ML18005A823

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Insp Rept 50-400/88-40 on 881121-890120.Violations Noted. Major Areas Inspected:Operational Safety Verification, Surveillance Observations,Maint Observations,Lers & Followup of Events at Operating Power Reactors
ML18005A823
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 02/16/1989
From: Bradford W, Dance H, Shannon M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18005A821 List:
References
50-400-88-40, NUDOCS 8903270396
Download: ML18005A823 (13)


See also: IR 05000400/1988040

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

'l01 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report No.:

50-400/88-40

Licensee:

Carolina

Power

and Light Company

P. 0.

Box 1551

Raleigh,

NC

27602

Docket No.:

50-400

Licensee

No:

NPF-63

Facility Name:

Harris

1

Inspection 'Conducted:

November

21,

1988 - January

20,

1989

Inspectors:

2//6 $ $

Approved by

W.

H. Bradford

M.

C.

Shannon

H. Dance,

Section Chief

Reactor Projects

Section

1A

Division of Reactor Projects

Date Signed

Z 4a

Da

Si

ed

>

h-;

K'a

e Signe

SUMMARY

Scope:

This

routine

sa,ety

inspection

was

conducted

in

the

areas

of

operational

safety

verification,

surveillance

observations,

maintenance

observations,

licensee

event 'reports,

followup of events

at

operating

power

reactors,

and

plant

nuclear

safety

committee

meeting.

Results:

Within the area~

inspected

two violations were identified.

The first

violation involved

a failure to adequately

pe~form post maintenance

testing

which resulted

in

a safety related

room cooling unit being

inoperable

for approximately

61

days,

paragraph

2.b.

The

second

violation involved

a failure to follow a clearance

procedure

which

resulted

in

a loss of approximately

55,000 gallons of water from the

spent fuel pool to the

new fuel storage

pool, paragraph 2.c.,

Additionally, the licensee

has established

a task force .to determine

the

root

cause

for the

turbine

driven auxiliary

feedwater

pump

overspeed

trip which occurred

on January

16,

1989.

Resolution

of

this matter is under inspector follow-up.

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8

REPORT

DETAILS

Persons

Contacted

A

'R.

A. Watson,

Vice President,

Harris Nuclear Project

  • C. G. Hinnant, Plant General

Manager

C.

R. Gibson, Director,

Progra'ms

and Procedures

"D. L. Tibbits, Director, Regulatory

Compliance

C.

S.

Bohanan,

Director, Special

Programs

"R.

B.

Van Metre,

Manager,

Technical

Support

  • T. C. Morton, Manager,

Maintenance

J.

M. Collins, Manager,

Operations

"J.

R.

Sip'p,

Manager,

Environmental

and Radiation Monitoring

D. A. Braund, Supervisor,

Security

T.

F. Lent,

Systems

Engineering

W.

R. Wilson, Reactor/Performance

Engineering

L. J.

Woods, Testing

and Maintenance

Support

W.

H. Batts,

Supervisor,

Mechanical

Maintenance

"J.

H. Smith, Supervisor,

Operations

Support

C.

S. Oleik, Supervisor,

Shift Operations

"G.

L. Forehand,

Director,

QC/QC

~F.

E. Willet, Manager,

Outages

and Modifications

Other

licensee

employees

contacted

during

this

inspection

included

technicians,

operators,

mechanics,

security

force

members,

engineering

personnel

and office personnel.

~Attended exit interview

Acronyms and initialisms used

throughout this report are listed in

paragraph

9.

2.

Operational

Safety Verification (71707)

Plant Tours

The inspectors

conducted

routine plant tours during this inspection

period to verify that the

licensee's

requirements

and

commitments

were

being

implemented.

These

tours

were

performed

to verify that:

systems,

valves,

and breakers

requi red for safe plant operations

were

in their

correct

position; fire protection

equipment

and

spare

equipment

and materials

were

being maintained

and

stored

properly;

plant

operators

were

aware

of

the

current

plant

status;

plant

operations

personnel

were documenting

the

status

of out-of-service

equipment;

security

and

health

physics

controls

were

being

implemented

as

required

by procedures;

there

were

no

undocumented

cases

of unusual

fluid leaks,

piping vibration,

abnormal

hanger

or

seismic

restraint

movements;

all

reviewed

equipment

requiring

calibration

was current;

and general

housekeeping

and control of fire

hazards

were

satisfactory.

