ML17312A497
| ML17312A497 | |
| Person / Time | |
|---|---|
| Site: | Palo Verde |
| Issue date: | 01/10/1996 |
| From: | Kirsch D NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV) |
| To: | |
| Shared Package | |
| ML17312A495 | List: |
| References | |
| 50-528-95-21, 50-529-95-21, 50-530-95-21, NUDOCS 9601190477 | |
| Download: ML17312A497 (32) | |
See also: IR 05000528/1995021
Text
ENCLOSURE
1
U.S.
NUCLEAR REGULATORY COMMISSION
REGION IV
Inspection
Report:
50-528/95-21
50-529/95-21
50-530/95-21
Licenses:
NPF-51
Licensee:
Arizona Public Service
Company
P.O.
Box 53999
Phoenix,
Facility Name:
Palo Verde Nuclear Generating Station,
Units 1,
2,
and
3
Inspection At:
Palo Verde Nuclear. Generating Station,
Units 1,
2,
and
3
Inspection
Conducted:
November
5 through
December
16,
1995
Inspectors:
K. Johnston,
Senior Resident
Inspector
D. Garcia,
Resident
Inspector
J.
Kramer,
Resident
Inspector
. D. Acker, Senior Project Engineer
'Approved:
irsc
,
C se
,
eactor
roJects
rane
ate
Ins ection
Summar
Areas
Ins ected
Units
1
2
and
3
Routine,
announced
inspection 'of onsite
response
to plant events,
operational
safety,
maintenance
and surveillance
activities, onsite engineering,
plant support activities,
and followup items.
Results
Units
1
2
and
3
0 erations
Operator
response
to
a Unit
1 loss of load transient
and subsequent
reactor trip and main steam isolation was adequate.
However, operations
management
plans to review expectations
and guidance to operators
concerning taking manual control of automatic
systems
and
when to
initiate manual
(Section
2. I)
t
~
An auxiliary operator,
attempting to close
a pneumatically operated
condenser
vacuum breaker,
did not meet licensee
expectations
in that
he
'P60i i'F0477 960i i0
ADOCK 05000528
8
did not inform the control
room prior to taking actions,
nor had
he
previously identified an apparent deficient condition (Section 2.2).
Operators
performed Unit 3 midloop operations
in a controlled manner.
The use of a designated
midloop operating
crew was
seen
as
a strength
(Section 4.1).
~
The licensee's
evaluation of previous reactor startup reactivity control
weaknesses
was found to be
an indepth
and critical evaluation.
The
training developed to address
these
weaknesses
was creative
and thorough
(Section 4.4).
Maintenance
Surveillance
~
Although the Unit 2 Train
B emergency
diesel
generator
experienced
another non-safety related trip during
a surveillance test, it was noted
that the team established
to investigate
these
probl'ems
had
made
considerable
progress
and
had developed
an indepth understanding
of the
systems
which were causing
these trips (Section
5. 1).
Mechanical
maintenance
efforts to investigate
and repair the Unit 2
Train A charging
pump were
seen
as
a strength
(Section 5.2).
Mechanical
maintenance
efforts to troubleshoot
and repair the Unit 3
turbine driven'uxiliary feedwater
pump were well planned,
well
controlled,
and provided with appropriate
management
oversight
(Section 5.4).
The inservice test procedure for the containment
spray
pump had
instrumentation correction factors which were in error.
Subsequent
licensee
investigation determined that several
other inservice tests
had
less significant correction factor errors
(Section
6. 1).
En ineerin
and Technical
Su
ort
Problems
experienced
with refrigerant levels in the essential
chillers
in Units
1 and
3 did not appear to be well understood.
It did not
appear that clear
and consistent
guidance
had
been provided for both
refrigerant levels
and oil levels during cold weather operation of the
chillers (Section 5.5).
Management
made
a conservative
decision to perform an on-line test of a
Unit 2 letdown isolation valve to resolve remaining operability concerns
(Section 9.1).
The licensee identified that data
communicated
by maintenance
technicians
to engineers
performing
an operability determination for
letdown isolation capabilities
was in error in a non-conservative
direction (Section
9. 1).
Plant
Su
ort
~
The inspectors
observed that the Unit 3
licensee's
containment restart closeout
has
been
observed
in the past,
although
was not sufficient to render
any safety
(Section 4.2).
Summar
of Ins ection Findin s:
containment,
following the
inspection,
was not as clean
as
the size
and
amount of debris
systems
~
One unresolved
item (529/9521-01)
was
open concerning
problems
experienced
with the essential
chillers in Unit
1 and Unit 3
(Section 5.5).
One unresolved
item (528/9521-02)
was
opened
concerning
a condition
potentially outside the design basis
which could lead to the turbine
driven
AFW pump tripping on overspeeed
(Section 7.2)':
One non-cited violation was identified concerning
inadequate
inservice
testing procedures
for the Unit 3 containment
spray
pump (Section
6. I).
One non-cited violation was identified concerning the failure of
operators
to follow procedures
when removing the Unit
1 Train
N
pump from service
(Section
8. 1).
This closed
Unresolved
Item 528/9514-02.
~
Unresolved
item 528/9431-01
was reviewed
and remains
open
(Section
9. 1).
~
Licensee
Event Reports
528/93-011,
Revision
1 and 528/95-001,
Revision
0
were closed
(Section
10. 1).
Attachments:
1.
Persons
Contacted
and Exit Meeting
2.
List of Acronyms
1
PLANT STATUS
1.1
Unit
1
Unit
1 began the inspection period at
100 percent
power.
On November 26,
1995,
a reactor trip occurred following a loss of condenser
vacuum (Section 2).
The
unit was returned to 100 percent
power operation
on December
1.
On December
7, reactor
power was reduced to 40 percent to identify and isolate
a potential circulating water leak into Condenser
Hotwell
1C.
On December
9,
a reactor trip occurred after
a startup transformer tripped (Section 3).
On
December
13, the unit was returned to 100 percent
power operation
and operated
at this power for the remainder of the inspection period.
1.2
Unit 2
Unit 2 began the inspection period at
100 percent
power arid operated
at this
power for the remainder of the period.
1.3
Unit 3
Unit 3 began
the inspection period with the core offloaded to the spent fuel
pool.
On November 6, the unit began the core reload
and entered
Mode 6.
On
November
28 the reactor
was taken critical.
On November 30, the unit ended
a
site record
47 day refueling outage
and synchronized
to the grid.
The unit
ended
the inspection
period at
100 percent
power.
2
REACTOR TRIP FOLLOWING A LOSS
OF CONDENSER
VACUUM UNIT 1
(93702,
71707)
On November 26, Unit
1 experienced
a main turbine trip from 100 percent
power
when
a condenser
vacuum breaker failed open causing
a low vacuum turbine trip.
Following a seven minute loss of load transient,
a high steam generator level
condition initiated
a reactor trip and
a main steam isolation signal.
During
the initial loss of load transient,
steam
bypass control valves to the
condenser
were only available for the first 13 seconds,
due to their closure
by condenser
vacuum protection logic.
After closure of the steam
bypass
control valves to the condenser,
secondary
pressure
increased
and three main
steam safety valves lifted.
One of the main steam safety valves remained
open
following the reactor trip and subsequently
reopened
at'pproximately five
percent
below its set pressure.
The inspector's
review of the licensed
operator
response
to the transient is discussed
in Section
2. 1,
During the event
and during subsequent
post-trip recovery,
the unit
experienced
several
equipment
problems.
These
included the following:
~
The condenser
vacuum breaker to the
C hotwell spuriously
opened
(Section 2.2).
Although Hain Steam Safety Valve 561
opened within one percent of its
set pressure, it remained
open for approximately ll minutes
and reset at
a pressure
below its expected
blowdown range.
It subsequently
reopened
at
a pressure
approximately five percent
below its setpoint
(Section 5.3).
~
Wh'en operators
attempted
to start the Train
(AFW)
pump, it tripped
on low suction pressure.
~
Unrelated to the trip, the Train
8 essential
chiller tripped
on low
refrigerant temperature
(Section 5.5).
The Train
B AFW pump was
declared
since this essential
chiller provided cooling for
the
AFW pump room.
As
a result,
Technical Specifications
required the
licensee
to enter
Mode 4.
~
After the licensee
removed the Train
N AFW pump low suction pressure
trip from service,
they could not reopen the downcom'er isolation valves,
which had automatically closed
on the main steam isolation signal
(Section 2.3).
2.1
0 erator
Res
onse to the Turbine Tri
and Reactor Tri
The licensee initiated
an incident investigation
team,
by Nuclear
Assurance,
to review the cause of the reactor trip and the operator
response.
The inspector
performed
an independent
review of the event
and interviewed the
control
room supervisor
and shift supervisor.
The inspector discussed
the
preliminary results of the licensee's
investigation with their- team
on
December 12.'he licensee's
preliminary conclusion
was that operators
had
performed properly and
had met management
expectations.
