ML18033B647
| ML18033B647 | |
| Person / Time | |
|---|---|
| Site: | Browns Ferry |
| Issue date: | 02/19/1991 |
| From: | Kellogg P, Patterson C NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML18033B645 | List: |
| References | |
| 50-259-90-40, 50-260-90-40, 50-296-90-40, NUDOCS 9103050451 | |
| Download: ML18033B647 (68) | |
See also: IR 05000259/1990040
Text
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UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETTASTREET, N.W.
ATLANTA,GEORGIA 30323
Report Nos.:
50-259/90-40,
50-260/90-40,
and 50-296/90-40
Licensee:
Valley Authority
6N 38A Lookout Place
1101 Market Street
Chattanooga,
TN
37402-2801
,, Docket Nos.:
50-259,
50-260,
and 50-296
License Nos.:.
and
Facility Name:
Browns Ferry Units 1, 2,
and
3
Inspection at Browns Ferry Site near Decatur,
Inspection
Conducted:
December
19,
1990 - January
18,
1991'nspector:
~
~
C. A.
atterson,
Senior Resident
Inspector
Z l~ q]
Date Signed
Accompanied
by:
E. Christnot, Resident
Inspector
M. Bearden,
Resident
Inspector
K. Ivey, Resident
Inspector
G.
Humphre
, Resident
Inspector
Approved by:
a
Inspecti on
r
rams,
TVA Projects Division
SUMMARY
g/
Date
signed
Scope:
This routine resident
inspection
included surveillance observation,
maintenance
observation,
operational
safety verification, modifications,
post modification
testing, electrical
issues,
SPOC, restart
experience
reviews,
and
DCRDR
Audit,, LLRT, essential
design
calculations,
operational
readiness
review,
reportable
occurrences,
Part
21
Reports,
actions
on
previous
inspection
findings,
and bulletins.
Results:
'
violation was identified for failure to implement design control measures,
paragraph
5.
This violation was
not
a programmatic
problem with the design
r
910305045k
9 i0220
PER
ADMEN 05000259
Q
process.
Several
instances
of incorrect design
implementation
occurred.
One
example
involved the installation of unqualified cables 'in three applications
after the cable
usage
was restricted.
A second
example
involved one instance
where
the
drawings, used
in the
design
had
not
been
updated
following an
Appendix
R modification,
and
two instances
where the correct drawings were not
used in modification workplans.
A
NCV was identified
by the
NRC for improper rigging from a safety related
structure,
paragraph
3.
A chain hoist
was
suspended
from a support
and the
loading
had not
been
analyzed.
The licensee
promptly removed
the hoist
and
initiated a detailed review of the problem.
A NCV was identified, by the
NRC for failure to maintain configuration control
of the
DG air starting
system,
paragraph
4.
The licensee
promptly corrected
the problems
and initiated
a review of the configuration control status
sheets.
'A
NCV was identified for the failure to follow workplan instructions
during
modi.fications
on
the
2C1
RPS circuit protector,
paragraph
5.
The licensee
promptly corrected
the deficiencies
and initiated an incident investigation to
identify and correct the root cause.
A URI
was identified for deficiencies
which occurred
during integrated
testing,
paragraph
2.
The deficiencies
were identified during the Units I/2 A
and
D train
DG load acceptance
tests.
During two tests
the
pumps would
not start.
The
problem
was attributed
to
a
load cell switch inside the
output
breaker
compartment
not making contact.
The licensee
reported this
problem to the
NRC and is conducting
an incident investigation.
A
was identified for .resolution of
SPDS reliability and
human factors
concerns,
paragraph
10.
These
items were identified during the
and
DCRDR
audit.
The
licensee
is
continuing
to
have
problems
with the
implementation
of
equipment
clearances,
paragraph
5.
There
appears
to
have
been
inadequate
corrective
action with respect
to
YIO 90-29-01.
Additional
examples
were
identified in
IR 90-33.,
The root cause
of this
problem
may not
have
been
addressed
and the continuing problem represents
a concern with the licensee's
ability to protect personnel
and equipment during ongoing work activities.
Additional examples
of VIO 90-33-01,
Failure to
Make
and
50.73
Reports,
were identified, paragraph
2.
The licensee
has
denied
one
examp'le of
this violation which
was
identical
to
these
isolations.
The
denial
is
currently being reviewed
by the
NRC.
The closeout
inspection of the Unit
2 torus identified several
material
and
cleanliness
problems,
paragraph
4.
There
was
a lack of licensee
management
involvement in the closeout.
Another walkdown is planned prior to closeout.
REPORT
DETAILS
Persons
Contacted
Licensee
Employees:
0.
- L
- M
J.
R.
B.
R.
A.
G.
p.
- p
- J
R.
Zeringue, Site Director
Myers, Plant Manager
Herrell, Operations
Manager
Rupert, Project Engineer
Johnson,
Modifications Manager
McKinney, Technical
Support
Manager
Jones,
Operations
Superintendent
Sorrell, Maintenance
Manager
Turner, Site guality Assurance
Manager
Carier, Site Licensing Manager
Salas,
Compliance Supervisor
Corey, Site Radiological
Control Manager
Tuttle, Site Security Manager
Other
licensee
employees
or contractors
contacted
included
licensed
reactor operators,
auxiliary operators,
craftsmen,
technicians,
and public
safety officers;
and quality assurance,
design,
and engineering
personnel.
NRC Personnel:
- C. Patterson,
Senior Resident
Inspector
E. Christnot, Resident
Inspector
- W. Bearden,
Resident
Inspector
- K. Ivey, Resident
Inspector
G.'umphrey,
Resident
Inspector
+Attended exit interview
Acronyms used throughout this report are listed in the last paragraph.
Surveillance
Observation
(61726)
The inspectors
observed
and reviewed the performance of required SIs.
The
inspections
included
reviews
of the
SIs for technical
adequacy
and
conformance
to
TS,
verification of: test
instrument
calibration,
observations
of the conduct of testing,
confirmation of proper
removal
from service
and return to service of systems,
and reviews of test data.
The inspectors
also verified that
LCOs were met, testing
was accomplished
by qualified personnel,
and
the SIs
were
completed within the required
'frequency.
The following SIs were reviewed during this reporting period:
a.
O-SI-4.9.A. l.a(c),
Diesel
Generator
"C" Monthly Operability Test.
The inspector
observed
several
portions of this SI being conducted
in
the Unit I/2 Control
Room and
DG Building on December
18,
1990.
This
procedure
had
been
validated
during
a previous
performance.
No
deficienci'es
were identified during the observation of this SI.
b.
2-SI-4.2.B-45A(II), Loop II
RHR Logic System
Functional
Test.
The
inspector
observed
several
portions of the SI being conducted
in the
Unit I/2 Control
Room
on December
22,
1990.
The procedure
was being
Validated
during this
performance.
The inspector
noted that the
licensee
issued
a non-intent
change
to step 7.10.13 to clarify the
requirement
to reclose
valve 2-FCV-74-59.
Also licensee
operations
personnel
stopped
the SI performance
during one step
when they became
unsure of the correct contacts
where test leads
were to be connected.
Assistance
in clarifying the correct contact information was obtained
from the
RHR and electrical
system engineers
prior to proceeding with,
the remainder of-the SI.
- No deficiencies
were identified during the
observation of this SI.
I
c.
2-SI-4.2.K.2,
Reactor Building Exhaust
Vent Radiation Monitor Source
Calibration
and Functional
Test 2-RM-90-250.
An inspector
observed
this SI being performed
as
a
PMT.
The SI
had not been validated at
the time of the inspection.
,No deficiencies
were identified.
d.
Integrated
ESF Testing
During this reporting
period,
the
licensee
performed
a series
of
seven
ESF tests.
The inspectors
reviewed the SIs, observed
the tests
being
performed
and
reviewed
the
preliminary test
data.
The
following observations
were noted:
(1)
I/2-SI-4.9.A.3.a,
Common
Accident
Signal
Logic.
This
infrequently performed
SI tests
the
RHRSW initiation logic and
verifies that both divisions of the
common accident signal logic
will function on actuation of the
CS system of each reactor to
provide
an
automatic start
signal
to all four Unit 1/2
DGs.
Additionally this SI served
as
a portion of the
PMT associated
with
DCN
W14030
which is
described
in the modifications
paragraph.
The
inspector
observed
several
portions
of this
being
conducted
in the Unit I/2 Control
Room and shutdown
board
rooms
on December
23,
1990.
This procedure
was being validated during
this
performance.
Although
no
hardware
related
deficiencies
were
identified
during
the
testing,
and
the
testing
was
eventually
completed with no test exceptions,
the testing
was
halted during performance
when
a portion of the test could not
be performed
due to
a recently installed modification, referred
to as
the slow bus transfer.
The SI
was revised
and the test
was completed.
(2)
3-SI-4.9.A.3.a,
Common Accident Signal Logic.
This infrequently
performed
SI tests
the
RHRSW initiation logic and verifies that
both divisions of the
common accident signal logic will function
on actuation
of the
system of each
reactor
to provide
an
automatic start signal
to all'our Unit 3
DGs.
The inspector
observed
several
portions of this SI being conducted
in the Unit
3 Control
Room
on
December
22,
1990.
This procedure
had
been
validated
during
a
previous
performance
and
no significant
changes
to the Unit 3 equipment
had occurred since the previous
performance.
No deficiencies
were
identified during
the
observation of this SI.
'
1/2-SI-4.9.A.3.b,
480 Volt Load Shedding
Logic System Functional
Test.
This SI
was
performed" to verify that the
480V load shed
logic functioned
in conformance
with the
requirements
of TS 4.9.A.3.b.
The inspector
observed
several
portions of this.SI
being conducted
in the Unit 1/2 Control
Room and shutdown board
rooms
on December
26,
1990.
This procedure
was being validated
during this performance.
During the observation of this SI the
inspector
noted that the
ASOS assigned
lead responsibility for
performance
of the testing
authorized
disabling of the
load
shedding
function associated
with the
lA
FPC 'Pump,
1A
Pump,
and
2B
RWCU Pump.
Step 7.1(8) of the SI allows functional
testing of local logic relays with disabled
load shed contacts
when the
ASOS determines
that the shedding of any load needs
to
be
prevented.
If disabled
the
relay contacts
are
to
be
documented
on Attachment
3 of the SI.
O-SI-4.9A.l.b-l,
2,
3,
and
4,
Diesel
Generators
A.thru
D
Emergency
Load Acceptance
Test.
I
DG A Testing
During the initial performance
of the emergency
load acceptance
test for
DG ~,
the Al
Pump failed to start
due to
an
erroneous
initial system line
up specified in the procedure.
The procedure
was corrected,
the
system realigned,
and
a second
attempt
was initiated.
During the
second
attempt of the
A test,
the
sequence
of
events that should
have occurred
was
as follows:
t= 0 sec
Trip breaker
1614,
4160V
Shutdown
Board
A Normal
Feeder
Breaker,
A starts
and accelerates
to full
speed.
t=O
sec
Breaker
1818 closes,
reenergizing
4160V Shutdown
Board
A from
DG A,
pump
2A starts,
and
480V load shed
logic is initiated.
t=7
sec
pump
2A starts.
t=l4 sec
RHRSW pump Al starts
8
0
I.
t=40 sec
Load shed logic timer times out, sequencing
on various
loads
During this test
perfo'rmance,
only the events
through t=0 sec
actually occurred.
A review of the strip'ecorder
monitoring
the load
shed logic indicated that it was only energized for
approximately
0.5 seconds.
The
2A
pump
and the Al RHRSW
pump did not start.
A followup review of the
event
indicated
that
a
possible
defective
breaker cell switch contact,
which closes
when the
DG,
breaker
closes,
caused
the failure of the logic.
The breaker
was exercised
on
a dead
bus
and the test proceeded.
During
the third attempt
of the
A test
the
equipment
performed
as required.
No deficiencies
were identified.
8 and
C Testing
During the initial performance of the load acceptance
tests for
B and
C; no deficiencies
were identified.
However, the
B
test strip recorders
indicated
a momentary
loss of generator
field voltage.
D, Testing
During the initial performance
of the
D test,
the
DG came
up
to speed
and voltage
and the
DG breaker closed onto the shutdown
board.
However,
the
RHR pump,
the
pump,
and the
RHRSW pump
failed to start.
The
480V load
shed logic did not function
properly.
As
a result of this failure, the licensee
obtained
technical
assistance
from the
vendor
and
determined
that
a
contact
on the cell switch did not close.
Consequently,
the
equipment
did not
perform
as
expected.
The
breaker
was
exercised
on
a dead
bus
and the test proceeded.
During the
second
attempt
of the
D test, all
equipment
performed
as required.
No deficiencies
were identified.
The
licensee
completed
the
series
of 'integrated
ESF testing
by
performing
a total of
10 tests,
seven of which were successfully
completed
and three
which were not.