Tours

of the plant included

review of

site

documentation

and

interviews

with plant

personnel.

The

inspectors

reviewed

the control

room operators'ogs,

tagout

logs,

chemistry

and

health

physics

logs,

control

boards,

and

panels.

During these

tours the inspectors

noted that the operators

appeared

to

be alert,

aware

of changing

plant conditions,

and manipulated

plant controls properly.

The inspectors

evaluated

operations

shift

turnovers

and

attended

shift briefings.

They

observed

that

the

briefings and turnovers provided sufficient detail for the next shift

crew and verified that the staffing met the

TS requirements.

Site security

was

evaluated

by observing

personnel

in the protected

and vital

areas

to .ensure

that

these

persons

had

the

proper

authorization

to

be

in the .respective

areas.

The inspectors

also

verified that vital area portals

were

kept

locked

and

alarmed.

The

security personnel

appeared

to be alert and attentive to their duties

and those officers performing

personnel

and vehicular

searches

were

thorough

and

systematic.

Responses

to security

alarm conditions

appeared

to be prompt

and adequate.

Selected activities of the licensee's

Radiological Protection

Program

were

reviewed

by the

inspectors

to verify conformance

with plant

procedures

and

NRC

regulatory

requirements.

The

areas

reviewed

included:

operation

and

management

of the plant's

health

physics

staff,

ALARA implementation,

Radiation

Work Permits for compliance to

plant procedures,

personnel

exposure

records,

observation

of work and

personnel

in radiation

areas

to verify compliance

to

radiation

protection

procedures,

and

control

of radioactive

materials.

No

discrepancies

were noted.

Several

inspector

hours

were

spent

on

back shift inspections

and

observations.

This included observing

the unit coming off line and

cooling down for

a maintenance

outage

and

the

subsequent

restart

of

the, unit.

Various other aspects

of plant operation

were observed

and

evaluated.

The operators

appeared

to be awake, alert,

knowledgeable,

and

compentent

in their duties.

The licensee

has

developed

a high

degree

of professionalism

in the control

room staff.

'I

Inoperable

RAB Emergency

Exhaust

System

During the last refueling

outage

the licensee

replaced

the bearings

on

26 air handling

motors.

This work was

performed

under

two Work

Request

(WR/JO)

No.

88-AQPN2

and

88-AQPM2.

A master

clearance

was

prepared

and

Equipment

Inoperable

Records

(EIRs)

were initiated to

track the status

of the equipment.

On

September

16,

1988,

heating

and

ventilating

equipment

room

number

2 cooling unit,

AH-26 ( 1A-SA),

was tagged

out of service

and

on

September

23,

1988,

the

fan motor leads

were disconnected.

The

motor bearings

were

replaced

on

September

24,

1988,

and

the safety

clearance

was

canceled

on

September

28,

1988'ost

maintenance

testing

requirements

(PMTR) were prescribed

which required

a check

for proper rotation

and

a check for unusual

noise or vibration after

the

fan

was started.

This testing

was not adequately.

performed,

in

that only the supply breaker indicating light was

checked

to verify

fan operation.

On

December

5,

1988, during preventative

maintenance activities,

the

licensee

discovered

the motor leads

had not been terminated

on AH-26.

AH-26 functions

as

a room cooler to support

RAB Emergency

Exhaust

Fan

E6-1A-SA (Train A) by maintaining

room air temperature

less

than

104

degrees

fahrenheit.

E6-1A-SA is required to operate

during

a design

basis

loss of coolant accident to minimize the off-site dose

from

a

postulated

leak of

RCS water into the

RAB.

The licensee

immediately declared

RAB Emergency

Fan

E6-lA-SA to

be

inoperable.

AH-26 motor leads

were terminated,

properly tested,

and

AH-26 and

E6-1A-SA was declared

operable.

The licensee

inspected

the

other

25 fan units to verify that

maintenance

and post

maintenance

testing

had

been

properly

completed.

This

event

appears

to

be

isolated in that it was

1 of 26 fan units which received the bearing

modification and did not receive

proper post maintenance

testing.

The

FSAR states

that

each train of the

RAB Emergency

Exhaust

System

consi sts of 100:o'apacity

fan and filter subsystems.

Upon receipt of

an

SIS,

the

normal

ventilation

penetrations

close

and

both

RAB

Emergency

Exhaust

Systems

are automatically

energized.

Either unit

may

then

be

manually

stopped

from the control

room

and placed

in

standby.

