ML18012A259

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Insp Rept 50-400/96-04 on 960317-0427.Violations Noted. Major Areas Inspected:Plant Status,Shifts Logs & Facility Records,Security Control,Fire Protection & EP
ML18012A259
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 05/20/1996
From: Brady J, Shymlock M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18012A257 List:
References
50-400-96-04, 50-400-96-4, NUDOCS 9606110192
Download: ML18012A259 (38)


See also: IR 05000400/1996004

Text

~g REGS

0

++**+

Report No.:

50-400/96-04

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W., SUITE 2900

ATLANTA,GEORGIA 303234199

Licensee:

Carolina

Power

8t Light Company

P. 0.

Box 1551

Raleigh,

NC 27602

Docket No.:

50-400

Facility Name:

Harris

1

Inspection

Conducted:

March

17 - April 27,

1996

Inspector:

ra y,

en>or

es>

ent

ector

License No.:

NPF-63

ate

1gne

Approved by:

D. Roberts,

Resident

Inspector

B. Crowley, Maintenance

Inspector,

paragraphs

3. 1, 3.2.4, 3.2.5,

3.2,6, 3.3.1.

>=~-9c

ym oc

,

C

~S9

Reactor Projects

Branch

4

Division of Reactor Projects

SUMMARY

Scope:

Inspections

were conducted

by the resident

and/or regional

inspectors

in the

areas of Plant Operations

which included plant status, shift logs

and facility

records, facility tours

and observations,

event followup, effectiveness

of

licensee

control in identifying, resolving,

and preventing problems;

Maintenance

which included maintenance

observation,

surveillance observation,

and review of licensee

event reports

(LERs); Engineering

which included onsite

engineering

and review of LERs;

and Plant Support which included plant

housekeeping

conditions, radiological protection,

security control, fire

protection,

emergency

preparedness,

licensee self assessment

and review of

LERs.

Results:

Plant

0 erations

Plant operations

were generally performed well.

Operators

were challenged

by

plant equipment

problems

on the shutdown

and startup related to the feedwater

isolation valve outage

and after the reactor trip.

The Plant Nuclear Safety

Committee performed thorough reviews for the root causes

of the events.

ENCLOSURE

2

'pI60biiOi92 960520

PDR

ADQCK 05000400

8

PDR

Assessments

by the Nuclear

Assessment

Section during the startups

and shutdown

were thorough.

One violation was identified for inadequate

corrective action

related to

a resin transfer event which resulted in the spread of

contamination

{paragraph 2.5. 1).

One non-cited violation was identified that

related to an inadequate

procedure for placing the pressurizer

pressure

master

controller in automatic

(paragraph

2.3. 1.1).

Maintenance

One violation was identified which involved failing to correct

a documented

deficiency

on

an installed voltmeter switch prior to using it in a

surveillance

{paragraph 3.2.2).

One non-cited violation was identified which

involved failure to follow procedure for re-qualification of maintenance

personnel

(paragraph 3.2.6).

Overall, for the activities observed,

the maintenance

and surveillance

programs

were being effectively implemented.

The activities observed

were

planned

and conscientiously

executed

in accordance

with detailed procedures.

Personnel

were qualified for the task performed,

Interface

between

maintenance

and operations

personnel

was good.

Extensive detailed trending of important parameters

is being performed

by the

system engineer for the main transformers.

The maintenance

backlogs for corrective maintenance

work tickets

and overdue

PHs has

been high.

However, the overdue

PH backlog

has

been significantly

reduced with plans to eliminate it.

A reduction plan for the

CN backlog is

being worked with a goal to cut the backlog in half during 1996.

En ineerin

Engineering

was challenged

during the period by the Technical Specification

Surveillance

Review Program

and the two forced outages.

Engineering

performed

good root cause

analyses

and supported

the operations

organization well during

the period.

Plant

Su

ort

Plant housekeeping

and the material condition of components

was satisfactory.

The licensee's

adherence

to radiological controls, security controls, fire

protection requirements,

emergency

preparedness

requirements

and Technical

Specification requirements

in these

areas

was satisfactory.

REPORT DETAILS

Acronyms used in this report are defined in paragraph

9.

1.0

PERSONS

CONTACTED

2.0

2.1

Licensee

Employees

  • D. Alexander,

Supervisor,

Licensing

and Regulatory

Programs

D. Batton, Superintendent,

On-Line Scheduling

D. Braund,

Superintendent,

Security

  • A. Cockerill, Superintendent,

I&C Electrical

Systems

  • J. Collins, Manager, Training
  • J. Dobbs,

Manager,

Outage

and Scheduling

  • J. Donahue,

General

Manager,

Harris Plant

W. Gautier,

Manager,

Maintenance

  • W. Gurganious,

Superintendent,

Chemistry

  • H. Hamby, Supervisor,

Regulatory

Compliance

H. Hill, Manager,

Nuclear Assessment

D. McCarthy, Superintendent,

Outage

Management

  • K. Neuschaefer,

Acting Manager,

Environmental

and Radiation Control

W. Peevyhouse,

Acting Superintendent,

Mechanical

Systems

  • W. Robinson,

Vice President,

Harris Plant

  • G. Rolfson,

Manager,

Harris Engineering

Support Services

S. Sewell, Superintendent,

Design Control

  • T. Walt, Manager,

Performance

Evaluation

and Regulatory Affairs

  • A. Williams, Hanager,

Operations

Other licensee

employees

contacted

included office, operations,

engineering,

maintenance,

chemistry/radiation control,

and corporate

personnel.

PLANT OPERATIONS (93702,40500,92700,92901)

The Harris Operations unit officially completed its reorganization

on

April 4,

1996.

This transition involved the renaming of positions in

the main control

room,

and the redefinition of key roles

and

responsibilities.

The Shift Foreman position was retitled Shift

Superintendent

of Operations.

A second level of supervision,

Control

Room Supervisor,

was also created.

Both positions

are filled by

licensed

SROs.

The reorganization

involved several

promotions within

the Operations unit.

The position of Manager - Shift Operations

(who

previously was the link between the control

room staff and the Manager

of Operations)

was deleted.

While it was still too early to assess

its

effectiveness,

licensee

management

believed this reorganization will

streamline

and enhance

operations

performance.

Plant Status

The plant continued in power operation until March 22,

1996.

On March 22,

1996 at 9:52 p.m., the Harris plant completed

a Technical

Specification required

shutdown after declaring both trains of automatic

load sequencers

inoperable.

The sequencers

had

been declared

inoperable

at 3:00 p.m. that day due to previously missed surveillances

identified

by the licensee's

ongoing Generic Letter 96-01 Technical Specification

Surveillance

review effort.

The required

sequencer

testing

was

completed later on Harch 22,

1996, for Train "A" and

on Harch 23,

1996,

for train "8".

A further plant cooldown to Hode

5 was completed at 5:35 a.m.

on

Harch 24,

1996, after testing of the "8" steam generator

feedwater

isolation valve indicated valve stem

and disk separation.

After repair

of the valve the plant was taken critical on Harch 29,

1996,

and went

on-line on Harch 30,

1996.

On April 2,

1996, at approximately 4:30 p.m.

power was reduced to

approximately

90 percent reactor

power to replace

a leaking relief valve

on the 38 feedwater heater.

While placing the 38 and 48 feedwater

heaters

back in service after replacement

of the relief valve, the plant

experienced

a runback from approximately

89 percent to 82 percent,

due

to a trip of the

A heater drain

pump.

The plant continued in power operation until April 25,

1996,

when the

plant tripped from 100 percent

power due to a failure of the phase

A

disconnect for unit output breaker 52-7.

The plant began startup

on

April 27,

1996,

and entered

Hode

1 at 11:40 p.m.

Shift Logs and Facility Records

The inspector

reviewed records

and discussed

various entries with

operations

personnel

to verify compliance with the

TS and the licensee's

administrative procedures.

In addition, the inspector

independently

verified clearance

order tagouts.

Logs were legible

and well organized,

and provided sufficient

information on plant status

and events.

Clearance

order tagouts

were

properly implemented.,

The inspector identified no violations or

deviations in this area.

2.3

Facility Tours

and Observations

Throughout the inspection period, the inspectors

toured the facility to

observe activities in progress,

and attended

morning status

meetings to

observe

planning

and management activities.

The tours included

monitoring instrumentation

and equipment operation, verification that

operating shift staffing met

TS requirements,

and that the licensee

was

conducting control

room operations

in an orderly and professional

manner.

The inspectors additionally observed

several shift turnovers to

verify continuity of plant status,

operational

problems,

and other

pertinent plant information.

During the shift tur novers

and meetings,

plant personnel

clearly communicated

important plant status

changes,

weather related problems,

and other deficiencies.

Overall, licensee

performance

observed

during facility tours

and observations

was

satisfactory.

Plant

Shutdown

and Startup

From Forced

Outage

The inspectors

observed

the shutdown

and startup related to the forced

outage in Harch

1996.

Operator performance

was adequate.

Several

equipment

problems during the shutdown

and startup challenged

the

operators.

In general,

they responded

appropriately

by stopping the

shutdown or startup to repair the equipment.