The licensee
issued
a
CARR and
initiated
an incident investigation
to determine
the
cause
of the
test failures.
In addition,
the licensee
plans to initiate a design
change
to parallel
the cell switch contacts
with other contacts
on
the actual
breakers.
The inspectors will monitor the progress
on
a
routine
basis.
This
item is identified
as
URI 259,
260,
296/
90-40-01, Deficiencies Identified During Integrated
ESF Testing.
On January
7,
1991, during the performance of O-SI-4.2.A-17,
Refuel
Floor Ventilation Logic
System
Functional
Test,
two refuel
zone
ventilation trips were received.
When the fans
were shifted from
slow to fast, speed
as part of the SI, the low static pressure
relays
dropped,out,
tripping the Refuel
Floor fans
and isolating the refuel
zone ventilation system
on Unit 2.
The trip signal cleared
when the
fans
stopped.
Performance
of the SI
was
stopped while the licensee
determined if,the test
could
be
conducted
with t'e fans
in slow
speed.
During this time
PMT 65-211
was star ted
on the
SBGT system
requiring
SBGT trains
B 'and
C to
be placed
in service.
The
caused
the Refuel Floor pressure
to drop below the actuation
pressure
of the
low static
pressure
switches
so that the ventilation trip
signal
was sealed
in when the SI was started'gain.
Both tests
were
stopped until the conflict could be resolved.
'0
CFR 50.72 requires
that licensee's
notify the
NRC within four
hours of any event'r condition that results
in manual
or automatic
ESF actuation.
The refuel
zone ventilation
system is designed
to
isolate
upon receipt of a
PCIS group
6 actuation
signal
which is an
ESF.
These
events
were not reported
to the
NRC within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />
as
unanticipated
ESF actuations.
The failure to report these
events
are
,examples
of VIO 90-33-01,
Failure to Make
and
50.73
Reports,
-which was
issued
on
December
17,
1990.
The licensee
has
denied
one
example
of
VIO 90-33-01
which is identical
to these
isolations.
This denial is currently under review by the
NRC.
On
December
20,
1990,
during the performance
of 2-SI-4.2.B-45A(I),
Loop I
RHR Logic System
Functional
Test,
the
2D
pump started
unexpectedly.
The
pump
was
secured
iomediately
and the test
was
stopped.
No injection to the vessel
occurred
because
the system
was
out of service
and could not perform its intended function.
The licensee
initiated
an incident investigation
( II-B-90-152) to
determine
the
cause
of this event.
Preliminary reviews
indicated
that
a volt-ohm meter
being
used
to verify continuity completed
a
pump start circuit because it was
connected
between
two terminals
instead of between
a lifted wire and
a terminal.
This issue will be
followed by the resident
inspectors until
a review of the completed
incident investigation report can
be performed.
On
December
30,
1990,
during
the
performance
of 3-SI-4.2.K.2.a,
Reactor
Building Ventilation Exhaust Monitor Source Calibration
and
Functional
Test,
radiation monitor 3-RM-90-250
was
valved out of
service
several
times
during
the test.
At the
time of the
performance
a
temporary
continuous
monitor
was
installed
on
3-RM-90-250 to satisfy
the
compensatory
requirements
of TS 3.2.K.
This
TS requires
a
4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> flow rate estimate,
'an
8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> grab sample
for noble gases,
and continuous
sampling for iodine and particulates.
During the SI, the compensatory
monitor was valved out each time the
permanent
monitor was.
The
was
begun
on
December
30,
1990, at
2:05 p.m.
and completed
on January
1,
1991 at 4:00 a.m.
At various
times
during
the
test,
the
Chemistry
Laboratory
placed
the
compensatory
monitor
back into service
to per'form the
sample
flow
estimates
and collect grab
samples.
The compensatory
monitor was
placed into and
removed from service several
times during the next
14
hours.
The licensee 'determined that the continuous
function of the
compensatory
monitor was never out of service for greater
than three
hours at
a time (per Chemistry Laboratory records of flow estimates);
however,
the aggregate
time that the monitor was out of service
was
estimated at up to
12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.,
The licensee
initiated
an incident investigation
( II-B-91-002) to
determine
the
cause
and establish
corrective actions for this event.
The
inspector
discussed
this
event
wi'th
licensee
personnel
responsible
for the investigation.
Licensee
personnel
stated that
a
configuration
problem in which the sampling
taps
were
downstream of
the process
flow from the isolation valves contributed to this event.
Licensee
personnel
further
stated
that
the ventilation
exhaust
radiation monitors for the refuel
and reactor
zones,
radwaste,
and
turbine buildings
had
been modified with sampling
taps
upstream of-
the isolation
valves.
The
use of these
taps will ensure
that
sampling continues
even if the monitor is
isolated.'he
inspector
and
a
compliance
engineer
walked
down the affected
radiation monitors
in the plant.
The inspector
noted that
each
monitor had been'odified
to include the
new sampling taps;
however,
the
inspector
noted
that
a temporary
sampling unit connected
to
2-RM-90-252,
Radwaste
Ventilation Exhaust Air Particulate
Monitor,
was
connected
to the
downstream
taps.
This would make the temporary
sampling unit susceptible
to the failure discussed
above.
This
problem
was brought to the licensee's
attention for review.
This issue will be followed by the resident
inspectors until a review
of the completed investigation report can
be performed.
2-SI-4.2-3(A),
Revision
6,
Instrumentation
That Initiates
Rod
Blocks/Scrams,'ntermediate
Range
Channel
A Calibration.
The inspector
observed
this calibration while in progress
from the
control
room
on January
9,
1991.
The inspector
noted that
the
procedure
had
been validated,
prerequisites
had
been
performed,
and
procedural
steps
were
performed
in
the
proper
sequence.
No
deficiencies
were noted during the performance.
No violations
or
deviations
were
identified 'in
the
Surveillance
Observation
area.
3.
Maintenance
Observation
(62702,
62703)
Plant maintenance
activities
were
observed
and/or
reviewed for. selected
safety-related
systems
and
components
to
ascertain
that
they
were
conducted
in accordance
with requirements.
The following items
were
considered
during
these
reviews:
LCOs maintai'ned,
use of approved
procedures,
functional testing and/or calibrations
were performed prior to
returning
components
or
systems
to service,
gC records'aintained,
activities accomplished
by qualified personnel,
use of properly certified
parts
and materials,
proper
use of clearance
proce'dures,
and
implementa-
tion of radiological controls
as required.
Work documentation
(MR, -WR,
and
WO) was reviewed'o
determine
the status
of outstanding
jobs
and to assure
that priority was assigned
to safety-
related
equipment
maintenance
which might affect plant safety.
The
inspectors
observed
the following maintenance
activities
during this
reporting period:
a.
WOg 90-24128-00,
Troubleshoot
Breaker
1818
and
Switch
52STA per
EMI-106 "Troubleshooting
and Configuration
Control of Electrical
Equipment."
This work was
performed
on the Units 1/2
D
DG output breaker
and
switch following failure of the switch to actuate
relays
as required
during load acceptance
testing.
No deficiencies
were identified.
b.
WOO 90-21017-00,
Replace
Damaged
Stainless
Steel
Braided Flexible
Conduit.
co
This work was
performed
January
9-10,
1991 to replace
a section of
. special
Eg flexible conduit that
had
been
damaged
due to an unknown
cause.
The inspector
observed
portions of the
ongoing
work and
reviewed
the uncompleted
work package.
The inspector
noted that the
work instructions
included in the package
were adequate
and contained
sufficient detail to allow satisfactory
completion of the work.
Improper Rigging from Snubber Support
During a tour of the Unit 2 Reactor Building on January
10,
1991, the
inspector
observed
an electric
1000 pound rated chain hoist suspended
from a snubber
support,
2-478450H0036.
The snubber
was attached
to
the
RHRSW piping
and
the
support
was
anchored
to the
con'crete
building structure wall at one
end
and the opposite
end
was supported
from the building ceiling by 4 anchor bolts,
1/2 inch in diameter.
A
review of the situation
revealed
that the
support
had not
been
analyzed
to support
a
load
as
required
by SDSP-14. 14,
Safe
Practices
For Operation
Of Overhead
Handling Equipment,
Attachment 9,
Safe
Operating
Practices
For Rigging
Personnel,
Step
1.21
which
states
that "Limitations assigned
to the
use of temporary
support
structures for rigging purposes
shall
be based
upon the determination
of
a
designated
person
who is
competent
in this field.
Such
determinations
shall
be documented
and recorded appropriately."
The situation
was
immediately
brought
to the attention
of the
maintenance
manager
who took prompt action to have the hoist removed.
The licensee initiated
an incident report, II-B-91-015, to determine
any
adverse
effects
and
to
determine
" corrective
actions, if
applicable.
Criteria specified in Section
V.A of the
NRC enforcement
Policy were
satisfied
and therefore this
NRC identified violation is not being
cited.'his
NCV is identified as 260/90-40-02,
Improper Rigging From
Safety Related Structures.
d.
Preventive
Maintenance
on
DG Stationary Auxiliary Sw'itches
During
the
reviews
and
observations
of
System
57,
Auxiliary
Electrical, activities the inspector
noted that the
PN for the 4160V
shutdown
boards
did not specifically address
the stationary auxiliary
switches.
Information received
by the inspector
indicated that the
switch contacts
had never
been cleaned,
the switches
are
changed
only
when they fail, and
the manufacturers
recommendations
for cleaning
the switches
are not followed.
The inspector
was
informed that the
switches
are inaccessible
and consequently
have never
been
cleaned.
The inspector'atched
a vendor representative
observing
the contacts
of a stationary auxiliary switch
by using
a mirror.
The inspector
was also
informed that these
switches
were not removed
and
checked
for proper operation
and cleanliness
when
the
4160V breakers
were
sent off site for the five year overhaul.
This item will be further
reviewed
as
part
of IFI
259,
260,
296/90-40-01,
Deficiencies
Identified During Integrated
ESF Testing.
One
NCV was identified in the Maintenance
Observation
area.
4.
Operational
Safety Verification (71707)
The
NRC inspectors
followed the overall plant status
and
any significant
safety matters
related to plant operations.
Daily discussions
were held
with plant
management
and various
members of the plant operating staff.
The inspectors
made
routine visits to the control
rooms.
Inspection
observations
included
instrument
readings,
setpoints
and
recordings,
status
of operating
systems,
status
and alignments of emergency
standby
systems,
verification of onsite
and offsite power supplies,
emergency
power sources
available for automatic operation,
the purpose of temporary
tags
on
equipment
controls
and
switches,
alarm
status,
adherence
to
procedures,
adherence
to
LCOs,
nuclear
instruments
operability,
temporary alterations
in effect, daily journals
and logs,
stack monitor recorder traces,
and control
room manning.
This inspection
activity also
included
numerous
informal discussions
with operators
and
supervisors.
General
plant tours
were conducted.
Portions of the turbine buildings,
each reactor building, and general
plant areas
were visited.
Observations
included
valve
position
and
system
alignment,
and
hanger
conditions,
containment
isolation
,alignments,
instrument
readings,
housekeeping,
power
supply
and
breaker
alignments,
radiation
and
contaminated
area controls,
tag controls
on equipment,
work activities in
progress,
and radiological protection controls.
Informal discussions
were
held with selected
plant personnel
in their functional areas
during these
tours.
a ~
b.
Configuration Control
.During
a routine tour on
December
17,
1990, of the Units I and
2
building, the inspector identified
a configuration control
problem.
'The
D
DG air compressor
right bank circuit breaker
was in the off
position
on
DG 480V Auxiliary Board A.
In the
B
DG room, the right
bank air
compressor
hand
switch,
O-HS-86-503B,
was
in the off
position.
The inspector
reviewed
the configuration status
control
book in the control
room
and only found
a
PMI-78 configuration
control status
sheet for the
B
DG air compressor.
The lack of a
status
sheet. for the
D
DG was
discussed
with the
ASOS.
A PMI-78
status
was initiated for the
D
DG air compressor.
It was also found
that the system cross-connect
valves
were opened
connecting
the right
and left bank.
The reason for the circuit breaker
being in the
OFF
position
was not
known but was apparently
due to an air leak on the
compressor.
This problem
was discussed
with Operations
Management.
The specific
problem
was corrected
by the completion of a valve lineup for the
system
and
PMI-78 configuration control status
sheet.
Additional
action
was taken to assign
personnel
to review the status
sheets
and
insure they were kept correct.
This
NRC identified violation is not being cited .because
criteria
specified
in Section
V.A of the
NRC
Enforcement
Policy
were
satisfied.
This
NCV is identified
as
260/90-40-03,
Failure to
Maintain Configuration Control of DG Air Starting System.
Equipment Clearances
The
inspectors
reviewed
the
clearances
identified below to verify
compliance
with SDSP-14.9,
Equipment
Clearance
Procedure,
and that
the clearances
contained
adequate
information to properly isolate the
affected
portions of the
systems
being
tagged.