A single

active failure

in

any

component

of

the

RAB

Emergency

Exhaust

System will not

impair the

system's

ability to

fulfill the objectives

given in the design

basis'he

licensee

identified this

event

and

reported it to NRC'n

LER-88-34.

The licensee

performed

an analysis

on the post accident

affects

on

E6-1A-SA caused

by loss

of its

associated

AH-26

room

cooler.

From this analysis,

the licensee

determined that:

(1)

The E6-1A-SA fan motor qualified life would not be

a factor.

(2)

The vortex damper actuator qualified life would be reduced

from

1.85 years to 62.5 days.

(3)

Failure of the vortex damper would result in the damper failing

open.

(4)

With the vortex

damper failed open,

negative

pressure

would be

maintained greater

than the

TS requirement of negative

1/8-inch

water wi.h no detrimental effect to the motor or ductwork.

(5)

The dose rates at E6-1A-SA would be

.25 to 2.5 mrem/hour,

which

would permit operators

to manually control the vortex damper.

(6)

The radiation monitors

on the

E6-1A-SA discharge

duct and

on the

vent stack would give warnings of any releases

past the system's

filter unit if possible

damage

were to occur.

Based

on the

above,

the licensee

concluded that the consequences

of

the loss of AH-26 during

a post accident condition is minimal

and

can

be safely compensated

for by operator action.

TS 3.7.7 requires

that

two independent

RAB Emergency

Exaust

Systems

be operable

in Modes

1-4.

Although the operability of AH-26 is not

directly addressed

in

TS 3.7.7, it is required to support

the

long

term operation of the

E6-1A-SA fan,

and is therefore

considered

to be

a support

system for the

A train of the

RAB Emergency

Exhaust

System.

Accordingly,

when

the

plant

entered

Mode

4

on

October

5,

1988,

EG-1A-SA

was

technically

inoperable.

This

is

a

violation

of

Technical Specification 3.7.7

and 3.0.4.

which require both trains to

be operable

before changing

Modes

from

5 to 4.

Additionally, since

AH-26 was

inoperable

from October 5,

1988, until

December

5,

1988,

approximately

61

days,

the

limiting condition

for operation

of

TS 3.0.3

was exceeded.

The

licensee's

post

maintenance

testing

program

for

fan

motors

requires that the rotation is verified and that the unit is monitored

for

unusual

vibration or noise.

The

operations

staff failed to

perform the required

PMTR which resulted

in the unit being inoperable

for approximately

61

days.

Additionally,

the

maintenance

staff

failed

to

properly

reconnect

the

fan

motor

leads

during

the

maintenance

process.

The

maintenance

procedure

for ventilation

motors did not

have

an

adequate

signoff step

to

ensure

the

motor

leads

would

be

reconnected

following maintenance.

The

licensee's

failure to perform adequate

post maintenance

testing is considered

to

be

a violation of

NRC requirements

and is identified

as violation

400/88-40-01:

Failure

to

Adequately

Perform

Post

Maintenance

Testing.

Loss of Spent

Pool

Level

At 2: 15 a.m.,

on January

17,

1989, approximately five feet of water

from the

spent

fuel

pool

was inadvertently

drained

to the

new fuel

storage

pool.

The event occurred during the improper restoration

of

clearance

OP-89-0071

which

had

been

issued

to support preventative

maintenance.

Maintenance

Work Request

MWR/JO 88-NSI404

had been

issued

in order to

perform preventative

maintenance

on

a

spent

fuel cooling

pump.

The

clearance

authorization

required that valve

1SF-19,

crosstie

to

new

fuel pool,

be verified "closed" before opening valve 1SF-11, crosstie

to spent

fuel pool.

These

valves

are

located

in the

overhead

and

require

a ladder for operation.

The operator

did not

use

a ladder

and

instead

climbed

on equipment in order to reach the valves.

From

his vantage

point he could not see

the valve position indicator for

1SF-19

and mispositioned

the valve to the

open position.

Valve

1SF-11

was

opened

as

required,

which crosstied

the spent fuel

pool to the

new fuel pool.

The control

room received

a

low spent

fuel

pool

level

alarm

and

immediately initiated

a valve

lineup

verification.

Valve

1SF-19

was

found to

be

mi spositioned

and

was

returned to its required position.

The

loss

of five feet

in

spent

fuel

pool

level

calculates

to

approximately

55,000 gallons of water.

