ML18036A398
| ML18036A398 | |
| Person / Time | |
|---|---|
| Site: | Browns Ferry |
| Issue date: | 09/11/1991 |
| From: | Kellogg P, Patterson C NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML18036A396 | List: |
| References | |
| 50-259-91-26, 50-260-91-26, 50-296-91-26, NUDOCS 9110080218 | |
| Download: ML18036A398 (34) | |
See also: IR 05000259/1991026
Text
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UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETTASTREET, N.W.
ATLANTA,GEORGIA 30323
Report Nos.:
50-259/91-26,
50-260!91-26,
and 50-296/91-26
Licensee:
Valley Authority
6N 38A Lookout Place
.'101 Market Street
Chattanooga,
TN
37402-2801
Docket Nos.:
50-259,
50-260.
and 50-296
Licerse Nos.:
and
Facil',ty Name:
Browr,s I=erry Ur,its I,
"., and
3
Inspectior. at Browns ;erry Site near D~-atu..
Alaoa;,a
Irspec-.ion
Conducted:
July
16 - August 16,
1991
Inspector:
C.
. Patter
. Senio
es'.Oent
'nspector
D
e Signea
E. Christno.,
Resident
'Il spe"tor
Bearaen.
REsident Inspector
K. ivey, Resident
Inspector
. Humohrey.
Residen.
Inspector
Approved by:
Pa'
pect
I
o rams,
IVA Project
vis)on
Oa
e Siqnea
SUMMARY
Scope:
This routine resident
inspection
inc.'uded
sustainea
cnntrcI
room ODservatiors,
power ascension
test
program, test
program review, operational
safety verifica-
tion, procurement,
reportable
occurrences,
and actions
on Drevious
inspec
iori
f',ndirgs.
Resu'.
s:
The licensee
successfully
completed
the
power ascerision test
program for Unit
2
on
August
6
199',
and
re.urned
tne
un'.t
tn
normal full power opera'ion,
9110080218
910911
ADQCK 05000259
8
paragraph
two.
Completion
of this
program without
an
and
continuous operation of the Unit for 34 days
was
a significant strength.
Two
violations
occurred
this
period.
Both
violations
involved
Unit
3
activities
and control of contractor personnel.
One violation identified by
a
NRC inspector
was for removing fire wrap from
equipment without posting
paragraph
5.
was
removed
from Residual
Heat
Removal
Service
Water
pump
power
cables
in ihe
intake structure.
The work was performed to support Unit 3 walkdowns
although
it
was
determined
that
the
inspections
had
previously
been
performed
on
Unit 2.
Contractor
personnel
preparing
the
walkdown inspections
did not
use
Unit 2/Unit
3 separation
drawings
to plan the work.
The licensee
stopped all
Unit 3 walkdowns until correcti ve actions
could be implemented.
At the
end of
this report period the corrective action plan was not complete
and Unit 3 work
had not resumed.
The
second violation was for two fuel
movement errors
performed during
a two
week period during Unit 3 fuel
sipping
and inspections,
paragraph
5.
After
corrective
actions
including
independenz,
verification were
implemented
for
the first error,
a
second
error occurred.
Although overseen
by
a licensed
operator,
contrac
or
personnel
on the bridge
crane
performed
the actual
fuel
movements.
One
non-cited
violati'on
was identified for failure to dis.ribute
an urgent
intent change
to
a surveillance instruction in the control
room,
paragraph
2.
The control
room operator
identified this error.
The licensee
took prompt
corrective action to remedy this document control distribution problem.
REPORT
DETAILS
1.
Persons
Contacted
Licensee
Employees:
"0. Zeringue.
Vice President,
Browns Ferry Operations
"H. McCluskey, Vice President,
Browns Ferry Restart
L. Myers, Plant
Manage
- J. Swindell, Restart
Manager
"M. Herrell, Operations
Manager
4
J.
Rupert, Project Engineer
M. Bajestani,
Technical
Support
Manager
R. Jones,
Operations
Superintendent
A. Sorrell, Maintenance
Manager
G. Turner, Site Quality Assurance
Manager
- P. Carier, Site Licensing Manager
"J. McCarthy, Unit 3 Licensing
"P. Salas,
Compliance Supervisor
- J. Corey, Site Radiological
Control Manager
Other
licensee
employees
or contractors
contacted
included
licensed
reactor
operators,
auxiliary
operators,
craftsmen,
technicians,
and
public safety officers,
and quality assurance,
design,
and
engineering
personnel.
NRC Personnel:
P. Kellogg, Section Chief
C. Patterson,
Senior Resident
Inspector
- E. Christnot,
Resident
Inspector
M. Bearden,
Resident
Inspector
"K. Ivey, Resident
Inspector
G.
Humphrey,
Resident
Inspector
R. Bernhard,
Project Engineer
"Attended exit interview
and initialisms
used
throughout this report are listed in the
last paragraph.
2.
Sustained
Control
Room and Plant Observation
(71715)
Tne
inspectors
reviewed
and
observed
the
licensee's
activities
in the
control
room
on
a continuing
basis.
The
observation/reviews
included
control
room conduct, shift turnover
and relief, shift logs
and records,
event
response,
surveillance
testing.
and
maintenance
activities.
The
inspectors
attended
licensee
operational
and
management
meetings,
performed
plant
walkdowns,
and
discussed
observations
and
reviews with
licensee
personnel.
Specific observations
and reviews are noted below.
e
a.
Plant Status
The unit was at
50:; power during
the start of this report period.
The major items that occurred this period were
as follows:
July
17
Released
from final
NRC
hold point.
Authorized
to
exceed
55zo power at 1:00 p.m.
July 28
August
2
Fire wrap found removed at intake structure
Reactor
was
shutdown
as
part of
a
planned
reactor
trip.
Prior
to
this
the
unit
operated
for
34
consecutive
days
August
6
The
power
ascension
test
program
was
completed.
Continuous control
room observation
by
NRC ended.
Successful
completion
of
the
power
ascension
was
noted
as
a
significant str'gth.
The .foresight
of senior
TVA management
to
supplement
the
plant staff with
experienced
GE test
engineers,
improve
secondary
plant material
condition,
and
implement
lessons
learned
from other utility test
programs
was noteworthy.
Technical
support
strengths
were test
organization
and test
briefings.
The
expertise
of
the
plant
operating
crews
was
noted
by
many
NRC
personnel
during
sustained
control
room operations.
The
accurate
scheduling
and
lack of significant problems
during the test
program
were strengths.
b.
Document Control
On July
13, during the control
room briefing for the conduct of the
2-SI-4. 1.A-11(II), NSIV Closure -
RPS Trip Functional
Test
(Channel
Bl/B2), the
UO noticed that the control
room copy
he was going to use
during the
conduct of the
SI did not
have
the latest
UIC entered.