The inspector
discussed
concerns
regarding the following issues:
Operators
opened
the atmospheric
dump valves to control the secondary
pressure
approximately four minutes into the event.
The slow response
of the feedwater control
system
(FWCS)
appeared
to
contribute to the high steam generator level condition.
A high level over-ride
(HLO) signal,
which terminates
feedwater flow on
high steam generator level,
appeared
effective in one steam generator
and not in the other.
Instruments
indicated that reactor trip setpoints
were approached
in
three instances
and operators
did not manually trip the reactor.
Following the reactor trip, it appeared
that secondary
pressure
and
primary temperature
exceeded
emergency
operating
procedure
guidance.
2. 1.1
Atmospheric
Dump Valve Control
The steam generator
atmospheric
dump valves
(ADVs) used at Palo Verde operate
solely on the
demand signal manually positioned
by the operators.
The ADVs do
not have
an automatic capability to relieve steam generator
pressure
and take
approximately
30 seconds
to open after operators
position their controller.
The inspector noted that the main steam safety valves,
which first lifted
approximately
one minute into the event,
were
open for approximately
two
minutes before the operators
opened the
AOVs.
The inspector discussed
the
delay in opening the
ADVs with the licensee.
The licensee
stated that the
operators
had
been trained with an operating philosophy that manual
action
should only be taken
once the transient
cause is understood.
They noted that
during the time the safety valves were open,
the operators
had focused
on
system
(RCS) pressure,
which was also high.
In addition, the
secondary
side operator
was evaluating the loss of condenser
and the loss of
six of the steam
bypass control valves.
The licensee
indicated that although
the operator
response
to open the
ADVs was not quick, the licensee
determined
the operat'or
response
had met their expectations.
The inspector
agreed with
this assessment.
e
2. 1.2
Level Control
The inspector
reviewed several
parameter
trends to evaluate
the cause of the
high steam generator
(SG) level reactor trip.
The inspector
compared
feedwater flow to reactor
power and noted that the feedwater flow to each
was approximately
500 gallons per minute
(gpm) greater
than the amount
required for the given reactor
power.
In addition, the inspector
noted
a slow
SG level increase.
The inspector
noted that the operators
had not expected
and
had not recognized that the
SGs were being overfed until late in the
Approximately 30 seconds
before the reactor trip, the operators
closed the
SG economizer isolation valves to limit any leakage
past the
economizer control valves.
However, the operators
did not take manual
control
of the feedwater
system to control the feedwater flow before the high level
trip occurred.
The inspector
reviewed the system description
manual for the
FWCS.
The
inspector
noted that the
FWCS has
a lag network to effectively delay the
complete
implementation of a level deviation signal in single element control
(power less
than
15 percent).
The inspector questioned
engineering
about the
response
of the single element
FWCS during the plant transient.
The engineer
indicated that the system
was not designed
to handle the transient that was
experienced
on November 26.
The system
was designed
to be slow,
and not
overreact,
to allow stable operation during reactor startups.
The engineer
indicated the
FWCS responded
as designed.
0
The inspector discussed
the overfeeding observation
and
FWCS response
in
single element control with the licensee's
incident investigation
team.
The
team reviewed the inspector's
findings and evaluated
the trends.
The licensee
subsequently
determined that the
FWCS was not designed
to mitigate this event
before the
SG water level reached
a reactor trip setpoint.
The licensee
determined that,
in single element control, the
FWCS was designed
for power changes
of up to one percent
per minute.
Actual power had
been
changing at approximately
two percent
per minute.
The licensee
determined
that, in three element control, the
FWCS was designed for power changes of
five percent
per minute.
Actual power had
been
changing at approximately
eight percent
per minute when in three element control.
The inspector questioned
several
operators
in all three units about their
knowledge of the
FWCS in single element control.
The inspector
noted
weaknesses
in the operators'nowledge
of the limitations of the
FWCS.
The
inspector
found that operators
expected
the
FWCS to be responsive
in single
element control
and that they were not aware of the limits of the
FWCS in
single element control.
The inspector
noted that operator training seldom
includes plant operational
at low power operations.
In addition,
during plant shutdowns,
plant operators
manually trip the reactor from
approximately
20 percent
power and, therefore,
single element control is not
utilized.
The inspector discussed
the operators'nowledge
of the
FWCS with the
licensee.
The licensee's
investigation
team
had determined that operators
had
responded
appropriately during the event.
They had noted that the event
was
complex with several
parameters
'in transient conditions throughout the event.
They concluded that these conditions would have
made it difficult for
operators
to conclude
what manual
actions, if any,
were appropriate.
However, they indicated that they would evaluate
the licensed operator
knowledge of the
FWCS and determine if additional training of the
limitations at low power may enhance
operator
performance.
The licensee
also
planned to evaluate
the current
FWCS design
and determine if it can
be
improved or optimized.
2. 1.3
High Level Override
The inspector
noted that the function of the
HLO was to close the feedwater
economizer
and downcomer valves
when the level in the affected
SG reached
88 percent to prevent excessive
moisture carryover to the main turbine.
The
reactor trip and main steam isolation signals
are set at 91.5 percent level.
The inspector
reviewed the post trip sequence
of events
and noted that
approximately
two minutes prior to the reactor trip on high level in
SG 11,
the operators
had
a high level in
SG 12.
The inspector
found that the
HLO
isolated
feedwater to
12
and prevented
the reactor trip.
The inspector
noted that the
HLO for SG ll occurred three
seconds
before the reactor trip on
high level in
SG 11.
The
HLO did not prevent
an automatic safety function
actuation
in the three
second
time span.
The inspector discussed
the
HLO response
with the licensee's
incident
investigation
team.
The incident investigation
team indicated that the
HLO
responded
as designed
and that the
as found setpoint
was within the setpoint
tolerance.
The inspector questioned
whether the
HLO was nonfunctional
since
it failed to isolate feedwater flow to the
SG ll before the reactor trip and
main steam isolation occurred.
The incident investigation
team indicated that
they would review the setpoint
and setpoint tolerance
to determine if the
setpoints
or function could be enhanced
to prevent reactor trips.
The
inspector
concluded that the licensee
action to further evaluate
the
HLO
design
was appropriate.
2. 1.4
Hanual Operator Actions
The inspector noted that the shift supervisor
and control
room supervisor
discussed
manually tripping the reactor three times during the event.
The
first time occurred
when the pressurizer
pressure
increased
to .the pretrip
setpoint;
however,
pressure
turned
and remained
under control.
The second
time occurred
when
12 high level increased
to the high level pretrip;
however,
the
HLO turned the
SG level.
The third time occurred
when
11 high
level increased
to the high level pretrip setpoint;
however,
the reactor
automatically tripped 'before the operators
could manually trip the reactor.
Licensee
management
stated that operators
had appropriately
implemented the
expectations
that manual
action not be taken if it appeared
that control
systems
were responding
appropriately.
The inspector noted that licensee
management
planned to evaluate
management's
expectations
for taking manual
actions including manual control of automatic control
systems
during plant
The inspector
concluded that the licensee's
corrective actions
were appropriate.
In addition, the licensee
planned to evaluate their
guidance to operators
on when to initiate
a manual trip.
2. 1.5
ADV Control Following the Reactor Trip and Hain Steam Isolation
The inspector noted that following the reactor trip, the reactor coolant
system temperature
and
pressure
gradually increased for
approximately four minutes" before the operator
reduced
the steam generator
pressure
to allow the open main steam safety valve to close.
In addition,
temperature
and
pressure
increased
to above the
band specified
in emergency
operating
procedures.
The inspector discussed
the secondary
operator's
performance
in controlling plant parameters
with the licensee.
The
licensee
reviewed the post trip trends
and discussed
the requirements for
plant control that training uses to evaluate
operator
performance
on the
simulator.
The licensee
determined that the operator
performance
was
satisfactory,
but not optimal.
The inspector
agreed with the licensee's
assessment
of the performance.
2.2
S urious
0 enin
of the Condenser
Vacuum Breaker
The condenser
has three
vacuum breakers.
They are air to open,
spring to
close butterfly valves that can
be opened
from the control
room.
Prior to the
event,
an auxiliary operator
(AO) was touring the turbine building and
had
just ensured that the
vacuum breaker for the
C hotwell
had
an adequate
water
seal
on its upstream
side
when
he heard
a "loud sucking noise"
from the vacuum
breaker.
He observed that the vacuum breaker
was in the mid-position instead
of the required closed position.
He took control of instrument valves
on the
actuator
and eventually closed the breaker,
although his action
caused
the
vacuum breaker to open slightly farther than it already
was for a short period
of time.
The inspector
reviewed the licensee's
evaluation of the AO's performance
and
the evaluation of the cause of the failure.
2.2. 1
Auxiliary Operator
Performance
The licensee
concluded that the
AO should
have contacted
the control
room
prior to attempting to close the
vacuum breaker.
The licensee
noted that
were not trained in the operation of the
vacuum breaker actuator.
