ML17305B447

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Insp Repts 50-528/91-01,50-529/91-01 & 50-530/91-01 on 910106-0216.Violations Noted.Major Areas Inspected: Previously Identified Items,Review of Plant Activities, Monthly Surveillance Testing & Monthly Plant Maint
ML17305B447
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 03/20/1991
From: Wong H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17305B445 List:
References
50-528-91-01, 50-528-91-1, 50-529-91-01, 50-529-91-1, 50-530-91-01, 50-530-91-1, NUDOCS 9104090135
Download: ML17305B447 (34)


See also: IR 05000528/1991001

Text

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION V

or I

)los

Docket Nos.

License

Nos.

Licensee:

Facilit

Name:

50-528/91-01,

50-529/91-01

and 50-530/91-01

50-528,

50-529,

50-530

NPF-41,

NPF-51,

NPF-74

Arizona Public Service

Company

P.

0.

Box 53999, Station

9012

Phoenix,

AZ

85072-3999

Palo Verde Nuclear Generating Station

Units 1, 28

3

Ins ection Conducted:

January

6 through February

16,

1991

Inspectors:

Approved By:

a

e

sgne

D.

Coe,

Senior

Resident

Inspector

F.

Ringwald,

Resident

Inspector

J.

Sloan,

Resident

Inspector

D. Kirsch,

Chief, Reactor Safety Branch

W. Ang,

Project Inspector

3

ong,

hl e

Reactor Projects,

Se tion II

Ins ection

Summar

Ins ection

on Januar

6 throu

h Februar

16

1991

Re ort Numbers

50-528 91-01

50-529 91-01

and 50-530 91-01

Areas Ins ected:

Routine, onsite,

and regular

and backshift inspection

y the resident

inspectors

and inspectors

from the Region

V staff.

Areas

inspected

included: previously identified items; review of plant

activities; monthly surveillance testing;

monthly plant maintenance;

reactor coolant system

(RCS) cooldown rate limit exceeded - Unit 1;

apparent

reactor coolant system

(RCS) stratification in loop 1 hotleg-

Unit 1; incorrect lube oil added to auxiliary feedwater

pump and boric

acid makeup

pump - Unit 2; emergency diesel

generator air start system

leakage - Unit 3; 'violation of surveillance

requirement to perform

emergency diesel

generator

(EDG) inspections

during plant shutdown-

Unit 3;

use of an engineering

evaluation

(EER) request

not formally

approved - Unit 3; potential for small break

LOCA due to tube rupture in

the reactor coolant

pump seal

cooler - Units 1, 2,

and 3; Probabilistic

Risk Assessment

- Units 1, 2,

and 3; Plant Review Hoard activities-

Units 1, 2,

and 3; and review of licensee

event reports - Units 1, 2,

and

3 ~

During this inspection the following Inspection

Procedures

were utilized:

30703,

40500,

61726,

62703,

71707,

71710,

92700,

92701,

92702

and 93702

'104090135

910321

PDR

ADOCK 05000528

Q

PDR

Results:

Of the

15 areas

inspected,

two violations were identified in

Un>t 3.

The violations pertained to an

NRC identified departure

from the

plant conditions specified for performing an Emergency Diesel Generator

surveillance

inspections

and the failure to promptly correct

an

identIfied deficiency and perform an adequate

evaluation of the

deficiency.

General

Conclusions

and

S ecific Findin

s

Si nificant Safet

Matters:

Summar

of Violations:

None

2 Cited Violations - Unit 3

Summar

of Deviations:

0 en Items

Summar

7 Items closed,

3 Items left open,

and

6

New Items opened.

j

t

DETAILS

Persons

Contacted:

The below listed technical

and supervisory personnel

were

among

those contacted:

Arizona Publ'ic Service

Com an

(APS)

"R. Adney,

  • J. Auston,
  • J. Bailey,

"H. Bieling,

¹"T. Bradish,

"M. Czarnylas,

  • J. Draper,

"E. Dotson,

¹"T. Engbring,

"R. Flood,

R. Fullmer,

D.

