ML17310B398

From kanterella
Jump to navigation Jump to search
Insp Repts 50-528/94-13,50-529/94-13 & 50-530/94-13 on 940329-0507.Violations & Deviations Noted.Major Areas Inspected:Plant Status,On Site Response to Events,Weak Ca,Operational Safety Verifications & Maint Observations
ML17310B398
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 06/02/1994
From: Wong H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17310B394 List:
References
50-528-94-13, 50-529-94-13, 50-530-94-13, NUDOCS 9406300028
Download: ML17310B398 (50)


See also: IR 05000528/1994013

Text

APPENDIX C

U. S.

NUCLEAR REGULATORY COHHISSION

REGION IV

Inspection

Report:

50-528/94-13

50-529/94-13

50-530/94-13

Licenses:

NPF-41

NPF-51

NPF-74

Licensee:

Arizona Public Service

Company

P. 0.

Box 53999, Station

9082

Phoenix,

Arizona

85072-3999

Facility Name:

Palo Verde Nuclear Generating

Station

Units 1,

2,

and

3

t

Inspection At:

Haricopa County, Arizona

Inspection

Conducted:

Harch

29 through

Hay 7,

1994

Inspectors:

K. Johnston,

Senior Resident

Inspector

H. Freeman,

Resident

Inspector

J.

Kramer,

Resident

Inspector

A. HacDougall,

Resident

Inspector

B. Olson, Project Inspector

Accompanying Personnel:

J. Ganiere,

NRR Intern

Approved By:

(

ong,~

Ins ection

Summar

>e,

roJect

rane

~/~/q

ate

Areas

Ins ected

Units

1

2

and

3

Routine,

announced,

resident

inspection

of:

~:

Plant Status

(93702)

On Site Response

to Events

(93702)

Weak Corrective Actions (37551,

40500,

62703

and 71707)

Operational

Safety Verification (71707)

Haintenance

Observations

(62703)

Surveillance Observation

(61726)

Followup

(92901,

92902,

92903,

and 92904)

In Office Review of LERs (90712)

9406300028

940624

PDR

ADOCK 05000528

6

PDR

'

l

I

Results

Units

1

2

and

3

Strengths:

Operator

response

to

a slipped control element

assembly

(CEA) in Unit

1

was

good (Section 2.1).

Plant

and engineering

management

took conservative

action in response

to

operability concerns

with Emergency Diesel

Generator

(EDG)

8 in Unit 3.

In addition,

management

promptly addressed

a safety concern with

electrical splice connections

(Sections

3.2

and 4.1).

~

Good coordination

and communication

were noted during the core off-load

in Unit 3 (Section 5.1).

~

management

involvement in the planning

and

subsequent

oversight of on-

line maintenance

of the pressurizer

spray valve in Unit

1 contributed to

the successful

performance of the job (Section 5.2).

l

e

A maintenance

training instructor displayed

a questioning attitude

and

discovered

a potential safety concern with raychem electrical

splices

(Section

4. 1).

Weaknesses:

Corrective actions:

During the inspection,

three

problems

were identified

that highlighted the licensee's

apparent failure to ensure that previous

inspector identified problems

were aggressively

pursued

and effective

corrective actions

implemented.

~

The licensee

had not implemented

a comprehensive

instrument out of

calibration program

as committed in response

to

a

1992 violation which

highlighted program weakness

(Section

3. 1).

This resulted

in

a

deviation.

~

The inspectors

identified an uncontrolled security badge,

which was

similar to problems identified in NRC Inspection

Report 50-

528,529,530/94-02

in which the licensee

received

a notice of a violation

(Section 3.2).

~

Operators

failed to correctly rack out

a breaker,

which was identical to

problems

the inspector previously identified to the licensee

and

described

in

NRC Inspection

Report 50-528,529,530/94-09

(Section 3.3).

This resulted

in

a violation.

t

Postmaintenance

testing:

A noncited violation highlighted weaknesses

in

postmaintenance

testing

acceptance

criteria'

'

l

1

~

Although two postmaintenance

tests

provided data which could have led to

the identification of incorrectly installed gears

in a motor-operated

valve,

weak acceptance

criteria

and weak test reviews resulted

in the

condition not being identified (Section 8. 1).

Summar

of Ins ection Findin s:

~

One violation was identified (Section 3.3).

~

One deviation

was identified (Section 3. 1).

I,

~

One noncited violation was identified (Section 8. 1).

~

Deviation 528/9326-02

was left open

(Section 9).

~

Violation 528/9340-06

was left open

(Section 7).

Inspection

Followup Items 529/9409-01

and 528/9402-03'ere

closed

(Section 8).

O.

Licensee

Event Reports

528/94-01,

Revision 0; 529/93-04,

Revision 0;

and

530/94-01,

Revision 0, were closed

(Section

11).

Attachment

1:

Persons

Contacted

and Exit Meeting

'

1

l

I

f

DETAILS

1

PLANT STATUS

1.1

Unit

1

Unit

1 began

the inspection period in Hode

1 at 86 percent.

On April 4,

1994,

power was reduced

to approximately

60 percent

in response

to

a slipped

CEA

(see

Section

2. 1).

Power

was raised

back to 86 percent late

on April 4 and

remained

there throughout the inspection period.

The licensee

continued to

monitor

a very small primary-to-secondary

leak in Steam Generator

12,

which

remained

less

than

1 gallon per day.

1.2

Unit

2

Unit 2 began

the inspection period in Hode

1 at 85 percent

power

and

on

Harch 30,

1994,

raised

power to 86 percent.

On April 30, the unit reduced

po ~r to

51 percent for a steam generator

hideout teii.

Power was raised to

86 percent

the

same

day

and remained

there throughout

the inspection period.

1.3

Unit 3

Unit 3 began

the inspection period in Hode

6 and remained

in an outage

conducting refueling operations

throughout the inspection period.

The

licensee

discovered

16 axial crack indications during eddy current inspection

of Steam Generator

32 tubes.

These indications

were similar to those

previously discovered

in Unit 2 steam generators.

The licensee

had conducted

a midcycle outage

at the

end of 1993 specifically to look for but did not find

these

types of axial indications.

During the current outage

the licensee

identified

16 axial indications after chemically cleaning the

steam

generators.

The licensee

expanded

the

scope of the eddy current inspections

to bound the location of the indications.

The licensee

also identified one

axial indication in steam generator

31.

At the

end of the inspection period,

the licensee

was completing

steam generator

tube inspections.

2

ONSITE

RESPONSE

TO

EVENTS

(93702)

2. 1

Sli

ed

CEA

Unit

1

0

On the morning of April 4,

1994,

CEA 36 slipped to approximately

139 inches

(the all rods out position was

147 inches)

during the performance of monthly

CEA exercise testing.

The licensee

declared

the affected

CEA inoperable,

complied with the appropriate

Technical Specification

(TS) requirements

and

began

reducing

power.

About

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> after the

CEA slipped,

the other

CEAs in

Shutdown

Group

B were inserted

to within the

TS limit of 6.6 inches of CEA 36.

At this point, the downpower

was stopped

and reactor

power was stabilized at

about

61 percent.

4

']

The licensee

found

a faulted optical isolator that

was only providing

2 out of

3 phases

of current to the upper gripper of CEA 36.

The card

was replaced

and

satisfactorily retested.

CEA 36 was subsequently

aligned to the other

CEAs in

Shutdown

Group

8 and declared

operable.

Operators

began

a power ascension

and

reactor

power was restored

to 86 percent late

on the evening of April 4.