Additionally, the
inspectors
verified,
on accessible
equipment,
that the required tags
were
installed.
No deficiencies
were
identified
during
the
performance of these
reviews.
Clearance
0-91-051
0-91-064
E ui ment/Pur
ose
Electric Fire
Pump
B.
Tagged
out to support
change
out of the motor bearings.
RHRSW Pump C3.
Tagged out to support maintenance
on
a
root valve for the
pump local pressure
indicator.
0
10
2-91-034
2-91-057
RPS Circuit Protectors
2Cl and
2C2.
Tagged
out to
support
modifications
to
the trip setpoints
and
underfrequency
relays.
RPS Circuit Protectors
281
and
2B2.
Tagged
out to
support
modifications
to
the trip setpoints
and
underfrequency
relays.
During the conduct of other activities, the inspectors
noted that the
licensee
is continuing
to
experience
problems
in the
area
of
equipment
clearances.
The
two
examples. detailed
below
were
identified during this reporting period.
(1)
On January
15,
1991,
a licensee
employee failed to notice hold
tags
on valves
2-FCV-20-530
and
2-FCV-20-554 which resulted
in
those
valves
being
operated
and
a piece of equipment
being
returned
to service.
Both valves were'under
HO¹ 2-90-529 which-
had 'not been
released
by the authorized
clearance
holder.
This
event
was discovered
by the licensee
and
an incident investiga-
tion
was initiated.
The licensee
determined
that the valves
were properly tagged.
In addition, the individual involved was
not an operator
and would not normally be authorized to operate
- equipment.
Disciplinary action
was taken against
the individual
involved.
(2)
On
January
10,
1991,
Operations
personnel
implemented
a
"standing
hold order" for the
performance
of wiring modifica-
tions
on the
2C1
RPS circuit protector.
This "standing 'hold
order"
involved
removing
power
to the
2C1 circuit protector
cabinet
by opening
the
"110
Backup
Supply to
Disconnect
Switch" in the Unit 2 Battery Board
room and opening breaker
SCI
Unit Preferred
AC Regulating Transformer
TUP 2,
on
RMOV Board
28
in Shutdown
Board
Room 28.
Procedure
SDSP-14.9
allows the performance of work not under the
controls of the clearance
procedure
provided it is authorized
on
a case-by-case
basis
by the responsible
supervisor
and
SOS/ASOS.
An example
of this given in SDSP-14.9
is
"work of a limited
scope
where full control
can
be provided
and maintained
in the
immediate proximity to the involved equipment."
The operator
remained
in the Battery
Board
room during the work activities
and
was
in the
immediate
proximity of the
backup
supply
disconnect
switch;
however,
the
operator
was
not
in the
immediate proximity of breaker
SCI during the performance of the
work activities.
The failure to provide and maintain control of
breaker
SCI is
a violation of equipment clearance
requirements.
The above instances
of clearance
deficiencies
are additional
examples
of VIO 90-29-01 which was
issued
on November 8,
1990; for clearance
related
problems.
Two additional
examples
were
subsequently
0
L
11
identified in
IR 90-33 which was
issued
on
December
17,
1990.
A
supplemental
response
to address
these
new examples
is pending.
LCO Tracking
The inspectors
reviewed
the
LCO tracking
items identified below to
verify compliance with PMI 15.10, Tracking of Limiting Conditions for
Operations.
This system
provides current status of each
LCO to the
on-shift Operations
personnel
and provides
the restrictions
on the
plant
and
compensatory
actions
to
be
taken for each
LCO.
The
inspectors
reviewed
the tracking
system
information for the
LCOs
listed below'.
LCOP
Title
19900492
19910022
TS 3.1.A and
RPS inoperable until SIs are
performed.
Monitor 3-RM-90-250
due
to
modifications.
Continuously collect
samples
with
auxiliary sample
system
and analyze
every
7 days
when
ventilation is in service.
No deficiencies
were noted.
Torus
Walkdown
The inspectors
were notified by the licensee
that
a Unit
2 Torus
walkdown
would
be
performed for final inspection
and
closure
on
December
21,
1990.
The licensee
stated that persons
representing
an
upper level of management
would participate in the walkdown and that
security would perform their final check
and lock the entrance
to the
hatch
upon completion
and final acceptance
of the equipment.
However,
the
walkdown consisted
of
NRC inspectors,
a plant operator,
a
gC
inspector,
a security officer,
and
radwaste
personnel.
No utility
senior management
was present.
During the walkdown, the inspectors
identified various
problems
that
included
some debris
found floating in the water (ball point pen,
tape,
and what appeared
as pieces of paint), debris
on the walkway,
a
pipe
extended
into the torus that
was not coated
and
was heavily
oxidized,
coating that
was
badly scratched
on the
vacuum breakers,
position
indicator
switches
on
two of the
vacuum
breakers
that
appeared
to be corroded
to the extent that they may not operate,
and
visibility was limited to approximately
18 inches in the water.
After management
personnel
were
informed of the above condition it
was
determined
that this area
would again
be reviewed
and another
walkdown for acceptability
would
be
performed.
The
inspectors
notified the licensee that they plan to participate in that walkdown.
12
One
NCV was identified in the Operational
Safety Verification area.
5.
Modifications (37700,
37828)
The inspectors
maintained
cognizance of modification activities to support
the restart
of Unit 2.
This 'included 'reviews of scheduling
and
work
control,
routine
meetings,
and
observations
of field activities.
Throughout
the observation of modifications being performed in the field
gC inspectors"
were
observed
monitoring
and
documenting verification at
work activities.
a
~
Design Control
In previous inspection reports
the inspectors
documented
observations
'and
reviews
involving the installation of electrical
cables
for
modifications,
the modification of systems
for Appendix
R purposes,
and
the
change
of unqualified electrical
cables for 10 CFR 50.49.
The specific actions
observed
and reviewed were the following:
(I)
In IR 90-33,
an inspector
opened
a
URI involving the instal-
lation of unjacketed
electrical
cable.
These
activities
involved four
DCN/ECNs.
Additional review
by the
inspector
indicated that
a
PRD BFP900189P,
initiated on June 6,
1990,
and
signed off on September
6,
1990, identified the fact that Site
Procurement
Service
failed to specify
appropriate
quality
assurance
and
technical
requirements
as
required
to
meet
qualification of Class
1E cable
and failure to procure cable to
meet
the requirements
of
GDC BFN-50-758.
This
PRD listed
as
recurrence
control six items.
One item required
NE to issue
a
gDCN which listed acceptable
cable
contracts,
including TIIC
cable,,for
use at
BFN.
This item was completed
on August 28,
1990, with the
issuance
of gDCN-gl3819A.
An additional
item
required
that modifications,
maintenance
and
any other plant
organization with cable
intended for installation in a Class
I
structure
must obtain
concurrence
from engineering
that
the
cable
has
been
drawn
from
an
approved
contract, if not
on
DCN-f13819.
This item was completed
on October 5, 1990.
As
a result of the installation of unjacketed electrical
cable
the licensee
issued
additional
CARR/PRDs;:
BFP900376,
Okonite
Un-jacketed,
Type
PX Cable,
Mark
Number
WOV-2;
BFP900378,
Anaconda
Cable
Installation
in
System
90;
and
BFP900386,
Installation of Type
THHN Cable for Drywell Lighting.
These
three
CA(R/PRDs
indicated that
the root
cause
for the cable
installation
was that the corrective action for
BFP900189P
did not establish
necessary
controls to ensure notification of
employees
of the qualified cable list issued
by gDCN g13819A.
Due to this modification, Maintenance
Management
did not have
adequate
direction to train employees
in the use of the
ODCN.
These
items are considered
examples
of a failure to prevent the
installation of electrical
cables
not meeting design criteria..
0
13
This failure is
considered
a violation,
VIO 259,
260,
296/
90-40-04, Failure to Implement Design Control Measures.
1
(2)
In
IR 90-33,
the inspector
documented
the observation
of the
performance
of PMT-BF-268-006,
Test of RHR Valve '2-MOV-74-53A,
RHR Inboard Injection Valve.
The
PMT identified a problem with
a modification,
DCN
W10017A,
which
negated
a
previously'nstalled
Appendix
R modification.
The inspector
observed
a
recent-PMT involving DCN W14030,
which modified the Unit 1/2
4
KV Shutdown
Boards
and the Shutdown
Buses.
This portion of the
modification
required
that
the
four alternate
power
feed
breakers
to the four shutdown
boards
be tripped during
the'resence
of an accident signal.
This would prevent overloading
one of the
shutdown
buses.
During the performance of procedure
1/2-ETV-SMI-I-C-4, Functional
Test of
C shutdown
board,
the
alternate
breaker tripped free
and would not close.
The problem
was
traced
to
an
Appendix
R modification which modified the
breaker
to obtain electrical
isolation from the control
room.
DCN W14030 did not use the latest modification
DCA when it was
approved for installation.
These
items are considered
examples
of a failure to use
the latest
design
change when'installing
additional
modifications.
This failure is
a
second
example
of
VIO 259,
260,
296/90-40-04,
Failure to
Implement
Design
Control Measures.
b.
RPS Circuit Protector Modifications
On January 3, 1991, the
NRC issued
TS amendments
178,
184,
and
149 to
change
the
RPS circuit protector setpoints
for Units 1,
2,
and
3
respectively.
The licensee
had previously revised 2-SI-4. 1.B.16,
Circuit Protector Calibration/FT, to include the
new setpoints
and
placed the SI
on administrative hold until the
TS change
was issued.
During this reporting period,
the licensee
implemented modifications
WP 2460-90,
WP 2461-90,
and
WP 2462-90
to wire the underfrequency
relay contact in series with the time delay coil for each of the Unit
2 circuit protectors.
Modifications for Units
1 and
3 were completed
during previous
reporting periods.
The inspector
observed
portions
of the
performance
of
WP
2462-90
on
the
2Cl
and
2C2 circuit
protectors
and
WP 2461-90
on the 281 and
282 circuit protectors.
The
inspector
also
observed
the performance
of PMTP-BF-99.003
conducted
on the
2C1 circuit protector.
The
PMT corisisted of performing the
revised
SI to verify correct time delay operation,and
set the relays
to the
new setpoints.
No deficiencies
were identified during these
observations.
Prior to conducting
the
PMT on the
2C1
and
2C2 circuit protectors,
the
system
engineer
noted that the
2C1 circuit protector
had
been
wired incorrectly.
The licensee initiated an incident investigation
(II-B-91-008) to determine
the
cause
of the wiring error.
The
investigation
concluded
that
a wire was incorrectly removed during
the work, contrary to the written steps
in the workplan.
14
The licensee
took immediate action'o revise the workplan to correct
the wiring errors.
The modification was reperformed
and the
PMT was
conducted satisfactorily.
The inspector
observed
the performance of
the revised workplan.
No deficiencies
were observed.
This licensee
identified violation is
not
being
cited
because
the criteria
specified
in Sec'tion
V.G. 1 of the
NRC Enforcement
Policy were
satisfied.
This violation is identified
as
NCV 260/90-40-05,
Modifications Wiring Error.
.,c.
P0901.
This
design
change
provided
a
longterm
(72
hours)
alternate
source of nitrogen to the drywell control air header to be
used
in the event that the drywell control air compressors
are not
available
due to
a fire.
The modification installed
a
new one inch
sup'ply line
and
two manual
isolation
valves
to provide crosstie
capability between
the
B
CAD Tank and the compressor
discharge line.
Existing drywell penetration,
X-22, will still be used for drywell
control air.
The inspector
reviewed
the
ECN closure
package
and
observed
selected
portions of the installed
hardware
located in the
Unit 2 Reactor Building. The inspector
determined that the
ECN was
field complete
and in the closure
process
pending
NRC approval of TS
Change
251.
The
closure
package
included
identification
of
modification training
requirements.
Additionally the
inspector
verified that
2-0I-32A,
Drywell
Control
Air
System
Operating
Instruction,
2-AOI-32A-1, Loss of Drywell Control Air, and 2-0I-84,
Containment
Atmosphere
Dilution System
Operating Instruction,
have
been revised to reflect
TS 3.7.A.5 and 3.7.G.3 requirements
that the
B
CAD train
be considered
(placing the plant in a 30 day
LCO) or when plant control air is
used
(placing the plant in a
24
hour
LCO) whenever
the crosstie
valves
are
open.
The inspector did
not identify any discrepancies
with this modification activity.
d.
.ECN P3176.
This design
change
replaced-existing limit switches
on
various
isolation
with environmentally
qualified switches.
These
are required to isolate
primary
containment
on
a
LOCA.
The
ECN required
the replacement
of the
existing limit switches with Eg Snap-Lock type switches,
installation
of CONAN seals,
and installation of stainless
steel
braided flexible
conduit
and
seismic
conduit supports.
The design
change
was field
complete
and in the process
of being closed
by the licensee.
The inspector also reviewed portions of work plans 2182-87,
2326-89,
2079-89,
2080-89,
and
2351-89.