Gouge,

¹"S. Guthrie,

~K. Hall,

"B. Hazelwood,

"R. Henry,

.

P.

Hughes,

~M. Ide,

"S. Kanter,

F. Larkin,

"J. Levine,

J. Minnicks,

"J. Napier,

"G. Overbeck,

"R.

Rouse,

R. Rogalski,

J. Scott,

¹G. Shell,

S. Terngino,

'N. Thibodaux,

Plant Manager,

Unit 3

Fire Department,

Deputy Chief

Vice President,

Nuclear Safety

8 Licensing

Emergency/Fire

Protection,

Manager

Compliance,

Manager

Fire Protection,

Deputy Chief

SCE, Site Representative

Engineering

8 Construction,

Site Director

Lead Engineer,

Systems

Engineering

Plant Manaqer,

Unit 2

gA and Monitoring, Manager

Plant Support,

Manager

(Ch. Plant

Review Bd.)

equality Department,

Deputy Director

El Paso Electric Co., Site Representative

equality Assurance,

Monitoring, Supervisor

Salt River Project, Site Representative

Site

Rad. Protection,

General

Manager

Plant Manager, Unit 1

Sr. Coordinator,

Owner Services

Security,

Manager

Vice President,

Nuclear Power Production

Maintenance

Manager,

Unit 3

Compliance,

Lead

Technical

Support, Site Director

Compliance,

Supervisor

gA, Supervisor

Operations

Manager,

Unit 1

equality

Systems,

Manager

Management

Services,

Supervisor

System Engineer,

EDG System

The inspectors

also talked with other licensee

and contractor

personnel

during the course of the inspection.

"Attended the Exit meeting held with NRC Resident

Inspectors

on

February 21,

1991.

¹Persons

contacted

by M. Ang.

2.

Previousl

Identified Items - Units 1

2 and

3 (92701

and 92702)

A.

Unit 1:

(Closed)

Unresolved

Item (528/90-20-01):

"RCP

Lube Oil

Collection

S stem

ubln

- Un)t 1

92

1

This item involved improper restoration of RCP lube oil

collection system tubing following replacement

of the

RCP

motors.

The inspector questioned

the requirements

for

quality control classification

and controls over this

piping.

The licensee

has classified the

RCP lube oil

collection system tubing as equality

Augmented

(gAG) and is

finalizing the specific requirements

as part of the Fire

Protection

Task Force effort.

The licensee

is also

correcting the deficiency in procedure

31MT-9RC06,

"Reactor

Coolant

Pump Disassembly

and Reassembly"

to

include steps for restoring this tubing and will include

references

to the drawings

and documents

required for

proper installation.

The Manager of Maintenance

Standards

committed to issuing the revision to 31MT-9RC06 prior to

the start of the Unit 3 outage refueling (approximately

March 1991).

This item is closed.

(0 en) Followu

Item

528/90-20-04

"Inadvertent

Shutdown

Cool a n

B

ass

-

Uns t 1

92 01

This item involved the discovery of bypass

flow through

valves SI-HV-690/691 when they are slowly jogged closed

because

they are not driven into their seat

by the motor

operator.

The licensee initiated Engineering Evaluation

Request

90-SI-093 which concluded that

a plant

modification would be required to fully address

this

problem.

The

EER is closed

and engineering is pursuing

a

plant modification as long term corrective action.

As an

interim measure,

the licensee

has revised procedures

4XOP-XSI01,

"Shutdown Cooling Initiation," to require

operators

to manually shut these

valves to ensure that

they are fully closed, eliminating any bypass

flow.

The

inspector

reviewed

EER 90-SI-093

and noted strong

recommendations

which differed from the interim measures

established

prior to closure of the

EER and that the

EER

discusses

problems with manual

operation of these

valves

in that it applies

indeterminate

torque to the valve stem.

