ML18010B089

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Insp Rept 50-400/93-08 on 930320-0416.Violation & Deviation Noted.Major Areas Inspected:Plant Operations,Radiological Controls,Security & Surveillance Observation
ML18010B089
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 05/05/1993
From: Christensen H, Darrell Roberts, Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18010B086 List:
References
50-400-93-08, 50-400-93-8, NUDOCS 9305180240
Download: ML18010B089 (27)


See also: IR 05000400/1993008

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report No.:

50-400/93-08

Licensee:

Carolina

Power and Light Company

P. 0.

Box 1551

Raleigh,

NC 27602

Docket No.:

50-400

/

Facility Name:

Harris

1

Inspection

Conducted:

March 20 - April 16,

1993

Inspectors:

J.

edrow

en or Resident

Inspectop

D.

obert

,

ident Inspector

Approved by:

H. I.hristensen,

Section Chief

Division of Reactor Projects

SUMMARY

Licensee

No.:

NPF-63

ssH

Da e

igned

Date Signed

Dat

igned

Scope:

This routine inspection

was conducted

by the resident

inspectors

in the areas

of plant operations,

radiological controls, security, surveillance

observation,

maintenance

observation,

design

changes

and modifications, fire

protection/prevention,

essential

services chilled water system reliability,

licensee

event reports,

and licensee

action

on previous inspection

items.

Numerous facility tours were conducted

and facility operations

observed.

Some

of these tours

and observations

were conducted

on backshifts.

Results:

One violation and

one deviation were identified:

Failure to properly

implement inservice testing for components with data in the alert range,

paragraph 2.c.(l); Performance of non-emergency

safety-related

maintenance

without appropriate

preplanning,

paragraph

4.a.

A licensee identified non-cited violation was identified regarding the failure

to maintain apropriate actuation setpoints

for the containment

vacuum relief

system,

paragraph 2.c.(2).

Maintenance activities to identify and correct deficiencies with air handler

AH-92A were considered

to be poor.,

paragraph

4.b.

Engineering

support

and contingency planning for a potentially inoperable

emergency battery cell were considered

to be weak,

paragraph

4.d.

9305180240

930506

PDR

ADDCK 05000400

8

PDR

REPORT

DETAILS,

1.

Persons

Contacted

Licensee

Employees

  • J. Cribb, Manager,

equality Control

  • C. Gibson,

Manager,

Programs

and Procedures

  • H. Hamby,

Manager,

Regulatory

Compliance

  • D. McCarthy, Manager,

Regulatory Affairs

  • T. Morton, Manager,

Maintenance

  • J. Nevill, Manager,

Technical

Support

  • W. Robinson,

General

Manager,

Harris Plant

  • W. Seyler,

Manager,

Outages

and Modifications

H. Smith, Hanager,

Radwaste

Operation

  • D. Tibbitts, Manager,

Operations

  • G. Vaughn, Vice President,

Harris Nuclear Project

  • W. Wilson, Manager,

Spent Nuclear Fuel

  • L. Woods,

Manager,

Systems

Engineering

Other licensee

employees

contacted

included office, operations,

engineering,

maintenance,

chemistry/radiation

and corporate

personnel.

  • Attended exit interview

2.

Acronyms

and initialisms used throughout this'report

are listed in the

last paragraph.

Review of Plant Operations

(71707)

The plant continued in power operation

(Mode 1) for the duration of this

inspection period.

a.

Shift Logs

and Facility Records

The inspector

reviewed records

and discussed

various entries with

operations

personnel

to= verify compliance with the Technical

Specifications

(TS)

and the licensee's

administrative procedures.

The following records

were reviewed:

shift supervisor's

log;

control operator's

log; night order book; equipment

inoperable

record; active clearance

log; grounding device log; temporary

modification .log; chemistry daily reports; shift.turnover

checklist;

and selected

radwaste

logs.

In addition, the inspector

independently verified clearance

order tagouts.

The inspectors

found the logs to be readable,

well organized,

and

provided sufficient information on plant status

and events.

Clearance

tagouts

were found to be properly implemented.

No

violations or deviations

were identified.

Facility Tours

and Observations

Throughout the inspection period, facility tours were conducted to

observe operations,

surveillance,

and maintenance activities in

progress.

Some of these

observations

were conducted during

backshifts.

Also, during this inspection period, licensee

meetings

were attended

by the inspectors

to observe

planning

and

management activities.

The facility tours

and observations

encompassed

the following areas:

security perimeter fence;

control

room; emergency diesel

generator building; reactor

auxiliary building; waste processing

building; turbine building;

fuel handling building; emergency

service water building; battery

rooms; electrical

switchgear

rooms;

and the technical

support

center.

During these tours,

the following observations

were made:

Monitoring Instrumentation

- Equipment operating status,

area

atmospheric

and liquid radiation monitors, electrical

system lineup, reactor operating

parameters,

and auxiliary

equipment operating

parameters

were observed

to verify that

indicated parameters

were in accordance

with the

TS for the

current operational

mode.