These
work plans
implemented
P3176.
With the exception of the problem with
WP 2182-87 described
in paragraph
3.b,
the inspector
did not identify any discrepancies
with this modification activity.
One violation and
one
NCV was identified in the modifications area;
C
15
6.
Post Modification Testing
(37700,
37828)
a ~
SBGT Decay Heat
The inspector
reviewed
and
observed
the
PMT activities associated
with
DCN
W 10416A.
This
DCN installed
manual
decay
heat
removal
cross-tie
dampers for the standby
gas treatment
system.
Procedure
PMT-BF-65.2ll aligned
the
and
manipulated
system
in order to achieve 'a throttled
decay
heat
bypass
position.
When
the
decay
heat
removal
were
properly
throttled,
the design
flow required, to remove
decay
heat
from the
charcoal, absorber .would
be
achieved;
The
was
to provide
information that
manipulation
would have
no effect
on the
required containment differential pressure.
Two TDs were identified during this
PMT.
TD-03 documented that
Train A inlet damper leaked excessively
during the decay heat
removal
lineup for Train A.
TD-04 documented
that
SBGT Train
B inlet damper
also
leaked
excessively
during the
decay
heat
removal
lineup for
Train B.
The licensee initiated
CARR BFN 900015
and
NE dispositioned
this item as Use-As-Is.
The inspector also reviewed information that
during
a single failure event where
one of the three trains of SBGT
fails to start,
an excessive
amount of back flow'will go through the
idle train
due to excessive
leak-by through the back flow dampers.
No additional testing
was
performed
by the licensee
to determine if
the
two remaining operating trains
would achieve
the required flow
rate.
An additional
problem identified during
the
PMT,
was
that
the
licensee
could not verify that the following TS was met: 4.7.B.1.c.
"Air distribution is
uniform within 205 across
HEPA filters and
charcoal
absorbers."
The
inspector will followup on
these
test
deficiencies.
b.
DG Stationary Auxiliary Switch
The inspector
reviewed
and
observed
the
PMT associated
with
DCN
15894A.
This
DCN installed additional contacts
in parallel with the
stationary auxiliary switch for the shutdown
board A, B, C,
and
D,
normal supply breakers
and the
DG breakers.
The modification was originally for the Unit 3
DGs.
However, after
additional
review the licensee
determined
that the modification to
the Unit 3
was
not necessary
to support Unit 2 operations.
A
modification specifically for Unit 3
DGs will be installed prior to
Unit 3 restart.
The
PMTs were
BF 57.038
and
BF 57.039.
The first PMT was
performed
while the individual shutdown
boards
were deenergized
and the actions
of the
DG breaker
and the normal
feed breakers
could
be exercised.
During the performance of PMT 57.038,
the inspector
noted that when
16
the
DG breakers
were manipulated,
only two of the four logic relays
for initiating the start of the
RHR pump, the start of the
CS pump,
the start of 480V load
shed logic and the start of the
pump
actuated.
This
was
later
traced
to
an incorrectly installed
modification
performed
by plant
maintenance
personnel.
-.After
additional
review,
the
inspector
determined
that this
item
was
caused
by having inadequate
drawings
associated
with this modifica-
tion.
This item is identified as part of example
two of Violation
259,
260$ 296/90-40-04.
On violation was identified in the Post Modification Testing area.
7.
Electrical
Issues
- Cable Ampacity and Separation
(37700)
The
inspector
was
informed that
due to reviews
by
NE of System
31,
additional
cable rerouting/replacement
was
needed.
The review identified
at least
3 cables
buried in flammastic that must
be replaced
because
of
the
issue.
The
cables
are
the
normal
feeder
to Ventilation
Board A, Shutdown
Board
Room
3B Supply
Fan,
and Battery Board
Room
C
Exhaust
Fan.
The inspector
was also
informed that
two additional
cables
'may require
rerouting/replacement.
One
cable is
a
System
31
and
the other is
a
System '57 cable."
These
cables
appear to be in the cable separation
issue,
with the control
power
and
the
power feed
cables
being supplied
from
different safety divisions.
The inspector will continue
to follow the
licensee's
activities
in this
area.
These:problems
are
apparently
centered
around 'application of the 9-list for these
programs.
No violations or deviations
were identified in the Electrical
Issues
area.
8.
System Pre-Operability Checklist
(71707)
The
inspectors
continued
to review the
licensee's
progress
in their
efforts to upgrade
the plant equipment
and documentation
to insure that
systems
are acceptable.to
support restart of Unit 2.
At the end of this
reporting period,
35 of the
38 systems
required to support fuel load have
been
completed
and
49 of the
78 required for Unit
2 restart
have
been
completed.
The
number of systems
required for each
phase is based
on the
licensee's
most
current
evaluation
as
listed
in the
Master
Star tup
Operations/Test
Instruction, 2-SOI-100-1,
Rev. 0.
The systems
reviewed
by the inspectors
during this reporting period are
listed
as follows:
a.
Control Air (System
32)
The
inspector
reviewed
the
package
for the
CA System
and
performed
a
walkdown of
a major portion of the
system
equipment.
This system
includes
both the
CA and the
DCA systems.
Four deferrals
were issued for items that could not be finalized due to restraining
plant conditions.
Each of the
4 were reviewed
and
none were found to
e
17
b.
c ~
impair system operability.
In addition, the engineering
summary was
reviewed
which concluded
that the configuration of this
system is
satisfactory to support restart of BFN Unit 2.
Based
on
a review of
the
system
by the inspectors',
no areas,
were identified to prohibit
system operability.
Annunciator and Sequence
of Events
Recorder
(System
55)
The inspector
walked
down this system which consisted of the control
room annunciators
and recorders
and reviewed the licensee
completed
SPOC documentation.
Part of the package'onsisted
of an update of
the work efforts
performed
during the latter part of 1989 for the
fuel load at that time. It was noted that only one deferral
remained
open
and
was
deemed
not to affect system operability.
Within the
areas
reviewed,
no deficiencies
were noted.
Auxiliary Electrical
(System
57)
The inspector
observed
and reviewed the licensee's
activities in the
SPOC processes
for the following auxiliary electrical
systems:
57-2 120/208 volt AC Distribution
57-3 250 volt DC Distribution
57-4 480 volt AC Distribution
57-5 4160 volt AC Distribution
The inspector
observed
walkdowns
performed
by licensee
personnel.
During these
walkdowns,
the inspector
noted that breaker maintenance
involving overload settings, modifications to insure cable separation
and breaker modifications involving the change
out of overloads
were
in progress.
Most of the breaker modifications involved Micro Verse
Trip installations.
Although these
activities
were
performed
on
numerous
switch gear,
the majority of activities were associated
with
the
systems
served
such
as
and
HVAC.
The switchgear
themselves
were viewed for SPOC
purposes
separately
from the systems
serviced.
The inspector
reviewed
the
PMs for the
systems
and
noted that of
eleven electrical
systems
involving 477
PM items.
These electrical
systems
included both safety related
and non-safety related
equipment
PMs.
Of the
477 items reviewed,
27 items
were considered
late
and
each late item had engineering
approval.
The inspector also reviewed
the status
of SIs
performed
such
as
the
DG operability,
common
accident signal,
480V load
shed,
and
DG load acceptance.
All SIs
were performed with minor changes.
The
inspector
reviewed
the
packages
which
included
the
exceptions
and deferrals.
The inspector
noted that
no unverified
assumptions
were
documented
as
being outstanding.
The inspector
reviewed
RTP Test Exception
No. I System 57-2, which documented that
TI-73B was not performed.
This TI verifies that the electrical
loads
on
Backup Control Panel, will transfer to the
120V
18
Unit Preferred
Power. Source
when the transfer switches
are placed in
the emergency position.
Due to this panel
not being considered
as
a
part of System
57-2, the system
can
be returned
to service prior to
completion of TI-73B.
The inspector
noted that at the
end of this
reporting period, site
QA personnel
were reviewing several
CAQRs that
impacted
these
systems.
Reactor Building Closed Cooling Water (System
70)
The inspector
reviewed the completed
package for this system
on
December
20,
1990.
There
were
two ..exceptions
and four deferrals.
One exception
was taken
because
the drywe11
head must
be installed to
balance
the drywell ventilation systems
and associated
RBCCW supply
to the drywell coolers.
The
second
exception
was
because
of a
TS
change
to. add
the
RBCCW containment
isolation valves
to
TS Table
3.7.A.
For three of the deferrals all of the work was complete for
System
70,
but the
ECNs were not closed
due to remaining
work on:
other
systems..
The fourth deferral
was
a
RTP-70 test
exception
requiring
a
heat
load in the drywell to perform.
The inspector
concluded there
was
a logical basis for each exception
and deferral.
The inspector
noted that in the
SPAE Evaluation Checklist,
Attachment
E of
BFEP
PI 88-07,
numerous
signature
steps
were
marked
as
"not
applicable".
The steps
were denoted with a footnote that the step
was only required for SPAE packages
identified in Attachment I.
This
attachment
provided
the
system
mode descriptions
by system.
For
Revision
6 of PI 88-07,
dated
July 7,
1990,
RBCCW was listed in
Attachment I.
For
Revision 7, dated July 27,
1990,
RBCCW was not
listed
as
a separate
system.
This was
done apparently
because
the
only item to
be
reviewed
was
isolation which
listed
System
70
under
System
64.
This
was
considered
a weakness
of the
SPAE review of System
70.
Several
open
issues
remained
with the
NRC concerning
RBCCW such
as
seismic
qualification outside the drywell and containment isolation valves at
the time of the system
SPOC.
Radiation Monitoring System
(System 90)
The radiation monitoring system consists
of various
CAMs, ventilation
and liquid effluent monitoring equipment,
and
ARMs.
This system
has
undergone
a series of major modifications during this extended
outage
which are further described
below:
W1073,
this
DCN replaced
many of the
chart
recorders
and
existing
CAMs associated
with the ten building effluent monitors
with newer
Eberline
equipment.
This
DCN is associated
with
equipment
that
is
necessary
to
support
fuel
load
and
is
substantially field complete.
H6910, this
DCN replaced
many of the chart 'recorders
and
existing
not part of
DCN
W6910 with
newer
Eberline
equipment.
Various work still remains to complete for this
DCN
which is associated
with equipment that the licensee
does
not
consider
required
to support fuel load.
However the primary
19
containment
leak
detection
monitor,
2-RM-90-256,
which is
included in this modification has
been replaced
and tested.
P0354, this
ECN added
the
new Stack'ide
Range Monitor required
by
This modification consisted of,,installation
a
substantial
amount of new equipment
and construction of a
new
building directly'djacent
to the plant stack
to house that
equipment.
Hl263,'his
DCN
was
associated
with the
main
steam
line
radiation monitors.
It replaced
the existing
GEMAC drawers
in
the control
room with newer
NUMAC components.
The
MSL radiation
detectors
and other
remote
equipment
located
outside of the
control
room was unchanged.
The
was delayed
due to numerous
problems associated
with the ten
building effluent monitors.
Many internal
wiring problems
were
discovered
during
system
setup/testing
which resulted
in
many
troubleshooting
work requests
and over 40
FDCNs.
The inspector
accompanied
licensee
personnel
during the final system
walkdown conducted
on January
7,
1991.
During the
walkdown the
following minor material deficiencies
were identified:
Although the
CAMs located
in the Reactor Building were mounted
to satisfy
seismic
requirements,
each
CAM is
equipped
with
wheels
to allow portability and
those
CAMs located
in the
Turbine Building are free to move.
The
new design
includes
an
apparent
permanent
installation with stainless
braided flexible
hoses
which does
not allow much
freedom for movement
and the
hoses
are therefore
subject to potential
damage
due to movement
during operation.
CAM 3-RM-90-249 already
had
a flex hose that
appeared
to
be
damaged
possibly
due to addition of
a quick
disconnect fitting.
During the control
room portion of the walkdown the inspector
noted that the 9-2 and 9-10 panels still include recorders
which
are associated
with online liquid effluent monitors which are
no
longer used.
Although offline monitors
are
now available
and
provide for monitoring of liquid effluents
and
the
online
monitors are
no longer in service
nor maintained with no plans
to ever
use
the online monitors, the control
room recorders
are
tagged
as temporarily removed
from service.
The inspector
was
informed
by licensee
personnel
during the walkdown that TYA's
policy was to abandon
equipment of this nature
in place rather
than
expend
the
money to
remove it.
The licensee
plans
to
'mplement
numerous
human factors
upgrades
to the control
room
during the next refueling outage
and the inspectors will follow
the licensee's
work in this area.
0
20
Based
on
discussions
with licensee
personnel
the
inspector
determined
that adequate
training
on the
new equipment
may not
have
been provided to operations
personnel.
This issue
was also
raised
by licensee shift management
personnel.
Although the
system
was accepted
by the plant staff with this deficiency,
a
representative
from Eberline
was onsite during this period
and
was
used
for
specialized
training
for
instrumentation
technicians
that perform work on this equipment.
