ML17312B184

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Insp Repts 50-528/96-17,50-529/96-17 & 50-530/96-17 on 961117-1228.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support
ML17312B184
Person / Time
Site: Palo Verde  
Issue date: 01/14/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17312B182 List:
References
50-528-96-17, 50-529-96-17, 50-530-96-17, NUDOCS 9701210456
Download: ML17312B184 (53)


See also: IR 05000528/1996017

Text

e

ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket Nos.:

License Nos.:

Report No.:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved By:

50-528

50-529

50-530

NPF-41

NPF-51

NPF-74

50-528/96-1 7

50-529/96-1 7

50-530/96-1 7

Arizona Public Service Company

Palo Verde'uclear Generating Station, Units 1, 2, and 3

5951 S. Wintersburg Road

Tonopah, Arizona

November 17 through December 28, 1996

K. Johnston,

Senior Resident Inspector

J. Kramer, Resident Inspector

D. Garcia, Resident Inspector

D. Carter,'esident

Inspector

D. Acker, Senior Project Engineer

G. Good, Senior Emergency Preparedness

Analyst

Dennis F. Kirsch, Chief, Reactor Projects Branch F

ATTACHMENT: Supplemental

Information

9701210456

970114

PDR

ADQCK 05000528

6

PDR

0

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EXECUTIVE SUMMARY

Palo Verde Nuclear Generating Station, Units 1, 2, and 3

NRC Inspection Report 50-528/96-17; 50-529/96-17; 50-530/96-17

~Oe rations

Although the conduct of operations was generally professional

and

safety-conscious,

inspectors identified issues in each unit involving failure to follow

procedures.

In Unit 1, known equipment problems and human performance errors

contributed to the overflow of the spray pond hypochlorite tank.

In Unit 2,

operators did not initiate a manual safety equipment status system (SESS) alarm for

inoperable emergency core cooling system

(ECCS) equipment, which was an

example of a violation of Technical Specification (TS) 6.8.1.

In Unit 3, inadequate

communications

between operations

and maintenance

during the performance of a

work activity contributed to the degraded

condition of a charging pump, which was

an example of a violation of 10 CFR Part 50, Appendix B, Criterion V

(Section 01.4).

The licensee has established

an effective program for assessing

and correcting

operator work arounds that have an impact on event response.

Although the

licensee corrected'operator

work arounds which had an impact on routine

operations,

and existing work arounds were not an undue burden to operators, their

program did not assure that all work arounds were assessed

for their cumulative

impact (Section 02.1).

The training for clearance

process changes

has been acceptable

and the changes

were properly communicated to operators.

The licensee's

plans for upcoming

training were acceptable

(Section 05.1).

Three issues were identified where the operations crew involved in a performance

weakness

or error did not promptly initiate a condition report/disposition

request

(CRDR) to assure that the problems were identified to management

in a

timely manner for their consideration

and resolution (Section 07.1).

'Maintenance

~

The licensee did not properly apply their work control process following their

~decision to install a temporary restraining device to reactor coolant pump (RCP) 2B

shaft impeller.

No written instructions were provided to the craft for installation and

the work was not adequately documented

on a clearance.

These issues

are

examples of a violation of TS 6.8.1.

The licensee's initial event evaluation was

inadequate

in that it did not recognize these weaknesses

(Section M1.3).

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The licensee identified that maintenance

personnel failed to contact operations,

as

instructed by a work order, to secure charging pump seal lubrication water.

This

was an example of a violation of 10 CFR Part 50, Appendix B, Criterion V (Section

01.4).

Maintenance

personnel did not adequately communicate with site management

the

status of emergent gas turbine generator

(GTG) issues.

As a result, site

management

was not provided the opportunity to factor these emergent issues into

planned vital equipment

outages

(Section M3.1).

~En ineerin

Workers installing a pipjng modification to the essential cooling water (EW) system

did not ensure that the modification was installed according to design

specifications, by verifying required tolerances for the distance of piping from pipe

supports.

This is an example of a violation of 10 CFR Part 50, Appendix B,

Criterion V. In addition, workers installing the piping had not had all the required

training in pipe installations (Section E1.1).

The licensee was proactive in addressing

problems with offsite power and keeping

the staff informed.

The inspectors

also concluded that the licensee's

administrative

actions were acceptable to maintain offsite power operable.

However, the

inspectors concluded that Revision 2 of the Licensee Event Report (LER) and

CRDR 9-6-0273 were incomplete, in that they did not address the root cause of the

problem (Section E8.2).

Plant Su

ort

The process for performing onshift dose assessments

was described

in the

emergency plan and implementing procedures

(Section P3,1).

~

An escort, visitor, and supervisor failed in their responsibilities to prevent an

unescorted

visitor from gaining unrestricted access to an area containing vital safety

equipment, which was a violation of TS 6.8.1.

The corrective actions performed by

the licensee and contractor were thorough (Section S4.1).

l

Re ort Details

Summer

of Plant Status

All units operated

at essentially 100 percent power for the duration of the inspection

period.

I. 0 erations

01

Conduct of Operations (71707)

01.1

S ra

Pond

H

ochlorite Tank S ill Unit 1

a.

Ins ection Sco e-

During a review of the Unit 1 unit log, the inspectors observed

an entry, on

November 14, 1996, describing an incident where the spray pond hypochlorite tank

had overflowed, spilling 'hypochlorite out of its vent and into a berm surrounding the

tank.

The inspectors discussed

the event with operations

personnel

and operations

management.

b.

Observations

and Findin s

A hypochlorite addition system was provided as part of the nonsafety-related

chemistry control for the spray ponds.

Each unit has a hypochlorite tank, two

hypochlorite addition pumps, and supply lines to each spray pond.

Hypochlorite is

provided to all three units from the water reclamation facility. A level control valve

is provided in each supply line from the water reclamation facility to control the

level in the hypochlorite tanks.

The unit log entry of 10:20 p.m. on November 14 identified that an auxiliary

operator (AO) had discovered that the hypochlorite tank was overfilling and had

shut a manual isolation valve, which was in series with the level control valve.

Operations initiated a work request to have the level control valve repaired,

The inspectors did further inspections of the system and determined the following:

~

The level control valves had a history of leaking and system operating

procedures

required that the manual isolation be kept closed except during

fill operations.

The hypochlorite tank had a high level control room annunciator.

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The licensee had not initiated a CRDR to evaluate the November 14 event.

There had been a history of both equipment problems and operator

performance

errors on the hypochlorite system.

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The inspectors discussed

these concerns with operations management

and on

December 2, a CRDR was initiated.

The shift supervisor (SS) on shift during the

spill event was contacted

during the CRDR evaluation.

He said that he had intended

for a CRDR to have been initiated but had not ensured

one was written. Further

discussion

on situations where a CRDR was not initiated in a timely manner is

.contained

in Section 07.1.

At the end of the inspection period, the licensee had not determined when the

manual isolation valve had been opened.

They did determine that some crews were

not aware of the hypochlorite operations procedure requirement to have the valve

closed except while fillingthe tank.

In addition, the licensee determined that a local level indicator was out of service

and had been since May 1996.