UIC-07 had.been
approved
on July
3
and
should
have
been
entered
in
this "Controlled" copy of the SIs by July
5 in accordance
with SDSP
2. 12,
Paragraph
3.6.6.
The control
room copy of the SI was corrected
at
that
time
and
the
was correctly
performed.
An inspector
researched
the cause
of this error
and determined
the following:
( 1)
The preparer
of the
change
delivered
UIC-07 to the
TIC in the
POB at about 5:30 a.m.
on July 3.
(2)
The .POB TIC clerk carried
out most of the actions specified in
Appendix H, "Holiday, Meekend,
or Third Shift Distribution," of
instruction
DCRYi-1-306. 1.
However,
the
POB TIC clerk did not
'ile UIC-07 in the control
room binder as specified in step
8 of
Appendix
H.
Since it was
near the
end of the shift, the clerk
gave the copy of the UIC-07 to
a day shift
POB TIC clerk to
be
entered
in the control
room binders.
The day shift
POB TIC
0
0
clerks either forgot or misplaced
the control
room copy of the
UIC and did not enter it in the control
room binder.
(3)
Subsequent
standard
distribution
procedures
also
assumed
that
the action
in step
8 of Appendix
H had
been
carried out,
so
UIC-07 was never entered
in the control
room binder.
The licensee
instituted
a revised
receipt
log to
be
used
to insure
that UICs get entered
in the control
room copies
as
soon
as they are
processed'in
the TIC.
The
inspector
concluded
that
a violation of
10 CFR 50 Appendix
B
Criterion VI, Oocument
Control,
had
occurred.
This requires
that
measures
shall
be established
that documents,
including changes,
are
distributed
to
and
used
at
the
location
where
the
prescribed
activityi s performed.
This item was identified and corrected
by the
licensee.
The violation is
not
being cited
because
the criteria
specified
in Section
V.G of the
Enforcement
Policy were satisfied.
This is identified
as
NCV 260/91-26-01,
Failure
to
Update
Control
Room Procedure.
3.
Power Ascension
Test
Program
(72300,
72302,
72508,
72509,
72514,
72516)
The
inspectors
witnessed
in-progress
testing
described
in the
Master
Startup
Operations/Testing
Instruction,
2-SOI-100-1.
These
tests
were
designed
to demonstrate
that control
systems
and equipment
would perform
as designed.
The major testing activities
reviewed during the reporting
period include, but were not limited to the following:
a
~
2-TI-130, Main Steam
Pressure
Control
The inspectors
observed
the performance
of Section
7.3 of this TI on
July 28,
1991.
This phase
of the test
was conducted
at high power to
demonstrate
smooth
pressure
control
and stability of the
steam
loop
during step
changes
of the pressure
setpoint
and to demonstrate
the
takeover capability of the backup pressure
regulator
upon fai lure of
the controlling pressure
regulator.
The power level during the test
was approximately
91% full power, which provided
a margin to the
fixed scram setpoint of approximately
22%.
The testing
extended
over
two operating shifts,
and
thorough briefings of Operations
and test
personnel
by the test director were observed
by the inspectors.
The
test
results
met
the
acceptance
criteria,
and
no adjustments
were
required to the pressure
regulators
or other process controllers.
No
deficiencies
in the conduct of the testing
were identified.
TI-131, Feedwater
Level Control
System Testing
The inspector
observed
and
reviewed
the results
of Phase
3 of this
TI.
The purpose of the test
was to verify and adjust
as
necessary,
the stability of the
control
system.
This consisted
of
placing the feedwater control
system in single
element
and in three
element
control
method.
The
showed instability in that
the desired
level
and the actual
level
would diverge.
This in turn
caused
instability and resulted
in several
on the system.
The operators
and the test personnel
were eventually able to get the
desired
and actual
level to converge
thereby creating
stabi::ity in
the
system.
The final physical
testing
was
completed
on July
28,
1991
with the
reactor
at
approximately
100'o
power.
One
TD was
identified
involving
information
going
to
the
computer.
The
inspector
concluded
from the observations
and
review that the test
was
conducted
in
accordance
with
an
approved
test
procedure,
activities
were
performed
in
a
step
by step controlled
manner,
and
the test personnel
performed
the required
adjustment
as
needed.
No
deficiencies
were identified.
2-TI-132, Recirculation
Flow Control
The inspectors
observed
the performance
of Section 7.5 of'his TI on
July 29,
1991, ior the conditions
of high
power with all reactor
pumps operating.
This phase of the test
was to demonstrate
proper performance of the reactor recirculation flow control
system
following the insertion of
a large
and rapid neoative
ramp
on the
Master Yianual
Flow Controller to ensure
that recirculation
pump
speed
reduction
and reactor
recirculation
flow reduction
would respond
as
anticipated.
This
was
accomplished
by the
operator
reducing
the
controller setpoint
to approximately
55;o in one
continuous
manual
step,
which
corresponded
to
a
recirculation
HG
set
speed
of
approximately
65:o'.
The plant
power level at the beginning of the
test
was
approximately
93;o',
and
decreased
to
approximately
78;o
following the flow reduction.
Thorough briefing of Operations
and
test
personnel
by the test director were observed
by the inspectors.
The test results
met the
acceptance
criteria,
and
no adjustments
to
plant
process
controllers
were
required.
No deficiencies
in the
conduct of the testing
were identified.
2-TI-149 Reactor Mater Level Yieasurements
This test collected
data
to verify that reactor
vessel
wax,er level
inszrumentation
was operating correctly between
0 and
960 psig.
The
test
included collection of temperature
data
on the reference
leg
condensing
chambers
and
on the reference
leg three
inches
below the
condensing
chamber.
The test results
contained
two TDs.
( 1)
Two of the temperatures
measured
from the top of one condensing
chamber
were
below the specified
350 to
425 degree
F range
of
the procedure.
(2)
One
of the
temperatures
measured
on
the
reference
leg three
inches
below the condensing
chamber
was
more
than
20 degrees
F
above
drywell
temperature,
.he permissible
range
specified
in
the
procedure
(reference
leg
was
226
degrees
F,
drywell
approximately
135 degrees
F).
The
licensee
attributed
the
TDs to
the fact that
the
hand-held
pyrometer failed during the test
due to the high ambient temperature
conditions
that
existed
during
the test.
Since
the reactor
water
level
system
has
performed
satisfactorily
(good
level
agreement
between all instruments)
during the
PATP, the licensee
continued with
the
PATP.
The inspectors
concluded
that the
TDs did not adversely
affect continuation with the
PATP,
based
on the
system
response
and
routine observations
of the systems'erformance.