The inspector

reviewed the licensee's

actions

and concluded that the

licensee's

overall

response

to the event

was good.

The operators

were alert

to earlier problems with CEA 36, quickly entered

the appropriate

TS action

statements

and reduced

power,

and safely recovered

from the condition.

3

WEAK CORRECTIVE ACTIONS

(71707,

62703,

40500)

The following section discusses

three

examples of issues

that

had

been

brought

to th~ licensee's

attention

'he inspectors

in previous inspections.

In the

first example,

the inspector

found that the licensee

had not implemented

a

comprehensive

instrument Out-of-Calibration

(OOC) program despite

a

1992

violation which highlighted program weakness.

In the second

example,

the

in pectors identified

an uncontrolled security

badge,

which was similar in

nature

to

an event identified in

NRC Inspection

Report 50-528,529,530/94-02

in

which the licensee

received

a violation.

The third example

involved the

failure of operators

to correctly rack out

a breaker,

which was identical to

events

described

in

NRC Inspection

Report 50-528,529,530/94-09.

These

events highlighted

a concern regarding the licensee's

apparent failures

to ensure that inspector identified problems

are aggressively

pursued

and

effective corrective actions

implemented.

At the exit meeting,

licensee

senior

management

assured

the inspectors

that they shared

the

same

concern

and

would take action to ensure that these,

and

any subsequent

problems identified

by the inspectors,

would be carefully considered

and fully addressed.

3.1

Review of OOC Pro ram

The inspector

reviewed the

adequacy of the licensee's

OOC program for

instruments that are important to safety to determine

whether adverse

conditions or trends

were identified and corrected.

The primary focus of this

inspection

involved the low lube oil pressure

switches

(LLOPS)

on the

EDGs.

The inspector previously determined that the preventive

maintenance

(PH) tasks

used to calibrate

the

LLOPS did not have guidance

as to when

an

OOC condition

required identification and evaluation

(see

NRC Inspection

Report 50-

528,529,530/94-09

for details).

The inspector

found that the licensee's

OOC review program

was not

comprehensive

for all safety-related

instruments.

In addition,

the inspector

found that:

~

The licensee

had not taken action to ensure that

OOC conditions in the

LLOPS received

reviews,

despite

the fact that repeated

OOC conditions

for these

switches

were the basis of a

1992 Notice of Violations

0

l

~

Similar repeated

OOC conditions in the essential

chiller (EC)

instrumentation

had not received

formal review.

~

The response

to the

1992 violation did not accurately reflect the

licensee's

intended interim corrective actions for OOC reviews.

~

The licensee

was slow to address

the inspector's

concerns,

despite

discussion

with senior

management

in

a previous exit meeting.

3. l. 1

LLOPS

OOC Reviews

In

NRC Inspection

Report 50-528,529,530/94-09,

the inspector

observed

the

calibration of Unit

1

EDG

LLOPS.

The technicians

performing the test noted

that the switches

were acting erratically

and subsequently

replaced

the

switches.

The inspector

noted that there were

no instri ctions provided to t4;

technicians

to indicate

whethe~

an

OOC review was required.

The inspector

noted that the licensee

was

issued

a Notice of Violation in

NRC

Insp

tion Report 50-528,529,530/92-14

due to

a failu e to trend

OOC

conditions with the

LLOPS.

The licensee's

response

to the violation indicated

to the inspector that the licensee

would develop criteria for evaluating

instruments

which exceed

the as-found

acceptance

criteria.

The response

indicated that

a

CRDR would be initiated when instruments

exceeded

the

screening criteria threshold.

At the exit meeting for NRC Inspection

Report 50-528,529,530/94-09,

the

inspector questioned

whether there

had

been

OOC conditions identified on the

LLOPS since

the response

to the violation and whether these conditions

had

received

an engineering

review.

The licensee

conducted

a review and determined that,

from August

1992 until

March 30,

1994,

there

had

been

a total of 33 calibrations of the

LLOPS.

Of

the total, only eight as-found setpoints fell within the

band specified in the

PH instructions

(+0.38 pounds

per square

inch (psi) of the 30 psi decreasing

setpoint).

The percentage

of OOC incidents in this period correlates

well

with the results

reviewed in

NRC Inspection

Report 50-528,529,530/92-14.

The

inspector

found that

no screening criteria

had

been established

for the review

of OOC conditions with the

LLOPS and that

no

CRDRs

had

been initiated.

The inspector also questioned

the licensee

as to whether their failure data

trending

(FDT) program

had identified and documented

any of the

LLOPS

OOC

conditions.

The licensee

conducted

a review and determined that

a majority of

the

OOC conditions

were identified and inputed for trending.

The inspector

concluded that the

OOC conditions with the

LLOPS were identified in the

FDT

system

and were available to the system engineer to identify potentially

adverse

trends.

The inspector

reviewed the significance of the

25

OOC conditions.

Twenty-two

as-found setpoints fell within a band of +3 psi of the setpoint.

This band

'

was determined

to be acceptable

by the licensee

in their review performed

following the violation in

NRC Inspection

Report 50-528,529,530/92-14.

However,

the

LLOPS

PM work orders

(WOs) were not updated to include the H psi

as the acceptance

criteria

and the

22

OOC as-found setpoints

were not checked

to see if an additional

review was necessary.

Three instruments

had as-found setpoints that were outside the z3 psi

band

and

were not evaluated.

On March 30,

1994,

the licensee

issued

a setpoint

basis

document for the

LLOPS and established

a +3.26/-4.61

psi band.

Two of the

three pressure

switches

were inside this band.

The other pressure

switch had

an as-found setpoint of 36.89 psi, which was more than twice the acceptance

criteria.

The inspector

asked

the licensee

to evaluate

the significance of the

one

pressure

switch whose setpoint

was outside

the calculated

band.

The licensee

determined

that this one

OOC was not signiricant

based

on

a statistical

analysis of the expected drift of these particular pressure

switches

and the

narticular function of the switch.

The inspector

reviewed 'the licensee's

setpoint calrulatior

and the previous

CRDR desc~ibing

the function of the

LLOPS and concluded that the

one switch being

OOC was not safety significant.

3. 1.2

Condition of

EC Instruments

Based

on the

above review and several

discussions

with the licensee,

the

inspector determined that the licensee's

OOC program did not include the

quality class

instruments that were not directly related to TS and were

calibrated

using

a routine

PM work order.

The inspector discussed

this

concern

to the licensee.

The licensee's initial response

was that the issue

did not represent

a programmatic

weakness

and that they had met their

commitments

as expressed

in the

1992 response

to the violation.

Additionally,

they placed confidence

in the system engineer's

review of the

FDT reports for

their systems.

The inspector questioned this response.

The inspector

concurred that the

OOC conditions

on the

EDG

LLOPS had not been safety

significant.

However,

the review performed to demonstrate

the lack of safety

significance

was largely in response

to the violation in

NRC Inspection

Report 50-528,529,530/92-14.

The inspector questioned

whether there

were

other safety-related

instruments

which were not receiving

OOC reviews

and were

also not included in the

FDT program.

To substantiate

the potential

programmatic

weakness,

the inspector

reviewed

the

PM tasks to calibrate

several

instruments

important to the operation of

the

EC.

The

ECs provide

room cooling

or safety-related

equipment

and ensure

control

room habitability during accident conditions.

The inspector

reviewed

the last work order for each of the six

ECs

(two per unit)

and noted that the

as-found setpoints of three out of 12 low lube oil pressure differential

pressure

switches

(LLOPDPS) were outside the acceptance

band.