(2)

Shift Staffing - The inspectors verified that operating

shift staffing was in accordance

with TS requirements

and

that control

room operations

were being conducted

in an

orderly and professional

manner.

In addition,

the inspector

observed shift turnovers

on various occasions

to verify the

continuity of plant status,

operational

problems,

and other

pertinent plant information during these turnovers.

(3)

Plant Housekeeping

Conditions

- Storage of material

and

components,

and cleanliness

conditions of various areas

throughout the facility were observed to determine whether

safety and/or fire hazards

existed.

(4)

Radiological

Protection

Program - Radiation protection

control activities were observed routinely to verify that

these activities were in conformance with the facility

policies

and procedures,

and in compliance with regulatory

requirements.

The inspectors

also reviewed selected

radiation work permits to verify that controls were

adequate.

Security Control - The performance of various shifts of the

security force was observed

in the conduct of daily

activities which included:

protected

and vital area

access

controls;

searching of personnel,

packages,

and vehicles;

badge

issuance

and retrieval; escorting of visitors;

patrols;

and compensatory

posts.

In addition, the inspector

observed

the operational

status of closed circuit television

monitors, the intrusion detection

system in the central

and

secondary

alarm stations,

protected

area lighting, protected

and vital area barrier integrity,

and the security

organization interface with operations

and maintenance.

The inspectors

found plant housekeeping

and material condition of

components

to be satisfactory.

The licensee's

adherence

to

radiological controls, security controls, fire protection

requirements,

and

TS requirements

in these

areas

was satisfactory.

Review of Nonconforman'ce

Reports

Adverse 'Condition Reports

were reviewed to verify the following:

TS were complied with, corrective actions

and generic

items were

identified and items were reported

as required

by 10 CFR 50.73.

(1)

ACR 93-126 reported that the "A" spent fuel pool cooling

pump (FPC-lA) entered

the high alert range for differential

pressure

during

a quarterly surveillance test

on June

23,

1992,

but the

pump

had not been placed

on

an increased

testing frequency

(ITF) or analyzed

as required

by Inservice

Inspection

Program

Procedure

ISI-203,

ASME Section

XI Pump

and Valve Program Plan.

The licensee

discovered this error

while reviewing the data for a March 12,

1993 quarterly

test.

Following the licensee's

discovery,

the

pump was

immediately placed

on an ITF and the licensee

reviewed other

pump data to determine if any more

pumps

had

been missed.

During discussions

with the

NRC inspector,

the licensee

indicated that this review yielded

no additional

examples of

oversight

and that the above instance

appeared

to be

an

isolated

case.

When the inspector reviewed historical data

for all of the

pumps in the

IST program,

12 instances

of

missed

ITFs or the failure to perform an analysis for pumps

that had gone into either the high or low alert ranges for

flow, differential pressure,

or vibration over the last four

years

were found.

Examples

included high alert differential

presure

data for the "A" containment

spray

pump in February

1990

and again

on FPC-lA in December

1991.

The "B" service

water booster

pump went into low flow alert

on three

separate

occasions

(August 1991,

March 1992,

and September

1992) prior to being placed

on ITF in September

1992.

The

TDAFW pump went into high alert for vibration on six

occasions

between

1989

and

1992 without any required

corrective actions.

When the inspector reviewed the files

for these

pumps with the licensee, it was found that no

records of corrective actions existed for the unacceptable

test data identified by the inspector.

,The inspector

considered that

a lack of a proceduralized

review process

for IST data,

which could potentially fall into the alert

range,

contributed to this problem.

Currently, the

ASME

Section

XI required action range,

which defines

pump

operability, is referenced

as acceptance

criteria in

Operations

Surveillance

Test procedures.

This provides

a

formal means of identifying data which falls in the required

action range.

The inspector verified that none of the

required actions

were missed

and that

pump operability was

not affected

by the missed

ITFs.

The inspector also

verified that the

pumps are currently being tested

on

a

frequency

commensurate

with recent test data.

The test results for the spent fuel pool cooling

pump

identified by the licensee

and the twelve examples

found by

the inspector

were all considered

to be in violation of the

licensee's

inservice testing procedure.

Although the

licensee identified the first example, this violation is

being cited due to the excessive

number of examples later

identified by the

NRC inspector during his followup review.

Violation (400/93-08-01):

Failure to properly implement

inservice testing for components

with data in the alert

range.

In addition to the above issue,

the inspector identified

several

borderline

cases

where surveillance test data fell

right on the margin for the acceptable

and alert ranges.

For pumps,

Section

XI of the

ASHE Code defines the

acceptable

range for flow to be 0.94 to 1.02 of the

established

baseline

flow.

