ML18033A939
| ML18033A939 | |
| Person / Time | |
|---|---|
| Site: | Browns Ferry |
| Issue date: | 08/07/1989 |
| From: | Carpenter D, Little W, Patterson C NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML18033A937 | List: |
| References | |
| 50-259-89-27, 50-260-89-27, 50-296-89-27, IEB-87-001, IEB-87-1, IEC-76-03, IEC-76-3, IEIN-82-51, IEIN-86-044, IEIN-86-44, IEIN-88-079, IEIN-88-79, NUDOCS 8909080294 | |
| Download: ML18033A939 (35) | |
See also: IR 05000259/1989027
Text
gy,R RFCI
ci
0
Cy
I
ClO
I
Op
+~
+0
+~*y4
UNITEDSTATES
NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETTASTREET, N.W.
ATLANTA,GEORGIA 30323
Report Nos.:
50-259/89-27,
50-260/89-27,
and 50-296/89-27
Licensee:
Valley Authority
6N 38A Lookout Place
1101 Market Street
Chattanooga,
TN
37402-2801
Docket Nos.:
50-259,
50-260,
and 50-296
License Nos.:
and
Facility Name:
Browns Ferry Units 1, 2,
and
3
Inspection at Browns Ferry Site near Decatur,
Inspection
Conducted:
June
16
uly 15,
1989
Inspector.
R.
Car
en
,
NRG
S te Manager
Da
e
igned
A.
Pa te
n,
NRC Restart Coordinator-
Da
gned
Accomp nied by:
E. Chri stnot,
Resident
Inspector
W. Bearden,
Resident
Inspector
K. Ivey, Resident
Inspector
o nso
, Pr
ect Engineer
Approved by:
W.
S.
Li tie
Section Chief,
Inspect>on
Programs,
TVA Projects Division
Da
e
igned
SUMMARY
Scope:
This routine resident
inspection
included the areas of maintenance
observation,
followup
of
NRC
bulletins,
operational
safety
verification, reportable
occurrences,
action
on previous
inspection
findings,
and site management
and organization.
Results:
The licensee
continues
to have difficulty meeting
TS requirements.
This is partially due to the divisional
outages
in progress
which
maintain the minimum TS required
systems
RHR configuration
control
continues
to
be
a problem.
A violation was identified for
not
maintaining
the
TS
required
number
of
Loops,
paragraph
4.
Examples
were
found where
the licensee
has not been conservative
in
submitting
LERs within 30 days of the discovery of the event per
The
approach
has
been
to fully analyze
an
event'+j()/LIVE
>2>4 ~;:~080/
I='Dt i
tlfIC'LK
O"OOOO
I;!
F Ei('
prior to submitting.a
LER although indication exists of
a problem
when the event is discovered.
A violation with three
examples
for
failure to submit
a
LER within 30 days of the discovery of the event
was identified, paragraph
6.
REPORT DETAILS
Persons
Contacted
Licensee
Employees
0. Zeringue, Site Director
~G. Campbell,
Plant Manager
R. Smith, Project Engineer
- J. Hutton, Operations
Superintendent
"A. Sorrell, Maintenance
Superintendent
- D. Nims, Technical
Services
Supervisor
- G. Turner, Site guality Assurance
Manager
- P. Carier, Site Licensing Manager
"W. Ivey, Acting Compliance Supervisor
J.
Corey, Site Radiological
Control Superintendent
R. Tuttle, Site Security Manager
Other
licensee
employees
or contractors
contacted
included
licensed
reactor operators,
auxiliary operators,
craftsmen,
technicians,
and public
safety officers;
and quality assurance,
design,
and engineering
personnel.
NRC Resident Staff
J
- D. Carpenter,
Site Manager
- C. Patterson,
Restart Coordinator
E. Christnot,
Resident
Inspector
- M. Bearden,
Resident
Inspector
- K. Ivey, Resident
Inspector
- Attended exit interview on July 14,
1989
Acronyms used throughout this report are listed in the last paragraph.
Maintenance
Observation
(62703)
Plant
maintenance
activities
of
selected
safety-related
systems
and
components
were observed/reviewed
to ascertain
that they were conducted
in
accordance
with requirements'he
.following items were considered
during
. this review:
the limiting conditions for operations
were met; activities
were
accomplished
using
approved
procedures;
functional
testing
and/or
calibrations
were
performed prior to returning
components
or
system
to
service;
quality
control
records
were
maintained;
activities
were
accomplished
by qualified
personnel;
parts
and
materials
used
were
properly certified;
proper
tagout clearance
procedures
were
adhered
to;
Technical
Specification
adherence
and
radiological
controls
were
implemented
as requi red.
Maintenance
requests
were reviewed to determine
the status of outstanding
jobs and to assure
that priority was assigned
to safety-related
equipment
maintenance
which might affect plant safety.
The inspectors
observed
the
maintenance activities listed below. during this report period:
a.
Maintenance
of Diesel Generators
The
NRC inspector
reviewed
ongoing
maintenance
activities involved
with the Unit 1/2 "B" DG. These activities
were initiated
by eight
and
one minor modification.
The
MRs included activities
such
as
replacement
of stripped bolts,
and
high potential
testing of
output
electrical
cables,
governor
booster
pump
check
and
crankcase
pressure
switch
retorquing.
The
minor
modification
involved the installation of
a thermowell
and temperature
indicator
in
the
'DG
cooling
system
and
is
discussed
in
more
detail
in
paragraph 5.b.'he
review of the
MRs indicated that the work to be
done
was clearly stated
and that applicable
plant
procedures
were
referenced
such
as
SDSP
6.9,
"Cleanliness
of Fluid System",
and
PNI-6. 10,
"Maintenance Material Control."
The
NRC inspector
observed
the activities
in the field for the
following NRs:
(1)
MR A898156
This
MR required the meggering
and high potential testing of the
DG output electrical
cables
from the generator
to the
"B" 4160V
shutdown
board.
The activities
were
governed
by
procedure
SEMI-65,
"Special
and
DC High Potential
(20 KV),Test."
The responsibility for the overall
work was
assigned
to the
site
modifications
group.
The
actual
performance
of
the
meggering
and
high
poting,
using
appropriate
M&TE,
was
completed
by the
TSC group.
All personnel
were familiar with
thei r particular job assignments;
and the testing
was
successful.'2)
MR A874405
This
.MR required
that
the
crankcase
pressure
switch
be
checked
and that
the bolts
holding
the
switch in place
be
adequately
torqued.
This activity was
governed
by procedures
CCI-O-PS-82-038,
"Emergency Diesel
Generator
Crankcase
Pressure
Switch
Calibration",
and
SIMI
301.4,
"Special
Instruction
Troubleshooting
Maintenance
Instruction",
and
required
the
participation of
a
gC inspector.
All personnel
were
fami 1'iar
with
the
procedures
and
showed
knowledge
in their
work
assignments.
(3)
NR A874587
This
required
the
calibration
of
a
pressure
switch
on
the
starting air
system
air
compressor
for the
DG starting air
banks.
This activity
was
governed
by procedure
SCI
202.6,
"Standard
Calibration Instruction
For Mercoid Control
Series
D
Pressure
Switches."
The Heise
pressure
indicator
used
by the
technicians
was within its calibration
period.
The
personnel
appeared
to be knowledgeable
in the job assignments.
b.
Fuse
Replacement
The
licensee
reported
an
unplanned
ESF actuation
to the
NRC per
on July
2,
1989
when Unit
2 received
a
containment
isolation
actuation
from the
reactor
and
refuel
zone
radiation
monitors.
This
unexpected
actuation
was
caused
by
the
deenergization
of. the monitor power supplies during fuse replacement
activities.
An
improperly
placed
jumper
which
was
intended
to
prevent
an
actuation
resulted
in the
loss of power to the
power
supplies.