Additionally,

the inspector

noted that the compressor

bearing

high oil temperature

switch

could not

be calibrated

and the switch was replaced.

The inspector

found that

no

CRDRs

had

been initiated to review these conditions.

'

The inspector

asked

the licensee

to determine

the significance of these

OOC

conditions.

The licensee

determined that the most significant

OOC condition

was the

LLOPDPS

as found setpoint of 19 pounds

per square

inch

differential (psid) vice

13 psid.

The licensee

determined that the normal

differential pressure

was 24-28 psid.

Therefore,

the lube oil differential

pressure

would have to change

about

5 psid before the chiller would

potentially trip with a

19 psid setpoint.

The licensee

concluded that this

particular

00C condition was not safety significant.

The inspector

agreed

with the licensee's

conclusion.

The inspector

asked

the licensee

to determine if the

OOC conditions were

identified by the

FDT program.

The licensee

determined that the

OOC

conditions were not inputed in the

FDT data

base.

The inspector

reviewed the

licensee's

procedure for inputing data into the

FDT program

and determined

that the program did not consider

OOC condition.

as failures.

As

a result,

OGC conditions identified by routine

PM tasks

were riot generally entered

into

the

FDT data

base.

In December of 1993, the licensee

provided guidance to the

work planners

to input any

OOC conditions that are greater

than two times the

acceptance

criteria.

The inspector

noted thai th:

OOC conditions with the

EC

instruments

occurred prior to this time.

The inspector

concluded that the

licensee

did not have

any programmatic

requirements

to screen

PM tasks for OOC

conditions for entry into the

FDT program.

The inspector considered this to

be significant because

the overall

OOC program relied

on the

FDT program to

identify any potentially adverse

trends.

3. 1.3

Licensee's

Response

to Violation 9214-02

Based

on the inspectors

findings, the licensee

took

a broader look at the

setpoint basis

program

and identified approximately

240 safety-related

instruments that were included in the setpoint basis

program

and were not

calibrated

as part of a

TS requirement

or to support

a

TS required test.

The

licensee

committed to review these particular instruments

and to ensure that

the

FDT program

was capturing all the

OOC data for identification and possible

evaluation.

The licensee initiated

CRDR 9-4-0287 to perform the

investigation.

The inspector

noted that,

in response

to the violation in

NRC Inspection

Report 50-528,529,530/92-14,

dated

August 7,

1992,

the licensee

stated that

~

the following.corrective actions

would be taken to ensure failed instrument

loop components

were properly identified, evaluated,

and dispositioned:

~

.

Screening criteria

and threshold

would be developed for use

by the work

group supervisors

to identify which instrument loop components

that

exceed

the specified

as-found test

acceptance

criteria required further

evaluation

by the engineering

organization.

Preventive

maintenance

and surveillance testing

procedures

would be

revised to require the initiation of a condition report/disposition

request

(CRDR) when instruments

exceed

the screening criteria threshold

limits.

The inspector

questioned

the licensee

on

how they met the above

commitment for

the approximately

240 safety-related

instruments

described

above.

The

licensee

responded

that it had not been their intent that the response

to the

violation apply to these

instruments.

Their intent was that the commitments

would apply only to those

instruments

which were required to be tested

in the

TS or were

used to support

TS required testing.

The inspector

reviewed the

licensee's

documentation

used to develop the corrective actions

in response

to

the violation and found that the licensee's

intqnt was not well established.

Upon further review, the inspector

considered

that none of the licensee

personnel

involved had

a clear understanding

of the overall

.00C program

and

that there

was substantial

confusion regarding

the nature of the corrective

actions.

It was apparent

to the inspector that this confusion resulted

in the

differences

between

the licensee's

letter

and the actions that were taken.

The inspector

found that the licensee's

letter was clear in'ts commitment to

apply the

OOC review screening criteria threshold 1'mits to the

PH tasks

performed

on the

LLOPSs.

This conclusion

was

based

on the fact that the

letter responded

to

a violation concerning

these

same

instruments

and that the

letter did not exclude these

instruments

or any category of safety-related

instrumentation.

Based

on this, the inspector determined that the licensee's

failure to apply the screening criteria to the

LLOPS

PH tasks

was

a deviation

from their commitment in the letter (Deviation 528/9413-01).

F 1.4

Licensee

Response

to Inspector's

Findings

At the exit meeting for this inspection report,

the licensee

committed that

they would perform

an in-depth evaluation of the

OOC review program to

determine

the extent of instruments

not presently

covered

and committed to

evaluate

the calibration history of safety-related

instruments

which had not

received

previous review.

The inspector

noted that these

steps

were

appropriate.

However,

the inspector

found that the licensee

had

been

slow to

take

a broader look at the overall

OOC program after the inspector raised

the

specific concerns

with the

LLOPS.

For example,

on Harch 8,

1994,

the inspector noticed that there

was not any

guidance

in the field as to when

an engineering

review of OOC conditions

was

required.

The inspector notified Unit

1 management

of the concern

on

approximately

Harch

11.

On Harch

14, the inspector discussed

the problem with

the

EDG system engineer

and the Instrumentatio

and Control supervisor

responsible

for the procedure

to calibrate

the

LLOPS.

By Harch

18, the

inspector

brought the issue to

a representative

from licensing

and the

Instrumentation

and Control supervisor responsible

for the

OOC program.

Finally, during the exit meeting for the previous inspection period at the end

of Harch,

the inspector

communicated

the concerns

about the adequacy

of the

OOC program

and the specific concerns

about the condition of the

EDG

LLOPS to

senior

management.

,

I

-10-

In early April, the licensee

conducted

a review of the condition of the

LLOPS

but had not initiated any corrective actions to review the adequacy of the

overall

OOC program.

At that time, the inspector

was again forced to discuss

with senior

management

the potential

programmatic

weaknesses

with the

OOC

program.

By the

end of April, after the inspector

had additional

meetings

with the supervisors

responsible

for the

00C program,

the licensee finally

initiated

an evaluation of the overall

00C program.

3.2

Em lo ee Control of Automatic Controlled Access

Device

and Dosimetr

Units

1

2

and

3

On May 3,

1994,

the inspector

observed

an unattended

automatic controlled

access

device

(ACAD) and dosimetry near the Unit 2 radiological controlled

area

(RCA) exit.

The inspector contacted

plant security,

who subsequently

took control of the

ACAD.

Further investigation revealed that the items were

inadvertently left there

by

a contract

employee.

The licensee initiated

a

CRDR to evaluate

the event.

The inspector

had identified recurring events

where the licensee

employees

had failed to properly control

ACADs and

dcsimetry.

On January

25,

a contract

employee

removed his

ACAD and dosimetry while

working within the radiologically controlled area.

The licensee

received

a

violation for this event (Violation 529/9402-01).

The licensee's

corrective

actions

included suspending

all work by the contractor

and conducting

crew

briefings to emphasize

the responsibility of personnel

to wear

and control

their ACADs and dosimetry at all times.

The inspector

concluded that, unlike

the January

25 event,

where

an employee consciously

removed the

ACAD and

dosimetry to perform work, the employee

who removed his

ACAD and dosimetry

on

Nay 3 unintentionally left the items near the radiologically controlled area

exit.

On February

7, the inspector

noted several

instances

where personnel

were

wearing their dosimetry in the incorrect location

(see

NRC Inspection

Report 50-528,529,530/94-02

for details).

The licensee

acknowledged

the

problem.

The licensee

committed to have all managers

and supervisors

review

with their employees

the proper location for the dosimetry

and

ACAD and

committed to review employee training/retraining to determine if the location

was properly defined.