However, Section

XI also defines

the low and high alert ranges

as 0.90 to 0.94

and 1.02 to

1.03 of the baseline

flow respectively.'ence,

the alert

range

boundaries

overlap with the acceptable

ranges

at its

margins

and allows data which falls on the border to be

interpreted either way.

This same ambiguity exists for

vibration (0 to

1 mil acceptable

and

1 to 1.5 mil high

alert)

and the other monitored parameters.

The inspector

found flow data for three successive

tests

(September

1992,

December

1992,

and February

1993) performed

on the "A"

service water booster

pump

and

one

(Harch

1992) for the "A"

RHR pump that were

on the acceptable

and alert range

margins.

Several

instances

were found for the

TDAFW pump

and others

where vibration data

was exactly

1 mil.

Since

Section

XI was

ambiguous

in this regard,

the licensee

had

interpreted this borderline data to be acceptable

and

consequently

did not place the

pumps

on ITF or perform any

analysis

on the data.

Although

a number of items in

subsection

IWP are subject to interpretation

and have

documented

interpretations

in the licensee's

implementation

procedure

ISI-203,

no such formal interpretation existed for

the analysis of data which falls on the margins of the alert

ranges.

The inspector discussed this matter with the

licensee

who agreed that there should

be

a procedural

interpretation for qualifying borderline test data.

ACR 93-142 reported that the containment

vacuum relief

system actuation setpoint

was not within the limits

established

by the TS.

Technical Specification 3.6.5

requires

the containment

vacuum relief system

be operable

with an actuation setpoint of equal to or less negative

than

-2.5

INWG differential,pressure

(containment

pressure

less

atmospheric

pressure).

During a review of maintenance

procedures

for a plant modification, licensee

personnel

discovered that the differential pressure

transmitters,

'used

to actuate

the system,

sense

a differential pressure

between

the containment building and the Reactor Auxiliary Building

(RAB).

This instrumentation

has

been maintained

by the

licensee

by the performance. of loop calibration procedures

for the transmitters with a setpoint of -2.5

INWG with a

tolerance of 0.25

INWG.

Since the

RAB pressure

is

maintained

at

a negative pressure relative to outside

atmosphere

so

as to monitor and filter potential

airborne

radioactive release

pathways,

the effective actuation

setpoint for the vacuum relief system includes the actuation

setpoint plus the negative pressure

at which the

RAB is

maintained

(-0.2 - -0.4

INWG).

This condition exceeded

the

TS required actuation setpoint.

When informed of this situation

on Parch

31,

1993,

operations

personnel

secured

the

RAB normal ventilation to

equalize the

RAB pressure

with atmospheric

pressure.

This

was

a conservative

action until plant engineering

could make

a determination of system operability.

On April 1,

1993,

an

engineering

evaluation

concluded that system operability was

not affected

and that the current configuration was in

accordance

with plant design.

The

RAB normal ventilation

was subsequently

returned to service.

On April 2,

1993, the

RAB normal ventilation was again

secured

due to concerns

regarding'compliance

with the exact wording of the TS.

The

containment

vacuum relief valve actuation setpoint

was

subsequently

revised via a temporary modification (PCR-6852)

to establish

a value of -1.0

INWG which allowed

a margin for

RAB pressure- control.

The inspectors

researched

the

FSAR and licensee calculations

which supported

operation of the system.

Section 6.2. 1

.1.3.4 of the

FSAR supported

the present

design of the

containment

vacuum relief system.

Calculation 012, dated

May 2,

1986,

assumed

an initial containment

vacuum of -4.0

INWG before actuation of the vacuum relief system.

The

results of this calculation concluded that the maximum

differential pressure

between

containment

and the

RAB

atmosphere

would be less

than the design value of 2.0 psi

as

specified in the

FSAR.

Since the negative

pressure

maintained

in the

RAB in conjunction with the actuation

setpoint of -2.5

INWG would not have exceeded

the maximum of

-4.0

INWG assumed

in the calculation,

the inspector

concluded that no safety concern existed

and that the

current plant design

was in accordance

with the

FSAR.

However, the licensee

was encouraged

to correct the wording

of the

TS to reflect the actual plant design configuration

which 'measures differential pressure

between

the containment

building and the

RAB.

This violation will not be subject to

enforcement

action because

the licensee's

efforts in

identifying and correcting the violation meet the criteria

specified in Section VII.B of the Enforcement Policy.

NCV (400/93-08-02):

Failure to maintain appropriate

actuation setpoints for the containment

vacuum relief

system.

Surveillance Observation

(61726)

Surveillance tests

were observed to verify that approved

procedures

were

being used; qualified personnel

were conducting the tests;

tests

were

adequate

to verify equipment operability; calibrated

equipment

was

utilized;

and

TS requirements

were followed.

