ML18011A392

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Insp Rept 50-400/94-05 on 940115-0218.Violations Noted. Major Areas Inspected:Plant Operations,Safety Sys Walkdown, Cold Weather Preparations,Review of Nonconformance Repts, Followup of Onsite Events,Maint & Fire Protection
ML18011A392
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 03/04/1994
From: Christensen H, Darrell Roberts, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18011A390 List:
References
50-400-94-05, 50-400-94-5, NUDOCS 9403150203
Download: ML18011A392 (36)


See also: IR 05000400/1994005

Text

~pit RK0y

.v,

%eport No.:

50-400/94-05

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETlASTREET, N.W., SUITE 2900

ATLANTA,GEORGIA 30m4199

Licensee:

Carolina

Power

and Light Company

P.

O.

Box 1551

Raleigh,

NC 27602

Docket No.:

50-400

Licensee

No.:

NPF-63

Facility Name:

Harris

1

Inspection Conduc:

January

15 - February

18,

1994

Inspectors:

J.

C$

c

wt

Qe ior

esident

Inspector

C~

D te Signed

g

Cpl

D

o erts,

si

en

Inspector

Date

igned

Approved by:

H. Christensen,

Section Chief

Division of Reactor Projects

a

Si

ned

SUMMARY

Scope:

This routine insphction

was conducted

by two resident

inspectors

in the areas

of plant operations,

safety system walkdown, cold weather preparations,

review

of nonconformance

reports,

followup of onsite events,

maintenance

observation,

surveillance observation,

design

changes

and modifications,

system

engineering,

plant housekeeping,'adiological

controls, security, fire

protection,

preparations

for refueling, review of licensee

event reports,

and

licensee

action

on previous inspection

items.

Numerous facility tours were

conducted

and facility operations

observed.

Some of these tours

and

observations

were conducted

on backshifts.

Results:

Two violations with multiple examples

were identified:

Failure to implement

procedures

properly,

paragraph 2.c., 2.d(2)

and 4.a(1);

Failure to implement

corrective actions,

paragraphs

2.d(l)

and 2.e.

A non-cited licensee identified violation regarding control of locked. high

radiation areas is discussed

in paragraph

5.b.

Several

areas of improvement

were noted:

Operator identification and response

to

a failed condensate

booster

pump recirculation valve prevented

a potential

plant trip, paragraph 2.a(l)(a);

The number of operator standing orders

was

reduced,

paragraph

2.a(1)(b);

Operator turnover process

strengthened

by daily

meetings with work control/managers,

paragraph 3.a(l);

The average

age of

9403150203

94030

PDR

ADOCK 05000 00

8

PDR

maintenance

backlog tickets

has

been

reduced,

paragraph

3.a(2);

Assessments

of the maintenance

functional

area

were good,

paragraph

3.a(3);

Preliminary

efforts for outage safety-related

breaker

replacement

modifications were

beneficial,

paragraph

4.a(2);

Good technical

support

was evident during

a

plant downpower,

paragraph 4.b(l);

Conduct of testing for the

new security

perimeter fence

was good,

paragraph 5.c(l);

Fuel receipt inspection

activities were found to be very thorough,

paragraph

6.a;

and scheduling of

safety train outages

was effective,

paragraph

S.a.

Several

weaknesses

were also identified:

classification of emergency

work was

too general,

paragraph

3.a(4);

poor initial written safety evaluation for a

plant modification, paragraph

4.a(3); superior housekeeping

standards

were not

being maintained

in several

plant areas,

paragraph

5.a; deficiencies

were

identified in the

new security perimeter fence,

paragraph 5.c(l); poor escort

control of visitors was noted,

paragraph

5.c(2); receipt inspection of Siemens

fuel indicated quality problems with the manufacturing of new fuel, paragraph

6.a;

and improvement

was needed

in the licensee's

safe

shutdown analysis,

paragraph

S.c.

REPORT DETAILS

1.

Persons

Contacted

Licensee

Employees

  • D. Batton,

Manager,

Work Control

  • B. Christiansen,

Maintenance

Manager

  • J. Collins, Manager, Training
  • M. Hamby,

Manager,

Regulatory

Compliance

  • J. Dobbs,

Manager,

Outages

  • J. Kiser, Manager,

Radiation Control

  • D. McCarthy, Manager,

Regulatory Affairs

J. Hoyer,

Manager, Site Assessment

  • R. Prunty,

Nanager,

Licensing

and Regulatory

Programs

  • W. Robinson,

Vice President,

Harris Plant

~ *W. Seyler,

Manager,

Project

Management

H. Smith,

Manager,

Radwaste

Operation

  • D. Tibbitts, Manager,

Operations

B. White, Manager,

Environmental

and Radiation Control

  • 0. Wilkins, Manager,

Spent

Fuel

  • L. Woods,

Manager,

Technical

Support

  • H. Worth, Manager,

Onsite Engineering

Other licensee

employees

contacted

included office, operations,

engineering,

maintenance,

chemistry/radiation

and corporate

personnel.

"Attended exit interview

2.

Acronyms

and initialisms used throughout this report are listed in the

last paragraph.

Operations

a ~

Operational

Safety Verification (71707)

The plant continued in power operation

(Mode 1) for the duration

of this inspection period.

(1)

Shift Logs and Facility Records

The inspector

reviewed records

and discussed

various entries

with operations

personnel

to verify compliance with the

Technical Specifications

(TS)

and the licensee's

administrative

procedures.

The following records

were

reviewed:

shift supervisor's

log; control operator's

log;

night order book; equipment

inoperable

record; active

clearance

log; grounding device log; temporary modification

log; chemistry daily reports; shift turnover checklist;

and

selected

radwaste

logs.

In addition, the inspector

independently verified clearance

order tagouts.

'

The inspectors

found the logs to be readable,

to be well

organized,

and to provided sufficient information on plant

status

and events.

Clearance

tagouts

were found to be

properly implemented.

(a)

On January

24,

1994, at approximately 5:30 a.m.,

a

control

room operator noticed that the "B" condensate

booster

pump recirculation valve (ICE-261) indicated

partially open

on the main control board.

The normal

valve position was fully closed.

An auxiliary

operator

was dispatched

to isolate the recirculation

line manually.

The line was isolated before the

recirculation valve had completely failed open.

The

inspector discussed

the operator's

action with

licensee

personnel

and

was informed that no alarms

were received prior to the identification of the

problem by the operator.

If the problem

had not been

identified by the operator then

a plant trip would

have occurred

when sufficient condensate

flow was

diverted

away from the suction of the main feedwater

pumps with resultant

low suction pressure

pump trips

followed by the associated

turbine trip/reactor trip.

The operator's

attentiveness

to control

board

indications

was good

and prevented

a potential plant

transient.

(b)

The inspectors

reviewed operating standing orders to

determine if previously identified deficiencies

as

noted in

NRC Inspection

Report 50-400/93-14

had

been

corrected.

Also, the content of the standing orders

was discussed

with the manager of shift operations.

The licensee's

policy is to use the standing orders to

provide interim guidance until applicable

procedures

can

be revised.

Specific deficiencies identified

earlier

had

been corrected

by either deletion or by

inclusion into appropriate

procedures.

In addition,

the inspector

noted that the number of standing orders

had

been

reduced to approximately

10, which was about

one-half of the previous

number.

The licensee

had

made

improvements

in the dissemination of this

guidance.

No violations or deviations

were identified.

(2)

Facility Tours

and Observations

Throughout the inspection period, facility tours were

conducted to observe operations,

surveillance,

and

maintenance

activities in progress.

Some of these

observations

were conducted during backshifts.

Also, during

this inspection period, licensee

meetings

were attended

by

the inspectors

to observe

planning

and management

activities.

The facility tours

and observations

encompassed

the following areas:

security perimeter. fence; control

room;

emergency diesel

generator building; reactor auxiliary

building (RAB); waste processing

building (WPB); turbine

building; fuel handling building; emergency

service water

building; battery rooms; electrical

switchgear

rooms;

and

the technical

support center.

During these tours, observations

were

made

on monitoring

instrumentation

which included equipment operating status,

area

atmospheric

and liquid radiation monitors, electrical

system lineup, reactor operating

parameters,

and auxiliary

equipment operating

parameters.