No deficiencies
were identified
2-TI-188,
RCIC Injection
The inspectors
observed
the performance
of Section 7.3 of this TI on
July 30,
1991.
The testing
was
performed at approximately
91~ full
power.
The
purpose
of the test
was to perform
a cold start of the
system
and
in,iect water
from the
CST to the
reactor
vessel
following the injection of a simulated
low water level signal to the
ECCS logic.
The
system
flow controller
response
and stability was
evaluated
to determine if tuning of the controllers
was required.
Thorough briefing of Operations
and
test
personnel
by
the
tes
director
was
observed.
The
system
responded
as
anticipated
with
minor
adjustment
of
the
flow controller
required.
No
testino
deficiencies
were observed
by the inspectors.
2-TI-189,
HPCI Injection
The inspectors
observed
the performance
of Section
7.3 of 2-TI-189 on
July 31.
1991.
The testing
was performed at approximately
75:o power.
The control
rods
were adjusted
to
an approximately
75<< rod line in
order to avoid potential instability problems in case
a recirculaxion
system
runback
occurred.
The purpose
of the test
was to perform
a
cold quick start of the
HPCI system
by simulating
a
low water level
(-45") signal
and demonstrating
that injection of 5000
gpm flow to
the
vessel
was
achieved within
30
seconds.
Final
tuning of
control
systems
was also to be performed if required.
Following initiation of HPCI for the test,
a momentary
low suc;ion
pressure
condition
resulted
in
a trip of the turbine;
the
auto-restarted
when the low suction pressure
condition cleared.
The
test
was
aborted
several
minutes later in accordance
with the test
abort
requirements
when it was
determined
that
the
Level
I test
criteria of less
than
30 second starting time was not achieved.
was tripped
and declared
and
a four hour
ENS report was
made.
During the
pump start transient,
the
upper
head gasket
on the
gland
seal
steam
condenser
ruptured
and
requi red
replacement
following shutdown.
The
licensee
reviewed
the results
of the test
and
developed
and
installed
a
temporary
alteration
consisting
of
a
time delay of
approximately
5
seconds
in the
suction
pressure
trip circuitry to
prevent
starting conditions.
The test
procedure
was
revised
to incorporate
additional
requirements
from
2-SI-4.5.E.1.d
such that
a rerun of the test
would also satisfy
TS
requirements
for demonstrating operability.
A repetition
of the test
was
performed
successfully
on August
1,
1991.
Minor adjustments
were required
during the test
on the
gain
and drift settings
on the control
board
flow controller.
The torus
temperature
exceeded
95 degrees
F, which required entry into EOI-2.
The maximum temperature
reached
was
98 degrees
F,
and
was moni-ored
closely by the
ASOS in command of the evolution
and the
SOS.
During
the test
run
a leak developed
on the lower head gasket for the gland
seal
steam
condenser.
It was
noted
by the inspectors
that
the
low
suction pressure
setpoint
was not reached
during this test run.
The
inspectors
attended
both test briefings
and
observed
that the
briefings
were thorough
and that anticipated
problems
were discussed
and compensatory
actions
planned.
The
command
and control
function
by the control
room operators
of the test
evolution
and
the
requirements
was excellent.
No testing deficiencies
other than thos
discussed
above
were observed
by the inspectors.
2-TI-191,
Pump Trip
The inspectors
observed
the performance
of this TI on July 29,
1991,
following the completion of 2-TI-132.
The
reac or power level
was
increased
to
approximately 94.5;.'ull
power
for the test.
The
purpose
of the test
was to acquaint
Operations
personnel
with the
integrated
plant
response
to
a trip of one reactor
pump.
The
response
of the reactor recirculation
system
was
monitored
to
demonstrate
the capability to prevent
a
low water level
scram in the
event water level decreased
to
a point where the automatic rec'.rcula-
tion
runback circuit
was
activated
to
decrease
reactor
power to
within the capability of the remaining
two feedwater
pumps.
Thorough
briefing of Operations
and
test
personnel
by the test
director
were
observed
by the inspectors.
The testing
was performed
smoothly,
but the automatic recirculation
runback circuit was
no.
activated
due
to
the
response
of the
running
feedwaier
pumps
to
maintain
water
level
above
the
27" actuation
setpoint
during
the
A test deficiency was declared
and the test results
were
investigated.
Review of transient
data
indicated that water level
decreased
to only 27.5",
but observation
of the
SPDS indicated that
water level
was
reduced
below 25".
The
licensee
planned
to perform
additional
testing
of
the
runback circuitry to
ensure
that
the
setpoints
were correct
and that the
system
would have
responded
as
designed.
The difference
between
the water level
observed
on the
and the water level
based
on the transmitter output feeding the
runback circuit was
also
being investigated.
Reperformance
of the
test
was
not
anticipated.
No
other
testing
deficiencies
were
observed.
Q
2-TI-193, Turbine Trip and 2-TI-180,
Backup Control
Panel
Testing
The inspectors
observed
the performance
of these
TIs August 2,
1991.
The tests
were initiated
from
a
power level of approximately
45:o.
The purpose of the tests
was achieved
by initiating a plant
shutdown
by operator
performance
of
a turbine trip, resulting
in
a reactor
Following stabilization of plant conditions,
a test
crew of
operators
proceeded
to the
shutdown control
panel
and to local plant
control panels
and
shutdown
boards
and demonstrated
the capability io
control
reactor
pressure
and
water
level
via
the
shutdown
board
control of safety relief valves
and
the
RCIC system.
Cooldown
and
depressurization
was continued until
a cooldown of 45 degrees
F was
achieved
over
a
30
minute
or greater
time period
to demonstrate
adequate
operator
control
from the backup control panel.
Control of
other plant systems
was maintained
from the main control
room.
Water
level
and
pressure
control
was
returned
to
the
main control
room
following completion of activities from the remote stations.
The
test
crew
and
the
onshift operating
crew attended t aining
sessions
consisting of inplant walkdowns
and simulator demonstrations
in preparation
for the tests.
The inspectors
attended
one of the
training sessions
and
observed
their value in identifying potential
problem areas.
A test brie,ing
was
conducted
by the test director
and
was
observed
to
be
thorough
and
comprehensive.
Additional
discussions
on
equipment
alignments
and operator
personnel
assign-
ments were held immediately following the briefing.
No deficiencies
were observed
in the conduct of the testing.
Set Electrical/Mechanical
Reci rc Control Stops,
SIi-2-SE-96-3
Surveillance
Instrument instruction, SII-2-SE-96-3,
was performed to
adjust
and limit the
speed
on the reactor recirculating water
pumps.
The limit was set at recirculation flows equal
to an approximate
1025
power level. It was
accomplished
by limiting the variable
speed
on
the
generator
sets
which
supply
power
to the
pumps.