The

SROs in the control

room conducted mini-briefs with their control

room operators prior to

starting complicated or infrequently performed evolutions or when

unexpected

equipment

responses

were received.

The inspectors

considered

that these mini-briefs provided

good direction

and focus to the

coordination of the operator actions.

Several

evolutions that caused

the operators

some problems

are discussed

below.

Because of the nature of the forced shutdown,

the reactor coolant system

did not receive the normal cleanup time that the licensee instituted

on

planned

outages.

As a result, radiological

dose rates

were higher from

the

RHR system piping in the

RAB than they would have

been if the

additional

cleanup time was available.

2.3. 1. I

Pressurizer

PORV Lifted Unexpectedly

In Hode

3 on Harch 29,

1996 at 12:55 p.m.,

an operator error occurred

when placing the pressurizer

pressure

controller in automatic.

The

operator placed the controller in automatic without matching the

reference

pressure

to the actual

pressure.

General

Procedure

GP-002,

Normal Plant Heatup from Cold Solid to Hot Subcritical

Hode

5 to Hode 3,

Revision 9, described

steps for placing the pressurizer

pressure

master

controller in automatic.

It directed the operator to verify the

pressure controller (PK-444A) was set at 2235 psig and was in auto after

actual pressurizer

pressure

reached

2235 psig.

The controller was set

below the actual

pressure.

After approximately five minutes,

one of the

pressurizer

PORVs (valve 444B) opened.

The

PORV block valve was shut

after determining that pressurizer

pressure

was below 2235 psi.

No

significant pressure

transient

occurred.

The controller

was taken

back

to manual

and after realizing the mistake in not setting the reference

value correctly, the controller was set to the proper value, taken

back

to auto,

and

PORV 444B was unblocked (I:05 p.m.).

At approximately I:25

p.m., the

PORV opened

again.

The

PORV block valve was again closed

and

the controller was taken

back to manual.

No significant pressure

transient

occurred.

After initial investigation

by engineering

and discussion with the

operations'shift

crew, the licensee

concluded that

some of the operators

did not fully understand

the capability and responsiveness

of the

controller to the integrator function (described

in system description

SD-100.03,

Pressurizer

and Controls,

Revision 3/2).

The master

controller circuit takes the difference

between the actual

pressure

and

reference

pressure

(Pact- Pref)

and

adds to that

a signal proportional

to the time integral of the difference

(Pact- Pref) to obtain the

controller output signal.

The purpose of the time integral function is

to allow pressurizer

sprays

and heaters

time to return pressure

to the

reference

set point prior to lowering pressure

by opening the

PORV.

After sufficient time with actual

pressure

and reference

pressure

at the

same value,

the controller was successfully

taken to auto.

This third

time involved placing the master controller in automatic,

then rapidly

placing the heaters

and sprays in automatic.

Substep

64.a in section

5.0 of procedure

GP-02 required verification

that the pressurizer

master controller was in automatic.

Subsequent

substeps

directed the operator to verify the pressurizer

heaters

in auto

(64.b)

and spray loops in auto (64.c).

The operator for the initial two

attempts,

which resulted

in

PORV lifts, indicated that

he

had placed the

master controller in automatic without subsequently

doing the

same with

the heaters

and spray loops.

There were

no instructions in the

procedure to accomplish

steps

64.a,

64.b,

and 64.c in rapid succession.

The inspectors

concluded that not having the pressurizer

heaters

and

spray valves in the controlling equation

caused

the

PORV's unexpected

opening.

Had the operator placed the spray

and heater

loops in

automatic prior to placing the master pressure controller in automatic,

the spray valves

and heaters

would have

by design controlled pressurizer

pressure

around the setpoint

and not required the

PORV to open.

The

inspectors

considered

the order of these

steps to be

a procedural

inadequacy.

The engineering

review that was performed immediately

following the second

PORV liftto assess

the operational

adequacy of the

master controller prior to continuing the startup also identified the

procedural

inadequacy.

The operator's failure to follow the procedure to match the setpoint

with current operating conditions,

the apparent

operator

knowledge

deficiency regarding the time integrator function in the pressure

controller,

and the procedural

inadequacy related to the order of

placing components

in automatic were all contributors to the unexpected

PORV lifting.

The

PORV lifts did not result in any significant plant

transient or radiological

consequences.

Licensee corrective action was

to counsel

the operators

involved, revise the procedure,

and conduct

training to address

the operator

knowledge problem.

The failure to

follow procedure

and the procedural

inadequacy

are considered

violations

of TS 6.8. 1 and are identified as

NCV 50-400/96-04-01.

This licensee

identified and corrected violation is being treated

as

a Non-Cited

Violation, consistent

with Section VII.B.I of the

NRC Enforcement

Policy.

2.3. 1.2

Rod Withdrawal Block

In Node I on March 30,

1996, at approximately 2:45 p.m., the licensee

received

an intermediate

range rod block after synchronizing the

generator to the grid.

The licensee

had experienced

some turbine

governor problems

when preparing the turbine for operation which had

delayed synchronization.

The governor

had

been repaired

and control

circuits adjusted.

The inspectors

observed

slow swings of approximately

'I

0

~.4

3-5 r.p.m.

immediately prior to synchronization.

Immediately after

synchronization

the generator

picked

up approximately

60

HW which was

slightly higher than the operators

anticipated

(30 HW).

As

a result,

a

mild RCS temperature

transient

occurred

which necessitated

operators

to

pull rods out to compensate.

Rods were slightly higher in the core than

normal, resulting in less

rod worth.

The intermediate

range rod stop,

interlock C-l, was reached

at about the time the transient

stopped.

The inspector

observed that the operators

were not anticipating the rod

withdrawal block.

When the block was received the operators

established

that the conditions from General

Procedure

GP-005,

Power Operation

(Hode

2 to Hode 1), Revision

12, step

98, to block the intermediate

range high

flux trip were met, which also

removed the rod block.

Once

a hold point

was reached

in the power ascension

process,

the operations shift

superintendent

briefly critiqued the circumstances

surrounding the rod

block with the crew.

Points that

he made were that the crew had not

adequately

anticipated

the rod block which indicated to him that they

were not monitoring intermediate

range

power indication as carefully as

power range indication.

He pointed out that they should

have noted the

slightly higher position of the rods in the core

and discussed their

overall affect on power indication and rod worth in their mini-brief

held prior to generator

synchronization.

The inspector

concluded that

the shift superintendent's

critique of his crew's performance

was

accurate.

Onsite

Response

to Events

On April 25,

1996 at 9:07 p.m. the plant tripped from 100% power due to

a failure of the phase

A disconnect for unit output breaker 52-7.

The

licensee

made

a 4-hour report

as required

by 10 CFR 50.72 at 12:45 a.m.

on April 26,

1996.

The other unit output breaker,

52-9,

had

been taken

out of service

22 minutes prior to the trip to perform maintenance.

The

turbine tripped

on generator

lockout with a resulting reactor trip.

The licensee

found that the

A phase

disconnect

switch blade

on the 52-7

output breaker .had not fully rotated

90 degrees

into the jaws of the

receptacle.

This resulted

in a high resistance

due to reduced contact

surface

area.

With the high resistance

and doubled current from the 52-

9 breaker

being open, the heating

was increased

by a factor of 4 which

resulted

in the receptacle

melting and

a ground fault.

The licensee

replaced the disconnect

and verified that the other breakers

in the yard

were properly aligned.

Some adjustments

were necessary

on the other

breakers.

Operators

received training from engineering

on how to tell

if the knife blades

are properly aligned.

After the generator trip, the

B train emergency

bus tripped on

undervoltage

and

was reenergized

from the

B train

EDG.

The A train

successfully

completed

a fast transfer to the startup transformer,

therefore

the

A train

EDG was not called

on to start.

The licensee

determined that the

B

EDG started

as required

and that

a valid under

voltage condition existed

on the

B train emergency

bus.

The fast

transfer

was determined to have occurred

on the

B bus,

but not before

0

2.5

the emergency

bus tripped

on under voltage (I second

time delay

allowed).

The licensee

was still investigating

why the

8 train

emergency

bus transfer did not occur within the time limits.

The A train

EDG was found shortly after the reactor trip with local

indications that it was in the operational

mode with the maintenance

mode lights illuminated.

The'nspectors

verified at the

EDG control

cabinet that this condition existed.

The indications in the control

room were that it had tripped.

These annunciators

indicated that the

diesel

received

a stop signal.

The diesel did not receive

an emergency

start signal during the event

and should not have since the

A train

busses

had successfully

completed

a fast transfer to the startup

transformer,

and

no under voltage condition existed.

An operator in the

diesel

building at the time of the event

was at the A EDG control panel

and confirmed that the

A EDG did not attempt to start.

Having the

EDG

in the operational

mode with the maintenance

mode lights on would not

have prevented

the diesel

from starting

on

an emergency signal.

However, the licensee

conservatively declared

the

A train

EDG inoperable

because

of the unexplained indications.

A previous similar instance

occurred during

a lightning strike.

The licensee

investigated

the

situation

and determined that the stop signal coil is susceptable

to

induced voltages

which causes

the circuit to be overly sensitive.

The reactor trip caused

a pressurizer

level transient

due to the change

in

T,,.

Initially, as part of the

EOPs,

letdown was checked

and was in

service.