Indicated parameters

were

verified to be in accordance

with the

TS for the current

operational

mode.

The inspectors

also verified that

operating shift staffing was in accordance

with TS

requirements

and that control

room operations

were being

conducted

in an orderly and professional

manner.

In

addition, the inspectors

observed shift turnovers

on various

occasions

to verify the continuity of plant status,

operational

problems,

and other pertinent plant information

during these turnovers.

The licensee's

performance

in this

area

was satisfactory.

No violations or deviations

were

identified.

Safety

Systems

Walkdown (71710)

The inspectors

conducted

a walkdown of the Auxiliary Feedwater

(AFW) system to verify that the lineup was in accordance

with

license requirements

for system operability and that the system

drawing

and procedure correctly reflected "as-built" plant

conditions.

The inspectors

found minor drawing discrepancies

on drawings

2165-S-0544

and 2165-S-0545 pertaining to normally depicted valve

positions

and valve labeling.

The licensee's

valve lineup

procedures

OP-126

and OP-137

agreed with actual

valve labeling in

the field.

The inspectors

also noted several

housekeeping

deficiencies

in the steam tunnel

and slight general

corrosion

on

the

TDAFW pump trip and throttle valve.

The inspectors

were

informed that

an existing

PCR

(PCR-7088,

CPL-2165-S-0544

Drawing

Correction for 1AF-55) already

addressed

one of the inspector's

comments

and that the inspector's

other

comments

would also

be

incorporated

into this

PCR.

The licensee's

system engineer

inspected

the general

corrosion

on the trip and throttle valve and

determined that this condition was acceptable

for a steam

admission valve.

No violations or deviations

were identified.

Cold Weather Preparations

(71714)

Between January

15 - 20;

1994, the plant experienced

extremely

cold, ambient air temperatures

which affected various plant

equipment

and caused

several

alarms

and erroneous

indications in

the main control

room.

On January

16,

ambient temperatures

were

recorded to be below

10 degrees

F.

Several

cases

of frozen

instrument sensing lines for non-safety related

components

occurred.

Examples

included the

RAB Normal Ventilation supply

fans which tripped numerous

times due to inadequate

heating for

the fan units.

The high discharge

pressure trips for all three of

the circulating water

pumps

had to be disconnected

due to frozen

pressure

channels

indicating dangerously

close to the

pump trip

setpoints.

Other equipment affected

by the record low

temperatures

(as low as

2 degrees

F) included the diesel driven

fire pump which auto started

due to frozen instrument lines,

and

condenser

pressure

indicators

on the main control

board which

began to show

a decrease

in condenser

vacuum.

Recognizing that

the instruments

on the

HCB did not provide input to the main

turbine trip on low condenser

vacuum,

operators verified that the

instruments

providing the trip input were indicating correctly.

One safety-related

system

was also affected

by the cold weather.

A frozen

RWST level transmitter located

near the

RWST resulted in

a high level alarm in the main control

room.

Eventually the level

channel,

LT-990, failed high and

was declared

inoperable placing

the plant in a seven

day Limiting Condition for Operation

(LCO).

Licensee

personnel

found

some of the affected instrument cabinets

with permanently installed heaters

that were not functioning.

In

other cases

instrument lines were found not to be adequately

insulated or heat traced.

Work tickets were initiated to correct

all of the above deficiencies

and other temperature

related

problems

and included

such actions

as installing heat tracing,

insulation,

and portable heaters.

As a temporary measure for the

RWST level channel,

a heat-emitting light fixture was installed

near the transmitter.

As noted in NRC Inspection

Report 50-400/

93-24,.the

inspectors

observed that the maintenance

backlog for

heat tracing, and temperature

maintenance

systems

had not been

reduced.

This backlog primarily affected non-safety related

equipment.

Although none of the above problems

posed

a threat to

the safe operation of the plant, the inspectors

concluded that

a

more aggressive

approach

by the licensee

to address

the backlog

and identify potential

freeze protection deficiencies

could have

prevented

some of the incidents of frozen instrumentation

noted

above.

During the

same cold week in January,

the inspector

reviewed data

sheets for Procedure

OST-1021, Daily Surveillance

Requirements

(DSR).

Per this procedure,

operators

logged various

TS required

operating

parameters,

such

as tank levels

and

room temperatures.

The inspector noticed that for the

DSR dated January

17,

1994, the

"B" ESW electrical

equipment

room temperatures

were between

47-

49'F for each of the four six-hour surveillance intervals.

The

other rooms in the

ESW intake structure

were all indicating above

60'F.

The inspector further noted that the "B"

ESW electrical

equipment

room temperature initially dropped

below 50'F

on

January

15,

and dipped

as low as 38'F

on January

19,

1994.

Although only maximum room temperatures

for the

ESW structure

were

specified in the TS, the

FSAR, Table 9.4.0-1,

indicated

minimum

temperatures

of 51'F for the

ESW intake structures,

specifically

the

pump rooms

and the electrical

equipment

rooms which house

associated

safety-related

HCCs

and air handlers.

In the

discussion

of the design of plant

HVAC systems,

Section 9.4.0 of

the

FSAR stated that, in winter, the air is heated

by the supply

units'lectrical

heating coils or electrical

heating units to

assure

the minimum design

space

temperature

stated

in FSAR Table

9.4.0-1 is maintained.

The discrepancy

between

the statement

in

the

FSAR and the actual

temperatures

logged for the "B"

ESW

electrical

equipment

room was discussed

with licensee

personnel.

It was later noticed

by the licensee that the recorded

temperatures

for the "A" and "B" EDG rooms

had also dropped

below

51'F.

On January

19,

1994, licensee

personnel

initiated actions

to evaluate

the intent of the

FSAR statement

and to correct the

low temperature

conditions in the

ESW structure

and the

EDG

building.

Immediate actions

included placing air supply fan AH-

86B in service

so that its heating coil could heat the "B"

ESW

electrical

equipment

room intake air.

This action brought the

room temperature

to above 51'F before the fan was

removed from

service

due to frozen fan cooling coils which burst

and leaked

water into the fan housing

and the

ESW structure

(see

paragraph

4.a.(3) of this report).

Later,

a portable heater

was placed in

the room to maintain temperatures

above the

FSAR minimum value.

Portable

heaters

were also placed in the

EDG structure

in an

attempt to raise

room temperatures.

During

a tour of the

ESW intake structure

on January

19, the

inspector noted that

a deficiency tag dated January

12,

1994,

had

been

placed

on the permanent

space

heater installed in the "B"

ESW

electric equipment

room.

A tour of the "A" and "B" ESW pump rooms

identified several

heaters

which were also inoperable

and

had not

been tagged.

Operators later wrote deficiency tags for the

remaining inoperable

heaters

in both the

EDG rooms

and the

ESW

structure.

The inspector noted that administrative

Procedure

AP-301, Adverse

Weather Operations,

had

been in effect for extended

periods over

the previous

two months

when ambient temperatures

were below 35'F.

The procedure

contained guidelines for monitoring, operating

and

maintaining equipment

and instrumentation

during periods of severe

cold weather.

Operator responsibilities

were outlined in

Procedure

AP-301

and included inspecting

equipment often to

minimize the effects of adverse

weather conditions.

Step

5. 1. 1.4.c directed auxiliary operators

to verify heaters

were

operable

in all buildings

and structures.

Nany of the deficient

heaters

in the

ESW intake structure

had not been identified or

corrected until after inspectors

questioned

the cold temperatures

in the "B" electrical

equipment

room.

The failure to implement

Procedure

AP-301 adequately

to verify heaters

were operable

in the

outlying areas is

a violation of the 'requirements

of TS 6.8. I.a.

Violation (400/94-05-01):

Failure to implement procedures

adequately.

Licensee

personnel

stated that they considered

the

FSAR minimum

value of 51'F

(and other minimum values referenced

in Table 9.4.0-

1) to be

a design

standard for the

HVAC systems

in the

ESW

structures

and other plant areas.

Licensee

personnel

are

currently developing

an engineering

evaluation to determine

the

minimum temperatures

at which safety-related

equipment in outlying

areas,

such

as the

ESW structure

and the

EDG buildings,

can still

perform their intended safety functions.

Review of Nonconformance

Reports

(71707)

Adverse Condition Feedback

Reports

(ACFR) were reviewed to verify

the following:

TS were complied with, corrective actions

and

generic

items were identified and items were reported

as required

by 10 CFR 50.73.