Operations
management
stated that it was their expectations
that the
AO contact the
control
room prior to taking actions
in the field on equipment that the
AO did
not have either written instructions or had not had specific training.
The licensee's
investigation
team found that the
AO had previously observed
that there
appeared
to be leakage
past the solenoid,
and that this condition
was not observed
on the other vacuum breakers.
However, the
AO had not
initiated
a work request
to have the condition investigated,
as expected
by
management.
'he licensee
planned to review this event with the
AOs and reinforce the
appropriate
requirements
expected of the
AOs before
and after taking action in
the field.
In addition,
the licensee
planned to evaluate
the current task
analysis
and training for AOs and determine whether additional training was
warranted to enhance
knowledge of air operated
valves
and actuators
similar to
the
vacuum breaker operator.
2.2.2
Vacuum Breaker Failure
The licensee
determined that the apparent
cause of the vacuum breaker solenoid
failure was attributed to component
age.
The licensee
inspected
the solenoid
valve and noted that the middle insert gasket (0-ring) within the solenoid
appeared
degraded
and flat.
The seating
surfaces
on the piston/guide
subassembly
also
showed indications of wear.
The licensee
checked
the other vacuum breaker solenoid valves for leaks
and
noted
two additional
solenoid valves in Unit 2.
As an interim corrective
action,
these
valves were replaced.
Valve Services
Engineering
planned to
perform
a root cause
analysis of the solenoid valves.
Based
on the results of
the analysis,
the licensee
planned to make
a determination of any preventative
maintenance
requirements
or recommend
an alternative corrective action.
-10-
2.3
Downcomer Isolation Valves Failed Closed
On the day after the reactor trip, with Unit
1 in Mode 4, the licensee
completed actions to disable the low suction pressure trip for the Train
N AFW
pump
and successfully
started
and ran the
pump.
Operators
proceeded
with
actions to place the Train
N AFW pump inservice.
The Train
N AFW pump provides
condensate
storage
tank water to the upstream
side of the downcomer'feedwater
control
and isolation valves.
The Train A and
B AFW pumps provide condensate
storage
tank water downstream of these
valves.
For each
there are two (spring to close, air to open)
isolation valves which close
on
a main steam isolation signal.
When operators
attempted to open the downcomer isolation valves,
they could only get one out
of three
open
and could not establish
flow from the Train
N AFW pump to either
Operators,
with the assistance
of the shift technical
advisor,
attempted
various combinations of venting the upstream
and downstream
pressures.
After
troubleshooting for four hours,
they were able to open the remaining three
downcomer isolation valves
when they established
discharge
pressure
of the
Train
N AFW pump to the upstream
side of the valves.
At the end of the inspection period,
the licensee
had not established
a root
cause of the failure to open.
The inspector
noted that Technical Specification 3.7. 1.2 for the
AFW system required that the Train
N AFW pump
and its associated
flow path were required to be operable.
On December
12,
the inspector requested
the licensee
to explain why they considered
the
'rain
in light of the problems experienced
following the reactor trip.
On December
15, in a conference call with the Region
IV management,
the Site
Shift Hanager stated that the flow path
was considered
since the
downcomer isolation valves could
be opened with the assistance
of the
discharge
head of the Train
N AFW pump.
The Region
IV staff questioned
whether this sequence
was explicitly covered in operating instructions.
The
licensee
noted that operating
procedures
allowed this sequence,
but did not
specifically require it.
They stated that
a night order would be issued to
all units discussing
the downcomer event
and the success
path
used
by the Unit
1 operators
to open the valves.
The inspector
subsequently
reviewed the night order
and found that it
discussed
the failure of the downcomer valves to open,
speculated
that it was
caused
due to pressure
binding,
and noted that applying pressure
from the
Train
N AFW pump to the downcomer isolation valves
had allowed operators
to
open the valves.
The licensee
concluded that they had
a high degree of confidence that with or
without the night order, plant operators
could have
opened
the downcomer
valves in similar circumstances.
To assess
the validity of this conclusion,
the inspector discussed
the night order with control
room supervisors
and
-11-
shift supervisors
in all three units.
The inspector noted that prior to the
night order,
the supervisors
in Units
2 and
3 were
aware that there
had
been
problems with the downcomer valves in Unit 1, but were not cognizant of the
success
path for opening the valves.
The inspector
found that although the
night order did not provide specific instructions,
each supervisor
appeared
to
understand its message.
Additionally, the supervisors
interviewed
appeared
confident that they would have taken this course of action if the night order
had not been provided.
The inspector
found that while there
appeared
to be reasonable
basis for the
licensee's
assertion
that other crews could have
reopened
the downcomer
isolation valves in a timely manner,
the night order to communicate this issue
was prudent.
The inspector noted that the licensee
was investigating the cause of the valve
failures.
At the
end of the inspection period, the licensee
considered that
pressure
binding of the flex-wedge gate valves to be
a probable
cause.
Additionally, the licensee
was evaluating the design basis for these
valves to
establish their function to support the Train
N AFW flow path.
The inspector
will review the licensee's
root cause
evaluation in a future inspection.
2.4
Conclusions
The inspector concluded that the licensee's
actions,
both completed
and
planned,
to assess
this event
and its implications were appropriate.
3
FOLLOWING STARTUP TRANSFORMER TRIP UNIT 1
(93702,
71707)
On December
9, the Unit
1 reactor tripped from 40 percent
power on low steam
generator level.
Two minutes prior to the trip,
a ringtail cat
(a desert
mammal similar to a raccoon)
caused
a momentary
phase to ground path
on the
startup transformer
NAN-X03, which resulted in a loss of power to the Unit
1
bus
PBA-S03 (vital Train A 4160 volt) and the Unit 2 bus
PBB-S04 (vital
Train
B 4160 volt).
Both the Unit
1 Train A diesel
generator
and the Unit 2
Train
B diesel
generator
started,and
operated
as expected.
In Unit 1, the
120 volt ac control
power bus
NNN-D11, which supplies
the
and the steam
bypass control
system, failed to complete
an automatic transfer
from its "alternate"
power supply bus
PBA-S03 to
a "normal" non-class
power
supply,
causing
a loss of power to bus NNN-Dll.
As
a result of the loss of
power to the
pumps went to minimum speed
and
feedwater control valves closed,
causing
levels to decrease.
12 level decreased
below the reactor trip setpoint,
resulting
in a reactor trip.
The licensee classified the event
as
an "uncomplicated trip" and all systems
responded
as expected.
Bus NNN-Dll was re-energized
when it automatically
transferred
back to bus
PBA-S03 after its auxiliary transformer
powered
normal
power supply de-energized
as
a result of the turbine trip.
In addition,
two
pumps
and two circulating water
pumps tripped following the
-12-
turbine trip since they could not fast transfer from the auxiliary transformer
to startup transformer
NAN-X03.
This resulted
in a loss of condenser
vacuum
and the unavailability of six of eight steam
bypass control
system
(SBCS)
valves.
Secondary
side pressure
rose to 1246 psia
and
one main steam safety
valve lifted and relieved for approximately two minutes.
The licensee
subsequently
determined that the safety valve lifted and reset within its
design margins;
The licensee
determined that
a mechanical
linkage problem prevented
bus
NNN-Dll from completing its transfer
sequence
from its alternate
power supply
to its normal
power supply,
as explained
below.
The licensee
has
had
bus
NNN-
Dll aligned to its alternate
power supply since initial startup.'uring
the
post-trip review, the licensee
determined that it would be preferable to re-
align NNN-Dll to its normal
power supply
and confirmed through testing that it
would reliably automatically transfer
from its normal to alternate
power
supply.
On December ll, at 0605, Unit
1 went critical
and returned to full power on
December
13.
Unit 2 remained
at
100 percent
power throughout the event.
The
resident
inspectors
responded
to the site following the reactor trip and
followed the licensee's initial post-trip review.
On July 17,
1995, Unit 2 experienced
a similar event
when
a breaker operation
error resulted in the loss of 13.8
Kv bus
NAN-S05.
During this event,
NNN-Dll
transferred correctly from its alternate
supply to its normal supply.
However, the transfer
was designed
as break before
make and,
as
a result,
during the brief period the bus
was de-energized,
the
FWCS switched to manual
'ith zero demand.
This event
was discussed
in Inspection
Report 95-14
and
Licensee
Event Report
(LER) 50-529/95-05.
During the initial post-trip review following the Unit 2 trip, the licensee
suspected
that bus NNN-Dll had not properly transferred.
They subsequently
discovered that it had transferred
as designed.
They concluded that
an
initial design of the bus transfer did not provide for uninterrupted
power to
NNN-D11, resulting in an inconsistent transfer of the
FWCS and the
SBCS.
The
licensee
had established
a December
29,
1995,
due date for modification
recommendations
to address
this design
weakness.
At the time of the Unit
1
trip, the licensee
had completed
most of their review, but had not finalized
'heir
recommendations.