AOs had been using level control valve position as

an indication of tank level ~ Work on the level indicator had been canceled

based on

plans to abandon the automatic hypochlorite addition system.

This modification,

however, had not yet been implemented.

Accordingly, the inspectors considered

that the level indicator work cancellation decision was premature and not well

coordinated.

Operations management

considered the use of the level control valve

in lieu of level indication to be an operator work around that had not been

previously identified. They used it as an example to operators of the type of

problem that should be brought to management

attention to assure prompt repair.

Further discussion

on operator work arounds

is contained

in Section 02.1.

Operations reviewed annunciator printouts and determined that there had not been

a high tank level alarm.

They subsequently

determined that the alarm, which

receives its input from the level control valve controller, was not functioning.

This

condition was subsequently

repaired.

Operations discussed

this event with the crew involved and distributed

a night order

to inform other crews.

In addition, the level instrument and control room alarm

were repaired.

The licensee plans extensive modifications to the system, which

would retire the hypochlorite pumps and tank.

01.2

Control Room Observations

Unit 2

a.

Ins ection Sco

e

On November 25, Unit 2 was performing a post accident sampling system

surveillance.

The inspectors were performing a routine walk down of the control

boards and noticed an ECCS valve out of its normal position.

The inspectors

questioned

operators,

reviewed logs and observed the performance of operator

actions.

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b.

Observations

and Findin s

The inspectors, while walking down the control boards, observed the licensee

performing a post accident sampling system surveillance in accordance

with

Procedure

74ST-9SS03.

During this surveillance the Train A low pressure safety

injection pump was running on full flow recirculation to allow a sample to be taken.

While in this condition the inspectors observed valve SIA-UV-660 (the combined

miniflow recirculation valve from the ECCS pumps back to the refueling water tank)

closed.

The inspectors questioned

the SS regarding the reason that a manual SESS

alarm input was not initiated.

The SS indicated that the A train of ECCS was

declared inoperable and that a manual SESS input was not required.

The inspectors reviewed the Conduct of Shift Operations procedure which indicated

that a manual SESS alarm was required.

The inspectors discussed

this with the SS

who agreed with this conclusion.

Subsequently,

the inspectors

polled other crews

and supervisors

and found that there was not a consistent understanding

of the

requirements.

The ability to initiate a manual SESS was provided so that operators,

in response

to an event, would have a visual reminder of equipment status.

Operator action would have been required to prevent ECCS pump damage

in the

event of a safety injection actuation signal with reactor coolant system

(RCS)

pressure

above the ECCS pump discharge

pre'ssure.

The failure of the operations staff to initiate a manual SESS alarm, as required by

procedure, was an example of a violation of TS 6.8.1 (Violation 50-529/96017-01).

The licensee issued

a Night Order describing this occurrence

and stated that

operators should have inserted

a manual SESS alarm.

In addition, the licensee

initiated an instruction change request to add a step to Procedure 74ST-9SS03, to

have a manual SESS alarm input initiated when performing these sections of the

procedure.

The operations department planned to review the conduct of shift

operations procedure for possible clarification and/or improved guidance

on specific

use of the manual SESS.

The licensee did not promptly initiate a CRDR to evaluate the implications of this

occurrence.

The licensee's

program requires that a CRDR be initiated when it is

identified that personnel failed to follow a procedure.

Although, operations

otherwise took appropriate corrective action in response to this issue,

a CRDR

would have been useful in establishing performance trends.

A CRDR was

subsequently

written on December 23, recommending

the above actions.

See

Section 07.1 for further discussion of instances where operations

did not promptly

initiate a CRDR.

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01.3

Water Intrusion in Char in

Pum

B Unit 3

a.

Ins ection Sco

e

The inspectors reviewed CRDR 3-6-0197 issued on November 15, 1996, describing

the water intrusion to charging Pump B crankcase

oil during a routine preventative

maintenance

task on charging Pump

E on November 7. The inspectors

also

reviewed the evaluation performed by mechanical maintenance

engineering.

b.

Observations

and Findin s

In the past, the drain lines have become clogged, causing

a backfill of water to

flood the well (see NRC Inspection Report 50-528/95-16; 50-529/95-16;

50-530/95-16).

The accumulated

water in the well would drain directly into the

pump crankcase through drainage holes in the oil baffle packing region.

As part of

the corrective action, a preventive maintenance

task was initiated to perform a

periodic flush of the drain lines.

On November 7, 1996, a maint'enance

team performed

a routine drain line flush on

charging pump E, in accordance

with work order (WO) 0775357.

There are three

charging pumps, each with a well that drains to a common header leading to a

charging pump oil drain tank.

The well is located between the power block and the

oil crankcase.

The well drain collects both seal lubricating water leakage and oil

leakage,

and directs it to the tank for processing.

After maintenance

completed the drain line flush of charging Pump E, and had not

identified any problems,

an AO identified that it appeared that the oil level in

charging Pump B had increased and'suspected

that charging Pump B well drain had

backed up with water. The SS initiated a work request to sample the oil in the pump

crank case for possible water intrusion.

Both charging Pumps

B and

E were placed

in service.

An oil sample was drawn sometime before noon on November 8.

On November 14, the oil sample revealed 27,000 ppm water in the charging

Pump B oil. The acceptance

criteria for water in the oil was 1000 ppm.

On

November 15, the mechanical maintenance

engineer notified the control room and

charging Pump B was declared inoperable,

The oil was changed

and the pump was

returned to service.

The mechanical maintenance

engineer initiated CRDR 3-6-0197

to evaluate the event.

The inspectors reviewed the evaluation performed by the mechanical maintenance

engineer.

The following missed barriers were identified in the evaluation:

WO 0775357 had a precaution for maintenance

to contact operations to

secure seal lube if one of the pumps has excessive

seal lube leakage.

On

November 2, a work request was initiated for excessive

seal lube leakage on

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charging Pump B. The evaluation found that while operations was aware of

the condition they were not informed of the WO precaution by maintenance

and seal lube was not secured for this pump.

WO 0775357 included a step for maintenance to stand by and observe the

other two pumps to ensure that water did not back up into those drains.

Maintenance subsequently

observed that the plexiglass covers over the wells

were difficultto see through due to condensation.

The inspectors observed that it had taken eight days to receive the results of the oil

analysis and take action to change the oil in the pump.

On November 7, operations

had not informed the site shift manager or engineering of the situation and had not

documented

the event by either a log entry or a CRDR. The inspectors were

concerned that operators

had not promptly responded

with sufficient urgency in

light of the circumstances

surrounding the increased

oil level.

The Unit 3 Unit

Department Leader shared this concern and discussed it with operations personnel.

The licensee conservatively concluded. that charging Pump B was inoperable,

although it had operated satisfactorily for 8 days and showed no signs of wear.

However, during this period, they maintained the TS minimum requirement of two

operable charging pumps.

In addition, the licensee concluded that this event should

be tracked as a functional failure in accordance

with 10 CFR 50.65.

The inspectors

determined that the failure to isolate seal lube water to charging Pump B was an

example of a violation of 10 CFR Part 50, Appendix B, Criterion V, for failure to

follow work instructions (Violation 50-530/96017-02).

