ML18011A489

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Insp Rept 50-400/94-10 on 940403-0506.Violations Noted.Major Areas Inspected:Plant Operations,Refueling Activities,Safety Sys Walkdown,Review of Nonconformance Repts,Maint & Surveillance Observations & Security
ML18011A489
Person / Time
Site: Harris 
Issue date: 06/03/1994
From: Christensen H, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18011A485 List:
References
50-400-94-10, NUDOCS 9406270253
Download: ML18011A489 (31)


See also: IR 05000400/1994010

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W., SUITE 2900

ATLANTA,GEORGIA 30323-0199

Report No.:

50-400/94-10

Licensee:

Carolina

Power

and Light Company

P.

O.

Box 1551

Raleigh,

NC 27602

Docket No.:

50-400

Facility Name:

Harris

1

Inspection

Conducted:

April 3 - Hay 6,

1994

Lead Inspector:

J.

e row,

Se

r Re

ent Inspector

Other Inspectors:

D. Roberts,

Resident

Inspector

R. Hoore,

Reactor Inspector

Approved by:

H.

h istensen,

Acting

Reactor Projects

Branch

Division of Reactor Projects

Licensee

No.:

NPF-63

ate Signed

e

ige

SUHHARY

Scope:

This routine inspection

was conducted

by two resident

inspectors

in the areas

of plant operations,

refueling activities, safety

system walkdowns, review of

nonconformance

reports,

evaluation of licensee self assessment,

maintenance

observation,

surveillance observation,

design

changes

and modifications,

system engineering,

plant housekeeping,

radiological controls, security, fire

protection,

review of licensee

event reports,

and licensee

action

on previous

inspection

items.

Numerous facility tours were conducted

and facility

operations

observed.

Some of these tours

and observations

were conducted

on

backshifts.

Results:

One violation was identified:

Failure to establish

and

implement procedures

for system fill and vent

and for procedure

changes,

paragraphs

2.a(2)(a),

and

4.a(3).

Additionally, two non-cited violations were identified:

Failure to implement

fire protection procedures

adequately,

paragraph

5.d.;

and failure to

adequately

post dress

requirements for a high contamination

area,

paragraph

S.b.

9406270253

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PDR

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Inspection of opposite trains for similar deficiencies

was strong,

paragraph

2.d.

Improvement

was noted in line organization self assessment,

paragraph

2.e.

Plant management

demonstrated

a commitment to resolving deficiencies

prior to accident

occurrence

by stopping all outage work, paragraph

3.a.

Pre-

evolution briefs for complex tests

were effective in avoiding plant upsets,

paragraph

3.b.

Excellent radiation protection efforts demonstrated

during

containment modification work, paragraph

5.b.

Weaknesses

were identified in configuration control of circuits for the fuel

manipulator,

paragraph

2.b; initial documentation

of an engineering

evaluation

for a loose object in the

"C" steam generator,

paragraph

4.a(4);

performance

and verification of new nuclear instrument intermediate

range currents,

paragraph

4.b; lack of attention to detail in radiological posting,

paragraph

5.b;

and fire protection activities,

paragraph

5.d.

~ ~

\\

REPORT

DETAILS

1.

PERSONS

CONTACTED

Licensee

Employees

D. Batton,

Hanager,

Work Control

D. Braund,

Hanager,

Security

  • B. Christiansen,

Hanager,

Haintenance

J. Collins, Nanager,

Training

  • J. Donahue,

General

Hanager,

Harris Plant

J.

Dobbs,

Nanager,

Outages

  • H. Hamby,

Hanager,

Regulatory

Compliance

  • H. Hill, Nanager,

Site Assessment

  • D. HcCarthy,

Hanager,

Regulatory Affairs

  • J. Nevill, Hanager,

Technical

Support

  • R. Prunty,

Hanager,

Licensing

& Regulatory

Programs

  • W. Robinson,

Vice President,

Harris Plant

W. Seyler,

Hanager,

Project

Hanagement

  • H. Smith, Hanager,

Radwaste

Operation

D. Tibbitts, Hanager,

Operations

  • B. White, Hanager,

Environmental

and Radiation Control

A. Williams, Hanager, Shift Operations

Other licensee

employees

contacted

included office, operations,

engineering,

maintenance,

chemistry/radiation

and corporate

personnel.

  • Attended exit interview

2.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

Operations

a ~

Operational

Safety Verification (71707)

The plant began this inspection period in refueling operations

(Node 6).

Fuel

was off-loaded from the reactor vessel

at

8:27 a.m.

on April 4.

Refueling operations

were

recommenced

at

9:37 a.m.

on April l9 with the core being completely reloaded

on

April 21 at 11:30 p.m.

At 6:30 a.m.

on April 27 the reactor

vessel

head

studs

were tensioned

and the plant was placed in the

cold shutdown

(Node 5) condition.

On Hay 4 a plant heatup

was

commenced

and the hot standby

(Node 3) condition reached

at 5:07

p.m.

on Nay 5.

The plant remained in hot standby for the

remainder of this inspection period.

(1)

Shift Logs and Facility Records

The inspector

reviewed records

and discussed

various entries

with operations

personnel

to verify compliance with the

Technical Specifications

(TS)

and the licensee's

administrative

procedures.

The following records

were

reviewed:

shift supervisor's

log; outage shift manager'

log; control operator's

log; night order book; equipment

inoperable record; actiVe clearance

log; grounding device

log; temporary modification log; chemistry daily reports;

shift turnover checklist;

and selected

radwaste

logs.

In

addition, the inspector

independently verified clearance

order tagouts.

The inspectors

found the logs to be readable,

well

organized,

and provided sufficient information on plant

status

and events.

Clearance

tagouts

were found to be

properly implemented.

No violations or deviations

were

identified.

Facility Tours

and Observations

Throughout the inspection period, facility tours were

conducted to observe

operations,

surveillance,

and

maintenance activities in progress.

Some of these

observations

were conducted

during backshifts.

Also, during

this inspection period, licensee

meetings

were attended

by

the inspectors

to observe

planning

and management

activities.

The facility tours

and observations

encompassed

the following areas:

security perimeter fence; control

room; emergency diesel

generator building; reactor auxiliary

building; Reactor

Containment Building (RCB); waste

processing

building; turbine building; Fuel Handling

Building (FHB); battery rooms; electrical

switchgear

rooms;

and the technical

support center.

During these tours,

observations

were

made

on monitoring

instrumentation

which included equipment operating status,

area

atmospheric

and liquid radiation monitors, electrical

system lineup, reactor

operating

parameters,

and auxiliary

equipment operating parameters.

Indicated parameters

were

verified to be in accordance

with the

TS for the current

operational

mode.

The inspectors

also verified that

operating shift staffing was in accordance

with TS

requirements

and that control

room operations

were being

conducted

in an orderly and professional

manner.

In

addition, the inspector

observed shift turnovers

on various

occasions

to verify the continuity of plant status,

operational

problems,

and other pertinent plant information

during these turnovers.

(a)

On April 16,

1994,

the inspector

observed

control

room

operator activities associated

with filling and

venting the

RHR,

CVCS,

and SI systems.

These

systems

were being filled to establish

a flowpath of water to

the

RCS.