This
was
successfully
completed
on the
second effort after
a procedural
er ro,
was
found
and
corrected
after
the first attempt.
The
inspectors
reviewed this effort while in
progress
and
determined
that
the
, activity was accomplished within the guidelines of the procedure.
4.
Power Ascension
Test
Program
Review (72301,
72532)
The inspectors
reviewed testing
performed in accordance
with 2-SOI-100-1,
Master
Startup Operations/Testing
Instruction.
The inspectors
performed
a
review of TDs recorded
during performance of the TIs comprising the
PATP,
and noted several
TDs that required further evaluation
by the licensee
as
follows.
0
a.
2-TI-131 Feedwater
Level Control
System
This TI adjusted
the feedwater control
system for satisfactory water
level
con rol,
and ultimately will verify that
components
of the
control
system
can
control
reactor
water
level
satis-
factorily.
After initial controller adjustments
were
made
per the
TI, the procedure
was
completed with no difficulties encountered
in
maintaining
adequate
level control at low power levels.
However, the
time response
to insertion of
a
manual
step
(5
and
10 'hange)
in
feed flow still failed to meet
Level
2 response
criteria.
Notwith-
standing,
a decision
was
made to proceed with the test
program.
and
perform additional
feed
pump tuning at
a higher
power (about
58>)
l evel
.
Additional feed
pump tuning was accomplished
a
a higher power level,
but the time response
of individual feed
pumps to insertion oi manual
steps
(5 and
10'o) did not meet acceptance
criteria.
Technical
support
engineers
acknowledged
.hat the
response ti >es oi
individual feedpump turbines is slower than
Level II test
acceptance
criteria
and
FSAR commitments,
however tney also concluded that the
overall
response
of the ieedwater control
system in single
and three
element
control
was
adequate
to safely
suppor. continued operation;
further evaluation
and review is ongoing.
Based
upon
the
overall
system
response
and
observation
of daily
operations,
the inspectors
concluded
that this
TD did not adversely
affect continued
power operations.
b.
2-TI-174 Recirculation
System
Flow Calibration
The
purpose
of this
test
was
to
perform
a calibration
of the
installed
recirculation
system
ilow instrumentation
at
near-rated
conditions.
The test
was
performed
iour times
at iour difierent
flows.
Test
results
ai led
to
meet
acceptance
criteria
in
two
categories
oi deficiencies.
The first category of deficiencies
was the failure to meet acceptance
criteria.
During the conduct of the test,
the core flow calculated
by the test did not agree, within plus or minus
one Mlb/hr, with the
core
flow as
read
on meter
2-FR-68-50,
Total
Core
Flow,
on
Panel
2-9-5, or with the core flow value obtained
from the process
computer
OD-3 op-2 edit program.
The single
loop proportional amplifiers,
and
and total
c;
low meter,
2-FR-68-50,
were
recalibrated,
but
the
acceptance
c
eria
was still not met.
The
closest
values
received
were:
Calculated
core flow
Process
Computer
OD-3
Meter 2-FR-68-50
99.7 Mlb/hl
101.46 Mlb/hr
101. 5 Mlb/hr
The licensee
noted during the last test that
.he calculated
core flow
appeared
low based
on the fact that the
Loop A flow was low.
However,
there
was
no identified corrective action or information to support
that conclusion.
This deficiency requires further resolution.
The
second
category
of deficiencies
was
caused
by inconsistent
results (i.e., lack of repeatabi lity).
For example:
(1)
The
GAF calculated for the
APRN/RBM loop proportional amplifiers
and the
GAFs calculated
for the single
tap
loop proportional
amplifiers were
not consistently
between
0.99
and
1.01,
which
was the
acceptance
criteria for these
calculations.
The
GAFs
were acceptable
during the first test,
but
some were outside
the
acceptance
criteria limits on the
second
test
and others
were
outside
the
acceptance
criteria limits during the third tes
.
In
some
cases
the amplifier had
not
even
been
adjusted
between
tests.
Test results
were satisfactory
in
one test,
but not in
the
subseauent
test,
i.e.
inconsistent
results.
The
licersee
noted that the
probable
cause
of the inconsistent
GAFs for the
proportional amplifiers was due to noise in the measured
signal
circuits.
This deficiency requires further resolution.
(2)
The calculated
nozzle
plugging criteria
was at the
acceptance
criteria limit for
one
se
of jet
pumps
and
exceeded
the
acceptance
criteria limit for another
set of jet
pumps during
the last test.
The nozzle plugging criteria
had been
me. durino
previous tests,
i.e.
inconsistent
resul
s.
The licensee
noted
that
the probable
cause
of the
unacceptable
calculated
nozzle
plugging criteria
was
noise
in
the
measured
signal,
which
resulted
in incorrect values
being recorded.
Since satisfactory
results
had
been
obtained
during previous
performances
o. this
test,
the
licensee
concluded
the test results
were
a
one
time
occurrence
and
no further action
was necessary.
None of the deficiencies
noted during the test violated or exceeded
any
TS limits,
and all .the deficiencies
involved Level
2 Criteria.
The
inspector
concluded
that
the deficiencies
did not
adversely
affect continued
plant operation.
However,
the
core
flow and
GAF
calculation deficiencies
need to be resolved.
There
may be equipment
problems
causing
the circuit noise or procedure
changes
necessary
to
eliminate
these
type of deficiencies
and accurately
monitor these
parameters.
2-TI-189,
High Pressure
Coolant Injection System
This test verified proper
system
operation,
including
a manual
start to verify system
parameters
and
absence
of leaks,
a hot "quick"
start,
and
a
cold "quick" start
(the latter is
a
simulation
of
conditions for an
emergency
injection).
Two TDs requi ring further
evaluation
were documented
during this test.
10
(1)
During initial startup of the
HPCI turbine from cold conditions
(at
150 psig),
the
HPCI turbine
stop
valve exhibited
a rapid
opening,
closing
and
re-opening.
This
valve action
was
not
inconsistent
with expected
system
response
during cold, "jack-
rabbit" starts
addressed
in the
system operating instruction
and
GE advisory
information
No.
352),
indicating
too
low
a
balance
chamber
adjustment.
The
turbine
stop
valve
performed satisfactorily during tests
at rated reactor pressure.
(2)
During HPCI flow tests
to the reactor
vessel
at normal operating
pressure,
step
changes
in flow demand
(3,000
to
2,500
gpm)
exhibited
a
decay
ratio
of
0.60
(test
criteria
<0.25).
Acceptable
decay ratios were exhibited for step
changes
at full
flow (5,000 to 4,500).
The licensee
evaluated
these
TDs as not adversely affecting the
system
performance
because
the deficiencies
were
observed
during
conditions other than
normal
expected
conditions (i.e.,
low pressure,
low flow).