A short time later pressurizer

level reached

17 percent

and

letdown isolated.

Volume control tank

(VCT) level

was slightly above

the auto-makeup

level

(24 percent

vs.

20 percent)

at the time.

Charging

was at

a high flow rate

(140 gpm) which rapidly depleted

VCT inventory

and

an auto makeup signal

was initiated.

At the low level

VCT swapover

point the

VCT suction valves to the charging

pumps closed

and the

RWST

valves

opened.

The licensee's

investigation

showed that this occurred

as designed.

The investigation

showed that auto

makeup to the

VCT was

initiated but, timed out when the boric acid makeup

pump did not start.

The licensee

has tested this circuit but was not able to obtain

a repeat

of the event.

Even with auto makeup to the

VCT working, the swapover to

the

RWST would still have occurred.

Because

the trip occurred

two days before the end of this inspection

period, analysis of the post-trip review will be performed during the

next inspection period.

Effectiveness of Licensee

Control in Identifying, Resolving,

and

Preventing

Problems

Condition Reports

(CRs) were reviewed to verify that

TS were complied

with, corrective actions

and generic

items were identified,

and items

were reported

as required

by 10 CFR 50.73.

Several

Plant Nuclear Safety

Committee meetings

were attended

pertaining to the forced outage

and

reactor trip.

The inspector determined that quorum requirements

were

met as required

by TS 6.5.2.

Discussions of the events

were thorough

'll

and probing.

The inspector also observed that

NAS personnel

were in the

control

room for the forced shutdown

and startups.

The inspector

reviewed the

NAS summary of observations

and determined that the

NAS

assessment

was thorough,

providing good self assessment.

Resin Transfer Incident

On April 10,

1996, the licensee

became

aware of a problem with resin

around

a floor drain in the waste processing

building.

This problem was

identified when attempting to determine

how two individuals,

who had

been walking down

a modification,

became

contaminated.

The individuals

had alarmed the monitors at the control point to the radiological

controlled area.

The licensee

found small

amounts of resin

around the

floor drains

on elevation

236 of the waste processing

building.

Approximately 7200 square feet of floor space

had

become

contaminated,

mostly because

the contamination

had

been tracked

around that elevation.

The licensee

established

a boundary

and decontaminated

the areas.

A

condition report was written

(CR 96-01007)

and

an investigation

was

initiated.

A resin transfer

was performed

on April 6,

1996,

several

days prior to

the resin being found around the floor drain.

The resin

bed

was part of

the liquid radwaste

processing facility.

During resin transfers,

the

spent resin is transferred

from the resin

bed pressure

vessel,

then the

vessel

is filled with new resin.

During the filling, pressure

builds

up

in the vessel.

The vessel

is vented after the filling process

through

a

vent line on the top of the vessel

that is routed to the floor drain

system.

The licensee

concluded that during the venting operation

a

small

amount of resin in the vent line was vented into the floor drain

collection system.

The pressure

from the venting process

apparently

blew some of the resin out several

other floor drains in the system.

Since the floor drain system

was considered

contaminated,

the venting

operation

spread

the contamination

outside the floor drain system.

Some licensee

personnel

were

aware of a similar incident having occurred

before.

The inspectors

reviewed

CR 95-00053 dated January

4,

1995,

which described

the previous event.

The event

was identical except that

no personnel

contaminations

resulted.

One of the corrective actions

was

to change

the operating

procedure to eliminate the use of the vent

valves.

The corrective action

was later revised to issue

a night order

to use caution

when venting the vessels

to prevent carryover of resin to

the sumps.

The licensee

also stated that the resin

beds

were at one

time a temporary modification that later became

a permanent

modification.

The inspector concluded that introducing gas into an open

system

designed for the draining of liquid was

an improper practice that had

resulted

in (I) contaminating

two personnel

and (2) the spread of

contamination to

a noncontaminated

area within the radiological

controlled area.

10 CFR 50, Appendix B, Criterion XVI, Corrective

Actions requires that measures

be established

to assure that conditions

adverse to quality,

such

as deficiencies

and defective material or

0

2.6

equipment,

are promptly identified and corrected.

This requirement is

further delineated

in Revision

18 to the licensee's

Corporate guality

Assurance

Program manual.

The failure to correct this condition after

the January

1995 event is identified as

example

one of Violation 50-

400/96-04-02:

Inadequate

Corrective Action, Failure to Correct Resin

Venting Problems.

Close Out Issues

- Plant Operations

(Closed)

IFI 400/94-12-02:

Review the Licensee's

Transition of Mork

Control Following Startup

from an Outage.

This item was originally opened to track the licensee's

process for

transitioning from a risk-based

outage

schedule to an on-line work

schedule.

Following the

1994 refueling outage,

on-line work was being

scheduled

during the

same time interval

as work listed

on the outage

schedule without the

same risk reviews associated

with the latter.

Since that outage,

the licensee

has

enhanced its on-line maintenance

schedule

by using

a risk-based

approach to conducting

system outages.

Risk significant maintenance activities were scheduled

using

a 12-week

rolling system

outage

approach

based

on

a risk matrix in accordance

with

procedures

PLP-710,

Revision 4, Mork Management

Process;

and PLP-402,

Revision 2,

NRC Maintenance

Rule Implementation

Program.

This

enhancement

was previously addressed

in NRC Inspection

Report 400/95-18.

Since the licensee

now uses

a risk-based

assessment

process

in

scheduling

both on-line and outage-related

work, the concern with the

previous practice of transitioning

between

the two configurations

has

been alleviated.

This item is closed.

2.7

3.0

3.1

Conclusion

- Plant Operations

Plant operations

were generally performed well.

Operators

were

challenged

by plant equipment

problems during shutdowns

and startups

related to the feedwater

isolation valve outage

and after the reactor

trip.

The Plant Nuclear Safety Committee performed thorough reviews for

the root causes

of the events.

Assessments

by the Nuclear Assessment

Section during the startups

and shutdown were thorough.

One violation

was identified for inadequate

corrective action related to a resin

transfer event,

which resulted

in the spread of contamination

(paragraph

2.5.1).

One non-cited violation was identified related to an inadequate

procedure for placing the pressurizer

pressure

master controller in

automatic

(paragraph

2.3. 1.1).

MAINTENANCE - (62703,

61726,

92700,

92702,

92902)

Hai nten ance Observati ons/Revi ews

The inspectors

observed/reviewed

portions of selected

maintenance

activities

as detailed

below to determine if these activities were

conducted

in accordance

with Technical Specifications

(TS), the Final

Safety-Analysis

Report

(FSAR), approved

procedures,

and appropriate

industry codes

and standards.

In addition to verification that

procedures

were followed and

TS requirements

were met, the inspectors

verified that personnel

were knowledgeable

and qualified, that post

maintenance

testing

(PHT) was performed

and

was appropriate,

that

required clearance

requirements

were met,

and that calibrated

measuring

and testing

equipment

was used.

3. 1.1

WR/JOs

AJAW 002 and

AWAY 002 - Inspect

and Calibrate the following 6.9KV

AC Distribution Ground Alarm Relays

- (Tag 1A-10:006):

Bus Tie lA to

1A4

Bus Tie lA to

1C

Bus Tie

1D to lA-SA

Bus Tie

1D to 1-4A

This calibration was accomplished

in accordance

with Process

Instrument

Calibration

(PIC) Procedure

PIC-E016,

Revision 6, Gould-Brown Boveria

Ground Fault Relay

GR-5 Calibration.

3.1.2

WR/JO

ADDG 001 - Preventive

Maintenance

on Air handling Unit 480

VAC

Motor - (Tag lAV-A93X:005):

This routine Preventive

Maintenance

(PH) was performed in accordance

with procedure

PH-E0009,

Revision 5,

480

VAC Motor Preventive

Maintenance.

~

~

~

~

3. 1.3

WR/JO AEHR 001 - Preventive

Maintenance

on Limitorque Operator for HVAC

Motor Operated

Valve

(HOV) - (Tag 1CZ-35:002):

This routine

PH was performed in accordance

with procedure

PH-I0020,

Revision 8, Limitorque Operator Inspection.

3. 1.4 WR/JO ABSN 002 - Preventive

Maintenance

on Condenser

Vacuum System

480

VAC Load Breaker - (Tag 1D3-3D):

This routine

PH was accomplished

in accordance

with procedure

PH-E0012,

Revision 9,

480

VAC ABB Type

LK Load Center Breaker

and Cubicle P.M.

3.1.5 Main Transformer Maintenance

The inspectors

reviewed the maintenance

practices for the main

transformers.

The following summarizes

the results of this review:

The main transformers

are maintained

by the licensee's offsite

Transmissions

Department

using Substation

Maintenance

Standards

(SHSs).

However, the site system engineer for the switchyard

coordinates

Transmissions

Department

maintenance activities for

the transformers with the site

and tracks results of the

Transmissions

Department

PHs.

The main transformers

are Maintenance

Rule components.

In

addition to tracking the Transmissions

Department

PH results,

the

Systems

Engineer performs weekly walkdowns in accordance

with site

10

procedure

THM-117, Revision 3, Plant Engineer

Walkdown,

Observation,

and Assessment

Procedure,

and records

and trends

a

number of parameters

for the transformers.

