ML18036A702

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Insp Repts 50-259/92-11,50-260/92-11 & 50-296/92-11 on 920314-0417.Violations Noted.Major Areas Inspected: Surveillance,Maint,Operational Safety Verification,Unit 3 Restart Activities & Fire Protection & Prevention Program
ML18036A702
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 04/29/1992
From: Kellogg P, Patterson C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18036A701 List:
References
50-259-92-11, 50-260-92-11, 50-296-92-11, NUDOCS 9205190128
Download: ML18036A702 (48)


See also: IR 05000259/1992011

Text

y.

(41PS RE@II'a

UNITED STATES

NUCLEAR REGULATORY COMMtSSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

~w*w+

Report Nos.:

50-'259/92-11, 50-260/92-11,

and 50-296/92-11

Licensee:

Tennessee

Valley Authority

3B Lookout Place

1101 Market Street

Chattanooga,

TN 37402-2801

Docket Nos.:

50-259, 50-260, and 50-296

License Nos.:

DPR-33, DPR-52, and DPR-68

Facility Name:

Browns Ferry Units 1, 2, and 3

Inspection at Browns Ferry Site near Decatur, Alabama-.

Inspection Conducted

March

14 - April 17; 1992

t

Inspector: C.. Patt,

or R

ident

spector

e/

Date Signed

Accompanied by:

E. Christnot, Resident Inspector

W. Bearden, Resident Inspector

R. Bernhard, Project Engineer

M. Murphy, Regional Inspector

Approved by:

Paul

Reactor Proje

s, Section 4A

Division of Reactor Projects

SUMMARY

Date Sig ed

~ Scope:

This routine resident inspection included surveillance observation

maintenance

observation, operational safety verification, Unit 1

activities, Unit 3 restart activities, fire protection/prevention pl'ogram,

9205190128

920501

PDR

ADOCK 05000259

8

PDR

Browns Ferry Nuclear Performance

Plan Post-Restart commitments,

reportable occurrences,

action on previous inspection findings, and

management

changes.

One hour of'backshift coverage was routinely worked during the

week.

Deep backshift inspections-w'ere conducted on March 22 and

March 28, 1992.

One violation with two examples was identified for failure to perform

independent verification, paragraphs two and three.

The first example

was identified by the inspector during the performance of a

surveillance test for the diesel driven fire pump, paragraph two.

Steps

in the body of the procedure required independent verification but the,

entire test was performed before in'dependent verification steps were

completed.

This was thought to be the desired method of performing

the test by personnel performing the surveillance.

The second

example was found when the rod sequence

control system was still

enforcing rod movement constraints after power had been increased

above 30 percent power, the normal bypass point, paragraph three.

Surveillance instruction steps to open the first stage pressure

transmitter isolation valve were not adequately performed.

Independent verification that the valve was opened was performed by

visual observation from outside a controlled surface contamination

area.

Two previous violations were identified during the last two

years concerning independent verification. These were 90-14-05

during cable determination and 91-24-02 during fuse installation.

This

indicates problems with how and when to perform independent

verification.

An unresolved item was identified concerning adequacy of

independent verification steps, para'graph two. Two steps in a diesel

driven fire pump surveillance procedure do not.require independent

verification that control switches were returned to "AUTO" following

system restoration.

Initial discussion with the licensee indicate that

credit may have been taken for clearing of annunciator alarms

following completion of the test.

This item will be unresolved until

this practice and applicability to this procedure are reviewed further.

A violation was identified for failure to take corrective action for a

previous violation, paragraph,.three.

The inspector identified that the

wrong chart recorder paper had again been placed in two control room

recorders required by technical specifications.

This problem was the

reason for part of a previous violation 91-24-01.

The problem

C,

'3

was identified after the licensee had presented

a closure package for

the previous violation.

An inspector followup item was identified concerning Unit 3 circuit

breaker refurbishment, paragraph eight.

This concerned the proper

identification of breakers shipped and used as substitutes.

An

inspector walkdown identified tagging inconsistencies

in the plant.

This item is a concern because

a previous breaker substitution in

1990 resulted in a power supply failure to automatically transfer.

REPORT DETAILS

Persons Contacted

Licensee Employees:

'. Zeringue, Vice President, Browns Ferry Operations

"H. McCluskey, Vice President, Browns Ferry Restart

"J. Scalice, Plant Manager

J. Rupert, Engineering and Modifications Manager

"J. Swindell, Restart Manager

"M. Herrell, Operations Manager

J. Maddox, Project Engineer

"M. Bajestani, Technical Support Manager

R. Jones,

Operations Superintendent

A. Sorrell, Special Programs Manager

"C. Crane, Maintenance Manager

G. Turner, Site Quality Assurance Manager

"R. Baron, Site Licensing Manager

"J. McCarthy, Unit 3 Licensing

"P. Salas, Compliance Supervisor

J. Corey, Site Radiological Control Manager-

A. Brittain, Site Security Manager

Other licensee employees or contractors contacted included licensed reactor

operators, auxiliary operators, craftsmen, technicians, and

public safety

officers; and quality assurance,

design, and engineering personnel.

'RC

Personnel:

1

P. Kellogg, Section Chief

"C. Patterson,

Senior Resident Inspector

E. Christnot, Resident Inspector

"W. Bearden, Resident Inspector

R. Bernhard, Project Engineer

M. Murphy, Regional Inspector

"Attended exit interview

Acronyms and initialisms used throughout this report are listed in the last

paragraph;

Surveillance Observation (61726)

The inspectors observed and/or reviewed the performance of required Sls.

r.

0

The inspections included reviews of the Sls for technical adequacy and

conformance to TS, verification of test instrument calibration, observations

of the conduct of testing, confirmation of proper removal from service and

return to service of systems,

and reviews of test data.

The inspectors also

verified that LCOs were met, testing was accomplished by qualified

personnel, and the Sls were completed within the required frequency.

The

following Sls were reviewed during this reporting period:

The inspector observed the performance of.O-SI-4.11.B.2.a,

Diesel Driven

Fire Pump Operability, Test.

Following completion of the Sl, the inspector

reviewed the completed

Sl and noted the IV steps had not been, signed for

IV. Six steps in the Sl require IV following performance of.the step and prior

to continuing with the next step.

As an example, step 7.2.6.3 closes drain

valves from the fuel tank and requires IV. Another step requires the engine

air cleaner be disassembled,

inspected,

and reassembled

with IV before the

diesel is operated.

When the operator was questioned,

he stated that

another operator would be dispatched to perform the IV. He further stated

that the IV were once performed immediately following completion of the

step but that this philosophy had changed and that now the. Sl is performed

in it's entirety before the IV is performed.

This represents

a fundamental

misunderstanding of IV when required in the body. of a procedure.

This is a

violation of SSP-12.1,

Conduct of Operations, step 3.14.2.B, which requires

that procedures which are not routine, frequently performed (once per shift),

and easily accomplished,

be performed "step-by-step".

Additionally, TS

.6.8.1

requires that procedures

be followed during surveillance and test

activities of safety related equipment.

This is the first example of violation,

259,260,296/ 92-11-01, Failure To Perform Independent Verification. This

event is similar to events associated

with previous violations concerning the

performance of IV and procedural compliance which are documented

as NRC

violations 260/90-14-05,

and 260/91-24-02.