Nevertheless,
the licensee
continued its
e 'aluation of
the test data.
Based
upon
observation
of
nominal
system
performance
at
design
conditions,
the inspectors
concluded
that
these
system
TDs did
not
adversely
affect
continued
power
operations.
However,
the
inspectors
also
noted that
HPCI operation
may
be required
at other
than
normal operating
pressure
and/or full flow, thus the
TDs must
be
evaluated
further.
The licensee will submit
a final report to the
NRC within 60 days after
completion of the
PATP.
This report will contain the final disposition of
TDs.
The inspectors will review this report
when received.
5.
Operational
Safety Verification (71707)
General
plant :ours
were
conducted.
Portions of the turbine buildings,
each reactor building,
and general
plant areas
were visited.
Observations
included valve position
and
system
alignment,
and
hanger
condi-
tions,
containment
isolation
alignments,
instrument
readings,
house-
keeping,
power supply
and breaker
alignments,
radiation
and contaminated
area controls,
tag controls
on equipmen.,
work activities in progress,
and
radiological
protection
controls.
Informal discussions
were
held with
selected
plant personnel
in their functional areas
during these tours.
During
a routine tour
on July 28,
1991,
the inspector
iden ified several
problem
areas
around
the
outside
of the
reactor
building
and
intake
structure.
These
items
were
immediately
discussed
with the
SOS
on
July 28,
1991,
and other plant management
on July 29,
1991.
0-
11
Fallen Unit Separation
Signs
Several
Unit 2 Operating
Space
signs
had fallen
down.
These
signs
were placed at various locations in .he plant as part of the Unit 2/
Unit
3 separation
program.
Examples
were
one of the outside
doors
for the
Unit 1/2
DG doors,
Unit
1 reactor
building ventilation
intake,
and mechanical
equipment
room A (door 830).
This indicated
a
need
for periodic
inspection
and
maintenance
for the
separation
program.
The signs
have orange lettering
on
a black background.
Due
to rain the
orange
lettering
had
been
washed
out of several
signs
leaving white lettering
on
a black background.
Smoking In No Smoking Areas
The inspector
observed that
a temporary
machine
shop
had
been erec.ed
on top of the Unit 3
DG building.
At each entrance
to the roof were
No Smoking Signs specifically stating to not
smoke
on the
DG building
roof.
There
was
evidence
of
an estimated
50 to 100 cigc retie butts
on the roof indicating
a blatant disregard
of the
No
Smo! ing Signs.
Fire Wrap Removal
From Operating
Equipment
In the intake structure
the inspector identified that fire wrapping
around
power
cable
junctions
boxes
for the
pumps
had
been
removed.
All of the
pumps
were operable
at the time.
The fire wrap
is used to provide
a one hour fire resistance
barrier rating between
redundant
safe
shutdown
equipment.
The
two electrical divisions of
RHRSW power cables
do not meet the minimum separation
distance of 20
feet,
and the fire wrap is required.
One division is routed
in
a
cable tray tunnel
and the other division routed in a conduit tunnel.
The
pumps
provide cooling
as
the ultimate hea.
sink at
BFNP.
If for
some valid reason
the fire wrap is
removed,
a fire watch is
required
to
be posted within one
hour.
The
inspector
knew of
no
reason this should
be
removed
because
of the operable
equipment.
The
inspector
reviewed the listing of fire protection 'active
impairment
permits
called
Attachment
F to
No permits or compensatory
actions
were in effect for the fire wrap.
Upon notification
the
SOS
took
immediate
action
to correct
the
problem.
An Attachment
F
was
completed
and
posted.
Licensee
senior
management
was contacted
and
a detailed
action
plan
initiated to identify and correct
the
problems.
It was determined
that the fire wrap was
removed
under
WO 91-35664-00
to support Unit 3
walkdown
inspections.
The
was
approved
by the Operations
Work
Control
Group
on July
17,
1991.
The
licensee
stopped
all
Unit,
3
wal kdown
inspections
until
the
problems
were fully identi fied and
corrected.
The
inspector
concluded
that
a violation of
TS
3. 11.G. l.a
had
occurred.
This requires
that all fire rated
assemblies
such
as
conduit wraps separating
systems
important to safe
shutdown within
a
12
fire area
shall
be operable
at all times.
If the assembly
device is
must
be established
within one
hour.
This
was identified as
VIO 259,260,296/91-26-02,
Fire Wrap Inappropriately
Removed.
Later
the
licensee
determined
that
the contractor
preparing
the
walkdown inspection
plan did not
use
the Unit 2/Unit
3 separation
drawings.
This would
have
prevented
walkdowns
in this
area.
The
licensee
at the
end of this report period
had
not resumed
work and
still was developing their corrective action plan.
These
issues will
be followed during the rou.ine resident
inspec.ions prior to resuming
work activities,
and violation closure.
Unit 3 Fuel Sipping
and Inspections
During this reporting period,
the licensee
conducted
fuel sipping
and
inspection
of fuel
assemblies
located
in the
Unit
3
SFSP.
The
purpose of these activities was to assess
the condition of fuel for
possible
use
in Unit 3 cycle
6 by identifying failed fuel
a semblies.
The
sippinq
and
inspection
were
conducted
by
GE personnel.
The
inspectors
reviewed
and observed
tnese activities
on
an ongoing basis
during the reporting period.
No deficiencies
were identified wi
h
the fuel inspection activities;
however,
fuel handling errors
were
made during fuel sipping operations.
Fuel
sipping
was
performed
in accordance
with special
test
3-ST-
90-03,
Unit 3 Fuel Sipping.
Two fuel sipping cans
were utilized and
were
addressed
as
the
"north"
and
"south"
sipping
cans.
Fuel
assembly
transfer
forms
were
prepared
and
approved
for each
fuel
movement in ihe
SFSP.
Procedure
SDSP
26. 1, Special
Nuclear Material
Management,
establishes
the
admin',strative
requirements
for
the
handling of
SNM and the transfer of SNM from one item control area to
another.
Because
the Unit 3
SFSP
is considered
as
a single "Item
Control Area," the requirements
for second party verificacion of fuel
assemblies
were no. in place.
Fuel
assembly identification was being
performed
bv
SFSP
row-rack-column location only.
Procedure
3-ST-90-03
required
that
fuel
handling
be
performed
in
accordance
with 3-GOI-100-3,
Refueling Operations,
and
the
approved
FATFs for moving fuel assemblies
between
the
sipping
cans
and their
SFSP locations.
Procedure
3-GOI-100-3 required
thar, all steps
on the
be
performed line by line.
The fuel handling errors
were
a-
follows:
( 1)
On June
29,
1991,
the fuel
handlers
grappled
a fuei
assembly
from
a different
SFSP
location
than
that identified
on
the
approved
FATF.