Parameters

trended

include, oil levels, winding/top oil temperatures,

oil dielectric

strength,

and various

gas concentrations.

The trending is

accomplished

in accordance

with site procedure

ADM-NGGC-0101,

Revision 2, Maintenance

Rule Program.

The inspectors

noted the following SHSs which defined the

Transmission

Department

program for PM of the transformers:

SHS-01 - Equipment Maintenance

Schedules

SHS-02

- Monthly Substation

Inspections

SHS-03-1

- Inspections

and Maintenance of Stationary

Power

Transformers

3. 1.6 Maintenance

Indicators

The inspectors

reviewed licensee

Haintenance

Indicators for the period

January

- Harch,

1996.

The following two indicators

were reviewed in

greater detail

and discussed

with maintenance

management:

Overdue

PHs - In January

1996, the backlog of overdue

PMs was

approximately

250.

The licensee

recognized this to be

a problem

and initiated corrective actions to evaluate

the significance of

the

PM items overdue

and eliminate the backlog.

The following

summarizes

the results of reviews

and discussions

with licensee

maintenance

management:

Nuclear Assessment

H-HA-96-01-12 identified the backlog of overdue

PHs

as being

a problem.

The problem

and corrective actions

are

documented

in

CR 96-0139.

Based

on discussions

with the

Maintenance

Manager,

the excessive

PM backlog occurred

due to

postponement

of work because

of (1) loaning maintenance

personnel

to the Robinson Plant for outage work, (2) extensive

pre-outage

effort for the Harris

RF06 outage,

and (3) the forced outage

immediately after RF06.

The backlog consisted of routine

PH tasks

and not TS or regulatory

required tasks.

An engineering

evaluation

determined that no

safety issues

existed

because

of the backlog.

Reducing the backlog of overdue

PHs has

been

a high priority, with

weekly status

reports provided to plant management.

By April 1,

1996,

the backlog

had

been

lowered to 22, which showed significant

progress

toward elimination.

Corrective Maintenance

(CM) Backlog -

In January

1996, the

CH

backlog

was approximately

800 work tickets.

On April 1,

1996, the

backlog

was still 809 work tickets.

The licensee

has also

11

3.2

recognized

the

CH backlog to be

a problem

and

has developed

plans

to work the backlog off to approximately

400 by the end of 1996.

Based

on discussions

with the Haintenance

Hanager,

the causes

for

the high

CH backlog are the

same

as for the high overdue

PHs.

The backlog

has

been prioritized with the most important jobs

(emerging work, maintenance

rule items,

open work-around items,

main control board items, etc.)

planned first.

Two backlog items,

in addition to routine work, are being assigned

to each work crew

with a goal of reducing the backlog

by approximately

64 tickets

per month.

By April 15,

1996, the backlog

had

been

reduced to 740

work tickets.

Surveillance

Observation

3.2.1

EST-724,

Shutdown

and Control

Rod Drop Test

The licensee

performed hot control rod drop testing using Engineering

Surveillance Test

EST-724,

Shutdown

and Control

Rod Drop Test Using

Computer,

Revision 4, to address

NRC Bulletin 96-01, Control

Rod

Insertion

Problems.

The inspector witnessed

the dropping of control

bank

A which was associated

with the higher burnup Westinghouse

Vantage

5 fuel.

The licensee

used

a contractor with sophisticated

computerized

data acquisition capabilities to record the data.

All of the rods in

the bank dropped within the required time of 2.7 seconds

(TS 3. 1.3.4).

The G-41 rod had the highest time of 2.288 seconds.

The inspector

observed that rebound occurred for this bank, indicating that sticking

problems

were not occurring.

The inspector

reviewed the

EST-724 results

which showed that the remaining rods were all less

than 2.0 seconds

in

drop time except rod J21 which took 2.068 seconds

to drop.

The

inspector

concluded that all rods met the Technical Specification

requirements.

The licensee

submitted the results of the testing to the

NRC on April 8,

1996, in a response

to the

NRC Bulletin.

The response

was consistent

with what the inspector

had observed.

3.2.2 HST-I0320, Revision 9, Train

B Solid State Protection

System Actuation

Logic 5 Haster Relay Test.

On April 2,

1996, the inspector

observed portions of this procedure

which tested logic and permissives

associated

with the "B" train SSPS.

This procedure satisfied,

in part, surveillance

requirements

contained

in TS Tables 4.3-1

and 4.3-2.

Procedure

section 7.5 directed operators

to verify the availability of Permissive

P-4 (Reactor Trip permissive

that actuates

a turbine trip and enables

the safety injection block and

reset logic,

among other items).

This was accomplished

by shutting the

"B" train reactor trip bypass

breaker,

depressing

an auto shunt trip

pushbutton,

verifying the "B" train (main) reactor trip breaker

opened,

and measuring

voltage across

two contacts

in the reactor trip breaker

switchgear cabinet.

The licensee

had previously installed

a permanent

voltmeter (hard-wired into the circuit) to take the voltage reading.

Step

28 directed operators

to verify that the meter read

48 volts (or

between

37 and

49 volts) when its selector switch was placed in the

"BY"

12

position.

While performing this step during the initial test run on

April 2, technicians

obtained

readings of zero voltage.

This indicated

that either the voltmeter switch contact

had not closed properly, or the

P-4 permissive

was not available.

The P-4 permissive

was appropriately

declared

inoperable until it could be satisfactorily tested.

Believing

that the problem was with the switch, technicians

used

a portable

voltmeter (appropriately calibrated)

and measured

the correct voltage

across

the contacts.

This confirmed that the earlier problem was with

the permanent

voltmeter selector switch. 'owever,

the P-4 permissive

remained

inoperable

because

the procedure'pecified

the use of the

permanently installed voltmeter and did not provide allowances for using

portable digital voltmeters.

The inspector

was informed by the licensee that

a deficiency tag

had

been previously initiated for the voltmeter selector switch.

This tag

was dated

February 2,

1996.

In reviewing the associated

work ticket,

WR/JO AA(Yl, the inspector

noted that it had identified

a similar

instance

where the switch contacts failed to close

on demand during this

procedure.

The work ticket had

recommended

the switch be replaced,

and

that the work be conducted

during the next plant outage

due to the risk

associated

with a plant trip.

Discussions with plant personnel

indicated that the ticket was coded for the next refueling outage.

In

the interim, technicians

had planned to work around the deficiency by

"jogging" the switch until proper contact closure

was

made

and the

acceptable

voltage obtained.

Discussions with personnel

indicated that

this practice

had worked in the past,

however, it did not work on

April 2,

1996.

Consequently,

the licensee

had to initiate a temporary

procedure

change to allow the use of the portable voltmeter.

The time

associated

with the procedure

change required that the technicians

reopen the reactor trip bypass

breaker,

and continue through

a 48-hour

TS limiting condition for operation

(LCO) for the P-4 permissive.

Additionally, because

of the delays during the test

and the time

associated

with restoring the breaker alignment,

the two-hour limit for

having the bypass

breaker shut

was exceeded,

placing the licensee

in a

six-hour shutdown action statement

in accordance

with TS

LCO 3.3.2.

This action statement

was exited within minutes

when the bypass

breaker

was opened.

The procedure

was later changed

and the test re-performed.

During the

second

attempt,

the voltage reading slightly exceeded

the upper limit of

49 volts using the portable meter.

Licensee

engineering

personnel

evaluated this voltage reading to be acceptable.

The P-4 permissive

was

then declared

operable

and the 48-hour

LCO exited.

The selector switch

was replaced later that day

and the

HST was re-performed with

satisfactory results.

The inspector

concluded that this test evolution involved several

examples of negative

performance.

First,

a previously identified

deficiency

had

been

ignored

by technicians

who decided to use the

permanent

voltmeter anyway.

Secondly,

the switch replacement

had

been

coded for the refueling outage

due to the risk associated

with possibly

tripping the plant.

The licensee

had completed

a week-long forced

13

3.2.3

outage

on March 29, just days before this test

was scheduled,

yet the

work ticket was not considered for work during the shutdown.

10 CFR 50, Appendix B, Criterion XVI, Corrective Actions requires that

measures

be established

to assure

that conditions

adverse to quality,

such

as deficiencies

and defective material

or equipment,

are promptly

identified and corrected.

This requirement is further delineated

in

Revision

18 to the licensee's

Corporate guality Assurance

Program

manual.

The failure to promptly correct the deficiency associated

with

the selector

switch contributed to the licensee

entering

two TS

LCOs and

is contrary to those requirements.

This is identified as example

two of

Violation 50-400/96-04-02:

Inadequate

Corrective Action, Failure to

Correct Voltmeter Switch Deficiency.

OST-9018T,

Revision 0, Test of the

A Train Sequencer

Blocking Functions,

18 Month Interval.

This temporary test procedure

was developed to test several

blocking

relays in the emergency

safeguards

sequencer

panels.

These

relays'unction

were to ensure that normal process

demand signals

were blocked,

thereby preventing non-essential

or undesirable

safety loads from

energizing

and overloading the emergency diesel.

The licensee

had

previously identified (as part of the review per Generic Letter 96-01,

Testing of Safety-Related

Logic Circuits) that these

blocking relays

had

not been properly tested.