At the exit meeting,

the inspector

expressed

concern that licensee

employees

appeared

to have

a lack of sensitivity towards their responsibility to

properly wear

and maintain

ACADs and dosimetry.

The licensee

was performing

a

CRDR evaluation for the

Hay

3 event.

3.3

Load Center Breaker - Unit 3

On April 6,

1994,

the inspector

observed

a safety-related

480V breaker

in

Unit 3 racked out with its closing springs not discharged.

The inspector

notified the shift supervisor

who immediately

had the breaker correctly racked

out.

I

0

-11-

Procedure

430P-3PGOI,

Revision 3,

"480V Class

IE Switchgear,"

Appendix J,

required that the closing springs

be discharge

as indicated

by the "springs

charged" indicator on the face of the breaker

when

a breaker is racked out.

The inspector

concluded that the operator failed to follow Procedure

430P-

3PGOI, which is

a violation of TS 6.8. 1 (Violation 530/9413-02).

The inspector

had noted several

previous

instances

where the licensee failed

to follow procedures

and incorrectly racked out load center breakers.

On

February

24, the inspector

observed

a charging

pump breaker in Unit 3 not

correctly racked out (closing springs

not discharged)

with a clearance

tag

attached

to the breaker.

On February

28, the inspector

checked that vital

load center breakers

in all three units

and discovered that

18 of 39 breakers

were incorrectly racked out.

The licensee initiated two

CRDRs to address

the

incorrectly racked out breakers.

The licensee

performed

an inspection of the

load center breakers

to ensure

they were all correctly racked out.

Operations

management

made

an entry into the night order book indicating management

expectations

for operators

to correctly rack out breakers.

The inspector

considered

these

instances

where the licensee failed to

correctly rack out breakers

to be

a noncited violation (see

NRC Inspection

Report 50-528,529,530/94-09).

The problem was not cited based

on the low

safety significance of the events

and

on the licensee's

indicated corrective

actions.

The April 6 event

was considered

a cited violation because it was

determined to be

an event which should

have

been

prevented

by previous

corrective actions.

The inspector

reviewed the corrective actions for the April event.

The

licensee

again performed

an inspection of the load center breakers

to ensure

they were all correctly racked out and

made another entry into the night order

book indicating management

expectations

for operators

to correctly rack out

breakers.

The licensee

then closed the

CRDR to "trend."

The

CRDR did not

address

why the operators

had not properly racked out the breaker.

It was not

apparent

in the

CRDR discussion

whether this event

had ever

been discussed

with the operators.

At the exit meeting,

the inspector questioned

whether

a

thorough review had

been

performed.

The inspector

noted that guality Assurance

(gA) had reviewed the

CRDR written

for the February

28 events

and

had identified that the time allowed to

complete the corrective actions

was excessive.

The changes

to the electrical

PHs were not scheduled until August

31

and the training for nuclear operators

and maintenance

personnel

was not scheduled until October 30.

In addition,

gA

requested

that engineering

address

the implications of having the load center

breakers

in the drawout (fully racked out) position since the vendor technical

manual

indicates that the breakers

are not designed

to be left in the drawout

position.

The inspector

agreed with the

gA assessment

that the planned

corrective actions for the, February

events

were not timely and noted

gA

performed

a thorough review of the issue.

'

J,,

I

-12-

4

OPERATIONAL SAFETY VERIFICATION

(71707)

The inspectors

performed this inspection to ensure that the licensee

operated

the facility safely

and in conformance with license

and regulatory

requirements

and that the licensee's

management

control

systems effectively

discharged

the licensee's

responsibilities for safe operation.

The methods

used to perform this inspection

included direct observation of

activities

and equipment,

observation of control

room operations,

tours of the

facility, interviews

and discussions

with licensee

personnel,

independent

verification of safety

system status

and

TS limiting conditions for operation,

verification of corrective actions,

and review of facility records.

4. 1

Environmental

ualification of Electrical

S lice Connections

- Units

1

2

and

3

On April 22,

1994,

the licensee

identified

a potential

generic

problem with

the environmental qualification of electrical

splices

manufactured

by Raychem

u :d to seal

4160

V electrical

connections.

During site training in which

electrical

maintenance

personnel

were being trained

on vendor

and site

instructions

on the installation of Raychem splices,

an instructor opened

a

completed

connection

and discovered

that the

2 inch wide adhesive strip

applied over

a joint had not fused to the outer casing.

The licensee

tested

additional splices

and discovered that in some instances,

even

when the

vendor's instructions

were strictly adhered to, the splices

may not completely

seal.

The inspector

noted that the instructor's

questioning attitude

was

a

strength.

The licensee

conducted

a plant review board

(PRB) meeting to discuss

the

safety significance of the issue.

The licensee

determined that the splices

were

needed

to ensure that safety-related

motors were not adversely affected

by

a high energy line break

(HELB) which would result in a

100 percent

humidity environment.

The licensee

determined that the only safety-related

components

that would be vulnerable to

a

HELB and also

needed for safe

shutdown of the plant were the two low pressure

safety injection (LPSI) pumps,

the two containment

spray

(CS)

pumps,

and the motor driven auxiliary feedwater

pump.

The licensee

concluded that they had

a reasonable

assurance

that these

pumps were operable,

This conclusion

was

based

on the fact that these

pumps

were not subjected

to

a

100 percent

humidity environment

and,

based

on the

testing they conducted,

that they had

a reasonable

assurance

that the splices

were at least partially bonded,

The

PRB members

concluded that although they believed the affected

pumps were

operable,

they had

a potential

concern that needed

to be quickly resolved.

As

a result,

by April 23, the licensee

completed

inspections

of the motor

connections

for the

10 affected

pumps in the operating units.

Since Unit 3

was in an outage,

the inspections

were scheduled

prior to entering

mode 4.

The inspector

attended

the

PRB meeting

and concluded that the licensee's

operability determination

and initial inspection

plan were appropriate.

e

)

I

-13-

On May 5, the licensee

completed all the inspections

of the motor connections.

Six of the connections

were determined

to be satisfactory

and nine were

determined

to questionable.

The licensee

conducted

additional testing that

demonstrated

that

a complete

seal

would occur if the outer casing

was heated

until the surface

developed

a glossy appearance.

The vendor determined that

reheating

the surface of the splice

and using

a glossy

appearance

as the

acceptance

criteria was acceptable.

The nine questionable

connections

were

subsequently

reheated

and the affected

pumps

were returned to service.

The

licensee

could not conclusively determine if the splices that were reheated

were degraded

and if they would have prevented

moisture intrusion in

a

100 percent

humidity environment.

The licensee initiated

CRDR 9-4-0254 to

evaluate

the significance of the conditions

and

any potential

generic safety

issues.

The licensee

also sent

a Nuclear Network note to the industry

on the

issue.

The inspector

concluded that the licensee's initial resulution of this

potential

problem was good.

The licensee

scheduled

a meeting with Raychem to

determine

the extent of changes

to the installation procedure.

The inspector

planned

to attend

the meeting to ensure that any generic

concerns

were

adequately

resolved.

At the exit meeting,

the licensee

indicated their

intention to submit

a voluntary licensee

event report

(LER) describing

the

potential

safety concern with these particular

Raychem splices.

4.2

EDG

B 0 erabilit

Determination

Unit 3

On May 6,

1994,

the licensee

declared

EDG

B inoperable

due to

a engineering

concern with five rocker

arms that were hardness

tested

and determined

to have

less

than

an acceptable

yield strength.