The

RCS was being filled via this process

to

a level which would allow continued filling using

General

Procedure

GP-009,

Refueling Cavity Fill,

Refueling

and Drain of the Refueling Cavity.

While observing the system filling activities, the

inspector noticed

a

memo in the control

room written

by an off-shift supervisor containing steps,

notes,

and caution statements

similar to those normally

contained

in operating

procedures.

The memo, dated

April 16,

1994,

contained specific sequential

instructions to operators

on which valves to

manipulate in order to fill the

ECCS systems.

The

inspector

asked

the on-shift

SCO if the

memo was being

referenced for the filling and venting then in

progress.

The

SCO responded

that the

memo was indeed

being used.

The inspector then inquired

as to whether

any other operating

procedures

were being

used

and if

not, should the steps

contained

in the

memo appear

in

such

a procedure.

The operator

responded

that the

memo was being

used to concurrently fill the

RHR,

CVCS

and SI systems

because

plant operating

procedures

did

not cover the concurrent filling of these

systems.

While the majority of system filling was accomplished

using steps outlined in the

memo, the document did

reference

using procedure

OST-1107,

ECCS Flow Path

and

Piping Filled Verification Honthly Interval,

as

a

guide to vent the

RHR and SI systems.

Only venting

for the

CVCS system

was to be accomplished

by

manipulating valves

as specified in the

memo.

The

inspectors

did not note

any technical

problems with

the sequence

of actions

used

by the operators

to fill

and vent the systems

as prescribed

by the

memo.

However, Regulatory

Guide 1.33

recommends

procedures

be established

and implemented for filling and venting

the systems

noted

above.

The inspectors

considered

the licensee's

actions to fill and vent the

RHR,

CVCS,

and SI systems

without a formally approved

procedure

to be

a violation of the requirements

contained in TS 6.8.1.a.

Violation (400/94-10-01):

Failure to establish

and

implement procedures.

Refueling Activities (60710)

The inspectors

witnessed

several shifts of fuel handling

operations

and verified that the refueling was being performed in

accordance

with TS requirements

and approved

procedures.

Areas

inspected

included containment integrity, housekeeping

in the

refueling area, shift staffing during refueling, surveillance

testing,

and periodic monitoring of plant status

during refueling

operations.

In addition, partial

implementation of the following

procedures

was observed:

~ GP-009

Refueling Cavity Fill, Refueling,

and Draindown of the

Refueling Cavity

~ FHP-010

Core Mapping Following Fuel

Loading

~ FHP-014

Fuel

and Insert Shuffle Sequence

~ FHP-020

Fuel Handling Operations

~ HPP-625

Performance of Radiological

Surveys

The inspectors

viewed the video tape

made of the core verification

performed in accordance

with procedure

FHP-010.

In addition, the

inspectors verified that locked high radiation areas

were properly

posted during the spent fuel transfer

between the

FHB and reactor

cavity.

The licensee's

implementation of the refueling activity

was satisfactory with proper oversight of the contractor

performing the activity.

The inspectors

reviewed the manipulator crane

and auxiliary hoist

checkout during fuel movement

on April 21,

1994.

This activity

was controlled by procedure

FHP-020 attachment

3 and included

startup

checks to verify proper equipment operation prior to

latching onto fuel elements.

The inspector

noted that step

3. 1.4'.g

had not been initialed to signify that circuits seven

through ten were off in the

MCC distribution panel

on the

manipulator crane.

An operator

was requested

to check the status

of the circuits which were found to be

on instead of off.

The

circuits were labeled

as spares.

The inspector

requested

licensee

personnel

to explain the function of these circuits.

The

applicable

CWD's depicted

these circuits to have

no function so

the inspector

concluded that the circuits were spares

and served

no safety related function.

However, the inspector considered

the

licensee's

configuration control of the manipulator

MCC circuits

was weak.

No violations or deviations

were identified.

Safety

Systems

Walkdown (71707)(71711)

The inspectors

conducted

a walkdown of the passive

safety

injection system to verify that the lineup was in accordance

with

license requirements for system operability and that the system

drawing

and procedure correctly reflected "as-built" plant

conditions.

In addition, portions of the high head safety

injection, low head safety injection,

emergency

service water,

containment

spr ay,

and auxiliary feedwater

systems

located inside

containment

were walked down.

The inspectors

also walked

down

containment

penetrations

located inside the steam tunnel

area.

~ ~

d.

e.

The inspector

found the material condition of components

to be

generally good.

Hinor boric acid leaks were evident

on

a few

passive

safety injection vales

and flanges.

These

items were

corrected

by the licensee.

No violations or deviations

were identified.

Review of Nonconformance

Reports

(71707)

Adverse Condition Feedback

Reports

(ACFR) were reviewed to verify

the following;

TS were complied with, corrective actions

and

generic

items were identified and items were reported

as required

by 10 CFR 50.73.

ACFR 94-1194 identified that the stem for primary

PORV 1RC-114 was

disconnected

from the valve disk.

The licensee's

preliminary

investigation revealed that the roll pin which fastens

these

two

parts together

had sheared.

An inspection of the other two

PORVs

revealed similar damage to valve

1RC-116

and

no damage to valve

1RC-118.

An operability determination

was performed

by licensee

personnel

who determined that the valves remained

operable

in this

condition because

system pressure

underneath

the valve disc would

force open the valve when the actuator

opened

the valve stem.

The

valves were subsequently

repaired.

Licensee

personnel

had noticed

that valve

1RC-114 exhibited seat

leakage during the previous

operating cycle.

In addition to the

PORVs, licensee

personnel

investigated

opposite

train components

when problems

were identified on the

CCW heat

exchangers

and the shaft failure of the "8" CSIP.

When the "A"

CSIP was disassembled

for inspection,

no evidence of similar

cracking

was found.

However, the disassembly

resulted

in damage

to threads

on the shaft for the balance

drum lock nut which

necessitated

the replacement of the rotating element.

The

practice

by licensee

personnel

to examine other train components

when problems

were identified is considered

to be

a strength.

No violations or deviations

were identified.

Evaluation of Licensee Self Assessment

(40500)

The inspectors

attended

selected

PNSC meetings to observe

committee activities

and verify TS requirements for committee

composition, duties

and responsibilities.

Heeting minutes

were

also reviewed to verify that activities were accurately

documented.

During a meeting

on Hay 6, preparations

for starting

the unit were discussed

as

was

a service advisory letter from the

nuclear

steam supplier which alerted the licensee to

nonconservatisms

in the overpower reactor trip setpoint

calculations for operation with inoperable

main steam safety

valves.

Technical specification 3.7. 1. 1 requires that the main steam

safety valves

be operable.

Action statement

3.7. 1. I.a specifies

that with a safety valve inoperable,

power operation

may proceed

provided that the overpower reactor trip setpoints

be reduced

per

Table 3.7-1.

The licensee's

nuclear

steam supplier vendor advised

that the calculations for the setpoints

specified

by this table

were nonconservative.

The

PNSC decided to implement

an internal

TS interpretation to require

a plant shutdown if a main steam

safety valve was inoperable.

This interpretation will remain in

effect until new setpoints

can

be developed.