Additionally, the inspector reviewed 3-SI-4.9.A.1.a(3c), 3C DG Monthly

Operability Tests.

In the body of this procedure are IV steps performed

befo're the DG is started.

The 20 cylinder tests valves are opened and IV

perform'ed.

Next, the engine is manually rolled and fluid drainage checked.

The test cylinder valves are closed and IV'performed before running the DG

It was also n'oted that steps 7.3.8.9 and 7.3.12.5 did not require IV. These

steps place the Diesel Driven Fire Pump Strainer Backwash Control Switch

and Pump Controller Selector Switch, respectively, in the normal standby

lineup following it's use during performance of the Sl.

These actions align

the system for automatic'operation

in the event it is needed.

SSP-12.6,

Independent Verification, step 3.1

~ 2, states that IV is required for all valves,

breakers, and other components

in safety-related

or fire protection systems

I

3

where an inappropriate positioning could adversely affect system operation

'r

the ability to supply extinguishing media to the fire. These issues were

discussed with the Fire Protection Manager and Operations Superintendent

immediately after the Sl was performed on April 15, 1992.

Initial

discussions with the licensee indicated that credit may be taken for clearing

of annunciator alarms as the IV steps.

This approach and the acceptability

of the circuits involved will be unresolved until further review. This will

tracked as URI 259,260,296/92-11-02,

Missing Independent Verification

Steps.

One violation was identified in the Surveillance Observation area.

3. 'aintenance

Observation (62703)

Plant maintenance activities were observed and/or reviewed for selected

safety-related systems and components to ascertain that they were

conducted in accordance with requirements.

The following items were

considered during these reviews:

LCOs maintained, use of approved

procedures, functional testing and/or calibrations were performed prior to

returning components or systems to service, QC records maintained,

activities accomplished

by qualified personnel, use of properly certified parts

and materials, proper use of clearance procedures,

and implementation of

radiological controls as required.

Work documentation

(MR, WR, and WO) were reviewed to determine the

status of outstanding jobs and to assure that priority'was assigned to safety-

related equipment maintenance

which might affect plant safety.

The

inspectors observed the following maintenance

activities during this

reporting period:

a

e

Failure to Open a Valve and Perform Independent Verification

0

.

WO 92-49879-00,

was written during power ascension

on March 2,

1992, to correct a problem with the RSCS.

The RSCS restraint was

still active at greater than 30% power which restricted control rod

movement to group notch mode, thereby slowing power'ascension.

During work activities associated

with this work order, instrument

maintenance

personnel identified that the isolation valve for pressure

transmitter, 2-PT-85-61B, was closed.

This transmitter senses

turbine

first stage pressure which is an indicator of reactor power.

With this

valve closed the pressure transmitter was effectively out of service,

resulting in the RSCS restraint not being bypassed at 30% power

even though actual power was greater than 30%.

The inspector

reviewed II.Report, II-B-92-018, which documented the licensee's

investigation into the circumstances

associated

with this event.

In

that report the licensee attributed the event to a failure to adequately

perform IVfollowing a routine surveillance performed on February 25,

1992.

The valve was closed in step 7.11.5 of 2-SI-4.2.C-SFT,

Instrumentation that Initiates Rod Blocks/Rod Sequence

Control

.

System Restraint Functional Test.

The valve was left closed following

that portion of the testing.

Valve position restoration and verification

was provided for in steps 7.13, 7.14, and 7.23.

These steps were

initialled as being performed.

The inspector noted that in this. case the

individual that signed for IV had relied on the observed actions of an

individual located within the contamination zone that was actually

performing, the task, i.e., the individual did not enter the contamination

area and physically verify the actual valve position rather that

individual remained outside and observed the effort to operate the

valve.

Furthermore the individual responsible for perfor'ming the IV

had been an actual member of the crew performing the work rather

than a qualified individual not involved in the work activity. These

actions are in violation of SSP-12.6,

Independent Verification, steps

2.2 and 3.1.8.A.

This event should have been prevented by the

corrective actions associated

with previously identified problems with

performance of IV by licensee personnel

~ These separate

events are

documented

in NRC violations 260/90-14-05

and 260/91-24-02.

This is the second example of VIO 259,260,296/92-11-01,

Failure to

Perform Independent Verification.

Use of Incorrect Chart Paper

During observation of maintenance

activities associated

with control

room recorder, 2-RR-90-272CD, the inspector noted that the recorder

had the incorrect chart paper installed.

Usage of incorrect chart paper

in this recorder had been previously identified by the inspector as part

of violation 260/91-24-01

and had been due to use of an unverified

and incorrect operator aid.

The incor'rect chart paper contains a range

of MR/HR rather than R/HR as required.

Use of the incorrectly scaled

. paper could result in a non-conservative interpretation of containment

radiation levels during an accident. This previous violation is discussed

in greater detail in paragraph

10 of this report.

The'Division II

recorder, 2-RR-90-273CD, also contained the same incorrect paper.

These multipen recorders provide the high range containment radiation

level indication required by TS Table 3.2.l- and NUREG 0737.

The

inspector informed the onshift SOS of this condition and the chart

paper in both recorders was immediately replaced with the correct

chart paper.

During a subsequent

meeting with licensee management

the. inspector was informed that the use of the incorrect chart paper

~

7

~

had occurred due to storage by operations of the older incorrect chart

paper in the same locker location as the newer correct paper.

The

'controlled chart paper cross reference developed for the Unit 2 control

room was not used to verify the chart paper taken from the-locker

prior to use.

Although this item would normally be considered

a non-cited violation,

it does not meet the criteria since it is an example of failure by the

licensee to carry out corrective action for a previously identified

discrepancy. This constitutes VIO 260/92-11-03, Ineffective

Corrective Action on Control Room Radiation Monitors.

C.

Rosemount Transmitter Replacements

The inspector reviewed several ongoing work activities associated

with replacement of existing Rosemount Model 1153 transmitters

with refurbished transmitters.

This replacement effort was performed

to resolve problems identified by NRC Bulletin 90-01.

The inspector

, observed that adequate

controls were in place to insure that the work

activity did not interfere with operability of an'other safety rela'ted

system or component..

The work instructions contained sufficient

details to allow for satisfactory performance of the intended work

activity. Additionally the inspector noted that each work instruction

contained

a precaution that stated that each of the transmitters

should be replaced one at a time to prevent possible unplanned

ESF

actuation during the work. Specific work activities reviewed included

the following:

WO 91-27777-00 was issued to replace Drywell High Pressure

Transmitter, -2-PT-64-58B.

The inspector noted that LCO 2-92-96-

3.2.B was entered at 9:05 am on April 6, 1992, and that the LCO

was exited at 4:04 pm on the same date after performance of post

maintenance testing.-

WO 91-27778-00 was issued to replace Drywell High Pressure

Transmitter, 2-PT-64-58C.

The inspector reviewed the work package

and determined that it appears adequate for the planned work activity.

However, this work activity was delayed due to other work.

WO 91-29043-00 was issued to replace Drywell High Pressure

Transmitter, 2-PT-64-67.

The inspector noted that LCO 2-92-97-

3.2.F was entered at 1:15.am on April 7, 1992, and that the LCO

was exited at 6:20 am on the same date after performance of post

maintenance testing.

d.