In April the licensee

conducted

hardness

tests of the rocker arms

on

EDG

B and

found that

12 rocker

arms

had

a yield strength

less

than

25 thousand

pounds

per square

inch (ksi).

The vendor

recommended

value

was greater

than

32 ksi

and the licensee

had performed

an analysis that concluded that greater

than

25 ksi would be acceptable.

The licensee

only had nine rocker

arms in the

warehouse

and there

were

no more available

from the vendor.

As

a result,

the

licensee

replaced

seven of the rocker arms,

kept two rocker arms for spares,

and conducted

an analysis

to accept

the five other rocker arms

as is.

EDG

B

was retested

and declared

operable

on April 21.

Engineering

management

decided to perform an independent

assessment

of the

conditional release

and

10 CFR 50.59 evaluation to validate the decision to

declare

EDG

B operable.

The review team did not identify any specific issues

that would invalidate the acceptance

of the five rocker arms.

However,

they

did raise

issues

concerning

the rigor of the engineering justification for

determining the acceptably of the condition.

Based

on these

concerns

and

a

recommendation

from engineering

management,

the Unit 3 plant manager

conservatively

declared

EDG

B inoperable

on May 6.

At that time,

EDG A was

also inoperable

to repair

a leak in the

6L cylinder jacket water line.

'

j

I

0

-14-

The licensee

appropriately

entered

the

TS action statement

for two inoperable

EDGs in Mode 6.

The action statement

required

suspension

of any core

alterations

and to ensure that at least

23 feet of water over the reactor

vessel

flange

was available.

At the time,

EDG

B was declared

inoperable,

the

licensee

had drained

the refueling water level to the reactor flange

(114

feet)

and

was beginning to install the reactor vessel

head.

The licensee

stopped

the

head installation

and flooded the refueling cavity back

up to 137

feet.

The inspector

concluded that the licensee's

actions to declare

EDG

B

inoperable

and reflood the refueling cavity were conservative.

The inspector

will review the licensee's

basis for initially declaring the

EDG operable with

the five marginal

rocker arms

and the licensee's

final resolution of the

operability concern during ongoing inspection of the

EDGs.

0

5

MAINTENANCE OBSERVATIONS

(62703)

During the inspection period,

the inspectors

observed

and reviewed the

sel <<ted maintenance

activities listed below to veri "y conpliance

vith

regulatory requirements

and licensee

procedures,

required quality control

department

involvement,

proper

use of safety tags,

proper equipment

alignment

and

use of jumpers,

personnel

qualifications,

appropriate radiation worker

practices,

calibrated test instruments,

and proper post-maintenance

testing.

Specifically, the inspectors

witnessed

portions of the following maintenance

activities:

5. 1

Outa

e Activities - Unit 3

On March 30,

1994,

the inspector

observed

core off-loading.

The inspector

reviewed the core reloading

procedure

and witnessed

the off-load of

approximately eight fuel assemblies.

The inspector

noted

good coordination

and communication

between

the refueling senior reactor operator

and the

control

room.

The inspector

also observed

the installation of main steam safety valves,

the

disassembly

and inspection of a reactor coolant

pump thrust bearing,

and the

installation of the

EDG

B connecting

rod.

The inspector

concluded that these

activities were appropriately

conducted.

5.2

Pressurizer

S ra

Valve Maintenance

Unit

1

On April 5,

1994,

the licensee

made

a containment

entry to repack pressurizer

spray valve

100E which had

been isolated

due to excessive

packing

leakages

The licensee

had

made several

attempts

to tighten the valve packing but was

unable to reduce

the leakage

into the reactor drain tank (see

NRC Inspection

Report 50-528,529,530/93-55

for details).

The inspector

reviewed the

licensee's

plan for conducting the maintenance

and the methods

used to

determine that the single valve isolating the spray valve was not leaking.

The inspector

noted that the licensee

had good controls to verify the

condition of the isolation valve.

'

t

'

-15-

The licensee

completed

maintenance

and testing of the spray valve

and returned

it to service

on April 6.

The inspector

concluded that the maintenance

activity was well coordinated

between

the maintenance,

engineering,

and

operations

departments.

Additionally, the inspector

observed

a high level of

management

involvement in the activity.

On April 9, the licensee

began to see

a rise in the leakage

into the reactor

drain tank.

Another containment entry was

made

and

a leak of about

10 gallons

an hour was identified from the bypass

valve for Spray Valve 100E.

The spray

valve was subsequently

isolated.

The inspector discussed

this problem with

the licensee

and determined that the leak on the. bypass

valve was previously

being hidden

by the large

amount of leakage

from Spray Valve 100E.

As

a

result,

the licensee

had not planned to repack the bypass

valve when they

repacked

Spray Valve 100E.

The inspector

concluded that the licensee's

actions to detect

the leakage

and again i"olate Spray Valve 100E were

appropriate.

.3

~EO

L

lid <<h

d

On April 6,

1994, during monthly testing of the Unit

2

EDG B, the licensee

noted

an unusual

noise in the diesel's

Cylinder 4L.

The licensee

removed

the

cylinder head

and found that the cylinder's intake crosshead

roller, which

transfers

the

cam lobe profile to the push rod,

had seized.

The licensee

replaced

the crosshead

assembly

and performed

several

inspections

to determine

the scope of the damage.

On April 8, during post maintenance

testing,

the licensee

discovered

that

Cylinder 4L was not firing.

During subsequent

inspection,

the licensee

found

that the exhaust

valve crosshead

was stuck in the inserted position, holding

the exhaust

valves

opens

The licensee

removed the

4L cylinder head

and

replaced it with an identical

assembly

from the Unit 3

EDG B.

The original

Cylinder 4L was quarantined

for a root cause

evaluation.

At 5:46 a.m.

on April 9,

EDG

B tripped

as

a result of a spurious

overspeed

signal during the postmaintenance

testing.

At 8 a.m.

the licensee initiated

enforcement discretion discussions

with NRC management

since the 72-hour

action statement

was

due to expire in 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.

With the

EDG inoperable,

the

plant

TS would require

a plant shutdown.

The licensee

requested

an 18-hour

extension of the 72-hour action statement

to troubleshoot

and correct the

overspeed trip system

problems,

to perform final inspections

of the

EDG,

and

to test the

EDG.

At 12: 15 p.m. the

NRC granted

a notice of enforcement

discretion,

agreeing

to an 18-hour extension of the action statement.

The inspector

observed

the installation of the

new crosshead

assembly,

observed

the troubleshooting

of the overspeed trip, attended

the licensee's

Plant

Review Board,

and revie.jed the licensee's

basis for requesting

an

extension of the action statement.

The inspector

concluded that the licensee

took

a deliberate

and safe

approach

to restoring the operability of the

EDG.

Additionally, the inspector

reviewed the licensee's

inspection criteria

and

e

-16-

concluded that they provided

a sufficient level of confidence that the problem

was isolated to Cylinder 4L.

The licensee

determined that the overspeed trip was caused

by

a loose bracket

on

a limit switch in the

EDG's overspeed trip system.

The licensee

readjusted

and successfully

tested

the bracket.

The trip input was part of the

EDG's

maintenance

testing trip system

and would not have resulted

in an

EOG trip had

it been started

in the emergency

mode

The licensee

subsequently

completed

EDG testing

and declared

the

EOG operable.

The licensee

and

a vendor representative

conducted

an inspection of

Cylinder 4L after the engine

was declared

operable,

The licensee

and vendor

concluded that there

was

no abnormal

wear

on the crosshead

or cam follower.