The design

of the crosstie

penetrations

into the spent fuel pool is such that

a maximum of five

feet of spent

fuel

pool

level

could

be lost following equipment

failures or personnel

errors.

By design this maintains

18.5 feet of

water above the spent fuel.

Technical Specification 3.9. 11

requires

that

at

least

23 feet of

water shall

be maintained

over the top of spent

fuel seated

in the

storage

racks.

Following the loss of level the action statement

was

followed, in that

no crane operations

or fuel movements

were allowed.

Level was restored within six hours

and was considered

to be timely,

even

though the action

statement

requires

level to be restored within

four hours.

Clearance

OP-89-0071

required valve 1SF-19 to be verified closed.

No

valve manipulation

was required,

in that the valve was danger

tagged

in the closed position.

The operator failed to follow the clearance

instructions,

in that

he did not actually verify the position of

1SF-19

and manipulated

a valve that did not require

manipulation.

The operator's

error in not following the clearance

is considered

to

be

a violation of HRC requirements

and is identified

as

a violation

400/88-40-02:

Failure to Follow Procedures.

Two violations

and

no deviations

were identified.

3.

Monthly Surveillance

Observation

(71709)

The

inspectors

witnessed

the

licensee

conducting

surveillance

test

activities

on safety-related

systems

and

components

to verify that

the

licensee

performed

the activities in accordance

with applicable require-

ments.

These

observations

included witnessing

selected

portions of each

surveillance,

review

of

the

surveillance

procedure

to

ensure

that

administrative

controls

were

in force,

determining

that

approval

was

obtained prior to conducting

the surveillance test,

and verifying that the

individuals conducting

the test

were qualified in accordance

with plant

approved

procedures.

Other

observations

included ascertaining

that test

instrumentation

used

was

calibrated,

data

collected

was

within the

specified

requirements

of

TS,

identified

discrepancies

were

properly

noted,

and

the

systems

were correctly returned

to service.

Portions of

the following test activities were observed

or reviewed

by the inspectors:

OST-1013

OST-1023

OST-1029

OST-1027

OST-1026

OPT-1510

OST-1006

OST-1411

OST-1124

EPT-031T

Emergency

Diesel Generator

( lA-SA) Operability

Offsite Power Availability Verification

Containment

Penetrations

Outside

ECCS Accumulator Valve Breaker Verification

RCS Leakage

Measurement

A and

B Diesel Generator Daily Check

Boron Flowpath Verification

Auxiliary Feedwater

( 1X-SAB) Quarterly

6.,9

kv

Emergency

Bus

Undervoltage

Trip Actuating

Device

Operability

6.9

kv

1A-SA Emergency

Bus Undervoltage

Contact Actuation

Procedure

OST-1124

and

EPT 031T

On

December

20,

1988,

the

licensee

performed

OST-1124,

6.9

kv Emergency

Bus

Undervoltage

Trip Actuating

Device

Operational

Test.

This

is

a

monthly test

and is required

in Modes

1 through 4.

In this test both the

lA-SA and

1B-SB trains

are

tested

to verify that

proper

alarms

are

actuated

when

primary

and

secondary

undervoltage

devices

of the

6 '

kv

.Emergency

Buses

are actuated

from a local test

push

button.'he

test

was

successful

on "B" tr ain,

but

was not sati sfactory

on "A"

train

due to certain

bus relays

not functioning properly and resulted

in

an inadvertant

bus

loss.

A similar event

occurred

on

May 20,

1988,

and

was reported

in

LER 88-013.

Following the initial failure, the licensee

made

several

attempts

to repeat

the failure;

however,

the failure

was

elusive

and

could not

be

repeated.

As the

cause

of the initial failure

could

not

be

determined,

the

equipment

was

returned

to

service

and

satisfactorily

passed

the monthly surveillance

from June

through

November.

Following the failure

on

December

20,

1988,

the

licensee

developed

a

special

test procedure,

EPT-031T, 6.9.kv

1A-SA Emergency

Bus Undervoltage

Contact

Instrumentation

Procedure,

which was

performed

on

December

29,

1988.

The

inspectors

observed

the

performance

of this test

procedure.

The procedure

instrumented

certain contacts for the degraded

grid and loss

of offsite power relays.

The test

found that relays

UVTX (agastat

model

87014)

and

2/SA (General

Electric

Model

012SAMLlB22A) were

not operating

properly.

These

relays

were

replaced

and

OST-1124

was

conducted

on

December

29,

1988.

