ML17333A838

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Insp Repts 50-315/97-02 & 50-316/97-02 on 970106-0215. Violations & Deviations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support
ML17333A838
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 03/27/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17333A835 List:
References
50-315-97-02, 50-315-97-2, 50-316-97-02, 50-316-97-2, NUDOCS 9704040147
Download: ML17333A838 (38)


See also: IR 05000315/1997002

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos:

50-315, 50-316,

License Nos:

DPR-58, DPR-74

Report No:

50-31 5/97002; 50-31 6/97002

Licensee:

Indiana Michigan Power Company

Facility:

Donald C. Cook Nuclear Generating Plant

Location:

1 Cook Place

Bridgman, Mi 49106

Dates:

January 6, 1997 - February 15, 1997

Inspectors:

B. L. Bartlett, Senior Resident Inspector

B. J. Fuller, Resident Inspector

J. D. Maynen, Resident Inspector

Approved by:

Bruce L. Burgess. Chief

Reactor Projects Branch 6

9704040i47

970327

PDR

ADOCK 050003i5

8

PDR

Ex cuiv

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D. C. Cook Units

1 and 2

NRC Inspection Report 50-315/97002, 50-316/97002

This inspection included aspects of licensee operations, maintenance,

engineering, and

plant support.

The report covers a 6-week period of resident inspection and includes the

follow-up to issues identified during previous inspection reports.

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The procedure revision process required the procedure writer to determine the

appropriate procedure review requirements for evaluating the acceptability of a

procedure change.

The procedure detailing the procedure review process contained

limited guidance to help the writer select one or more methods to ensure

a

procedure change was adequate.

The licensee's attempt to improve a procedure

resulted in an inadvertent entry into TS 3.0.3 when the procedure caused

a loss of

four loop injection capability.

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Licensee repairs to 2-MRV-212 and 2-MRV-241 were completed as planneo.

The

licensee expended many hours of preplanning to ensure all aspects of the job were

considered

before entry into a time-limited LCO, and displayed a conservative

decision making philosophy.

The inspectors concluded that mechanical

maintenance

procedures

needed improvement regarding some aspects of

mechanical maintenance

procedure review and parts preparation (Section M1.2).

After an emergent oil leak the licensee's engineering organization identified that the

oil level in the Sl pumps was being maintained at too high a level. While this high

'evel did not adversely affect the operability of the pumps it did reveal a failure to

maintain levels as recommended

by the vendor technical manual.

A non-cited

violation was issued for the failure to have a procedure that adequately reflected

vendor recommendations

or to have an approved alternative level.

(Section M1.3)

The inspectors concluded that a complacent attitude about new fuel receipt existed.

Each group involved in the receipt process carried out tasks to complete the job,

without a team effort to ensure the job was done in accordance with requirements.

Command and control of the new fuel was not the responsibility of a team leader,

but was dispersed

among the workers performing the tasks.

Seven violations and

one deviation were identified during new fuel receipt in preparation for the Unit 1

refueling. (Section M4.1)

The licensee's self-assessment

organizations, including Quality Control, the

maintenance

workers, their supervisor, and the other work groups involved, failed

to identify the significant and pervasive problem with procedural adherence

and

quality.

(Section M4.1)

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During new fuel receipt inspection the inspectors'observed

the reactor engineer

closely inspecting new fuel assemblies.

However, the reactor engineer was not

cognizant of maintenance workers, involved in new fuel receipt inspection, not

following their procedures.

While it was not a procedural requirement that monitor

the job performance of the other work groups it appeared that he was too

complacent.

(Section M4.1)

Pl

o

Routine observations were made by inspectors with no discrepancies

noted.

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Unit 1 main transformer temperature limitations forced operation of the Unit to be between

90 percent to 99 percent power during the inspection period.

Unit 2 entered the inspection period at full power.

On January 10, 1997, reactor power

was reduced to 70 percent as part of testing and repair of the dump valves to the steam

generator stop valves.

On February 7, 1997, power was reduced to approximately 55

percent power to perform repairs of the east main feedwater pump. At the end of the

inspection period the Unit was still at 55 percent holding for the repairs on the feedwater

pump.

1

01

Conduct of Operations

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01.1

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717

7

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations.

The conduct of operational activity that was observed

was generally good.

Specific events and noteworthy observations

are detailed in

the sections below.

03

Operations Procedures and Documentation

03.1

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On January 12, 1997, the safety injection (SI) pump discharge cross-tie valve was

closed before the residual heat removal (RHR) discharge cross-tie valve was opened

in accordance with procedure, ""01 OHP 4021.008.004,

"Adjusting the Level of

Accumulators," Revision 6. As a result, four loop injection requirements were not

met for approximately a one minute period.

The inspectors interviewed the

procedure writer and the procedure writer's supervisor.

In addition, the following

documents were reviewed:

Licensee Condition Report (CR) 97-0151

Licensee Event Report 50-315/95004-00,

"Technical Specification 3.0.3

Entered On Loss of Four Loop Injection Capability Due to Personnel

Error

during Performance of Surveillance"

Licensee Event Report 50-315/97001-00,

"Technical Specification 3.0.3

Entered On Los's of Four Loop Injection Capability Due to Incorrect

Procedural Guidance"

NRC ~nspection Report 50-315/316-95009

NRC Inspection Report 50-315/316-96004

Procedure ""01 OHP 4021.008.004,

"Adjusting the Level of

Accumulators," Revision 6

OPM.002, "Operations Department Procedure Review Manual"

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This was the first time Revision 6 of procedure ""01 OHP 4021.008.004,

"Adjusting the Level of Accumulators," was used.

The licensee had revised the

procedure to address operator concerns with filling accumulators with the Sl pump

discharge cross-tie valves open.

A good questioning attitude by the operators was

exhibited when they questioned the operability of the Sl pump during the filling of

the accumulators.