The inspector

observed testing activities

under the "A" train procedure,

although

a similar procedure

was

developed to test the "B" train components

which had also

been missed

previously.

The fact that these

components

had not been previously

tested

required that the licensee

enter

TS

LCO 4.0.3,

which allowed

24

hours to complete the testing or declare

the affected

system inoperable.

After 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />,

because

both trains of the emergency

sequencer

were

involved, the licensee

entered

TS

LCO 3.0.3.

This ultimately lead to a

TS-required

shutdown

when delays

associated

with the procedure

and other

unrelated plant equipment

problems occurred

as discussed

in paragraph

2.1 of this report.

The inspector

observed

good workmanship during the procedure.

Steps

were appropriately followed,

and the procedure

accomplished

the stated

goal of verifying proper relay actuation.

One stumbling block occurred

during the initial test while performing Section 7.4.

While all other

continuity readings

had

been

measured

in ohms (resistance),

one of the

data points in Section 7.4 was specified in voltage (potential).

The

procedure's

authors

expected to see potential

across

the contacts

associated

with this particular step.

During the test,

technicians

measured

zero volts (DC), requiring

an evaluation

and procedure rewrite

to specify acceptance

criteria in ohms.

This correction

was

made

and

the procedure

completed satisfactorily later that night after the plant

was shut down.

The delays

associated

with the error in Section 7.4 may

have contributed to the forced shutdown,

however, this complex procedure

was well coordinated

and implemented.

1 4

3.2.4

HST-

T-I0026, Revision 6,

Steam Generator

B Narrow Range level

(L-0484)

Calibration

WR/JO

AAGS 001 - Calibration of Steam Generator

(SG)

2B Narrow Range

Level

Loop L-0484 Protection

Set I covered the surveillance of the

2B SG

Narrow Range

Level

Loop to meet

TS 3/4.3. 1, 3/4.3.2,

and 3/4.3.3.6.

Requirements

were also specified in paragraphs

3. 1.17, 7.2.2.2.3.10

7.3.2.2.10.1

and 15.0.6 of the

FSAR.

3.2.5 HST-I0270, Revision 4,

Lo-Lo T., P-12 Interlock (T-0432) Operational

WR/JO AFZA 017 - Operational

Check of Loop T-0432 Lo-Lo T., P-12

Interlock covered the surveillance of Loop T-0432 Lo-Lo T., P-12

Interlock to meet Table 4.3-2,

Item 10b, of the TS.

Requirements

were

also specified in paragraphs

3.1. 17, 7.3.2.2. 10. 1 and 15.0.6 of the

3.2.6

HST-

.

.6 HST-I0126, Revision 4, Main Steamline

Pressure,

Loo

(P-0475)

Operational

Test

e,

oop

-

),

WR/JO AASH 017 - Operational

Test of Hain Steam

(HS) Line Pressure

Loop

1 P-0475 Protection

Set III covered the surveillance of the

HS Line

Pressure

Loop

1 P-0475 Protection

Set III to meet

TS 3/4.3.1, 3/4.3.2,

and 3/4.3.3.6.

Requirements

were also specified in paragra

hs 3. 1. 17

7.3.2.2. 10. 1 and 15.0.6 of the

FSAR.

Du

'

'

ai

e

in paragraphs

During observation of the surveillance activities

d t

'1

d

'

,

and 3.2.6 above,

the inspectors

reviewed qualification

records for IRC technicians

performing the surveillances.

A

gualification Checkout

Card System

(gCC)

was

used to

ualif

and

document qualifications.

Inn accordance

with Training Program Procedure

-102, Revision 2,

Conduct of On-The-Job Training

and Task

Performance

Evaluation, re-qualification review was re

'

years

(maximum 30 months).

equire

every two

The qualification status for all personnel

with'

maintained

b

the suerv'n

a wor

crew was

y

e supervisor of the crew.

Training procedures

provided

kee t

a gualification Checkout

Card matrix as

a tool for th

~

~

~

o

or

e supervisor to

not

a mandator

re

p

rack of qualifications for his crew.

The matrix

t

1

d

y

equirement.

In reviewing the matrix for the supervisor

ix was

a

oo

an

of the personnel

performing the surveillances

of par agraphs 3.2.4,

3.2.5,

and 3.2.6 above,

the inspectors

noted that

2 technicians

had

exceeded

the 30-month re-qualification review.

One of the two had

performed

one of the surveillances

observed.

His re-qualification

review was

due in April 1994.

The other technician

was due for re-

qualification in June

1995.

For the individual due in June

1995,

within

official records

showed

he did receive the re-qu 1'f

in the required time,

even though the supeqvisor's

matrix showed

otherwise.

No records

were found to show the other individual had

received his re-qualification review.

15

The licensee

issued

CR 96-1001 to document this issue

and took immediate

corrective actions for this problem.

The following summarizes

the

corrective actions taken

and the results

obtained

by the licensee:

The technician

was not allowed to perform any work that required

OCCs until the official Document Control records

could be reviewed

to determine if records

could be retrieved to support his re-

qualification review.

No records

were found.

Therefore,

the re-

qualification review was performed to bring the individual's

qualification up to date.

No problems

were identified in the re-

qualification review.

The technician's training records

were reviewed

and compared with

other

I&C technicians

on similar job responsibilities.

The

records

showed his training was in alignment with his peers

and

continued participation in routine

IEC training and attendance

in

appropriate

specialty training.

In addition, maintenance

management

reviewed the individual's work practices

over the

period in question

and found no evidence of degraded

performance.

Maintenance

and Training supervisors

reviewed the maintenance

staff qualification status

and identified no additional

occurrences

of lapsed qualifications from not performing prompt

re-qualification reviews.

In addition, Training management

reviewed qualification status for the Environmental

and Radiation

Control personnel,

who have re-qualification requirements

similar

to the Maintenance

Department,

and found no errors.

The Training organization

began

a process

in January

1996,

of

listing all qualifications

on the station's

computerized training

tracking system

and considered

the loading process

would have

identified the one error found above

and corrections

would have

been taken.

The new computerized

system will enable

anyone to

view the qualification record

and status

at any time and can

be

used to automatically forecast expiration dates

and

keep

supervisory

personnel

informed of qualification status.

The licensee is currently reviewing the existing two-year re-

qualification process

and considering replacing the two-year

across-the-board

requirement with a process

w'hich includes

a

routine training/retraining

program for critical (to safety or

operations),

infrequently performed,

and difficult tasks.

This

review and resulting actions

are expected to be complete

by June

1996.

The inspectors verified the above corrective actions

by reviewing the

following documentation:

MEMO to File dated April 18,

1996

gualification Review Form dated April ll, 1996 for technician

whose qualification had lapsed

I

Condition Report 96-01001

16

Training Record history for technician

whose qualification had

lapsed

The technician that performed the observed

surveillance

was also not re-

qualified.

Failure to follow procedures

for Re-qualification

Review is

identifed

as

a violation of 10 CFR 50, Appendix B, Criterion V.

This

ailure constitutes

a violation of minor significance

and is being

treated

as

a Non-Cited Violation, consistent with Section

IV of the

NRC

Enforcement Policy.

This item is designated

as

NCV 50-400/96-04-03,

Failure to Follow Procedure for Re-qualification of Maintenance

Personnel.

This item is closed.

3.3

Close Out Issues

- Maintenance

3.3.1

(Open)

VIO 400/95-17-02:

Failure to Provide Adequate Instructions for

Repairing Isolation Valve Pressure

Sealing

Surfaces

This violation involved failure to provide adequate

procedures for

repair of Hain Feedwater

Isolation Valve 1FW-217 and Pressurizer

PORV

PCV-444B.

The cause of the problem was attributed to a failure to

properly implement Regulatory

Guide

(RG) 1.33,

Appendix A.

The inspectors

reviewed the following documentation

to verify that

appropriate corrective actions

had

been identified and performed:

Procedure

CH-H0204, Revision 2, Hain Feedwater

Isolation Valves

HFIVs.

(MFIV), which provided appropriate instructions for repa'r f

1

0

A Maintenance

memorandum

and flowchart, dated January

9,

1996,

which implemented

a review process

to determine

when procedures

are required

by

RG 1.33.

If a procedure is required for a

maintenance activity and is not available,

one will be developed

before the maintenance

is allowed to proceed.

Internal

memorandum,

dated January

9,

1996,

documenting review

with maintenance

and training personnel

of the causes

and

circumstances

of this violation.

Procedure

CH-H0206, Revision 0, Pressurizer

Power Operated Relief

Valve (PORV), which provided appropriate instructions for

disassembly,

inspection,

and re-assembly of PORYs.

Action Item 5 of CR 95-03003,

which documented

review of

maintenance activities which could affect performance of safety-

related

equipment in accordance

with

RG 1.33 to identify those

components

requiring detailed procedures.

The review included

greater

than 20,000

EDBS safety-related

tags to determine if

procedures

existed.

In addition, maintenance

procedure lists from

other licensee sites

and other utilities were reviewed.

This

0

17.,

effort identified the need for an additional

18 procedures.

At

the time of this inspection,

only a few of these

procedures

had

been written.