(1)

ACFR 94-404 documented that

on January

28,

1994,

an operator

discovered that the room temperature

for the Boric Acid

Transfer

Pump

(BATP) valve gallery had dropped to 62 F.

Operable

boron injection flow paths

are required to be at

least 65'F by TS.

The operator discovered that the room was

colder because

the door leading to the

RAB hallway had

been

left open following maintenance activities

on the

BATPs.

The operator

immediately closed the door and secured

a

cooling fan to raise the room temperature

above

65 F.

The inspector

reviewed the history of temperature

maintenance

issues

associated

with borated water systems

and

violations documented

in NRC Inspection

Report 50-400/91-24.

Licensee corrective action for the deficiencies identified

in that report included increased

monitoring of the boration

system flowpath temperatures.

As a result of the increased

awareness

of temperature

requirements

for the boration

flowpath, licensee

personnel

noted difficulties in

maintaining the

BATP valve gallery above the minimum

requirement.

Room heaters

could not maintain the required

temperature

when adjacent

area cooling units were in

operation.

Licensee

personnel

generated

a work ticket

(WR

92-AALL1) on January

8,

1992, to fabricate

a plexiglass

door

to this room to prevent cooler outside air from entering.

Two years later,

on February

18,

1994, the inspector noted

that

a plexiglass

cover had still not been fabricated

and

the deficiency tag was still on the door.

Instead licensee

personnel

had installed

a sheet of plastic over the door

cage to prevent air flow.

Licensee

personnel

also

discovered that the area

room heater

in the

BATP valve

gallery had

been inoperable

and under clearance

since August

1993.

10 CFR 50, Appendix B, Criteria XVI, requires that measures

shall

be established

to assure that conditions

adverse

to

quality such

as failures, malfunctions, deficiencies,

deviations,

defective

equipment

and non-conformance,

be

promptly identified and corrected.

The licensee's

failure

to correct deficiencies

associated

with the

BATP valve

gallery door promptly led to the inability to maintain the

room above the

65 degree

F minimum requirement.

This is

contrary to the requirements

of 10 CFR 50, Appendix B,

Criteria XVI, and is considered

to be

a violation.

Violation (400/94-05-02):

Failure to implement adequate

corrective actions to prevent recurrence of deficiencies.

ACFR 94-615 reported that

on February

18,

1993,

RCS letdown

was inadvertently isolated during

an

RCS filter backflushing

evolution.

This evolution is controlled by two procedures

OP-107,

Chemical

and Volume Control

System,

and

OP-

120.02.39,

Fuel Handling and Reactor Auxiliary Building

Filter Backflush,

and necessitates

coordination

between

Main

Control

Room

(MCR) and radwaste

personnel.

Radwaste

operators

had previously experienced

problems with the

automatic operation of the backflushing

system,

therefore

the local

manual

mode of backflushing the

RC filter was

implemented

per section 8.5 of Procedure

OP-120.02.39.

Procedure

steps

specify that

MCR personnel

open the

RC

filter bypass

valve

1CS-112

and then direct radwaste

operators

to shut the

RC filter inlet and outlet isolation

valves

(1CS-114,

1CS-118).

When the evolution is complete,

radwaste

personnel

inform the main control

room that the

filter is backflushed,

isolated,

and ready to be placed into

service.

When directed

by

MCR personnel,

radwaste

operators

reopen valves

1CS-114

and

1CS-118

so that valve 1CS-112

can

be closed.

Upon completion of the filter backflush

on

February

18,

MCR personnel

closed

1CS-112 prior to valves

1CS-114

and

1CS-118 being opened.

This action isolated the

letdown system

and raised

system pressure

which potentially

challenged

a system relief valve.

The licensee

is presently

evaluating the cause for this event.

Statements

made

by the

operators

involved indicated that

MCR personnel

were

informed that the backflush

was finished.

MCR personnel

assumed that this meant that the filter was also unisolated

and ready to be returned to service.

Licensee

personnel

have experienced

previous problems with

coordinating filter backflush evolutions.

In NRC Inspection

Report 50-400/92-15

the licensee

was issued

a violation

(400/92-15-01) for failing to implement procedure

OP-107

properly.

This violation occurred

on August 7,

1992, during

an attempt to backflush the seal

water return filter when

the associated

bypass

valve was not opened

as required.

This event also resulted

in a pressure

increase

and

challenge to system relief valves.

In response

to this

event the licensee clarified procedures

OP-120.02.39

and

OP-107 to identify the action required

by the

NCR.

These

actions

were completed

on October

19,

1992.

In addition,

NRC Inspection

Report 50-400/91-27

contained

a non-cited

violation (400/91-27-02) for the failure to

implement

procedure

OP-109 properly,

Boron Recycle System.

This

violation also involved the failure to open the recycle

evaporator

feed filter inlet and outlet valves

when the

filter was returned to service

on December

15,

1991.

Procedures

were clarified in response

to this event.

The

inspectors

reviewed the procedures

involved and found them

to be clear

and concise.

However, the failure of licensee

personnel

to implement procedure

OP-107 properly,

even after

the recurrent

problems

encountered

during this evolution, is

contrary to the requirements

of TS 6.8. l.a and is considered

to be another

example of the violation listed in

paragraph

2.c of this report (400/94-05-01).

Followup of Onsite Events

(93702)

At 12:30 p.m.

on February

17,

1994, the licensee

declared

an

unusual

event due to a plant computer

(ERFIS) failure.

A licensee

system engineer notified the

MCR that his display of reactor

power

had not changed

during the previous

two days.

At 9:55 a.m. it was

determined that the

SPDS display in the

NCR was not updating data

as required.

The licensee's initial investigation determined that

this condition

had existed since ll:00 a.m.

on February

15.

Although the computer failure had

been corrected at 9:55 a.m.

by

restarting the

SPDS program,

an unusual

event

was declared

and

terminated

at 12:30 p.m.

when the investigation results

revealed

that the

SPDS function had

been inoperable for greater

than four

hours.

The inspectors

reviewed the licensee's

emergency

plan

and

determined that the event

was properly classified

and the

emergency

plan was properly implemented.

The licensee

has experienced

previous

problems with ERFIS.

On

February 6,

1993,

an unusual

event

was declared

upon the complete

failure of ERFIS.

LER 92-02 reported the failure to properly log

containment

sump level

and calculate leakrate during an

ERFIS

failure which was unnoticed

by operators.

" The l,icensee's

corrective action for this event included procedure revisions to

provide adequate

details to ensure

proper operation of TS related

functions performed

by ERFIS.

Again in

NRC Inspection

Report

50-400/93-21,

the licensee's

action in response

to the

LER were

considered

to be weak as

a degraded

condition of ERFIS to

calculate

AFD went undetected

by operators.

In response

to this

I

event,

licensee

management

directed that

an event review team

be

formed to address

the computer problems.

The corrective action

proposed

by the event review team

and accomplished

by the licensee

included revising guidance to determine that

AFD indications

are

updating properly prior to declaring the function operable,

increasing

the numeric

AFD display by one additional digit

(thousandths),

and additional training to operators

and computer

maintenance

personnel.

Since the February

17,

1994,

event involved the failure of the

SPDS function of ERFIS

and

was not

a TS related function,

operators

were not periodically checking these

parameters

to

ensure

the data

was updating.

Operators

instead

simply monitored

the computer clock display which was updating correctly for this

event.

The

SPDS function was required

by the emergency

plan but

not included in previous corrective actions.

The failure to take adequate

corrective action to provide

operators with sufficient guidance to determine

the proper

operation of ERFIS is contrary to the requirements

of 10 CFR 50

Appendix B, Criterion XVI and is considered

to be another

example

of the violation discussed

in paragraph 2.d(l) of this report

(400/94-05-02).

3.

Maintenance

~

~a.

Maintenance

Observation

(62703)

The inspector

observed

and reviewed maintenance activities to

verify that correct equipment clearances

were in effect; work

requests

and fire prevention

work permits were issued,

and

TS

requirements

were being followed.

Maintenance

was observed

and

work packages

were reviewed for the following maintenance

activities:

Reset impeller clearance for "A" ESW screen

wash

pump in

accordance

with Procedure

CM-M0195, Emergency Service

Water

Screen

Wash

Pump Disassembly,

Inspection

and Re-assembly.