The licensee

',nitiated

CRDR 2-4-0148 to perfor!! a root cause of failure

analysis of the crosshead

failures.

The inspector

met with the system

engineers

to discuss

the

scope of the evaluation.

The inspector

asked

the

engineers

whether

a

CRDR was initiated t~ eve> nate the safety significance

and

transportability of ;he overspeed trip.

The

ic .nsee

determined that although

the system engineer

was working on the issue,

a

CRDR was not initiated to

document

the evaluation.

The system engineer initiated

CRDR 2-4-0169 to

document

the evaluation of the over speed trip.

The inspector will review the licensee's

evaluation during ongoing inspection

of the licensee's

corrective actions.

5.4

S ra

Pond

Pum

Bushin

and Sleeve

Oama

e

Unit 3

Early in the Unit 3 refueling outage,

the licensee

discovered

pieces

from

Spray

Pond

Pump

B in the Train

B essential

cooling water

(EW) heat

exchanger

inlet bowl.

The licensee

had scheduled

an inspection of the Train

B

EW heat

exchanger after they had identified

a rattling noise in the heat

exchanger.

Subsequent

to the heat

exchanger

inspection,

the licensee

inspected

Spray

Pond

Pump

B and found that the pieces identified in the heat

exchanger

corresponded

to damage

to

a sleeve for the

bowl bearing

(located

on the pump's shaft

above

the impeller).

The bowl bushing

and the spider bushing

(located

midway on the

pump shaft),

both

made of Buna-N rubber,

were also

damaged.

The inspector

observed

portions of the work and reviewed the licensee's

safety evaluation.

The spray

pond

pumps

are

deep draft

pumps which supply ultimate heat sink

cooling the

EW heat

exchanger

and to diesel

generator

systems.

The

pumps

have

four bearing surfaces.

The inboard bearing

has

a graphite

bushing

and the

outboard

bearing

has

a bronze bushing.

Both the

bowl

and spider bearings,

which are approximately

12 inches long, were originally supplied with Buna-N

bushings.

These

bushings,

which are held in place

on the

pump housing,

ride

against stainless

steel

sleeves

which are affixed to the

pump shaft.

The

licensee

has not perFormed

maintenance

on these

bearing

since original

installation.

I

1

-17-

The pieces that

had broken

from the Spray

Pond

Pump

8 bowl bearing

sleeve

were

from the upper

end of the sleeve

and represented

a

180 degree

section

approximately

2 inches

long.

The cracking

appeared

to start at

a key-way on

the top of the sleeve.

The licensee

found that the

bowl bearing

sleeve

had

low tensile strength

and low ductility and

was filled with porosities.

The

licensee

surmised that these deficiencies

resulted

from a bad casting.

The inspector

noted to the licensee

that the

pump vendor

had previously

supplied

substandard

components.

In one case,

a subsupplier for the vendor

had supplied

a

pump impeller which had not been properly heat treated.

The

licensee

followed up by asking the vendor to review the traceability of the

damaged

sleeve

and the sleeves

on all six Palo Verde spray

pond

pumps.

At the

end of the inspection period,

the vendor

had not provided

an

answer

.

The licensee

found the

bowl bushing to be damaged.

The Buna-N surface

appeared

hardened

and substantially tom around in the area

where the sleeve

was

damaged.

The area

below the

damaged

part of the sleeve

was hardened,

but

intact.

The licensee

concluded that the majority of the

damage

was

due to the

damaged

sleeve.

The licensee

found the spider bushing

Buna-N to be severely

damaged.

It. was

found to be hardened

and swollen.

The licensee

discussed

this with the rubber

supplier

who concluded that the

damage

was due to heat.

The licensee

considered

whether the heat

was chemically induced. 'he licensee

reviewed

current spray

pond chemistry

and found it to be comparable with the Buna-N.

However,

the licensee

recognized that past chemistry controls of the spray

ponds

may have not been

comparable.

At the

end of the inspection period,

the

licensee

was assessing

the source of heat to the bushing.

The licensee

replaced

the Buna-N bushing material with bronze material

supplied

and approved

by the vendor

and reinstalled

the

pump.

Subsequently

the licensee

removed

Spray

Pond

Pump

A for inspection.

The bowl bushing

was

found to be hardened

but intact.

The spider bushing

was found to be

significantly degraded,

comparable

to the

Pump

B spider bushing.

Both

bushings

were replaced with bronze material.

Both the associated

sleeves

were

intact.

At the

end of the inspection period,

the licensee

was planning to

examine

the material of the Spray

Pond

Pump

A sleeves

to determine

whether

they were properly cast.

The licensee

reviewed both the operation histories of Spray

Pond

Pumps

A and

B

and found that

pump performance

data provided

no indication of pump

degradation.

In addition,

the licensee

reviewed records of pump starting

currents

and determined that there

had

been

no significant changes.

The

licensee

requested

the vendor to provide

a design review of the spider bearing

and to review the capability of the spray

pond

pumps in the degraded

condition.

Preliminarily, the licensee

determined that the bearing

was to

provide shaft stability dur'ing

pump starts.

In the as-found condition, the

spider bearing

appeared

to provide adequate stability.

The licensee

determined that in the as-found condition,

the

pump was capable of performing

its safety related function.

They requested

the

pump vendor to evaluate

the

l

I

i

l

-18-

ability of the

pumps to operate

continuously for 30 days with the bearings

in

the degraded

condition.

The inspector

found the interim evaluation to be acceptable

and will follow

the licensee's

continued evaluation of the spray

pond

pumps.

6

SURVEILLANCE OBSERVATION

(61726)

The inspector

observed

portions of a Unit 3 7-day surveillance test of station

batteries

procedure

32ST-9PK01.

The inspector

concluded that the test

was

conducted

in accordance

with TS and approved

procedures.

7

FOLLOWUP OPERATIONS

(92901)

7. 1

fO en

Violation 528 9340-06:

Overtime Limit Exceeded

This violation occurred

when

one individual exceeded

the work hour limitations

nf TS 6.2.2. I.b.

The occurrence

would have

been

considered

a noncited

!iolation; however, after the issue

was recognized,

the inspector

found that

gA had identified other instances

where the work hour limitations had

been

exceeded.

The licensee's

corrective actions

included issuing

a temporary

Stop

Work

Notice prohibiting affected

Palo Verde departments

from taking exceptions

to

the Overtime Policy until interim corrective actions

were implemented,

issuing

a corrective action report

(CAR) to track

and verify corrective actions,

and

initiation of an investigation.

The inspector

reviewed

CAR 93-0179 which identified five areas for evaluation:

(1) the computer report

used to identify overtime violations,

(2) the accuracy

and timeliness of time tickets/data

entry,

(3) Procedure

02AC-OEHOI, "Overtime

Limitations," (4) the noncompliances

with overtime exceptions,

and

(5) communication

and training.

At the time of the inspection,

the licensee

had not completed all of the evaluations,

and

a recent

gA audit identified

additional

instances

where work hour limitations had

been

exceeded.

The inspector

observed that the licensee

monitors work hours

and that large

numbers of personnel

have not exceeded

work hour limitations.

Therefore,

the

inspector

concluded that

a breakdown of the licensee's

program

has not

occurred.

This item remains

open pending the identification and

implementation of corrective actions

associated

with CAR 93-0179.

8

FOLLOWUP NAINTENANCE

(92902)

8.1

Closed

Ins ection Followu

Item 529 9409-01:

Hi

h Pressure

Safet

In ection Valve Postmaintenance

Testin

PHT

Unit 2

This item involved the failure of a

HPSI cold leg header flow

control/isolation valve to close during design differential pressure

testing

in Unit 2.