However,

as noted

above,

maintenance

on the

components will not be allowed until procedures

are written and

issued.

3.4

Action Items 6, 7, 8,

and

9 of CR 95-03003,

which documented

review of procedures

in other areas to ensure

proper

implementation of RG 1.33

and

TS 6.8. l.a.

This violation remains

open pending further reviews to verify issuance

of the additional

18 procedures

identified by the licensee's

review.

Review of LERs - Haintenance

(Open)

LER 400/96-002:

Failure to Properly PerForm Technical

Specification Surveillance Testing.

This

LER was supplemented

twice during the inspection period

as

additional findings were discovered

by the licensee

during

a continuing

review per Generic Letter 96-01.

LER Supplement

96-02-02

was issued

on

Harch 22,

1996

and discussed

three additional

missed surveillance

requirements.

These involved logic testing for control

room ventilation

fans which start

on high radiation signals, ventilation dampers

associated

with the reactor auxiliary building electrical

equipment

protection

room,

and trip actuating device operational

testing for the

main feedwater

pump trip following safety injection actuation.

LER

Supplement

96-02-03

was issued

on April 10 and discussed

two additional

missed requirements.

One of these

involved

a "channel

out of service"

alarm test or control

room annunciation verification for four radiation

monitors.

The second

involved the blocking relays associated

with the

emergency

safeguards

sequencers.

This latter item was discussed

in

report paragraph 3.2.3.

Hecause

the plant entered

TS 3.0.3.

and later

completed

a TS-required plant shutdown

due to the missed

sequencer

surveillance

requirements,

the licensee

reported

these

events

under the

same

LER.

The inspector determined that the

LER supplements

appropriately

described

the circumstances

for these

events.

LER 400/96-02

and its

supplements will remain

open until the licensee

completes its Technical

Specification Surveillance

Review program later this year.

At that time

the inspector will review the licensee's

long-term corrective actions

for the deficiencies

and causes

noted.

3.5

Conclusion

- Haintenance

One cited violation and

one non-cited violation was identified.

The

cited violation involved failing to correct

a documented

deficiency

on

an installed voltmeter switch prior to using it in a surveillance

(paragraph 3.2.2).

The non-cited violation involved failure to follow

procedure for re-qualification of maintenance

personnel

(paragraph

3.2.6).

4.0

4.1

4.1.1

18

Overall, for the activities observed,

the inspectors

concluded that the

maintenance

and surveillance

programs

were being effectively

implemented.

The activ'ities observed

were planned

and conscientiously

executed

in accordance

with detailed

procedures.

Personnel

appeared

to

be well qualified for the task performed.

Interface

between

Maintenance

and Operations

personnel

was good.

Extensive detailed trending'f important parameters

was being performed

by the system engineer for the main transformers.

The maintenance

backlogs for corrective maintenance

work tickets

and

overdue

PMs has

been high.

However, the overdue

PM backlog

has

been

significantly reduced with plans to eliminate it.

A reduction plan for

the

CH backlog is being worked with a goal to cut the backlog in half

during 1996.

ENGINEERING (37551,

40500,

92700,

92903)

Onsite Engineering

Feedwater

Isolation Valve Problem

On March 19,

1996, the system engineer

had noted

a flow reduction trend

on the main feedwater line.

The trend

showed

a change

in the split in

flow between

the normal feedflow path to the steam generator

and the

bypass flow through the

AFW feed line path.

This split is normally 80

percent

through normal feedwater

and

20 percent through the bypass line

but on March 4,

1996,

had changed to 70/30.

The trend indicated that

the reduction

had occurred

when the feedwater isolation valve was

stroked in accordance

with surveillance

procedure

OST-1018.

Condition

Report 96-00774

was written to document this problem.

On March 22,

1996, during the forced shutdown,

the licensee

cycled the valve and

determined that there

was

a problem.

The licensee

drained the

B steam

generator

and disassembled

the

B feedwater isolation valve (a wedge gate

valve).

The valve stem was found broken just prior to where the stem

and disc connect.

Condition Report 96-00792

was initiated to document

the problem

and Engineering Service

Request

96-00168

was initiated for

engineering

assistance

in determining the cause of the failure.

Metallurgical analysis of the valve stem indicated

low cycle fatigue

as

the failure mechanism.

The analysis

also confirmed that the stem was

made from 17-4 ph stainless

steel

which had

been properly heat treated.

The stem was part of the original installation prior to 1986

and

had in

excess of 133 valve cycles.

Inspection of the valve, disc and bonnet

revealed

marks where the disc and bonnet

had

come in contact.

The valve

is not designed for the disc and bonnet to come in contact,

but is

designed for the stem to backseat

in the bonnet under hydraulic

pressure.

The contact points were offset from the valve centerline

by

approximately

1/4 inch.

The valve is also oriented approximately

50

degrees

from vertical.

The licensee

consulted with the valve

manufacturer

and

an engineering

consulting

company.

The licensee

19

concluded that the following factors

had contributed to the failure of

the stem:

1.

The backseat

was deeper

than normal in the bonnet.

2.

With the valve oriented at 50 degrees

from vertical, the disc was

riding on the lower side valve disc guides.

These

two resulted

in the disc hitting the bonnet in a 1/4 inch offset

from center causing

a bending

moment

on the stem.

Computer modeling by

the engineering

consultant

confirmed that the bending

moment

on the stem

was sufficient to have caused

low cycle fatigue failure based

on the

number of cycles the stem

had received.

The crack initiation point on

the stem identified by the metallurgical failure analysis

matched with

that predicted

by the computer analysis.

The licensee,

after consultation with the valve manufacturer,

modified

a

replacement

stem

based

on the above conclusions

and measurements

taken

in the field to ensure that. the bonnet

and disc would not

come in

contact.

The modified stem design did not change

the stem weak link

analysis.

The valve was reassembled

with the modified stem

and was

checked to make sure the disc and bonnet did not come in contact

when

the stem was in the backseat.

The licensee's

analysis

showed that the other two feedwater

isolation

valves

have relatively new stems with approximately

20 cycles each.

They were both disassembled

in the last two years

due to unrelated

problems.

The licensee

stated that valve disc to bonnet contact

marks

were not evident

when the other two valves

were disassembled.

The inspectors

reviewed the metallurgical failure analysis,

observed

the

failed stem under the microscope

at the licensee's

metallurgical lab,

and discussed

the failure mechanism with the metallurgist.

The

inspectors

viewed the disassembled

valve and valve parts,

including the

stem,

and confirmed that the disc and bonnet

had

made contact.

The

inspector

attended

the

PNSC meeting where the root cause of the failure

was discussed.

The inspector

concluded that the licensee

had done

a

good job of investigating the failure.

4.1.2 Auxiliary Feedwater

Flow Control Valve Deficiency

The inspectors

reviewed system engineer activities associated

with the

three automatic flow control valves for the motor-driven

AFW pumps.

Each valve controls

AFW flow to one of the steam generators

and is in

the

AFW flowpath upstream of the motor-operated

AFW isolation valves

near the containment building penetrations.

Operators

used the flow

control valves during the forced outage

in Harch

1996

and in prior

outages

to control

steam generator levels within their required

operating

bands.

After entering

Hode

4 on Harch 23,

1996, operators

noted that two of the three valves failed to open under high

differential pressure

(AFW pump discharge

pressure

minus steam generator

pressure).

Operators

had worked around this problem in the past

by

20

4.2

4.2.1

shutting the motor-driven

AFW isolation valves,

thereby reducing the

differential pressure

across

the flow control valves.

The valves would

then

open allowing operator control of AFW flow.

The

AFW system engineer

had

been investigating this operator work-around

just prior to the recent plant shutdown

and

had documented this in a

CR

after discussing it with off-shift operators 'the week before.

The newly

assigned

engineer

had just recently

become

aware of the sticking problem

and

had raised operator

awareness

to the point where they should provide

feedback

on any related recurrences.

After the sticking in Harch, the

engineer

decided that

a special

surveillance test should

be performed

prior to exiting Hode

4 to determine

SG pressures

under which the valves

were sticking.

This testing would provide data points below which the

valves would have to be administratively maintained full open or the two

motor-driven

AFW pumps would be declared

inoperable.

Such

a test

was

developed

and completed during plant heatup activities at the

end of the

Harch outage.

Based

on the results of this test

(EPT-711,

Revision 0,

Hotor Driven Auxiliary Feedwater

Pumps

Flow Control Valve Stroke Test),

plant personnel

determined that the two AFW pumps should

be declared

inoperable

any time these

valves were less

than full open with steam

generator

pressures

less

than 320 psig.

The inspectors

considered this deficiency to represent

a significant

operator work-around.

It required that operators

perform special

manipulations to open the flow control valves in Hode

4 or Hode

3 while

at low steam generator

pressures

with the

AFM pumps running.

These

manipulations

(shutting motor-operated

isolation valves prior to opening

flow control valves)

could

be pe}formed from the main control

room and

were covered in auxiliary feedwater

system operating procedures.

The

new system engineer's

efforts in raising the awareness

of these

deficiencies to plant management's

attention

was commendable.

At the

end of the inspection period, the system engineer

had communicated

the

sticking problems to the valve vendor for consideration

as

a potential

application or design deficiency.