Although the violation was

identified by the licensee, they missed an opportunity to promptly correct the

condition.

As a result, charging Pump B was in a degraded

condition for 8 days.

01 A

Conclusions

on Conduct of 0 erations

Although the conduct of operations was generally professional

and

safety-conscious,

inspectors identified issues

in each unit involving failure to follow

procedures.

In Unit 1, known equipment problems and human performance errors

contributed to the overflow of the spray pond hypochlorite tank.

In Unit 2,

operators

did not initiate a manual SESS alarm for inoperable

ECCS equipment.

In

Unit 3, inadequate

communications

between operations

and maintenance

during the

performance of a work activity contributed to the degraded

condition of a charging

pump.

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02

Operational Status of Facilities and Equipment

02.1

0 erator Work Arounds

a 0

Ins ection Sco

e 71707

The inspectors reviewed the licensee's

methods for addressing

operator work

arounds.

In addition, the inspectors reviewed different operator aids found in the

control room and discussed

the observations with control room operators

and

licensee management.

b.

Observations

and Findin s

The inspectors found that operator work arounds did not appear to have a

significant impact on plant operators during routine operations

and would not be

expected to have a significant impact during a plant event.

The licensee had

developed

a formal Procedure

79DP-9ZZ01 which required the shift technical

advisors to perform a weekly review of plant conditions which could impact their

response to an event.

The resultant lists were submitted to operations management

and work control to assure that the condition receives priority for repair.

In

addition, the lists were reviewed by the plant review board every month.

The inspectors found that there were a number of methods used to assure that

operator work arounds, which did not impact event response,

were promptly

addressed.

The control room deficiency log (CRDL) items, which included

deficiencies with an impact on control room controls and annunciation,

were

addressed

with high priority. In addition, other conditions identified as operator

work arounds were added to the operations,

engineering,

and management

concerns list, which were routinely discussed

in the operation's morning meeting.

The inspectors performed

a review of "temporary notes" active in the Unit 3 control

room. Temporary notes, controlled in operations

Procedure 40DP-90P14, "Control

of Operator Information Aids," were defined as supplementary

information, of a

temporary nature, concerning the operation or maintenance

of plant systems,

subsystems,

or components.

At the time of the inspector's review, there were 43

active temporary notes in Unit 3. The inspectors found that a significant number

could be considered

operator work arounds

in that they represented

deficiencies

that complicated normal operation of plant equipment and were compensated

for by

operator action.

Most of these had not been addressed

in the programs used to

highlight work around conditions.

Many of the conditions listed in the temporary notes were appropriately scheduled

for repair during the next scheduled

refueling outage, to begin in late February

1997.

The remaining conditions appeared to be addressed

in the work control

process with sufficient priority. However, since the licensee had not included most

of these items in their processes

to identify operator work arounds, they had not

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provided themselves

the opportunity to assess

the cumulative impact of the

conditions on plant operators.

The inspectors

also found four notes for which the

associated

work had been completed and the condition no longer existed.

This

indicated a weakness

in the process for removing the notes.

Based on discussions with the inspectors

and independent

review, licensee

management

initiated an evaluation of their program for assessing

operator work

a rounds.

Conclusions

The licensee had established

an effective program for assessing

and correcting

operator work arounds that have an impact on event response.

Although, the

licensee corrected operator work arounds which had an impact on routine

operations,

and existing 'work arounds were not an undue burden to operators, their

program did not assure that all work arounds were assessed

for their cumulative

impact.

03

Operations Procedures

and Documentation

03.1

0 erations Shift Turnover

Ins ection Sco

e 71707

The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR) Section

18.I.C.2 and compared it to Procedure 40DP-9OP33, "Shift Turnover."

UFSAR

Section 18.I.C.2 documented

the licensee's

response

to NUREG 0737 item

requirements for shift relief and turnover procedures.

b.

Observations

and Findin s

The inspectors found that the shift turnover procedure was consistent with UFSAR

Section 18.I.C.2, with one exception.

The UFSAR included a reference to a

jumper/bypass

checklist,

Procedure 40DP-9OP33 did not have a specific check of

jumpers or bypasses.

The inspectors informed the licensee of the apparent

discrepancy.

The licensee initiated a CRDR to evaluate the guidance provided-in Procedure

40DP-90P33.

The licensee found that most jumpers and bypasses

would be

reviewed as part of other portions of the shift turnover.

For example, jumpers were

used on the plant protection system pa'rameters

during modes of operation when

aspects

of the plant protection system were not required.

These jumpers were

documented

in the technical specification component condition record and reviewed

during shift turnover.

Additionally, the licensee has periodically jumpered

malfunctioning annunciator inputs.

These jumpers have been documented

as CRDL

entries, with blue stickers placed near the annunciator window to indicate a

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discrepancy.

There was no explicit direction provided in the turnover checklist to

review CRDLs, however, reactor operators were required to perform control board

walkdowns, which includes control room annunciators.

The inspector concluded that the lack of an explicit step in the shift turnover

procedure for the review of jumpers and bypasses

was a minor deficiency and was

being appropriately addressed

through the licensee's corrective action program and

other licensee administrative control methods.

06

Operator Training and Qualification

05.1

Clearance

Process Trainin

a.

Ins ection Sco

e 71707

The inspectors reviewed the licensee's clearance process

and discussed

the training

aspects of the process with the training department personnel,

licensed operators,

and nonlicensed

operators.

b.

Observations

and Findin s

Plant operators indicated that their biggest challenge with the clearance

process

was that the program requirements were often changing.

The inspectors discussed

this concern with the clearance

process owner.

The process owner indicated that

their evaluation of the program also identified that the numerous revisions to the

clearance procedure

have caused difficulties for the operators.

As a result, only

minor word clarifications were planned for the procedure revision prior to the Unit 3

outage in February 1997.

Training department personnel indicated that all operations department personnel

were required to receive training on the clearance process during the training cycles.

The licensee performed

a clearance training session prior to the Unit 1 outage in the

fall of 1996.

However, the inspectors noted that although operators were tested on

the clearance

process early in 1996, they have not been tested on the revisions that

have since been implemented to the clearance

process.

Training department personnel indicated that previous clearance training highlighted

only the changes

in the clearance

process.

The training planned prior to the Unit 3

outage would include a comprehensive

review of the entire clearance

process to

reinforce the fundamentals

of the process

and ensure that all operators

have a clear

understanding

of the entire program, not just the recent changes.

To improve the quality of the recent clearance training, the licensee ensured that the

clearance procedure

and process owner was available to answer detailed questions

about the procedure

changes

and to provide background

as to why the changes

were performed.

In discussions

with operators,

the inspectors noted that operators

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found the training more beneficial when the system or process expert was available

to answer detailed questions

beyond the normal expected knowledge of the

instructor.

In addition, operators indicated that the overall training received on the

clearance changes

was acceptable..

C.

Conclusions

The training for clearance

process changes

has been acceptable

and the changes

were properly communicated to operators.

The licensee's

plans for upcoming

training were acceptable.

07

Quality Assurance

in Operations

07,1

CRDRs Not Prom tl

Initiated for 0 erations Issues

a.