Although the licensee
is still investigating the
cause
of
the event,
the
NRC inspector
was informed that the fuse replacement
activities performed in accordance
with MI-92 failed to insuqe that
the
jumper
was
properly
placed
prior to the
fuse
removals
This
occurred
notwithstanding
the
requirement
for
two
party
performance.
The
NRC
inspector
was
informed
that
a
possible
deficient
maintenance
instruction
and/or
drawings
which
did
not
explicitly show the ci rcuits could
have contributed to the failure.
Inspector
Followup Item 260/89-27-01,
Fuse
Replacement
Jumpers, will
be opened
pending further review of this event.
Followup of NRC Bulletins (92701)
(CLOSED) IEB 87-01, Thinning of Pipe Walls In Nuclear
Power Plants.
On August
31,
1988 the
NRC issued its Safety
Evaluation
Report
on the
response
of Browns Ferry Nuclear Plant to
NRC Bulletin 87-01, Thinning of
Pipe Walls in Nuclear
Power Plants
226, 227).
The
NRC staff
reviewed TVA's past activities and plans for this topic and found them to
be
programmatically
acceptable.
The
inspector
reviewed
plant
procedures
that
were
developed
in
response
to the
IEB for monitoring
susceptible
areas
of corrosion/erosion
and the trending of results.
The
procedures
2-TI-140,
"Pipe Wall Degradation
Monitoring Program for Dual
Phase
Systems,"
and 2-TI-148, "Pipe Wall Degradation
Monitoring Program for
Single
Phase
Fluid Systems",
were found to be acceptable.
This bulletin is
considered
closed for Unit 2 only.
4.
Operational
Safety Verification (71707)
The
inspectors
were
kept
informed of the overall plant status
and
any
significant safety matters related to plant operations.
Daily discussions
were held with plant management
and various
members of 'the plant operating
staff.
The
inspectors
made
routine visits to the
control
rooms.
Inspection
observations
included
instrument
readings,
setpoints
and
recordings;
status
of operating
systems;
status
and alignments
of emergency
standby
systems;
onsite
and
offsite
emergency
power
sources
available
for
automatic
operation;
purpose
of temporary
tags
on equipment controls
and
switches;
alarm status;
adherence
to procedures;
adherence
to
limiting conditions
for
operations;
nuclear
instrument
operability;
temporary alterations
in effect; daily journals
and logs;
stack monitor
recorder traces;
and control
room manning.
This inspection activity also
included
numerous
informal discussions
with operators
and supervisors.
General
plant tours
were
conducted.
portions of the turbine buildings,
each reactor building,
and general
plant areas
were visited.
Observations
included
valve
positions
and
system
alignment;
and
hanger
conditions;
containment
isolation
alignments;
instrument
readings;
housekeeping;-
proper
power supply
and breaker
alignments;
radiation area
controls;
tag controls
on
equipment;
work activities
in progress;
and
radiation
protection
controls.
Informal
discussions
were
held
with
selected
plant personnel
in their functional areas
during these tours.
The
NRC
inspectors
reviewed
the
following issues
during this report
period:
a
~
A fai lure to maintain
TS requirements
for operabl'e
RHR Loops
The licensee notified the
NRC per
10 CFR 50 '2 at 10:33 a.m.
on June
23,, 1989 of .a condition which occurred
due to the licensee's
failure
to properly perform required
surveillance
testing
on
Loop II of the
Unit 2
RHR System. on June
18,
1989,
when the
RHR Loop II was declared
On May 22,
1989, operations
personnel
had requested
that the due date"
for 2-SI-3.2.2,
"Valves Cycled During
Cold
Shutdown",
be
extended
from its
scheduled
due
date
of
- May
26,
1989,
to its
maximum
allowable extension
due date of June
17,
1989.
This extension
had
been
approved
by plant
management
and
had
been considered
necessary
to allow a procedure
revision to reflect color changes
in the valve
and disc position indicating lights resulting
from a recent control
room
design
review.
On
June
8,
portions
of
2-SI-3 '.2
we'e
performed.
This
performance
included testing
the
RHR and
Core
Spray primary containment
inboard
as
directed
by the
ASME Section
XI system
engineer.
This partial
was
completed.
However,
Test
Discrepancy
¹2 identified that
in
the
drywell
prevented
installation
of
hoses
necessary
to test
the
Loop II testable
check
valve,
2-FCV-74-68.
After contacting
the
Section
XI
system
engineer
the
decision
not to test
these
valves
was
made
and the surveillance
was dispositioned
by use of
TD
¹2 for tracking the'teps
applicable
to testing
of this valve.
Since at this point Loop I of the
RHR system
was being maintained in
an operable
status,
the requirements
of TS 3.5.B.9 were satisfied.
Operations,
personnel
subsequently
declared
Loop II of the
system
on
June
18,
1989
based
on
performance
of
2-SI-4.5..B. l.d;
however
the
Loop
II
testable
check
valve,
2-FCV-74-68,
was inoperable
because
the surveillance
band,
including
the allowable extension for testing,
had expired at midnight on June
17,
1989.
The required
ASME Section
XI testing
was not performed
on
2-FCV-74-68 until June
22,
1989.
Meanwhile the redundant
loop of the
Unit 2
RHR System
was
made inoperable
on June
18,
1989, for scheduled
Division I outage activities.
This resulted
in both
loops of
being inoperable for the period of June
18-22,
1989,
and could
have
prevented
the Unit 2
RHR system
from maintaining reactor
vessel
level
during an inadvertent draining of the
RPV.
TS 3.5.B.9 requires
that
at least
one
RHR loop with two pumps or two loops with one
pump per
loop be operable
when the reactor vessel
pressure
is atmospheric
and
irradiated fuel is in the reactor vessel.
At the time of the event,
Unit 2 was in cold shutdown with irradiated fuel in the vessel.
The
vessel
was
in the
flooded
up condition with the
fuel
pool
gates
installed.
The failure to satisfy.
TS requirements
is identified
as
Violation 260/89-27-02.
This
RHR configuration control
problem is
similar to the violation which was identified on May 25,
1989,
where
TS 3.5.B.9 for the
Unit
2
system
was
not satisfied
due
to
inadequate
post modification testing
and violation 260/89-20-01
was
issued for the licensee failure to meet
TS requirements
for operable
.
RHR pumps.
Turbine Building Spills
During this reporting period,
two separate
eve'nts
occurred resulting
in large
amounts of non-contaminated
water spilling into the Turbine
, Building.
On June
26,
1989, at approximately 9:00 p.m.,
a portion of the Unit
1
area
of
the
turbine
building
experienced
excessive
overflow of
uncontaminated
water spilling
from
an
opening
in the
Raw Cooling
Water
piping
for
the
Unit
1
Generator
Cooling
Heat
Exchangers.
The even't occurred
due to the inadvertent closure of the
1A gate
in the Circulating Water System which caused
an increase
in
the static
head
in the
CCW piping
and resultant
increase
in water
level in the affected portion of the
RCW system.
Water subsequently
spilled
out of the
RCW
system
which was
open
for maintenance,
flooding
a portion of the turbine building
and electrical
shop.
The
licensee
has not determined
the cause for the inadvertent
closure of
the
1A CCW gate.
On June
28, at approximately ll:30 a.m.,
a similar event
occurred
when
excessive
water
overflowed into
the
Unit
2
condensor
room
during
performance
of
an
operating
instruction
checklist.
This
event
appears
to
have
occurred
due
to
personnel
error
during
restoration
of
several
valves
to their
normal
configuration
and
possibility also
due to 'an inadequate
equipment clearance
associated
with the Unit 2 condensor
water box.
The licensee
is continuing to evaluate
the
causes
for both events.
Although neither spill resulted
in either
a radiological
problem
or
an uncontrolled release
and the licensee
has determined that the two
events
are not reportable,
the
NRC inspectors
are concerned that
such
'events
are indicators of poor control of work and work practices.
5.
Modifications (37700)
a.
DG Output Breaker Modification
During the
closeout
r evi ew of significant di scr epanci es identi fied
during
the
LOP/LOCA
series
of tests
the
NRC
inspector
noted
an
item involving
a modification installed
in the
logic for the
eight
output
breakers.