Review of LERs - Engineering

(Closed)

LER 94-003:

Improperly Analyzed Single Failure in Emergency

Service Mater

This

LER reported the event that was the subject of Violation

400/94-21-01.

The inspector reviewed the

LER corrective actions

and

determined that they were the

same

as those for the violation.

The

violation was closed in paragraph

4.3 below.

This item is closed.

4.2.2

(Open)

LER 400/96-006:

Feedwater Isolation Valve Stem

and Disk

Separation.

This

LER was related to the forced shutdown discussed

in paragraphs

2. 1

and 4. 1. I above.

The licensee

plans to revise Corrective Haintenance

Procedure

CH-H0204 by August 31,

1996 to include verification that the

21

4.3

feedwater isolation valve disc does not strike/contact

the bonnet.

This

item remains

open.

Close Out Issues

- Engineering

4.3.1

(Closed)

VIO 400/94-21-01:

Inadequate

Design Control for

ESW

System/CSIP

Coolers

This violation was issued

because

two independent trains of emergency

service water were not achieved for all postulated

single failure

conditions.

With the existing valve lineups, train cross-connects

existed at each of the charging

pump coolers which would have allowed

backflow of hot water causing

pump damage

when the single failure of

auxiliary reservoir return valve

1SW-270 was postulated.

The licensee

corrected this problem by closing the charging

pump cooler cross-train

valves.

The Emergency Service

Water system flow drawings

CPL-2165-S-

0547

and CAR-2165-G-047 were revised to reflect the

new positions

as

well as Operating

Procedure

OP-139,

Service

Water System,

Revision 6.

The inspector field-verified the valve positions, verified that the

drawing changes

were made,

and verified that the operating

procedure

had

been

changed.

Single failure training was given to the onsite

engineers.

The inspector reviewed the attendance

records for the

training and concluded,

based

on sampling, that the engineers

received

the training.

The licensee

also performed

a review of other decay heat

removal

systems for similar cross-connect'problems

and self-initiated

a

Service

Water System Operational

Performance

Inspection.

No other

similar problems

were found.

This item is closed.

4.3.2

(Closed) IFI 400/94-12-01:

Review of Licensee Activities to

Upgrade/gualify

AFW MOVs for Higher Thrust Values

This item was

opened

because

the licensee

had increased

the torque for

several Auxiliary Feedwater

Valves above the calculated

long term

allowable.

The short term values

(extended thrust ratings)

were

determined

through engineering

evaluation

PCR 7284 to be acceptable

until the end of refueling outage

6 (October 1995).

The valves were

qualified for

a higher thrust rating on

a short term basis to ensure

valve closure.

This item was

opened to track the licensee

long term

resolution

and ensure that long term valve damage

would not occur.

The inspector

reviewed Engineering Service

Request

ESR 95-00021 which

evaluated this condition for long term acceptability.

The

ESR

determined that

a 98 percent

closed torque switch bypass

would allow the

torque switches to be set at

a minimum value which removed

them from

short term operability status.

The valve disc will cover the valve

seating

surface

by 98 percent of the stroke.

The new setup

was

determined to allow the full output of the

MOV motor to isolate flow but

does not over thrust the valve when seating it.

Two valves,

lAF-55 and

lAF-74, had

been set at the higher thrust ratings although several

others

had

been qualified for it.

The inspector

reviewed the work

request/job

orders that implemented the changes for the subject valves

(WR/JOs

95-ABKH1, 95-ABKI1, 94-AHUZ1, 95-ABMU1, 94-AHWB1, 94-AHWB1, 95-

22

4.3.3

ABNWl, 95-ABNTl, 94-AHWC1, 95-ABNU1, 94-AHWDl).

The work orders reset

the torque values for the two valves

and set the torque switch bypass

for all the valves.

The documentation

supported that the described

changes

had

been

implemented.

The two valves that had their thrust reset,

1AF-55 and 1AF-74, were

post-modification tested

using

a dynamic test at design basis

differential pressure

conditions per Engineering Periodic Tests

EPT-301,

revision 1/1, for 1AF-55 and

EPT-302, revision 1/2 for 1AF-74.

In

addition,

lAF-93 was dynamically tested.

The inspector

reviewed the

test results

and determined that they met the test criteria.

The other

valves,

which were identical,

were diagnostically tested

under static

conditions.

This item is closed.

(Closed)

IFI 400/94-17-02:

Biofouling Potential

in

ESW Systems.

This item was

opened

because

the licensee

found, some asiatic

clams in

the service water intake structure.

A program of monitoring the

ESW

system through periodic inspection of components

had

been ongoing.

At

the time the

ESW system

was not being chlorinated,

although the

circulating

and normal service water systems,

and the cooling tower

basin were under continuous chlorination.

The licensee clarified/revised their commitment in relation to

chlorination in an April 16,

1996 submittal.

The revision was based

on

experience

with intermittent chlorination with sodium hypochlorite.

The

change did not revise what systems

would be chlorinated,

but did

identify action that was being taken to control

and identify the spread

of the asiatic clams.

This included inspecting the intake structure

where the clams were first identified.

The inspector verified that

procedure

PLP-620,

Service

Water Program

(Generic Letter 89-13),

Revision

1, contained that requirement.

The inspector discussed

the

inspection results with licensee

personnel

who indicated that there

have

been

no clams found in the service water systems,

only in the intake

structure.

They stated that when the clams are found during the

inspection,

they are removed.

Procedure

PLP-620 also requires safety-

related

heat

exchangers

to be inspected.

There

has

been

no evidence of

biofouling from these

inspections.

The inspector concluded that their

was

no evidence that the clams

had spread into the service water systems

and that the licensee

program

was effective in preventing their spread.

This item is closed.

4.4

Conclusion

- Engineering

Engineering

was challenged

during the period by the Technical

Specification Surveillance

Review Program

and the two forced outages.

Engineering

performed

good root cause

analyses

and supported

the

operations

organization well during the period.

0

E

j

5.0

5.1

5.2

23

PLANT SUPPORT

(71707,

71750,

40500,

92700,

92904)

Plant Housekeeping

Conditions

The inspectors

found plant housekeeping

to be adequate.

Radiological Protection

Program

The inspectors

reviewed radiation protection control activities to

verify that these activities were in conformance with facility policies

and procedures,

and in compliance with regulatory requirements.

The

inspectors

also verified that selected

doors which controlled access

to

very high radiation areas

were appropriately locked.

Radiological

postings

were likewise spot checked for adequacy.

On April 10,

1996,

the licensee

had two personnel

contamination

events

which were related

to the resin transfer

issue

discussed

in paragraph

2.5. 1.

Radiological

protection personnel

did

a good job of containing

and cleaning

up the

contamination.

5.3

5.4

Security Control

During this period, the inspectors

toured the protected

area

and noted

that the perimeter

fence

was intact

and not compromised

by erosion or

disrepair.

The fence fabric was secured

and barbed wire was properly

installed.

Isolation zones

were maintained

on both sides of the barrier

and were free of objects which could shield or conceal

an individual.

The inspectors

observed

various security force shifts perform daily

activities, including searching

personnel

and packages

entering the

protected

area

by special

purpose detectors

or by a physical

patdown for

firearms,

explosives

and contraband.

Other activities included vehicles

being searched,

escorted

and secured;

escorting of visitors; patrols;

and compensatory

posts.

In conclusion,

the inspectors

found that

selected

functions

and equipment of the security program complied with

requirements.

Fire Protection

5.5

The inspectors

observed fire protection activities, staffing and

equipment to verify that fire alarms,

extinguishing equipment,

actuating

controls, fire fighting equipment,

emergency

equipment,

and fire

barriers

were operable.

During plant tours, the inspector looked for

fire hazards.

The inspector

concluded that the fire equipment

and

barriers

inspected

were in proper physical condition.

Emergency

Preparedness

On Harch 21,

1996 the inspectors

observed portions of an

EP drill

exercise

in the plant simulator control

room and the

Emergency Operation

Facility.

Each of the four site emergency

teams

were receiving the

same

training and the

same scenario.

Three of those

teams

were observed

during the last reporting period

as documented

in IR 50-400/96-02.

This

5.6

was the first series of exercises

that the Harris Plant simulator was

utilized to simulate plant conditions

and feed information to the

ERFIS

data display screens

in the Technical

Support Center

and

Emergency

Operation Facility.

The inspector considered

the performance of the

emergency

teams to be adequate.

The inspector discussed

the use of the

simulator-fed

ERFIS displays with several

Emergency Operation Facility

team members

including the Director.

The overwhelming response

was that

it enhanced

the realism of the drill and simplified communication flow.

The inspector

noted that several

additional

issues

were

added to the

scenario for this performance

as

compared to the previous three

discussed

in IR 50-400/96-02.

The additions

improved the scenario.

Licensee Self Assessment

The licensee's

Nuclear Assessment

Section

completed

two assessments

this

month,

as listed below.

The inspectors

reviewed the assessments,

discussed

the findings with the licensee

NAS organization,

and concluded

that the assessments

were thorough

and resulted

in substantive

findings.

Areas

assessed

were:

Inservice Inspection

and Testing Functions

Assessments

(H-ISI-96-01)

Emergency

Preparedness

Program Assessment

(H-EP-96-01)

The inspectors

identified no violations or deviations in the Nuclear

Assessment

area.