Observations

and Findin s

Sections 01.1,-01.2, and 01.3 of this report identify a common element involving

CRDRs not being initiated in a timely manner; although CRDRs were eventually

issued.

~

Section 01.1 described

a spray pond hypochlorite overflow event in Unit 1.

In this event, where operator error and equipment problems were

contributors, the SS had delegated

CRDR initiation, but had failed to ensure

his direction was accomplished.

~

'-Section 01.2 described the failure of operators to input a manual SESS alarm

for a condition which rendered

a train of ECCS equipment inoperable.

Although the licensee initiated corrective actions such as a procedure

revision and a night order, they did not initiate a CRDR.

Section 01.3 described

an event where water inadvertently got into the

crankcase

oil of a charging pump.

In this instance, operators waited for the

results of the oil sample to initiate a CRDR, rather than at the time of the

event.

The inspectors discussed

these issues with the Director of Operations, who took

action to discuss the threshold for initiating CRDRs with all crews and was

evaluating the clarity of initiation criteria. The inspectors found that in 1996, the

licensee initiated approximately 3000 CRDRs and, overall, did not identify any

lowered sensitivity to initiating CRDRs.'owever,

the. inspectors were concerned

that these, seemingly, isolated situations may indicate a negative trend in the

thoroughness

of problem identification and resolution.

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b.

Conclusions

Three issues were identified where the operations crew involved in a performance

weakness

or error did not promptly initiate a CRDR to assure that the problems

were identified to management

in a timely manner for their consideration

and

resolution.

08

Miscellaneous Operations Issues

08.1

TS Inter retations

The inspectors conducted

a survey of the licensee's TS interpretations

and

determined that none of the documents

contained informal references to NRC

review and approval without formal NRC documentation.

The inspectors

emphasized to the licensee that any informal reference to NRC review and approval

in a TS interpretation is not recognized

by the Commission and is not an acceptable

practice.

II. Maintenance

M1

Conduct of Maintenance

M1.1

General Comments on Maintenance Activities

a.

Ins ection Sco

e 62707

The inspectors observed

all or portions of the following work activities:

WO 781258:

test K227 relay and associated

contacts for the essential

chiller (Unit 3)

~

WO 070666:

shim emergency diesel generator

(EDG) B fuel pumps for

adjustment of firing pressure

(Unit 1)

~

WO 780386:

reactor switchgear undervoltage

and short trip circuit testing

(Unit 2)

b.

Observations

and Findin s

The inspectors found the work performed under these activities to be professional

and thorough.

All work observed was performed with the work package present

and in active use.

Technicians were experienced

and knowledgeable

of their

assigned tasks and demonstrated

good communications

between work groups.

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M1.2

General Comments on Surveillance

Activities

a.

Ins ection Sco

e 61726

The inspectors observed

all or portions of the following surveillance activities:

~

43OP-3DG01:

EDG A

= ~

43ST-3CH03:

Boron Injection Flowpaths Operating

70TI-9ECO1:

Essential Chilled Water (EC) System Flow Balance

~

43ST-3EC01:

EC Valve Verification.

The inspectors found these surveillahce were performed acceptably

and as specified

by applicable procedures.

M1.3

RCP Restrainin

Device Failure - Unit 1

a e

Ins ection Sco

e

~

On October 24, 1996, while Unit 1 was in Mode 5 after the completion of refueling,

maintenance

personnel

installed a temporary device to prevent reverse rotation of

the shaft of RCP 2B. After initial RCP sweeps, the device was found wrapped

around the shaft of RCP 2B, clearly indicating that the impeller had rotated in the

reverse direction during the start/stop cycles of the other RCPs.

The inspectors

observed the damage

and the licensee's subsequent

repairs.

In addition, the

inspectors evaluated the thoroughness

and depth of the licensee's event

investigation.

b.

Observations

and Findin s

Event Descri tion

On October 22, 1996, Unit 1 was in Mode 5 on shutdown cooling and operators

were in the process of restoring the RCS for operations.

Maintenance was in the

process of testing RCP 2B motor, a refurbished motor installed to replace the

existing motor, which was scheduled

for refurbishing.

During initial uncoupled

motor testing, the motor was energized

in reverse rotation due to an error in wiring.

Although the motor antirotation device prevented the motor from turning

backwards, the motor experienced

a locked rotor condition for approximately

20 seconds.

Maintenance subsequently

performed testing on the motor to assure

it had not been damaged.

Concurrently, as part of the RCS restoration,

Operations planned to start RCPs for

short runs to sweep the air from the steam generator tubes.

However, the

inspection and testing of RCP 2B motor had delayed the coupling of this motor to

the impeller shaft.

Since the motor has the antirotation device, without the motor

coupled to the impeller shaft the impeller was free to spin in either direction.

The

I

-1 2-

licensee planned to start RCPs 1A and 2A for pump sweeps,

but was concerned

that this would cause the impeller of RCP 2B to spin in reverse with no restraint.

Mechanical maintenance

engineering was requested

to evaluate whether there was

a means to temporarily restrain the shaft.

Mechanical maintenance

engineering

recalled that, in 1986, a tool, used to move

the impeller shaft to line up the coupling to the motor, had been used to restrain an

impeller so that its motor could be uncoupled while the other three pumps were

running.

This was documented

in an engineering

evaluation request

(EER); a

technical review process

no longer used by the licensee.

On the night shift of

October 22, mechanical maintenance

installed the device to temporarily restrain the

shaft of RCP 2B.

The restraining device consisted of a U-shaped,

6 inch radius 5/8 inch thick plate,

which had three 2 inch holes fitted perpendicularly with 3 inch lengths of stainless

steel pipe.

These were designed to fit over the impeller coupling bolts.

The center

of the U had a fitting for a 48 inch length of 1/2 inch schedule 80 stainless steel

pipe.

This shaft had a hole near its end used to pass the hooks for two chain falls.

The two chain falls were directed horizontally and perpendicular to the restraint

shaft.

One chain fall was secured to a handrail and the other to scaffold used to

support shielding.

Maintenance workers installed the restraining device as an add-on to RCP 2B motor

installation WO 0756527.

No work steps or instructions were provided for the

installation of the restraining device.

In addition, the 1986 EER, used as the basis

for installing the restraining device, was not referenced

by or attached to

WO 0756527.

The only documentation

of the installation was in a work activities

sheet attached to the WO following the maintenance,

stating: "Install holdback on

upper rigid coupling, tied come-a-longs to handrail and scaffold.

Tied tool onto rigid

[coupling] with tie wraps."

A maintenance

engineer inspected

RCP 2B after both RCPs 1A and 2A had been

run.

The shaft of the restraining device was found completely wrapped around the

shaft of the RCP.

The hooks for the chain falls were still secured to the shaft of the

restraining device.

Both the scaffold and the handrail had been deformed; drawn

towards the shaft.

One of the chain fall hooks was slightly deformed.

The

licensee's subsequent

inspection of the shaft identified that only a RCP speed probe

had been damaged.

On October 24, the licensee initiated CRDR 1-6-0269 to document the inspection,

repairs, and event investigation.