The
modification
required
the
installation of
a time delay relay in the logic of each breaker to
ensure that the eight output breakers
would not be locked out during
a loss of power followed immediately
by
a loss of coolant accident
signal.
The time delay relay is set at
3 seconds.
However,
due to
the
band
on -the relay,
the time could
be shorter
than
3
seconds.
The
licensee
has
determined
that
each
of the
DG output
breakers
recharging
motor must
be able to recharge
the breaker
in 2.5 seconds
or less.
At the
end of this reporting period,
the
NRC inspector
was
unable
to verify in what procedure this 2.5
second
requirement
is
located.
This item is identified
as
Inspector
Followup
Item 259,
260,
296/89-27-03,
Verification That
DG Output Breakers
Recharge
In
Less
Than 2.5
Seconds.
This item applies
to all
three
units
and
must
be addressed
prior to restart.
DG Temperature
Control Modification
The
NRC inspector
reviewed a'inor modification installed
on. the "B"
DG which involved the installation of
a thermowell
and
temperature
indicator
in
the
coolant
discharge
line
from the
DG to
the
temperature
control valve.
The work activity was initiated by
DCN
W1887
and
the activity
was
governed
by
Work
Package
1022-89.
The craft
and the
gC inspector
had the
WP at the job location
and
they
appeared
to
be
knowledgeable
in the
work required.
The
gC
.inspector
appeared
to verify that
the
minor
modification
was
installed
according
to
approved
methods.
Various
sign-offs
were
performed in an acceptable
manner.
C.
EECW Piping Modifications
The
NRC inspectors
reviewed selected activities associated
with three
major modifications to the
EECW and
RCW systems.
These modifications
are
identified
by
DCNs
H5120A,
H5121A
and
H5122A.
These
modifications
are part of the licensee's
corrective actions
due to
the discovery, of the
presence
of multiple discharge
flowpaths which
include vitrified clay piping in portions of the
RCW buried yard
piping.
Vitrified clay piping cannot
be seismically qualified
and
the
affected
lines
are
part of the
EECW discharge
flow path for
various safety related
components.
DCN H5120A reroutes
'the
EECW discharge
piping for the Unit 1/2
Control
Bay Chillers lA 5
1B from the Unit 1, Reactor Building
RCW discharge
line to the Unit
1
EECW discharge
piping which is
seismically qualified.
This modification was completed
on July
12,
1989.
I
DCN H5121A reroutes
the
EECW di scharge
piping for the
Unit
2
Shutdown
Board
Room Air Conditioning
Units
from the
Unit
2
Reactor
Bui ldin'g
RCW discharge
line to the Unit 2
EECW discharge
piping which is seismically qualified.
This modification
had
not started
as of July 14, being restrained
by need to maintain
Unit
2
while
Loop I
was inoperable
due to other work.
DCN H5122A reroutes
the
EECW discharge
piping for the Unit 3
Control
Bay Chi llers 3A from the Unit 3 Reactor
Building
RCW
discharge
line to the Unit
3
EECW discharge
piping which is
seismically qualified.
This modification was field complete
as
of July 14,
1989.
Although the specific activities associated
with the clay pipe issue
only involved work in the respective
unit portions of the
Reactor
Building, the modifications also
included
work to
remove
Secondary
Containment Isolation Check Valves,
1-67-556,
1-24-851,
2-67-598,
and
3-67-656
and
the
installation
of
spectacle
capable
of
isolating
EECW flow in each respective
10 inch
EECW system discharge
lines
located
in
the
RHRSW tunnels.
The
l,icensee
stated
that
although
the
check
valves
were originally installed
as
secondary
containment
boundaries
the
requirement
for these
valves
had
been
deleted
and the failure of these
check valves to open
when required
would inhibit EECW discharge
flow (constitute
an active failure which
violates
single failure criteria).
This additional
work
had
been
included within the
scope
of these
OCNs
due to the
need for common
work boundaries
and equipment clearances.
The spectacle
are
being
installed
only to
provide
a
means
to maintain
secondary
containment integrity during maintenance
to the
EECW System.
The
NRC inspectors
noted that for each of the above modifications
a
local
EECW stress
analysis
had been
performed to demonstrate
that the
new design
was within allowable stress
limits for the
EECW system
piping with
new piping
supports
and/or existing
supports
modified
based
on the revised
stress
analysis.
Additionally a pressure
drop
calculation
was
performed to demonstrate
that the
new design
would
not affect the ability of the
EECW discharge
lines to
meet
flow
requirements.
The
NRC inspectors
accompanied
the cognizant modification engineer
for, a walkdown of ongoing
and
planned
work associated
with these
modifications.
Craft
.personnel
and
responsible
foremen
had
appropriate
documentation
at the job location.
The
NRC inspectors
e
examined
several
of the
and
noted that the exterior of the
appeared
adequate
with
no
visible
flaws.
All
licensee
.
personnel
involved including the nuclear security officers displayed
a high level of technical
knowledge
and
a professional
attitude about
the job.
No violations were identified in modifications area.
Reportable
Occurrences
(92700)
a.
Review of Events for
LER Submission
The inspector
reviewed three
events
that
have
occurred
in the past
three
months for submission of a
LER per the requirements
of
The licensee
reported
two events
per
10 CFR 50.72 along with
a voluntary
LER for one event.
However, the licensee
did not submit
an
LER within
30
days
for any of the events.
The events
were
a
failure of the fuel
pool anti-siphon
RHR and
room
coolers
at less
than
design
flow, and
a single failure of the fire
pump lockout relay.
(1)
Failure of the fuel pool anti-siphon
On
September
16,
1988, plant personnel
conducted
a special test
of Unit '2
spent, fuel
pool anti-siphon
2-78-526
and 2-78-527,
and found the valves inoperable'n
ENS four-hour
report
of
an
unanalyzed
condition which could
have
prevented
the fulfillment of
a- safety function was
made to the
NRC under
10 CFR 50 '2.
This
item
was initially determined
to
be
reportable
per
on
September
22,
1988,
by
LRED
number
88-2-208.
Later,
on
October
5,
1988,
the
event
was
reclassified
as not reportable
because
a
low level
alarm would
warn of inadvertent
draining through
the
Thus,
an
LER was not submitted.
The logic for not reporting
the event did not meet
the intent
of
the
LER
requirements
in
In
Supplement
One,
guestion
7.6,
the
answer
given
states
that
a
system
is
expected
to
perform
without
operator
action.
Similarly, the Unit
were
found
stuck
open
on
June
14,
1989.
The
LRED
number
89-1-103
stated
that
no
new
reporting
requirements
were
found to apply
since
this
item
had been previously reported.
This indicated that this item was
still considered
reportable.
Subsquently,
the
same Unit 3 check
valves were also found stuck open.
(2)
Single failure of the fire pump lockout relay
During the design
baseline verification review
a concern
about
the ability of the plant to meet
the single failure criterion
was identified.
On March 22,
1989,
the licensee
made
an
report per
10 CFR 50.72 of an unanalyzed
condition where the A,
B,
and
C diesel
generators
could
be
overloaded
due
to
the
single failure of the lockout relay which prevents
the three
motor
driven fire
pumps
from starting
during
an
accident
condition.
An
LER was not submitted within 30 days after the
discovery
of the
event.
A voluntary
LER (50-259/89009)
was
submitted within on
May 31,
'1989.
The
LER stated
an analysis
indicated that the relay failure could result in the overload
of one
DG.
The loss of a
DG during
a design basis
event
was
an
analyzed
condition for the plant.
Stated
in the
LER was that
the
scenario
discussed
was thought to
be
bounding
but it was
more
economical
to install
an additional
lockout relay than to
perform detailed
analysis to ensure this was the bounding
case.
Since
the original
concern
was
not totally resolved within 30
days,
an
LER was required within 30 days of discovery of this
event.