Additionally,
the inspector
was informed that .a lesson
plan
had .been
developed
in this
area
and training for operations
personnel
was in
progress.
The
system
checklist
was
completed
on
January
13,
1991.
The
inspector
reviewed
the 'ompleted
package
with the
system
engineer
on January
15,
1991.
The inspector did not identify any
outstanding
problems
with the
system that affected operability to
support Unit 2 fuel reload.
f.
Cranes
and Hoists
(System
111)
The inspector
reviewed the licensee's
completed
System Checklist for
the efforts associated
with the cranes
and hoists.
This activity was
limited to four overhead
cranes
which were selected
on the basis that
each
could
be
used
to lift nuclear
and safety-related
materials
located
in areas
with materials
and
equipment
important to plant
safety.
The limited checklist
was further influenced
as
a result of
the cranes
and hoists
being maintained throughout the outage.
Only minor discrepancies
were identified during the
walkdown which
consisted
of two missing labels,
one minor repair
and
some cleaning
of the reactor building crane trolley.
Each
has
now been corrected.
NE evaluated
the
system
and
determined:
(1) that all primary and
critical drawings associated
with the system
were being evaluated
as
parts
of other
systems,
(2) the applicable
primary
and critical
drawings
have
been
computer-aided
drafted
restored,
and
(3)
no
drawing discrepancies
or outstanding
DCNs existed against
the system
and that the drawings for the system will support unit 2 operation.
Based
on the review,
no deficiencies
were noted.
No violations or deviations
were identified in the System Pre-Operability
Checklist area.
9.
Restart
Experience
Reviews
(71707)
The
inspectors
reviewed
the
licensee's
program
implemented
to
take
advantage
from the restart
experiences
at Peach
Bottom and Pilgrim Nuclear
Power Plants.
The experiences
consisted
of a list of 26 major problem
areas
to
be considered
during restart of those plants.
Those identified
were:
(1) major equipment failures
and preventative
actions that should
be
21
considered,
(2)
personnel
assignments
to critical specific
areas;
(3)
communication
enhancements
within the licensee's
organization
and with the
NRC, and (4) operational
precautions
to be aware of during power ascension
and testing.
The licensee
has
reviewed
each of the
26 major areas
identified.
A
letter
from the Technical
Support
Manager to the Plant Manager,
dated
December
10,
1990, stated
that
17 of the
26 items
have
been
implemented,
an additional
6 items will be
implemen'ted prior to plant startup,
and
3
of the
items
were not applicable
to
BFN. Within the
6 items identified
that were not completed,
some require specific plant conditions prior to
their performance
and those conditions
had not been
met prior to issuing
the subject letter.
,This effort will be
monitored
during
the
remainder
of the restart
'ctivities by the inspectors.
10.
Safety
Parameter
Display System
and Detailed Control
Room Design
Review
Audit
During November
13-15,
1990,
an
NRC audit team conducted
an onsite audit
and
DCRDR.
The results of this audit are detailed
below.
a
~
Safety Parameter
Display System
The
purpose of the
SPDS audit was to assess
the
BFN-2 interim SPDS
against
the requirements
in Supplement
1 to NUREG-0737 for an
SPDS.
The audit
team determined
that the licensee's
interim
met the
requirements
concerning
(1) continuous
display of safety
status
information,
(2) location convenient
to control
room operators,
and
(3) concise
display.
The audit
team
found that the
requirement
regarding
minimum information about
the five safety functions
was
satisfactory for the interim SPDS;
however, this requirement
would
not
be
completely satisfied
for the
operational
SPDS until the
licensee fulfills its
commitment
to provide additional critical
safety
function
parameters.
The audit
team
concluded
that
the
licensee
would
meet
the
requirement
related
to training
and
procedures
when
the
licensee
satisfies
its
commitment
to
have
procedures,
and trains operators
with and without the
before
restart.
The requirement
related
to isolation of electronic
and
electrical
interference
is currently under review by the Instrumen-
tation and Control
Systems
Branch
(SICB) of NRR.
The audit
team
determined
that the licensee's
interim
SPDS did not
meet
two of the eight
SPDS requirements
as follows:
( 1) rapid
and
reliable (e.g.,
unreliable
touch screens
and function keys,
unclear
how sensor
inputs with different rates
would be handled,
weaknesses
regarding
configuration
management,
and
clarifications
needed
concerning
security
controls
for
data
base);
and
(2)
incorporates
accepted
human factors principles (i.e., glare
on
22
I
cathode
ray tubes'nd
SPDS status
box
on display obscured
by the
anti-glare
hood when operator is standing).
The staff expects
that the noted examples of SPDS
system unreliabil-
ities, the glare
on the
CRTs,
and the .obscured
SPDS status
box,
will be resolved
prior to restart. of BFN-2.
Resolution of these
items will be followed
as
URI 260/90-40-06,
SPDS Reliability and
Human Factors
Concerns.
, b.
Restart
Human Engineering Discrepancies
The audit
team
concluded
that
TVA had satisfactorily
implemented
corrective actions for the nine restart
HEDs.
The results
were
as
follows:
(I)
HED
109
concerned
electrical
shock
that
operators
could
encounter
when
changing control
room annunciator light bulbs.
Two screws that hold annunciator light bulb mounting panels
in
place
are
located
very close to the
48V
DC buses
which supply
power to the bulbs.
The licensee
wrapped
the portions of the
buses
adjacent to the screws with electrical insulating material
to prevent personnel
from receiving shock while manipulating the
screws.
The staff found the corrective
action
adequate
to
resolve this
HED.
(2)
HED 201 indicated that operators
were required
by procedure
-to
determine if drywell pressure
had
reached
55 psig
on
a control
instrument that
had
a range of 0-40 psig.
The licensee
changed
the drywell pressure
instrument
range to 0-60 psig.
The staff
found that the corrective action satisfactorily resolves
this
HED.
(3)
HED 202
and
HED 292 concerned
EOI ambiguities.
The audit team
evaluated
a sample of these ambiguities
and determined that they
had
been
resolved
in subsequent
revisions of the
EOIs.
In
addition,
the licensee
implemented
a formal
process
to ensure
that revisions
to
do not have
problems with clarity and
ambiguity.
This process
is
implemented
through
the following
PMIs:
PMI 12.6,
"Implementation
and Maintenance
of Emergency
Operating Instructions";
PMI 12.7, "Writers Guide for Emergency
Operating
Instructions";
PMI 12.8, "Verification of Emergency
Operating Instructions";
and
PMI 12.9, "Validation of Emergency
Operating Instructions".
The staff found that the licensee
had'atisfactorily
resolved
these
HEDs.
(4)
HED 283 concerned different zero references
for reactor
vessel
level
instruments.
The
licensee
changed
the
affected
instruments
to the
same
zero reference.
The staff found that
this
HED was resolved.
V
0
23
(5)
HED 287 noted that,
when
emergency
standby lighting is in use,
some
areas
of the control
room did not meet the design lighting
illumination level of 10 footcandles.
The licensee
modified the
emergency
standby
lighting
and
conducted
light illumination
surveys.
For those
areas
that still did not meet the lighting
illumination design criteria,
the
licensee
performed
a task
analysis -'and evaluation
of requisite
operator
actions.
The
results
of the evaluation
indicated that operator
tasks
would
not be impaired by,the reduced
illumination levels.
The staff
reviewed
the
task
analysis
and evaluation,
and
performed
a
walkdown of those
areas
having reduced
illumination levels
and
observed
what operator
actions
were required
to
be performed.
The staff determined
that operator
tasks
could
be performed in
the
reduced
illumination conditions
and
was satisfied that the
1'icensee
had corrected this
HED.
(6)
HED 290 indicated that-control
room indication regarding
steam
line flow was
inconsistent
with emergency
EOIs.
The licensee
completed
an
change
that provides
consistency.
The staff
found that this
HED was resolved.
(7)
HED
299
and
HED 300
concerned
an
EOI step
regarding
reactor
building differential
pressure
that
did
not specify
what
operator
action
was
required
and
an associated
control
room
annunciator with multiple inputs that was ambiguous with respect
to this procedure
step.
The
EOI step was~hanged
to indicate
what operator action should
be taken
and dedicated
specifically for reactor
building differential
pressure
have
been
provided in the control
room.
The staff found that the
licensee
had satisfactorily resolved this
HED.
During
a Unit 2 Control
Room walkdown, the audit team observed that
two suppression
chamber
water
level
instruments,
2-LI-64-54A and
2-LI-64-66, with
a
range
from negative
25 to positive
2 inches,
lacked indication of negative
values.
The licensee
reported that
this discrepancy
was not identified during the
DCRDR.
In addition,
the
resident
inspectors
identified
in
IR 90-33 that
B
channel
recorder
XR-64-199
had
no units designation
label.
These
problems
will also
be tracked
under
URI 260/90-40-06,
SPDS Reliability and
Human Factor Concerns.
No violations or deviations
were identified in the
and
DCRDR area.
ll.
Local Leak Rate
Rate Testing
(61720)
The inspectors
continued
to follow the progress
of the licensee's
program.
As of January
10,
1991,
51.4X of the individual
LLRT tests
required
to
be
completed prior to performance
of the
ILRT have
been
completed.
The
ILRT is presently
scheduled
to be performed
on March 16,
1991.
24
The
inspectors
monitored portions of LLRT testing
associated
with four
of the eight
This testing
was
performed
on January
6,
1991.
This testing
was
performed
in accordance
with 2-SI-4.7.A.2;i-3/la,
A
. Main
Steam
Line
LLRT, associated
with 2-FCV-1-14
8
2-FCV-1-15
and
2-SI-4.7.A.2.i-3/1b,
B Main Steam Line LLRT, associated
with 2-FCV-1-26
8
2-FCV-1-27.
This testing is intended to satisfy
ASME Section
XI testing
for leak tightness
in accordance
with TS 4.6.G
and
TS Definition 1.0.MM
along
with verification of primary
containment
operability
per
TS 4.7.A.2.i.
The stated
acceptance
criteria
shown in the SIs is 11.5
while maintaining
a minimum pressure
of 26 psi.
The two SIs observed
by
the inspector failed the above acceptance
criteria with 149.7
A and
81.7
SCFM for
MSL B.
Subsequent
testing
on
MSL" C also
ended
with unsatisfactory
results.
As the result of the unsatisfactory
results
the
licensee
performed
various
corrective
measures
such
as
stroking of the valves,
attempts
at flushing of the valve seats,
and
disassembly
and maintenance
of valve internals for the inboard
MSIV on
C.
Licensee corrective action
was still in progress
in this area at the
close of .this reporting period.
The inspectors will continue to follow
licensee
actions
in this area.
No violations or deviations
were identified in the
LLRT area.
The inspectors
reviewed various
completed
essential
calculations
selected
from the Calculation
Cross
Reference
Information System printout.
The
calculations
were reviewed for a partial
check of mathematical
equations
and to determine
the adequacy
of the licensee's
methodology
and approach.
The inspectors
also verified that inputs
and assumptions
were current
and
valid, and that they reflected
the controlling conditions with reasonable
results
considering
the inputs,
method,
and objectives.
The calculations
reviewed were
as follows:
a
~
b.
ND-(0064-890010,
Revision
1, Secondary
Containment/Zonal
Boundaries.
This calculation
defines
the
secondary
containment
boundaries
and
zonal separations
to provide
a technical
basis for future studies
and
modifications which identify penetrations
that breach
a boundary.
No
deficiencies
were identified.
ND-(2063-890014,
SLC System
Boron-10 Necessary
to Meet
Requirements.
This calculation
was
performed
to determine
the
minimum amount of boron-10
and the minimum volume of enriched
pentaborate
necessary
to respond
to an
ATWS event.
No deficiencies
were identified.
co
BFN-BF53-003,
Systems
Required for Fuel
Loading.
This calculation
was performed to identify the systems
required to be evaluated
by the
DBVP prior to fuel loading for Unit 2.
The calculation listed the
Unit 2 systems
necessary
to mitigate accident and/or transient
events
during fuel
movement.
Through discussions
with licensee
personnel,
the inspector
found that the calculation
was performed to support the
0
25
fuel
load conducted
in 1988
and not the cur'rent
SPOC process.
For
this reason,
the licensee
placed this calculation in the archives for
history only.
This calculation
was not used to support
the current
core reload.
No violations or deviations
were identified in the
area of Essential
Design Calculations.
13.
Operational
Readiness
Review (93806)
The
inspector
reviewed
the
status
of the
licensee's
program
for,
implementation
of corrective actions
associated
with concerns
identified-
as
part of the licensee's
ongoing
ORR program.
TVA's
ORR program
was
designed
to be
a comprehensive effort to assess
the material
and personnel
readiness
at Browns Ferry necessary
to support
safe plant operation.
The
ORR
team
has
conducted
two phases
of their review of Browns Ferry's
operational
readiness.