Pending a formal analysis, the licensee had considered the Sl

pump to be inoperable when using it to fillan accumulator.

Revision 6 also

changed the sequence

of valve manipulations used to fillaccumulators using a Sl

pump.

Changing the sequence

resulted in both Sl and RHR discharge cross-tie

valves being shut simultaneously,

a condition outside the design basis of the plant.,

The licensee made a one hour notification to the NRC on January 16, 1997 and

submitted Licensee Event Report 50-315/97001-00 to document this event.

Revisions to operations department procedures

are reviewed using the Operations

Department Procedure Review Manual, OPM.002.

According to this instruction,

the procedure writer was responsible for determining the review requirements,

but

at a minimum, the revision process required an administrative review. Also,

functional reviews were done for revisions of a technical nature.

The procedure

writer for Revision 6 chose both administrative

and functional reviews for

this'evision.

A qualified licensed operator performed the functional review of the

procedure, but the review failed to identify the sequencing

problem.

This failure

occurred even though the functional review checklist, asked "Is the sequence

of

actions correct?"

Licensee corrective actions included discussions with the procedure writers on the

importance of an adequate technical verification of procedures,

training on source

document requirements,

10 CFR 50.59 reviews and functional reviews.

In addition,

operator aids were placed on the control panels to provide guidance on Sl pump

and RHR pump discharge cross-tie valve controls.

C.

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Procedure OPM.002 contained limited guidance to help the writer determine the

appropriate method for review of a procedure.

Both the writer and procedure

reviewer were narrowly focused during their review to revision 6 to procedure ""01

OHP 4021.008.004.

The inspector's determined that the review process contained

the necessary

controls to adequately review procedure changes,

including having a

system engineer review the procedure or validating the procedure on the plant

simulator, but these methods were not used.

The licensee's attempt to improve a

procedure resulted in an inadvertent entry into TS 3.0.3 when the procedure caused

a loss of four loop injection capability.

This licensee-identified and corrected failure

to adequately review changes to procedures is being treated as a Non-Cited

Violation, (50-315/316-97002-09)

consistent with Section VII.B.1 of the NRC

Enforcement Policy.

08

Miscellaneous Operations Issues

08.1

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- 4 22- 2: Limiting Condition for Operation

(LCO) Management:

Entry into LCOs to perform maintenance activities was considered an unresolved

item pending further review by the NRC. The inspectors were concerned that the

licensee was entering LCOs to perform maintenance without adequate justification.

The licensee has begun tracking system performance and availability as required by

the NRC maintenance

rule.

Goals and limitations on equipment and system

availability were set by the licensee and tracked for performance.

Those goals and

availabilities, reviewed by the inspectors and by the NRC maintenance

rule

inspection team, were found to be reasonable

and within limits. A recent example

of good LCO management for maintenance

is discussed

below in Section M1.2.

This unresolved item is closed.

08.2

I

LER

0-

1

4-: Main Generator Trip on Main transformer Sudden

Overpressure

Due to Lightning Strike Causes Reactor Trip. At 0049 on September

21, 1996, a reactor trip occurred due to a turbine trip. The cause of the turbine

trip was a spurious main transformer sudden pressure

signal due to a lightning

strike. The plant responded to the trip as designed.

This event was discussed

in

detail in Inspection Report 50-315/316-96011.

The inspectors concluded that

operators responded

promptly and effectively to the unit trip and had no further

concerns.

This LER is closed.

08.3

I

ER

-

1

7

1- 0: Technical Specification 3.0.3 Entered On Loss of

Four Loop Injection Capability Due to Incorrect Procedural Guidance.

This LER is

discussed

in paragraph 03.1, above.

The LER was reviewed as part of inspector's

followup to the loss of four loop injection capability.

No new issues were revealed.

This LER is closed.

M1

Conduct of Maintenance

a.

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The inspectors observed

all or part of the following maintenance

and surveillance

activities:.

C0038395Repair Water Leak on Inlet to. Oil Cooler on Unit 1 Turbine Driven

Auxiliary Feedwater Pump (TDAFWP)

C0039248Change

Oil/Replace Inboard Oiler Pipe Fitting on Unit 1 TDAFWP

C0038858Repair 2-MRV-212, Steam Generator

1 Stop Valve 2-MRV-210 Steam

Cylinder Train 'A'ump Valve

C0038948Repair 2-MRV-241, Steam Generator 4 Stop Valve 2-MRV-240 Steam

Cylinder Train 'B'ump Valve

R0010418Replace

ASCO Solenoid Valve 1-XSO-256, TDAFWP test valve control

solenoid

R006600502-OHP 4021.STP.051N

Revision 6, Unit 2 North Safety Injection Pump

Operability Test

R006600502-OHP 4021.008.007,

"Operation of the Safety Injection Pumps,"

Revision 0

!

!

R006600502-OHP 5030.001.001,

"Operations Plant Tours," Revision 8

R0056617Unit

1 East Motor Driven Auxiliary Feedwater Pump Essential Service

Water Suction Strainer Lubricate Chain Drive

R0056934Unit

1 East Motor Driven Auxiliary Feedwater Pump Change Oil and

Handpack Coupling

""12MHP4050.FDF.001Receipt

and Storage of New Fuel Assembly Shipping

Containers,

Revision 4

""12MHP4050.FDF.002Unloading

of New Fuel Assemblies from Shipping

Containers, Revision 6

""12MHP4050.FDF.005Handling of New Fuel Assemblies for Inspections and

Associated Work, Revision 3

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""12QHP4050.QC.001Recejpt,

Inspection, and Storage of New Fuel Assemblies

and Inserts, Revision 0

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Overall, observed maintenance was performed correctly, with few problems noted;

however, some maintenance activities observed resulted in significant NRC identified

issues.