RHR and
CS room coolers less
than design flow
On May'5,
1989
an flow verification test
performed
on the
2C
room cooler air
found
the
flow to
be
less
than
design.
Tests
were
performed
on
the
other
room coolers
and similar
results
were
obtained.
These
results
contradicted
results
obtained
in
March
1988 after
replacement
of the
cooler
fan
motors with
Eg motors.
A
summary
of the
results
obtained
follows,:
Cooler
Desi
n
March 1988
Ma
1989
2A RHR
2B
2C
2D
2A8(C
2BED
10,000
10,000
10,000
10,000
12,700
10,000
10,671
10,977
10,687
10,811
13,195
10,919
8,263
7,443
8,786
8,154
8,328',415
All values
are
given
in
cfm with
an uncertainty
of plus or
minus
10%.
The
licensee
determined
this
event
not
to
be
reportable
because it was
not
known if the condition existed
while the plant
was .operating.
No
LER was
submitted within '30
days after the discovery of the condition.
The
low flows were
reviewed
and
determined
acceptable
by the
licensee
for the
plant conditions.
The
inspector
reviewed
the
licensee's
Incident Investigation
Report
89-41
and
noted
the
apparent
cause
was
an
inadequate
procedure,
the basic
cause
was not used,
and the root cause
was
no
procedure.
There
was
no
procedure
for periodically
or
conditionally measuring
the air flow.
As
a result of the lack
of
a
procedure
and
no historical
data, it could
not
be
determined if the air flow had deteriorated
over time or if
there
was
a step
change
in air flow.
Due to the lack of data
this
item,
was
classified
as
not
reportable
until
more
information was available.
10
The inspector did not agree
with the licensee's
reportability
determination.
First,
the
room coolers
are
a
TS requirement.
The
TS state
that
the
associated
RHR or
CS- pumps
cannot
be
considered
unless
the
room coolers
are operable.
With
degraded ventilation flows for RHR and
CS, this condition could
have
lead to the'inability of all
low pressure
emergency
core
cooling
systems
to -function
as
designed.
Second,
sufficient
information
was
available
to
determine
that
the
conditions
could
have
occurred while the plant
was operating.
The
cause
of the flow difference
between
March
1988
and
May
1989 could
not be determined.
Test results
in May 1989, which indicated
a
low flow condition,
were, checked
and
rechecked.
The original
raw data
used in, the March 1988 test
was unavailable,
suggesting
a testing error as
a possible
cause.
In conclusion,
10 CFR 50.73 requires that
an
LER be submitted within
30 days after the discovery of an event or condition. that resulted
in
the
plant
being
outside
the
design
basis
and for any
event
or
condition that
alone
could
have
prevented
the fulfillment of the
safety
function of structures
or
systems
that
are
needed
to
(A)
shutdown
the reactor
and maintain it in
a
safe
shutdown condition;
(B)
remove
residual
heat;
(C) control
the
release
of radioactive,
material;
or
(D) mitigate
the
consequences
of
an, accident.
This
requirement
was not met for the three
examples
above
(A,B,C) and is
a violation of 10 CFR 50.73 for failure to submit
an
LER within 30
days.
(259,260,296/89-27-04)
Furthermore,
the
licensee
was
not
following
Plant
Managers
Instruction
PMI-15.4,
"Unique
Reporting
Requirements,"
Procedure
step
4. 1.4 stated
the following:
"It is
NRC policy and plant position "that when there is doubt
regarding
whether
to report
a situation
or not
the
licensee,
should
make
the
report.
This will ensure
conservatism
is
employed
when utilizing engineering
judgment
and
experience
to
determine
the significance of an event or condition."
The
inspector
acknowledges
that- the licensee
had identified these
problems
and in two cases
made
a four hour report per
b.
Review of LERs
The
Licensee
Event
Reports listed
below were
reviewed to determine
if the information provided'met
NRC requirements.
The determination
included
the verification of
compliance
with- TS
and
regulatory
requirements,
and
addressed
the
adequacy
of the event description,
the corrective
action
taken,
the
existence
of potential
generic
problems,
compliance
with reporting
requirements,
and the relative
safety significance 'of each
event.
Additional in-plant reviews
and
discussions
with plant personnel,
as appropriate,
were conducted
(CLOSEO)
Rev.
1,
Cooling Water Flow Blockage to
RHR Pump.
This
LER addressed
the significant loss of
EECW cooling water
flow thr u the
~ RHR
pump
seal
water
heat
exchangers
due to
a
buildup of clams
and sediment.
The system
was flushed until flows reached
acceptable
levels
and
the
system returned to service.
TVA stated
in
an internal
memorandum
dated Sept.
10,
1986 that
,GE determined that seal
water cooling was not normally required
for
pump operability.
Only under certain
extreme
emergency
operating
conditions
would
seal
damage
occur
after
extended
periods with high temperature
seal
water.
Therefore
the loss
of cooling water to'he
seal
water
heat
exchangers
was
not
considered
as
adversely
affecting
pump operability
and
system
operating instructions
were changed
accordingly.
The
NRC
inspector
reviewed
this
issue
with
emphasis
on
the conditions leading
up to the loss of cooling and actions to
prevent recurrence
as well as the impact
on
pump seals from'oss
of seal
water cooling.
Loss of cooling water to heat exchangers
from clam and sediment
fouling of open
systems
had been'addressed
in IEB 81-03
and
IEN
86-96.
The
NRC continues
to review this important topic through
proposed
requirements
for improving the reliability
of
open
cycle service
water systems
discussed
in Generic
Issue
51.
was found to have
a program of system testing to diagnose
system
flow degradation
resulting
from
such
fouling.
This
program
should predict
and prevent recurrence
of this condition.
The
licensee
position that
seal
water
coolers
were
not
required
for
pump
operability
'as
evaluated
by the inspector.
The
inspector
found that
the
seal
water
coolers
serve
2
functions:
1) to provide
a flow path
from the
pump discharge
to the
pump
seals
for lubrication water
and
2) to provide
for the
cooling
of
the
"lubrication" water.
The
TVA memo
discussed
earlier permits deleting
the
cooling function.
The
pump vendor
manual
and
GE specs still require the seal
faces to
be lubricated at all times by pumpage
or liquid from an outside
source.
Therefore
the
seal
water
side of the heat
exchanger
must
remain in-service for
pump operability.
Since
the
seal
water
side of the
Heat
Exchanger
cannot
be isolated
from the
pump,
the lubrication function cannot
be
bypassed.
This fact
combined
with the
minimum flow capability of the
RHR system
12
ensures 'ome
cooler
seal
water is
forced
through
the
system
which aides in cooling the
pump seals
under low flow conditions.
Therefore isolation of the cooling water
side of the seal
water
heat
exchanger
does
not negate
the lubrication function of the
system.
The
NRC inspector
reviewed
the
changes
to
RHR system
operating
instruction
(OI-74),
and'bserved
the
physical
installation in the field of several
Unit 2 heat exchangers,
and
had
no comments.
The
LER is considered
closed.
(2)
(CLOSED)
Personnel
Error Initiates
Engineered
Safety Features.
On July
1,
1988,
at
12:05 p.m.,
and
again at 1:10 p.m.,
a low
reactor
water
level
signal
was
received
by the
RPS.
Thi s
initiated various engineered
safety features.
The
second
event
occurre'd
during
the investigation
of the first event.
Both
events
were
caused
by the
performance
of
a modification
on
a
Unit 2 reactor
vessel. level transmitter
and
a reactor pressure
transmitter.
The
NRC inspector
reviewed the
LER, dated July 29,
1988,
and the
LER
closure
package,
and
verified
that
the
LER
met
the
requirements
for timeliness,
content,
and corrective
action.
The root
cause
was
determined
to
be
an
incomplete
clearance
request
which
did
not
identify all
adverse
actions,
and
improper
establishment
of the final clearance.
The
licensee
immediately
corrected
the
actuations
and
issued
a
new
clearance.