The fuel assembly
was
moved to the south sipping
can.
After the assembly
was sipped
the fuel handlers
attempted
to place it in the position called for
on
the
FATF.
Upon
finding that
SFSP
location
occupied,
all fuel
nandling
was
stopped
and
the
refueling
was
notified.
The
licensee
13
conducted
an
incident
investigation
(II-B-91-130)
which
concluded
that
the
event
was
caused
by personnel
error
and
failure to follow procedures.
Immediate
corrective
actions
included
verifying that
surrounding
fuel
assemblies
were
in
- heir proper locations; initiating
a field change
to place
the
errant
fuel
assembly
in its proper location;
and
conducting
a
briefing on the importance of verifying correct
SFSP
locations.
In addition
to
these
corrective
actions,
the
licensee
also
implemented first and
second party verification of both the fuel
assembly
serial
number
and
SFSP
location during the
remaining
fuel moves.
(2)
On July 6,
1991,
the licensee
identified that
a fuel
assembly
was
placed
in
SFSP
location
05-10-G
instead
of 05-10-F
as
designated
on the
FATF.
The licensee
determined
tha
the error
occurred
when
the
assembly
was
being
moved
from the
soutr
sipping
can to its
SFSP location.
A second error then
occurred
when thefuel
assembly
serial
number
was incorrectly identifed
and
the incorrect
assembly
was
returned
to the
south
sipping
can.
A third error occurred
when the fuel assembly
in the north
sipping
can
was
placed
in
SFSP
location
05-10-F
instead
of
05-10-G.
All fuel
handling
was
stopped
and
the
licensee
initiated
an
incident
investigation
(I'I-B-91-132).
The
investigation
concluded that the mistake
was caused
by personnel
error
and
ailure to follow procedures.
The
licensee
took
immediate corrective
actions
in response
to these errors which
included
comparing
the
SFSP
storage
racks
to the
FATFs; field
changes
to
place
the
fuel
assemblies
in
the
correct
SFSP
locations; counselling fuel handlers
on the importance of second
party verification; placing
a supervisor
on the fuel handling
bridge to monitor operations;
and establishing
an operator
aid
to formalize
communications
between
the
bridge
and
the
fuel
handling
SRO.
In addition,
personnel
disciplinary actions
were
taken against
the individuals involved.
The failure to follow steps
on the
FATFs line by line is
a violation
of
TS section 6.8. 1. 1 for the failure to implement
procedures
(VIO
296/91-26-03,
Fuel Handling Errors).
The inspectors
are concerned
by
these
fuel handling errors
and
the apparent
ineffectiveness
of the
corrective actions for the first event.
6.
Procurement
(38702)
The
inspector
reviewed
information
,from
Connex
Pipe
Systems
Inc.,
forwarded
by Region III, that
BFN had received
12
one
and
one half inch
socket
weld unions
and three
150 lbs. pipe flanges,
which were processed
as
B31. 1 non-nuclear
instead
of under
Connex's
program.
The
unions
were
shipped
on
BFN order
and
the pipe flanges
on
The
licensee
initiated
CAQR
BFP
910110,
dated April 4,
1991,
which indicated
that
the
ma-erial
was
received
without adeaua~e
documentation.
The
CAQR also indicated that
Connex
was contacted
about
the deficiency.
The inspector
reviewed
the following items:
DCN W457A, which added
iwo
pieces of one-and-one-half-inch
diameter pipe,
each
two feet long, to the
demineralized
water
supply for the
RHR heat exchanoers.
and was done for
stress
reduction
in order to enhance
the ability of the
RHRSW piping to
maintain
a Seismic Class
I boundary;
MR 891015103,
which replaced
flanged
fittings on drywell cooler
A5 inlet and outlet which is part of the
system;
QDCN Q16640A, which indicated that the
use of a B31. 1 union in tne
nonsafety-related
DI water system
was acceptable;
and
QDCN Q1667A,
which
indicated that
an
ASTM B-61 was
an acceptable
material
in accordance
with
ANSI
B 16.24,
Bronze
Pipe
and
Flanged Fitting, for the flanges
installed
on drywell cooler
A5 inlet and outlet.
The inspector
concluded
from these
reviews that the material
was shipped
from
Connex
without the
proper
vendor
QA reviews
and
approvals,
receipt inspection initially identified the problem,
the material
was
used
in the
RBCCW and
DI systems,
and the
use of ;ne material
was acceptable.
7.
Reportable
Occurrences
(92700)
The
LERs listed
below
were
reviewed
to determine if the
information
provided
met
NRC requirements.
The determinations
included
the verifi-
cation of compliance with
TS
and regulatory
requirements,
and
addressed
the
adequacy
of the
event description,
the corrective actions
taken,
the
existence
of
potential
generic
problems,
compliance
with
reporting
requirements,
and
the
relative
safety
significance
of
each
event.
Additional in-plant
reviews
and
discussions
with plant
personnel,
as
appropriate,
were conducted.
(CLOSFD)
Unplanned
Actuation
Following
Deenergization
of
Bus
By Unknown Cause.
On April 5,
1991,
an
unplanned
ESF actuation
occurred
upon the loss
of
Bus
3B.
The
bus deenergized
when the
3B1 circuit protector
tripped.
All equipment
responded
as designed io the
ESF signal.
The
cause of the event could not be determined.
An inspector
reviewed the
LER, dated
May 5,
1991,
and determined that
it met the requirements
of 10 CFR 50.73.
The inspector also reviewed
the
incident
investigation
which
was
conducted
on this
event
( II-B-91-078).
The
investigation
did
not
discover
any
failed
components
or plant conditions
which could
have
caused
the circuit
protector to trip.
However,
during troubleshooting
on the circuit
protector internal
components,
the overvoltage relay setpoint
jumped
from 129.7 volts to 131.4 volts and then continued- to repeat
in the
range
of the higher value.
Even
though this test did not indicate
fai lure of the overvoltage
relay, it was
replaced
for conserva.ism.
No discrepancies
or
concerns
were identified during the
review of
this
LER.
0
0
15
(CLOSED)
Gaseous
and Liquid Effluent Samples
That Were
Missed
Due
To Improper
Work Activities Caused
TS Requirements
To Be
Exceeded.
On
March
1,
1991,
the
licensee
discovered
that security
data
could
not support
the
performance
of effluent
samples
for two inoperable
radiation monitors.
Based
on this finding, the
licensee
determined
that
TS required compensatory
measures
were not implemented.
An inspector
reviewed
he
LER, dated April 1,
1991,
and
determined
that it met the requirements
of 10 CFR 50.73.
A violation was issued
for this
event
(VIO 91-10-02)
in
a
previous
NRC
report.