The inspector

considered

the licensee's

action to be conservative.

The licensee recently implemented

procedure

PLP-614, Self-

Assessment

for Restart

Readiness

to Startup.

Highlights of this

new program included field walkdowns of 41 systems

on the primary

and secondary

side of the plant as well as electrical distribution

systems

by both senior reactor operators

and system engineers.

Walkdown deficiencies

were evaluated

to determine

the need for

correction before

commencement

of startup.

Along with the systems

readiness

element of this program,

organizational

readiness

was

also assessed.

Managers

were required to ensure staffing levels

were adequate,

personnel

training was conducted

as appropriate,

ACFRs/FBRs/CAP items were completed,

backlog items reviewed,

and

regulatory items were completed.

The program also contained

an

operational

readiness

assessment

from each shift supervisor

and

a

verification of the core configuration by engineering

support

organizations.

Predetermined

assessment

hold points were placed

in the outage

schedule prior to changing to Mode

4 and to Mode

2

to ensure

management

expectations

were met.

The

PNSC meeting

attended

by the inspector discussed

the readiness

for changing to

Mode 2.

The inspector

noted very detailed discussions

between

the

plant general

manager

and

PNSC members.

The inspector considered

this activity to be valuable to ensure items/deficiencies

received

appropriate

management

review prior to plant startup.

This

program was considered

to be

a substantial

improvement in licensee

self assessment

efforts.

Licensee Action on Previously Identified Operations

Inspection

Findings

(92901)

(I)

(Closed) Violation 400/93-12-02:

Failure to properly

implement plant procedures.

This item was previously discussed

in

NRC Inspection

Report

50-400/93-24.

The inspectors

reviewed

and verified

implementation of the corrective actions listed in the

licensee's

response letter dated July 30,

1993.

Training

was provided to operations

personnel

and lesson

plans for

continuing training revised.

Placards

were installed inside

the breaker cubicles to indicate the location for verifying

HOC alignment.

(2)

Maintenance

(Closed) Violation 400/93-25-03:

Failure to properly

establish

procedure

OP-131.01.

The inspectors

reviewed

and verified completion of the

corrective actions listed in the licensee's

response letter

dated July 30,

1993.

The licensee

has discussed

the

violation with shift supervisors

and counseled

involved

personnel.

The procedure

steps for reducing turbine load

have

been

removed

from procedure

OP-131.01,

revised

and

included into procedure

GP-006,

Normal Plant Shutdown

From

Power Operation

To Hot Standby.

'a ~

Maintenance

Observation

(62703)

The inspector observed/reviewed

maintenance activities to verify

that correct equipment clearances

were in effect; work requests

and fire prevention work permits were issued

and

TS requirements

were being followed.

Maintenance

was observed

and work packages

were reviewed for the following maintenance activities:

~

Rebuild main steam isolation valve

1HS-84 in accordance

with

procedures

CH-M0061, Hain Steam Isolation Valve Disassembly

and,Maintenance,

and

CH-H0062,

Main Steam Isolation Valve

Operator.

Breaker replacement for the "A" service water booster

pump

and supply breaker for HCC-1A32-SA in accordance

with

modification PCR-6526.

Weld repair of "A" CCW heat exchanger

web cracks in

accordance

with procedure

HAP-04, Plant Management

Work

Control Procedure,

PLP-710,

Work Management

Process,

HHP-

006, Installation of Structural

Steel

and Electrical,

Instrumentation,

and

HVAC Supports,

and modification

PCR-

7238.

Replace

PSU-Ill connectors

in

DC HCCs DP-1B2-SB

and DP-1A2-

SA in accordance

with modification PCR-7167.

Place placards

inside the breaker cubicles for the "A", "B",

and

"C" RCPs.

Clean

and inspect the intake manifold to the right bank

intercooler

on

EDG-1A,

and replace

the intercooler in

accordance

with procedure

MST-H0001,

Emergency Diesel

Generator

Intercooler Inspection

and Cleaning.

Perform EDG-lA fuel injector nozzle inspection

and cleaning

in accordance

with procedure

HST-H0016,

Emergency Diesel

Generator

Fuel Injection Nozzle Inspection

& Cleaning.

~

~

~ ~

I

b.

~

Perform

EDG-1A and

EDG-1B Cold Compression

and

maximum

firing pressure

checks

in accordance

with procedure

HST-

H0014,

Emergency Diesel

Generator

Cold Compression

& Haximum

Firing Pressure

Checks.

~

Inspect motors for "A" and "B" CSIPs for oil buildup.

~

Perform

EDG-1B cylinder liner inspection in accordance

with

procedure

HST-H0010,

Emergency Diesel

Generator Cylinder

Liner Visual Inspection.

In general,

the performance of work was satisfactory with proper

documentation of removed

components

and independent verification

of the reinstallation.

During the inspection of the "A" CCW heat

exchanger for fouling, the interior channel

lower web was found to

be bent

and cracked.

In addition, the baffle partition plate

was

also found to be bent.

Hodification PCR-7238

was initiated to

repair this condition.

An inspection of the "B" CCW heat

exchanger

was subsequently

performed

and revealed similar damage

(See

paragraph 4.a.(1)).

The inspector attended

safety meetings

held for licensee

personnel

on April 12.

Outage

work was stopped for approximately

one hour

to conduct these

meetings.

The meetings

were held because

licensee

management

and

NAD noted several

instances

of personnel

safety equipment not being utilized properly and examples of near

misses

to potential

accident situations.

Examples

included

situations

where licensee

personnel

identified poor electrical

safety practices of using under rated extension

cords

and use of

multi-plug power strips without adequate

overload protection.

Also, personnel

were noted to be working without proper eye

protection

and without tie-offs while working in elevated

positions.

Housekeeping

problems

had also

been identified.

The

near misses

included

a fire extinguisher which was dropped

from a

high elevation in the

CST as well as several

tools which had

been

dropped

from elevations

inside the

RCB.

An electrocution

was

narrowly avoided

when electricians incorrectly removed

access

covers to the

22

KV isophase

buss duct instead of accessing

the

intended

deenergized

neutral

grounding enclosure.

The isophase

buss duct was energized for backfeeding electrical

power from the

switchyard to the plant electrical distribution system.

The

energized

buss

was discovered

before

any personnel

injury/equipment

damage

occurred.

The inspector considered

the

conduct of these

meetings to be appropriate

considering all the

events

discussed

above

and demonstrated

licensee

management's

commitment to resolving deficiencies prior to the occurrence of

events/accidents.

Surveillance

Observation

(61726)

Surveillance tests

were observed to verify that approved

procedures

were being used; qualified personnel

were conducting

=

the tests;

tests

were adequate

to verify equipment operability;

calibrated

equipment

was utilized; and

TS requirements

were

followed.

The following tests

were observed

and/or data reviewed:

~ OST-1046

Hain Steam Isolation Valve Operability Test quarterly

Interval

~ OST-1088

Low Head Safety Injection Valves ISI Test quarterly

Interval

~ OST-1801

ECCS Throttle Valve,

CSIP,

and

Check Valve

Verification 18 Honth Interval.