The licensee
also
counseled
the personnel
involved
and required that. operations
and modifications
personnel
review
the
event
(Operations
Critique 88-041).
Based
on in-office
review of the
LER and corrective
actions
taken,
this item is
closed.
(CLOSED)
Inadvertent
Transfer
Switch Operation
Initiates. Engineered
Safety Features.
This item involves the actuation
of engineered
safety features
during
post
maintenance
testing
of the
2A motor generator
set
on September
4,
1988.
The licensee
determined
the cause
of
this
event
to
be
personnel
error.
The
assistant
shift
operations
supervisor
inadvertently
operated
the
normal/alternate
transfer switch while removing
a clearance
tag,
causing
a loss of power to the bus,
which in turn actuated
and
ESF.
The unit operator,
after
determining
the
cause
of. the
event
and
verifying that
ESF initiation signals
were
not
present,
returned
the affected
systems
to normal.
Subsequently,
the
ASOS
was individually counseled,
the
event
was
discussed
with the remainder of the operating
group
on shift at the time,
and other
operating
groups
were required to read
a review of
the
event.
The
'inspector
reviewed
the
licensee
actions
- described
above
and determined
them to be
appropriately
13
This item is closed.
(4)
(CLOSED)
Unplanned
Actuation
During
Electrical
Board Power Transfer.
This event involves the unplanned
actuation of engineered
safety
features
due
to
loss
of power to the
2B Reactor
Protection
System
bus.
This
occurred
when
power
for
the
2B
480V
shutdown
board
was
transferred
back
to its
normal
supply
following special test 88-24 of Diesel Generator
D.
The breaker
on the
D 4KV shutdown board,
which supplies transformer
TS2B and
is the
normal
power
source for the
2B 480V shutdown board,
was
inadvertently . left
in
the
open
position.
Therefore,
transferring
power
to deenergized
transformer
TS2B
caused
a
loss of power at the
2B 480V
shutdown
board,
with
a
subsequent,
loss of power at the
2B
bus.
The licensee
determined
the
cause
of this event to
be
personnel
error
on the part of the
assistant
shift operations
supervisor
in that
he
did
not
verify the
presence
of voltage at
TS2B prior to transferring
power
sources.
A contributing factor was determined to be that
the
test
procedure
did
not
contain
adequately
specific
instruction
on
how to return
the plant to normal configuration
following completion of the test.
Licensee
actions
taken to prevent recurrence
are
as follows:
The
ASOS involved was individually counseled
and the event
was
discussed
with the
remaining
members
of the shift.
These
discussions
focused
on
the
necessity
for strict
attention
to detail
and attentiveness
to the task at hand.
The other operations
groups
reviewed the event
as
required
readihg.
A memorandum
(RIMS
R42881024940)
was distributed
to all
Plant Operations
Review Committee
members
and -alternates
describing
the
event
and directing
them to
ensure
that
special
test
instructions
include
adequate
specific
'irection for returning
systems
to normal
upon
completion
of the test.
The
NRC
inspector
reviewed
the
above
licensee
actions
and
determined
them to be appropriate.
This item is closed.
(5)
(CLOSED)
Unplanned Start of RHRSW Pump.
This item involves the
unplanned
start of the
B1 Residual
Heat
Removal
pump during the monthly operability test
of the
3A diesel
generator
performed
on July
18,
1988.
The
cause
of this inadvertent
pump start
was determined
to
be the
transfer of 250V
DC control
power
on the
3EC
4KV shutdown
board
while the dieselwas
running,
causing
a
momentary
voltage
drop
14
to the
pump start logic, allowing the time delay start relay
and the auto start lock-out relay to reset to their'eenergized
state
and reinitiate
the
auto start logic.
Therefore,
after
the preset .28 se'cond delay,
the
pump automatically started.
The
licensee's
original
corrective
action
was
to
revise
Special
Operating
Instruction
X-X
23
to
include
a
note
alerting operators
to this type of occurrence.
However, further
review revealed
that
SOI-23
was
a special
one-time
procedure,
and
has since
been cancelled.
Therefore it was determined
that
the
appro'priate
location
for inclusion
of
such
a
caution
statement
would be in
DC Electrical
System Operating Instruction
0-OI-57D.
The
NRC
inspector
reviewed
Revision
3 of this
instruction
and
found
that it contains
(in
two
places)
statements
to caution the operator that the transfer of 250V
control
power to
a
4KV shutdown
board with
a diesel
generator
operating
may cause
an inadvertent start of a
RHRSW pump.
The
inspector
agrees
that this
instruction
is
the
appropriate
location for the caution statement.
This item is closed.
(6)
(CLOSED)
L'ER 259/88-28,
EECW Pressure
Switches
Not Purchased
to
Seismic
Class
I Requirements.
This item involves the discovery,
in February of 1988, that the
pressure
switches 'which auto-start
the
Emergency
Equipment
Cooling Water strainers
had
been
procured
in
1973
to
Seismic
Class II requirements.
Since
the
EECW system
i s identified in
the
as
a Seismic
Class
I system, it was determined
that
these
switches
should
be replaced with new switches
procured to
Seismic
Class
I requirements.
The
installation
of
the
Seismic
Class
I
switches
was
"accomplished
via
Work
Plans
2587-88
and
2704-88,
and
was
completed
in November of 1988 and reviewed
by the
NRC inspector.
This item is closed.
(7)
(CLOSED)
Unplanned
Engineered
Safety
Feature
Actuations
Due to Circuit Protector
Trip
Caused
by
Damaged
Indicating Light Socket.
The
LER
involved
two
separate
actuations
of
containment
isolations
systems that resulted
from loss of
bus
1A power
due to
a blown fuse in the
RPS power supply circuit protectors.
In both cases,
the fuse operated
because
of
a short circuit in
a status
indication light socket
on the local ci rcuit protector
panel.
Immediate corrective actions
were to repair the loose
sockets of
the
indicating
lamps
and
restore
the
system
to
service.
Subsequent
investigations
revealed
that
overheating
of
the
15
indicating
lamp contributed
to the event.
Modifications were
proposed
to correct the overheating
condition.
The
NRC inspector
observed
the circuit protector panels in the
field and found Unit 2 lamps satisfactory.
However, Unit
1 and
Unit
3
lamps still
showed
distorted
lenses
as
a result of
overheating..
The
NRC inspector
found that maintenance
requests
had already
been
issued for the conditions
(MRs 881131,
881134,
881135,
881141,
881142).
The
NRC inspector
also
determined
that proposed modifications
had
been
accepted
and
DCNs
H5627A,
H5628A
and
H5629A
had
been
issued
to correct indicating
lamp
deficiencies.
The
DCNs were
found to
be logical
and thorough.
Corrective actions
were considered
timely and adequate.
This
LER is considered
closed.
(8)
(CLOSED)
Unplanned
Caused
by
Spurious
Radiation Monitor Spike.
This event involves the actuation of engineered
safety features
due
to
an
upscale
spike
experienced
by
refuel
zone
ventilation
exhaust
radiation monitor 2-RM-90-140
on
March 23,
1989.
The initiating signal
immediately cleared.
The spike was
verified to
be
erroneous
by
comparison
to
other
radiation
monitor, indications.
An
inspection
of the
monitor
and
the
surrounding vicinity revealed
the most'ikely cause
of the spike
to
be
a communications
cable with exposed
conductors within one
foot of the detector.
Readings
taken
on the
exposed
conductors
indicated
a
48 volt
DC potential.
The detector
manufacturer
confirmed that arcing of the conductors
in the vicinity of the
detector
could result
in spurious
spikes.
Immediate corrective
action
was to tape
the
exposed
conductors
and
move the cable
away from the detector,
with permanent repair being effected via
maintenance
request
A-912567
on April 25,
1989.
In order to
ensure
that the arcing
had not damaged
the monitor, appropriate
calibration
and testing
was
performed prior to declaring
the
monitor operable.
The
NRC inspector
reviewed
the
licensee's
actions
and determined
them to
be
appropriate.