5.7

Review of LERs - Plant Support

(Closed)

LER 94-005:

Failure to Perform Analysis Prior to Release

This

LER was issued to report

a failure to perform an analysis of the

Treated

Laundry and Hot Shower Tank prior to release

as required

by

Technical Specification Surveillance

Requirement

4. ll.l.l.l.

Licensee

personnel

took the sample but entered

the wrong counting detector into

the computer

when the analysis

was performed.

The release

was

made with

erroneous

values

on the discharge

permit.

When the problem was

discovered

several

hours later during

a radiation monitor trending

evaluation,

the sample

was reanalyzed

and the discharge

permit was

updated to the correct value.

The licensee

counseled

the personnel

involved and briefed the other applicable

department

personnel.

The

licensee's

analysis

concluded that there

was

no adverse

safety

consequences

because

the sample reanalysis

showed

no abnormal

radioactivity levels

and because

the radiation monitor that monitored

the release

was set at

a conservative

value

and

showed

no abnormal

radioactivity levels.

The inspector reviewed the

LER, the licensee's

Adverse Condition

and

Feedback

Report (94-02763-4),

the

human factors

analysis,

and concluded that the licensee

had completed the corrective

action.

The inspector

concluded that this was

an isolated instance of

personnel

error that resulted in no radiological

consequences.

This

item is closed.

25

5.8

6.0

Conclusion

Plant Support

The inspectors

found plant housekeeping

and material condition of

components

to be adequate.

The licensee's

adherence

to radiological

controls, security controls, fire protection requirements,

emergency

preparedness

requirements

and

TS requirements

in these

areas

was

satisfactory.

OTHER

NRC

PERSONNEL

ON SITE

7.0

On Harch

19 - 20,

1996, Hr. Johns

Jaudon,

Deputy Director, Division of

Reactor Safety,

was

on site to tour the facility and discuss

previous

issues relating to the

SALP board meeting

on April 3,

1996.

On Harch 29,

1996, Hr. Jon Johnson,

Deputy Director, Division of Reactor

Projects,

was

on site to tour the facility and discuss

previous

issues

relating to the

SALP board meeting

on April 3,

1996.

SPECIAL

FSAR REVIEW

A recent discovery of a licensee

operating their facility in

a manner

contrary to the Updated Final Safety Analysis Report

(UFSAR) description

highlighted the need for a special

focused review that compares

plant

practices,

procedures

and/or parameters

to the

FSAR descriptions.

While

performing the inspections

discussed

in this report,

the inspectors

reviewed the applicable portions of the

FSAR that related to the areas

inspected.

The following inconsistency

was noted

between

the wording of

the

FSAR and the plant practices,

procedures

and Technical

Specifications

by the inspector

and licensee.

The licensee

entered

TS 4.0.3

when

a review for condition report 96-1137

revealed that control

room ventilation had not been tested

per Technical

Specification Surveillance

Requirement 4.7.6.d,3

in that the positive

pressure

was only measured

in reference to one adjacent

area,

not all

adjacent

areas.

In discussing this issue at the

PNSC meeting

on

April 27,

1996, the licensee

and inspector discovered that the

TS and

FSAR were in conflict with respect to the computer

room being adjacent

to the control

room.

FSAR Section 9.4.9. 1. 1 states

that the computer

room will be maintained at

a positive pressure

to prevent

inleakage of

the surrounding

environment.

This was in conflict with the control

room

ventilation

TS bases

which requires

the control

room ventilation

be

maintained

at

a positive pressure

with respect to adjacent

areas,

including the computer

room.

This issue

was resolved

by performing

a

modification under

a

10 CFR 50.59 review to the plant ventilation

system.

The modification placed the computer

room ventilation system in

a configuration that will not pressurize

the computer

room.

The

licensee

was planning to issue

a

FSAR change to include this item.

Due to several

FSAR discrepancies

noted in this report

and in

IR 400/96-02

URI 400/96-04-04 Tracking

FSAR Discrepancy

Resolution is

opened.

Inspector

Followup Item 400/96-02-04,

Tracking Licensee's

Progress

in Resolving

FSAR Spent

Fuel

Pool Cooling Discrepancies

is

26

closed.

The licensee

has

scheduled

a meeting

on Hay 30,

1996 with the

NRC, in Washington, to discuss their approach

to deal with CP&L FSAR

discrepancies

at all of their sites.

8.0

EXIT

The inspection

scope

and findings were summarized

on April 30,

1996,

by

the Senior Resident

Inspector with those

persons

indicated

by an

asterisk in paragraph

1.0.

An interim exit was conducted

on April 12,

1996.

The inspector described

the areas

inspected

and discussed

in

detail the inspection results.

A listing of inspection findings is provided.

Proprietary information

is not contained

in this report.

Dissenting

comments

were not received

from the licensee.

~T

e

Item Number

NCV

96-04-01

VIO

96-04-02

NCV

96-04-03

URI

96-04-04

Status

Open/Closed

Open

Open/Closed

Open

Descri tion and Reference

Inadequate

Procedure for

Placing Pressurizer

Haster

Pressure

Controller in

Automatic,

Paragraph

2.3. 1. 1.

Inadequate

Corrective Action:

1) Failure to Correct Resin

Venting Problems,

Paragraph

2.5. I;

2) Failure to Correct

Voltmeter Switch Deficiency,

Paragraph

3.2.2.

Failure to Follow Procedure

for Re-qualification of

Haintenance

Personnel,

Paragraph

3.2.6.

Tracking

FSAR Discrepancy

Resolution

IFI

94-12-01

IFI

94-12-02

IFI

94-17-02

Closed

Closed

Closed

Review of Licensee Activities

to Upgrade/gualify

AFW HOVs

for Higher Thrust Values,

Paragraph

4.3.2.

Review the Licensee's

Transition of Work Control

Following Startup

from an

Outage,

Paragraph

2.6.

Biofouling Potential

in

ESW

Systems,

Paragraph

4.3.3.

VIO

94-21-01

VIO

95-17-02

Closed

Open

27

Inadequate

Design Control for

ESW System/CSIP

Coolers,

Paragraph

4.3.1.

Failure to Provide Adequate

Instructions for Repairing

Isolation Valve Pressure

Sealing Surfaces,

Paragraph

3.3.1.

IFI

96-02-04

LER

94-003

LER

94-005

LER

96-002

LER

96-006

9.0

ACRONYMS

Closed

Closed

Closed

Open

Open

Tracking Licensee's

Progress

in Resolving

FSAR Spent

Fuel

Pool Discrepancies

Improperly Analyzed Single

Failure in Emergency Service

Water,

Paragraph

4.2. 1.

Failure to Perform Analysis

Prior to Release,

Paragraph

5.7.

Failure to Properly Perform

Technical Specification

Surveillance Testing,

Paragraph

3.4.

Feedwater

Isolation Valve Stem

and Disk Separation,

Paragraph

4.2.2.

AFW

ALARA

CFR

CM

CR

CSIP

EDBS

EDG

EOP

EP

ERFIS

ESR

FSAR

g pill

HVAC

IS,C

IFI

IR

KV

Auxiliary Feedwater

As Low As Reasonably

Achievable

Code of Federal

Regulations

Corrective Maintenance

Condition Report

Charging/Safety

Injection

Pump

Engineering

Data

Base

System

Emergency Diesel

Generator

Emergency Operating

Procedure

Emergency

Preparedness

Emergency

Response

Facility Information System

Engineering

Service

Request

Final Safety Analysis Report

gallons per minute

Heating Ventilation and Air Conditioning

Instrumentation

and Control

Inspector

Follow-up Item

Inspection

Report

Kilovolts

LCO

LER

NFIV

NOV

HS

HSIV

HST

NW

NAS

NCV

NRC

NRR

NSW

OST

PDR

PH

PNSC

PORV

PSIG

RAB

RCS

RFO

RII

RWST

SALP

SG

SNS

SRO

SSPS

Tavg

TPP

TS

UFSAR

VAC

VCT

VIO

WR/JO

28

Limiting Condition for Operati on

Licensee

Event Report

Hain Feedwater

Isolation Valve

Motor-Operated

Valve

Main Steam

Main Steam Isolation Valve

Maintenance Surveillance Test

Megawatt

Nuclear Assessment

Section

Non-Cited Violation

Nuclear Regulatory

Commission

Nuclear

Reactor Regulation

(NRC Office)

Normal Service

Water

Operations

Surveillance Test

Public Document

Room

Preventive

Maintenance

Plant Nuclear Safety Committee

Power Operated Relief Valve

Pounds

Per Square

Inch Gage

Reactor Auxiliary Building

Reactor Coolant System

Refueling Outage

Region II (NRC Office)

Refueling Water Storage

Tank

Systematic

Assessment

of Licensee

Performance

Steam Generator

Substation

Haintenance

Standard

Senior Reactor Operator

Solid State Protection

System

Average Reactor Coolant Temperature

Training Program

Procedure

Technical Specification

Updated

Final Safety Analysis Report

Volt Alternating Current

Volume Control Tank

Violation (of NRC requirements)

Work Request/Job

Order