Specifically, the receipt of new fuel assemblies was a work evolution poorly

handled by licensee personnel

~ The items identified by the inspectors revealed the

existence of fundamental weaknesses

in the licensee's maintenance

organization. (Section

M4.1) Other jobs reviewed by the inspectors revealed challenges to the maintenance

organization.

This included the repairs to 2-MRV-212 and 2-MRV-241 which received

extensive advanced

planning due to the complex nature of the conditions required to

complete the work. (Section M1.2) Additionally, during the Unit 2 North Safety Injection

Pump operability test, an oil leak on the pump outboard bearing resulted in remaining in an

LCO longer than planned. (Section M1.3)

M1.2

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MRV-212

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MRV-241

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On December 3 and 4, 1996, the licensee identified that two valves, 2-MRV-212, Steam

Generator

1 Stop Valve 2-MRV-210 Steam Cylinder Train 'A'ump Valve, and 2-MRV-

241, Steam Generator 4 Stop Valve 2-MRV-240 Steam Cylinder Train 'B'ump Valve,

had seat leakage.

On January 11, 1997, on-line repairs and testing of both valves were

completed.

The inspectors observed job planning and peiformed continuous observation

of maintenance activities including post maintenance testing.

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Significant preplanning was involved in this job before the work was allowed to begin, due

in part to a previous plant trip during on-line repairs to 2-MRV-241 and the attendant entry

into a very short duration limiting condition for operation (LCO). On-line repairs and testing

of valves 2-MRV-212 and 2-MRV-241 required two separate entries into the Technical

Specification (T.S.) action statement 3.7.1.5.

T.S. 3.7.1.5 required restoration of the

main steam stops within eight hours.

Additionally, if both 2-MRV-212 and 2-MRV-241

leaked excessively, then the plant would have been in an unanalyzed condition requiring

entry into TS 3.0.3.

However, pressure decay leak testing of both 2-MRV-212 and 2-

MRV-241 showed that both valves had less than 10 percent of the allowable leakage (200

gpm); therefore, the main steam stop valves were operable and the safety significance of

the leakage was small.

All work observed was done with the work package present and in active use.

The

inspectors observed continuous coverage by Mechanical and Instrumentation and Controls

(l&C) supervisors and the Main Steam system engineer.

As the work progressed,

a

number of discrepancies

were noted:

A peer inspector, performing a parts receipt inspection as required by the work

package, rejected a valve disc that had been receipt inspected before commencing

the job.

Rejection of the part showed good attentiveness to the inspector's duties.

However, the fact that this part was not thoroughly inspected until the workers

were at the job site on an LCO time-limited repair showed a lack of attention to

detail when preplanning this job.

~

A discrepancy was discovered between what parts were installed internal to the

valve and what the procedure drawing showed.

A "typical" valve configuration

was reflected on the drawing, not the valve as installed in this application.

This

procedure had been used for prior repairs of the dump valves, but the discrepancy

had not been identified. A revision to the procedure was required delaying

completion of the work by more than one hour.

The inspectors observed that the

licensee had started planning this LCO time-limited job at least three weeks prior to

commencement

but still did not do a thorough procedure review.

While reassembling

the actuator for 2-MRV-212 to the valve body, the sequence

of

limitswitch parts (jam nut, indicator disc, adjusting nut, limitswitch arm) on the

valve stem was questioned.

The mechanical maintenance

procedure did not

contain any reference drawing for the stack-up of these parts and inspection of the

throe adjacent actuators showed a different arrangement

on each installation.

Valve actuator reassembly was based on the memory of the ISC technician as to

the as found configuration.

A reference drawing was found after the actuator

reassembly and confirmed that the as left configuration was correct.

Actuator

configuration on 2-MRV-241 was changed to match the reference drawing during

maintenance

on that valve.

The licensee planned to reconfigure the actuators on

the other dump valves during later maintenance.

Repairs to 2-MRV-241 had few problems, and the only delays were due to

correcting material condition deficiencies identified during the procedure.

Correcting minor material condition deficiencies was within the work scope, and the

delays did not challenge the operators or maintenance staff. Condition Reports

were written to document these problems.

Shortly after the repair, 2-MRV-241 began leaking past the seat again.

The licensee

speculated that the leak may have started following cycling the valve for the post-

maintenance

operability surveillance. Valve 2-MRV-241 remained operable since the

leakage was determined to be less than the as found leakage by visual observation.

A

Condition Report was written to document the leak.

Licensee repairs to 2-MRV-212 and 2-MRV-241 were done as planned.

The licensee

expended many hours of preplanning to ensure all aspects of the job were considered prior

to entry into a time-limited LCO, and displayed a conservative decision making philosophy.

The inspectors observed that an area for improvement existed in some aspects of

mechanical maintenance

procedure review'and parts preparation.

M1.3

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On January 22, the inspectors observed the performance of Operations Procedure, 02-

OHP 4030.STP.051N,

"North Safety Injection Pump System Test," Revision 6, which was

performed following maintenance

on the pump.

During the surveillance test, the auxiliary

equipment operators (AEOs) noticed an oil leak on the outboard bearing of the Unit 2 North

Safety Injection (Sl) pump.

The inspectors followed up on the licensee's resolution of the

oil leak. The following documents were reviewed:

02-OHP 4021.008.007,

"Operation of the Safety Injection Pumps," Revision 0

02-OHP 4030.STP.051M, "Unit 2 North Safety Injection Pump Operability Test,"

Revision 6

02-OHP 5030.001.001,

"Operations Plant Tours," Revision 8

Condition Report 97-0218

Condition Report 97-0219

Pacific Pumps Vendor Technical Manual VTM-PACP-0002.

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The inspectors attended the pre-job brief given by the reactor operator (RO) and observed

the AEOs perform the test.

The brief was thorough, and all operator responsibilities were

clearly defined.

The inspectors noted good operator self-checking and communications

during the test.

Operating Procedure 02-OHP 4030.STP.051N was in hand and in use

throughout the test, and the AEOs followed the procedure.