The licensee

determined that the valve would not close

because

the

'

/

e

-19-

actuator

gears

were incorrectly installed during corrective maintenance

performed

in April 1993.

This item was

opened

to determine

why the

PMT did

not identify this error.

The incorrect installation of the actuator

gears

resulted

in

a valve stroke

time approximately half of the normal stroke time.

Two postmaintenance

tests

performed in 1993,

an

ASME Section

XI stroke test

and

a static diagnostic test

of the motor-operated

valve

(MOV), included data which showed the reduced

stroke time.

However,

the licensee

did not recognize that this data

demonstrated

a degraded

condition in the actuator.

The inspector

reviewed the

PMT to determine

why the licensee

did not identify the reduced

valve stroke

time.

The inspector

noted that the purpose of the

MOV full diagnostic test

was to

verify the capability of the valve to perform its design function.

Therefore,

the primary function of the diagnostic test

was to ensure that the operator

developed

enough thrust to operate

the valve under design basis conditions.

The inspector

found that the diagnostic testing

procedure

i'ncluded

a checklist

used

to determine

the condition of the

MOV.

The cf ecklist included

18 specific inspection criteria (e.g,, thrust/torque

outside target

band) with

acceptance

criteria of either

"Yes" or "No" for both the as-found

and the as-

left diagnostic tests.

The inspector

was informed that the purpose of the

checklist

was to compare

each

one of these

individual acceptance

criteria and

ensure

the as-left condition was satisfactory.

The inspector

concluded that

this approach

would provide

18 separate

"snapshots"

of the valve's

performance.

However,

the diagnostic test

was not used to ensure that the

maintenance

activity was correctly performed

and did not provide

an overall

assessment

of the valve's

performance.

The inspector

noted that there

was not

a requirement

in the retest

section of

the work order or in the diagnostic testing procedure

to compare

the as-left

to the as-found

valve signatures

to identify any differences

in the traces,

Had the signatures

been

compared,

the traces

would have clearly showed that

the as-left stoke time was about one-half the as-found stroke time.

The inspector

also noted that the entire

PMT was not completed

by the

same

organization.

Specifically, the valve services

group

who performed the

maintenance

relied

on the

ASME Section

XI test group to verify proper valve

stroke time.

The valve services

engineers

assumed

the Section

XI test would

identify not only slower but faster valve stroke times.

Additionally, the

planners

appeared

to rely on existing test

procedu> es to develop the retest

requirements.

These existing procedures

may not have all the specific

acceptance

criteria for the maintenance

that

was

performed'ased

on this review, the inspector

concluded that the licensee

did not have

appropriate

acceptance

criteria in the full diagnostic test to identify the

maintenance

error with the gear changeout.

This is

a violation of 10 CFR Part 50, Appendix

B, Criteria V, which states

in part that procedures

shall

include appropriate quantitative or qualitative acceptance

criteria for

determining that important activities

have

been satisfactorily accomplished.

0

'

-20-

The inspector

noted that,

in March 1994,

the licensee's

testing

program

and

subsequent

evaluation of the valve's failure to close identified the problem

with the incorrectly installed gears.

The licensee's initial actions to

correct the maintenance

error

and evaluate

the significance of the condition

were appropriate.

As long-term corrective action,

the licensee

changed

the

MOV diagnostic

procedure

to ensure

the as-left

and as-found valve stroke times

are within ~5 percent of each other.

The inspector

concluded that these

corrective actions

were appropriate

to prevent

a similar problem with

installing the wrong gears

in the

MOV actuator.

At the exit meeting,

the

licensee

stated that the qualitative comparison

between

the as-left

and as-

found valve signatures

was included

as

a corrective action to the diagnostic

procedure.

Additionally, the inspector

noted that the safety significance of the valve

not closing

was low because

the primary safety functi~.. of the valve was to

open.

The basis for this observation

was discussed

in

NRC Inspection

Report 50-528,529,530/94-09.

The inspector also noted that although the

licensee

did not promptly respond to the inspector's

questions

concerning

the

adequacy of the

PMT, the final corrective actions

t'rom the 60-day

CRDR

evaluation of the event

appeared

to address

the problem with the post

maintenance

diagnostic testing.

Based

on these

considerations

the violation

is not being cited because

the criteria specified

in Section VII.B of the

Enforcement

Policy were satisfied.

8.2

Closed

Ins ection Followu

Item 528 9402-03:

Atmos heric

Dum

Valve

PMT

This followup item involved

a review of the licensee's

evaluation of the

required retests

for atmospheric

dump valve

(ADV) maintenance.

In January

1994,

the licensee

discovered that they did not perform

a nitrogen drop test

as

a retest after maintenance

on ADV-178.

The purpose of the drop test is to

verify system integrity and ensure

there is enough nitrogen to stroke the

ADYs

on

a loss of the normal air supply.

The licensee initiated condition

report/disposition

request

(CRDR) 1-4-0044 to evaluate

the test requirements

for ADVs.

The inspector

reviewed the

CRDR and discussed

the corrective actions with

Unit

1 management.

The licensee identified three factors that contributed to

not performing the nitrogen drop test after replacing the positioner

on

ADV-178.

First, the planner

used

a copy of a previous

work order

(WO) in the

data

base that did not include the drop test

as

a retest.

Second,

the

PM task

to replace

the positioner did not include the drop test

as

a retest.

Third,

the inspector

noted that the retest

requirements

were determined

by the unit

planners

and that the shift supervisor

must concur prior to releasing

the

WO

to the field.

The shift supervisor

and the shift technical

advisor did not

recognize

the

need for the drop test to ensure operability prior to approving

the work.

Additionally, the back end review of the work did not identify the

problem.

'

J

!

l

-21-

The licensee

determined that the requirement to include the drop test

as

a

retest

was not consistent

between all three units.

The licensee

checked all

twelve

ADVs to ensure

a drop test

was satisfactorily completed.

Based

on this

review, the licensee

determined that all the

ADVs had satisfactorily completed

the drop test

and were operable.

Additionally, the licensee

updated

the

computer

based

copies of work orders to include the requirement for a drop

test.

The licensee

planned to include this event

as part of the industry events

briefing.

Additionally, the licensee initiated

an action to review all the

PH

tasks

associated

with the

ADVs and include the

$rop test for any

PH that

breaches

the nitrogen

system.

The inspector

concluded that the licensee's

corrective actions

were

appr )riate to verify the

operability of the

ADVs and to minimize the

potential for similar testing errors with the ADVs.

Based

on this review,

this specific issue

was closed.

However.

the inspector

noted that there

appeared

to be

a broader

issue

concerning

an over reliance

on the experience

of the work planner to correctly determine

the appropriate retest

requirements.

In this particular

case,

the planner did not factor in previous

history with this type of maintenance

on the

ADVs or the experience of the

other units.

At the exit meeting,

the licensee

stated that they

had

previously recognized this potential

problem

and were beginning to use

standardized

maintenance

instructions that would correct the problem.

The

inspector will continue to observe

the area of retests

to verify that the

appropriate retest

requirements

were identified in the work instructions.

9

FOLLOWUP ENGINEERING

(92903)

9. 1

0 en

Deviation

528 9326-02:

Desi nation of En ineer-In-Char e-

Units

1

2

and

3

This deviation occurred

when the licensee

designated

two managers

as

Engineer-in-Charge,

even though they were not in

a functional position to be

cognizant of complex problems

emerging

from plant operations.