In their review of the bus NNN-Dll transfer logic, the licensee
determined
that the original design required the
bus
be supplied
by the auxiliary
transformer,
through
bus
NAN-S01.
However, during initial plant startup,
the
licensee
had established
a practice of lining up the bus to its alternate
source,
from bus
PBA-S03.
This change
was apparently
made after reliability
problems with the automatic fast bus transfer,
between
bus
NAN-S01 (supplied
by the auxiliary transformer)
and
bus
NAN-S03 (supplied
by the startup
transformer),
caused
frequent challenges
to the bus
NNN-D11 transfer.
At the
time, the alternate
supply was considered
a more reliable power source.
-13-
On December
9, the licensee
determined that aligning bus NNN-Dll with its
normal
supply was preferable
to aligning it with its alternate
supply.
They
noted that in recent years
power had
been interrupted
on the startup
transformers
more frequently than
on the auxiliary transformers.
Additionally, the fast transfer of the 13.8
Kv buses
had worked reliably.
The
licensee
also noted that further efforts to address
the reliability of power
to sensitive non-vital
AC instrument
and control loads were still in progress.
4
OPERATIONAL SAFETY VERIFICATION
(71707)
4. 1
Midloo
0 erations
Unit 3
On November
15, the inspector
observed
several
aspects
of the midloop
performance.
The inspector
observed that the control
room staff maintained
positive control of the evolution.
The inspector
noted that the licensee
had
again
used
two control
room supervisors
from another unit,
who had
been
involved in recent midloop operations,
to supervise
midloop operations
in
Unit 3.
The continuity established
appeared
to be effective.
The inspector
reviewed the refueling water level indicating system
(RWLIS)
instrumentation calibration
and noted
no discrepancies.
The inspector
performed
a walkdown of the
RWLIS inside containment
and noted that the system
was properly aligned.
The inspector
noted
one of the
RWLIS instrument tubing supports
was loose.
The inspector
informed the licensee of the problem.
The licensee
promptly
corrected
the deficiency.
In addition, the inspector
noted that the condition
of work areas
and the general
housekeeping
in containment
were not as
good
as
the inspector
observed
in previous outages.
The inspector
informed the
licensee
about the observations.
Maintenance
management
determined
the major
contributor to the problem was contract workers
and took actions to correct
the work practices.
The inspector
concluded that the licensee's
response
to
the deficiencies
was appropriate.
4.2
Containment
Closeout
Ins ection
Unit 3
On November 22, the inspector
performed
a containment
closeout
inspection.'he
inspector
found several
small debris
items
and noted that the containment
cleanliness
was not as
good
as it has
been
observed
in the past.
The
inspector
noted that the reactor coolant
pump bays contained
the majority of
the debris.
The items discovered
in containment
included:
tape, plastic, tie
wraps,
and leather gloves.
The inspector
concluded that the size
and volume
of the items would not impact the containment
and, therefore,
the debris
items did not constitute
a safety concern.
The inspector discussed
the observation with the licensee.
The licensee
performed additional
walkdowns prior to startup.
The licensee
planned to
evaluate
the inspector's
walkdown findings prior,to the next refueling outage.
4.3
Use of Com uter to Monitor Chan in
Plant Conditions
Unit 3
On November
17, the inspector
observed
a start of a reactor coolant
pump in a
solid plant condition.
The inspector noted that the operators
reviewed the
pump operating
procedure
and discussed
when the
pump should
be
manually tripped before
RCS pressure
decreased
below the minimum net positive
suction
head
(NPSH) pressure
requirement.
The inspector
noted that the
operator
used the emergency
response facility data acquisition display system
(ERFDADS) to monitor
a single suction pressure
value.
The inspector monitored
the pressure
on the four safety channels
of pressurizer
pressure.
During the
pump start,
the inspector
noted that the pressure
dropped
below the
minimum NPSH pressure
for the
pump before the
pump tripped
on
an unrelated
speed
sensor failure.
The inspector noted that the
ERFDADS pressure
monitored
by the operator still indicated
adequate
NPSH pressure
when the
pump tripped.
The inspector questioned
the
ERFDADS response
with the system engineer.
The
system engineer
indicated that the
ERFDADS has
a minimum of a 1.5 second
delay
compared to the analog safety channel
indication.
The inspector
informed the
operations
department
leader of the observations
and expressed
a concern that
the operator
used
a time delayed indication in a transient condition.
The
operations
department
leader
agreed with the inspector
and issued
a night
order to all operators
indicating that
ERFDADS should not be solely used for
indication during
a transient condition.
The inspector
concluded that the use
of the
ERFDADS in this instance
had
no safety impact
on the'lant
and that the
licensee's
corrective actions
were appropriate.
4.4
A
roach to Criticalit
Process
Review
The inspector
reviewed the licensee's
corrective actions in response
to
'inspector identified weaknesses
in the licensee's
performance of 1/m plots
for monitoring the approach
to criticality during
a Unit 2 reactor startup
(Inspection
Report 95-14).
The inspector
noted that the licensee
evaluated
crew performance,
including the shift technical
advisor
and reactor
engineering,
during several
plant startups
on the simulator.
The licensee
identified performance
and knowledge weaknesses
of both the crew and the
training staff.
The licensee initiated
a condition report/disposition
request
(CRDR) to evaluate
and correct the weaknesses.
The inspector
concluded that
the licensee
performed
an extremely thorough
and indepth
assessment
of the
weaknesses
in both the performance of personnel
and the startup
process.
At the exit meeting,
the inspector
noted that the licensee's
review of the
startup
process
identified
a need for continued training
on complex evolutions
that are performed infrequently.
The licensee
agreed with the inspector 's
statement
and planned to continue evaluating operator training requirements.
5
MAINTENANCE OBSERVATIONS
(62703)
5. 1
Emer enc
Diesel
Generator Tri
s
Unit 2
On November
16, the Unit 2 Train
B diesel
generator
experienced
a
non-emergency trip during
an operability surveillance test.
This trip was
similar to the previous three trips that
had recently occurred
on this diesel
-15-
generator.
During the last inspection period,
a multi-discipline diesel
generator
task force team
was established
by management
to determine
the root
cause of failure of the recent trips.
The inspector
documented this effort in
Inspection
Report 95-18.
The inspector
observed
troubleshooting efforts by the electrical technicians.
The task force team leader developed
an extensive four stage action plan to
determine
the cause of the trips, verify proper restoration of the diesel
generator
following maintenance
activities, monitor diesel
generator
performance for spurious trips,
and obtain additional data for assessment.
The diesel
generator
was returned to service
on November
18, following
maintenance activities
and
a satisfactory operability surveillance test.
The inspector
concluded that the task force team appeared
thorough in their
review and the troubleshooting efforts observed
were adequate.
5.2
Char in
Pum
Power
End
Re lacement
Unit 2
On November 21, the inspector
observed
some portions of the work that
mechanical
maintenance
technicians
were performing
on the Train A charging
pump.
The technicians
were replacing the power end of the
pump.
The
inspector
concluded that the work performed
was adequate
and well controlled.
In September,
an auxiliary operator identified
a low lube oil pressure
condition
on the Train A charging
pump.
The
pump was declared
and
mechanical
maintenance
engineering
was notified.
The power end internals
were
inspected
and found to have significant damage.
The licensee initiated
a
CRDR
and
a formal root cause investigation.
The inspector attended
meetings with the maintenance
engineering staff to
discuss
the status of the investigation.
The inspector
noted that maintenance
engineering
had developed
an extensive
action plan to troubleshoot
and
investigate
the cause of the power end internal
damage.
The main contributor to the problem was
an alignment problem that existed
between
the
pump block and power end of the
pump,
as
a result of maintenance
performed several
years
ago.
The shifted alignment
was caused
by defective
power end studs
and installation errors
on this
pump which do not appear to be
applicable to the other pumps.
Maintenance
engineering
management
decided to
replace the power end of the
pump.
The inspector
concluded that appropriate
actions
were taken
by mechanical
engineering.
The investigation effort was extensive
and thorough.
The
pump
was placed in service
and
has since maintained oil pressure
in the acceptable
ranges.
5.3
Main Steam Safet
Valve Res
onse Followin
Reactor Tri
Unit
1
During the secondary
plant pressure
transient following the November
26
reactor trip (Section 2), three
(MSSVs) lifted.
All
-16-
three safety valves
were set to lift at
1250 psig
+ 3 percent.
Plant
recorders
indicated that the three valves lifted within tolerances
and that
pressures
had not exceeded
1250 psig + 3 percent,
indicating that the fourth
valve, set at
1250 psig, could have remained
seated
and still been within
setpoint tolerances.
Although two of the safety valves reseated
within three minutes,
HSSV 561
appeared
to continue to modulate
open
and closed until pressure
dropped
below
1130 psig.
Plant recorder data indicated that the reseat
pressure
would have
been approximately
10 percent
below the lift pressure.
The licensee
concluded
that. the blowdown could be expected
to vary between three
and nine percent.