Inspection

and cleaning of bus

lA1 in accordance

with

Procedure

PM-E0015,

480 Volt and 6.9

KV Transformer

Electrical

and Preventive

Maintenance

Checks.

Repair sodium hydroxide leakage

from level transmitter

L-

7166.

Replace

B phase

overload relay for cooling fan AH-5 (lA-SA)

breaker.

Plug leaking cooling coils for cooling fan AH-86 (1B-SB) in

accordance

with PCR-7157,

Plugging of AH-86B Cooling Coil

Tubes.

10

~

Troubleshoot/Replace

closing coil

on supply breaker

1Al-B2

from emergency

bus

IA-SA to emergency

bus

1A1.

In general,

the performance of work was satisfactory with proper

documentation

of removed

components

and independent verification

of the reinstallation.

(2)

(3)

The inspectors

attended

several

Plan" of the

Day meetings

held

among the shift supervisors,

work control,

and

maintenance

management

personnel.

The licensee

described

the purpose

and conduct of this meeting in procedure

PLP-710,

Work Hanagement

Process.

These meetings

are held

each

weekday at 7: 15 a.m.

Emergent

items

and items

requiring rescheduling

are discussed

at these

meetings.

Operating

personnel

review the schedule

to develop the

necessary

equipment

clearances

to perform the work.

The

inspector considered this meeting

and process

to be

beneficial

as it enhanced

the operator turnover process

to

include craft related

work planned during the upcoming

shift.

In addition, the status of lit main control

board

annunciators

was discussed

with necessary

action to remove

the alarming condition.

As

a followup to the comments

contained

in NRC Inspection

Report 50-400/93-14,

the inspectors

reviewed the current

backlog of uncompleted

maintenance

work tickets.

The

present

backlog of non-outage

work tickets is approximately

1100.

Licensee

management

plans to continue to reduce this

number to an established

goal of 600.

This equates

to

approximately

seven

weeks of work.

The inspector

noted that

the average

age of work tickets

has

been

reduced to 216 days

from a high of approximately

310 days.

The licensee

attributed this reduction to the

new work control center

which has concentrated

on scheduling

the older tickets for

work.

The inspector considered this aspect of work

planning/scheduling

to be effective.

The inspectors

reviewed

an

NAD assessment

dated

February ll,

1994,

performed in the maintenance

functional area.

This

assessment

was requested

by plant management

to determine

the effectiveness

of the maintenance

program.

The

inspectors

considered this pro-active

assessment

to be good

and the assessment

findings indicated that

a thorough look

had

been

performed of the maintenance

organization.

Issues

identified by

NAD included poor initial planning of work

packages,

poor implementation of work package directions,

and poor maintenance

practices.

In addition, significant

problems

were identified with maintaining the data

base for

the

PH program which included incorrect classification

oF

safety-related

PH's, incorrect classification of

environmentally qualified

PH components,

and inappropriate

11

extension of overdue

PH's.

The inspectors

considered this

assessment

to be effective.

Previous

NAD assessments

were also reviewed.

In June

1993

NAD identified deficiencies

in maintenance

program

procedures

which defined independent verification

requirements.

An assessment

of the

new work management

process

was performed in December

1993.

A strength

was

identified in the implementation of safety

system train

outages

as well as deficiencies

noted in the

new work

control/scheduling

process.

The inspectors

concluded

from

these

assessments

that this effort was effective in

identifying areas

in need of improvement.

While reviewing Procedure

PLP-710,

the inspectors

noted that

the licensee

had established

new criteria for establishing

work priorities.

Attachment

5 to this procedure lists the

five new priority classifications.

Priority

E work

was'efined

as

emergency

work that would have

an immediate

and

direct impact

on the health

and safety of the general

public

or work to prevent the deterioration of plant conditions to

unsafe or unstable levels.

This type of work could

be

authorized to begin prior to planning being completed

and

documented after the fact.

The procedure listed three

examples of emergency

type of work:

I)

Technical Specification 3.0.3 entry.

2)

Significant acid or caustic

system leaks that directly

impact personnel

safety or the environment

and cannot

be isolated.

3)

Large condenser

vacuum leak that results in a

continuous

load reduction to prevent

a unit trip.

The inspector disagreed

with the statement

that emergency

work could be authorized during all

TS 3.0.3 entries.

In

NRC Inspection

Report 50-400/93-08 the licensee

was issued

a

deviation

(400/93-08-03) for performing non-emergency

safety-related

maintenance

without preplanning.

The

licensee

responded

to this deviation by revising the work

control procedure to specify that emergency

work would only

be authorized for those conditions to protect the health

nad

safety of the public, to protect equipment or personnel,

or

to prevent the deterioration of plant conditions to unsafe

or unstable levels.

The inspectors

closed out this

deviation

based

on these corrective actions

being

implemented.

The licensee

has entered

TS 3.0.3

on several

occasions

in

the past.

Some of these

occasions

were documented

in

LER

93-05, safety-related

room cooling units inoperable,

LER

12

93-02, failure to stroke test charging

system valves,

and

LER 92-12, relay failure exceeded

out of service time.

Since

each

one of these

TS 3.0.3 entries did not jeopardize

the ability to safety

shutdown the plant, the inspector

concluded that not all

TS 3.0.3 entries

should

be classified

as

emergency situations necessitating

alleviation of work

planning requirements.

The inspector discussed

this

condition with licensee

management

personnel

who stated that

procedure clarifications would be made.

No violations or deviations

were identified.

b.

Surveillance

Observation

(61726)

Surveillance tests

were observed

to verify that approved

procedures

were being used; qualified personnel

were conducting

the tests;

tests

were adequate

to verify equipment operability;

calibrated

equipment

was utilized;

and

TS requirements

were

'ollowed.

The following tests

were observed

and/or data reviewed:

~

OST-1021

Daily Surveillance

Requirements

Daily Interval

~

OST-1026

Reactor Coolant System

Leakage

Evaluation Daily

Interval

~

OST-1214

Emergency Service Water System Operability Train

A quarterly Interval.

~

OST-1813

Remote

Shutdown

System Operability 18 Month

Interval

~

MST-I0183

Containment

Spray Additive Tank Level

Loop (L-

7166) Calibration.

~

MST-I0254

Reactor Coolant

Loop Cold Leg Temperature

Instrument Operational

Test.

The performance of these

procedures

was found to be satisfactory

with proper

use of calibrated test equipment,

necessary

communications

established,

notification/authorization of control

room personnel,

and knowledgeable

personnel

having performed the

tasks.

No violations or deviations

were observed.

Engineering

Design

Changes

and Modifications (37828)

Plant

Change

Requests

(PCR) involving the installation of new or

modified systems

were reviewed to verify that the changes

were

reviewed

and approved

in accordance

with 10 CFR 50.59, that the

changes

were performed in accordance

with technically adequate

and

approved

procedures,

that subsequent

testing

and test results

met

13

approved

acceptance

criteria or deviations

were resolved

in an

acceptable

manner,

and that appropriate

drawings

and facility

procedures

were revised

as necessary.

In addition,

PCRs

documenting engineering

evaluations

were also reviewed.

The

following modifications and/or testing in progress

were observed:

~

PCR-6526,

Frequently Cycled

LK Breakers

PCR-7144,

Wires Are Swollen

on 3AV-B45B-1002

~

PCR-7157,

Plugging of AH-86B Cooling Coil Tubes

As noted in

NRC Inspection

Report 50-400/93-25,

on

Jan'uary

8,

1994, the

B RAB Emergency

Exhaust

Fan inlet valve

(AV-B4) failed to operate satisfactory after the

implementation of modification PCR-7144.

The inspectors

reviewed the modification and implementing work packages

(WR

94-AAIE1).

The repair replaced

swollen wires found inside

the motor operated

valve in accordance

with procedure

EH-

003, Termination

and Testing of Wire and Cable.

Attachment

1 to this procedure

provides

a checklist of the important

attributes for conducting the wire terminations

and provides

for signature

blocks to document

accomplishment.

This

attachment

also specified that

a guality Verification (gV)

signature

was required to verify that the cable conductor

identification was correct.