~ OST-1809

Switchover to Recirculation

Sumps:

ESF Response

Time

18 Honth Interval.

~ OST-1824

1B-SB Emergency Diesel

Generator Operability Test

18

Honth Interval.

~ OST-1835

MSIV Remote

Shutdown With MSIV And Bypass Isolation

Remote Position Indication Test

18 Honth Interval

~ OST-1841

ESF Response

Time Heasurement for 1C-SAB CSIP

18 Honth

Interval

~ HST-I0044 Calibration of Nuclear Instrumentation

System

Power

Range

N41

~ HST-I0045 Calibration of Nuclear Instrumentation

System

Power

Range

N42

~ HST-I0046 Calibration of Nuclear Instrumentation

System

Power

Range

N43

~ HST-I0047 Calibration of Nuclear Instrumentation

System

Power

Range

N44

~ HST- I0167 Excore Nuclear Instrumentation

System Intermediate

Range

N35 Operational

Test

~ HST-I0168 Excore Nuclear Instrumentation

System Intermediate

Range

N36 Operational

Test

The performance of these

procedures

was found to be satisfactory

with proper

use of calibrated test equipment,

necessary

communications

established,

notification/authorization of control

room personnel,

and knowledgeable

personnel

having performed the

tasks.

As discussed

in

NRC Inspection

Report 50-400/94-06,

licensee

personnel

continued the pre-evolution briefs for the

complex surveillance tests.

This practice

was effective in

avoiding potential plant upsets.

No violations or deviations

were

observed.

~ ~

l

10

C.

Licensee Action on Previously Identified Maintenance

Inspection

Findings

(92902)

(1)

(Closed) Violation 400/93-25-02:

Failure to promptly

correct

a deficiency in

MCC wiring and prevent recurrence.

The inspector

reviewed

and verified completion of the

corrective actions listed in the licensee's

response letter

dated

March 7,

1994.

The licensee

has completed

work

tickets to restrain electrical

cables with tie-wraps to

prevent

movement

and

has replaced

the terminal connections

with a non-separable

connection.

(2)

(Closed) Deviation 400/93-24-01:

Failure to request

NRC

extension for corrective actions

committed to.

Engineering

The inspectors

reviewed

and verified implementation of the

corrective actions listed in the licensee's

response letter

dated

February

14,

1994.

Licensee

personnel

have installed

visual aids inside the "A", "B" and

"C" RCP breaker cubicles

to indicate the location for conducting

MOC alignment

verifications.

In addition, the licensee

has revised the

process for controlling action items to improve visibility

of regulatory commitments.

a ~

Design

Changes

and Modifications (37828)

Plant

Change

Requests

(PCR) involving the installation of new or

modified systems

were reviewed to verify that the changes

were

reviewed

and approved in accordance

with 10 CFR 50.59, that the

changes

were performed in accordance

with technically adequate

and

approved

procedures,

that subsequent

testing

and test results

met

approved

acceptance

criteria or deviations

were resolved in an

acceptable

manner,

and that appropriate

drawings

and facility

procedures

were revised

as necessary.

In addition,

PCR's

documenting engineering

evaluations

were also reviewed.

The

following modifications and/or testing in progress

was observed:

~ PCR-7167

Replacement

Terminal for DP-IA2-SA, DP-1B2-SB

~ PCR-7238

CCW Heat Exchanger Baffle Plate

~ PCR-0420

RTD Bypass Elimination

~ PCR-4888

Loose Parts in Steam Generators

A, B,

and

C.

~ PCR-3525

"A" and

"C" Steam Generator

Loose Parts

~ PCR-6526

Train "A" Load Centers

LK Breaker

Replacement

I

~ PCR-7171

Pressurization

of

B CSIP while under clearance

~ PCR-7274

CSIP Runout Technical Specification

Compliance

~ PCR-6831

1A-SA and

1B-SB CSIP Replacement

~ PCR-6925

Remove

AFW NOVs

~ PCR-7251

Foreign Object in

B Steam Generator

Secondary

Modification PCR-7238

was initiated following the

identification of cracks in the interior channel

lower web

of the "A" CCW heat exchanger.

The baffle partition plate

was also found to be bent.

Licensee

personnel

analyzed this

condition and believe that it was caused

by normal

system

operation in conjunction with inadequate

component

design

margin.

The modification reinforced the horizontal

partition web and baffle plate.

This modification was

performed

on both the "A" and

"B" CCW heat exchangers.

The inspector

found the engineering

evaluation

associated

with PCR-6831 to be very thorough

and included the effect of

rotating element

replacement

on the accident analysis,

systems

operation,

design basis

issues,

pump protection

concerns

and any electrical

impacts.

As

a result of the

pump rotating element replacement,

the licensee

plans to

startup using the

"C" CSIP in place of the "A" CSIP to

facilitate smooth operation of the normal charging flow

control valve.

In addition, the

TDAFW pump controller

setpoint

was adjusted to 28 percent to accommodate

less

margin in the steam generator

tube rupture analysis.

The

RTD bypass elimination modification removed

and capped

the

RTD bypass manifold piping and installed

new

RTD

thermowells

and fast acting

Weed Instrument

Company

RTDs.

In addition to the hardware

changes,

circuit changes

were

made to the Protection

Instrument Cabinets

(PIC-1, PIC-2,

PIC-3,

and PIC-8).

The instrumentation

portion of the

modification was reviewed to determine if adequate

instrument overlap

was incorporated

in post modification

testing to assure

appropriate verification of RTD instrument

protection

channel

performance.

Additionally, the

acceptance

criteria was reviewed to determine if the

RTD

instrument

response

time assumptions

assumed

in the Final

Safety Analysis Report

(FSAR) accident analysis

would be

verified by the testing.

The

RTD instrument loop was separated

into three sections

for response

time testing.

Section

one was from the

RTD

detector to the input of PIC-1, PIC-2,

and PIC-3 (thermal

response

time).

Procedures

HST-10635, Self Heating Test of

Installed Resistance

Thermometers,

and I0636, Insitu

a

12

Response

Time Testing of Installed

RTDs, provided guidance

for this test.

Section

two was from the

PIC input to the

output of the Train A and Train

B Solid State Protection

System

(SSPS) drivers (circuit response

time).

Procedures

HST I0644,

Group

1 of 3 Channel

RTS and

ESFAS Response

Time

Test,

I0645,

Group

2 of 3 Channel

RTS and

ESFAS Response

Time Test,

and I0646,

Group

3 of 3 Channel

RTS and

ESFAS

Response

Time Test,

provided guidance for this test.

Section three

was from the

SSPS drivers to trip breakers

A

and

B (breaker

response

time).

Procedures

HST I0647, Train

A UV Output Driver to Reactor Trip Breaker

Response

Time

Test,

and

10648, Train

B UV Output Driver to Reactor Trip

Breaker

Response

Time Test,

incorporated this test.

Although section three

was not impacted

by this

modification,

a surveillance test

was performed to determine

the breaker

response

time of trip breaker

A.

All procedures

used for response

time testing were existing procedures.

The inspector

concluded

the scope of post modification

testing incorporated

adequate

instrument loop overlap.

Section

one testing

had not been

completed at the end of

this inspection period.