It also recognizes

that "...both overthrust

and

underthrust

are both of equal

concern in terms of valve

operability and reliability."

The licensee is considering

revising the interim measures.

This item will remain open

until these

discrepancies

are resolved.

i

3.,

(0 en

Enforcement

Item 50-528/90-25-01:

"Ino erable

mer enc

L> htsn

In resp";,s='o

concerns

regarding the application of

quality assurance

criteria to various aspects

of the fire

protection

system,

the licensee

submitted

a Justification

for Continued Operation

by letter dated July 20,

1990.

In

addition, the licensee

responded

to the

Emergency Lighting

Notice of Violation by letter

dated

November 15,

1990.

These

two documents

contained

several

commitments for

licensee

action.

The licensee

has identified 254 action items

and entered

all of these various

commitments into the Commitment

Action Tracking System.

The tracking system tracks item

status,

responsibility,

source,

due date,

and completion

date.

The licensee

appears

to be making acceptable

progress

in resolving these

items.

Only about four of the

licensee's

internal

commitments

were overdue;

the licensee

was aware of these

and dealing with those

items.

The licensee is tracking emergency lighting failures

quarterly by means of a Component Failure Data Trending

Report.

The report is provided to the System Engineering

Manager.

Failures

can

be accessed

in real time by System

Engineers

using networked

computer terminals accessing

the

maintenance

data

base.

The licensee

plans to have

a

terminal in all System Engineer work spaces

by about

mid-year.

Emergency Lighting Unit No.

3E(DNF02 failed the

8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />

test in January,

1991,

and

has not been retested

satisfactorily since.

This unit is one of two redundant

units for the Unit 3 control

room.

The inspector

discussed

the circumstances

at length with licensee

representatives

and ascertained

the following:

a.

A nonconformance

report was written to document the

situation

and provide

a vehicle for resolution

and

corrective action.

b.

A problem resolution sheet

was written to initiate

the necessary

reviews to determine reportability.

The licensee

did not consider the situation

reportable

because

the failed unit is backed-up

by a

redundant unit.

C.

d.

Licensee

engineering evaluation

was that the unit

batteries

need replacement.

Because

the licensee

does

not have sufficient spares

on hand,

new batteries

were placed

on order.

\\

The licensee

has readjusted

the low voltage cut out

on the two control

room battery banks in each unit to

properly compensate

for cable voltage drops.

The

inspector

reviewed these calculations

and found them

acceptable.

The inspector considers

that the licensee is dealing with

the above failure

$ n an acceptable

manner.

The inspector discussed

the licensee's

actions to deal

with emergency lighting failures.

The licensee

has taken

action to see that future emergency lighting failures are

documented

using the nonconformance

reporting system to

assure that problems

are dealt with in a timely manner

with the benefit of engineering

and management

involvement.

The inspector discussed

the

EER backlog with licensee.

representatives

and found that the

EER backlog

had only

been

reduced

by about

10K and the average

EER age

was

excessive.

The licensee

acknowledged

the problem and was

evaluating actions to effect better control of the

EER

backlog and age.

This item remains

open pending further review of the

overall issue

by the inspector.

B.

Unit 3

(Closed)

Enforcement

Item (530/90-20-01):

"Atmos heric

um

a ve

atro

en

ccumu ator

oun

so ate

n)t

This item involved an improper valve lineup performed

by

Unit 3 operators

which isolated the

AOV accumulator

when

the isolation valve should

have

been

locked open in

accordance

with procedure

40AC-OZZ06, "Locked Valve and

Breaker Control. 'he operators

involved were counselled,

all operators

were briefed

on the importance of attention

to detail,

an investigation

was conducted utilizing the

.

Human Performance

Evaluation

System

(HPES) program,

and

each shift received training on independent verification.

The inspector

reviewed the corrective action,

had

no

further questions,

and concluded that these actions

appear

appropriate to address this event.

This item is closed.

C.