The licensee's

investigation of

the valve operating

problem revealed that two of the seven

cables

involved were terminated to the incorrect terminal

due to incorrect labeling of the cable conductors.

The inspector discussed

this matter with craft and

gV

personnel.

Craft personnel

believed that they had

terminated

the cable conductors correctly.

The

gV

individual involved admitted that

he had only verified that

three of the seven cable conductors

were labeled correctly

and that based

on this

he did not consider verification of

the other four necessary

to meet this requirement.

The

gV

inspector

had nevertheless

signed the attachment

on January

7,

1994,

documenting satisfactory labeling of the cable

conductors.

The two cable conductors

which were incorrectly

terminated

had not been verified by gV.

The failure to verify correct labeling of the cable

conductors

properly is contrary to the requirements

of

Procedure

Bl-003 and is considered

to be

a violation.

Although this matter

was identified by licensee

personnel

during the post modification testing, it is being cited due

to the importance of the breakdown of the independent

verification process.

This procedural violation is

considered

to be another

example of the violation noted in

paragraph

2.c. of this report (400/94-05-01).

In accordance

with modification PCR-6526,

the licensee

installed

a new breaker for the "A" station air compressor

in non-safety

bus

1A1 to replace the old LK-16 breaker.

Licensee

personnel

decided to install

a non-safety

breaker

before

any subsequent

safety-related

breaker modifications

to identify potential

problem areas for correction prior to

the safety-related

bus maintenance

presently

scheduled for

the next refueling outage.

Licensee

personnel

experienced

physical

problems with the

new Siemans

breaker

and cradle

assembly

when inserted into

the breaker cubicle.

Minor fit-up problems

were noted with

fuse/terminal

block sizes.

In addition, licensee

personnel

found that the

new breaker

was extremely hard to rack in.

Physical alterations

were

made to install the breaker

successfully.

Two wiring deficiencies

were also identified

by licensee

personnel

during the installation process.

The

licensee

decided that

a wire to wire check would be

beneficial for future installations.

Deficiencies

were also

identified with the post-modification testing procedure

and

PH procedure.

The licensee

plans to revise these

procedures

accordingly.

The licensee

held

a post-modification critique meeting to

discuss

these

problems

and corrective action.

A video of

the installation process

was

made

and viewed during this

meeting.

During the restoration of bus lAl, the feeder breaker

from

bus

1A-SA failed to properly close electrically.

Licensee

personnel

replaced

the closing coil on the feeder breaker

which subsequently

operated satisfactorily.

This breaker

will also

be replaced

during the refueling outage

breaker

modification.

The inspectors

considered

the licensee's

preliminary efforts for the outage

breaker

replacement

work

to be beneficial.

The inspectors

reviewed maintenance activities to replace

cooling coils on air handler

AH-86 (1B-SB) in the

ESW intake

structure.

The work was

done in accordance

with PCR-7157.

The inspectors

reviewed

PCR-7157,

Revision

0 and Revision

1

to verify that appropriate technical

and safety reviews were

documented.

A safety review package

was completed for each

revision of the

PCR.

This activity was required

by

Procedure

AP-011, Safety Reviews,

and included

an Unreviewed

Safety guestion Determination

as mandated

by 10 CFR 50.59.

During a review of the safety

package for PCR-7157,

Revision 0,

(completed

and approved

January

20,

1994) the

inspector noted that the

same generic written basis

appeared

in the answers to four different and distinct questions

related to the malfunction of equipment

and the probability

of accidents

as evaluated

in the Safety Analysis Report.

15

Specifically, the words "the leaking coils are

removed

from

service via a proven method"

were documented

as the only

written basis for answering

"no" to each

one of the

following questions:

guestion I:

May the proposed activity increase

the

probability of occurrence of an accident

evaluated

previously in the Safety Analysis Report?

guestion

3:

Hay the proposed activity increase

the

probability of occurrence of a malfunction of equipment

important to safety evaluated

previously in the Safety

Analysis Report?

guestion

5:

Hay the proposed activity create

the

possibility of an accident of a different type than

any

evaluated

previously in the Safety Analysis Report?

guestion

6:

Hay the proposed activity create

the

possibility of a malfunction of equipment

important to

safety of a different type than

any evaluated

previously in

the Safety Analysis Report?

The answers

to the questions

were simplistic and lacking in

depth to address

the specifics of each question.

Section

3.2 of procedure

AP-Oll stated that qualified safety

reviewers shall perform safety reviews in accordance

with

the program manual

(Attachment 6).

Attachment 6,

Rev. 3,

Section 8.2,

Documentation,

stated

in part that although the

answers

in Part

IV (Unreviewed Safety guestion

Determina-

tion) are simply "yes" or "no", there must

be

an

accompanying justification.

Making a simple statement of

conclusion is not sufficient.

The inspector noted,

however,

that the accompanying

Safety Analysis for the plugged

cooling coils did address

the overall safety concern.

The diminished ability of the air handler to cool the intake

structure

was minimized by the current

season

and the fact

that the coils would be permanently

replaced during

RFO-5

beginning in March 1994.

In addition,

Rev. I to the

PCR had-

been

completed

and approved

one day later

and effectively

superseded

Rev.

0 to the

PCR.

Rev. I contained

a more

detailed safety anslysis,

a better documented

technical

review,

and more detailed

answers

to all seven of the

questions

related to the unreviewed safety question

determination.

The inspectors

noted that Rev. I had

been

completed

by the license

before the inspector identified the

deficiency in Rev.

0.

While the accompanying

safety analysis for Revision

0 was

considered

to be adequate

to address

potential safety

concerns,

the inspectors

considered

the licensee's

answers

16

to the questions for the unreviewed safety question

determination

in Revision

0 to be weak.

NRC Inspection

Report 50-400/93-07

documented

a similar example where two

separate

and distinct modifications contained similar

wording as the basis for determining that

no unreviewed

safety question existed.

However,

as with the previous

example,

the inspectors

agreed with the safety reviewer's

conclusion that

an unreviewed safety question did not exist

for PCR-7157.

The inspector also considered

the safety

review for PCR-7157,

revision I to be good.

ll

System Engineering

On January

22,

1994, plant power was reduced to

approximately

84 percent to perform main turbine valve

testing.

The inspectors

were previously informed that the

reactor engineering

group

had recently obtained

a new

computer software

system

(POWERTRAX) to anticipate/calculate

core parameters

in three dimensions to assist

the operators

during the downpower.

Appropriate recommendations

were

suggested

to the operating shift on rate of power change,

rod bank insertion values,

and boration/dilution volume

estimates.

The inspectors

noted that

AFD predictions

and

actual

values closely agreed

and little problems

were noted

during the downpower evolution.

The inspectors

concluded

that technical

support for this plant evolution was good.

(2)

The inspector discussed

a recent industry event involving

the failure of an NSIV to operate

properly with the

responsible

system engineer.

During the industry event,

a

34 inch air-to-open/spring-to-close

globe valve manufactured

by Atwood and Norrill failed to close following receipt of a

main steam isolation signal

which resulted in steaming

a

steam generator dry.

The cause for this condition was

attributed to valve reassembly

and alignment following

maintenance

at

a temperature

other than the valve's

normal

operating temperature.

The system engineer

informed the inspector that the plant

main steam

system design utilizes

a similar

Y type

32-inch

globe valve manufactured

by Rockwell for the main steam

isolation function.

These

valves

are likewise air-to-

open/spring-to-close

operated.

To aid in

disassembly/reassembly,

the valves

have alignment pins

and

are marked to ensure satisfactory

realignment following

maintenance.

In addition, the valves are subsequently

stroke tested while the plant is in the hot standby

(Node 3)

condition following maintenance.

No violations or deviations

were identified.

17

Plant Support

a ~

b.

I

Plant Housekeeping

Conditions

(71707)

- Storage of material

and

components,

and cleanliness

conditions of various areas

throughout

the facility were observed to determine

whether safety 'and/or fire

hazards

existed.

As noted in paragraph

2.b the general

house-

keeping in the steam tunnel

was considered

to be poor.

Also

during plant tours,

the inspectors

noted poor housekeeping

in the

boric acid transfer

pump room (loose insulation canning,

cotton

gloves discarded

on floor) and in the

286 foot elevation of the

RAB by NCC lA31-SA (discarded

tie-wraps

and tape).