The first phase
was performed during May 1989 with
the results
documented
in
an interim report
dated
June 9,
1989.
The
second
phase
was
performed
during February
1990.
A total of 47 general
concerns
with 501 associated
action items were identified during these
two
-phases
of review.
These
items
are tracked
on the licensee's
TROI system
along
with other
corrective
and
administrative
control
programs.
According to the licensee's
ORR status
report dated
December
21,
1990, the
corrective
actions,
have
been
completed for. 64K of the concerns
and
92K of
the individual action items.
The inspector
selected
several
individual action items from the
TROI that
the licensee
has listed as having corrective action complete.
These
items
were
reviewed
to determine
adequacy
and extent of licensee
corrective
actions
in each
area.
A manager
has
been
assigned
responsibility for
coordination of the corrective actions
in this area
and closure
packages
have
been
prepared for many of the items.
Those individual action items
reviewed along with the inspector's
comments
are listed below.
Phase II Concern
A Item
P2.
During the
ORR team's
review of the
licensee's
self
assessment
program, it was
noted
that
routine
observation
checks
by non-shift operations
managers
were not being
performed
as
required
by the licensee's
program.
The inspector
examined
documentation
that verified the
performance
of routine
observation
checks
performed
during
the
period of November
and
December,
1990.
These
observation
checks
were
performed
by both
operations
shift
management
and
non-shift
management
personnel.
Several
were
performed
by
the
Operations
Superintendent
and
Operations
Manager.
The inspector
believes
that the original
ORR
concern
has
been adequately
addressed.
Phase II Concern
B Item h2.
During the
ORR team's
review of General
Operating
Instructions, it was
noted that the plant procedures
for
shutdown
from powered operation
to cold shutdown,
2-GOI-100-12A and
2-GOI-100-12C,-
placed
the unit in
a condition requiring very careful
operator action to ensure
the reactor
remains
shutdown during plant
.26
cooldown.
The
GOIs
had
been
revised to,eliminate
a reactor
from about
30K power requiring fully inserting all control
rods per
the rod program
as
the normal
means of plant shutdown.
Cooldown was
permitted
to start
as
soon
as
the reactor'as
taken subcritical.
This
concern
for difficulty in
balancing
the effects
of rod
insertion,
heat
removal,
decay
heat
generation,-
and
Xe buildup is
significant considering
the recent event that occurred at another
where
an inadvertent criticality occurred
while conducting
such
a
cooldown.
The inspector
reviewed the closure
package for this item
and held discussions
with members of licensee
management.
Although
the licensee
has
not reached
a final decision
concerning
the exact
method of control rod insertion to be used during plant shutdowns
and
a revision to the
GOIs
may
be required
in this area,
the
above
licensee
procedures
hav'e
been .revised to include caution to not begin
forced
cooldown until all control
rods
are full in.
The inspector
believes that the original
ORR concern
has
been adequately
addressed.
Phase
II Concern
D
Item ¹1.
During the
ORR team's
review of
resolution
of various
identified technical
issues,
a
concern
was
identified where
an item that
had previously been identified during
'the
Phase
I
ORR
review
had
not
been
aggressively
pursued
to
completion.
This item associated
with Category
I
in August
1985,
which recommended
the inspection of certain
one inch
Hancock
gate
valves
in the
HCU.
The planned
inspections
had
been
postponed
due to lack of parts after having
been
delayed for over
four years.
The
inspector
reviewed
the
closure
package
which
contained
documentation
to verify the
completion of this
item.
Specifically the inspection of al,l
185 gate valves
(2-HCV-85-617)
had
been
completed
by July 30,
1990,
under
WO 90-04598-00.
As the result
of the inspections
various cracked,
broken or otherwise
damaged
valve
wedges
were identified.
A total of 63
(34%)
wedges
had
to
be
replaced.
The inspector believes that the original
ORR concern
has
been adequately
addressed.
Phase
II Concern
D
Item ¹5.
During the
ORR team's
review of
resolution
of various identified technical
issues,
a
concern
was
identified during
a partial simulator validation of 2-GOI-100-lA and
2-GOI-100-1C.
The
GOI
and
SI referenced different power levels at
which the
Intermediate
Range
and
Average
Power
Range
Monitors
overlap
is verified.
The inspector
reviewed
the closure
package
which contained
documentation
that verified that both of the
above
GOIs
were
revised
to clarify the
requirement
for verification of
proper overlap prior to exceeding 5l power by a visual
check of IRMs
and
APRMs instead of performing 2-SI-4.1.8.1,
IRM Calibration.
The
SI is
now required to be performed at
10-25'A power.
The inspector
believes that the original
ORR concern
has
been adequately
addressed.
Phase II Concern
E Item ¹6.
During the
ORR team's
review of the
licensee
s line organization/training
interface, it was identified
that
revised
reactor
water
level
curves
were
needed
to support
27
training
on the modified water level instrumentation.
During the
extended
outage
reactor
vessel
level
instrumentation
lines
were
relocated
as part of ECN-7131.
These
curves
had not been
prepared
by
NE although
the training was in progress.
Senior
NE management
was
not aware of the critical need for this information.
The inspector
reviewed
the
closure
package
which contained
NE
memo
to Plant
Operations
(R62
901101
891)
dated
November
1,
1990,
which provided
the required curves.
Training for operations
personnel
to cover this
information is scheduled
to be provided during the licensee's
restart
training during the
r equalification cycle starting
February
11,
1991.
The
inspector
believes
that
the original
ORR
concern
has
been
adequately
addressed.
Phase II Concern
H Item'3.
During the
ORR team's
review of the
license'e's
Preventative
Maintenance
Program, it was identified that
one monthly
PM had not been
performed in an extended
period of time
even
though
the
system
had periodically been
in service
during the
period while fuel
was
in the reactor
vessel
during
1989.
The
inspector
reviewed the licensee's
closure
package
on this item..
The
licensee
had closed this
item based
on the fact that although
the
RHRSW system
had
been
in service several
times during that period it
had
been for only short periods
and the total accumulative
service
time
was actually minimal.
The
PM,
RHRSW Flow Blockage Monitoring
Measurement,
has
no performance criteria
and is performed to record
differential pressure
data
which would~ be
used to identify adverse
trends
during normal operation.
The licensee further stated
in the
closure
package
that the
PM would be performed for baseline prior to
fuel load.
The inspector
determined
from discussions
with licensee
personnel
that
this
was
originally scheduled
for early
January
1991,
but had
been
delayed
and is scheduled
to be performed
prior to=-fuel load.
The inspector will continue to follow the licensee's
progress
in this area
by reviewing more completed
ORR items during the next reporting period.
14.
Reportable
Occurrences
(92700)
The
LERs listed
below were
reviewed
to determine if the
information
provided met
NRC requirements.
The determinations
included the verifica-
tion of compliance with TS and regulatory requirements,
and addressed
the
adequacy
of the
event description,
the corrective
actions
taken,
the
existence
of potential
generic
problems,
compliance
with reporting
requirements,
and
the relative
safety
significance
of each
event.
Additional in-plant reviews
and
discussions
with plant personnel,
as
appropriate,
were conducted.
a
~
(CLOSED for Units
1
and
2 only)
Failure to Install
Core Spray Hanger.
This
LER concerns
the July 21,
1985 discovery that
a pipe support
(No.
H-81)
had
not
been installed
on the Unit 3
CS system
10-inch
0
28
pump test line as
required
by the
system
design
drawings.
The
LER
indicated that
an engineering
evaluation of the condition determined
the line to be seismically qualified'but that it could not be shown
to
be qualified for the
loss of coolant accident
induced
torus
hydrodynamic loads.
The licensee
attributes
the
cause
of the
LER to the
process
then
being utilized,for the revision
and
issuance
of plant drawings. It
appears
that the system in place at the time allowed for the issuance
and revision of drawings without an attendant
revision to the
data
sheet.
This introduced
the potential for incorrectly closin'g
,
out
an
ECN prior to completion of wor k scope
changes
that might have
arisen
subsequent
to the initial issuance
of the
ECN.
The following procedures
and/or
procedure
changes
have
since
been
implemented to correct the noted process
deficiencies:
Procedure
SDSP-8.4,
"Modification Workplans" has
been revised to
require all
work plans
to contain
marked-up
drawings
to
be
utilized
and
an associated
drawing list which references
all
drawings required to implement and/or inspect
a modification.
The design control
process
is presently
managed
via NEP-6. 1 Rl,
"Change
Control" (Revision
0 issued 7/I/86).
Attachment I to
NEP-6. 1
Rl requires
that
when
adding,
deleting or changing
information about
a drawing, the associated
Data Sheet revision
number
be entered
on
Forms
10575A and
10575E.
On
December
17,
1990
the
NRC inspector
visually inspected
the
counterpart
locations
on the Unit I and Unit 2
CS system test lines
and ascertained
that the required
supports
were in place
in the
comparable
area
where support
H-81 was found missing
on Unit 3.
This
item will remain
open for Unit 3 pending installation of the missing
support
scheduled
to take place prior to Unit 3 startup.
Thi.s item
is closed for Units I and 2.
(CLOSED)
Procedural
Inadequacy
Results
in Start
of,
Control
Room Emergency Ventilation System.
This event
was
an automatic start of the
CREV system
as
a result of
inadequacies
in a restart test procedure
being utilized on December
4,
1987 to align
4
KV electrical
boards for maintenance.
It appears
that the restart
procedure
did not specify
a desired position for the
4
KV shutdown
boards
A and
B transfer switch.
After the alignment of
the electrical
boards,
4
KV shutdown
boards
A and
B were left
connected
to their alternate
power sources.
In the
absence
of
a
procedurally prescriptive position,
the operator
placed the transfer
switch for 4
KV shutdown
board
A in automatic.
This resulted
in a
transfer of the
board
back to its normal
power supply.
During the
transfer,
the
relay for the
480V shutdown
board
tripped ultimately causing
normally energized
radiation monitoring
0
29
equipment
serving the control
bay ventilation duct to trip, thereby
resulting in'he completion of the
CREV start logic.
A commitment to revise the restart test procedure
to specify transfer
switch position is contained
in the licensee's
LER submittal.
This
revised restart test
procedure
was successfully
run and its results
were
approved'- by the licensee's
Joint Test
Group
as
documented
in
Meeting Minutes88-062.
Considering that after the successful
run of the revised restart test
procedure its
use is
no longer required,
the licensee
expanded their
corrective action to include
a review of all other existing plant
procedures
whose
present
and future
use is contemplated,
and which
are associated
with 4
KV shutdown board alignments to ensure that the
desired
position of the
subject
transfer
switches
is adequately
addressed.
This additional
procedure
review was
conducted
by the licensee
and
resulted
in
no adverse
findings.
A statement
to this effect
was
included
on January
16,
1991
in the licensee's
closure
statement
package for this
LER by cognizant
TVA Licensing
and Transmission
and
Customer Services
engineers.
Based
on
an
examination
of the
above
reviews,
the
inspector
determined
that the
concerns
associated
with this event
have
been
adequately
addressed.
(CLOSED)
Single
Failure of Electrical
Fire
Pump
Lockout Relay During LOP/LOCA Could Overload
a Diesel Generator.
This
LER details
a condition in which, during
a LOP/LOCA, the single
failure of
a lockout relay intended to prevent the starting of the
.
fire pumps during
a LOP/LOCA, could cause
the overloading of a single
diesel
generator.
Aspects of this
LER were previously reported
in
NRC IR 90-33 during
the
followup
and
closure
of
VIO 89-27-04.
The
circumstances
associated
with this
LER had
been
presented
in the violation as
one
of three
examples of an apparent failure to report.
An NRC Region II
letter
dated
November
2,
1990
expressed
concurrence
with TVA's
commitment
to install
an
additional
lockout relay
as
adequate
corrective
action for the conditions
described
in the
LER.-:;: As
indicated
in
NRC
IR 90-33,
an
inspector
had verified field
installation of the additional lockout relay noting that
PMT remained
to be performed prior to closeout of DCN PW6909A.
Procedure
O-SI-4.11.B. l.f, Simulated
Automatic
and
Manual Actuation
of the High Pressure
Fire
Pump System,
was performed
on December 4,
1990.
A functional test of the lockout relays
was performed via step
7.6 of the surveillance instruction.
Block 23 of the Retest Control
Form
(Form
SDSP-417)
was
signed
on
December
7,
1990
by the
system
30
engineer
and the systems
supervisor attesting
to the completion
and
satisfactory
approval of the results of the surveillance test.
(CLOSED)
Failure of Residual
Heat
Removal
Service
Water
Pump
Level Switch Resulted
in a Condition Prohibited
by
Technical Specifications.
On
December
21,
1989,
an
AUO identified that the
number of
pumps
was
less
than
the
number
required
by TS.
The
pump
inoperability was
the result of the loss of'wo redundant
B series
pumps.
The
B series
pumps
are considered
to be
technically inoperable'ithout
the support of their associated
pump.