This
item is
closed.
7.
Action on Previous
Inspection
Findings (92701,
92702)
(CLOSED)
IFI 259,
260,
296/85-53-04',
Emergency
Preparedness
Drill
Concerns.
A previous
NRC inspection
(IR 85-53)
identified various
concerns
during the
performance
of an
Emergency
Preparedness
drill conducted
on November
13,
1985.
The inspector
held discussions
with licensee
personnel
and
reviewed
the
licensee's
closure
package,
other
NRC
inspection
reports,
and
licensee
actions
to address
the
items
of
concern.
The findings are
summarized for each
issue
below.
16
(1)
Problems with TSC phones:
This issue
was also identified as IFI
86-32-12,
item
a (closed
.in
IR 88-05) during
a
subsequent
drill on
September
24,
1986.
No further followup is required
and this issue is closed.
(2)
Incorrect
IP-20 drill data
sheet
for 9:30
a.m.:
This
was
a
drill specific
comment.
No
further
followup
is
required
and this issue is closed.
(3)
Communication
of
Reactor
Mater
Level:
This
issue
was
also
identified as IFI 86-32-12,
item b (closed in IR 88-05) during
a
subsequent
EP drill on September
24,
1986.
No further followup
is required
and this issue is closed.
'I
(4)
Confusion
over
a real contamination
event which occurred during
the drill: This was
a drill specific issue which was discussed
in
another
section
of
IR
85-53.
This
issue
is closed.
(5)
IP-20
Attachment
A incomplete.:
This
was
a drill specific
comment.
Also,
the
IP-20
Attachment
A has
been
updated
(see
finding 8).
No further followup is required
and this issue is
closed.
(6)
The microphone
used
by the site director
was beneficial:
This
was
a drill comment.
No followup is required
and this issue is
closed.
(7)
No guidelines
for
recovery
from
a
fuel
handling
accident:
There are
no specific requirements
for a fuel handling accident
recovery
procedure
and the licensee
does
have general
recovery
guidelines
(EPIP - 16,
Recovery
Procedures)
~
This
issue
is
closed.
(8)
IP-20 Attachment
A out of date:
This
was
a duplicate
of 'IFI
85-52-05 which was,closed
out in IR 86-33.
No further followup
is required
and this issue is closed.
b.
(CLOSED) IFI 259,
260, 296/86-25-08,
Technical Specification
Revision
on Fire Protection
System.
The plant
Technical
Specifications
did not contain
the
sprinkler
systems
as
a fire
protection
system
load.
TVA's
plant fire
protection engineer
agreed that the fire protection sprinkler
system
should
be included in the Technical Specifications.
The
inspector
reviewed
documentation
provided
by
the
licensee
including the current version of Technical
Specifications
and
noted
that section
3. 11, "Fire Protection
Systems",
has
been
revised
as of
Amendment
162
dated
December
27,
1988.
This constituted
a total
revision
of
the
section,
with
replacement
of
the
original
0
17
Table 3.11.A with s'everal
separate
tables.
The Hydraulic Performance
Criteria included in the original Table 3.11.A had been deleted.
The
current
version
of Table
3.11.A,
Fire
Detector
Instrumentation,
includes
operability
requirements
for
detections
instruments
associated
with instal
1 ed spray/sprinkl er
systems.
Tabl e
3. 11. B,
"Spray/Sprinkler
Systems",
includes
plant
areas
required
to
be
protected
by spray/sprinkler
systems.
The inspector
concluded that the licensee
had adequately
addressed
the inspector's
concerns
and this item is closed.
(CLOSED)
IFI
259,
260,
296/86-36-04,
Jet
Pump
Operabi
1 ity
Survei=l 1 ance Instructi on (SI) 4.6. E. 1
This item involved whether jet
pump plugging
can
be detected
prior
to
pump
failure
in
the
absence
of
the
performance
monitoring
techniques
contained
in Technical
Instruction
52.
This TI had
been
utilized to monitor jet
pump performance
in order to detect
cracks
in the jet pump hold-down
beams,
which would lead to jet
pump mixer
displacement
and recirculation
system
performance
degradation,
as
identified
in
General
Electric
Service
Information
Letter-330.
Subsequently,
the
hold-down
beams
were
replaced,
eliminating
the
necessity
to perform the TI-52 testing
for that
reason.
However,
SIL-330 also
recommended
that
some
form of performance
monitoring be
continued in order to preclude jet
pump degradation
due to plugging
of the
pumps.
The
concern
was that, with the discontinuation
of
TI-52 testing,
the then-current
revision of SI-4.6.E. 1 might not
be
adequate
to detect
such plugging.
A review of SIL-330, SI-4.6.E. 1
Rev.
1,
and
TVA memo dated 4-13-88
(RIMS R42880406946)
revealed
the following:
paragraph
5.2.F 1
states
that jet
pump
flow or
differential
pressure
deviation
from
average
is
the
most
sensitive
indicator
of jet
pump
performance
degradation,
and
that monitoring
D/P deviation
from loop
average
on
a daily
basis
is
an
acceptable
method
of performance
monitoring
to
detect jet pump plugging.
SI-4.6.E. 1,
section
7.7 requires verifi'cation of individual jet
pump D/P within 10 percent of average
on
a daily basis.
It is therefore
determined
that SI-4.6.E. 1
now contains
adequate
provisions with which to monitor jet
pump performance
in order to
detect degradation
due to plugging.
This item is closed.
18
(CLOSED) IFI 259/86-40-09,
Tornado Missle.Protection
For Vent Towers.
This item involves
a request for the licensee
to submit
a revision to
Rev.
1
so that
NRC review of the
event
could
be
completed.
During
a
1986
design
evaluation
of
control
bay
ventilation modifications',
an
unanalyzed
condition
was
identified
involving tornado missile protection
for
equipment
located
in the
vent
towers.
A Probabi listic
Risk
Assessment
was
performed
which
determined 'that the risk to the subject
equipment
was sufficiently
low that
no modifications
were
required.
When
questioned
about
docketing
the
PRA,
TVA stated
that it was
considered
to
be
an
unreviewed draft from which no meaningful conclusions
could be drawn.
It was
requested
that
TVA formally submit their final position
on
the
subject,
including
the
approved
PRA,
in
the
form
of
a
revision to the
LER.
In accordance
with the
above
request,
Rev.
2, dated
9-18-87,
was issued to document
TVA's final position,
and the
PRA has
been
reviewed
and
accepted
by
NRC.
The
review
of
the
(RIMS B81870622050),and
closure
of the
LER
have
been
previously
addressed
in
Inspection-
Report
88-32.
Therefore,
this
item is
closed.
(CLOSED) IFI 259,
260, 296/88-10-05,
Performing Special
Test
To Meet
Restart
Test
Program
Requirements.
This item was originally identified during the review and performance
of the
and
was written to identify an administrative
concern
involving the specific plant procedures
that would be
used
to meet
RTP test
requirements.
A review of an
immediate
Temporary
Change
Notice,
dated
May 17,
1988,
and
Revision
4 of
SDSP
12. 1, "Restart
Test
Program",
clearly indicates
PMI-17. 1,
"Conduct of Testing", to
be
an acceptable
procedure
to be
used
as part of the
RTP.
A review
of
PMI-17 '
and
section
4.4 in particular indicated that
adequate
controls
are
in place
for the
performance
and
review of special
tests.
This item is closed.
(CLOSED) IFI 259,
260, 296/88-16-01,
Review of Response
to Licensee's
guality Surveillance Monitoring Report.
This
item
was originally written
as
a result of two incidents
involving
the
di,esel
generators
and
the
subsequent
reports
(gBF-S-88-0436
and 0455)
generated
by the licensee.
The first item
(88-0436)
concerned
a
DG 'which was started with the cylinder vent
valves
open
during
a
special
test.
The
second
item
(88-0455)
concerned
a
DG which was started
with the
load limit set
on
zero
instead of maximum during the
same
special test.