No problems were noted with

the performance of the surveillance test; however, while thb pump was running, the

operators noticed oil leaking past the outboard pump bearing and misting onto the splash

guard.

Due to the oil leak, the Unit Supervisor did not want to declare the pump operable

until Plant Engineering had assessed

the severity of the oil leak.

Operations Procedure

(OHP) 5030.001.001,

"Operations Plant Tours," required, in part,

that the operators check running equipment oil system sump level for a minimum level of

one-quarter of the range of the sight glass and a maximum level within the indicating range

of the sight glass.

The oil level in the Unit 2 North Sl pump was approximately seven-

eighths of the range of the sight glass, or about one inch below the top of the sump, while

the pump was running.

The idle level was higher, but still within the indicating range of

the sight glass; therefore, the operators signed off the test procedure showing that the oil

level of the Sl pump was within the normal operating range.

10

The licensee's engineering staff evaluated the oil leak and determined that it was too large

to declare the pump operable.

Emergent maintenance was done on the outboard pump"

bearing to clean the oil vent and drain lines, replace the bearing housing gasket, and RTV

the bearing housing.

The subsequent

operability test of the Unit 2 North SI pump again

resulted in oil leaking along the shaft through the labyrinth seal.

Further evaluation pointed to excessive

oil level in the oil reservoir as the cause of the leak.

The Pacific Pumps Vendor Technical Manual, VTM-PACP-0002, showed normal Sl pump

oil level as 3.5 inches below the top of the reservoir and the maximum oil level as 2.5

inches below the top of the reservoir; however, the "as found" oil level was approximately

one inch below the top of the reservoir.

The oil level was drained to within the vendor

technical manual limits, and the operability test was run again.

The Unit 2 North Sl pump

passed the operability test, and no oil leakage was evident.

The pump was declared

operable at on January 23, 1997.

Oil levels in the Unit 2 South SI pump oil reservoir and both'of the Unit 1 Sl pump oil

reservoirs were found to be above the vendor technical manual limits, so those oil

reservoirs were also drained.

The safety significance of this event was small because the

pumps would have remained operable if required.

The licensee's analysis showed that the

oil leak would continue until the level drained to within the vendor manual limits and then

stopped.

Operator aids were attached to the oil reservoirs on all four Sl pumps indicating the

acceptable vendor manual band for oil level. Additionally, the licensee planned to review

the vendor technical manuals for all other safety-related pumps and place operator aids on

all safety-related pumps to show what level range was acceptable for oil level.

C.

After an emergent oil leak the licensee's engineering organization identified that the oil

level in the Sl pumps was being maintained at too high a level. While this high level did

not adversely affect the operability of the pumps it did reveal a failure to maintain levels as

recommended

by the vendor technical manual

~ The failure to have a procedure that

adequately controlled Safety Injection pump oil level constituted

a violation of minor

significance and is being treated as a'Non-Cited Violation, (50-315/316-97002-10)

consistent with Section IV of the NRC Enforcement Policy.

M4

Maintenance Staff Knowledge and Performance

M41 NwF

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a.

Licensee preparation for the planned Unit 1 refueling outage was observed by the

inspectors.

This inspection primarily focused on the control of and movement of new fuel

during receipt inspection.

Receipt, storage and handling of the new fuel were safely

performed, but failures to meet NRC requirements and a lack of ownership over new fuel

were noted by the inspectors.

The following documents were reviewed:

11

""12MHP4050.FDF.001Receipt

and Storage of New Fuel Assembly Shipping

Containers

'"12MHP4050.FDF.002Unloading

of New Fuel Assemblies from Shipping

Containers

""12MHP4050.FDF.005Handling of New Fuel Assemblies for Inspections and

Associated Work

""12QHP4050.QC.001Receipt,

Inspection, and Storage of New Fuel Assemblies

and Inserts

ANSI B30.9-1971Slings

PMI-2011Procedure

Use and Adherence

MHI-4053Control of Heavy Loads

Regulatory Guide (RG) 1.33Quality Assurance Program Requirements

(Operation)

b.

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During routine inspection activities, the residents identified programmatic problems

concerning the licensee's receipt of new fuel assemblies,

including:

,procedural adherence,

maintenance of procedures,

command and control of new fuel receipt activities,

foreign material exclusion control, and

self assessment

of the new fuel receipt program.

1.

Procedural Adherence

Plant Manager's Instruction (PMI)-2011, Procedure

Use and Adherence, required that "in-

hand" procedures

(designated

by "" in the procedure number) to be at the job site, and in

use.

~

The inspectors identified that on January 28, 1997 the procedures for unloading

shipping containers from the truck (Procedure ""12MHP4050.FDF.001, "Receipt

and Storage of New Fuel Shipping Containers" ) and for unloading assemblies

from

the shipping containers (Procedure ""12MHP4050.FDF.002, "Unloading of New

Fuel Assemblies From Shipping Containers" ) were not being used "in-hand" for the

performance of the work.

In fact, the procedures were located outside the foreign

material exclusion zone (FMEZ) and were not being referenced.

12

Plant Manager's Instruction (PMI) 2011, "Procedure Use and Adherence," required that,

unless the procedure specifically allowed a different sequence,

procedure performance

shall be:

e

Read the step,

Perform the steo,

Document completion of the step,

Proceed to the next step.

On January 28, 1997, the inspectors identified that the unloading of new fuel

shipping containers was not performed in a step by step manner.

Procedure

"'12MHP4050.FDF.001, Receipt and Storage of New Fuel Shipping

Containers,'tep

6.7 attached rigging to the shipping container before lifting. Step 6.12

,established

a work loop back to step 6.8 to liftanother container. Step 6.8 did not

attach rigging, only a tag line. The procedure was not worked in a step by step

manner as required by PMI-2011.

