05000335/LER-1981-044-03, /03L-0:on 810928,during Fuel Movement W/Secondary Manways Removed,Two 3/16-inch Holes Drilled in a Main Feed Piping Between Main Feed Isolation Valve & Containment. Caused by Inadequate Definition of Work Scope & Location

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/03L-0:on 810928,during Fuel Movement W/Secondary Manways Removed,Two 3/16-inch Holes Drilled in a Main Feed Piping Between Main Feed Isolation Valve & Containment. Caused by Inadequate Definition of Work Scope & Location
ML17342A093
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 10/26/1981
From: Pace P
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17342A094 List:
References
LER-81-044-03L, LER-81-44-3L, NUDOCS 8111030246
Download: ML17342A093 (1)


LER-1981-044, /03L-0:on 810928,during Fuel Movement W/Secondary Manways Removed,Two 3/16-inch Holes Drilled in a Main Feed Piping Between Main Feed Isolation Valve & Containment. Caused by Inadequate Definition of Work Scope & Location
Event date:
Report date:
3351981044R03 - NRC Website

text

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R,PORT QA ~ 2 3O EVENT CESCRIPTION NO PROBABLE CONSECUKNCSS QO DURING FUEL HOVRIEIYT WXTH 'A'7G SECONDARY MAÃWAYS RE?COVED T)VO 3/16" HOLES WERE DRILLED IN THE 'A'AIN FEED PIPING BETWEEN THE MIN FEED XSOLA-TION VALVE A:K CONTAINMENT.

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