Additionally, they noted that the valve had
been
open for approximately
ll minutes
when it reseated
and considered
that the heating of the valve could
have lowered the reset
pressure.
Following'he reactor trip, operators
allowed secondary
pressure
to increase
(Section
2. 1.5).
HSSV 561 reopened
at
a pressure
between
1155 psig
and
1181 psig (5.5 to 7.6 percent
below its setpoint).
The valve was subsequently
declared
and gagged
closed.
While the unit was in Hode
3 and prior
to restart,
a licensee contractor,
Furmanite,
performed on-line testing using
their Trevitest method.
HSSV 561
was tested
11 times, with a total of five
separate
adjustments.
The licensee ultimately was able to meet their criteria
of three successive
tests within one percent of 1250 psig.
The inspector reviewed the test results with the inservice testing engineering
staff.
They stated that
HSSV 561
had initially lifted at
1197 psig.
The
inspector
noted that this was considerably
lower that its initial set
pressure,
as well as the pressure it appeared
to lift at during the plant
considering that no adjustments
had
been
made to the valve.
The
licensee
could not explain the change
in the setpoint.
After the first test lift, the valve nut was turned three flats of the nut.
Although historical trends indicate that this adjustment
should
have raised
the lift point approximately
30 psi, the next two tests
were at
1194
and
1192 psig.
The licensee
could not explain why this had occurred,
except that
the safety valves
do not respond consistently to nut adjustments.
Subsequently,
the valve appeared
to lift at
a consistent
pressure
after each
adjustment.
The licensee
noted that this safety valve had
been
placed in service in
November,
1993 after having been refurbished.
The inspector
observed that in
November,
1993
a similar valve in Unit
1 had lifted approximately
40 psi lower
than its setpoint.
As documented
in LER 528/93-0ll, Revision
1,
HSSV 572 was
gagged
closed for the remainder of the operating cycle when
a review of test
data
had indicated that it had not responded
consistently to adjustments
made
during testing.
The inspector questioned
how the performance of HSSV 561
was
different than the November
1993 performance of HSSV 572.
The licensee
noted
that
HSSV 572 had behaved
more erratically during testing than
HSSV 561.
The
inspector
reviewed documentation of the evaluation for HSSV 572
and concurred
with this assessment.
'
-17-
5.4
Auxiliar
Pum
Governor Valve Deficiencies
Unit 3
On November 23, the licensee
entered
Mode
3 following the refueling outage
and
began to perform testing
on the turbine driven
AFW pump.
Technical
Specifications
require that the
pump
be tested within the first 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> of
establishing
normal operating
temperature
and pressure
conditions.
During the
testing,
the licensee
observed that, after operating for extended
periods,
the
governor
had
a tendency to lock up at speeds
between
2000
and 3000 rpm.
The licensee
developed
an action plan
and
began investigating the problem.
The troubleshooting
and repair took over 70 hours8.101852e-4 days <br />0.0194 hours <br />1.157407e-4 weeks <br />2.6635e-5 months <br /> of the
72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> allowed
outage time.
The licensee ultimately discovered that the governor valve
had
been rotated approximately I/4 inch,
as indicated
by match marks,
when it was reinstalled during the refueling outage.
This resulted
in a
misalignment of the linkage between
the hydraulic servo
and the governor stem,
which caused
the linkage to bind.
The binding appeared
to be enhanced
as the
turbine heated
up and thermally shifted.
The licensee
subsequently
performed minor adjustments
to the mounting of the
hydraulic servo
and the linkage to align them with the rotation of the
governor valve bonnet.
They performed
subsequent
testing which demonstrated
that the linkage operated
smoothly.
In addition, in the following week, the
licensee
tested
the Units
1 and
2 turbine driven
AFW pumps to ensure that
similar binding was not occurring.
The inspector
observed
portions of the troubleshooting
and repairs
and
determined that they were well controlled.
The inspector
discussed
the
troubleshooting effort with maintenance
management.
They had determined
during the troubleshooting that there
was additional data which could
be
'athered
during the setup of the governor valve which would aid in future
maintenance
and troubleshooting efforts.
This included establishing
a
baseline of the electronic signal into the governor module
and the hydraulic
pressure
output
as
speed
demands
are changed.
In addition, maintenance
management
stated that they planned to address
the misalignment of the
governor valve bonnet
as
a maintenance
performance error and initiate
corresponding
corrective actions.
5.5
Essential
Chiller Problems
Units
1 and
3
During the inspection period,
the inspector
observed portions of
troubleshooting efforts by the heating, ventilation
and air conditioning
(HVAC) team to resolve
problems experienced
by the Unit
1 Train
8 essential
chiller and the Unit 3 Train A essential
chiller.
The
HVAC team was comprised
of representatives
from design engineering,
system engineering,
maintenance
engineering,
and the maintenance staff.
The essential
chilled water system supplies chilled water to the essential
air
cooling units
and air handling units in the Control Building and the Auxiliary
Building during essential
equipment operation.
The essential
chiller system
consists
of two separate,
redundant,
safety-related
flow trains.
The
-18-
essential
chiller system starts automatically
when essential
equipment
operation is required.
5.5.1
Essential
Chiller Trip Unit
1
On November 27, the Unit
1 operators
were recovering
from a reactor trip
(Section
2)
and
had started
the Train
B essential
chiller to support
room
cooling to the Train
pump.
Approximately 30 minutes
into the run, the chiller tripped due to low refrigerant temperature.
Operators
complied with Technical Specification action statements,
initiated
a
CRDR,
and contacted
HVAC personnel.
The
HVAC team initiated
an evaluation of the chiller trip.
The system
engineer
stated that the "low refrigerant temperature" trip appeared
to have
been
caused
by
a low refrigerant level in the cooler.
The cooler is
a shell
and tube heat exchanger.
Low pressure,
liquid refrigerant
on the shell side
absorbs
heat from chilled water flowing through the tubes
'as the refrigerant
flashes to vapor.
The refrigerant level prior to the trip was approximately
3.5 inches.
The
HVAC technicians
identified
some minor freon leaks
and restored
the
refrigerant level to approximately
6 inches.
The chiller was tested
and
returned to service.
The leaks
were subsequently
repaired during
an on-line
outage of the chiller.
The inspector discussed
the chiller trip with the system engineer.
The system
engineer
stated that during cold weather conditions the refrigerant
experiences
a "stacking"
phenomena.
During normal
oper ation,
vapor
refrigerant should condense
to
a liquid in the condenser
and flow to the
cooler.
However,
when essential
cooling water,
which flows through the
condenser,
is colder,
a low pressure
condition exists which causes
the liquid
refrigerant to stay in the condenser.
It appeared
that
a high level of
refrigerant in the cooler was necessary
to ensure that the stacking
phenomenon
would not result in a chiller trip.
The inspector discussed
the issue of refrigerant level with the system
engineer.
It appeared
that there
was competing guidance
on the appropriate
levels of refrigerant in the chillers.
~
Engineering evaluation request
(EER) 88-EC-003,
determined
the
recommended
refrigerant levels required during shutdown conditions.
The
Unit
1 Train
B essential
chiller refrigerant levels were 4.88 inches
minimum and 6.0 inches
maximum.
',
EER 90-EC-031,
which apparently'uperseded
EER 88-EC-003,
specified
a
shutdown refrigerant level
band for each chiller of 3.0 inches
minimum
and 7.0 inches
maximum.
This level
band
was incorporated
in the weekly
preventive maintenance
task.
-19-
During the Unit I fifth refueling outage,
HVAC technicians
identified
pitting on the compressor first stage impeller.
Design engineering
speculated
that the pitting was caused
by liquid refrigerant carryover.
The compressor
is
a two-stage,
centrifugal type.
It takes
suction
on
the cooler shell,
increases
the refrigerant
gas pressure,
and discharges
the refrigerant
gas to the chiller condenser.
The design
engineer
recommended
that refrigerant levels
be maintained
in the lower region of
the level
band to prevent impeller damage
by liquid refrigerant
carryover.
~
During discussions
with the system engineer
on December
21, the engineer
could not conclude that
a chiller could
be considered
operable with a
level of 3.5 inches.
~
On December
21, the inspector identified that
one of the chillers in
Unit 3 had
a level of about 3/8 of an inch above the
7 inch maximum.
This level did not appear to be consistent
with any of the guidance
provided.
The inspector
noted that the weekly preventative
maintenance
task still specified
a level from 3 inches to 7 inches.
The licensee
immediately lowered the level to 6 inches
and initiated
a
CRDR to
document
and resolve the problem.
The inspector
concluded that the licensee
did not have
a good understanding
of
the appropriate
levels for the chillers and
had not implemented sufficient
measures
to assure that chiller refrigerant levels were properly maintained.
5.5.2
Train A Essential
Chiller Low Lube Oil Unit 3
On October 2, the Unit 3 Train A essential
chiller was
removed
from service
for a maintenance
outage.
During this outage,
the rear motor bearing
seal
to
the compressor
was inspected
and the 0-ring seals
were replaced.