On January 28, 1997, the inspectors also identified that work was not performed in

a step by step manner for unloading new fuel. The work was being done in parallel

on three shipping containers, by breaking procedure ""12MHP4050.FDF.002 into

loops of steps:

remove container cover for three containers,

position lock tubes for three containers,

upright support frames for three containers,

remove assemblies from support frames for three containers.

The loops of steps were not specified by the procedure.

No allowance existed in the

procedures for parallel operations on more than one container.

The procedure was not

worked in a step by step manner as required by PMI-2011.

After procedure adherence

problems were pointed out by the NRC, the licensee

identified a procedure sequence

error on January 28, 1997.

Procedure

""12MHP4050.FDF.005, Handling of New Fuel Assemblies for Inspections and

Associated Work, step 6.17, required replacement of the NFSV plug after storage

of a new fuel assembly.

Before identifying the error, on January 25, 1997, the

licensee had performed ""12MHP4050.FDF.005 for twelve fuel assemblies without

replacing the floor plug in the new fuel storage vault after seating each fuel

assembly as required by the procedure.

The procedure was not worked in a step

by step manner as required by PMI-2011.

13

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II

1

Maintenance Head Instruction (MHI) 4053, "Control of Heavy Loads," requires in Section

3.6, that guidelines set forth in ANSI B30.9-1971, Slings, be followed. ANSI B30,9-1971,

Slings, Section 9-1.9, Safe Operating Practices, step 9-1.9.1b requires that the sling shall

have suitable characteristics

and rated capacity for the load and environment.

The inspectors identified that on February 3, 1997, the licensee lifted a load of

approximately 6,325 pounds using a lifting sling rated at only 6,000 pounds.

This

lifting sling was designated

as the tool to be used for this operation.

The date of

designation could not be recalled by the licensee, but was believed to have been

many years ago.

The licensee did not follow the requirements of MHI-4053 for

sizing slings.

Several violations of NRC requirements were identified in procedure use and adherence.

The failure to use the ""12MHP4050.FDF.001, "Receipt and Storage of New Fuel

Assembly Shipping Containers," and ""12MHP4050.FDF.002, "Unloading of New Fuel

Assemblies from Shipping Containers," in-hand were two examples of a violation of PMI-

2011 (50-315/97002-01a,b

(DRP)). Three examples of a violation of PMI-2011 were

identified in that ""12MHP4050.FDF.001, ""12MHP4050.FDF.002, and

""12MHP4050.FDF.005, "Handling of New Fuel Assembiies for Inspections and

Associated Work," were not followed step-by -.'.ep (50-315/97002-02a,b,c

(DRP)). A

violation of Maintenance Head Instruction 4053, "Control of Heavy Loads," was identified

for using an improperly rated sling (50-315/97002-03

(DRP)).

2.

Maintenance of Procedures

The inspectors identified that previous review and use of the new fuel receipt procedures

had not identified deficiencies with the procedures.

These procedures

had been used since

1991 with only minor changes in 1996. After the lack of procedural adherence was

pointed out by the inspectors, the licensee identified that procedure

""12MHP4050.FDF.005 would not work as written.

Changes to ""12MHP4050.FDF.002 were required to allow parallel operations on three

shipping containers after a lack of such instructions was identified by the inspectors.

This

parallel mode had been the licensee's method of unloading for many years.

Similar

changes were required in ""12MHP4050.FDF.001 to correct sequencing

errors.

Many additional changes to the procedures were made to correct work sequencing,

FME

practices, command

and control issues and rigging problems which were identified on

January 28 and February 3, 1997.

Some changes were licensee initiated enhancements

after the initial problems were identified by the NRC.

~

""12MHP4050.FDF.001 two change sheets since January 28, 1997

~

""12MHP4050.FDF.002 five change sheets since January 28, 1997

~

""12MHP4050.FDF.005 four change sheets since January 28, 1997

14

0

MHI-4053 Control of Heavy Loads, step 3.2.2 stated in part, "No load greater than 5 tons

should be traveled at a height greater than 7 feet above the floor except when clearing

obstacles

or installing or removing equipment from its storage location." This procedure

was inadequate

in that it did not fully implement a licensee commitment documented

in

AEP:NRC:0514F which stated, "Allloads of five tons or less listed in Table 2.1.3.C.1 of

our letter No. AEP:NRC:0514C will be moved as close to the floor as practical, but in no

case higher than 7 feet above the floor." On February 3, 1997, the inspectors observed

three new fuel shipping containers, each weighing approximately 4 tons, moved at a

height greater than 7 feet above the 650'evel floor.

The new fuel handling procedures were inadequate

in that they had errors in work step

sequencing;

lacked foreign material exclusion practices; and contained no detail on rigging

requirements and control of heavy loads requirements.

50-315/97002-06(DRP).

MHI-,

4053 step 3.2.2 constituted

a deviation from an NRC commitment. 50-315/97002-

08(DRP)

3.

Command and Control of New Fuel Receipt

While pursuing the issue of procedural adherence,

the inspectors interviewed the Reactor

Engineering representative.

The reactor engineer told the inspector that the procedure in

question (" "12MHP4050.FDF.002) was not an "in-hard" procedure, so it did not need to

be used step by step.

After the inspectors pointed out that it was an "in-<<~nd" procedure,

the inspectors were referred to the first line maintenance

supervisor, as it was a

maintenance

procedure that was in question.

The reactor engineer did not get involved in

resolving the issue, even though it concerned the handling of fuel.

The first line maintenance

supervisor also informed the inspector that the procedure was

not required to be used step by step and that it was there as a reference for the

mechanics.

The supervisor added that the procedure would be impossible to work in a

step by step fashion as written and that the mechanics were handling the fuel in

accordance with longstanding licensee practice.

The mechanical supervisor had been

observing the new fuel receipt, but not actively directing the sequence;

however, the work

appeared to be performed safely.