Proper

operation

of the

bus

undervoltage

device

was

verified.

The licensee

is continuing their investigation

of this matter

to verify that

no further hidden

sporatic

relay operations

occur.

The

licensee

is reporting

the incident in

LER 88-035.

The faulty relays

are

part of the 6.9

kv undervoltage test circuitry and did not appear to have

compromised

equipment operability.

No violations or deviations

were identified.

7

4.

Monthly Maintenance

Observations

(62703)

Station

maintenance

activities of safety-related

systems

and

components

were observed/reviewed

to ascertain

that they were conducted

in accordance

with approved

procedures,

regulatory guides,

industry codes

and standards,

and

were

in

conformance

with TS.

Items

considered

during

the

review

included verification that

LCOs were met while components

or systems

were

removed

from service;

approvals

were

obtained

prior to initiating the

work; approved

procedures

were used;

completed work was performed prior to

returning

components

or systems

to service;

quality control

records

were

maintained; activities were accomplished

by qualified personnel;

parts

and

materials

were properly certified;

and radiological

and fire prevention

controls

were

implemented.

Work requests

were also reviewed to determine

the status

of outstanding

jobs to assure

that priority was

assigned

to

safety-related

equipment

maintenance

which

could

affect

system

performance.

Portions of the following activities were observed

or reviewed:

RC-103

and

RC-107; Pressurizer

spray valve packing leaks

AFW-93, AFW-155,

and AFW-71; Auxiliary feedwater valve packing

HD-46; Feedwater

heater ¹4

packing

RCDT;

Pump shaft replacement

Main feedwater

pump seal

water leak-off line replacement

Cleaning

and inspecting various

460 vac load centers

"A" condensate

booster

pump fluid coupling repairs

Rod drive urgent failure

The

Shutdown

Bank

B Group

2 rod control cabinet

experienced

an urgent

failure

on December

20,

1988.

After replacement

of the

phase control

and

firing circuit boards, it was discovered that transformer

"T2" was faulty.

The inspector witnessed

the maintenance activities associated

with removal

and replacement

of the "T2" transformer

in an energized

cabinet.

No violations or deviations

were identified.

5.

Licensee

Event Reports

(92700)

The

following

LERs

were

reviewed

for potential

generic

problems

to

determine

trends,

to determine

whether information included in the report

meets

the

NRC

reporting

requirements,

and

to

consider

whether

the

corrective

action

discussed

in

the

report

appears

appropriate.

The

licensee's

action

was reviewed to verify that the event

has

been

reviewed

and evaluated

as

required

by TS; that corrective action

was taken

by the

licensee;

and that safety limits, limiting safety settings,

and

LCOs were

not exceeded.

The inspector

exami'ned incident reports,

logs

and records,

and interviewed selected

personnel.

The following reports

are

considered

closed:

LER-87-56

Reactor

trip

caused

by

de-energization

of

P-13

permissive

bistable

due to insufficient modification

installation instructions.

LER-87-57

Failure

to

implement

all

required

in-service

inspection

tests

for diesel

fuel oil transfer

pumps;

procedural

deficiencies.

LER-87-58

Excessive

RCS leakage

due to valve failure in

RCS

head

vent system during testing.

LER-87-59

Loss of offsite

power

due to incoming line breaker

opening

caused

by

personnel

error

and

a

loss

of

emergency

service

due to procedural

deficiency.

LER-87-60

Isolation

of

RHR during testing

of valve interlocks

due to test

equipment failures

LER-87-61

Technical

Specification violation due to missed

flow

rate estimate

caused

by personnel

error.

LER-87-62

Personnel

error

in

setting

steam

dump controller

resulted

in safety

injection,

main

steam isolation,

and reactor trip when

MSIVs were opened.

LER-87-63

Plant trip caused

by loss of main

feed water

due to

mispositioned

condensate

recirculation valve.

LER-87-65

First

stage

turbine

pressure

setpoints

for

P-13

permissive

were

incorrectly

set

due

to

personnel

error.

LER-87-66

Failure to perform satisfactory

actuation

logic test

for

containment

ventilation

isolation

due

to

procedural

inadequacy.

LER-87-67

Containment

ventilation

system

i solat'ion

due

to

a

spurious

high

radiation

alarm

while

sampling

at

monitor.

No violations or deviations

were identified.

6.

Follow-up on Plant Events

(92702)

a.

On

December

14,

1988,

the

Unit

was

shutdown

for

a

five

day

maintenance

outage.