HFA Relay Replacement

WO 92-51112-00 was issued to troubleshoot/repair

a problem with

Main Steam Line "C" Relief Valve Handswitch, 2-HS-1-30A; light

indication.

The problem'was found to be with relay 2-RLY-1-2E-K33

which was replaced.

The inspector observed portions of the ongoing

work activity including various controls in place during the ongoing

work. The inspector noted that ECI-O-OOO-RLY004, Replacement of

HFA Relay Components-and/or

Calibration of HFA Relays, was

referenced for use by the WO for specific instructions for removal and

replacement of the relay.

EMI-106, Troubleshooting and

Configuration Control of Electrical Equipment, was also used to

'-control wirelifts and reterminations.of all lifted leads.

No problems

were identified during the inspectors review of this work activity.

Two violations were identified in the Maintenance Observation area.

4.

Operational Safety Verification (71707)

The NRC inspectors'followed the overall plant status and any significant

-safety matters related to plant operations.

Daily discussions were held with

plant management

and various members of the plant operating staff.

The

inspectors'made

routine visits to the control rooms.

Inspection observations

included instrument readings; setpoints and recordings, status of, operating

systems, status and alignments of emergency standby systems, verification

of onsite and offsite power supplies, emergency power sources available for

automatic op'eration, the purpose of temporary tags on equipment controls

and switches; annun'ciator alarm status, adherence to'procedures,

adherence

to LCOs, nuclear instruments operability, temporary alterations in effect,

daily journals and logs,'stack monitor recorder traces, and control room

manning.

This inspection activity also included numerous informal

discussions with operators and supervisors.

General plant tours were conducted.

Portions of the turbine buildings, each

reactor building, and general plaht areas were visited.

Observations included

valve position and system alignment, snubber and hanger conditions,

containment isolation alignments, instrument readings, housekeeping,

power

supply and breaker alignments, radiation and contaminated

area controls, tag

controls on equipment, work activities in progress,

and radiological

protection controls.

Informal discussions

were held with selected plant

personnel in their functional areas during these tours.

0

a.

Plant Status

During this period the unit operated continuously at power. without

any significant'problems.

At the end of the report period the unit had

been on. line 47 days.

b.

Plant Tours

During a routine tour of the plant on April 7, 1992, the inspector

observed the following:

1.)

A local open indication light for RHR injection valve

2-HS-74-67B was not illuminated. This was discussed

with the

SOS and the valve indicated open in the control room.

A plant

operator was dispatched to check the light bulb.

2.)

A hold order tag 2-92-0333-2 had been placed on 480 volt

reactor building ventilation board 2B, Refueling Floor Supply Fan

2A, compartment 2B, on the inside of the cabinet with the-

cabinet door left open.

This was'discussed

with the SOS.

Normally, hold order tags are placed on the outside and the

cabinet doors closed for protection of an inadvertent water

intrusion into the breaker cabinet.

=

3.)

A health physics technician on the refuel floor had a red dot on

his plant access

badge.

About a year ago all red dots were

removed from the badges.

The red dot was to permit

emergency access into the TSC and control room without

logging entries into these areas.

The technician thought the red

dot was for vital area access

and was not clear of the purpose

of the red, dot.

He stated his badge had not been updated for

several years and no expiration date was visible on the badge.

This was discussed

with the Site Security Manager.

The

technician was a TVA employee and their plant badges have an

indefinite expiration period.

Security flagged the technician's

badge for update.

Plans to change all the site access

badges to

a new system within the next several months was discussed

by

Site Security.

E

4.)

Minor housekeeping

items were identified.

Dirt and dust was in

the 2A and 2C CS pump corner room.

A ladder, hose, spray

can of cleaner, poly bags, and a roll of tape under the torus..

8

Painting of valves in the overhead near the RCIC instrument,

rack resulted in paint dripping down on the instruments.

5.) 'he 'A'uel pool. cooling system was noted to be noisy. The

sound appeared to be caused by cavitation.

This was

discussed with the SOS.

6.)

On 480 volt RMOV BD 3A and 480 volt SD BD 3B several

circuit breakers had been removed for maintenance.

The circuit

breaker cabinet compartments

were labeled but the labeling

- was inconsistent.

On some, the label was a printed form and

on others a handwritten form.

Some breakers were. apparently

tagged as removed and taken to the shop but were installed.

Two breakers had been interchanged.

Although these were

labeled, the inspector questioned-if the controls were

acceptable.

A previous problem with breaker substitution was

identified in II-B-90-124. Two electrical boards failed to

automatically transfer because of incompatible breaker

substitution.

'.)

During tours of the Unit 3 plant area, many components were

tagged with six to eight hold order tags.

The inspector

questioned if a simpler system tag out might be acceptable

instead of trying to control numerous, hold orders for the same

item.

All of these items were discussed

with plant management

in a weekly

exit on April 9, 1992.

Unit 3 management

did not attend the weekly .

exit.

c.

Main Transformer Failure

The inspectors followed the licensee's activities associated

with the

March 5, 1992, event in which the Unit 1 Main Transformer "B"

Phase high side shorted to ground.

An explosion resulted which

severely damaged the transformer.

This transformer is normally used

through backfeed

as, a source of offsite electrical power for the unit

during an outage.

This failure was originally discussed

in IR 92-05.

~

To date licensee activities, in this area have been limited to

preparations for replacement of the damaged transformer.

A spare

transform'er located on site will be moved into place and will replace

the damaged transformer.

The inspector noted that licensee con'trois

of the activities in the switchyard have been very good.

An SRO has

been assigned to directly control all related ongoing work. Access

9

into the area was strictly controlled.

Personnel were briefed on recent-

industry switchyard events prior to performing any work. The

replacement transformer is not scheduled to be in, place until late in

May 1992.

The 1A and 1C Main Transformers,

.1A and 1B Unit

Station Service Transformers,

and Unit 1 Isophase

Bus were inspected

and electrically checked for damage.

No dama'ge was identified.

The inspector reviewed the final event report for Incident-

Investigation, II-B-92-019, which documented the licensee's

investigation associated

with this failure. The licensee report states

that the transformer failed due to'an electrical fault resulting in a

sudden high pressure transient (instantaneous

thermal expansion)

from the rapid heating of the transformer insulating oil. This resulted

in overpressurization of the transformer tank, destruction of two

bushings, and the activation of the sudden pressure relay.

Although

the investigation is complete the actual cause of the fault has not

been determined.

According to this report the cause of the failure is

to be determined by ASEA-Brown Boyeri after the failed transformer is

removed.

Although the report states that the immediate response to

the event by licensee personnel was good, several potentially adverse

findings were "identified. These findings include the following:

In addition to the Sudden Pressure

Relays which operates to

deenergize the transformer, the transformers are also equipped with a

Gas Operated Relay.

This relay is designed to alert operations of

overheating or a developing fault. This relay provides an annunciator

and can close a second set of contacts which would deenergize the

transformer if gas continued to accumulate.

This protective option

had been defeated through use of a selector switch on the relay.

This

function if used shares the same protective circuity that is used by the

sudden pressure relay.

The licensee's Technical Support Section was

assigned to determine why this function was disabled and whether to

operate in this manner.

At 11:54 a.'m. on the day before the event, the "Transformer Gas

Press High or Low" annunciation was received in the Unit 1 Control

Room.