The CRDR was determined by the CRDR review

committee to be "significant," requiring a root cause evaluation,

and the evaluation

was assigned to maintenance

for review.

Maintenance completed their review on

November 25.

I'

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-1 3-

In their initial CRDR evaluation, mechanical maintenance

engineering determined

that there were substantial differences in the conditions for which the 1986 EER

was initially used and its use during the Unit 1 outage.

In 1986, the device was

installed on an idle pump before the motor and impeller were decoupled.

This

ensured that the restraining device saw only a static load.

During the Unit.1

outage, the restraining device experienced

a dynamic load when other pumps were

started to sweep the generators.

Additionally, the licensee postulated that as air

was swept from the steam generators,

there could have been

a substantial

load

change at the restraining device as the voids were collapsed.

Nuclear Assurance performed an evaluation, requested

by the maintenance

department,

in accordance

with their "Human Performance

Evaluation System"

program.

The evaluation found that personnel

did not use documents that fully

evaluated current plant conditions when determining actions to be taken to restrain

an RCP shaft from reverse rotation and that no policy was provided for guidance to

personnel evaluating

a course of action using engineering information evaluated for

similar, yet different conditions.

0

Mechanical maintenance

proposed corrective actions to determine the appropriate

method for using previous engineering information for similar, yet different,

conditions and to develop the basis necessary for installing the modification in the

Fall, 1997, Unit 2 refueling outage.

Review of Initial Cause Evaluation

The inspectors reviewed the licensee's evaluation and found that, while it had

addressed

significant aspects

regarding the lack of technical rigor, it failed to

address the failure to implement processes

and procedures for the control and

documentation

of work activities.

The licensee's evaluation included a discussion of the use of the WO process

and

concluded that no work instructions were necessary

since the restraining device use

was within the skill of the qualified worker. The inspectors found that the

installation of the restraining device was not within the skill of the qualified worker

in that there were several aspects of the job which required technical and

procedural guidance.

For example, the craft chose to restrain the device with

rigging equipment secured to a handrail and to scaffolding.

The inspectors noted

that maintenance

had not referenced the licensee's

procedural requirements

on the

use of scaffolding to support rigging equipment.

Additionally, the use of the

handrail should have required

a specific evaluation considering the load at the

handrail, since handrails at Palo Verde have been typically designed to support

a

200 pounds force.

The evaluation stated that RCP 2B was tagged out under Clearance 96-01325 at

the time the restraining device was installed.

The inspectors found that this was

not accurate.

The motor had been restored from this clearance

on October 21 to

-14-

allow the uncoupled motor run and was not tagged out on this clearance

until

October 24. Additionally, Clearance 96-01325, the clearance initially specified for

WO 0756527, applied only to the motor for RCP 2B. To provide adequate

protection to the workers installing the restraining device, it would have been

necessary to provide a clearance that tagged out all four RCP motors.

The

licensee's work control procedure,

Procedure

30DP-9WP02, required that an

expansion of the clearance

boundary was an expansion of work scope requiring a

WO amendment

by the job planner.

The inspectors noted that the event evaluation had considered the use of the

restraining device as similar to the use of a maintenance

tool on equipment that was

out of service.

The inspectors found-that considering the restraining device as a

tool was an error in judgement and a significant causal factor in the event.

The

restraining device was installed to protect the RCP seals in that the licensee did not

have an evaluation of the impact on the seals of the shaft rotating in reverse.

The

RCP seals were in service as an RCS boundary when the restraining device was

installed.

Therefore, the restraining device was relied upon to perform a function to

protect the RCP during a routine startup procedure

and should have received

reviews consistent with a procedure

change or system modification.

Res

onse to Ins ector Issues

The licensee reperformed the evaluation of the event following discussions, with the

inspectors.

They determined that the WO was incomplete, deficient in detail and

direction, and not in compliance with the work control program.

Additionally, they

determined that the addition of the restraining device constituted

a change

in work

scope'requiring

a WO amendment

in accordance

with Appen'dix 0 of

Procedure 30DP-9WP02.

This is an example of a violation of TS 6.8.1 for failure to

follow procedure (50-528/96017-01)

~

The licensee determined that installing the restraining device had been adequately

covered by a Clearance 9-6-01734, which tagged out all four RCP motors.

The

inspectors

agreed that this clearance

provided adequate

protection; however, the

inspectors found that WO 0756527 was never listed as an active job on this

clearance.

The mechanical maintenance

work group supervisor noted that although

this WO was not listed on the clearance,

another job under his responsibility was.

He stated that he verified all four pumps were tagged out of service prior to

allowing his crew to install the device.

However, the clearance control procedure

required that the specific WO associated

with a clearance

be listed on that

clearance.

This assures that all work listed on the clearance

is completed before

the clearance

is removed.

This is an example of a violation of TS 6.8.1 for failure

to follow procedure (50-528/96017-01).

-1 5-

C.

Conclusion

The licensee did not apply their work control process following their decision to

install a temporary restraining device to RCP 2B shaft impeller.

No written

instructions were provided to the craft for installation and the work was not

adequately documented

on a clearance.

The licensee's

initial event evaluation was

inadequate

in that it did not recognize these weaknesses.

M3

Maintenance Procedures

and Documentation

M3.1

Assessin

the Im act of Ern'er ent GTG Maintenance

on Planned Maintenance

Activities

a.

lns ection Sco

e 62707

Beginning on December 3, 1996, the licensee experienced

several start attempt

failures of the two GTGs.

The inspectors observed maintenance

activities and

reviewed the application of maintenance

rule requirements for assessing

the risk of

the resultant emergent work on planned maintenance

activities.

b.

Observations

and Findin s

Palo Verde has two GTGs for coping with loss of offsite power during a station

blackout event.

These generators

are installed in parallel, and can be connected to

~

each of the three units at Palo Verde.

The licensee considered

only one of these

GTGs as required to cope with a station blackout event.

The GTGs are not included

in plant TS and their availability has been controlled through administrative

procedures.

Although the GTGs are maintained by site maintenance,

they are

outside the protected

area and are operated

by the site water reclamation facility

staff.

Since the installation testing of the GTGs, the licensee has had problems with

starting the GTGs during peak high and low temperatures,

and has included the

generators

in 10 CFR 50.65 Maintenance

Rule Category (a)1.

The licensee had

performed some adjustments

on GTG

1 during warmer weather and had not

established

confidence that it would start with cooler weather.

However, the

licensee had previously established

some confidence that the low temperature start

issue had been addressed

for GTG 2.

On the morning of December 3, 1996, the licensee initiated testing of GTG

1 as

part of their Maintenance

Rule Category (a)1 action plan to test the GTG

1 with

lowering ambient temperatures

(temperatures

around 35'F).

GTG

1 failed to start

on four successive

start attempts.

Later in the day, following adjustments,

GTG

1

was started successfully.

However, since ambient temperatures

had increased,

maintenance

personnel

had not established

confidence that the adjustments

enabled

the GTG to start during lower temperatures.

Additionally, based

on findings with

(

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-1 6-

GTG 1, maintenance

personnel

developed

concerns that GTG 2 may not start.