In addition,

the inspectors

noted the general

poor cleanliness

condition of the

NCB.

Dirt and dust

was observed

which indicated that poor

housekeeping

standards

were being maintained

in this highly

visible area of the plant.

The inspector

concluded that plant

management

needed to reenforce

high housekeeping

standards.

Radiological Protection

Program

(71707)

- Radiation protection

control activities were observed routinely to verify that these

activities were in conformance with the facility policies

and

procedures,

and in compliance with regulatory requirements.

The

inspectors

also reviewed selected

radiation work permits to verify

that controls were adequate.

On January

22,

1994, the licensee

discovered

an unlocked hatch

on

a cask

used to store spent demineralizer filters.

The cask

was

one of two located in the

211 foot elevation of the

WPB and

was

posted

as

a Locked High Radiation Area

(LHRA).

The hatch,

which

is located at the top of the cask

and is accessible

only with the

aid of a ladder,

was discovered

by technicians

performing routine

rounds approximately fifteen hours after the last

known entry was

made.

The hatch covers

a 24-inch diameter

opening into which technicians

routinely deposit highly radioactive

spent filters. It is usually

secured

by a padlock which engages

a small U-hook on the cask.

The lock was found to be locked, but not engaged

in the U-hook to

prevent the door from opening.

The inspectors

discussed

the

incident with licensee

personnel

who indicated that the unlocked

cask

was the result of personnel

error and that the involved

technician thought the lock was

engaged

when the key was removed.

Upon discovering the unlocked cask,

technicians

locked it and

performed

a radiological

survey of the area.

Surveys indicated

radiation levels of 800 mR/hr at the plane of the hatch'with it

opened

and 2.5 R/hr on contact with the filters which were stored

inside.

The top of the filters inside the cask were at

a level of

approximately

30 inches

below the plane of the hatch.

The

inspector toured the area

and observed that although the cask

opening

was big enough to allow a person to climb inside,

no

personnel

would routinely access

this hatch for reasons

other than

to drop filters inside.

Licensee

personnel

also indicated that

there

were

no unusually high exposures

recorded

on the day the

0

18

cask

was unlocked.

The inspector

concluded that

no personnel

over-exposure

occurred

as

a result of this incident.

The

inspector

also discussed

the potential for personal

overexposure

with NRC Regional Specialists

who concluded that,

given the

location

and configuration of the filter cask,

the potential for

excessive

exposure

was minimal.

The licensee's

administrative

Procedure

AP-504, Administrative

Controls for Locked, Restricted

and Very High Radiation Areas,

specifies

in Section

5. 1 that

LHRAs shall

remain locked at all

times unless

under the direct control of an individual controlling

access

to the area.

The licensee's

actions regarding the unlocked

filter cask are considered

to be

a violation of the above

requirements.

This violation will not be subject to enforcement

action

because

the licensee's

efforts in identifying and

correcting the violation meet the criteria specified in Section

VII.B of the Enforcement Policy.

Non-cited Violation (400/94-05-03):

Failure to maintain

a

LHRA

locked.

The licensee's

corrective actions for the above violation included

counseling

the involved individual

and other health physics

technicians,

and revising AP-504 to require

an independent

verification of LHRAs.

The above corrective actions

were

presented

before the

PNSC

on February

23,

1994.

Security Control

(71707)

- The performance of various shifts of

the security force was observed

in the conduct of daily activities

which included:

protected

and vital area

access

controls;

searching of personnel,

packages,

and vehicles;

badge

issuance

and

retrieval; escorting of visitors; patrols;

and compensatory

posts.

In addition, the inspector

observed

the operational

status of

Closed Circuit Television

(CCTV) monitors, the intrusion detection

system in the central

and secondary

alarm stations,

protected

area

lighting, protected

and vital area barrier integrity,

and the

security organization interface with operations

and maintenance.

(1)

During this inspection period the licensee

moved the

perimeter fence

such that the administration building was

located outside the protected

area.

The inspectors

walked

down the

new fence

and observed

portions of the testing

performed

on the modified intrusion detection

system,

CCTV,

and lighting systems.

Performance of the testing

was

observed

from the central

alarm station

and in the field.

To alleviate distractions,

security force personnel

routed

the majority of communications to the secondary

alarm

station during performance of the testing.

The inspector

considered

the conduct of the testing to be good with

satisfactory results.

19

During the walkdown of the

new perimeter fence,

on

February 8,

1994, the inspector

noted

two areas

along the

fence where gaps existed

between

the fence material

and

ground.

The inspector

measured

these

gaps

and found them to

be approximately six inches in depth.

The inspector

discussed this finding with security personnel

and

was

informed that the fence modification had not yet been

accepted

as complete.

The inspector

was informed that

a gap

size of six inches

was the maximum allowed

and that barbed

wire was to be installed at the bottom of the fence to

prevent

access

through the gap areas.

Appropriate action

was

implemented to correct the fence deficiencies.

The

licensee

continued the use of compensatory

guard posts until

the deficiencies

were corrected.

(2)

The inspector also discussed

the potential

change to the

security plan required

by this modification with licensee

personnel.

The inspector

was informed that

a change

was to

be submitted within 60 days in accordance

with

10 CFR 50.54(p)(2).

On February

17,

1994, while observing the reinspection

effort for the

new fuel assemblies,

the inspector

noticed

two vendor representatives

were standing

nearby with

visitors badges.

The inspector

asked the two individuals

who and where their escort

was.

The visitors indicated that

the escort

was involved in the fuel inspection activities

which were taking place

on the other side of the

new fuel

pool

some fifty to sixty feet away.

The inspector

noted

that although the visitors were visible to their escort,

the

escort

was clearly involved in the inspection activities

and

not in full observation of the visitors.

The inspector

directed the visitors to proceed to where their escort

was

located.

The inspector later discussed

this observation

with the security manager.

Although the inspector did not

,consider this incident to be in violation of security

requirements,

the control of visitors in this case

could

be

strengthened.

The inspector reviewed the Security Plan

and

verified that

no requirements

regarding the escorting of

visitors were violated.

d.

Fire Protection

(71707)

- Fire protection activities, staffing and

equipment

were observed to verify that fire brigade staffing was

appropriate

and that fire alarms,

extinguishing equipment,

actuating controls, fire fighting equipment,

emergency

equipment,

and fire barriers

were operable.

Except

as noted

above,

the inspectors

found plant housekeeping

and

material condition of components

to be satisfactory.

The licensee's

adherence

to radiological controls, security controls, fire protection

requirements,

and

TS requirements

in these

areas

was satisfactory.

20

6.

Preparations

for Refueling

(60705)

The inspectors

reviewed several

aspects

of the licensees

activities

associated

with the upcoming refueling outage

(RFO-5) which was

scheduled

to begin Harch

19,

1994.

This inspection

was performed to

ascertain

the adequacy of the licensee's

procedures for the conduct of

refueling operations,

and to determine

the adequacy of the licensee's

administrative requirements

and implementation of controls for refueling

operations

and plant conditions during refueling.

The inspection

was

accomplished

by reviewing procedures,

observing

new fuel handling

activities,

and interviewing various

key licensee

and contractor

personnel.

In addition, the inspectors

reviewed the licensee's

outage

schedules

and the licensee's

independent

pre-outage

shutdown risk

assessment,

dated January

21,

1994.

a.

New Fuel Receipt

The inspectors

reviewed procedures

and observed activities

associated

with receiving,

inspecting,

and storing

new fuel

assemblies.

Procedures

included

FHP-003,

Unpacking

and Handling

of New Fuel Assemblies

and

New Fuel Shipping;

FHP-004,

New fuel

Handling Tool Operation;

and

FHP-106,

New Fuel Receipt Inspection.

The licensee

received

52 new fuel assemblies

from Siemens

Power

Corporation during January

and February,

1994.

The inspector

observed that licensee

personnel

were moving the

new fuel in

accordance

with Procedure

FHP-003.

However during the first day

of inspections,

the inspector

noted several

unapproved

pencil

changes written into the working copy of the procedure.

The

pencil

changes

were primarily due to technical

terminology

differences

between

the licensee's

current

and previous fuel

vendors

and did not alter the scope of the fuel movement

activities.

The type of procedure

problems identified by the

pencil

changes

should

have

been identified,

and appropriate

procedure clarifications implemented,

prior to the first day of

fuel movement.