This single annunciator can originate from either the Gas

Operated Relay or a separate transformer relief device. Additionally it

can alarm based on conditions in several different transformers,

making it difficultto determine the source of the alarm. At 8:30 p.m.

on that date maintenance

personnel verified that the alarm was

originating in the 1B Main Transformer, but did not verify the validity.

by use of test equipment.

Had this determination been made and the

alarm found to be valid, the control room would have been alerted

0,

.10

that the transformer was already in the process of failing. The report

was critical of troubleshooting performed by licensee personnel in this

area.

Potential problems identified included delays in troubleshooting

which resulted from inadequate

planning, delays in determining alarm

validity, and limited results from the troubleshooting that was

performed.

The licensee committed to revise existing procedures to

increase the priority on work orders of this nature and to evaluate the

need to develop a standard text for annunciation validation.

A deficiency was noted in the operations training program in that

confusion existed over the source of the alarm.

Operations has

committed to train personnel on the event and conduct refresher

training on transformer" protective devicesalarm responses,

and an

overview of diagnostic tools available in this area.

The Alarm

Response

Procedure for this alarm was inadequate.

Operations

'committed to revise the ARP.,

The existing annunciator design associated

with the transformer,

switchyard and cooling towers is susceptible to grounds resulting in a

system that experiences

numerous false alarms.

Troubleshooting.

problems with this system is complicated by presence, of numerous

parallel contacts in the alarm circuity. This has res'ulted in a lack of

credibility and reduced sensitivity to those annunciators.

The transformer relief semaphores

are not painted a uniform color and

the 1B 'semaphore

was difficultto see, since it blended in with the

transformer paint.

The licensee committed to paint all semaphores

a

high visibilityyellow.

The inspector noted that the licerisee's final event report appeared to be

thorough and provided a good self assessment

of various conditions which

could have possibly contributed to the transformer failure. The inspectors

will continue to follow the licensee's

r'epairs to the 1B Main Transformer and

corrective actions associated

with the various findings identified in the

report.

Unit 1 Activities

j

The inspector reviewed and observed the licensee's activities involved with

the Unit 1 reactor-vessel.

This included reviews of procedures and records;

observations of field work, QA/QC, operations and contractor personnel

activities; and discussions with licensee and contractor

supervisors,

engineers,

and skilled craft personnel.

The reactor vessel disassembly

continued with the removal of shield plugs, drywell head, drywell ventilation

package, reactor vessel head, steam dryer, and steam separator.

The

contractor personnel detected

an unexpected amourit of rust on the drywell

flange face and water with sludge in the inner bellows.

All items were taken

care of and the work activities proceeded.

The inspector concluded from

these reviews and observations that all activities were adequately controlled.

6.

Unit 3 Restart Activities (30702)

The inspector reviewed and observed the licensee's activities involved with

the Unit 3 restart.

This included reviews of procedures, post-job activities,

and completed field work; observation of pre-job field work, in-progress field

work, and QA/QC activities; attendance

at restart craft level, progress

meetings, restart program meetings, and management

meetings; and

periodic discussions with both TVA and contractor personnel, skilled

craftsmen, supervisors, managers

and executives.

a.

Pilot/Prototypical Program

The inspector observed and reviewed the activities involved with the

Unit 3 Pilot/Prototypical program.

The specific areas reviewed

involved, the condenser upgrade, the first DCN issued to the field

DCN W17045, Unit 1 panel 3-9-2), the first CRDR design change; the

drawing, enhancement

program, and the integrated DCN, which was

tentatively identified an electrical cable DCN.

The inspector observed the ongoing activities involved with the

condenser upgrade and reviewed the drawing enhancement

program.

The licensee determined that prior to Unit 3 restart, deficiencies with

the accuracy arid legibility of the Unit 3 As-Constructed and

Configuration Control Drawings had to be corrected.

Drawing

restoration, drawing update, drawing enhancement,

and drawing

utilization are to be performed as coordinated effort. The program

was started by the licensee on January 6, 1992, and had an expected

duration of 18 months.

The program was staffed with a proper mix

of technically qualified individuals to ensure

a quality product.

The licensee performed a review during the Unit 3 Discovery Phase to

determine the scope of the Drawing Enhancement

Program.

This

review examined the requirements necessary to satisfy Unit 3 drawing

concerns as well as satisfy drawing enhancement

needs.

An

examination of the Unit 2 Drawing Enhancement

Program was

performed to determine the scope for Unit 2. The initial Unit 2 effort

identified 1600 drawings to be enhanced.

The 400 drawing

difference betwe'en Unit 2 and Unit 3 was due to the need for

common as well as a number of Unit 1 and Unit 3 drawings being-

required for support of Unit 2 operation.

The following represents the total drawing quantities associated

with

Unit 3, and the scope to be considered on the Unit 3 Drawing

Enhancement

Program:

o

750 Primary and Critical Drawings

o

450 High Use Secondary Drawings

, o

1200 Total Drawings to be Enhanced

In the program'the licensee plans to reproduce drawings in the CADD

format with the most up-to-date information obtainable from the

Document Control/Change Management System.

The drawings will

be updated and put in a Shadow file, so that as needs rise the

drawing. will be available.

The, shadow file for each of the 1200

drawings will be continually updated as the various inputs become

available from=walkdowns, completed designs,

PDDs, and scrubs.

The shadow file at any one time will provide the best latest

information on the drawings.

When all programs and the affected

system are in the SPOC/SPAE process, the drawing will be officially

issued for use by plant operations, maintenance,

technical support,

and design.

The inspector reviewed a technical assessment,

No. EE-0040, dated

March 23, 1992, performed by TVA Unit 3, Design Control involved

with drawing improvement.

The inspector noted that four

prototypical drawings were reviewed (3-47E3847-1, 3-47E610-32-1,

3-45E-614-9, and 45N620-7), and all outstanding change paper was

adequately identified.

The inspector observed the activities of the Bechtel drawing

improvement group and noted no deficiencies.

The use of the

shadow file and the issuance of the CCD when the various systems

are returned to service will continually prove the acceptability of the

Drawing Enhancement

Program.

Design Activities

The inspector reviewed the design activities associated

with the

pilot/prototypical program involving the return to service of cooling

13

towers 1, 5, and 6.

A total of four DCNs were reviewed.

DCN

W17581A, affected flow element FE-27-147 and flow monitor

FM-27-147, which were not wired per vendor recommendation; flow

indicator, FI-27-147, on 'panel 25-258'located

in the radwaste

building, range indication changed, from 20,000 - 200,000 GPM to 0-

200,000 GPM; and flow switch FS-47-147 set point changed from

50,000 GPM decreasing to 60,000 GPM decreasing.

This

modification, impacting TS 3/4.8.A would insure proper radwaste

dilution during both the closed loop and helper mode of operation for

the cooling towers.

The additional DCNs reviewed were DCN W17703A, which impacted

the emergency bearing lube water supply pumps no. 1, 2, and 12

flow control valves 0-FCV-25-49A-1 through 6 and 0-FCV-25-49B-1;

DCN W17748A, which impacted pipe support under the 79-02/14

program for the Unit 3 vacuum breakers on the discharge conduits to

the hot water channel; and DCN W-17771A, which impacted control

panel 0-9-56, Cooling Tower Control Panel and affected five areas.