The following tests

were

observed

and/or data reviewed:

~ OST-1013

1A-SA Emergency Diesel Generator Operability Test Monthly

Interval

~ OST-1023

Offsite Power Availability Verification Weekly Interval

~ OST-1026

Reactor Coolant System

Leakage

Evaluation Daily Interval

~ OST-1085

1A-SA Diesel

Generator Operability Test Semi-annually

~ EPT-033

Emergency

Safeguards

Sequencer

System Test

~ EPT-194T

Emergency Diesel

Generator

lA-SA Governor Adjustment

and

Response

Testing

The performance of these

procedures

was found to be satisfactory with

proper use of calibrated test equipment,

necessary

communications

established,

notification/authorization of control

room personnel,

and

knowledgeable

personnel

having performed the tasks.

No violations or

deviations

were observed.

a ~,

During the initial performance of procedure

OST-1085 at 9:07 p.m.

on March 20, the "A" emergency diesel

generator failed to

establish

a stable output frequency within the time limit of 10

seconds.

Plant operators

using

a hand held stop watch measured

a

time of 10.03 seconds for this parameter to stabilize.

The diesel

was subsequently

declared

inoperable.

A recorder device

was

installed to measure

the time for the diesel

generator to achieve

rated voltage

and frequency.

The diesel

was started

per

an

operating

procedure for a second

time at approximately 4:30 a.m.

on March 21 with satisfactory

frequency stabilization time.

At

b.

5:08 a.m.

on Harch 21, the diesel

was started

a third time in

accordance

with procedure

OST-1085 during which an acceptable

frequency stabilization time of 9.36 seconds

was obtained.

During

the two later starts,

the time was measured

with hand held stop

watches

and the recorder device.

These starts

showed that, in

some cases,

the times measured

by stop watch were longer than

those

measured

by the recorder

devices

by as

much

as

one second.

The licensee

concluded that

a time measuring

mistake

had

been

made

on the first start attempt

and declared

the diesel

operable.

As mentioned in NRC Inspection

Report 50-400/93-07,

several

previous diesel start times have

exceeded

the

10 second limit.

Licensee

personnel

discovered that most of the slow starts

occurred during the performance of surveillance tests

where safety

injection slave relays

were actuated

to produce the diesel start

signal

as

was the case with procedure

OST-1085.

The licensee

believes

the diesel starting time is being measured

inconsistently

during these tests

when the slave relays

are actuated.

Further investigation for the slow diesel

generator start time was

performed

by the licensee

between

Harch

24 and Harch 26.

The fuel

control shafts

and

pump racks were inspected

by the equipment

vendor representative..

No problems

were identified.

Procedure

EPT-194T was then performed

on Harch

26 to adjust the diesel

governor response.

After adjustments

were

made to the governor,

procedure

OST-1013

was performed during which

a substantially

improved frequency stabilization time of 8.6 seconds

was achieved.

During a review of the

TS associated

with surveillance

procedure

OST-1023,

the inspector noticed that

TS 4.8. 1. l.l.a required that

the connecting circuit for the offsite transmission

network and

the onsite safety-related distribution system

be verified operable

by checking correct breaker

alignment

and power availability.

Although the procedure

adequately

checked circuit breaker

positions, it did not contain

a requirement to verify that

switchyard voltage

was present.

Although power availability is

usually obvious, certain outage conditions could make the power

availability check important.

The inspector

recommended

that the

surveillance

procedure

be enhanced

to include this check.

Haintenance

Observation

(62703)

The inspector observed/reviewed

maintenance activities to verify that

correct equipment clearances

were 'in effect; work requests

and fire

prevention work permits were issued

and

TS requirements

were being

followed.

Haintenance

was observed

and work packages

were reviewed for

the following maintenance activities:

~ Troubleshooting/replacement

of fan bearings for air handler AH-92A.

~ Replacement of AH-92A supply breaker in accordance

with procedure

CH-

E0010,

480 Vac Holded Case Circuit Breaker Test.

~ Troubleshoot

cause for axial flux difference channel drifting in

accordance

with procedure

HST-I0045, Calibration of Nuclear

Instrumentation

System

Power

Range

N42.

~ Inspection of "A" emergency diesel

generator fuel control shafts

and

pump racks.

~ Troubleshoot/repair

the

TDAFW pump which tripped on mechanical

overspeed

during surveillance testing.

~ Rebuild "B" CSIP using

new rotating assembly

and mechanical

seals

in

accordance

with procedures

CH-H0019, Pacific Charging/Safety

Injection

Pump Size

2 1/2"

RL Type IJ Disassembly

and Maintenance,

CH-H0021,

Westinghouse

High-Speed

Gear Drives Type SU-19 for Charging/Safety

Injection

Pump,

Disassembly

and Maintenance,

and HPT-H0059,

Charging/Safety

Injection

Pump Nonmetallic Component

Replacement

-and

Lubrication (Mechanical

Environment gualification).

~ Calibrate pressure differential switch for containment

vacuum relief

system in accordance

with temporary modification PCR-6852.