They planned to test both GTGs the following morning as temperatures

dropped.

At 5 a.m. on December 4, 1996, the licensee initiated a planned outage of Train A

EDG and associated

train components

in Unit 1. At 7 a.m. on December 4, 1996,

the licensee initiated a planned outage of the turbine-driven auxiliary feedwater

(AFA) pump, and the A train high pressure safety injection (HPSI) pump in Unit 3.

At around the same time, the licensee attempted to start both GTGs and both failed

to start on the first attempt.

Both GTGs did start on a second attempt.

The

licensee subsequently

considered

GTG

1 unavailable,

and continued

troubleshooting,

and GTG 2 available, based on its ability to start within 3 start

attempts.

Palo Verde has a risk matrix, generated,

in part, to comply with the Maintenance

Rule, to assist operations

and maintenance

personnel

in determining the risk of

various components

being out of service.

The inspectors determined that site

management

was not fully aware of the concerns maintenance

had developed

on

December 3 regarding the ability of both GTGs to start during cold weather.

As a

result, they did not consider the GTG availability impact on the plan with the

December 4 outages of the Unit 1 EDG and the Unit 3 AFA and HPSI pumps.

The licensee's

risk matrix, which rates activities on a low, medium, and elevated

risk scale, identified that both the EDG and AFA/HPSI outages were medium risk.

The addition of a GTG outage would not have increased the risk out of the medium

range.

However, the matrix notes stated that a GTG outage and an EDG outage

should not be performed concurrently.

The shift manager recognized that had he been aware of maintenance

concerns

regarding the performance of GTG 2 in cold weather, further discussion would have

taken place on the need for testing GTG 2 and the planned outages

in Units

1 and

3.

The license issued an operations night order for unit operations to maintain status of

the gas turbine availability. Additionally, the licensee initiated a CRDR for this risk

management

issue.

Conclusions

Maintenance

personnel

did not adequately communicate with site management

the

status of emergent GTG issues.

As a result, site management

was unable to factor

these emergent issues into planned vital equipment outages.

lt

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-1 7-

M8

Miscellaneous Maintenance Issues

M8.1

Closed

LER 528 95011-01:

inadequate

main steam isolation valve and feed water

isolation valve operating air inservice tests in all three units.

The licensee noted

that they had not considered

all appropriate uncertainties

in testing the subject

valves, therefore, the existing tests did not insure operability in violation of

TS 4.0.5.

The licensee developed

interim procedures to maintain operability,

updated their test procedures,

and satisfactorily tested the valves.

The inspectors

verified the acceptability of the interim procedures

and verified the completed test

data for Unit 1 valves, including procedure

adequacy.

The inspectors concluded

that the licensee's corrective actions were adequate.

This licensee-identified

issue is being treated as a noncited violation consistent with

Section Vll of the NRC Enforcement Polic

(50-528;529;530/96017-03).

III. En ineerin

E1

Conduct of Engineering

E1..1

Modifications to the EW S stem Su

I

to the Essential Chillers

a.

Ins ection Sco

e 37551 and 92903

During this inspection period, the licensee completed portions of a modification to

the EW return from the EC condensers

in both trains of each unit. The inspectors

observed portions of the field work in each unit, reviewed the design modification,

and discussed

the modification with the craft, maintenance,

and design engineering

personnel.

b.

Observations

and Findin s

The modification was designed to reduce the overcooling of the EC condensers

in

the winter when low EW temperatures

and low system loading have resulted in low

condenser

pressure.

This has caused refrigerant to migrate from the evaporator to

the condenser

and has resulted in low refrigerant level trips (see NRC Inspection

Report 50-528/95-25; 529/95-25; 530/95-25),

To reduce overcooling, the licensee

installed a pressure control valve in the EW return line that modulated closed with

decreasing

condenser

pressures.

A manual bypass valve was placed in parallel with

the pressure

control valve to address worst case design basis conditions involving

EW supply to the spent fuel pool and EC heat loads.

The inspectors,

based

on interviews in the field, had questions

regarding the

familiarity of the installation work group supervisors with the piping design

specification as it applied to the piping installation and cold spring requirements.

The inspectors discussed

the concern with licensee management.

Nuclear

-1 8-

Assurance reviewed training requirements

and the qualifications of the contract

personnel

performing the work. They determined that the work group supervisor

had not completed

all the required classroom training in pipe installation.

The licensee performed

a review of the work group supervisor's

experience

at Palo

Verde and other nuclear facilities and determined that he had experience

in the work

performed.

They also determined that his work on the EW modification had

adequate

engineering

and Nuclear Assurance oversight.

The licensee initiated a

CRDR to evaluate this issue.

The pressure control valve was the final component installed to complete the piping

portion of the EW modification and it was installed using bolted flange connections.

Downstream of the pressure control valve was an elbow, followed by a box style

hanger.

Upstream of the pressure control valve was a piping tee with one end

going to the bypass valve, and the other end going to a flanged connection to the

chiller.

Th'e inspectors observed that as the piping modification was completed in Units 2

and 3, the piping passing through the box style hanger was in contact with the

hanger on the pressure control valve side.

The work instructions for the

modification referenced Specification 13-PN-204 for installation details.

This

specification allowed piping to be in contact with the hanger,

as long as the piping

was free to slide.

The inspectors were concerned that, had the piping been in

contact with the hanger on the pressure control valve side prior to bolting'the valve

in place, the act of bolting the flanges would have resulted in cold spring of the

piping and stressing both the hanger and the piping.

Specification 13-PN-204

stated'that

all situations involving cold spring should be evaluated

by engineering.

The inspectors discussed

this concern with the design engineer, who subsequently

initiated CRDR 9-6-1371 to evaluate this concern.

Design engineering

estimated

that bolting the flanges would provide roughly 0.1 inches of spring.

Engineering

calculated the additional stress that would be added to the hanger, the additional

stress added to the piping, and any impact this condition had on the response

to a

seismic event and to expected thermal expansion

and contraction.

Engineering

determined that the initial stresses

on the hanger and the piping corresponded

to

roughly half of the code allowable initial stress limits.

In addition, calculations

showed the system tended, with minor exceptions, to respond better to seismic and

thermal movement.

The inspectors

asked if this condition had been caused

by weaknesses

in either the

work instructions or the specification, or had it been caused by weaknesses

in their

application.

The licensee determined that both the work instruction, which included

a step requiring the verification that the hanger was free-to-slide, and the

specification, which included specific verification methods, were adequate.

They

also determined that all six trains were in similar configurations with the pipe in

contract with the hanger and no means available to determine if the pipe was free

t

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-1 9-

to slide.

The failure to perform the verifications required in the specification was an

example of failure to implement work instructions in violation of 10 CFR Part 50,

Appendix B, Criterion V (Violation 50-528/96017-02; 50-529/96017-02;

50-530/9601 7-02).

c.

Conclusion

Workers installing a piping modification to the EW system did not ensure that the

modification was installed according to design specifications and may have added

unanticipated

stress to the piping and hanger.

In addition, workers installing the

piping had not had all requisite training in pipe installations.