The areas affected by DCN W-1771A were:

disable towers 2, 3, and

4 input to common alarms to prevent masking inputs from tower 1, 5,

'nd 6; disable automatic mode from swanson control, on panel

0-9-56, to prevent inadvertent equipment operation; disable cooling

tower fan control capability for cooling towers 1, 5, and 6 from the

swanson controls, this leaving only manual forward operation of

cooling tower 1, 5 and fans at the local stations and the 480 volt unit

substation motor control centers;.disable

the pump bearing lube water

valve lights on panel 0-9-56; and disable the cooling tower 4160 volt

switchgear A, B, C, D and bus tie breaker control functions and

indications from panel 0-9-56.

Construction Activities

The licensee completed the first modification of the CRDR program on

Unit 3 panel 3-9-10.

Additional construction activities involved the

condenser upgrade project, initial drywell steel work plan writing,

cooling tower refurbishment, drywell blowers, offsite fabrication

facility, and initial drywell chiller modification schedule reviews.

Maintenance Activities

The inspector reviewed the licensee's circuit breaker overhaul

program.

This processes

were setup using the Unit 2 program plus

lessons learned.

The 4KV and 480 volt breaker rebuild project initially

shipped 28 breakers off site to GE for rebuild.

One return shipment

14

was received and an. additional shipment was sent off. The inspector

expressed

a concern about properly identifying the status of the

, breakers as they are shipped and what type breakers were being used

as substitutes,

see paragraph 4.b.

This item is identified as an

inspector followup item IFI 259, 260, 296/92-11-04,

Proper Tracking

of Circuit Breakers During Refurbishment

The licensee started

a walkdown of both 4 KV. and 480 volt electrical

switchgear.

This walkdown was conducted to ensure the tagging of

the breakers was consistent, verify.the breaker name plate data,

ensure that they are consistent with Unit 2, and proper use of PDDs

~

to correct any breaker, switchgear and drawing miss-matches.

The

inspector accompanied

licensee representatives

in the field and

observed work activities.

Pre-Operational/Return

to Service Activities

The licensee indicated the operability of Unit 3 systems

is dependent

on the controls established

over construction type testing, pre-

operational type testing, and system line-up statusing.

These controls

will ensure that the systems are capable of performing their design

.

functions.

This will be accomplished by the Unit 3 SPOC/SPAE

process.

A change from the Unit 2 SPOC/SPAE had been made and is

documented

in site procedure SSP 12.55, Unit 3 System

Pre-'perability

Checklist.

Cooling towers 1, 5, and 6 were scheduled to be returned-to-service

and a prototypical plan be implemented to validate its adequacy.

Return-of the cooling towers will allow Unit 2 to go into the helper or

closed mode of operation during periods of elevated river

temperatures.

Systems impacted by cooling -tower return-to-work were:

0

27

o

27C

o

25

0,

77

o

205

0

232

o

246

o

24

Condenser Cooling Water

Cooling Towers 1,5, and 6

Raw Service Water

Rad waste

4KV Cooling Tower Electrical Switch

Gear'80V

Cooling Tower Electrical Boards

Cooling Tower Transformers

Raw Cooling Water System, (Auxiliary RCW

Pumps)'he

inspector noted that the SPOC of cooling towers would not be

15

typical of the SPOC process.

Typically, all supporting systems

received their SPOC before the main system.

This cannot be done for

the cooling towers.

Consequently, the cooling towers along with

portions of the, supporting systems will be included in this SPOC.

Because this is not a typical SPOC, technical support developed

detailed boundary drawings to assist in identifying SPOC scope.

The SPOC process provides the licensee with a systematic method for

evaluation items and issues which potentially affect the ability of

systems to perform as designed, determining their status, and

. ensuring completion of those items which impact system return-to-

service for restart.

The SPOC, process differs from that used for Unit

2 in that it will be accomplished

in two phases.

Phase

I SPOC

addressed

the system testing milestone and established system status

control by operations.

Completion of the Phase

I SPOC process

constitutes

a technical support recommendation that the system is

ready for pre-operational testing and that the affects of system testing

upon the operating unit have been considered and addressed.

Phase

II

SPOC completion constitutes

a technical support recommendation for

system operability in support of Unit 3 restart.

System operability will

be declared by operations at the appropriate point after necessary

surveillance instructions have been performed, pre-operational

deficiencies have been adequately addressed,

and all support systems

are available.

The inspectors will continue to observe and review the return-to-

service process for the cooling tower.

Additional Activities

The inspector observed and monitored the Unit 3 integrated

scheduling meetings.

These meetings consisted of a weekly meeting-

at the Athens, Alabama, Bechtel office and a planned weekly meeting

at the onsite SWEC constructors facility. The Bechtel meeting

discussed, progress, problems, and a look ahead for the work of

producing design documents.

The SWEC meeting was planned to

discuss progress, problems, and looked ahead for the work of

implementing the design changes specified by the design documents.

The. Athens meeting was attended by supervisors, project managers,

and executives.

The inspector concluded that, except for the circuit breaker rebuild area, the

licensees Unit 3 restart activities observed and reviewed appeared to be in

accordance

with approved procedures,

group coordination appeared to be

-16

effective, and technical issues appeared to be in the process of resolution.

Fire Protection/Prevention

Program (64704)

The purpose of this inspection is to evaluate the overall adequacy of the

.

licensee's fire protection/prevention program and to determine that the

'icensee

was implementing the program in conformance with regulatory

requirements, technical specifications, and industry guides and standards.

P

a.

Program Review

The inspector reviewed the unit technical specifications, and the

- administrative procedures which constitute the approved fire

protection program.

The procedures reviewed were:

SSP,-12.15,

"Fire Protection," Revision 1, dated March 2, 1992

FPP-1, "Fire Protection Plant," Revision 6, dated March 2,, 1992

FPP-2, "Fire Protection-Attachments,"

Revision 7, dated March

2, 1992

FPP-3, "Fire Emergency Response

Organization and Pre-Fire

Plans," Revision 3, dated March 2, 1992.

This review verified that the licensee had technically adequate

procedures to implement the fire protection program.

Procedural

guidance was provided to control combustible material and reduce fire

hazards.

Administrative procedures also provided for maintenance

and surv'eillance of fire barriers, fire barrier penetrations, fire

suppression,

fire detection, and other support equipment.

Personnel

training, qualifications, and responsibilities were provided.

Maintenance evolutions that significantly increase fire risk were

properly controlled.

b.

Implementation

A tour of accessible

areas of the plant was conducted by the

inspector, accompanied

by licensee representatives,

to assess

general

area conditions, work activities in progress, and the'visual conditions

of fire protection systems and equipment.

Combustible materials and

flammable and combustible liquid and gas usage were restricted or

'properly controlled in areas containing safety-related equipmerit and

components.

Items checked included the position of selected

suppression

system valves; fire, barrier conditions, hose stations, and

fire extinguisher'for type, location, accessibility, and condition.

There was some light construction in process in the toured areas.

There were no welding, cutting, or use of open flame ignition sources

found in the areas toured.

Some maintenance work and surveillance

testing was noted.

Accessibility'to suppression system controls, hose

stations, and fire extinguisher was being maintained.