The
AUO determined
that the automatic start feature of the
redundant
pump
Bl failed
and
caused
the
pump
room to,
overfill..
pump
B2
was
tagged
out for maintenance.
The
changed
the control
switch position of the
pump Bl from
automatic
to manual.
The
pump started
and the water level in
the
returned
to
normal.
The control
room operator
was
subsequently
notified of the
event.
It was
determined
that
TS 3.5.C.7
was violated
and the event
was reportable in accordance
with
Based
on the event,
LER 50-260/89-29
was
issued.
The
inspector
reviewed
the
corrective
action
and
associated
documentation
provided
in
the
closure
package.
The
licensee
determined
that
the
event
resulted
from
a failure of the level
switches
associated
with the
pumps.
The licensee
reviewed
trend
data
and
determined
that existing switches
had
a history of
unreliability.
The licensee
issued
DCN H3916 to replace
the
pump level switches.
The inspector verified that all changes
associated
with this
DCN were complete.
(CLOSED)
LER 296/90-04 Rev.l,
Unplanned
Engineered
Safety
Feature
Actuation.
This event occurred in connection with the anticipated
deenergization
of the
3B
bus occurring during the October 20,
1990 transfer of
the
3B 480V
RMOV board to its alternate
supply.
The deenergization
of the
3B
bus
was
an expected
occurrence
since at the time it was
on its alternate
supply transformer
and
a board transfer
under these
circumstances
results
in
a trip of
RPS circuit protectors
3CI anJ
3C2.
The
deenergized
bus
caused
anticipated
isolations
of
ventilation
systems
(PCIS
Group
6)
and
the
outboard
RWCU system
isolation valves
(PCIS Group').
However, during verification of the
expected
isolations,
the
licensee
noticed
that
RWCU valve
3-FCV-69-1, inboard isolation valve,
had also closed.
The closure of
this valve was not anticipated
in association
with the deenergization
of
bus
3B.
Further investigation
revealed
that the valve
had
closed
due to
a blown fuse
(16A-F60C) in conjunction with the
3B
bus deenergization.
The blown fuse
was
caused
by a coil failure on
relay l6A-K60C.
As
a result of annunciator
Fuse Failure"
31
being
sealed
in
due to various modifications
and
hold orders
in
effect at the time,
and
due to the design inability of this multiple
device monitoring annunciator
to re-alarm
when
more than
one fault
has occurred,
Operations
was
unaware of the existence
of the failed
fuse at the time of transfer of the
3B 480V
RMOV to,.its alternate
supply.
This 'inability of the
main control
room annunciator
to
"re-alarm"
was, specified
by the licensee
as
the root cause
of the
event.
The licensee
stated
that .this condition could not occur
on Unit 2
since
as
a result
of
CRDR
recommended
modifications
the
isolation logic is provided with a specific annunciator
in contrast
to the general
fuse failure alarm presently provided for Unit 3.
The
licensee's
immediate
corrective
action
was
to replace
fuse
and relay
The licensee's
long term corrective
action
is to install
reflash
capabilities
for annunciators
with
multiple inputs.
This program is currently being tracked
by the
CRDR
Group
as
HED 0113.
The licensee
has
scheduled
completion of this
long term corrective action for Units
1 and
3 prior to the startup of
each unit and for Unit 2 during the cycle
6 refueling outage.
The failure to report this event to the
NRC as
an unanticipated
actuation,
within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> of occurrence,
was cited
as
an apparent
violation of regulatory requirements
in IR 90-33
(VIO 90-33-01).
Based
on the inspector's
review of the licensee's
LER submittal
and
event
report
II-B-90-122,
in addition to discussions,
held with
various'icensee
personnel
associated
with this event,
the inspector
determined
that the licensee's
evaluation
and corrective action for
the event are adequate.
I'CLOSED)
Failure to Perform Surveillance
Instruction
Within Required
Periodicity
Places
Plant
Outside
the
Technical
Specifications.
This event originated
from the incorrect changing of the performance
date for 1-SI-4. 11.A.3, Monthly Functional
Test of
Non-Supervised'larm
Circuits
which
caused
a violation of the
allowable
TS
surveillance test performance
extension of 25 percent
and resulted in
the failure to provide appropriate
compensatory
actions for the
smoke
and
heat
detection
circuits
during
the
September
30,
1989
to
October 4,
1989 period.
Personnel
error is listed
as
the root cause
of the event.
'The
cognizant fire protection section engineer
entered
the wrong date for
the SI performance
completion resulting in no change
in the SI band
for the next scheduled
performance.
Subsequently,
without notifying
the
Work Control
personnel,
on
October
14,
1989
the
cognizant
engineer
changed
the
completion
date
on the
SI review form from
September
1, 1989,to August 23,
1989, in addition to maintaining in
32
his possession
the original copy of the SI for closure of open TDs.
A work control
technician
discovered
the
discrepancy
when
the
original
package
was
ultimately
received
for closure
and
transmittal
to permanent
records.
As immediate corrective action,
the licensee
reviewed approximately
.
70 fire protection
SI packages
(approximately half of which had been
processed
by the involved 'FP cognizant engineer)
to determine if any
other inconsistencies
were noted
between
logged performance
date
and
other information in the SI.
No inconsistencies
or inadequacies
were
found.
TVA is
unable
to take
any personnel
action since
the involved
cognizant engineer is
no longer employed at
BFNP.
At the
time of the event,
PMI 17.1,
Conduct of Testing,
did not
contain
the
necessary
controls
to prevent this type of event
from
occurring.
As part of the corrective action,
the licensee
issued
procedure
PNI 17.12, Surveillance
Program Implementation.
Step 4.8.6
of this procedure
requires, that tests with TDs be promptly reviewed,
'igned
and submitted to Work Control;
Step 4.8.8 requires
the Work
Control section to verify that the SI performance
date is consistent
with information on the SI Review Form. prior to entering data in the
scheduling
system;
and
Step 4.8.9 stipulates
that the
Work Control
section is to be notified 'immediately, if, during the review cycle,
any information
on
an SI is changed that could have any impact on SI
scheduling
or work. control.
Although the inspector
determined that the corrective actions .taken
for this specific event,
were
adequate
to satisfy the identified
concerns,
an
assessment
of the
adequacy
of corrective
actions
associated
with broader
concerns
over inadequacies
in the overall
surveillance
program (of which this event
represents
an additional
example)
documented
in
IR 89-43, will be
performed
during
the
followup of the licensee's
response
to VIO 89-43-01.
(CLOSED)
Unplanned
ESF Actuation Caused
by Personnel
Error.
On September
16,
1990
an unplanned
ESF actuation
occurred
when
1D
autostarted
after receiving
a low reactor water level
ECCS initiation
signal.
The
to level indicating switches
2-LIS-3-58C
and
2-LIS-3-58D were
undergoing
Raychem Splicing
when
a
DG autostart
signal
came in causing
the
DG to start.
The splicing activities were
performed
while
the
associated
circuits
were
thought
to
be
deenergized.
The
Impact Evaluation
Sheet
associated
with the work
orders
being
implemented,
had incorrectly specified
the work as
related with Hold Order 2-90-571 listed.
The actual circuits were
ECCS related
instruments
rather
than
RPS.
The licensee's
incident
investigation
(II-B-90-103) concluded that personnel
involved in the
event failed to recognize
or identify the level instruments
as being
0
33
part of the
ECCS Logic instead of the
RPS -Logic.
These
personnel
errors
allowed the work activities to be incorrectly released
under
the belief that
the
work
was within the
bounds
of Hold Order
2-090-571.
The
licensee
has
reviewed
the
event with personnel
responsible
for evaluating
the
impact of work activities to stress
the
importance
of properly
and thoroughly completing
the required
impact evaluation sheet. for each work activity.
Since
various
aspects
associated
with this
event
represented
noncomplia'nce
with regulatory
requirements
and
were
so cited in
VIO 90-29-01,
an assessment
of the adequacy of implementation of any
additional
corrective
action will be
performed
during
the
NRC
inspector's
followup of the licensee's
response
to the violation.
15.
Part
21 Reports
a
~
b.
(CLOSED) Part
21
260/P21
89-18,
SMB Actuators
Found to
Have Melamine Torque
Switches
That
Undergo
Post
Mold Shrinkage
and
Cause
Cam Binding.
In
a letter
dated
November 3, 1988, the licensee
was
informed by the
vendor (Limitorque Corporation) that Melamine torque switch failures
at
another
nuclear
facility represented
a
common
mode failure
resulting from post mold shrinkage of Melamine
and that pursuant to
the requirements
of 10CFR21,
the licensee
was
being notified of a
defect
in
supplied
SMB-000
and
SMB-00
actuators.
Limitorque'ecommended
that all affected
torque switches
be replaced
with an environmentally qualified Fiberite torque switch.
CARR
BFP881117
was initiated
on
December
21,
1988
to track
the
identification and replacement of affected torque switches.
Revision
3 to
CARR BFP881117'ists
the affected
Unit
2 valves
and
the
maintenance
requests
under which the torque switches
were replaced.
This Part
21 is closed for Unit 2.
(CLOSED) Part
21 259,260,296/P21
90-04,
Rosemount
Precision
Resistors
in Model
710 Trip/Calibration Units
and
Model
414
E/F Resistance
Bridges
May Exhibit Premature
Degradation
Under Certain Combinations
of Humidity, Power,
and Duration.
Notification was
provided to the licensee
on October
10,
1989,
and
December
7,
1989,
by Rosemount,
Inc. that
a number of Rosemount
Model
710 Trip/Calibration Units and
Model
414 E/F Resistance
Bridges
may
exhibit premature
longterm degradation
of a component
(precision
resistors)
under certain combinations of humidity, temperature,
power
and duration.
Rosemount
included in the
above referenced letters to TVA the serial
numbers of five affected
Model
710 Trip/Calibration units previously
shipped to Browns Ferry under purchase
order numbers
and
These
five units
were
located
in the licensee's
0
34
c ~
warehouse
and were returned
to Rosemount for repair on November '27,
1989
and
June
30,
1990.
No Model
414 E/F Resistance
Bridges were
procured
by the licensee
during the affected
timeframe.
Although
other Model
710 units have
been
purchased
from Rosemount
in the past,
the licensee's
investigation
concluded that only the above five units
were within the
Rosemount
indicated 'production interval affected
by
the deficiency.
(CLOSED) Part
21 259,260,296/P21
90-05, Malfunction of Borg-Warner
Bolted Bonnet
Check Valves caused
by Failure of the Swing Arm.
This Part
21 and'he
associated
NRC IN 90-03 notified the licensee of.
the
potential
malfunctioning of Borg-Warner
bolted
check
valves
caused
by failure of the
swing arm.
The licensee
reviewed
their records
and the equipment at Browns Ferry and -dete'rmined that
there
are
no
Borg-Warner
swing check valves at
Browns
Ferry in a
safety related application.
The inspector
reviewed
a list of all
applicable
swing
check
valves
in safety
related
applications
at
Browns Ferry provided
by TVA's cognizant
NE-Materials engineer
and
confirmed
the
absence
of Borg-Warner
valves
from the list.
The
inspector
also reviewed the licensee's
closure 'package for this item
and considers
the, action taken to be adequate.
I
16.
Action on Previous
Inspection
Findings
(92701,
92702)
a.
(CLOSED) IFI 50-259,
260,
296/90-20-03,
RPS Circuit Protector Trip
Level Setpoints
and Surveillance.
This
item
was
reviewed
in
IR 90-33.
At that time the remaining
issues
for closure
were
issuance
of revised
TS to change
the circuit
protector
relay
setpoints
and
modifications
to
implement
the
setpoints
in Unit 2.
During this reporting period,
the licensee
received
the
amended
TS and modified the circuit protectors
with the
new setpoints.
No further deficiencies
or concerns
were identified
for this item.
" b.
(CLOSED)
URI 259, 260, 296/87-22-01,
Inadequate
Corrective Action for
Violation of Requirements.
This item was originally identified in IR 85-07
and
was
opened
to
track the adequacy of TVA's actions
taken with regard to allegations
concerning
Category
I pipe supports.
Following= the completion of
TVA's investigation of these
employee
concerns,
IR 87-22
was issued,
which summarized
the
NRC's conclusions
following a review of. the
report.
The licensee's
corrective actions
were considered
inadequate
in that there
was
a lack of timeliness
in taking the actions
due to
the personnel
turnover and the reorganizations
that were taking place
during the
1985 to 1987 time frame.
The licensee
responded
to the
IR
87-22
concerns
on
October 28,
1987.
The
corrective
actions
identified in this response
were reviewed
by the inspector
and were
found to
be satisfactory. It should
be
noted that the specific
o
35
c ~
programs
described
in the licensee's
response
have
been
modified
s'ince
the letter
was issued.
The inspector
reviewed the equivalent
programs
that
are
now in place that provide'he
same
corrective
actions.
Findings were acceptable.