Both of these
i'tems
were traced
to failure to follow procedures.
At the
time of the
incident,
the
DG was in a test configuration,
was not being tested
in
order
to return it to service,
and
was
not
under configuration
control.
The licensee
took immediate corrective
action to instruct
all personnel
involved with
DG testing
of requirements
to control
19
plant activities
and testing.
No similar incidents
occurred while
testing
the other
DGs.
This item is closed.
(CLOSED) IFI 259;
260,
296/88-18-05,
Major Discrepancies
Identified
During LOP/LOCA Test
C.
This item was identified during the-series
of LOP/LOCA tests
(A thru
D)
performed
by the
licensee
to
prove that
the
logic
and
functional
networks
were intact
and
working
as
required
by plant
.
design.
Due to the built in anti-pumping
network of the
4160V
shutdown board'ircuit
breakers,
which prevents
a
breaker
with
a
closed
command to continually open
and close
on
a
bus with
a fault,.
three breakers failed to function as required.
These Unit 3 breakers
locked out when they received
a close
command
on
the
LOP signal,
immediately
received
a
command
to
open
on
the
LOCA signal,
and
remained
open
due to the
anti-pump
network of the
breakers.
The
licensee
initiated
a design
change
to install time delay relays to
del'ay the close
command
in order
to allow the
charging
motor to
recharge
the breaker
and thereby
reclose
the breaker to satisfy the
LOCA logic.
The
NRC inspector
observed
the retest
of
LOP/LOCA "C"
and verified that
the modification
performed 'as
adequate.
This
item is closed.
(CLOSED)
259,,
260,
296/88-21-01,
violation
of
Procedural
Requirements
on Access to High Radiation Areas.
The
inspector
ascertained
through interviews with RadCon
personnel
and
an
SOS 'that high radiation
ai ea
door
keys
were
maintained
by
RadCon
and that
SOS
permission
was not sought
or obtained for all
entries
into the
locked
high radiation
areas.
The
only control
exercised
by the
SOS over the high radiation
area
door
keys
was
a
once
per shift acknowledgement
that the
SOS clerk had
performed
a
survey
of all
th'e
keys
and all
keys
were
accounted
for.
The
inspector
was concerned that the
procedures
controlling the
keys to
locked
high radiation
areas
were
confusing
and contradictory
and
this
was identified
as
an
unresolved
item pending clarification of
this issue.
TVA addressed
the
unresolved
item in the
November
23,
1988 response
to
a violation cited in IR 88-21.
TVA maintained
that the
program
for controlling locked high radiation
areas
was
adequate;
however,
implementing
procedures
would
be
enhanced
through
revisions
to
clarify lines of responsibility.
IE Circular
76-03,
IENs 82-51,
86-44,
and
88-79,
and
SOER 85-3 provide guidance
on control of locked high radiation
areas
and
were
reviewed
against
the
TVA program.
The
NRC inspector
reviewed
th'e
TVA November
23,
1989,
response,
previous
enforcement
history,
recent
gA audits
and
survei llances
of the area,
revisions
to the
implementing procedures
RCI-17 and OSIL-16,
as well
as
performed
an
20
observation
of locked high radiation
area
doors
and
key lockers for
Unit 2.
After reviewing the associated
procedures,
before
and after revision,
the
NRC inspector
determined
that while the controlling procedures
were not of high quality,
no violation of NRC requirements
occurred.
The procedures
met the
requirements
of
TS 6.8', "Radiation Control
Procedures"
as well as the industry standards
for control of keys'to
The revised procedures
provide
a better
representation
of the
actual
program.
This
item is
considered
closed.
i.
(CLOSED)
URI 259,
260,
296/89-20-03 'his
item was
upgraded
to
an
example of the violation in this report for failure to submit
a
LER
within 30 days per the requirements
of 10 CFR 50.73.
(CLOSED) VIO 296/84-45-01,
Violation of TS 6.3.A.1
This item involved concerns
about
the startup of the Unit 3 Reactor
on October
22,
1984 after completion
of
a refueling
outage
which
lasted
over
four
hundred
days.
This violation
contains
eight
examples,
each of which is discussed
below:
~Exam le l:
This
example
involved the failure to have'rywell
Floor Drain
Sump Level Transmitter 3-LT-77-1A in service
due to
a lack of specificity in procedure
OI-77, in that the data
sheet
was
common for all three units,
thereby not providing positive
identification
of
- which unit's
system
alignment
had
been
verified.
To
correct
this
condition,
the
licensee
has
individually listed
each
instrument,
referenc'ed
to
its
applicable
unit,
in later revisions
of the
Lineup Checklist,
currently
Attachment
4
(page
4 of 8)
to
Procedure
OI-77B,
Revision
2.
The
inspector
reviewed
this
checklist
and
determined it to
be
adequate
to
prevent
future
similar
occurrences.
Therefore, this example is closed.
~Exam le 2:
This
example
involved
the
Drywel1
Shield
Plug
Trolley Chain not being
padlocked prior to startup
as
required
by step I.B.2. a of procedur e GOI-100-1.
Thi s was determined
to
be the result of personnel
error.
The involved individual
was
reprimanded
and mechanical
maintenance
personnel
were retrained
in this
area
in
March of
1985.
This
example
is
considered
closed.
Exam les
3 and 4:
These
examples
involved
the
failure
to
complete
steps
27,
28,
and
29 of the
Master
Refueling
Test
Instruction prior to performing Refueling Test Instruction - 4,
"Full Core
Shutdown
Margin - Closed
Vessel".
Had these
steps
been
performed
when required,
the Shutdown Cooling System would
have
been
secured
arid the
RHR system
would have
been
The licensee, determined
that this
was
due to GOI-100-1
being
21
inadequate
to ensure
that
NRTI signoffs
were obtained prior to
plant
startup.
Revision
1
to
GOI-100-1
now contains
the
requirement
that,
for startups
following
a
r efueling
outage,
the
MRTI shall
be in the possession
of the
SOS,
who will verify
that all required
steps
have
been
performed.
These
examples
are considered
closed.
~Exam le 5:
This
example
involved
the
failure
to
perform
GOI-100-1,
Section II.A, steps
9,
10,
and
14 prior to pulling
control
rods for the initial
shutdown
margin test.
Step
9
secures
shutdown
cooling,
step
10
starts
the. recirculation
pumps,
and
step
14 secures
head vents.
The licensee
determined
the reasons
for thi s violation were that shift personnel
did not
interpret
the
pulling of control
rods for initial
shutdown
margin testing to constitute
a reactor startup
because
"reactor
'startup"
was
not clearly defined in the procedures.
To prevent
future recurrences,
GOI-100-1, Revision
1
now contains
measures
to identify steps
which must
be completed prior to every startup
and cannot
be bypassed
at the discretion of shift personnel.
In
addition,
Amendments
158 (Unit 1),
154 (Unit 2),
and
129 (Unit
3) to
the facility operating
licenses
contain
a clarified
definition of Startup
Condition.
These
amendments
were
issued
by the
NRC
on
November
18,
1988.
This example is
considered
closed.
~Exam le 6:
This
example involved the failure to attach
a graph
of K-effective to SI 4.3.B. l.a data
sheet
dated
10-22-84,
as
required
by GOI-100-1,
Pre-Startup
Checklist
step
I.R.2.
The
licensee
determined
the
cause
to
be inattention to procedural
detail,
in that
the K-effective'raph
was
not physically
attached
to the data
sheet
because it was being
used during rod
movement.
Revision
1 to GOI-100-1
no longer requires
the graph
to
be physically attached
to the data
sheet,
but that it be
posted
In addition,
personnel
have
been
counselled
regarding
attention
to
procedural
detail.
This
example is considered
closed.
~Exam le 7:
This example involved the
inadequacy
of Surveillance
Instruction
4.6.E.1
in that it did
not
accurately
reflect
the
acceptance
criteria for jet
pumps
contained
in
The
TS
acceptance
criteria
contained
in
Surveillance
Requirement
4.6.E.l.c
require
that
individual
jet
pump
differential pressures
be within 10 percent of the
mean
value
of all jet
pump differential
pressures.