General

housekeeping

conditions were found to be very good.

The inspector reviewed the following completed surveillance

inspections:

O-SI-4.11.B.2.a,

"Diesel Driven Fire Pump Operability Test,"

Revision 9, April 13, 1991, performed March 18, 1992

O-SI-4.11.G.2.b, "Daily Fire Door Inspection,'" Revision 4,

May 16, 1991, performed March 19, 1992

O-SI-4.11.B.1.a, "Electric Fire Pump Op'erability Test,"

Revision 5, January 17, 1992, performed March 18, 1992

O-SI-4.11.B.3.a, "Weekly Check for Diesel Fire Pump Batteries

1 and 2," Revision 6, November 25, 1991, performed March

18, 1992

O.-SI-4.11.B.1.e,

"High Pressure

Fire Protection System Valve

Cycling," Revision 4, April 9, 1991, performed December 9,

1991

O-SI-4.11.B.4, "Raw Service Water Logic System Functional,"

Revision 1, April 8, 1991, performed September

13, 1991

O-SI-4.11.E.1.b, "Inspection and Reracking of Fire Hose

Stations," Revision 2, June 8, 1990, performed October 22,

1991

O-SI-4.11.B.1.g, "High Pressure

Fire Protection System'Flow

Test," Revision 1, June 6, 1989, performed June 7, 1989

O-SI-4.11.B.1.e,

"High Pressure

Fire Protection System Valve

Cycling," Revision 4, April 9, 1991, performed December 9,

1991

2-SI-4.11.A.1, "Semiannual Smoke Detector Functional Test,"

Revision 8, October 30, 1991, performed November 11, 1991

18

O-SI-4.11.G.1.a(1),

"Visual Inspection of Fire Wraps," Revision

0, January 7, 1991, performed January 14, 1991

O-SI-4.11.G.1.a,

"Visual Inspection of Fire'Rated Barriers,"

Revision 3, November 30, 1990, performed January 3, 1991

O-SI-4.11.G.2, "Semi-Annual Fire Door Inspection," Revision 6,

May 24, '1991, performed October 28, 1991

Fire protection systems and equipment installed for protection of

'afety-related areas were found to be functional and tested in

accordance with requirements specified in the TS.

The inspector reviewed fire brigade training and drill records.

The

records were in order and "confirmed that training and drills were being

conducted at the specified intervals.

Fire brigade equipment, including

emergency breathing'apparatus,

was found to be stored and

maintained properly.

.The licensee's fire watch training and administrative controls were

reviewed by the inspector.

The training was found to be

comprehensive

and conducted in accordance

with the licensee's

approved schedule.

Administrative controls for fire watch

assignment,

and tracking were found to be acceptable.

The licensee's

revised definition of "Roving" and "Continuous" fire watch duties.has

effectively clarified technical specification requirements and clearly;

established that the term "Continuous" does allow movement, but

within a well defined area.

There were no problems identified in this

area.

The inspector reviewed the licensee's last quality assurance

audit,

BFA91104 of April 25, 1991, in the fire protection area and

characterized

as the annual and biennial audit.

The scope of this audit

included an inspection of plant areas, evaluation of fire brigade and

operations personnel performance during an unannounced fire drill,

review of fire brigade training and a programmatic review of program

procedures.

Discrepancies identified were formally presented to the

affected organizations.

Responses

were tracked to close out, and

actions taken were reviewed for adequacy.

e,

19

BFNPP Post-Restart

Commitment Status

The inspector reviewed'the post restart status of the BFNPP open items for

. Unit 2.

Prior to restart, the status of BFNPP items was summarized

in a

letter from TVA to the NRC dated April 16, 1991, "Browns Ferry Nuclear

Plant - Completion Status of Corrective Actions identified for Unit 2,restart

in Browns Ferry Nuclear performance Plan." This letter indicated some

BFNPP items would not be completed prior to restart and an implementation

schedule for those items would be provided 120 days after restart.

A letter

dated September 20, 1991, and a supplemental letter dated December 24,

1991, provided the implementation schedule and a status for these items.

At the time of this inspection there were 30 open items remaining open as

- post restart commitments.

Fifteen are currently scheduled to be completed

prior to restarting from the Unit 2 Cycle 6 outage.

In addition, six are on

hold pending NRC issuance of SERs on these topics.

Another item is

- complete and the package

is being reviewed for closure, two have schedule

dates in 1992, five have 1993 dates, and one item is scheduled for

completion prior to restart for the Unit 2 Cycle 7 outage.

For those items scheduled for completion in 1992 or in the Unit 2 Cycle 6

outage, the inspector verified planning was in place for their implementation.

Where activities are committed for completion by outage end, but are not

constrained by operational concerns, much of the work is scheduled for

completion prior to the outage.

The PRA scheduled for a September

1,

1992 completion, has work ongoing.

The level

1 portion of the PRA will be

complete, but the containment analysis has the bulk of its work yet to be

performed and the inspector could not verify it would meet'its scheduled

commitment. dat'e.

Four of the items awaiting SERs are issues concerning USI A-46. The SER

is in final draft and is expected to be issued soon.

However, implementation

of the SER may not be complete for three or four years, as permitted by the

SER.

Therefore those issues dealing with long term seismic qualifications

will probably stay open for- several years.

The inspector found that all the items sampled had ongoing management

attention and were included as part of the normal planning/scheduling

process.

0

~

20

Reportable Occurrences

(92700)

The LERs listed below were reviewed to determine if the

information'rovided

met NRC requirements.

The determinations included the

verification of compliance with. TS and regulatory requirements,

and

addressed

the adequacy of the event description, the corrective actions

taken, the existence of potential generic problems, compliance with

reporting requirements,

and the relative safety significance of each

event.'dditional

in-plant reviews and discussions with plant personnel,

as

appropriate, were conducted.

a.

(CLOSED) LER 260/91-10, Technical Specification Violation When 24

Hour Limiting Condition for Operation Expired Without Declaring

Affected Systems

Inoperable.

0

0

This LER reported to the NRC an event that occurred on May 14,

1991, where licensee personnel failed to declare systems inoperable

that were affected by a reactor vessel water level transmitter.

This

failure occurred when RPV water level transmitter, 2-LT-3-58D, could

not be calibrated during performance of a routine surveillance, 2-Sl-

4.2.B-1(D) and the incorrect LCO entry time was recorded by

operations personnel in the Unit 2 LCO Log.

The licensee investigated the circumstances

associated 'with this

failure which are documented

in final event report, II-B-91-111. The

inspector reviewed the licensee's investigation and determined that

the failure occurred due to miscommunication between personnel in

the licensee's operations and maintenance

groups.

The instrument

ha'd been originally valved'out of service at 2:38 pm on May 14,

1991. At 5:20 pm on the same day instrumentation personnel

determined that repairs were required before calibration could be

'erformed.

Operations was inform'ed of the problem at 6:20 pm and

'he

LCO was entered at 6:28 pm. At 3:50 pm the following day the

Unit 2 RHR, CS and DG.were declared inoperable.

Due to the

discrepancy that existed between the times that the instrument was

actually taken out of service, the actions required by TS 4.2.B to be

performed within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> were not taken.

The level transmitter'as

replaced and the calibration completed later that day.

The affected.

unit was in cold shutdown for the entire period of the event.