The inspectors then contacted the Maintenance

Mechanical Production Supervisor who agreed that the procedure was intended for "in-

hand" use.

The new fuel receipt was stopped until the maintenance

personnel were

briefed on procedure adherence.

The inspectors questioned

licensee management

team about the position designated

as

"Fuel Handling Supervisor".

The licensee's consensus

was that clear delineation of

responsibility during fuel handling was not evident. After meeting to discuss the

inspectors'oncerns,

licensee management

formally designated the maintenance

supervisor assigned for new fuel receipt as the Fuel Handling Supervisor and revised the

procedures to reflect the designation.

No violations of NRC requirements were identified; however, the inspectors noted that

command and control of the new fuel receipt was not established.

15

t

4.

Foreign Material Exclusion (FME) Control

The inspectors identified a significant amount of small pieces of foreign material around

the opening of the new fuel storage vault (NFSV) on the ledge where the plug had been

removed.

This debris was identified after the insertion of one fuel assembly into the vault,

The NFSV opening was within an established foreign material exclusion zone (FMEZ).

Specific findings are detailed below:

Plant Manager's Procedure,

12 PMP 2220.001.001,

"Foreign Material Exclusion,"

required that if the work evaluation results in an FMEZ designation of FMEZ-1 or

FMEZ-2,'then the work group supervisor shall complete a Foreign Material Exclusion

Requirement/Work Practices Determination, Attachment 2, to determine appropriate

FME requirements, work practices, and post-job inspections.

Additionally, the

procedure required that a copy of the completed Attachment 2 should be included

in the work package and should be used in the pre-job brief. However, Attachment

2 to 12 PMP 2220.001.001

was not completed for work performed in an FMEZ on

January 28, 1997, was not included in the work package,

and was not used in the

pre-job brief, although the supervisor stated that he covered FME practices in the

brief.

Procedure

12 PMP 2220.001.001

also required that while working within the

FMEZ,

clean-as-you-go" work practice shall be maintained to minimize the,

potential for introduction of foreign material into any equipment or system.

Licensee personnel failed to comply with the requirements regarding maintaining

cleanliness of new fuel.

Plant Manager's Instruction 2220, "Foreign Material Exclusion," Step 6.2 assigns

responsibility to the line supervisor for monitoring work and ensuring FME controls

are adequate

and being carried out. The mechanical supervisor assigned

responsibility for this job activity did not monitor the work and failed to recognize

that inspection and "clean-as-you-go" work practices were not implemented.

This

allowed foreign material to exist on the ledge, with the potential to enter the NFSV

with new fuel stored inside.

Procedure

""12MHP4050,FDF.005, "Handling of New Fuel Assemblies for

Inspections and Associated Work," which removed the plug from the vault,

contained no instructions to inspect and clean the opening of the vault.

Two violations of procedure 12 PMP 2220.001.001

were identified by the NRC inspectors

during the new fuel receipt.

First, Attachment 2, "Foreign Material Exclusion

Requirement/Work Practices Determination," was not completed and used in the pre-job

brief. (50-315/97002-07(DRP)).

Second, the "clean-as-you-go" work practices were not

used to prevent foreign material from entering the NFSV (50-315/97002-05

(DRP)).

One

violation of PMI 2220 was identified in that the mechanical supervisor assigned the

responsibility for monitoring the work did not ensure that the "clean-as-you-go"work

practices were implemented (50-315/97002-04

(DRP)).

Finally a violation of 10 CFR 50

Appendix B, Criterion V, "Instructions, Procedures,

and Drawings," was identified in that

procedure ""12MHP4050.FDF.005, "Handling of New Fuel Assemblies for Inspections and

Associated Work," contained no instructions to inspect and clean the opening of the vault

(50-31 5/97002-06(DRP))

~

5.

Self Assessments

of the Program

Plant Performance Assurance

(QC) personnel were tasked with performing new fuel

inspections and were present during all work periods where NRC inspectors identified

concerns with the licensee's performance.

QC personnel did not develop any independent

findings concerning the evolutions cited above.

Reactor Engineering and Maintenance

Mechanical personnel present at the job site or involved with the project also failed to

identify problems associated with new fuel receipt.

The inspectors also reviewed the licensee's response to NRC Bulletin 96-02, "Movement

of Heavy Loads Over Spent Fuel, Over Fuel In The Reactor Core, Or Over Safety-Related

Equipment."

Bulletin 96-02 requested the licensee to review plans and capabilities for the

handling of heavy loads.

The licensee's responded

on May 10, 1996, (AEP:NRC:0514Z)

and committed to initiate a self assessment

of their commitments to NUREG 0612.

The

licensee completed the self assessment

on December 27, 1996 (licensee report number

ENSP-96-01).

Guideline number 5, item number 3 of the licensee's assessment

plan

looked specifically at the commitment regarding 5 <on loads being handled as close to the

floor as possible.

Unfortunately, the licensee's assessment

plan did not verify the

commitment but instead venfied the same inadequate

procedural requirements that had

been included in the maintenance

procedures.

Specifically, the assessment

plan verified

that loads greater than 5 tons would be handled as close to the floor as possible and failed

to verify that loads less than 5 ton would not be handled at heights greater than 7 feet.

One deviation (50-315/316-97002-08

(DRP)) to a commitment was identified. On

February 3, 1997, the inspectors identified that the licensee moved new fuel shipping

containers, containing new fuel assemblies,

and weighing approximately four tons, higher

than 7 feet above the floor'when moving the containers to a location to be unloaded.

c.

g~nl i~in~;

The inspectors identified a total of seven violations and one deviation during new fuel

receipt handling and inspection.

The inspectors identified numerous examples of failure to

use fuel handling procedures in-hand, failure to follow procedures step by step, failure to

follow foreign material exclusion procedures,

failure to comply with requirements

and

commitments in weight handling procedures,

and numerous examples of inadequate

procedures.