The
technicians
had problems with. the replacement
of the rear seal
and the 0-ring
had to be replaced
again.
The compressor
and motor are refrigerant cooled
and oil lubricated.
A motor
driven,
compressor lubricating oil pump and reservoir are located in the
compressor
base.
There are two sight glasses,
an upper
and lower bulls-ey'e,
that represent
the minimum and
maximum oil levels.
The licensee
has
established
that the chiller should not be operated
with the oil level below
the lower sightglass,
which corresponds
to approximately 7.5 gallons of oil,
or with an oil level in excess of 25 gallons.
On October
29, the chiller was returned to service following the maintenance
outage with an initial volume of 15 gallons of oil.
On November
27, the
Train A essential
chiller was declared
inoperable after
an
AO noted that the
oil pump appeared
to be cavitating
due to low reservoir level.
technicians
added
more oil and retested
the chiller.
The chiller was then
returned to service.
-20-
The licensee
subsequently
determined that from November
10, through
November 27,
17 gallons of oil had
been
added to the system to maintain the
minimum oil level requirements.
Operations initiated
a
CRDR and the
personnel
developed
an action plan to resolve the apparent
loss of oil.
The
HVAC system engineer
explained to the inspector that during cold weather
conditions the oil tends to migrate with the refrigerant.
Once the chiller is
operated
under loaded conditions,
the oil will heat
up and return back to the
oil sump.
The guidance
given to operations
by the
HVAC engineer
was to have
an operator present
during any start of the essential
chiller.
Since there
was
a total of 32 gallons of oil in the system,
once the chiller is fully
loaded the oil would migrate back through the oil return system
and the
operator
would need to drain the oil. If the reservoir
becomes
too full of
oil,
a "high bearing temperature trip" could result.
On December
5, the inspector
observed
HVAC technicians
perform maintenance
activities
on the Train A essential
chiller.
The oil was removed from the
system.
The technicians
removed
and replaced
the rear motor bearing seal.
The technician
added
12 gallons of oil and the chiller was tested.
After a
successful
four hour run, the chiller was returned to service.
The repairs
appeared
to have addressed
the oil migration problem.
The inspector
was concerned
that the repair performed during the refueling
outage
may have
caused
the oil migration problem.
Additionally, the inspector
was concerned
that the licensee
had not established
an appropriate
basis for
considering
the chiller operable after it was identified on November
27 to
have excessive oil.
5.5.3
Summary
The licensee initiated
CRDRs to address
both the Units
1 and
3 problems.
Additionally, the Executive Vice President initiated
a Level
1 action item to
resolve these
issues.
The licensee initiated measures
to determine
the
refrigerant level required to assure chiller operability and resolve the
inconsistent
guidance.
The inspector considered this to be
an Unresolved
Item
(528/9521-01).
6
SURVEILLANCE OBSERVATION
(61726)
6.1
Containment
S ra
Pum
Testin
Unit 3
On November 5, while Unit 3 was in an outage,
operations
personnel
performed
surveillance test
"Containment
Spray
Pump Full Flow Inservice
Test,"
on the Unit 3 Train A containment
spray
(CS)
pump.
The
pump failed
both the
ASME Code Section
XI and design basis full flow tests.
The licensee
checked
the test instrumentation
and,
although they were able to demonstrate
some
improvement,
the
pump again failed its design basis flow test.
The
licensee
disassembled
the
pump
and
was unable to identify significant
degradation
or wear.
Mechanical
maintenance
technicians
replaced
the impeller
with another impeller to improve performance.
The licensee
performed
a
-21-
Section
XI test to establish
the
new pump curve
and found that the
pump had
improved performance.
The inspector
observed
portions of the corrective maintenance
and surveillance
testing,
reviewed inservice testing procedures
and performance history,
and
discussed
the cause of the apparent
degradation
with inservice testing
engineers,
maintenance
engineers,
and system engineers.
6. 1. 1
Testing Hethodology
The licensee
performed several
inservice tests of the
CS pumps.
The two
Section
XI tests,
a monthly test performed
on mini-flow recirculation
and
a
refueling outage test at 3525
gpm, were to verify that the
pump performed to
its baseline
pump curve.
A design
basis flow test to establish
that the
pump
could develop
a minimum differential pressure
at 4000
gpm was
added
in 1994
and
was being performed
on the Train A CS
pump for the first time.
The
acceptance
criteria for the full flow Section
XI test,
at 3525
gpm,
was
differential pressure
between
219 psid
and 233.6 psid.
The acceptance
criteria for the design basis-test,
at 4000
gpm,
was
a differential pressure
of greater
than
211 psid.
The Section
XI November
5 test result
was
217.3 psid
and the design
basis test result
was
198.3 psid.
During their investigation,
the licensee identified that the correction factor
used in both tests to compensate
for instrument
gauge location
was incorrect.
The correction factor used in the surveillance test procedure
was 1.3 psid.
This correction factor failed to properly compensate
for gauge elevation
differences
and the pressure
drop across
a flow orifice between
the
pump
discharge
and the discharge
pressure
The licensee
determined that the
correction factor should
have
been
11.7 psid for the Section
XI test
and
12. 1 psid for the design
basis test.
With the
new correction factor the Train A CS
pump would have passed its
Section
XI test with a differential pressure
of 227;7 psid,
but would not have
passed
the design
basis flow test,
which was being performed for the first
time.
6. 1.2
Correction Factors for Section
XI Tests
The licensee
was unable to determine
the basis for the 1.3 psid correction
factor used in the Train A CS
pump full flow tests.
They did discover that
the correction factor used in the mini-flow recirculation test
was correct.
They found that the correction factor for the full flow tests
had
been
established
in 1989
when full flow testing
was initiated.
The error in the
correction factor had not been identified when the procedure
was revised in
1994 to add the design basis flow test.
The licensee
subsequently
reviewed all other
pump tests
and found similar
errors in the full flow test correction factors.
However, the licensee
determined that these differences
had not impacted the conclusions of these
-22-
tests.
Additionally, the licensee
found minor discrepancies
with the
correction factors of other Section
XI tests.
At the end of the inspection period,
the licensee
was establishing
the basis
for the correction factors
used in all Section
XI tests with the intent of
maintaining the basis.
The inspector
found these
actions to be appropriate.
6. 1.3
Hotor Replacement
In 1987, the licensee
replaced
the Train A CS
pump motor with a motor having
a
lower nameplate
speed
(1757 versus
1779 rpm).
The licensee
did not rebaseline
the
pump curve with the
new motor.
This change
would have
had
a greater
effect on the
pump at higher loads.
The licensee
stated that the design basis
full flow test
loaded the motor to two-thirds of its capacity
and would not
have
had
a significant impact
on the
pump curve.
The inspector discussed
some uncertainties
that
may exist with the system
engineer
concerning the design
basis surveillance test.
He stated that in
addition to using the appropriate correction factor, if additional
uncertainties
were removed, for example,
taking credit for the miniflow valve
that does
not
come full open
and using
a more accurate
flow instrument, it
would be expected that the
pump would have marginally passed its design
basis full flow test.
6. 1.4
Conclus'ions
10 CFR 50, Appendix B, Criterion
V requires that procedures
shall
include
appropriate
acceptance
criteria.
The
CS full flow test procedure did not have
appropriate
acceptance
criteria in that the instrument correction factors
used
to determine differential pressures
were in error and this constituted
a
violation of more than minor safety significance.
The inspector
reviewed the
licensee
evaluation,
discussed
the corrective actions with management,
and
concluded that the corrective actions
were appropri ate.
Additionally, the
inspector
noted that the problem was identified by. the licensee
and that there
were
no similar violations identified by either the inspectors
or by the
licensee
which could have reasonably
prevented this occurrence.
This licensee
identified and corrected violation is being treated
as
a non-cited violation,
consistent
with Section VII of the
7
ONSITE ENGINEERING
(37551)
7. 1
Steam Generator Modifications Unit 3
The licensee
performed modifications to the Unit 3 steam generators
during the
refueling outage to reduce the dryout region in the upper portion of the tube
bundle.
The modifications included extending
and lowering the elevation of
the downcomer feedring,
removing orifices in the moisture separators
on the
hotleg side,
and cutting 45 three
inch diameter holes in the shroud
between
the downcomer
and the tube bundle.
-23-
Due to unanticipated
problems
associated
with the modification:
~
The licensee
cut only 27 holes in one
shroud
and
no
holes in the other generator
due to problems experienced
with the
cutting tool.
~
The licensee
discovered that
a cyclic low energy water
hammer developed
in the
new downcomer feedring
when low steam generator levels
and
flow below 200
gpm were established.
~
Operators
noted that the feedwater level control
system developed
oscillations of approximately
10 percent level
peak to peak with reactor
power between
25 and
45 percent.
7. 1. 1
Shroud
Holes
The licensee
attempted to cut 45 holes in the shroud
betwe'en the downcomer
and
the tube bundle using
a three inch diameter electrical
discharge
machining
(EDM) tool.