The acceptance

criteria was

specified to be

4 seconds for the

RTD thermal

response.

Documentation for section

two testing

was included in WRs

94-ABYE1, 94-ABYHl, and 94-ABYKI.

Section

two response

time

was 0.3 seconds.

Section three tests

were documented

in

WRs

94-JI(001

and 92-JIPOOI.

The breaker

response

time was

0.0675 seconds.

The acceptance

criteria for the overall

trip circuit electronic delay which included the scram

control rod gripper release

time was specified to be 1.25

seconds.

The total. trip circuit electronic release

time was

0.3675

and substantially less

than the specified

1.25

seconds.

Completion of the section

one testing will

determine if the

RTD response

time was within the

6 seconds

assumed

by the

FSAR chapter

15 accident analysis.

The

inspector concluded that scheduled

and completed testing

was

adequate

to verify the

FSAR assumption

regarding

RTD

instrument loop response.

The inspectors will follow

section

one testing during future routine inspection

activities.

Other instrumentation

post modification testing included

average

temperature

and differential temperature

loop

calibration

and operational

tests of PIC control functions.

These tests

were accomplished

by existing surveillance

procedures.

Overall, the inspector

concluded that the scope

of post modification testing

was adequate

to demonstrate

instrumentation

performance

and verify the accident analysis

assumption.

The inspector verified the main control board

and simulator

instrumentation

hardware

changes

were implemented

and that

I ~

~

(4)

13

operator training had

been developed

to address

the

RTD

modification.

The hardware

changes

included removal of

annunciators,

meters,

and control

channel

defeat

switches

for low bypass

manifold flow, average

temperature,

and

control differential temperature.

These

changes

were

completed for both the control

board

and the simulator.

Lesson

Plan

LOR 94-1,

RTD Bypass

Loop Removal

& Reduced

T-

Hot Hods,

addressed

the impact of PCR-0420 to operators.

The inspector

concluded that the control

board

and simulator

instrumentation

had

been appropriately

updated consistent

with the plant modification.

Training adequately

addressed

the impact of the modification to operators.

The breaker

replacement

modification replaced existing 480

VAC Asea

Brown Boveri

(ABB) LK breakers with Siemens

RLN

type 480

VAC breakers.

The licensee

had experienced

chronic

failures of the

ABB LK breakers

over the preceding years.

The breaker failure issue

was addressed

in

NRC inspection

reports

50-400/93-15,

50-400/92-26,

and 50-400/89-13.

Unable to resolve the cause of the failures, the licensee

elected to install breakers of a different manufacturer with

equivalent operating characteristics

and rating.

This

modification replaced

the breakers

on 480

VAC emergency

buses

1A2-SA and

1A3-SA.

Additionally, the breaker cradles

were replaced to permit mounting of the Siemens

breakers

in

the existing switchgear cubicles.

The inspector

reviewed the scope of post modification

testing specified

by the

PCR to determine if testing

requirements

provided adequate verification of breaker

performance.

Completed test documentation for breakers

1A3-

SA-5B and lA3-SA-6B was reviewed to determine if the

required testing

was performed

and acceptance

criteria were

satisfied

by the test.

Additionally, the inspector reviewed

the licensee's

safety analysis

which evaluated

the

suitability of the replacement

breakers for the plant

application.

The following WR implemented post modification testing of

breaker

1A3-SA-5B: 93-AKABl performed

HST E0072,

480

VAC

Siemens

Type

RLN Load Center Breaker

and Cubicle Test,

and

CH-E0016, Current Transformer Ratio and Polarity Test.

Verification of indication and control functions

was

performed with WR 93-AKAB3 and procedure

EPT-615T,

Temporary

procedure for Testing Indication

and Control functions of

Breaker Supply Motor Control Center

1&4 A33-SA.

This

WR

also verified the setpoint of the ground fault relay.

Post

modification testing identified an installation deficiency

related to missing jumpers

on breaker

1A3-SA-5B which was

corrected

by

WR 94-AEHK1.

Similar testing

was accomplished

for breaker

1A3-SA-6B on

WRs 93-AKDA1 and 93-AKAD3.

The

post modification testing

on 1A3-SA-6B identified

a breaker

indication deficiency caused

by an incorrect termination

which was corrected

by

WR 94-AENW1.

The inspector

concluded

that the scope of post modification testing required

by PCR-

6526 was adequate

to verify the equipment function.

Test

documentation

demonstrated

appropriate verification of

equipment control

and protection features.

The inspector

reviewed the licensee's

safety analysis

which

determined that the Siemens

RLN breakers

were

an acceptable

replacement for the previously installed

ABB LK breakers.

The analysis

addressed

breaker time-current characteristics

and over current devices to verify that proper coordination

was maintained with upstream

and downstream

breakers.

Applicable electrical calculations,

drawings,

and setpoint

documents

were referenced

in the analysis.

The Siemens

breaker current interrupt ratings of 65,000

amperes

instantaneous,

and 50,000

amperes

short term met or exceeded

the

ABB LK breaker ratings of 50,000

amperes

instantaneous

and short term.

The maximum available short circuit current

calculated

by the licensee's

electrical fault calculation

(E-6000)

was less than 50,000

amperes.

The inspector

concluded that the licensee's

analysis

adequately

evaluated

the suitability of the Siemens'reakers

for this

, application.

The inspectors

observed

some of the post modification

testing mentioned

above for the

new Siemens

breakers.

All

testing

was performed

by electricians

in accordance

with

various test procedures

that were developed

by a cognizant

test engineer.

To affect the cycling of the breakers,

certain sections of the procedures

required that control

power and auxiliary control

power fuses

be removed

and

reinstalled.

In some cases,

the test procedure

steps

specified the sizes of the fuses.

For example, test

procedure

EPT-609T,

Temporary Procedure for Testing

Indication of Control Functions of Breaker Supplying

HCC

IA35-SA, step 7.4.3, specified auxiliary control

power fuse

sizes of 35 and 30 amperes

to be installed in fuse locations

FU5 and

FU6, respectively.

The inspectors identified several

cases

where

pen

and ink

changes

were

made to the procedures

in order to complete the

tests.

The inspector

reviewed procedure

EPT-609T

and noted

that the specified fuse sizes of 35 and

30 amperes

had

been

lined through

and replaced with annotations

of 15 and

5

amperes,

respectively.

The inspector then noticed that

15

and

5 ampere

fuses

had actually been installed in the

breaker cubicle.

The inspector performed

a followup review

of various other test procedures

associated

with the

new

Siemens

breakers

and found three additional

examples

where

incorrect fuse sizes

were lined out and replaced

by pen

and

ink changes,

then initialed and dated

by the test engineer.

I

~ ~

~

15

The inspector discussed

the handwritten

changes

in these

procedures

with the test engineer

who indicated that the 35

and

30 ampere

fuse sizes

were

now incorrect

due to late

PCR-

6526 revisions.

The inspector

asked

why a temporary

procedure

change

was not initiated.

The engineer

stated

that the tests

were being performed in compliance with

applicable plant guidelines

on procedural

adherence

(AP-100,

Procedure

Use

and Adherence).

