materials, Contracts,

and Administrative Support; reporting to the V.P. Nuclear Assurance,

Licensing,

and Fuels.

This organization chart is in the N(AP.

A

proposed

change to the structure will change

the latter position title

to General

Manager Nuclear Support.

The present

NSRB makeup at each site includes the following:

a.

Site Members

1)

Site V.P.

2)

Licensing Manager

3)

guality Assurance

Manager

4)

Engineering

and Hodifications Manager

b.

Members from TVA Corporate

and other sites

1)

NSRB Chairman

2)

Six of 12 other members

each site is different and each of

the members

except for the senior consultant is

a V.P. or

reports directly to a V.P.

c.

Outside Advisors - three of seven outside advisors with expertise

in each plant design.

One advisor is also

an advisor to the

TVA

board

and serves

on all three boards.

On October

1,

1992, the membership

on

NSRB was changed to increase

the

number of TVA senior management

personnel

and reduce the number of

outside advisors

from five to three.

This change

was

made with the

philosophy that

TVA management

has strengthened

with the successful

return to operation of units at two sites permitting the reduction in

use of outside advisors.

The use of advisors to strengthen

the

NSRB was discussed

in TVA's

Corporate

Nuclear Performance

Plan,

Volume I.

The

NRC issued

an

SER as

NUREG-1232,

Volume I, in July 1987.

In 'the

SER,

page

27, it was stated

that the

NRC staff will determine the acceptability of each

NSRB as part

of its plant-specific reviews.

The activities of the

NSRB were reviewed

in IR 90-14.

This included

a review of resumes

of the

NSRB members

and

outside advisors.

The membership

was determined to be acceptable.

The

T.S. requirements

of the

NSRB are in section G.5.2.

The inspector

reviewed the

TS and

a quorum is five members.

Stated

in TS is that the

use of consultants

shall

be utilized to provide expert advise

as

determined

by the

NSRB.

The inspector

concluded that the composition of

the present

NSRB exceeds

the

TS requirements.

In addition, the outside

13

advisors

are

on

NSRBs of other utilities.

This provides

a broad

perspective

of industry activities for TVA plants.

The effectiveness

of the

NSRB was documented

in

NRC IR 92-33

and 91-33.

The inspector

concluded that the recent

changes

made to the

NSRB

reducing the number of outside advisors

was

a logical transition

based

on the demonstrated

effectiveness

of the board.

The

new structure still

exceeds all

TS requirement with senior

TVA personnel

with ample

seniority capable of challenging the plant staff on safety issues.

Exit Interview (30703)

The inspection

scope

and findings were summarized

on December

18,

1992

with those

persons

indicated in paragraph

one above.

The inspectors

described

the areas

inspected

and discussed

in detail the inspection

findings listed below.

The licensee

did not identify as proprietary

any

of the material

provided to or reviewed

by the inspectors

during this

inspection.

Dissenting

comments

were not received

from the licensee.

Item Number

Descri tion and Reference

260/92-41-01

260/92-41-02

IFI, Failure of Environmentally gualified

Limit Switch,

paragraph

three.

DEV, Drywell Control Air Dew point,

paragraph

four.

Licensee

management

was informed that

1

LER and

2 VIOs, were closed.

Acronyms

and Initial i sms

AUO

BFNP

CFR

CRD

CREV

DCN

DEV

DG

F

FCV

FWLC

GL

GPH

IFI

IR

IV

JTG

LCO

LER

HR

HSIV

Auxiliary Unit Operator

Browns Ferry Nuclear Plant

Code of Federal

Regulations

Control

Rod Drive

Control

Room Emergency Ventilation

Design

Change Notice

Deviation

Diesel

Generator

Fahrenheit

Flow Control Valve

Feedwater

Level Control

Generic Letter

Gallons

Per Hinute

Inspector Followup Item

Inspection

Report

Independent Verification

Joint Test

Group

Limiting Condition for Operation

Licensee

Event Report

Haintenance

Request

Hain Steam Isolation Valve

MSRV

NQAP

NRC

NRR

NSRB

OSIL

PCIS

QA

QC

QDCN

RHR

RPS

RWCU

SER

SI

SLC

SPOC

SRO

SRV

SSP

TI

TS

TVA

VIO

WO

WR

Hain Steam Relief Valve

Nuclear Quality Assurance

Plan

Nuclear Regulatory

Commission

Nuclear Reactor Regulation

Nuclear Safety

Review Board

Operations

Section Instruction Letter

Primary Containment Isolation System

Quality Assurance

Quality Control

Quality Design

Change Notice

Residual

Heat

Removal

Reactor Protection

System

Reactor Water Cleanup

System

Safety Evaluation Report

Surveillance Instruction

Standby Liquid Control

System Pre-Operability Checklist

Senior Reactor Operator

Safety Relief Valve

Site Standard

Practice

Technical Instruction

Technical Specification

Tennessee

Valley Authority

Violation

Work Order

Work Request