~ Charge Cell 828 on

1B-SB emergency battery per procedure

CH-E0003,

Station Battery Single Cell Charging,

and retest in accordance

with

procedure

HST-E0011,

lE Battery quarterly Test.

The performance of work was satisfactory with proper documentation of

removed

components

and independent verification of the reinstallation.

'a ~

The inspector requested

a listing of all priority work performed

in the previous thirty days.

This printout contained

19 work

tickets.

A review of work ticket approval

times

compared to

timekeeping data revealed that one priority 3 job which regarded

the repair of the "A" emergency diesel

generator

control panel

was

started

before preplanning

was performed.

The licensee's

procedure for controlling maintenance,

HHH-012,

Maintenance

Work Control Procedure,

contains provisions for the

conduct of priority/emergency maintenance

and allows the shift

foreman to authorize the performance of maintenance activities

without prior preplanning,

reviews,

and without a planned work

ticket in emergency situations

where immediate actions

are

required to protect the health

and safety of the public, protect

equipment

or personnel,

and prevent the deterioration of plant

conditions to potential

unsafe levels.

This procedure listed

priority level

1,

2 and

3 as potential activities which allow

maintenance initiation without the prior preplanning.

The

licensee

defines priority 2 and

3 maintenance

as that required to

correct

a condition which is in violation of regulatory require-

ments

and to correct

a condition which requires

an imminent plant

shutdown.

The inspector

reviewed Regulatory

Guide 1.33, guality Assurance

Program Requirements

(Operation),

section

1.8 of the

FSAR,

and

discussed

the intent of the work control procedure with licensee

management.

Section

9 of Regulatory

Guide 1.33,

Procedures

for

Performing Haintenance,

states that maintenance

that can affect

the performance of safety-related

equipment

should

be properly

preplanned

and performed in accordance

with written procedures.

Section

1.8 of the

FSAR describes

the extent to which the licensee

complies with Regulatory

Guide 1.33

and states that maintenance

shall

be preplanned

and performed in accordance

with written

procedures

except in emergency or abnormal

operating conditions

where

immediate actions

are required to protect the health

and

safety of the public, to protect equipment or personnel,

or to

prevent the deterioration of plant conditions to unsafe levels.

Although the inspector

agreed that certain situations

which

involve a danger to the health

and safety of the public, or to

protect plant personnel

and equipment,

must

be expeditiously

corrected,

the inspector considered

the omission of preplanning to

avoid imminent plant shutdowns to be

a deviation of the written

commitment in the

FSAR.

Deviation (400/93-08-03):

Performance of non-emergency

safety-

related

maintenance

without preplanning.

b.

Several

problems were experienced

with air handler AH-92A.

This

fan supplies cooling air to

a safety-related

motor control center.

On Harch

20 licensee

personnel

noticed that the fan was making

an

unusual

noise

and that the shaft

was moving excessively.

Haintenance

was performed which replaced

the outboard

fan bearing.

The cause for the

bad bearing

was determined to be

a loose nut on

the bearing locking collar.

On Harch 30 the fan again

had to be

worked because

the outboard fan bearing

had seized.

The fan shaft

was repaired

and both fan bearings

were replaced to corr'ect the

damage.

The cause for this condition was determined to be

overtight drive belts.

On April

1 excessive

vibration was noticed

on the fan motor.

Troubleshooting

uncovered that the motor sheave

was loose

and

a key which was supposed

to secure this component

in

place

was found on the bottom of the air handler unit.

The

licensee

determined that the key had

been

absent for some time and

. .this contributed to the motor vibration.

The key and

a new sheave

was installed.

The licensee is presently performing

an

investigation into the root cause for the problems

associated

with

this fan.

The inspector considered

the maintenance activities to

identify and correct the problems with AH-92A to be poor

as they

resulted

in excessive

equipment out of service times to repair.

.f

10

On March

18 licensee

personnel

discovered

an outboard

seal

leak of

approximately

one

gpm on the "B" CSIP.

Minutes earlier, control

room personnel

had received

low seal injection flow alarms to the

"A" and

"B" reactor coolant

pumps

as well as indications that the

charging

pump motor was running

on higher than normal current,

and

that

pump discharge

pressure

had decreased

to approximately

2500

psig from 2700 psig.

Control

room personnel

immediately secured

the

pump

and declared it inoperable.

During the

pump disassembly

and maintenance activities, licensee

personnel

unsuccessfully

attempted to remove the balancing

drum retaining nut which mates

with the

pump shaft

between the discharge

impeller and the

mechanical

seal

package.

The nut was jammed, indicating that the

pump shaft

had broken beneath it.

The balancing

drum, which

prevents

axial

pump thrust

and protects the outboard mechanical

seal

package,

had indications of wear.

The seal faces'ad

a wear

pattern which indicated that they had

seen

excessive

pressures

because

the balancing

drum had failed.

Following unsuccessful

attempts to fully disassemble

the old rotating element,

the

licensee

replaced

the entire element

and mechanical

seal

assembly

with spares.