Maintenance

work

was

performed

on

the

pressurizer

spray valves, auxiliary feedwater

valves,

reactor coolant

drain tank pump,

and various other components.

The Unit was returned

to power operation

on December

19,

1988.

b.

On January

16,

1989, at 3: 18 p.m.,

the Unit tripped from 100~ power.

The trip was

due to low condenser

vacuum in the main condenser.

The

vacuum loss

was due to

a open vent valve

on the auxiliary condensate

system which allowed atmospheric

pressure

to the main condenser.

All

systems

functioned

as

designed

with the, exception

of the turbine

driven auxiliary feedwater

pump.

The turbine received

a start signal

but tripped

on overspeed.

Condensate

in the main

steam line to the

turbine

was the apparent

cause

of the

overspeed

trip.

The licensee

has

had

previous

problems

with condensate

in this line

and

had

performed

a modification to the moisture

removal

system

during the

last

refueling

outage.

The

licensee

has

initiated

a

program

to

periodically

blowdown the

condensate

removal

system

to ensure

that

condensate

is removed

and not allowed to collect in the

steam line.

On January

17,

1989,

the

PNSC decided that

a task force would

be

appointed

to perform

a design

review of the turbine driven auxiliary

feedwater

system

to determine

the root cause

of the

over speed trip

and to recommend

action to totally resolve

any problems.

The inspectors will follow the efforts of this task force.

This item

will remain

open

pending

completion of the review and is identified

as

inspector

followup item,

IFI 400/880-40-03:

Review

Task

Force

Resolution of Turbine Driven Auxiliary Feedwater

Pump Overspeed

Trip.

No violations or deviations

were identified.

7.

Plant Nuclear Safety Committee

(40700)

The inspectors

attended

one of the routine weekly plant operations

review

committee

PNSC meetings.

The

PNSC

was established

to advise

the plant

general

manager

on all matters

related

to nuclear

safety.

Technical Specifications, Section 6.5.2 provides the requirements

for the

committee

concerning:

function,

composition,

meeting

frequency,

size

and

members

required, authority,

and in general

the responsibilities

assigned

to the

members.

A quorum was present.

During the meeting,

Plant

Change

Request

(PCR)

3547 - Radioactive

Waste

Demineralizer

Skid

and Draft

LER-88-035

were discussed.

No violations or deviations

were identified.

10

8.

Exit Interview

The

insoection

scope

and

findings

were

summarized

during

management

interviews throughout the reporting period

and

on January

20,

1988, with

those

persons

indicated

in paragraph

1.

The inspection

findings listed

below were discussed

in detail.

The licensee

acknowledged

the inspection

findings and did not identify as proprietary

any material

reviewed

by the

inspector during the inspection.

Item Number

400/88-40-01

400/88-40-02

400/88=40-03

9.

List of Initialisms

Status

Open

Open

Open

Descri tion/Reference

Para

ra

h

Violation - Failure to Adequately

Perform

Post

Maintenance

-Testing

(paragraph 2.b.)

Violation - Failure to Follow

Procedure - (paragraph 2.c.)

IFI - Review Task Force Resolution of

Turbine

Driven

Auxiliary

Feedwater

Overspeed

Trip - (paragraph 6.b.)

AFW

AH

ALARA

ECCS

EIR

EPT

FSAR

IFI

KY

LCO

LER

LOCA

MS

MSIV

Auxiliary Feedwater

Air Handling

As

Low As Reasonably

Achievable

Emergency

Core Cooling System

Equipment

Inoperable

Records

Engineering

Periodic Test Procedure

Final Safety Analysis Report

Inspector

Follow-up Item

Kilo Volt

Limiting Condition for Operation

Licensee

Event Report

Loss of Coolant Accident

Main Steam

Main Steam Isolation Valve

11

MST

NRC

OP

PCR

PMTR

PNSC

RAB

RCDT

RCS

RHR

RWP

SF

SIS

TS

Vac

WR/JO

Maintenance

Surveillance=Test

NRC Regulatory

Commission

Operating

Procedure

Plant .Change

Request

Post Maintenance

Test Requirements

Plant Nuclear Safety

Committee

Reactor Auxiliary Building

Reactor Coolant Drain Tank

Reactor

Coolant System

Residual

Heat

Removal

System

Radiation

Work Permit

Spent

Fuel

Safety Injection Signal

Technical

Specification

Volts A.C.

Work Request/Job

Order