However,
the
invoked acceptance
criteria contained
in Technical
Instruction
52,
which
requires
that
individual jet
pump
differential
pressures
be within
10 percent
of established
baseline
data,
which
in effect
would
allow values
of
up
to
15
percent
deviation
from the'ean
to
be
acceptable.
The
licensee
has
revised
SI-4.6.E. 1
to correct this condition.
The
inspector
reviewed Revision
1, dated
10-27-87,
and determined
22
that all
references
to TI-52
have
been
removed
and
the
TS
acceptance
criteria
are
now
specifically
stated
in
the
procedure.
This example is closed.
~Exam le 8:
This example involved the failure of Shift Technical
Advisors to document
unacceptable
test results
as required
by
procedure.
Surveillance
Instruction 4.6.E. 1, for demonstrating
jet
pump operability,
required,
in step
20 that any exceptions
to acceptance
criteria
be
noted
and explained
in the
remarks
section.
However,
when
SI 4.6.E. 1
was
performed
on Unit 3
on
October
21,
1984, with results that did not meet the acceptance
criteria, this
exception
was
neither
noted
nor explained
as
required.
The licensee
has revised
SI 4.6.E. 1,
as
discussed
in
example
7 above,
to more clearly state
TS requirements,
and has
provided training to
in
procedural
requirements.
This
example is considered
closed.
As individually discussed
above, all eight
examples
comprising this
violation have
been adequately
addressed,
and appropriate
corrective
actions
have
been
accomplished.
Therefore, this violation is closed.
(CLOSED)
VIO 259,
260,
296/85-57-06,
Example
C, High Radiation
From
LPRM Changeout.
This
item involves
the
set
point
(100 mr/hr) for
area
radiation
monitor
2-RM-90-141
being
exceeded
during
a
local
power
range
monitor
manipulation
on
November
20,
1985
which
resulted
in
a
secondary
containment isolation
and standby
gas treatment initiation.
During
movement
of
the
LPRN it
was
damaged,
causing
increased
difficulty in handling, which resulted
in it being caught behind the
source
pin rack.
During the attempt to free it from the rack,
the
highly radioactive
end
was raised
to within 18 inches
of .the water
surface,
thereby increasing
the dose rate in the
area
above
the
ARN
set point.
The following actions
occu'rred
almost simultaneously:
The
HP technician instructed the operator to lower the
LPRM.
The
ARN alarmed.
The
LPRN was lowered by the operator.
The estimated
duration of the
event
was
2
seconds
with the
maximum
exposure
received
by
an
individual of
30
mi llirem.
The
licensee
determined
the root causes
of the incident to be:
The
use of a procedure
which did not minimize the potential for
physical
damage
to the
A prejob briefing which did not
include all
aspects
of the
operation
0
23
An unanticipated
and
unplanned
configuration with the
damaged
LPRM caught behind the source
pin rack
The following corrective
measures
have
been
accomplished
in order to
preclude future recurrence:
Additi'onal
radiological
caution
statements
have
been
incorporated
into
procedure
SMI
192.2,
"LPRM
Maintenance
Instruction."
A statement
has
been
incorporated
into
SMI 192.2 requiring
a
formal operational
briefing prior.to starting work.
The
method of physically'oving the
LPRM has
been
revised
to
reduce
the potential
for incurring
damage
or for the
LPRM to
become
caught.
Appropriate
personnel
have
been
made
aware
of
the
above
procedural
revisions
and .have
received
a critique
of the
incident.
Subsequent
to the incorporation of the above procedural
enhancements,
seventeen
Unit 2
LPRM assemblies
were replaced
in December of 1988,
without incident,
thereby
demonstrating
that
the
above
corrective
measures
are
adequate.
Therefore,
this item is closed.
The other
examples
comprising this violation were
previously
closed
in IR's
88-34
and 88-35.
This violation is closed.
No violations or deviations
were identified during the
Followup of Open
Inspection
Items.
8.
Site Management
and Organization
(36301,
36800,
40700)
On
June
20,
1989,
the
licensee
began
a 60-day plant work schedule
to
demonstrate
to
TVA senior
management
BFNs ability to complete
a
complex
series
of work activities
on
schedule.
One of the
scheduled
activities
was to complete work on balance-of-plant
systems
such that main condenser
vacuum could be drawn
on July 20,
1989, with all required
systems fully
During this inspection period,
the licensee failed to maintain
the 60-day schedule.
This was due mainly to delays
in closing
ONE paper
work required to complete
SPOC signoffs for restart.
Concerted effort was.
expended
on the 60-day
schedule
of activities
and for the
most part the
field work
progressed
well.
Of particular
note
was
the effort
and
results
of the
Maintenance
Department;
they
exceeded
their
MR work off
rates,
decreased
the
overall
backlog,
and
reduced
unacceptable
work
rates.
The work performed
the
60-day
schedule will be
used
by TVA to develop
a
Unit 2 restart
schedule.
24
9.
Exit Interview (30703)
The inspection
scope
and findings were
summarized
on July 14,
1989 with
those
persons
indicated
in paragraph
1 above.
The inspectors
described
the areas
inspected
and discussed
in detail
the inspection findings listed
below.
The licensee
did not identify as proprietary
any of the material
provided
to or reviewed
by the inspectors
during this inspection.
The
plant manager
stated that the plant position would be to deny,
in part or
fully,
Violation
(259,260,296/89-27-04)
concerning
,LER
reporting,
because
of technical
disagreement.
Item
260/89-27-01
260/89-27-02
259,
260, 296/89-27-03
259,
260, 296/89-27-04
10.
Descri tion
IFI - Fuse
Replacement
Jumpers,
paragraph
2.b.
Violation -
Failure to Meet
TS
Requirements
for
Loops,
paragraph
4.
IFI Verification That
DG Output Breakers
Recharge
In Less
Than 2.5
Seconds,
paragraph
5.a.
Violation -
Failure to submit
a
LER within
30 days per
paragraph
6.
ASOS
CFR
DCN
D/P
IEB
IEN
IFI
IR
KV
Area
Range Monitor
American Society of Mechanical
Engineers
Assistant Shift Operations
Supervisor
Code of Federal
Regulations
Director Current
Design
Change
Notice
Diesel Generator
Differential Pressure
Emergency
Core Cooling Systems
Emergency
Equipment Cooling Water
Emergency Notification System
Emergency
Preparedness
.Environmental Qualification
Engineered
Safety Features
Final Safety Analysis Report
Health Physics
Inspection
8 Enforcement Bulletin
Information Notice
Inspector
Followup Item
Inspection
Report
Kilovolt
,
0
25
LER
LRED
LOP/LOCA
.MR
MRTI
NRC
OSIL
PMI
RCW
SDSP
SOI
SOS
SR
TD
TI
TS
V
WP
Licensee
Event Report
Local
Power
Range Monitor
Licensee
Reportable
Event Determination
Loss of Power/Loss of Coolant Accident
Maintenance
Request
Master Re'fueling Test Instruction
Measuring
and Test Equipment
Nuclear Regulatory
Commission
Operating Instruction
Operations
Section Instruction Letter
Plant Manager Instruction
Plant Operations
Review Committee
Probabi listic Risk Assessment
Quality Assurance
Quality Control
Raw Cooling Water-
Residual
Heat
Removal
Residual
Heat
Removal
Service
Water
Reactor Protection
System
Reactor
Pressure
Vessel
Refueling Test Instruction
Restart
Test Program
Site Director Standard
Practice
Surveillance
Instruction
Service Information Letter
Special
Operating Instruction
Shift Operations
Supervisor
Surveillance
Requirement
Shift -Technical Advisors
Test Discrepancy
Technical Instruction
Technical Specifications
Tech Support Center
Valley Authority
Unresolved
Item
Volt
Violation
Work Package