As

a result,

the oversight

intended

by ANSI/ANS 3. 1-1978,

regarding determining

when

consultants

are

needed

to support licensee

engineering

in resolving complex

problems,

was not provided.

The licensee's

corrective action

was to designate

the Assistant

Vice President

of Engineering

and Projects

as Engineer-in-Charge

after completing

a

10 CFR 50.59 evaluation of a change to the Updated Final Safety Analysis

Report

(UFSAR) for the commitment to the qualification requirements

of

ANSI/ANS-3. 1.

However,

equality Assurance

(gA) concluded that the change

in

commitment constituted

a reduction in the

gA plan

and that the change

in

commitment required

NRC approval prior to implementation.

At the completion

of the inspection period,

the licensee

had prepared,

but not submitted,

a

change

to the

UFSAR for NRC approval.

l

'

-22-

The inspector

concluded that the deviation still existed.

This item will

remain

open pending

NRC approval of the

USFAR change.

10

FOLLOWUP PLANT SUPPORT

(92904)

10.

1

Status of Actions to

Im rove the Environment for

Em lo ee Identification

and Resolution of Safet

Concerns

0

On July 7,

1993,

the

NRC requested

that the licensee

provide

a written

description of actions to be taken to correct

any potential chilling effect

after

a Department of Labor Administrative

Law Judge

(DOL/ALJ) found that the

licensee

discriminated

against

a contract

employee for engaging

in protected

activity.

At the time, the

DOL action represented

the third DOL/ALJ finding

against

the licensee

in 4 years.

The

NRC previously issued Notices of

Violation and

imposed Civil

P nalties after the first two DOL/ALJ findings.

The licensee

response

to the

NRC request

was provided in a letter dated

August 20,

1993.

Some of the completed or planned actions described

in the

'e.i~r included:

discussi ins of expectations

and

r~ sponsibilitie.

between

the

Executive Vice President,

Nuclear

and Palo Verde supervisors,

managers,

and

directors; training in the area of employment discrimination for managers,

supervisors,

and front-line employees;

an independent

assessment

of the

factors which assist

or impede

Palo Verde employees

in raising safety issues;

meetings with employees

regarding

management's

expectations

for raising safety

concerns;

an evaluation of the Palo Verde Employee

Concerns

Program;

and plans

for additional training to encourage

employees

to report concerns

and to

provide managers

with guidance

in responding to concerns,

Through discussions

with licensee

personnel

and review of documents,

the

inspector confirmed that the licensee

had completed

most of the actions

described

in the August 20,

1993, letter.

The inspector also reviewed

memorandums

to all employees

and publications

which described

expectations

for

fostering

an environment

where concerns

can

be raised

and for resolving

concerns

once they are identified.

In April 1994,

the licensee initiated

a

training course for front-line employees

which was designed

to promote the

communication of issues

to management.

The training course,

"Can

We Talk,"

was scheduled

to continue through July 1994.

A different version of the

course,

with emphasis

on accepting

and resolving concerns,

had previously

been

presented

to management

personnel.

The

NRC held three

management

meetings with the licensee

on January

25,

March 21,

and April 28,

1994.

During these

meetings

the licensee

discussed

actions

they had taken to improve the

Employee

Concerns

Program.

In addition,

the licensee

had recently put

a

new program into effe'ct for management

issues

which are not resolved informally.

The program

was designated

as the

Management

Issues

Tracking Resolution

(MITR) and will be used for nontechnical

concerns.

Technical

concerns will be resolved

through the existing

CRDR

program although

changes

to the program

have

been

made to allow for an appeal

if an individual did not agree with the resolution of an issue.

'

I

'

'0

-23-

Although the overall effectiveness

of the licensee's

actions to foster

an

environment for employee identification and resolution of safety concerns

was

not assessed,

the actions

may be having

an effect.

In particular,

the rate at

which concerns

are being presented

to the

NRC has decreased

which may indicate

that licensee

personnel

feel

more comfortable with allowing management

to

resolve

the concerns.

A followup inspection will be performed to review the

effectiveness

of the licensee's

actions.

1 1

IN OFFICE

REVIEW OF

LERs

(90712)

Unit 1:

LER 528/94-01,

Revision 0, Surveillance

Requirement

4.8.4.

1 Not Fully Met

Unit 2:

LER 529/93-04,

Revision 0, Reactor Trip and Auxiliary Feedwater

Actuation

Signals

Following Degraded

Voltage

on Non-Class

1E 4160V Bus

Unit 3:

LER 530/94-01,

Revision 0, Daily Surveillance

Test for Reactor

Power Channel

Calibration

Checks

Not Satisfactorily Completed

0'

ATTACHMENT 1

1

PERSONS

CONTACTED

Arizona Public Service

Com an

R.

  • J
  • R.
  • S

J.

4'B

W.

  • S

J.

  • A.

R.

  • D

S.D

B.

  • W.
  • A.
  • D
  • J

D.

F.

  • K.
  • B
  • M
  • J

C.

  • B
  • E

J.

  • F

J,

S.

  • J
  • p

1.2

e 5 Haintenance

Others

Adney, Plant Manager,

Unit 3

Bailey, Assistant

Vice President,

Nuclear Engineering

Bouquot,

Supervisor,

equality Assurance

Audits

Burns, Supervisor,

Nuclear Engineering

Department

Dennis,

Manager,

Operations

Standards

Cherba,

Manager,

equality Assurance

Chapin,

Manager,

Refueling

and Maintenance

Services

Coppoch,

SupervIsor,

Valve Services

Dennis,

Manager,

Operations

Standards

Fakhar,

Manager,

Mechanical

Group, Site Technical

Suppo

Flood, Plant Manager,

Unit 2

Garchow, Director, Site Technical

Support

Gouge, Director, Plant Support

Grabo,

Supervisor,

Nuclear Regulatory Affairs

Ide, Plant Manager,

Unit

1

Kraini k, Manager,

Nuclear Regulatory Aiba. rs

Larkin, Senior Engineer,

Nuclear Regulatory Affairs

Levine, Vice President,

Nuclear Production

Hauldin, Director, Site Maintenance

and Modifications

Riedel,

Manager,

Operations,

Unit

1

Roberson,

Senior Engineer,

Nuclear Regulatory Affairs

Rosen,

Acting-Manager,

equality Control/equality

Assuranc

Salazar,

Supervisor,

Valve Services

Scott, Assistant

Plant Manager,

Unit 3

Seaman,

Director, equality Assurance

and Control

Simko, Hanager,

Valve Services

Simpson,

Vice-President

Nuclear Support

Steward,

Manager,

Radiation Protection

Swirbul, Manager,

Nuclear Engineering

Department

Terry, General

Manager,

Nuclear Records

Management

Troisi, Manager,

Site Technical

Support

Velotta, Director, Training

Wiley, Manager,

Operations,

Unit 2

  • J
  • R.
  • F

Draper,

Site Representative,

Southern California Edison

Henry, Site Representative,

Salt River Project

Gowers,

Site Representative,

El

Paso Electric

". Denotes

personnel

in attendance

at the Exit meeting held with the

NRC

resident

inspectors

on May 12,

1994.

0

I

0

2

EXIT MEETING

An exit meeting

was conducted

on Hay 12,

1994.

During this meeting,

the

inspectors

summarized

the

scope

and findings of the report.

The licensee

acknowledged

the inspection findings documented

in this report.

The licensee

did not identify as proprietary

any information provided to, or reviewed by,

the inspectors.

1

1

0