The
follow-up of the violation
and
associated
corrective
actions
are
discussed
in paragraph
8 of this report.
No further concerns
were
identified during the review of the
LER.
(CLOSED)
Unplanned
ESF Actuation Unit 3
DGs Started
On April 12.
1991,
an unplanned
ESF actuat'on
occurred
when the four
Unit 3 emergency
DGs unexpectedly
auto-started
during the performance
of the
common accident
signal logic SI.
The cause
of this event
was
personnel
error resulting
from
a lack of attention to detail during
installation
of
an inhibiting boot
between
two
contacts
on
the
Division II core spray logic
B relay.
Corrective
actions
performed
included Operations
personnel
ensured
that electrical
maintenance
personnel
stopped
the performance
of the
SI;
an incident investigation
was conducted
to determine
the cause of
the
event;
and
the
was
resumed
and
successfully
completed.
Maintenance
personnel
who install
boots
received
training
on
the
proper installa .ion
o
boots.
The
inspector
reviewed
the
LER and
supporting
documentation
which
included
electricai
maintenance
training
records
and
incioenv.
investigation
No. B-91-091 dated
June
13,
1991.
Based
on this review
the inspector
concluded that adequate
corrective action
was taken.
(CLOSED)
Potential
Failure of
RHRSW and
EECW Systems
Following A Seismic
Event
On
April
12,
1991,
the
licensee
determined
that
a
previously
recognized
condition
had
not
been
reported
in accordance
with the
requirements
of 10 CFR 50.73.
This condition involved the potential
for failure of the
RHRSW and
EECW Systems
during
a seismic event.
In
July 1987, during performance
of hydrostatic testing of
RHRSW piping,
a flexible joint,
Dresser
coupling failed
due
to excessive
axial
load.
Subsequently,
on
December
5,
1987.,
a condition
adverse
to
quality report
was written to
document
that protection
'of buried
piping from differentiaI movement of the soil and building structures
was not achieved
because
none of the existing flexible joint designs
could have
accommodated differential movement in the di rection
along
o
~,
~
16
the axis of
a the pipe.
This
was
the result of a rigid connection
called
a
saddle
which
was installed
across
the flexible joint to
prevent pressure
loads
from pulling apart the piping from the joint.
As
a result of this design,
a seismic
event could have
caused
loss of
and
EECW.
This condition existed
since original construction
of the plant.
The
inspector
reviewed
the
LER
and
supporting
documents.
The
corrective action
was consistent with the commitments
in Volume
3 of
the
NPP.
Programs
were
established
to resolve
past
deficiencies
which
led to
inadequately
documented
or analyzed
designs.
At ihe
requirements
for these
programs
were
developed
and
implemented.
Project instructions
were also issued
which augment
the requirements
of the
programs.
TVA added
a
section
to the
Rigorous
Analysis
Handbook
which established
guidelines
for design
and
analysis
of
flexible joints.
A clarifying statement
was also
added
to
a design
criteria
that
established
requirements
for analysis
of flexible
joints.
Based
on this review the inspector
concluded
that
adequate
corrective action
was taken.
(CLOSED)
ESF Actuation Resulting
from Leaking Packing
on the
DP Transmitter.
This
item
was
identified
on April 9,
1991
when
an
unplanned
actuation
occurred.
A Group
1
PCIS occurred
during the performance
of a SI when
IMs placed
Channels
A and
B in
an isolated
mode
and
a
leak
from 2-PDT-1-25B valve
caused
the depressurization
of the
low
side of the Channel
B transmitter.
The cause
of this event
was that
one
process
instrument
had
entrapped
air in the
low-side
sensing
line,
and
one process
instrument
had
a water leak from the packing in
the low-side manifold valve.
Both instruments
were part of the
MSL,
high flow logic.
f
The unit operator
contacted
in the
IMs,
and
work
on
the
was
stopped.
The
IMs
returned
the affected
instruments
to service.
Subsequent
corrective
actions
were
the
IMs
vented
trapped
air;
backfilled line for the first process
instrument;
and
-ightened
packing nuts
on the other process
instrument.
In addition,
SIs that
test
excess
flow check
valves
were
revised
to require
constant
communications with control
room Unit Operator
and to install jumpers
to bypass
the initiation of Group
1
PCIS logic on
main
steam line
high flow.
The inspector
reviewed
the licensee
corrective action.
It was also
noted that the SI, Z-SI-4.7.0. l.d-2, Instrument
Line Flow Check Valve
Operability Test,
was
resumed with no additional
problems.
(CLOSED)
Unplanned
ESF Actuation Following
Bus
Deenergization
Caused
By Random
Equipment Failure.
0
17
On
May 19,
1991,
an unplanned
ESF actuation
occurred
upon the loss of
Bus 2A.
All equipment
responded
as
designed
to the
ESF signal.
The cause
of the event
was the failure of the
Bus
2A normal
power
source,
MG set
2A.
An inspector
reviewed
the
LER, dated
June
17,
1991,
and determined
that it met the requirements
of
The inspector
also
reviewed
the
incident
investigation
conducted
for
this
event
(II-B-91-112).
The investigation attributed
the motor failure to
a
breakdown of the winding insulation.
There
was
no history of motor
failures
by this
method at
BFN and this
was
considered
an isolated
event.
The licensee
replaced
the failed motor
and returned
the
set to service.
No discrepancies
or concerns
were identified durin,
the review of this
LER.
8.
Action on Previous
Inspection
Findings (92701,
92702)
(CLOSED)
IFI 259,
260,
296/89-35-01,
Flexibility of Reactor
plater
Level Sensing
Lines.
This
item addressed
the inspector's
concerns
in two areas
associated
with the
replacement
of
a flexible instrument
piping
system
on tne
reactor
water level
sensing
lines
on Unit
2 with
a one-inch rigid
stainless
steel
piping:
The first concern
involves
the
need
for
preventative
maintenance
and
the
second
deals
with setting
the
spring-can
hangers
for operating
temperatures
("hot setting" ).
The
licensee's
corrective
actions
included
an
evaluation
and
determination
tha
the
system
has
been installed properly and that
no
prescheduled
preventative
maintenance
activities
are
required.
However,
the
system
engineers
are
required
to
walkdown their
respective
systems periodically to evaluate
the
need for maintenance.
The
actions
to disposition
the
second
part
of
the
issue
were
completed
when
z,he
spring
cans
were
evaluated
and
adjusted
as
required during the
performance
of TI-190,
Thermal
Expansion,
with
the reactor at operating
temperature
and pressure.
Based
on
the
above
actions
taken
by the
licensee.
this
issue
is
closed for Unit 2.
However,
the item is administratively closed for
Units
1 and
3 since it was
opened
based
on concerns
associated
with
the corrective actions for Unit 2 only.