After the inspector identified this matter to

licensee

personnel,

a temporary

change to Procedure

FHP-003

was

subsequently

initiated and

an advance

change

was implemented

on

February

16,

1994.

The inspector reviewed training certifications for six fuel

inspectors

and observed

fuel inspection activities done at the

Harris site in accordance

with Procedure

FHP-006.

The inspector

observed that the licensee

was especially sensitive to foreign

material

exclusion requirements.

The inspector also observed that

qualified fuel inspectors,

as well as

a quality control

representative

from the fuel vendor,

were present to oversee

fuel

assembly

inspections.

The fuel inspectors

did not restrict their

focus to those inspection objectives called

upon in Procedure

FHP-006.

This resulted

in the identification of discrepancies

in

the fuel assemblies

which resulted

in three defective

assemblies

being returned to the vendor.

Licensee

inspection findings

included the following:

P

21

~

Approximately five fuel bundles

were found with bent tabs

on

grid spacers.

In one case,

the tabs

were found bent

away

from the center

instrument thimble and touching two adjacent

fuel rodlets.

Some of the bent tabs

were able to be field

corrected.

Three assemblies

were sent

back to the vendor

for reworking.

~

A locking lug was found in the non-locked position

on

an

upper tie plate of one of the assemblies.

The locking lug

was immediately placed in the locked position

and

an

ACFR

was generated.

~

A washer

(approximately 3/8 inches outside diameter)

was

found lying on the lower tie plate of an assembly.

Following this discovery,

licensee

personnel

conducted

reinspections

of all 30 of the assemblies

that

had

been

previously inspected

in order to find the mating screw.

The

washer

and screw were believed to have

been dismantled

from

a lifting tool back at the vendor's manufacturing facility.

The missing screw was not found during the subsequent

inspections.

~

A small metal tab,

about the size of a fingernail, broke off

of a feeler gauge

used to measure

separation

between fuel

rodlets.

The measuring

tool

had

been supplied to the

licensee

by the vendor.

The tab,

which had

been spot welded

to the instrument,

was later retrieved

from a fuel assembly

that

had

been previously inspected.

The licensee's

efforts

in identifying the broken tool

and finding the missing piece

was particularly good.

~

During packaging at the manufacturer's facility, each

assembly

had

been

placed in a polyethylene

sleeve prior to

being loaded into a steel

container for shipping.

During

onsite inspections,

some of the steel

containers

were found

to have dust

and dirt located inside.

The fuel assemblies

were protected

from this foreign material

by their

polyethylene

covers.

However,

one of the polyethylene

sleeves

was found with moisture inside.

The moisture

was

attributed to the washing/drying process

back at the

manufacturing point and

was determined

not to be

a threat to

the future performance of the fuel assembly.

In addition to the above,

licensee

personnel

also inspected

each

new assembly for rod perpendicularity,

rod integrity, rod

separation,

and potential

bowing of rods.

ACFRs were generated

for all of the noted discrepancies

and were in the process of

being resolved

by the licensee's

corporate office at the close of

this inspection period.

Overall, the licensee's

fuel receipt

inspection activities were very thorough in identifying and

addressing

the deficiencies

noted

above.

22

Since the above fuel receipt inspections

indicated

a potential

vendor quality control problem,

the resident

inspectors

interviewed several

key vendor

and licensee

personnel

who had

been

involved in the licensee's

corporate oversight of the fuel

fabrication process.

The licensee's

corporate oversight

program

had

been

implemented

as

a result of fabrication problems

identified previously for the Robinson plant.

The vendor

representative

acknowledged that corrective actions

had only been

implemented related to the design

and fabrication of the

assemblies,

and for the exclusion of foreign material

at the fuel

services

side of the vendor's operation.

Foreign material

exclusion

had not been rigorously addressed

from a manufacturing

perspective,

which could have contributed to the washer intrusion

problem.

Vendor representatives

stated that they were in the

process

of developing corrective actions to address

the licensee's

findings.

The resident

inspectors

reviewed licensee

inspection

and trip

reports

documenting the results of the corporate oversight efforts

conducted prior to the fuel being shipped to Harris.

The

inspectors

noted that characteristic's

for some of the findings

noted

above

(bent tabs,

unlocked locking lug) were documented

in

the reports

as having

been inspected.

No deficiencies

were

identified.

However, licensee

personnel

indicated that the

inspection effort was not

a

100 percent effort in that, while

portions of the fabrication process

had

been

inspected for all of

the assemblies,

only a few assemblies

were completely inspected

during the entire manufacturing

process.

Administrative Controls for Refueling Operations

The inspector reviewed the licensee's

administrative controls for

refueling operations

as established

in Procedure

PLP-700,

Outage

Nanagement.

This procedure

defined lines of supervision within

the outage organization

and listed responsibilities for all key

personnel

including the outage

manager, shift outage

managers,

and

work activity coordinators.

The inspector noted that key

positions

had already

been

appointed

and,

through interviews,

concluded that the incumbents

were cognizant of their outage

responsibilities.

The inspector also interviewed

NAD personnel

to determine

what

gA/gC activities would be completed during the upcoming outage.

Licensee

personnel

indicated that both

an outage

assessment

and

a

vendor assessment

would be performed during RFO-5.

The vendor

assessment

would consist of daily surveillance

observations

from

gV personnel

in the

NAD organization.

The surveillances

would be

performed

by approximately fifteen gV inspectors for several

of

the major outage activities in which contractor personnel

would be

primarily involved.

These activities include steam generator

eddy

current testing,

LK-16 breaker replacement,

RTD bypass

removal,

auxiliary feedwater

pipe replacement,

and refueling.

The

23

inspector reviewed the surveillance

plan for the

RTD bypass

removal job and noted that the other plans

were currently under

development

at the close of this inspection period.

As required

by Procedure

PLP-700,

Step 5.2.2.2.7,

the licensee

completed

a pre-outage risk assessment,

dated

January

21,

1994.

The assessment

was performed using

PG0-060,

Outage

Risk Hanagement

Policy and Principles

and

PLP-700,

Attachment ll, Outage Risk

Management

Scheduling

and Assessment

Guidelines.

No mid-loop or

reduced

inventory conditions with fuel in the vessel

are planned

for RFO-5.

However, the licensee's

risk assessment

did identify

five issues

and several

recommendations

concerning the outage

schedule

and related

procedures.

The issues'ncluded

the lack of

a comprehensive

plan for containment

closure prior to core

boiling, the untimely scheduling of tasks that affect

RCS makeup

capability while fuel is in the reactor vessel,

procedure

conflicts,

and personnel

training issues.

The issues

were

required to be addressed

prior to

RFO 5.

The risk assessment

also verified the availability and control

over key plant safety

and support

systems

throughout the outage.

For example,

at least

one source of offsite electrical

power and

one

EDG were verified to be available

by schedule

throughout the

RFO

5 schedule.

Two

RHR trains were verified by the licensee's

assessment

to be available while fuel

was in the reactor vessel

with the upper internals installed.

The assessment

also verified

that the

ESW and

CCW systems

were available to support

RHR

operability requirements

per, TS 3.9.8.2.

The risk assessment

also verified that procedural

requirements for

LTOP operability and other

RCS pressure

control provisions were in

place.

Containment integrity was verified to be in place for

operating

modes I through 4.

The assessment

also verified that

procedural

requirements

existed for communications

between the

control

room and personnel

on the refueling floor.

The inspectors

will independently verify selected

assessment

attributes during

future routine inspection activities.

The licensee's

pre-outage risk assessment

was thorough

and for the

areas

reviewed

above,

the licensee's

administrative controls were

adequate

for establishing

control of plant conditions during

RF0-5.

Review of LERs (92700)

(Open)

LER 93-04:

This

LER reported that the required surveillance

testing interval for the control

room

HVAC system

had

been

exceeded

on

four occasions.

This matter

was previously discussed

in NRC Inspection

Report 50-400/93-10.

The licensee

has completed real-time training on

this event for operators

and has revised the inservice testing

program

to enhance

the review process.

In addition

PCR-7014,

Correct

EBASCO

Valve and

Damper Nomenclature

on Control

Room Switches,

has

been

initiated to correct the dual labeling systems

presently

employed for

this system.