The job was performed remotely by lowering the
EDM tool
on the
downcomer side of the shroud.
Each cut was expected
to take
up to ll hours to
perform.
The licensee
found that each cut was taking substantially longer than expected
to perform., In addition,
the
EDH tools,
which were expected
to last for up to
three holes were eroding after one hole
and in one instance
an
EDH tool
head
fell off the
EDH tool into the area
between
the shroud
and the tube bundle.
The majority of the
head
was retrieved
and
a safety evaluation
was performed
for the remainder which concluded that it could not damage
the steam
generator.
The licensee
had previously mocked
up the modification process
at
a vendor's
facility.
They determined that the conductivity of the water in the steam
generator
was greater
than the conductivity at the mock up facility and that
this difference
had contributed to the, problems in the rate of cutting and the
life of the
EDH tool.
The licensee
was evaluating the cause of the
differences
in conductivity.
The licensee
completed only 27 holes in steam generator
32 and elected
not to
cut holes in steam generator
31.
They revised the
10 CFR 50.59 evaluation to
disposition this interim condition.
The inspector
reviewed the evaluation
and
noted
no discrepancies.
The licensee
concluded that the condition was
bounded
by the evaluations
performed for the original design
and for the completion of
the entire modification.
Additional calculations
were performed
by the vendor
to address
flow velocities at the tube bundle
and found that the
new flow
velocities would be acceptable.
7. 1.2
Feedring
Water
Hammer
-24-
After the licensee
had entered
Mode 3, they lowered level in one steam
generator
as part of a chemistry control evolution.
Engineers
working on the
turbine driven
AFW pump noted
a cyclic banging in the
AFW discharge lines.
Engineers
subsequently
determined that the water
hammer condition had
been
established
in the modified feed ring under certain flow conditions.
The downcomer feed line rises
up the outside of the steam generator to the
nozzle.
On the inside of the generator
there is
a slip fit between the nozzle
and the feedring.
The line has
a 90 degree
bend
as it turns
downward
and tees
into the lines that form the feed ring.
The licensee
determined that with no
flow to the downcomer line,
a 40 inch section at the nozzle dries out.
At low
flow conditions, this portion did not completely fill.
As a result,
the vapor
in this space
would condense
in the environment of the cold
AFW water causing
the water
hammer.
The inspector
observed
the licensee
evaluate
the problem
and establish
a
special test to determine
the conditions where the water
hammer developed.
In
addition, the inspector
observed
portions of the testing.
The inspector
noted
that although the testing
was performed over
a holiday weekend,
appropriate
levels of licensee
management
were involved.
The testing determined that the
water
hammer
was occurring with steam generator levels below 25 percent of the
narrow range
instruments
and at flows less than
200 gpm.
Additionally, they
monitored pipe movement,
installed
an accelerometer,
and inspected
the
insulation
around pipe hangers
and determined that there
was
no discernable
movement in the piping.
Based
on these observations,
they concluded that the
water
hammer
was of low energy
and would not damage
the steam generators.
The licensee initiated
a
CRDR and planned to take action to revise operating
instructions to restrict
AFW flows to above
200
gpm when below 25 percent
SG level.
7. 1.3
Flow Oscillations At Low Reactor
Power
During reactor startup,
with reactor
power between
25 and
45 percent,
feedwater flow oscillations would cause
steam generator level swings of up to
10 percent
peak to peak.
Engineers
obtained data to evaluate
the cause of the
oscillations
and to establish if changes
to the
FWCS could be made to reduce
the oscillations.
The licensee
also provided guidance to operators
on actions
to take in this region if power is reduced.
7.2
Potential
Loss of Two AFW Pum
s Followin
a Steam Line Break
On December I, the licensee
made
a four hour non-emergency
report to the
NRC
in accordance
with the requirements
of 10 CFR 50.72 for a condition outside of
their design basis.
The licensee
had identified that, following a steam line
break of a specific size
and
a sequence
of events
could occur with design basis
assumptions
that could lead to the turbine
driven
AFW pump tripping on overspeed.
The licensee
postulated that with the
coincident single failure of the motor driven
AFW pump .and with no credit for
-25-
operator actions within the first 30 minutes of the event, that emergency
would be lost to the intact steam generator.
The licensee
planned to describe
the details of the event in Licensee
Event
Report 50-528/95-013.
The inspector
had discussed
the potential for this
sequence
of events with the licensee
in Inspection
Report 95-12.
At the. time,
the licensee
had not determined if there
was
a break size that could lead to
the event.
The licensee
has noted that the sequence
of events did not consider operator
action
and
assumed
some conservative initial conditions outside of normal
operating
parameters.
The inspector reviewed the initial conditions
and
operating
procedures
and found that they provided reasonable
assurance
that
emergency auxiliary feedwater
would be available following a steam line break.
This is an Unresolved
Item (528/9521-02).
8
FOLLOHUP OPERATIONS
(92901)
8. 1
Unresolved
Item 528 9514-02
Closed
Two Auxiliar
Pum
s
~Ino erabl e
This unresolved
item involved the failure of Unit
1 operators
to recognize
that one auxiliary feedwater
pump was already inoperable
when they prepared
to
remove
a second auxiliary feedwater
pump from service to perform
a breaker
modification.
Technical Specification 3.7. 1.2 required that, with two
pumps inoperable,
the unit be in hot standby within six
hours.
Hoth
AFW pumps were inoperable for approximately 5.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.
On August
9 at 6:00 a.m.,
the night shift removed the Train A spray
pond from
service prior to shift change.
Operators
entered
the action statement for
Technical Specification 3.7. 1.2 for the Train A AFW pump (the turbine driven
pump) since without the spray pond, the essential
ventilation for the Train A
was inoperable.
Around 9:15 a.m. the day shift crew removed the Train
N AFW
pump to perform
a modification on its breaker.
They did not recognize that
this placed
them in the six hour action statement.
At approximately
3:00 p.m., operators
racked in the breaker for the Train A spray
pond which
subsequently
tested satisfactorily.
Operators
on the subsequent
night shift recognized that the day shift had
removed
both
AFW pumps from service.
They returned the Train
N AFW pump to
service at around 8:00 p.m.
and initiated
a
CRDR.
The licensee
designated
the
CRDR as significant
and established
an investigation
team to review the event.
The licensee
subsequently
determined that they had met the Technical
Specification requirement
in that they had established
operability within the
six hours allowed.
The inspector
reviewed the licensee's
investigation.
The inspector
concurred
that the licensee
had not exceeded
the six hour shutdown requirement.
The
inspector
noted that the investigation
had identified tliat the work on both
the Train A spray
pond
and the Train
N AFW pump were pre-planned for the
same
-26-
day.
While the work on the Train A spray
pond was reviewed
as
a significant
job, the Train
N AFW pump had not been considered significant work.
The
investigation
focused
on the work control process
weaknesses
which had
resulted
in this oversight.
The inspector
reviewed this evaluation
and the
proposed corrective actions
and found them to be thorough.
The licensee
also noted that
a contributor to the scheduling
problem was the
inappropriate application of the recently
implemented probabilistic risk
assessment
matrix.
The matrix provided risk insights to operators for
emergent
work.
The matrix established
that combinations of equipment
which
place the plant in Technical Specification 3.0.3 are not allowed regardless
of
the risk significance.
However, the matrix did allow the more restrictive
Technical Specification requirement for two AFW trains inoperable,
in that it
suggested
that removing the Train
N AFW with the Train A spray
pond
had
provided
no additional risk.
The control
room supervisor
had referred to the
matrix prior to removing the Train
N AFW pump from service.
One of the
corrective actions
was to reinforce with operators that the matrix was
a tool
to be used in conjunction with Technical Specifications
and did not include
all restrictions.
The inspector
found this to be appropriate.
The inspector
noted that ultimately it was the operating
crews responsibility
to recognize that removing the Train
N AFW pump from service
was not
appropriate.
The licensee's
investigation identified that the control
room
supervisor,
who had authorized
the work,
had not discussed
the decision with
either the shift supervisor or the shift technical
advisor.
When
he
subsequently
discussed it with the shift supervisor,
the shift supervisor
had
not recognized that two trains of AFW were inoperable.
Additionally, the shift technical
advisor
was responsible for maintaining the
technical specification
component condition record log to track equipment
out
of service.
The procedure
governing this log required that equipment that is
out of service through
a shift change
be logged.
While the Train
N AFW pump
was not expected
to be out of service through the shift change, it ultimately
was.
The inspector considered
that this was
a failure to follow procedure.
The Operations
Department
Leader discussed
this weakness
and the expectations
on communications with all licensed operators
during the subsequent
training
cycle.
The licensee
also counselled
members of the crew involved.
The inspector considered
that the failure of operators
to follow procedure
"Technical Specification
Component Condition Record
Sims
Procedure,"
and log the Train
N AFW pump to be
a violation of Technical Specification 6.8. 1 of more than minor safety significance.