The engineer's

assumption

was

based

on the fact that the test procedures

contained

notes

directing technicians

to contact the on-shift test engineer

(or the maintenance

supervisor) for resolution of any

unexpected

results prior to continuing with the test.

The

engineer believed the notes

empowered

him to line through

the erroneous

fuse information and write in the proper

sizes.

(6)

During

a closeout

review of the other work packages

associated

with PCR-6526,

the inspector identified one

additional

example

where

a test procedure

had

been

completed

with erroneous

information lined through, corrected,

and

initialed by the test engineer.

Step 7.3.6.b of test

procedure

EPT-605T,

Temporary Procedure for Testing

Indication

and Control Functions of Breaker Supplying

RHR

Pump lA-SA, specified

a jumper with resistance

of 2.5k ohms

be installed

between

two terminations.

The 2.5k ohm value

had

been lined through

and annotated

with 1.25k ohms.

The

test

had

been

signed off as complete.

The inspectors

did not identify any technical

problems

associated

with the performance of these tests.

The test

engineer did reference

the correct data from PCR-6526 prior

to making the

pen

and ink changes.

However, Technical Specification 6.8. l.a and the licensee's

administrative

procedure

AP-100 require that procedure

changes

be

implemented

before continuing with a procedure

step which

would result in an incorrect action or inappropriate

response.

The licensee's

actions involving unofficial pen

and ink changes

to the various

480 volt breaker test

procedures

are contrary to the above requirements

and are

considered

to be another

example of the violation discussed

in paragraph

2.a(2)(a) of this report.

During sludge lancing of the secondary

side of the steam

generators

during this refueling outage,

licensee

personnel

found several

loose parts which could not be retrieved.

A

ball detent

was found in steam generator

B and two ball

detents

and

a small rod were found in steam generator

C.

The ball detents

had been previously analyzed to be

acceptable

for continued plant operation

by PCR-3525 for the

life of the plant.

Evaluation

PCR-3525 also analyzed

two

short weld rods which were left in the "A" steam generator

after the first refueling outage

and evaluation

PCR-4888

16

analyzed

a bolt shank which was discovered

in the "B" steam

generator

which could not be retrieved after the second

refueling outage.

Engineering

personnel

evaluated

the

foreign objects in the steam generators

found during this

refueling outage

and considered

them to be acceptable

for

continued operation

based

upon

PCR-3525

and

PCR-4888.

This

conclusion

was documented

in an internal licensee

memorandum.

The inspector reviewed the

PCRs

and the

memorandum

and noted that the

PCRs contained

statements

that

the evaluations for the weld rods

and bolt shank were valid

for only the next cycle of operation after which the

adjacent

tubes

were to be examined

and further attempts

made

to retrieve.

The memorandum only discussed

the loose object

identified in "B" steam generator

and failed to evaluate

the

objects in "C" steam generator.

When this matter

was

brought to the attention of licensee

management,

evaluation

PCR-7251

was performed to formally document the

acceptability for leaving the objects in the "B" and

"C"

steam generators.

Although the inspector

agreed with the

conclusions

reached

by the engineering

evaluations,

the

documentation of the initial analysis

was considered

to be

weak.

b.

System Engineering

(71707)

The inspectors

reviewed the licensee's

actions to adjust the

excore nuclear instrumentation

current for the

new values

expected

from the low leakage

core.

The new core load reduced

the flux

present

at the reactor vessel

and the flux detected

by the excore

nuclear instrument detectors.

To account for this change the

intermediate

and power range nuclear instruments

were recalibrated

to adjust the old cycle instrument currents to predicted

new cycle

instrument currents.

The inspectors

reviewed calculations

by

licensee

personnel

of the predicted

values

performed in accordance

with procedures

EPT-008,

Intermediate

and

Power

Range Detector

Setpoint Determination,

and

EPT-009,

Intermediate

Range Detector

Setpoint Verification, and verified through reviews of work

packages

that these predicted setpoints

were implemented into the

nuclear instrumentation

channels.

The setpoints

were implemented

through calibration procedures

HST-I0044, HST-I0045, HST-I0046,

HST-I0047,

HST-I0167,

and HST-I0168.

The inspectors

found that

the methodology utilized was approved

by the fuel vendor.

During the review of procedure

EPT-009,

the inspector

noted that

step 7.2.5 directed the reactor engineer to select

acceptable

intermediate

range nuclear instrumentation trip currents to an

equivalent

value of less

than or equal

to 26 percent reactor

power.

The reactor engineer

selected

a current equal to

approximately

23 percent for conservatism.

Although it was

intended for this selected

current to be applied to the

calculations

contained

in procedure

EPT-008,

the inspector

noted

that

25 percent currents

were utilized instead.

The inspector

17

discussed

this observation with licensee

personnel

and

was

informed that although

a personnel

error had

been

made in the

calculations,

the

25 percent current actually selected

was within

the procedure

requirement of less than

26 percent

and was

therefore

considered

satisfactory.

Since the calculations of

these current adjustments

received

independent verification from

other licensee

personnel,

the error should

have

been identified by

the licensee.

Therefore the inspector considered

the performance

and verification of this calculation to be weak.

No violations or deviations

were identified.

Licensee Action on Previously Identified Engineering

Inspection

Findings

(92903)

(1)

(Closed)

Inspector

Followup Item 400/93-25-04:

Follow the

licensee's

activities to replace indicating bulbs

on the

TDAFW pump control panel

and identify similar bulb

applications

in other equipment.

Licensee

personnel

have replaced

the NB-120 type bulbs with

LED lamps in the control panel.

A search of the equipment

data

bases

and

CWDs identified two other applications of the

HB-120 bulbs consisting of the waste neutralization control

panel

and the containment

personnel

airlock control panel.

Licensee

personnel

concluded that the circuits associated

with these control panels

do not perform safety-related

functions

and therefore

no further action

was taken.

(2)

(Closed)

Inspector

Followup Item 400/93-07-01:

Follow the

licensee's

activities to prevent oil intrusion into charging

pump motors or establish

a periodic motor cleaning schedule.

The inspector

accompanied

licensee

personnel

on

a visual

inspection of the "A" and "B" CSIP motors to determine the

amount of oil accumulation

on the rotors

and stators.

The

motor windings for each

pump

had

a small

accumulation of oil

and dust, with the "B" motor exhibiting

a sl'ightly larger

buildup.

The licensee

discussed

this observation with the

equipment

vendor

who indicated that

a small accumulation of

oil and dust is

a normal,

expected

occurrence.

The vendor

recommended

that the licensee

continue to monitor the stator

temperatures

for each motor as

a means of determining

whether

any problems existed with cooling air flow as

a

result of the dirt buildup.

Recent stator temperature

data

for the three

CSIPs taken during the previous operating

cycle demonstrated

running temperatures

averaging

150

degrees

F.

The vendor stated that

150 degrees

was

acceptable

for these motors.

The licensee

plans to continue

monitoring the operating stator temperatures

and will base

any further actions

on future data.

(3)

18

(Closed) Violation 400/92-17-02:

Failure to correct

a

deficiency with the emergency diesel

generator starting air

system.

The inspector reviewed

and verified completion of the

corrective actions listed in the licensee's

response letter

dated

November 2,

1992.