The

licensee attributed the failure to miscommunication caused by an

inadequate

procedure that did not require notification-to operations'of

the specific time that the required equipment is removed from service.

21

The inspector reviewed documentation provided by the licensee to

verify that the affected procedure was revised to include a

requirement to inform licensee personnel of the specific time that

required equipment is removed from service.

Additionally the licensee

reviewed 208 other Sis for which the electrical and instrumentation

sections have responsibility to determine the need for a similar

requirement.

The inspector also verified by review of training

attendance

records that the event was reviewed with site

maintenance

personnel.

The inspector determined that based on the

above completed corrective actions that recurrence of this problem

should not occur.

(CLOSED) LER 260/91-15,

High Pressure

Coolant Injection System

Did Not Fulfill Its Safety Function Resulting From Low Suction

Pressure

Condition During a Fast Start-up.

During HPCI System performance testing on July 31, 1991,

conducted as part of the Unit 2 power ascension

program the HPCI

turbine tripped from a low suction pressure transient.

Although the

HPCI trip signal automatically reset after 10 seconds

and the HPCI

syste'm successfully was restarted, the licensee declared the system

inoperable and determined the event to be reportable. under 10 CFR 50.73 as a coridition that could have prevented the HPCI System from

. fulfillingits intended safety function. The system failed to meet the

FSAR requirement to attain rated flow within 30 secon'ds.

The licensee determined that the event was due to a problem not

anticipated in design.

Based on information provided by the vendor,

TVA learned that the system was susceptible to momentary suction

pressure transients capable of tripping the HPCI turbine, and that

installation of'a time delay in the low pressure trip circuitry was one

possible option to correct the problem.

As immediate corrective

actions the licensee declared the system inoperable and installed a

temporary time delay relay in the low pressure trip circuitry. This

temporary relay was tracked under a TACF and the HPCI system

performance test was satisfactorily completed on August 1, 1991

~

Th'e inspector, reviewed documentation provided by the licensee to

verify that a permanent

5 second time delay relay was installed in the

Unit 2 HPCI circuitry under DCN W17015A.

Additionally, the

inspector noted that TACF 2-91-3-73, which was used to track the

temporary relay, was removed and closed.

The licensee has

committed to install similar relays in Units

1 and 3 prior to restart of

those units.

No similar events

of, this nature have occurred since the

22

licensee made this modification to the system.

(CLOSED) LER 260/91-19, Automatic Reactor Scram Following a

Turbine Trip Which was a Result of an Unexpected

Fuse Failure.

An unplanned automatic reactor scram occurred at 11:20 pm on

December 8, 1991, on Unit 2 from 80% power in conjunction with a

turbine trip and'unexpected

loss of one of the offsite power supplies.

This trip occurred when a Gould-Shawmut fuse failed. This fuse was

associated

with the 500KV Bus

1 Section

1 potential transformer

output and re'suited in a loss of restraint potential to the generator

backup impedance relay causing the relay to actuate.. Actuation of

this relay caused the Unit 2 main generator breaker and associated

supply breakers to trip. The relay also initiated an exciter field breaker

trip and subsequent

turbine trip. The various electrical boards

automatically transferred to their alternate power supplies and all

safety systems functioned as expected during the event.

The licensee

replaced the failed fuse and all existing 500KV Bus Potential

Transformer secondary fuses to minimize the possibility of spurious

relay operations due to any potential generic fuse failures.

As the

result of this event, TVA committed to evaluate the existing design at

Browns Ferry to determine if reconfiguring that design to eliminate the

possibility that a loss of the relaying potential from a single bus should

be accomplished.

Additionally, the licensee committed to further

investigate the spurious tripping of the Trinity 1 line during the event

and correcting any deficiencies.

The inspector reviewed documentation provided by the licensee to

verify that adequate corrective actions were carried out.

The licensee

decided to add a second generator backup relay for each unit that

senses

potential from the bus PTs opposite to those supplying the

existing relay for each respective unit, 'and logic requiring two-out-of-

'wo logic for operation of the respective relays.

This modification

was accomplished for Unit 2 under DCN W17480 during a recent

outage.

This modification is to be accomplished under DCN W17479

(Unit 1) and DCN W17481 (Unit 3) prior to restart of those units.

The

inspector noted that the licensee determined during the subsequent

investigation that the relaying logic associated

with the Trinity 1 line

operated properly and no further corrective actions were needed.

Based on the above review the inspector determined that the licensee

had taken adequate

corrective actions to preclude recurrence'of

a

'imilar

event.

0

e

~

~

~

23.

d.

(CLOSED) LER 296/92-01,

Engineered Safety Feature Actuation

Caused by a Failed Relay Coil.

An unplanned

ESF actuation occurred at 7:20 am on January 25,

1992, on the Unit 3 PCIS when a relay coil, GE type CR-120, failed.

This relay was associated

with the primary containment atmosphere

control valve logic charm'el A and resulted in an isolation of,the Unit 3

reactor building and refueling floor ventilation systems,

and actuation

of the B and C SBGT trains and B CREV train.

The licensee replaced

the failed relay coil and reset the associated

ESF actuation within

seven hours.

The licensee determined during a subsequent

evaluation that the relay

'oil

failure was a random failure due to end of life caused by thermal

aging of the rel'ay coil. This and other relay coils are now approaching

an average life of 15 years. Industry data indicates that the expected

service life of these type relays in the normally energized applications

is approximately 15-20 years. Based on this and other recent events

associated

with relay coil failures the licensee has planned the

following corrective actions:

The licensee has evaluated the affected relays for Unit 2 and

determined that 12 relays have a high potential for resulting in a

plant shutdown.

Replacement of these relays is planned for the

spring of 1992.

GE CR-120 relay coils used in the normally energized safety

related application are to be replaced in Unit 2 prio'r to startup

from the Cycle 6 refueling outage.,

GE CR-120 relay coils used in the normally energized safety

related application are to be replaced in Units

1 and 3 prior to

restart of each respective unit.

The inspector determined that the licensee has taken or'lanned

adequate corrective actions to justify closure of this

LER.'0.

Action on Previous Inspection Findings (92701, 92702)

a.

(CLOSED) IFI 259, 260, 296/90-03-01,

Review of Facility Operating

Licenses,

DPR-33 and DRP-52, for Appendix R versusSection X

requirements.

1,

24

During a review of NOV 88-20-01, example d, it was noted the BFNP

Unit 2 Facility Operating License, DPR-52, stated in section 2.c.(5),

"The facility may be modified as described in Section X of "Plan for

Evaluation, Repair, and Return to Service of Browns Ferry

1 and 2

(March 22, 1975 Fire)" dated April 13, 1975, and revisions thereto."

This review indicated that Section X of this plan may be in variance

with 10 CFR 50, Appendix R requirements thus requiring a licensee

review of Facility Operating Licenses, DPR-33 and DPR-52 for

Appendix R versusSection X requirements.

On April 4, 1988, per GL 86-10, the licensee submitted the Browns

Ferry Fire Protection Report to, the NRC for review and approval and

on April 14, 1989, submitted a license amendment application to add

License Condition 2.C.5(a) and administrative controls necessary to

implement the Units

1 and 2 Appendix R Safe Shutdown Program.