Following installation of the

new pump

and seals,

the

licensee

broke the drum retaining nut on the old assembly for

further investigation.

It was verified that the shaft had,indeed

been

severed

below the retaining nut and that this initiated the

pump failure.

According to licensee

personnel,

several

shaft

failures

have

been reported

by the industry for this type of

charging/safety

injection pump.

All three of the CSIPs

are

11-

stage centrifugal

pumps that were manufactured

and tested

by

Pacific

Pumps.

The inspector reviewed the

pump vendor's technical

manual

and the

licensee's

work packages

to verify that the

pump rebuild had

been

performed in accordance

with vendor

recommendations.

Although the

vendor manual specifies

performing

a full flow test prior to

returning the

pump to operable

status,

the licensee

has opted to

test the

pump on reduced flow due to current plant operating

conditions.

The licensee will develop

a special

procedure to

accomplish this post-maintenance

testing.

In the meantime,

the

performance of the "A" CSIP, which has

an operating life similar

to the old "B" CSIP,

and

had

a much lower level vibration, will be

monitored closely.

Licensee

management

has decided

not to replace

the rotating element

on the "A" CSIP until signs of impending

failure is seen or occurs.

Inspector

Follow-up Item (400/93-08-04):

Follow the licensee's

activities to retest

the "B" CSIP, determine

the root cause of its

failure,

and assess

any generic implications.

On March 16, during performance of procedure

MST-EOOll,

1E Battery

quarterly Test,

the individual cell voltage reading

on

1B-SB

battery cell

828 fell below the 2. 13 Vdc limit. The licensee

began

a 24-hour continuous individual cell charge

on March

18 to bring

the cell voltage

back above the Category

B requ'irement.

Technical

11

Specification 4.8.2. 1 states

that the

1E emergency batteries

may

be considered

operable for any Category

B parameter

outside the

"limits" shown

on Table 4.8-2

as long as the parameters

are within

their "allowable values"

and restored to within limits within 7

days.

On Friday, Harch 19, three

days after the adverse

condition

was identified, licensee

personnel

began

addressing

the

possibility that, following the continuous

recharge

which was

still ongoing at the time, the

k'28 cell voltage could dip even

further below the "allowable value" of 2.07 Vdc and render the

battery immediately inoperable.

This led the licensee to develop

contingencies

to help avoid

a TS required

shutdown.

Contingency

plans included the potential

replacement

of the affected cell with

another

.from one of the non-safety station batteries.

This option

would involve a dedication

process for the non-Class

1E cell

and

would require the erecting of heavy steel

equipment

over the

safety-related

battery for cell removal

and installation purposes.

Another option included jumpering out the affected cell

and

performing

an engineering

evaluation to show the battery remained

operable.

The later option was discarded

when the supporting

evaluation

would not be ready before the 6-hour

TS shutdown action

statement

expired.

Although the situation corrected itself when the cell voltage

stabilized at 2.25 Vdc following the

24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> recharge,

the

inspector

concluded that the licensee's

overall coordination of

contingency efforts was weak in two areas.

Engineering

personnel

were reluctant to explore more fully the safer option of jumpering

out the battery cell because

of a time constraint.

The other

weakness

was the fact that contingencies

were not even

addressed

until the cell recharge

was half completed,

three days after the

initial surveillance test.

The inspector

concluded that better

coordination of contingency planning

and engineering

resources

would have

been beneficial.

The licensee

has subsequently

developed

an engineering

evaluation

which will allow jumpering out

one

bad cell in the "A" and

"B" emergency batteries.

In addition,

modifications are being developed

which will install spare cells

in the "A" and "B" lE battery

rooms

and have them ready for

immediate installation.

Design

Changes

and Nodifications (37828)

Installation of new or modified systems

were reviewed to verify that the

changes

were reviewed

and approved in accordance

with 10 CFR 50.59, that

the changes

were performed in accordance

with technically adequate

and

approved

procedures,

that subsequent

testing

and test results

met

acceptance

criteria or deviations

were resolved in an acceptable

manner,

and that appropriate

drawings

and facility procedures

were revised

as

necessary.

This review included selected

observations

of modifications

and/or testing in progress.

The following modifications/design

changes

were reviewed:

~ PCR-3995

Emergency Diesel Starting Air Hodifications

12

~ PCR-6841

PCV-8400A Modification

~ PCR-6847

AH-92-1A Bearing Surface

Repair

~ PCR-6852

Containment

Vacuum Relief Actuation Setpoint

Temporary modification PCR-6841

was installed to reduce

containment

sump

inleakage.

As mentioned in

NRC Inspection

Report 50-400/93-07,

.containment

sump inleakage

had increased

to two gpm.

During this

inspection period,

sump inleakage

increased

to approximately four gpm.

On March 22 licensee

personnel

observed

a reduction in the leakage to

approximately 0.2 gpm.