E5

Engineering Staff Training and Qualification

E5.1

Trainin

and Qualification of Workers Performin

EW Modifications

Section E1.1 discussed

weaknesses

in the training and qualification of workers

performing the installation of EW modifications.

ES

Miscellaneous Engineering Issues

E8.1

Closed

Violation 50-529 94031-03: two examples of inadequate

corrective

actions.

The violation discussed

failure of the licensee to take adequate

corrective

actions for degraded

battery cells and for spurious tripping of the Train N AFA

pump.

As part of their corrective actions the licensee replaced the degraded

battery cells,

corrected the cause of the spurious tripping of the Train N AFA pump, and improved

the administrative directions for evaluation of technical problems.

The inspectors

reviewed the licensee's

program for monitoring individual battery cells and

determined that the licensee was trending individual cell data in sufficient detail to

predict individual cell degradation.

This violation had highlighted weaknesses

in the licensee's corrective action

program to resolve longstanding

equipment deficiencies.

The inspectors reviewed

the administrative changes

made by the licensee associated

with the CRDR program

and determined that the administrative directions had been improved in the area of

facilitating development of adequate

corrective actions.

Based on this review, the

inspectors concluded that the licensee had adequately

resolved this item.

-20-

E8.2

0 en

LER 50-528 93011-02:

potential safety-related

equipment problems due to

degraded

grid voltage.

a a

~Back round

Revision 2 of this LER, dated June 17, 1996, added two new potential conditions,

Scenarios

3 and 4, which could lead to double sequencing

of safety-related

equipment during a loss of coolant accident, concurrent with low offsite (grid)

voltages and described administrative controls that were put in place to maintain

operability of offsite power and safety-related

equipment.

In addition, subsequent

to issue of the LER, the licensee identified a potential

unreviewed safety question associated

with their offsite power arrangement,

A

new power line, not associated

with Palo Verde, had recently been installed which

crossed over two (Westwing) of the five total offsite power lines providing offsite

power to Palo Verde, although the UFSAR addresses

four offsite power sources.

Thus, a single failure of the new line, dropping across the two existing Westwing

lines could cause loss of these two lines to Palo Verde.

The licensee's

existing

analysis considered

the loss of only a single line, of the total four provided, reducing

the offsite sources to three,

a condition equivalent to loss of both Westwing lines.

On July 11, 1996, members of the licensee's staff met with the NRC staff to

provide an update of the degraded

voltage and double sequencing

issue identified

by Palo Verde.

On August 2, 1996, the licensee responded to questions raised by

the NRC in a docketed memorandum to the staff.

On September

18, 1996, members of the licensee's staff again met with the NRC

staff in Rockville, Maryland, to provide a second update for the NRC staff. A

summary of this meeting was issued on November 13, 1996.

b.

Ins ection Sco

e

The inspectors reviewed Revision 2 of the LER, the results of information Palo

Verde supplied the staff associated

with the July 11 and September

18 meetings,

the current status of Palo Verde actions associated

with offsite power, and selected

technical documents which supported

Palo Verde determinations that their offsite

power remained operable with existing administrative controls.

Observations

and Findin s

Palo Verde studies and calculations concluded that offsite power to the site would

remain operable

as long as the grid voltage level was maintained at 100 percent or

above.

This conclusion was based

on computer modeling of the grid from a model

provided by the Western States Coordinating Council (WSCC).

The licensee had

not done any software validation of the model

~ The Palo Verde offsite power

operability study did not include any uncertainty for the modeling and inquired

-21-

whether the model had been validated by modeling any of the recent grid

disturbances

in the western area and comparing the model results to what actually

happened.

The licensee found one study which modeled

a local disturbance for

short term dynamic response.

The model results were similar to the actual event,

but voltage levels after the disturbance

were not included.

The first new potential problem, added by Revision 2 of the LER, called Scenario 3,

concerned

potential uncontrolled AFA flow to intact and/or ruptured steam

generators

during a secondary

line break.

The scenario assumed

double sequencing

and no operator intervention.

The licensee administrative controls to block transfer

of nonsafety busses

adequately

addressed

this scenario.

The second new potential problem, added by Revision 2 of the LER, called Scenario

4, concerned

operators potentially overloading

a startup transformer when one of

the three transformers was out of service.

Scenario 4 appeared to be the same

technical issue identified by the NRC in NRC inspection Report 50-528/90-42;

50'-529/90-42; 50-530/90-42.

The licensee's

response to this finding was to

establish administrative controls to preclude potentially overloading the startup

transformers.

The inspectors questioned the licensee concerning the difference

between Scenario 4 and the previous NRC finding and found that they were the

same and the licensee had failed to maintain their administrative controls.

Licensee

engineering

personnel

had noted that licensee procedures

could allow overloading

the startup transformers

in March 1996.and

had initiated CRDR 9-6-0273.

A

preliminary review of CRDR 9-6-0273 indicated that the CRDR was closed without

addressing

several issues, including the root cause of how the licensee lost

administrative control of the potential for overloading the startup transformers.

Revision 2 of the LER appeared to be incomplete, in that it did not indicate that the

root cause of Scenario 4 was recent failure of the licensee to maintain committed

administrative controls, in lieu of licensee engineering identifying a new problem

with the existing design.

The inspectors

also considered that CRDR 9-6-0273

appeared to have been closed without adequately

addressing

the issue.

The inspectors noted that NRC inspection Report 50-528/96-16;529/96-16;

530/96-16, Section E8.3, identified that LER 528/95007, Revision 1, was

incomplete.

Other weaknesses

in the licensee's

evaluation of CRDRs are discussed

in Section M1.3

The inspectors discussed

this consideration with the licensee.

The licensee initiated

CRDR 961355 to evaluate the acceptability of the closing of CRDR 9-6-0273.

This

new CRDR indicated that the licensee planned to issue Revision 3 to the LER to

address the root cause inconsistency noted by the inspectors.

The inspectors determined that the licensee administrative controls to block transfer

of nonsafety busses

adequately

addressed

Scenario 4.

-22-

This LER will remain open pending:

Submittal of the information concerning

loss of the two Westwing lines to

the staff and staff approval.

Inspector review of the conservatism

used by Palo Verde to offset the

unknown accuracy of the WSCC modeling program.

Inspector review of offsite power studies which include lines out of service.

Inspector review of the results of the licensee's investigation of the

adequacy of LER Scenario 4 and CRDR 9-6-0273 (CRDR 9-6-1355).

d.

Conclusions

The licensee was proactive in addressing

problems with offsite power and keeping

the staff informed.

The inspectors

also concluded that the licensee administrative

actions were acceptable to maintain offsite power operable.

However, the

inspectors concluded that Revision 2 of the LER and CRDR 9-6-0273 were

incomplete,

in that they did not address the root cause of the problem.

IV. Plant Su

ort

P3

Emergency Preparedness

Procedures

and Documentation

P3.1

Licensee Onshift Dose Assessment

Ca abilities

TI 2515 134

a.

Ins ection Sco

e

Using Temporary Instruction 2515/134, the inspectors gathered

information

regarding:

~

Dose assessment

commitments in the emergency

plan

~

Onshift dose assessment

emergency

plan implementing procedure

~

Onshift dose assessment

training

b.