NUREG-1232, "Safety Evaluation Report on Tennessee

Valley

Authority: Browns Ferry Nuclear Performance Plant" (SER),

Volume 3, Supp. 2, was issued on January 23, 1991.

Section 3.1,

Fire Protection, stated that on the basis of previous staff SERs and

inspections, the NRC staff concluded that BFN Unit 2 complies with

Appendix R to 10 CFR part 50, and further stated that the staff must.

still approve before restart the license amendment application of April

14, 1989 (as discussed

in the previous paragraph).

This request was

subsequently

approved by the NRC on March 6, 1991

~

Subsequent to a NRC request for additional information regarding the.

Browns Ferry Fire Protection Report, the licensee found that much of

the information found in this report was out of date.

The report was-

subsequently withdrawn by the licensee on September

19, 1991 and

was updated and reissued for NRC review on January 15, 1992.

A

licensee amendment application to meet GL 86-10 requirements was

forthcoming from the licensee at the end of this inspection period.

Based on the above information this item is considered closed.

(OPEN) VIO 260/91-24-01,

Failure to Correct Containment Radiation

Monitor Problems.

During the Unit 2 restart on May 24, 1991, NRC personnel identified

several problems with control room instrumentation used to monitor

primary containment radiation levels.

The staff determined that these

problems constituted

a violation for failure to promptly identify and

correct'conditions a'dverse to quality. These problems were first

identified by NRC personnel rather than licensee control room

personnel,

in spite of the fact that the condition was readily apparent

on.the associated

recorder and control room personnel had just

responded to the recorder based on an control room annunciator.

The

problems involved drawihg/wiring errors, recorder range labeling

.

problems, and use of incorrect chart paper in control. room recorders

required by TS.

A previous field design change had been issued to

correct at least a portion of the problem but the FDCN had been

canceled without the knowledge of the system engineer.

The inspector reviewed the licensee's

response to the violation dated

September

5, 1991.

In that response the licensee attributed the

incorrectly canceled

FDCN to failure to follow the existing project

instruction covering design change control. Additionally the licensee

"

attributed the use of incorrect chart paper to personnel error when an

uncontrolled chart paper list was not revised to reflect the vendor

serial number of purchased chart paper.

Nuclear Enginee

recorders in the

main control roo

recorders were

I

paper. However

activities in the

incorrect paper

that work activi

inspector determ

been adequate t

pending further

11.

Management Changes

The inspector was informed that personnel involved were counseled

on the event and that licensee had committed, to revise existing

procedures to strengthen controls for drawing deviations.

The

.

inspector noted that SSP-2.11,

Drawing Deviation Program, was

revised to place overall focal point for dispositioning drawing

discrepancies

and Project Instruction, PI-89-06, Design Change

Control, was revised;to. require that the originator be informed

whenever a FDCN is disapproved.

The inspector reviewed completed

S-DCNs No. S17319A and,S1731.9B

which were issued to allow

ring to develop a controlled chart paper list for all

Unit 2 control room.

During subsequent tours of the

m, the inspector observed that the control room

abeled correctly and contained the correct chart

, on April 8, 1992, during observation of maintenance

Unit 2 main control room, the inspector observed the

was again in use in both recorders.

Observ'ation of

ty is discussed

in more detail in paragraph 3.b.

The

ined that the licensee's. corrective actions had not

o preclude recurrence.

This item is will remain open

"

review of licensee corrective actions in this area.

0

Two.management

changes became effective April 1, 1992.

Chris Crane

was named as the Browns Ferry Maintenance Manager.

Mr. Crane was

previously the Maintenance Program Manager.

26

Allen Sorrel was named as the Browns Ferry Program Manager.

Mr. Sorrel

was previously the Maintenance Manager.

He will assist the Plant Manager

and will take a leading role in the Unit 2 Cycle 6 refueling outage.

12.

Exit Interview (30703)

The inspection scope and findings were summarized on April 20, 1992, with

those persons indicated in paragraph

1 above.

The inspectors described the

areas inspected and discussed

in detail the inspection findings listed below.

The licensee did not identify as proprietary any of the material provided to or

reviewed by the inspectors during this inspection.

The Plant Manager stated that he did not see

a violation concerning the

diesel driven fire pump Sl because the Sl was performed and IV performed

with separation of distance and time.

The inspector stated to have uniformity of Sl performance and to ensure IV

steps are perforJned when expected the procedures should be performed

step by step unless specifically stated otherwise.

Item Number

Descri tion and Reference

259,260,296/92-1 1-01

Violation, Failure To Perform Independent

Verification, paragraph two and three.

259,260,296/92-1 1-02

Unresolved Item, Missing Independent

Verification Steps, paragraph two.

260/92-1 1-03

Violation, Ineffective Corrective Action On

Control Room Radiation Monitors, paragraph

three;

259, 260, 296/92-11-04

Inspector Followup Item, Proper Tracking

Circuit Breakers During Refurbishment,

paragraph six.

Licensee management

was informed that 4 LERs and

1 IFI were closed.

13.

Acronyms and Initialisms

0

AUOBD

BFNP

Auxiliary Unit Operators Board

Browns Ferry Nuclear Power Plant

'

0

27

BFNPP

CAD

CCD

CFR

CRDR

CREVS

DCN

EMI

ESF

FCV

FDCN

FPP

FSAR

GE

GL

GPM

HPCI

IFI

II

KV

LCO

LER

MR

NRC

NRR

PCIS

PDD

PRA

PT

PT

QA

QC

RCIC

RCW

RHR

.

RMOV

RPV

RSCS

SBGT (SGTS)

SD

SER

Sl

SOS

SPAE

Browns Ferry Nuclear Performance

Plan

Computer Aided Drafting

Co'nfiguration Control Drawing

.

Code of Federal Regulations

Control Room Design Review

Control Room Emergency Ventilation System

Design Change Notice

Electrical Maintenance Instruction

Engineered Safety Feature

Flow Control Valve

Field Design Change Notice

Fire Protection Procedure

Final Safety Analysis Report

. General Electric

Generic Letter

Gallons Per Minute

High Pressure

Coolant Injection

Inspector Followup Item

Incident Investigation

Kilovolt

Limiting Condition for 'Operation

Licensee Event Report

Maintenance Request

Nuclear Regulatory=Commission

Nuclear Reactor Regulatio'n

Primary Containment Isolation System

Potential Drawing Disc'repancy

Probabilistic Risk Assessment

Pressure Transmitter

Potential Transformer

Quality Assurance

Quality Control

Reactor Core Isolation Cooling

Raw Cooling Water

Residual Heat Removal

Reactor Motor Operated Valve

Reactor Pressure

Vessel

Rod Sequence

Control System

Standby Gas Treatment System

Shutdown

Safety Evaluation Report

Surveillance Instruction

Shift Operations Supervisor

"System Plant Acceptance Evaluation

t y ('s

1

'c

'e

0

28

SPOC

SSP

SWEC

TACF

TS

TSC

TVA

USI

VIO

WO

WP

WR

System Pre-Operation Checklist

Site Standard Practice

Stone

&. Webster Engineering Corporation

Temporary Alteration Change Form.

Technical Specifications

Tech Support Center

Tennessee

Valley Authority

Unresolved Safety Issue

Violation

Work Order

-Work Plan

, Work Request

0

0