The inspectors concluded that a complacent attitude about new fuel receipt existed.

The

job was considered routine, and as a result little effort had gone into identifying problems

or preparing for the job. Additionally, each group involved in the receipt process carried

out tasks to complete the job, without a team effort to ensure the job was done in

accordance with requirements.

Command and control of the new fuel was not the

responsibility of a team leader, but was dispersed among the workers performing the

tasks.

17

4

0

I

0

IVIS

MIscellaneous Maintenance Issues

M8.1

I

Vi

I

i n

1

14-

2

EA

- 2: Unit 1 West CCP inoperable due to

a miscalibrated overcurrent relay and Unit 1 East CCP inoperable for planned

maintenance.

This was one of three violations issued as part of EA 96-020.

Violation 315/95014-01

was closed in Inspection Report 50-315/316-96010.

This

violation was a consequence

of the CCP being inoperable for an extended period

due to the relay being out of calibration.

This violation will be addressed

as a part

of the closeout of violation 315/95014-03 discussed

below. This violation is

closed.

M82

I

Vi

I

1

-

E -: Calibration procedure inappropriate

to the circumstance for an overcurrent relay to the Unit 1 West CCP.

This was one

of three violations issued as part of EA 96-020.

Violation 315/95014-01

was

closed in Inspection Report 50-315/316/96010.

A miscalibrated overcurrent relay

would have rendered the 1W CCP inoperable during a loss of coolant accident.

The

cause of the miscalibrated relay was inexperienced

IRC technicians using a

procedure with an inadequate amount of d'etail.

The NRC inspectors interviewed personnel, reviewed procedures,

evaluated relay and test

equipment, reviewed licensee corrective actions, and verified Implementation of selected

portions of the corrective actions.

The NRC inspectors agreed with the licensee's root

cause analysis that a combination of inexperienced technicians and a weak calibration

procedure lead to the miscalibration of the relay.

In addition, a weak review of the

completed data failed to identify the miscalibrated relay immediately following the

surveillance.

Licensee corrective actions included:

Recalibrating the 1W CCP relay and testing 14 other safety related relays that had

not been operated under the most limiting conditions.

Retraining all lhC technicians on the correct calibration techniques,

as well as

enhancing the relay training program.

Enhancing the relay calibration procedure to add detail on the calibration of the

relay.

The procedure was also modified to add the requirement to record as found

data.

This data was to be used to help trend the reliability of the relays.

Additional training on reporting requirements of 10 CFR Part 50.72 was given to

Nuclear Safety, Licensing, and Fuel Division personnel to address the initial delay in

reporting this issue.

In response to a specific NRC request the licensee also evaluated the potential of

other maintenance activities being conducted, using technicians who had not

maintained their proficiency by requalification training, or on the job performance of

specialized procedures.

The licensee's evaluation determined that this event was

an isolated occurrence.

The NRC inspectors reviewed other procedures,

observed

18

4f

l

technicians performing the other procedures and did not identify any other

examples.

As stated above, all of the corrective actions listed above were sampled by the NRC

inspectors to ensure that the corrective had been implemented.

This violation is closed.

M8.3

I

i

F

II w-

I

m

1

-

24- 2: Review of future core

inspections to assess

effectiveness of the licensee actions to prevent foreign

material intrusion in the core.

During a previous inspection (IR 315/316-

95010(DRP), the inspectors had identified numerous examples of poor FME control

around the fuel handling areas (e.g., spent fuel pool, reactor vessel, refueling

cavity, etc.).

During previous inspection periods the licensee was noted to be

making improvements in the control of foreign material around fuel handling areas.

However, as noted in section M4.1, above, the licensee still has improvement items

to implement.

This inspection follow-up item is still open.

M8.4

I

LER

-

1 -: Reactor Protection System Actuation Results from

Personnel

Error During Calibration of Intermediate Range Nuclear Instrumentation.

On September 26, 1996, a reactor trip signal was generated

by Instrumentation

and Controls technicians when intermediato r~nge nuclear instrument power fuses

were removed without the Level Trip switcn being placed in the bypass position.

The reactor was shutdown in Mode 5 at the time of this event, and no actual

control rod movement occurred.

This event was the subject of a non-cited

violation'n

Inspection Report 50-315/316-96011,

and the inspectors had no further

concerns.

This LER is closed.

III

~Ein(~i

E1

Conduct of Engineering

During the resident inspection activities, routine observations were conducted in the areas

of engineering using Inspection Procedure 37551.

No discrepancies

were noted.

Engineering involvement in the auxiliary feedwater pump oiler issues discussed

in Section

M1.2 was noted to be prompt, thorough, and timely.

ES

IVliscellaneous Engineering Issues

E8.1

r

Iv

I

m

-

1

1

-

7-: Operability of the essential

"

service water system (ESW) with inoperable pump discharge strainers (both units).

Pending additional information from the licensee the issue of whether the ESW

pump discharge strainers were required to be operable in order to support the

operability of the ESW system remained an unresolved item. The licensee supplied

the inspectors with the additional information but the information did add any

substantive data to the issue.

This unresolved item will remain open pending the

response to a task interface agreement

being sent to the office of NRR.

19

0

t

R1

Radiological Protection and Chemistry Controls (71750)

During the resident inspection activities, routine observations were conducted in the areas

of radiological protection and chemistry controls using Inspection Procedure 71750.

No

discrepancies

were noted.

S1

Conduct of Security and Safeguards Activities (71750)

During normal resident inspection activities, routine observations were conducted in the

areas of security and safeguards activities using Inspection Procedure 71750.

No

discrepancies

were noted.

F1

Control of Fire Protection Activities (71760)

During normal resident inspection activities, routine observations were conducted in the

area of fire protection activities using Inspection Procerlure 71750.

No discrepancies

were

noted.