The licensee

also observed that

a back pressure

. control valve,

lBD-8, in the blowdown line for the "A" steam generator

had repositioned to the full'pen position.

The licensee

believes that

this valve backseated

and reduced

any secondary

valve packing leakage

which was present.

The temporary modification was installed to apply

a

false

open signal to the valve's differential pressure

transmitter

controller.

This action did not affect containment integrity since this

valve does not receive

any isolation signals.

No violations or

deviations

were identified.

Fire Protection/Prevention

Program

(64704)

Fire protection activities, staffing and equipment

were observed to

verify that fire brigade staffing was appropriate

and that fire alarms,

extinguishing equipment,

actuating controls, fire fighting equipment,

emergency

equipment,

and fire barriers

were operable.

The inspectors

observed

two fire fighting practice

sessions

which

involved most of the fire brigades.

During the practice

sessions

a fire

brigade

combats

an actual building fire which was fueled

by natural

gas.

These activities occurred at the

Wake County Fire Training Center which

is located adjacent to the plant.

Search

and rescue

techniques

were

also practiced.

The inspector considered

the response

of the fire

brigades to be acceptable

and that the use of appropriate fire fighting

equipment

and fire fighting techniques

were satisfactorily demonstrated.

The licensee

has relocated

the fire brigade turnout/dressout

area

from

the turbine building to the waste processing

building.

The inspector

toured the

new turnout area

and found the conditions to be satisfactory

with adequate

room for the manual firefighting equipment

and turnout

,

clothing.

As discussed

in NRC Inspection

Reports

50-400/91-23

and 50-'400/93-07,

fire brigade staffing duties were assigned

to radwaste

operations

personnel

and roving fire patrol/tours

assigned

to security personnel.

Therefore staffing was not checked during this inspection.

An inventory of control

room Self Contained

Breathing Apparatus

(SCBA)

was performed.

The licensee

maintains

10 SCBA's available with 10 spare

air bottles in the control room.

This equipment

was controlled in

accordance

with procedure

AP-200,

Emergency

Equipment Inventory.

The

13

inspector also checked

the

SCBA inventory in the fire brigade turnout

area.

The licensee

maintains eight SCBA's in the turnout area.

This

equipment

was controlled in accordance

with procedure

ORT-3001, Fire

Equipment Inspection Monthly Interval.

The inspector

found that all of

the observed

SCBA's had recently

been inspected to ensure it was ready

for emergency

use.

The inspector considered

the administrative controls

provided for SCBA'nventory

and inspection to be good.

Essential

Services Chilled Water System Reliability (71707)

During this inspection period, the operability and reliability of the

Essential

Services Chilled Water System

(ESCWS)

was reviewed.

Since

1987, four LERs have

been written on chiller inoperability,

LERs 87-07,

90-03,

90-17,

and 91-04.

These

problems

were reported

because

both

'rains

of ESCWS were inoperable

(one train down for pre-planned

maintenance

and the other train tripped for some reason).

Also, plant

adverse

condition reports

were reviewed

by the inspector

and

an

interview with the system engineer

was held to determine recurrent

chiller problems.

The two

ESCWS units utilize refrigerant to produce

cool chilled water

which is supplied to the cooling coils of the various safety-related

air

handling unit room coolers.

The 752 ton

ESCWS units are oversized for

the low heat loads generated

during normal'lant

oper ation.

Since these

units are also

used during normal plant operation,

the low load has

resulted in some operating

problems in the past.

The two

ESCWS trains

are located within the

same

room and in the

same fire area.

Each train,

however, is spacially separated

as per the fire protection hazards

analysis.

The chiller design incorporates

a 30 minute anti-recycle device to limit

the number of automatic starts, this does not pose

a safety concern

since this, feature is bypassed

on

a safety injection signal.

Various

trips have occurred

on the

ESCWS units since

1987.

In addition,

corrective actions

have

been taken to address

the identified problems

including; operating/maintenance

procedure

enhancements,

training,

and

plant modifications.

Corrective Action

1 Overcurrent Trip

2 Very Low Load

1 High Lube Oil Temperature

1 High Refrigerant

Pressure

No change.

Trip due to bad

overcurrent relay.

Relocated

service water modulating

valves.

Deleted condenser

water low flow

trip.

Added controls for ESW recirculation

pump (P-7).

Calibrated thermocouples.

Added

new filters/regulators for air

supply to expansion

tank.

1

Low Chilled Water Flow

4 Low Oil Pressure

14

Changed

expansion

tank makeup water

source

from fire service to

demineralized

water.

Valves upgraded to stainless

steel

disks

and bodies.

Same

as high refrigerant pressure.

Oil type changed

from C to B.

One hour minimum run time to

determine

proper oil level.

Setpoint

reduced

from 25 psig - 20

pslg.

Since the latest plant modifications during the last refueling outage in

November

1992, the

ESCWS chiller units have operated without additional

problems.