Observations

and Findin

s

On December 16, 1996, the inspectors conducted

an in-office review of the

emergency plan and implementing procedures to obtain the information requested

by the temporary instruction.

The inspectors conducted

a telephone interview with

the licensee on December 17, 1996, to verify the results of the review.

Based on

the documentation

review and the licensee interview, the inspectors determined

that the licensee had the capability to perform onshift dose assessments

using

V,

-23-

real-time effluent monitor and meteorological data and that the process was

described

in the emergency

plan and implementing procedures.

C.

Conclusion

The process for performing onshift dose assessments

was described

in the

emergency

plan and implementing procedures.

S4

Security and Safeguards Staff Knowledge and Performance

S4.1

Loss of Visitor Control

Unit 2

80

Ins ection Sco

e 71750

During a routine tour of the EDG room, the inspectors observed

a contract

employee, performing escort duties, not maintaining control of a visitor. The

inspectors discussed the observation with the supervisor present at the scene, the

licensee, and contractor management.

b.

Observations

and Findin s

On November 22, the inspectors observed

a contract employee cleaning the floor in

the Unit 2 Train A EDG control cabinet room.

Although the employee possessed

an

escort badge, the inspectors did not observe

a visitor. The escort's supervisor,

also

present in the room,

indicated that the visitor was in the adjacent engine room

paintirig the floor. The supervisor subsequently

obtained possession

of the escort

badge and gave it to another employee working in the vicinity of the visitor. The

inspectors determined that the visitor had been out of visual sight of the escort in

the control cabinet room.

Procedure

20AC-OSK04, Revision 17, "Protected/Vital Area Personnel

Access

Control,",step 3.7.5.4 required that escorts maintain positive control of visitors at

all times while in the protected/vital area, and step 3.7.6.2 required that visitors

shall remain in the line of sight and in positive control of their escort.

The failure of

the employees to follow procedure

and maintain positive control of the visitor within

a vital area was a violation of TS 6.8.1 for failure to follow procedures

(50-529/9601 7-04).

The inspectors questioned the escort about the duties and responsibilities of an

escort.

The escort indicated that there was only one exit out of the EDG room and

that the visitor could not get out of the EDG room without going past the escort.

The inspectors noted that the escort failed to realize that the visitor was already in a

vital area; in addition, there was another exit out of the room.

The inspectors

also

noted that the supervisor knew the location of both the escort and visitor and had

allowed them to become separated.

-24-

The inspectors informed security of the event.

Security personnel

responded

to the

scene, obtained personnel statements,

and reminded the personnel

involved of their

escort responsibilities.

Security contacted the SS and the SS dispatched

an

operator to verify the status of the EDG. The operator identified no discrepancies

to

the EDG. Another badged individual, who had been working with the visitor in the

EDG room; subsequently

stated that the visitor had been within his sight for the

duration.

The inspectors discussed

the event with the contract project manager.

The project

manager indicated that on the day of the event, the contractor stopped

all work in

the EDG room and performed

a training session

on escort duties.

In addition,

separate

counseling was performed for the escort and visitor. The following day,

the contractor performed prejob briefings to discuss the duties of an escort.

The

project manager indicated that the contractor planned to develop

a computer based

interactive training program on escort responsibilities by early 1997.

The inspectors discussed

the event with the Director of Emergency Services.

The

director planned to issue news flashes and flyers to reinforce the requirement of

escort responsibilities,

and that a security department

leader would meet with the

new classes of employees

and explain security requirements.

The inspectors found

these actions to be thorough.

c.

Conclusions

An escort, visitor, and supervisor failed in their responsibilities to prevent an

unescorted

visitor from gaining unrestricted access to an area containing vital safety

equipment.

The corrective actions performed by the licensee and contractor were

thorough.

V. Mana ement Meetin s

X1

Exit Meeting Summary

The inspectors presented

the inspection results to members of licensee management

at the

conclusion of the inspection on December 30, 1996.

The licensee acknowledged

the

findings presented.

The inspectors asked:the

licensee whether any material examined during the inspection

should be considered

proprietary.

No proprietary information was identified.

ATTACHMENT 1

PARTIAL LIST OF PERSONS CONTACTED

Licensee

R. Flood, Department Leader, System Engineering

R. Fullmer, Director, Nuclear Assurance

J. Hesser, Director, Design Engineering

W. Ide, Vice President,

Engineering

D. Kanitz, Engineer, Nuclear Regulatory Affairs

A. Krainik, Department Leader, Nuclear Regulatory Affairs

D. Mauldin, Director, Maintenance

R. Myrick, Department Leader, Mechanical Maintenance

G. Overbeck, Vice President,

Nuclear Operations

M. Powell, Department Leader, Civil/Mechanical Design Engineering

C. Seaman,

Director, Emergency Services

G. Shanker, Department Leader', Nuclear Assurance

Maintenance

D. Smith, Director, Operations

J. Taylor, Department Leader, Operations

M. Windsor, Section Leader, IVlechanical Maintenance

Engineering

C. Zell, Department Leader, Operations

t

Others

L. Gourley, Project Manager, Fluor Daniel

INSPECTION PROCEDURES USED

37551

61726

62707

71707

71750

92901

92902

92903

TI 2515/134

Onsite Engineering

Surveillance Observations

Maintenance

Observations

Plant Operations

Plant Support Activities

Followup- Plant Operations

Followup-Maintenance

Followup-Engineering

Licensee Onsite Dose Assessment

Capabilities

0 g

e'

'e

Sl

J

on

e

'J

-2-

I

ITEMS OPENED

CLOSED AND DISCUSSED

~Oened

50-528;

50-529/9601 6-01

50-528; 50-529;

50-530/9601 7-02

VIO

VIO

failure to.follow procedures

by operators with three

different examples

J

failure to follow written procedures

in the maintenance

area

with two different examples

50-528; 50-529;

50-530/9601 7-03

NCV

50-529/9601 7-04

VI0

inadequate

tests of main steam and feedwater isolation

valve air operating systems did not insure operability in

violation of TS 4.0.5

failure to follow security procedure visitor control

requirements

Closed

50-528/95011-01

LER

inadequate

main steam and feedwater isolation valve

operating air inservice tests in all three units

50-529/94031-03

Discussed

50-528/9301 1-02

VIO

two examples of inadequate

corrective actions

LER

Potential safety-related

equipment problems due to

degraded

grid voltage

V,

~

g45N,~ ~

-3-

LIST OF ACRONYMS USED

AFA

AO

CRDR

CRDL

EC

auxiliary feedwater

auxiliary operator

condition report/disposition request

control room deficiency log

essential chilled water

ECCS

EDG

EER

EW

GE

GTGs

HPSI

LER

RCPs

RCS

SS

SESS

TS

UFSAR

WO

WSCC

emergency core cooling system

emergency diesel generator

engineering

evaluation request

essential cooling water

General Electric

gas turbine generators

high pressure safety injection

licensee event report

reactor coolant pumps

reactor coolant system

shift supervisor

safety equipment status system

Technical Specifications

Updated Final Safety Analysis Report

work order

Western States Coordinating Council

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