The

LER will remain

open pending completion of the

PCR.

Licensee Action on Previously Identified Inspection

Findings

(92702

&

92701),

(Closed)

Inspector

Followup Item 400/92-08-01:

Follow the

licensee's

activities to improve the work scheduling

system.

The inspectors

reviewed

a system outage for the

TDAFM pump which

was planned

and scheduled

January

12,

1994.

This outage

was

completed successfully

and resulted

in many

PHs

and corrective

maintenance activities being accomplished

in a relatively short

time frame.

The coordination of these activities minimized

equipment out of service time for these

components.

The

inspectors

considered

the reduction in safety-related

equipment

unavailability time to be beneficial to the safe operation of the

plant.

The inspectors

also noted that work was scheduled

on the

RAB

emergency

exhaust

system

on two separate

occasions

within a two

week period,

however.

The

RAB emergency

exhaust

fan (E-6B) was

removed

from service

on January

4,

1994, for preventive

maintenance

on the fan's inlet and exhaust

dampers.

The system

was returned to service

and tested

on January

8.

In the following

week,

on January

13, the fan was again

removed from service for

preventive maintenance

on another

system

damper.

The fan was

again retested

and returned to service

on January

14.

Since both

scheduled activities required entering

an equipment

LCO, the

inspector considered

the scheduling of the activities to be

deficient

as they resulted in redundant

equipment testing

and

unnecessary

equipment out of service time.

The licensee

has experienced

previous

problems with scheduling

HVAC type of work.

As discussed

in NRC Inspection

Report

50-400/93-21,

the scheduling of control

room

HVAC maintenance

was

deficient.

The inspector discussed

the corrective action taken

for the previous

problem with licensee

work control personnel

to

determine if additional action

was required to properly schedule

these activities.

The inspector

was informed that the previous

action properly identified the work but personnel

error resulted

in the poor scheduling of the

RAB ventilation system work.

Again in this instance

no TS equipment out of service times were

exceeded

by the licensee.

Although the inspectors

considered

the

new scheduling/work control

system to be satisfactory with the

planning concept of system

outages

to be

a strength,

the

coordination of HVAC system outages

was considered

to be weak.

25

b.

(Closed)

Inspector

Followup Item 400/93-08-05:

Follow the

licensee's

activities to increase

ESCWS reliability.

Upon further review of PCR-6493,

ESCWS Chiller Low

Flow/Temperature. Trip Alarm, by the

PNSC, licensee

management

decided to cancel

the

PCR.

This decision

was

based

on the

reliable history of operation of the chillers since July 1992.

The inspector considered

the licensee's

action for this matter to

be satisfactory.

c.

(Closed)

Unresolved

Item 400/93-21-01:

Testing of control

circuits required for safe

shutdown.

The inspector reviewed analysis

E-5523, revision 1,

Instrumentation,

Control

and Transfer Switches for Components

Credited in the Event of a Fire Requiring Control

Room Evacuation,

which the licensee initiated to clearly state

which components

were required to perform the functions necessary

to achieve

safe

shutdown.

The inspector determined that procedure

OST-1813,

Remote

Shutdown

System Operability

18 Honth Interval,

was properly

implementing the requirements

of TS 4.3.3.5.2.

The licensee

has

incorporated this analysis

by reference

in the safe

shutdown

analysis.

The licensee

had corrected

previous

comments

on inaccurate

references

to non-existent

tables

and

an inaccurate

table of

contents for the safe

shutdown analysis.

However, the inspector

noted that even with the

new reference to analysis

E-5523 the safe

shutdown analysis still contained

no clear statement

of the "B"

train components fulfillingthe functions specified

by TS 4.3.3.5.2.

In addition, the inspector

found two component

numbers

in analysis

E-5523 which were incorrect.

Although the inspector

considered

the licensee's

action to be sufficient to close this

item, the safe

shutdown analysis

could be further clarified and

improved.

Exit Interview (30703)

The inspectors

met with licensee

representatives

(denoted

in paragraph

1) at the conclusion of the inspection

on February

22,

1994.

During

this meeting,

the inspectors

summarized

the scope

and findings of the

inspection

as they are detailed in this report, with particular emphasis

on the Violations addressed

below.

The licensee

representatives

acknowledged

the inspector's

comments

and did not identify as

proprietary

any of the materials

provided to or reviewed

by the

inspectors

during this inspection.

No dissenting

comments

from the

licensee

were received.

26

Item Number

Descri tion and Reference

400/94-05-01

400/94-05-02

400/94-05-03

Violation:

Failure to implement procedures

properly,

paragraphs

2.c, 2.d(2),

and 4.a(l).

Violation:

Failure to implement corrective

action to preclude recurrence,

paragraphs

2.d(1)

and 2.e.

Non-Cited Violation:

Failure to control

a

locked high radiation area,

paragraph

5.b.

Acronyms

ACFR

AFD

AFW

BATP

CCTV

CCW

CFR

CSIP

DSR

EDG

ESCWS

ESW

FASR

HVAC

LCO

LER

LHRA

LTOP

MCB

MCC

MCR

MSIV

NAD

NRC

PCR

PM

PNSC

QA/QC

QV

RAB

RCS

RFO

RHR

RTD

RWST

and Initialisms

Adverse Condition Feedback

Report

Axial Flux Difference

Auxiliary Feedwater

Boric Acid Transfer

Pump

Closed Circuit Television

Component Cooling Water

Code of Federal

Regulations

Charging Safety Injection

Pump

Daily Surveilance

Requirement

Emergency Diesel

Generator

Essential

Services Chilled Water System

Emergency Service Water

'inal

Safety Analysis Report

Heating Ventillation Air Conditioning

Limiting Condition for Operation

Licensee

Event Report

Locked High Radiation Area

Low Temperature

Overpressure

Protection

Main Control

Board

Motor Control Center

Main Control

Room

Main Steam Isolation Valve

Nuclear Assessment

Department

Nuclear Regulatory

Commission

Plant

Change

Request

Preventive

Maintenance

Plant Nuclear Safety Committee

Quality Assurrance/Quality

Control

Quality Verification

Reactor Auxiliary Building

Reactor Coolant System

Refueling Outage

Residual

Heat

Removal

Resistance

Temperature

Detector

Refueling Water Storage

Tank

26

Item Number

Descri tion and Reference

400/94-05-01

400/94-05-02

400/94-05-03

Violation:

Failure to properly implement

procedures,

paragraphs

2.c, 2.d(2),

and

4.a(1).

Violation:

Failure to implement corrective

action to preclude recurrence,

paragraphs

2.d(1)

and 2.e.

Non-Cited Violation:

Failure to control

a

locked high radiation area,

paragraph

5.b.

Acronyms

and Initialisms,

ACFR

AFD

AFW

BATP

CCTV

CCW

CFR

CSIP

DSR

EDG

ESCWS-

ESW

FASR

HVAC

LCO

LER

LHRA

LTOP

MCB

MCC

MCR

MSIV

NAD

NRC

PCR

PM

PNSC

QA/QC-

QV

RAB

RCS

RFO

RHR

RTD

RWST

Adverse Condition Feedback

Report

Axial Flux Difference

Auxiliary Feedwater

Boric Acid Transfer

Pump

Closed Circuit Television

Component

Cooling Water

Code of Federal

Regulations

Charging Safety Injection

Pump

Daily Surveilance

Requirement

Emergency Diesel

Generator

Essential

Services

Chilled Water System

Emergency Service

Water

Final Safety Analysis Report

Heating Ventillation Air Conditioning

Limiting Condition for Operation

Licensee

Event Report

Locked High Radiation Area

Low Temperature

Overpressure

Protection

Main Control

Board

Motor Control Center

Main Control

Room

Main Steam Isolation Valve

Nuclear Assessment

Department

Nuclear Regulatory

Commission

Plant

Change

Request

Preventive

Maintenance

Plant Nuclear Safety Committee

Quality Assurrance/Quality

Control

Quality Verification

Reactor Auxiliary Building

Reactor Coolant System

Refueling Outage

Residual

Heat

Removal

Resistance

Temperature

Detector

Refueling Water Storage

Tank

TDAFW-

TS

WPB

WR 27

Turbine Driven Auxiliary Feedwater

Technical Specification

Waste Processing

Building

Work Request