(CLOSED)
URI 259,
260, 296/87-22-02,
Inadequate
Response
to Employee
Concern
Program
Recommendation.
This
item
was
opened
to track the licensee's
corrective
actions
concerning
an
program
recommendation
which
was
incorrectly
assigned
to the
wrong unit.
During
a review of the corrective
actions
concerning
the piping supports, it was noted that the ac'tion
had
been
assigned
to Unit 3 vice Unit
1 as it should
have
been.
The
licensee initiated corrective action to also analyze the condition on
Unit 1.
On
November.
10,
1987,
NE
issued
the results
of their
analysis
on Unit
1 piping supports
and
determined
that the piping
in question
was not stressed
beyond the code allowable by the absence
of ,temporary
supports.
Additionally,
NE
determined
that
the
affected
pipe supports
had
not
been
degraded
as
a result of the
redistribution.
The inspector
reviewed the results of this evaluation
and
had
no further questions.
d.
(CLOSED)
URI 260/89-18-03,
Adequacy of Procedures.
This
URI concerned
the inadequacy of the procedure
screening
review
process.
The
inadequate
implementation
of the
procedure
review
process
had resulted
in either unacceptable
or nonexisting
10 CFR 50.59 evaluations.
The
NRC requested
that the licensee's
evaluation
of this
concern
address
why the licensee
believed that many of the
reviews
performed
apparently
failed;
what
changes
would
be
implemented
to
eliminate
the
procedure
inadequacy;
and
what
indications
are
there that the corrective actions
has
improved the
screening
review process.
Several
meetings
have
taken
place
between
the
NRC and the licensee
to discuss
the inadequacies
of BFNP procedures.
The licensee
issued
CARR
BFA890175902,,
as
the
result
of
a
procedural
audit
(No.
SSA89902), to address
problems identified.
The inspector
reviewed
the URI's closure
package
including the
CARR
and
subsequent
NRC inspection
reports.
The
CARR provided
cause
analysis,
corrective
actions,
and
preventive
actions.
Detailed
information was provided in each
area of the
CARR.
Subsequence
NRC
inspection
reports
indicate that
several
10 CFR 50.59 evaluations
were redone
and determine to be adequate.
Further evaluation of the
adequacy
of
10
CFR 50-59 evaluations will be addressed
during the
follow-up of VIO 89-17-01; therefore, this
URI is closed.
e.
(CLOSED)
URI 259,
260,
296/90-33-03,
Failure to Control
Design
in
Allowing Unqualified Cable Installation.
0
0
36
g
An inspector
identified that nonqualified electrical
cables
were
installed
in systems
important'o safety.
This involved
DCNs/ECNs
W10017A
and
W14589,
as well
as
AAFDCNs F15025
and
F15101.
After
additional
review, this
item
was
determined
to
be
a violation,
VIO 259,
260,
296/90-40-04,
Failure to
Implement
Design
Control
Measures.
(CLOSED) VIO 259, 260, 296/90-15-01,
DG Restart Test Falsification.
The
licensee
had identified that
a
TVA contractor
employee
had
falsified test records for a portion of restart test,
2-BFN-RTP-082.
During the inspector's
review of the circumstances
that led to this
violation the inspector
determined
that,the
licensee's
corrective
actions
were adequate
and complete.
No response
by the licensee
had
been required for this violation.
This item is closed.
(CLOSED)
259,
260/90-25-04,
Failure
to Protect
Emergency
Equipment.
This violation involved
a downpour of water onto emergency
equipment
from
an
hole
bored in the roof of the
emergency
diesel
generator
building.
The hole
was
a result of modifications work in progress
and
had not
been
sealed
to avoid water
damage until the work was
completed
as required
by the workpl'an.
The licensee
has corrected
the condition by closing the penetrations
in the
diesel
building roof.'n addition
the roof drains
were
cleaned
and verified clear.
No further corrective
steps
are to be
performed.
Based
on the licensee's
corrective actions, this item is
, closed.
17.
Bulletins
a
~
(CLOSED) 260/BU-80-06,
Engineered
Safety Feature
Reset Controls.
This
BU was
reviewed, in IR 87-42.
-The only remaining
open item was
completion of a modification to prevent energizing the TIP withdrawal
enable circuit upon reset of containment isolation.
The licensee,
by
the letter of November
11,
1990, notified the
NRC that the
BU was
completed.
The inspector
reviewed the licensee's
closure
package for
this item.
The modification was completed
on
PO 469.
The
installed
a pushbutton
switch, seal-in relay,
and associated
wiring.
PMT-BF-094-003
was
performed
on
October 29,
1990,
to verify the
modification
was installed correctly.
The inspector
discussed
this
modification with plant operators
in the Unit 2 Control
Room
on
January
12,
1991.
The operators
were knowledgeable of the modifica-
tion
and
purpose
of the
reset
switch.
TIP Isolation
Reset,
2-HS-94-70-52
is
located
on
panel
2-9-13,
control
and
modification cabinet.
This modification
was
completed for Unit 2
only.
37
(CLOSED)
260/BU-83-08,
Electrical
Circuit
Breakers
With
an
Undervoltage Trip Feature
in Use in Safety-Related
Applications Other
Than. the Reactor Trip System.
'VA
responded
to the
BU 83-08 by letter March 29,
1984.
None of the
480V type
AK-2 circuit breakers
referenced
were identified in
safety-related
systems.
GE molded
case circuit breakers
with an
undervoltage trip function were utilized on the output of the
sets.
The undervoltage
trips of these
breakers
were disabled
and
circuit protectors
were installed
between
the
normal
and alternate
power supplies
and
the battery
board supplying the
MG sets.
The
inspector
reviewed
completed
P0422 for the modification.
TS
number
286 to revise
the
RPS circuit protection trip level setpoints
was
approved
by the
NRC
in January
1991.
Completion of the
modification
and review of the
RPS circuit protectors
resolved
the
bulletin issues.
(CLOSED)
260/BU-89-02,
Stress
Corrosion
Cracking of High-hardness
Type 410 Stainless, Steel
Internal
Preloaded
Bolting in Anchor Darling
Model
S350W Swing Check Valves or Valves of Similar Design.
This bulletin was
issued
by the
NRC
on July 19,
1989, to request
licensees
to identify, disassemble
and inspect certain types of swing
,check
valves
which
may contain
Type
410 stainless
steel
bolting
material.
A possible
generic
concern
had
been identified based
on
the recent discovery of broken bolts of this type at other licensee
facilities.
The licensee
responded
to the
NRC on January
17,
1990, to document
their review of this- concern.
In that letter the licensee
stated
that
a thorough
review of all safety-related
had
been
performed
and
Browns
Ferry did not
have
any
check
valves
in
safety-related
systems within the=- scope of NRC Bulletin 89-02.
The
inspector
reviewed
the
above
licensee
response
along with other
documentation
provided
by the licensee
associated
with the licensee's
review of this issue.
The inspector
determined
that the licensee's
review was
based
on approximately
1400 safety-related
of which approximately
900 were not swing type check valves.
Since
check valves of these
design
would not contain hinge block preloaded
bolting, check
valves of such
design
were excluded
from considera-
tion.
A list identifying the
remaining
approximately
500
check
valves
was generated
which included
each valve's function, location,
Mark Number, manufacture,
model
number
and other related information.
This list was
then
reviewed
by the licensee's
Nuclear
Engineering
Department for applicability.
The inspector
held discussions
with
Materials
Engineering
personnel
and
determined
that the review was
based
on information available
from the g-List, plant maintenance
valve
database,
applicable
drawings,
manufacturers
information,
purchase
specifications,
and bill of materials.
Based
on that
review, the licensee
determined that
no check valves
were at
Browns
Ferry that were applicable to this bulletin.
0
38
Subsequent
to
the
above
licensee
response,
apparent
discrepancy
between
vendor information and 'the original
GE purchase
specification
was
discovered
which identified
two additional
check
valves
which
could contain the incorrect bolting material.
These valves
were four
inch and eight inch check valves manufactured
by Velan Valve Company.
Although the
GE purchase
specification specified that 410 stainless
material shall not be used for valve internal fasteners,
drawings
and
the bill of materials for the valves
in question
indicated that 410
stainless
could
have
been
used.
The licensee
disassembled
both
valves
in Unit 2, replaced
the bolting with Grade
B8 material,
and
performed
chemical
analysi's
on the older bolts.
The bolting removed
from the valves
was determined
to be type
B8 and type
BBM material.
Based
on the above review the inspector determined that the licensee
has adequately
addressed
the concern identified,in this bulletin.
18.
Exit Interview (30703)
The inspection
scope
and findings were summarized
on January
22,
1991 with
those
persons
indicated in paragraph
1 above.
The inspectors
described
the areas
inspected
and discussed
in detail the inspection findings listed
below.,
The licensee
did not identify as proprietary any of the material
provided to or reviewed
by the inspectors
during this inspection.
The licensee
stated
that the
examples
used in the violation wer'e not an
indication of a programmatic
problem with the design control
process
but
were instances
of personnel
error or failure to follow procedure.
Item Number
259, 260, 296/90-40-01
260/90-40-02
260/90-40-03
Descri tion and Reference
URI,
Deficiencies
Identified
During
Integrated
ESF Testing,
paragraph
2.
NCV, Improper
Rigging from Safety
Related
Structure,
paragraph
3.
NCV,
Failure
to
Maintain
Configuration
Control of DG Air Starting System,
paragraph
4,
259, 260, 296/90-40-04
260/90-40-05
Violation,
Failure
to
Implement
Design
Control Measures,
paragraph
5.
NCV, Modifications, Wiring Error,
paragraph
2.
260/90-40-06
URI,
SPDS Unreliability and
Human
Factor
Concerns,
paragraph
10.
. Licensee
management
was
informed that
7 LERs,
3 Part
21 Reports, I IFI, 4
URIs,
2 VIOs, and
3
BUs were closed.
39
AOI
ARI ~-
ASOS
BFNP
CA
CAQR
CATD
CFR
CRDR
DBVP
DCN
DCRDR
FDCN
GDC
GEMAC
- GOI
HED
HQ
IFI
Air Handling Unit
As Low As Reasonably
Achievable
Abnormal Operating Instruction
Average
Power Range Monitor
Alternate
Rod Injection
Area Radiation Monitors
American Society of Mechanical
Engineers
Assistant Shift Operations
Supervisor
Anticipated Transient Without Scram
Auxiliary Unit Operators
Browns Ferry Nuclear Plant
Boiling Water Reactor
Control Air
'ontainment Air Dilution
Continuous
Atmosphere Monitors
Condition Adverse to Quality Report
Corrective Action Tracking Document
Code of Federal
Regulations
Control
Room Design
Review
Control
Room Emergency Ventilation
Design Baseline Verification Program
Drywell Control Air
Design
Change Notice
Detailed Control
Room Design
Review
Diesel
Generator
Division of Nuclear Engineering
Engineering
Assurance
Emergency
Core Cooling Systems
Engineering
Change Notice
Employee
Concerns
Program
Emergency
Equipment Cooling Water
Electrical Maintenance
Instruction
Emergency Operating Instruction
Environmental Qualification
Engineered
Safety Feature
Flow Control Valve
Field Design
Change Notice
Fire Protection
Final Safety Analysis Report
General
Design Criteria
General
Electric/Manual
Automatic Controller
General
Operating Instructions
Hydraulic Control Unit
Human Engineering
Discrepancy
High Pressure
Fire Protection
Headquarters
Heating, Ventilation,
& Air Conditioning
Inspector
Followup Item
0,
40
IN
IR
JTG
KV
LCO
LER
LOP/LOCA
NEP
'RC
ORR
PMI
QDCN
SDSP
SPAE
TD
TI
TROI
TS
V
XE
Integrated
Leak Rate Testing
Information Notice
Institute of Nuclear
Power Operations
Inspection
Report
Intermediate
Range Monitor
Joint Test Group
Kilovolt
Limiting Condition for Operation
Licensee
Event Report
Loss of Power/Loss of Coolant Accident
Motor Operated
Valve
Non-Cited Violation
'uclear
Engineering'rocedure
Nuclear Regulatory
Commission
Operating Instruction
Operational
Readiness
Review
Primary Containment Isolation System
Preventive
Maintenance
Plant Manager Instruction
Post Maintenance/Modification Test
Problem Reporting
Document
Quality Assurance
Qual ity Control
Quality Design
Change Notice
Reactor Building Closed Cooling Water
Residual
Heat
Removal
Residual
Heat
Removal Service Water
Reactor Protection
System
Restart Test
Program
Standby
Gas Treatment
System
Site Director's Standard
Practice
Surveillance Instruction
Service Information Letter
Pump
System Plant Acceptance
Evaluation
Safety Parameter
Display System
System Pre-Operational
Checklist
Test Deficiency
,
Technical
Instruction
Tracking and Reporting of Open
Items
Technical Specification
Valley Authority
Unresolved
Item
Volt
Violation
Work Order
Work Request
0