X1

Exit Meeting

The inspectors presented the inspection results to members of the licensee management at

the conclusion of the inspection on February 14, 1997.

The licensee acknowledged the

findings presented.

20

i

PARTIALLIST OF PERSONS CONTACTED

~LI

n~~

¹J. Allard, Maintenance Superintendent

¹M. Ackerman, Manager Nuclear Licensing

¹R. Anderson,

¹G. Arent, Operations Procedure Supervisor

¹P. Barrett, Director Performance Assurance

¹A. Blind, Site Vice President

¹K. Baker, Manager Production Engineering

¹J. Kobyra, Manager Nuclear Engineering

¹M. Finissi, Supervisor Electrical Systems

M. Horvath, Plant Performance Assurance

¹D. Hafer, Manager Plant Engineering

¹S. Hodge, Manager Work Control

¹D. Rice, Mechanical Maintenance Supervisor

¹P. Leonard, Outage Management Team

¹A. Lotfi, Performance

Engineer

¹P. McCarty, Maintenance Procedures

¹D. Morey, Chemistry Superintendent

¹J. Moran, Plant Engineering

¹D. Noble, Radiation Protection Superintendent

¹T. Postlewait, Site Engineering Support Manage

¹D. Rodriguez, Maintenance

¹P. Russell, Plant Protection Superintendent

¹J. Sampson,

Plant Manager

¹P. Schoepf, Manager Safety-Related Systems

¹M. Schwartzwalder, Plant Engineering

¹D. Seipel, Ops Training

¹L. Smart, Nuclear Licensing

¹M. Stark, Supervisor Performance Testing

¹T. Quaka, Supervisor Project Management and

¹G. Tollas, Acting Operations Superintendent

¹J. Wiebe, Manager Engineering and Analysis

¹L. Van Ginhoven, Materials Management Dept.

¹A. Verteramo, Supervisor

Reactor Engineering

¹T. Walsh, Maintenance

¹S. Wolf, Performance Assurance

¹W. Zemo, Supervisor Preventive Maintenance

Installation Services

¹Denotes those present at the February 14, 1997 exit meeting.

21

INSPECTION PROCEDURES USED

IP 375510n-site Engineering

IP 61726Surveillance

Observations

IP 62703Maintenance

Observation

IP 71707Plant Operations

IP 71750Plant Support Activities

IP 60705Refueling Activities

ITEMS OPENED and CLOSED

Qggi~n

50-315/97002-01(DRP)VIOFailure to use procedures

in hand

50-315/97002-02(DRP)VIOFailure to follow procedures step by step

50-315/97002-03(DRP)VIOFailure to follow procedure (undersized sling)

50-315/97002-04(DRP)VIOFailure to follow pr;educe (supervisor monitoring of FMEZ)

50-315/97002-05(DRP)VIOFailure to follow procedure

(FMEZ work practices)

50-315/97002-06(DRP)VIOInadequate

procedures

(Step sequence,

FMEZ practices, rigging

requirements)

50-315/97002-07(DRP)VIOFailure to follow procedure

(FME briefings)

50-315/97002-08(DRP)DEVLifting heavy loads higher than 7 feet

50-315/97002-09(DRP)NCVFailure

to adequately review changes to operations procedures

50-315/316-97002-10(DRP)NCVFailure

to have a proceoure that adequately controlled

Safety Injection pump oil level

Ghmk

50-315/97002-09(DRP)NCVFailure

to adequately review changes to operations procedures

50-315/316-97002-10(DRP)NCVFailure

to have a procedure that adequately controlled

Safety Injection pump oil level

50-315/316-94022-02(DRP)URILimiting Condition for Operation Management:

50-315/97-001(DRP)LERTechnical

Specification 3.0.3 Entered On Loss of Four Loop

Injection Capability Due to Incorrect Procedural Guidance.

22

50-315/96-004(DRP)LERIVlain Generator Trip on Main transformer Sudden Overpressure

Due to Lightning Strike Causes Reactor Trip.

50-315/95014-02(DRP)NOVUnit

1 West CCP inoperable due to a miscalibrated

overcurrent relay and Unit 1 East CCP inoperable for planned maintenance.

50-315/95014-03(DRP)

NOVCalibration procedure inappropriate to the circumstance for

an overcurrent relay to the Unit 1 West CCP.

50-315/96-005(DRP)LERReactor

Protection System Actuation Results from Personnel

Error

During Calibration of Intermediate Range Nuclear Instrumentation

50-315/316-94024-02(DRP)IFIReview

of future core inspections to assess

effectiveness

of the licensee actions to prevent foreign material intrusion in the core.

50-315/316-96007-03(DRP)URIOperability

of the essential service water system with

inoperable pump discharge strainers.

23

List of Acronyms

AEO

AFW

CCP

CFR

CR

DG

DRP

EA

ESW

FMEZ

HVAC

I&C

LBLOCA

LCO

LER

MHI

MDAFWP

NFSV

NRC

OHP

OPM

PMI

PMP

PCR

PDR

QC

RHR

RG

SI

TS

VTM

Auxiliary Equipment Operator

Auxiliary Feedwater

Centrifugal Charging Pump

Code of Federal Regulations

Condition Report

Diesel Generator

Division of Reactor Projects

Enforcement Action

Essential Service Water System

Foreign Material Exclusion Zone

Heating, Ventilation, and.Air Conditioning

Instrumentation and Controls

Large Break Loss of Coolant Accident

Limiting Condition for Operation

Licensee Event Report

Maintenance Head Instruction

Motor Driven Auxiliary Feedwater Pump

New Fuel Storage Vault

Nuclear Regulatory Commission

Operations Head Procedure

Operations Department Procedure Review Manual,

Plant Manager's Instruction

Plant Manager's Procedure

Process Computer Room

Public Document Room

Quality Control

Residual Heat Removal

Regulatory Guide

Safety Injection

Technical Specification

Vendor Technical Manual

24

t