The inspector
found that the licensee's
actions
were appropriate.
Additionally, the
inspector
noted that the problem was identified by the licensee
and that there
were
no similar violations identified by either the inspectors
or by the
licensee
which could have reasonably
prevented this occurrence.
This licensee
identified and corrected violation is being treated
as
a non-cited violation,
consistent with Section VII of the
0
e
-27-
9
FOLLOWUP - ENGINEERING/TECHNICAL SUPPORT
(92903)
9. 1
Unresolved
Item 528 9431-01
OPEN
Letdown Isolation Valve Leaka
e
On December
8, the licensee
closed Unit 2 letdown isolation valve CHA-516 and
determined that it did not leak with approximately
2000 psi differential
pressure
across it.
This test supported
the licensee's
analysis
which
concluded that the three letdown isolation valves in Unit 2 could close
against
pressures
established
during
a letdown line break
and prevent
downstream flow from exceeding calculated limits.
The letdown isolation valve
operators
in Units
1
and
3 were replaced
during the past refueling outages
to
resolve the concern that they were undersized.
Earlier in the inspection period, the licensee identified that, in April 1995,
the as-found condition of Unit
1 letdown isolation valve CHB-515 had not been
accurately
described
to engineers
performing
Upon recognizing the flawed Unit
1 operability determinati'on,
the licensee
reperformed
and developed
a reasonable
assurance
that the Unit 2 valves were operable.
Subsequently,
they determined that
an
online test would establish
conclusively that all three Unit 2 valves were
The inspector
concluded that the decision to perform the test
demonstrated
conservative
engineering
and found that the licensee
had
performed substantial
reviews
and exercised
proper caution in performing the
test.
The inspector noted that the failure to properly characterize
the as-found
condition of Unit
1 CHB-515 was another
example of weak engineering.
10
ONSITE REVIEW OF LERs
(92700)
10.1
Closed
LER 528
529
530 93-011
Revision
1:
Potential
Safet -Related
E ui ment Problems
Due to
De raded Grid Volta e and
Closed
LER 528 95-001
Revision 0:
Entr
Into TS 3.0.3
Due to De raded Volta e
10.1. 1
Licensee
Reports
LER 93-011,
Revision
1,
was issued
February 6,
1995,
and noted that
a
previously unanalyzed
condition could occur due to low grid voltage.
The
unanalyzed
condition involved double sequencing
of safety-related
pumps during
an accident.
Following an emergency
safety features
actuation,
the licensee
noted that the potential
existed to not only start sequencing
safety-related
equipment
onto preferred offsite power, but also to initiate load shedding
due
to the Class
1E 4. 16 Kv undervoltage
relays dropping out due to low grid
voltage
and not resetting,
and then resequencing
the equipment
onto the
emergency
diesel
generator.
The licensee
stated if grid voltage were kept above
an administrative limit,
their calculations
indicated that the double sequencing
would not occur.
The
licensee
also discussed
long term corrective actions
and stated that pending
completion of these
actions
the grid would be kept above
100 percent.
-28-
However,
on February
15,
1995, the licensee
entered
Technical Specification 3.0.3,
due to grid voltage falling below 100 percent during
planned
switchyard evolutions.
The licensee
issued
LER 95-001,
Revision 0,
on
Harch
15,
1995, to report the February
15,
1995, occurrence.
10.1.2
Licensee Actions
0
The licensee
issued
a new procedure
specifying operator actions in response
to
a degraded grid and
added
degraded grid voltage to the Unit
1 Plant Monitoring
System displays.
The licensee
stated that the following long term corrective
actions
would make all three units operable
above
98 percent grid voltage,
the
design lower limit.
~
Removal of loads
from Unit 1, the most heavily loaded unit.
~
Addition of an accurate grid voltmeter in Unit 1,
so licensed operators
will have ability to routinely monitor grid voltage.'
Transformer
upgrades
and sequencer
changes.
~
Automatic block of fast
bus transfer.
10. 1.3
Summary of Inspector
Actions During Inspection
Report 95-12
The inspector
reviewed both
LERs, the licensee's
procedure for response
to
degraded grid voltage,
the licensee's
review of the potential for further
occurrences
of degraded grid voltage,
the licensee's
long term corrective
'actions,
and the requirements
the licensee
provided to grid operators.
The inspector
reviewed
Procedure
41AO-IZZ57, "Degraded
Grid Voltage,"
Revision 4.
This procedure
provided operator guidance for all three units for
response
to degraded grid voltage in various plant modes.
The basic action
was to restore
one emergency
bus in each unit by blocking the fast bus
transfer of nonsafety-related
loads to the startup transformers
which supplied
the safety-related
loads.
The inspector
reviewed the affect of blocking the
fast
bus transfer
and determined that licensee calculations
indicated this
block would allow safety-related
voltage to remain
above the degraded
voltage
relay setpoint.
The inspector
reviewed licensee
Letter File 95-005-419.8,
"PVNGS Expectations
Regarding
Evaluations Potentially Affecting Grid Voltage
Range Limits," dated
February
23,
1995,
and noted that grid operational
expectations
were clearly
stated.
The inspector
noted that the licensee
had
used the site main generators
to
raise grid voltage during the February
15 event
and questioned
the licensee
as
to whether grid operators
could have raised this voltage external
to the site
'n
February
15, or during future occurrences
when there
was
no site
generation.
The licensee
provided the inspector
a grid study titled,
-29-
525
Kv Voltage Regulation
Study Report."
This report concluded that the grid
could reliably be maintained
above
98 percent,
without site generation
support.
10. 1.4
Inspector Actions During This Inspection
and Conclusions
The inspector
reviewed licensee
progress
on the long term corrective actions
and determined that the licensee
was still within their internal
schedule for
completion of these actions.
The inspector questioned
control
room personnel
in Unit
1 and determined that they were familiar with offsite power
requirements
and procedure
The inspector
reviewed
updated
licensee calculations.
Based
on this review and the more detailed review
described
in Inspection
Report 50-528/95-12,
the inspector
concluded that the
licensee
had taken corrective actions to identify when
a low voltage condition
existed
on the grid,
and specified proper actions to take to ensure that Palo
Verde units remained
and complied with Technical
Speci.fication
shutdown criteria.
The inspector also noted that the lice'nsee
had provided
reasonable
assurance
of their-intent to complete the long term corrective
actions discussed
above.
I
'
I
,
f
I
0
ATTACHMENT 1
1
PERSONS
CONTACTED
- T
B.
- R.
- R.
- B
- R.
- W.
- A.
J.
- D
- W.
- G
- C
- J
M.
Arizona Public Service
Com an
Cannon,
Department
Leader,
Nuclear Engineering
and Projects
Chapin,
Department
Leader,
Mechanical
Maintenance
Flood,
Department
Leader,
System Engineering
Fullmer, Department
Leader,
Nuclear Assurance
Grabo,
Section
Leader,
Nuclear Regulatory Affairs
Hazelwood,
Engineer,
Nuclear Regulatory
Affairs'de,
Director, Operations
Krainik, Department
Leader,
Nuclear Regulatory Affairs
Levine, Vice President,
Nuclear Production
Mauldin, Director, Maintenance
Montefour, Senior Representative,
Strategic
Communications
Overbeck,
Vice President,
Nuclear Support
Seaman,
Director, Nuclear Assurance
Vellota, Director, Training
Winsor, Section
Leader,
Mechanical
Maintenance
Enginee'ring
1.2
NRC Personnel
e
- D. Kirsch, Chief,
Region
IV Reactor Projects
Branch
F
- K. Johnston,
Senior Resident
Inspector
- D. Garcia,
Resident
Inspector
- J. Kramer, Resident
Inspector
1.3
Others
- F. Gowers, 'Site Representative,
El
Paso Electric
- R. Henry, Site Representative,
Salt River Project
- Denotes those present
at the exit interview meeting held
on December
20,
1995.
The inspector also held discussions
with, and observed
the actions of, other
members of the licensee's
staff during the course of the inspection.
2
EXIT MEETING
An exit meeting
was conducted
on December
20,
1995.
During this meeting,
the
inspectors
summarized
the scope
and findings of the report.
The licensee
acknowledged
the inspection findings documented
in this report.
The licensee
did not identify as proprietary
any information provided to, or reviewed by,
the inspectors.
ATTACHMENT 2
ADV
CRDR
EDH
ERFDADS
gpm
HLO
'ER
HSSV
RWLIS
SBCS
LIST OF ACRONYHS
Atmospheric
Dump Valves
Auxiliary Operator
Condition Report/Disposition
Request
Containment
Spray
Electrical Discharge
Machining
Engineering
Evaluation
Request
Emergency
Response
Facility Data Acquisition Display System
Control System
Gallons
Per Hinute
High Level Over-ride
Heating, Ventilation and Air Conditioning
Licensee
Event Report
Net Positive Suction
Head
'
Refueling Water Level Indicating System
Steam
Bypass Control System