This item was previously discussed

in

NRC Inspection

Report 50-400/93-08.

Licensee

personnel

have reviewed existing

PCRs

and determined that

no

additional

ACFRs were required other than those already

written and submitted.

(4)

(5)

(Closed) Violation 400/93-21-02:

Failure to properly

review/approve

vendor procedures.

The inspector reviewed

and verified completion of the

corrective actions listed in the licensee's

response letter

dated

December

16,

1993.

The licensee

performed technical

and safety reviews of the vendor procedures

used in

safety-related

temporary leak repairs that were still in

place.

The licensee's

administrative

procedure

AP-032,

Procedure to Obtain

Non-Company

Labor and Services,

was

revised to clarify that vendor procedures

used for work on

safety-related

structures,

systems,

or components will be

formatted in accordance

with procedure

AP-005,

Procedures

Format

and Preparation,

and approved in accordance

with

procedure

AP-006,

Procedure

Review and Approval. If not

formatted

and approved in accordance

with procedures

AP-005

and AP-006, then the vendor procedure will be included in

the modification package

as

a work instruction

and will have

technical

and safety reviews along with the

PCR.

Designated

Contract Representatives

received training on the

new

requirements

of procedure

AP-032 prior to the start of the

current refueling outage.

(Closed) Violation 400/93-12-03:

Failure to establish

adequate

measures

to verify that designs

were technically

accurate with respect to the design basis for the

AFW

system.

The inspectors

reviewed

and verified completion of the

corrective actions listed in the licensee's

response letter

dated July 30,

1993.

The licensee

h'as completed

modification PCR-6925 to remove the motor operators for

valves

1AF-5 and

1AF-24 and replaced

them with manual

handwheels.

~

~

5.

Plant Support

a.

Plant Housekeeping

Conditions

(71707) - Storage of material

and

components,

and cleanliness

conditions of various areas

throughout

the facility were observed to determine whether safety and/or fire

~

~

~

19

b.

hazards

existed.

The inspectors

found plant housekeeping

and

material condition of components

to be satisfactory.

Radiological Protection

Program

(71707)

- Radiation protection

control activities were observed routinely to verify that these

activities were in conformance with the facility policies

and

procedures,

and in compliance with regulatory requirements.

The

inspectors

also reviewed selected

radiation work permits to verify

that controls were adequate.

Fuel sipping was performed during this outage to identify the

source of increased

RCS activity during the previous operating

cycles discussed

in

NRC Inspection

Report 50-400/93-04.

The

sipping process identified one fuel assembly,

HF04, which required

repair.

This assembly

was replaced

by another similar assembly

during the core re-load.

Extensive health physics

coverage

was provided to support the

implementation of PCR-0420,

RTD Bypass Elimination.

This coverage

included the use of cameras,

increased lighting, remote indicating

teledosimetry for workers located inside the containment bioshield

wall, and direct communications

between

health physics technicians

monitoring the job from an outside trailer and the workers inside

containment.

The inspector considered

overall performance

from

the health physics technicians

during this evolution to be good.

On one occasion

at the beginning of the

RTD bypass demolition for

RCS loop C,

a health physics supervisor actually stopped all work

associated

with the demolition when it was detected that the

workers were not coordinating work activities properly.

No work

was allowed to continue until

HP technicians

and workers regrouped

to resolve

problem areas.

This conservative

action

was taken

without regard to outage

schedule restraints,

and

was consistent

with the philosophy of ensuring that the job was done correctly

the first time with as few radiological or industrial incidents

as

possible.

In addition to the above activities, other controls

such

as the use of lead shielding helped

keep the total dose

recorded for the

RTD modification well below the industry average.

Approximately 60 man-rem

was expended for the modification.

Despite the overall

good performance

noted

above,

there

were

a few

minor examples of radiological control incidents which centered

around lack of attention to detail

and poor worker practices.

On

April 15, while observing inspections

on the "B" CSIP motor, the

inspector identified that the area

around the

pump baseplate

had

been

roped off and posted

as

a High Contamination

Area

(HCA).

The

dress

requirements for the area

were posted

as

shoe covers

and

gloves

as

a minimum.

Directly above the

HCA posting were three

signs posting the area

as

a Contamination

Area

(CA) with the

same

dress-out

requirements.

The inspector brought this dual posting

observation to the attention of HP technicians

who corrected

the

problem by removing the

CA signs

and upgrading the

HCA dress-out

requirements

to include overalls.

The technicians

noted that the

~

~

c ~

d.

20

CA signs were remnants

from before the outage

when the area

was

still a contamination

area.

The inspector

noted that no work was

ongoing inside the area

posted

as

a

HCA and that the potential for

worker contamination

in this area

was minimal due to the fact that

HPs were then requiring lab coats,

gloves

and

shoe

covers

as

a

minimum for entry into the "B" CSIP room.

Other examples of

inadequate

radiological posting were identified by the licensee

throughout the outage.

In addition,

examples of poor worker

practices

were noted including

a case

where

a worker removed

a

breathing

apparatus

required

by his

RWP in order to communicate

with a fellow worker.

Also, seven

personnel

contamination

events

occurred early during the

RTD bypass, demolition which were

directly attributed to poor worker practices.

Plant program procedure

PLP-511,

Radiation Control

and Protection

Program,

Section 5.7.4.4

and Health Physics

Procedure

HPP-625,

Performance of Radiological

Surveys,

Section 10.4.2. 11 require

full protective clothing, including head cover, coveralls,

gloves,

shoe covers,

and rubbers

be worn as

a minimum for entry into HCAs.

The procedure further required that posting for HCAs include,

as

appropriate,

minimum dress

requirements

required for entry into

the area.

The inadequate

posting of dress

requirements

for the

HCA in the charging

pump room is contrary to the requirements

of

procedures

PLP-511

and

HPP-625

and is considered

to be

a

violation.

This violation is not being cited because

the

licensee's

efforts in correcting the violation meet the criteria

specified in Section VII.B of the Enforcement Policy.

Non-cited Violation (400/94-10-03):

Failure to adequately

post

dress

requirements for a High Contamination Area.

Except for the examples

noted

above involving lack of attention to

detail, the licensee's

performance

in the area of radiological

controls

was satisfactory.

Security Control

(71707)

- The performance of various shifts of

the security force was observed

in the conduct of daily activities

which included:

protected

and vital area

access

controls;

searching of personnel,

packages,

and vehicles;

badge

issuance

and

retrieval; escorting of visitors; patrols;

and compensatory

posts.

In addition, the inspector

observed

the operational

status of

closed circuit television monitors, the intrusion detection

system

in the central

and secondary

alarm stations,

protected

area

lighting, protected

and vital area barrier integrity,

and the

security organization interface with operations

and maintenance.

The licensee's

adherence

to security requirements

was found to be

satisfactory.

Fire Protection

(71707) - Fire protection activities, staffing and

equipment

were observed to verify that fire brigade staffing was

appropriate

and that fire alarms,

extinguishing equipment,

21

actuating controls, fire fighting equipment,

emergency

equipment,

and fire barriers

were operable.

A weakness

was identified in the licensee's fire protection

activities during RFO-5.