Although the low oil pressure trip setpoint

was reduced in

September

1991,

two trips of this type reoccurred

in July 1992.

In one

of these

cases,

loose relay electrical

connections

were found to have

attributed to the trip signal.

In order to further increase chiller

'eliability,

the licensee

is developing

a plant modification (PCR-6493,

ESCWS Chiller Low Flow/Temperature Trip Alarm) to bypass

most of the

chiller trip signals during

an engineered

safeguards

actuation.'nspector

Followup Item (400/93-08-05):

Follow the licensee's

~

~

~

~

activities to increase

ESCWS reliability.

8.

Review of Licensee

Event Reports

(92700)

The following LER was reviewed for potential generic

impact, to detect

trends,

and to determine'whether

corrective actions

appeared

appropriate.

Events that were reported

immediately were reviewed

as

they occurred to determine if the

TS were satisfied.

LERs were reviewed

in accordance

with the current

NRC- Enforcement Policy.

(Closed)

LER 93-01:

This

LER reported that Operations

Surveillance Test

Procedure

OST-1024,

On-site

Power Distribution Verification, did not

'require operators

to check the position of the

2CB battery input

breakers

to the 7.5

KVa instrument inverters.

The breakers

must

be

closed for the inverters to receive

a backup

DC power supply from their

associated

125-volt

DC busses.

Because of the procedural

omission,

the

breaker positions

had not been verified during the weekly surveillance

test since plant startup,

which constituted

a TS violation.

The

licensee

has revised the procedure to include position verification for

the

2CB and

3CB backup

DC supply breakers.

A copy of the revised

procedures

has

been placed in the required reading for operator training

purposes.

S

15

Licensee Action on Previously Identified Inspection

Findings

(92702

&

92701)

(Open) Violation 400/92-17-02:

Failure to correct

a deficiency with the

emergency diesel

generator starting air system.

The inspector

reviewed

and verified completion of the corrective actions

listed in the licensee's

response letter dated

November 2,

1992.

The

licensee

completed modifications to the starting air systems

which

installed additional filtration and dryer units.

Also, the air system

was blown down with clean dry air and the

PCR process

has

been

removed

from the corrective action program subprogram classification.

Remaining

action to be accomplished

includes

a review of existing

PCRs to ensure

that

an

ACR exists for any adverse conditions.

Exit Interview (30703)

The inspectors

met with licensee

representatives

(denoted

in paragraph

1) at the conclusion of the inspection

on April 19,

1993.

During this

meeting,

the in'spectors

summarized

the scope

and findings of the

inspection

as they are detailed in this report, with particular emphasis

on the Violations, Deviation,

and Inspector

Follow-up Items addressed

below.

The licensee

representatives

acknowledged

the inspector's

comments

and did not identify as proprietary

any of the materials

provided to or reviewed

by the inspectors

during this inspection.

No

dissenting

comments

from the licensee

were received.

Item Number

Descri tion and Reference

400/93-08-01

400/93-08-02

400/93-08-03

400/93-08-04

400/93-08-05

Acronyms

and Initialisms

VIO:

Failure to properly implement plant

procedures,

paragraph 2.c.(1).

NCV:

Failure to maintain appropriate

actuation

setpoints

for the containment

vacuum relief

system,

paragraph 2.c.(2).

DEV:

Performance of non-emergency

safety-

related maintenance

without preplanning,

paragraph'4.a.

IFI:

Follow the licensee's

activities to

restore

the "8" CSIP to operable status

and

review the generic implications of the

pump

shaft failure, paragraph

4.c.

IFI:

Follow the licensee's

activities to

increase

ESCMS rel iabil ity, paragraph

7.

ACR

ASHE

Adverse Condition Report

American Society of Mechanical

Engineers

16

CFR

CSIP

EPT

ESCWS-

ESW

FSAR

gpm

IFI

INWG

ISI

IST

ITF

LER

HPT

HST

NCV

NRC

OST

PCR

pslg

RAB

RCS/RC-

RHR

SCBA

TDAFW-

TS

Vac

Vdc

VIO

Code of Federal

Regulations

Charging Safety Injection

Pump

Engineering

Performance

Test

Essential

Services Chilled Water System

Emergency Service Water

Final Safety Analysis Report

gallon per minute

Inspector

Follow-up Item

Inches Water Gauge

Inservice Inspection

Inservice Testing

Increased

Testing

Frequency

Licensee

Event Report

Haintenance

Performance

Test

Haintenance

Surveillance Test

Non-Cited Violation

Nuclear Regulatory

Commission

Operations Surveillance Test

Plant

Change

Request

pounds

per square

inch gage

Reactor Auxiliary Building

Reactor Coolant System

Residual

Heat

Removal

Self Contained

Breathing Apparatus

'Turbine Driven Auxiliary Feedwater

Technical Specification

Volt alternating current

Volt direct current

Violation