(CLOSED) VIO 259,
260, 296/91-10-02,
Missed Compensatory
Samples.
This
violation
was
issued
for
the
failure
to
implement
TS
compensatory
measures.
On March
1,
1991,
the
licensee
discovered
that
security
data
could
not
support
the
performance
of effluent
samples
for
two
radiation
monitors.
Based
on
this
finding,
the
licensee
determined
that
TS
required
compensatory
measures
were not implemented.
18
The
licensee
initiated
an
incident investigation
( II-B-91-045) to
determine
the root cause
of the
event
and corrective
actions
to be
taken.
The investigation
determined
that
the
causes
of the
event
included
failure
to
follow sampling
procedures,
the
misuse
of
checklists,
and
inadequate
chemistry
supervision.
The corrective
actions
included
personnel
actions
against
the
chemistry
analysts
involved;
discussions
with all
chemistry
personnel
of strict
procedural
compliance
and
the
meaning
of initials/signatures
in
procedures;
and
revisions
xo
procedures
for
the
oversight
of
compensatory
SIs.
.An inspector
reviewed
the licensee's
response
to this violation the
completed
incident investigation,
and
revised
chemi. try SIs.
Tne
inspector
determined that the corrective actions
had
been
completed.
No discrepancies
or concerns
were identified during
the
review of
this item.
(CLOSED)
VIO 259,
260.
296/91-17-01,
Failure to Follow Hold Order
Procedure.
The
licensee
had failed to follow SDSP-14.9,
Equipment
Clearance
Procedure,
in that
an
independent
verification
o
the
clearance
boundary
was
not performed prior the placing
the
hold tags
on the
applicable
equipment.
The
boundary
was that utilized
to isolate
Units
1 and
3 from Unit
2 for the restart
of Unit 2.
The licensee
stated that the tag-out
was
an extremelv large boundarv that involved
several
systems
and
was being initiated and verified
on
a
system
by
system
basis
rather
than
the entire
tag-out
being identified
and
verified and signed-off prior to the
placement
of any tags
on ihe
equipment
as required
by the procedure.
This issue
was identified by the inspector
and once the licensee
was
confronted,
changes
were
made
to the
tagging
process
to
meet
the
requirements
of the procedure.
Based
on this cor'rective action, this
item is therefore
closed.
(CLOSED)
Open
Item
260/91-202-01,
inadequate
Review
of
Plant
Conditions Prior To Beginning Surveillance
Test.
During the
NRC
ORAT followup inspection,
an inspector identified
a
concern
with
inadequate
Operations
shift
supervision
over
the
performance
of
an
SI.
A
UO
had
to
stop
the
performance
of
O-SI-4.2.B-67,
Service
Mater Initiation Test,
when it
was
realized that continuing would reduce
the
number
of operable
RHRSM
pumps below that required
by TS.
The procedure
required
a
EECM
pump
to
be
made
however,
the
other
EECM
pump
on the
same
was already inoperable
for reasons
not related to the SI.
The
inspector
considered
this
an
example
of inadequate
supervision
in
that off-normal conditions
were
not considered
prior to authorizing
the
performance
of the SI.
The inspector
discussed
this
item with
19
licensee
management
and
the
Operations
Manager
stated
that
the
following corrective actions would be taken:
( 1)
Discuss
with shift
supervision
the
importance
of properly
assessing
plant status prior to authorizing SIs.
(2)
Revise
the
SI to
assure
that
TS
pump requirements
cannot
be
inadvertently violated.
During this reporting period,
an inspector- reviewed
the licensee's
closure
package
for this item
and
the
revised
SI.
The
inspector
concluded
that
the
licensee
had
completed
corrective actions
which
should
preclude
the
recurrence
of this issue.
No discrepancies
or
concerns
were identified during the review of this item.
9.
Exit Interview (30703)
The inspection
scope
and findings were
summarized
on August 16,
1991 with
those
persons
indica;ed
in paragraph
1 above.
The inspectors
described
the areas
inspected
and discussed
in detail
the inspection findings'l:s.ed
below.
The licensee
did not identify as proprietary
any of the material
provided
to
or
reviewed
by
the
inspectors
during this
inspection.
Dissenting
comments
were not received
from the licensee.
Item Number
Description
and Reference
260/91-26-01
NCV,
Failure
to
Update
Control
Room
Procedure,
paragraph
2.
259,260,296/91-26-02
296/91-26-03
VIO, Fire Wrap Inappropriately
Removed,
paragraph
5.
VIO, Fuel Handling Errors,
paragrapn
5.
Licensee
management
was
informed that
6
LERs,
1 IFI,
2 VIOs, and
1
Item were closed.
10.
Acronyms and Initialisms
ANSI
ASOS
BFNP
CAQR
CFR
DCN
DP
American National
Standards
Institute
Average
Power
Range Monitor
Assistant Shift Operations
Supervisor
Browns Ferry Nuclear Plant
Condition Adverse to Quality Report
Code of Federal
Regulations
Design
Change Notice
Document Control
and Records
Management
Diesel Generator
Differential Pressure
Emergency
Core Cooling Systems
20
ECCW
GAF
GOI
GPM
IFI
IM
IR
LCO
LER
LRED
ATE
NRC
Oi
PATP
POB
Psig
QDCN
SDSP
SOI
TD
TI
TS
Essential
Component
Cooling Water
Emergency
Equipment Cooling Water
Emergency Notification System
Emergency Operating instruction
Engineered
Safety Feature
Fire Protection
Procedure
Final Safety Analysis Report
Gain Adjustment Factor
General
Electric
General
Operating instructions
Gallons
Per
Minute
High Pressure
Coolant Injection
Inspector
Followup Item
Instrument Maintenance/Mechanics
inspection
Report
Limiting Condition for Operation
Licensee
Event Report
Loss of Coolant Accident
Licensee
Reportable
Event Determination
Motor Operated
Valve
Measuring
and Test Equipment
Non-cited Violation
Nuclear Performance
Plan
Nuclear
Regulatory
Commission
Operating instruction
Power Ascension
Test Program
Primary Containment isolation
System
Plan- Operations
Building
Pounds
Per Square
Inch Guage
Quality Assurance
Quality Con rol
Quality Design
Change
Notice
Reactor Building Closed Cooling Water
Reactor
Core Isolation Cooling
Residual
Heat
Removal
Residual
Heat
Removal
Reactor Protection
System
Site Director Standard
Practice
Surveillance instruction
Service Information Letter
Special
Operating Instruction
Safety
Parameter
Display System
Test Deficiency
Technical Instruction
Technical
Information Center
Technical Specifications
Valley Authority
21
UIC
UO
WP
Urgent Intent Change
Unit Operator
Unresolved
Item
Violation
Work Order
Work Plan
Work Request