Fire-related

incidents occurred inside

the containment building and in the turbine building which

resulted

from less

than adequate

control of combustible materials

during hot work activities primarily performed

by contractor

personnel.

In addition,

one example of inadequate fire watch

activities was identified by the inspectors

and several

more

examples

were identified by licensee

personnel.

During

a two week period in April, four small fire-related

incidents occurred in the plant.

On April 4,

a small hand-held

dosimetry console

smoldered

inside containment.

This was due to

a

piece of welding slag from an upper elevation fell onto the

console

through

a small hole in the

protective covering used to

shield workers

and equipment

from just such

a hazard.

The

smoldering instrument

was extinguished within seconds,

but it was

not reported to the main control

room until several

days later

when the inspectors

and licensee

outage

management

began to

inquire about it.

On April 9 and

10, two small fire-related

incidents occurred in the turbine building.

Both involved poor

control of combustible material during welding activities.

In

each

case,

the fire was extinguished rapidly and the main control

room was properly notified.

On April 15,

a similar incident was

reported in the containment building.

A fire tech immediately

extinguished

a smoldering rag

and notified the main control

room.

None of the above incidents resulted in fires that were long

enough in duration

(10 minutes) to meet the licensee's

Unusual

Event declaration criteria.

Other examples of poor fire protection activities were also noted.

On April 6, the inspector

observed cutting/welding activities

associated

with the

AFW system pipe replacement

inside

containment.

The inspector

asked the associated

firewatch where

the Hot Work Permit was located.

The firewatch identified

a

permit posted

on

a nearby wall that

had expired the previous day.

It was later discovered that

a permit had

been

issued to allow the

work, but the copy required to be posted at the job site

had

been

lost.

The firewatch failed to identify the deficiency upon

assuming

his duties that afternoon.

In a separate

incident

on

April 8,

a roving firewatch in the containment building discovered

welding and grinding being performed

under

an expired hot work

permit.

Once again,

a firewatch was in place while the work was

ongoing,

but failed to identify the deficiency.

On April 15, licensee

personnel

discovered that there

was

no

firewatch personnel

monitoring the preheating of a certain section

of AFW piping inside containment.

It was determined

during the

licensee's

investigation that there

had

been

a firewatch posted

earlier,

but he was dismissed

when licensee

personnel

decided to

g

0

22

secure

the heating process.

Licensee

personnel

accidentally

shut

off power to

a different heating element leaving the subject

element

energized with no fire watch posted.

Upon discovery,

a

firewatch was immediately dispatched

to continue monitoring the

pre-welding activity on the heated

section of pipe.

Other

examples of deficiencies identified by the licensee

included low

pressure

gas containers

being

abandoned

at work sites following

completion of work.

Each

one of the items discussed

above

were documented

in ACFRs.

The inspectors

discussed

the above

problems with licensee

management

who acknowledged

the increased

trend in fire-related

incidents during the month.

Licensee

management

stated that

a

need existed to increase

the level of awareness

of potential fire

hazards

among firewatches

and the individuals performing the hot

work.

At the close of the inspection,

the licensee

was in the

process

of revising various fire protection procedures

and the

firewatch training lesson

plan to incorporate

more details

and

testing requirements.

Actions being considered

by the licensee

included required training for all personnel

performing hot work,

development of guidelines for containing hot work hazards,

and the

development of hot work permits requiring fire line supervision

signature signifying that all permit conditions

had

been

met prior

to starting work.

Fire Protection

Procedure

FPP-006,

Control of Ignition Sources

Hot

Work Permit, Section 5.0, requires

maintenance

supervisors

to

ensure that all maintenance

and modification activities involving

hot work employ

a Hot Work Permit,

and that

a firewatch is

assigned.

It further states that the maximum duration of any Hot

Work Permit is 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />,

and if the work requiring the

HWP has not

been

completed

when the permit expires,

a new permit will be

issued

in accordance

with Section 8.0.

Section 8.0 states

that

where Hot Work Permits apply, associated

work will not commence

until the Firewatch

has inspected

the work site.

It further

states

that

a copy of the

HWP is then conspicuously

posted

in the

work area.

The examples of poor firewatch activities identified

above

were considered

to be in violation of the requirements

of

procedure

FPP-006.

This violation will not be subject to

enforcement

action because

the licensee's

effort in identifying

and correcting the violation meet the criteria specified in

Section VII.B of the Enforcement Policy.

Non-cited Violation (400/94-10-02):

Failure to implement fire

protection procedures

adequately.

Exit Interview (30703)

The inspectors

met with licensee

representatives

(denoted

in paragraph

I) at the conclusion of the inspection

on Nay 6,

1994.

During this

meeting,

the inspectors

summarized

the scope

and findings of the

inspection

as they are detailed in this report, with particular emphasis

23

on the Violation addressed

below.

The licensee

representatives

acknowledged

the inspector's

comments

and did not identify as

proprietary

any of the materials

provided to or reviewed

by the

inspectors

during this inspection.

No dissenting

comments

from the

licensee

were received.

Item Number

Descri tion and Reference

400/94-10-01

(VIO)

400/94-10-02

(NCV)

400/94-10-03

(NCV)

Acronyms

and Initialisms

Failure to establish

and implement

procedures,

paragraphs

2.a(2)(a)

and

4.a(3).

Failure to implement fire protection

procedures

adequately,

paragraph

5.d.

Failure to adequately

post dress

requirements

for a high contamination

area,

paragraph

5.b.

ABB

ACFR

AFW

CAP

CCW

CFR

CSIP

CVCS

CWD

ECCS

EDG

ESF

ESFAS-

FBR

FHB

FSAR

HCA

HP

HVAC

ISI

KV

MCC

HOC

MOV

HSIV

NAD

NRC

PCR

PIC

PNSC

PORV

n System

tioning

Asea

Brown Boveri

Adverse Condition Feedback

Report

Auxiliary Feedwater

Corrective Action Program

Component Cooling Water

Code of Federal

Regulations

Charging Safety Injection

Pump

Chemical

and Volume Control

System

Control Wiring Diagram

Emergency

Core Cooling System

Emergency Diesel

Generator

Engineered

Safety Feature

Engineered

Safety Feature Actuatio

Feedback

Report

Fuel Handling Building

Final Safety Analysis Report

High Contamination

Area

Health Physics

Heating, Ventilation and Air Condi

Inservice Inspection

Kilovolt

Motor Control Center

Mechanism Operated

Cell

Motor Operated

Valve

Main Steam Isolation Valve

Nuclear Assessment

Department

Nuclear Regulatory

Commission

Plant

Change

Request

Process

Instrument Cabinet

Plant Nuclear Safety Committee

Power Operated Relief Valve

RCB

RCP

RCS

RFO

RHR

RTD

RTS

RWP

SCO

SI

SSPS

TDAFW-

TS

VAC

WR 24

Reactor

Containment Building

Reactor Coolant

Pump

Reactor Coolant System

Refueling Outage

Residual

Heat

Removal

Resistance

Temperature

Detector

Reactor Trip System

Radiation

Work Permit

Senior Control Operator

Safety Injection

Solid State Protection

System

Turbine Driven Auxiliary Feedwater

Technical Specification

Voltage Alternating Current

Work Request