Units 1

2

and

3

(0 en)

10 CFR Part 21

Re ort (89-18-P):

"ABB Power

1s

r1 ut1on

nc.

urrent

rans

ormer

nca

su ate Materia

'- Un)ts

1

2

3

2701)

This item involved a softening of the epoxy-anhydride

encapsulate

material in CTs due to high humidity

conditions.

The licensee

has evaluated this in EER

89-XE-28 which refers to

EER 89-NG-10.

The inspector

reviewed these

two EERs

and noted that the disposition

does

not clearly identify the licensee's

action

on this

issue.

This item will remain

open pending additional

information from the licensee.

(Closed

10 CFR Part 21

Re ort (89-24-P):

"BW/IP

nternatsona

nc.

s

ressure

win

ec

alve

Failure

- Units

1

2

& 3

92701

This item involved the failure of a check valve at

Comanche

Peak

Steam Electric Station.

The licensee

has

evaluated

the concern,

determined that 69 affected valves

exist in each unit, and concluded that only six valves per

unit would be

a safety concern if they failed to block

flow and potentially cause

an interfacing system loss of

coolant accident

(ISLOCA).

The first refueling outage after receipt of the associated

Information Notice (90-03) occurred in Unit 2 and

coincidentally included scheduled

inspections

of 17

affected valves

under the ongoing Check Valve Preventive

Maintenance

Program.

None of these

valves

had any defect

indications.

Additional affected valves will be inspected

in future outages

in accordance

with the ongoing program.

The licensee is currently performing

a fracture mechanics

study which preliminarily suggests

that

a critical flaw

size would have to be greater

than 0.25 inches for all

valves.

The licensee

is also performing

a Probabilistic

Risk Analysis

(PRA) to quantify the contribution of these

check valve failures to the probability of an

ISLOCA.

qualitative analysis

suggests

that if the

Commanche

Peak

and Palo Verde data is combined,

the resulting

contribution to ISLOCA appears

to be acceptably

low.

The licensee

expects to finish the fracture mechanics

and

PRA study during the second quarter of 1991.

The

inspector

concluded that these activities appear

appropriate

to address this issue.

This item is closed.

Closed)

10 CFR Part 21

Re ort (89-25-P):

"Deficienc

With

L)motor ue

-

0 an

B-00

otor

erator

or ue

Sw)tc es

- Units 1

2

2

1

This item involved a deficiency with cam-type torque

switches in that fiber spacers

permit loosening of

stationary contact

screws.

One consequence

of this type

of failure is the potential for affecting the torque which

will break the torque switch current and stop the operator

from delivering torque to the valve.

The licensee

issued

EER 89-XE-059 on November 27,

1989.

The

EER is still open

and the system engineer

expects to close it during the

next month.

The system engineer

noted that

PCN 3

I

4

to procedure

32MT-9ZZ48, "Maintenance of Limitorque

Motor Operators,"

issued

on January

3, 1991, requires

workers to inspect for fiber spacers

and write a work

request to replace

any torque switch found with fiber

spacers.

The inspector considers

the actions

taken to

have

been slow, but technically adequate for this issue.

This item is closed.

(Closed

10 CFR Part 21

Re ort

89-28-P

"Coo er-Bessemer

mer enc

iese

enerator

ran case

x

os)on

nsts

This item involved two crankcase

explosions of diesel

generators

at the Susquehanna

Steam Electric Station.

Cooper-Bessemer

has concluded that both of these

explosions

were due to casting defects

which they consider

to be "extremely rare."

They therefore

conclude "that

there is no generic

impact as

a result of the reported

incident" and that licensees

with similar diesels

need

take

no further action.

The licensee

has reviewed this

event

and

had discussions

with the Cooper-Bessemer

owner's

group and with Cooper-Bessemer.

As a result,

the licensee

has initiated several

actions which will limit the impact

of what is believed to be contributing factors to this

event.

These actions

include submitting

a Technical

Specification

change

request to move the llOX load test to

the

end of the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> Surveillance

Test run so the heavy

load test

can occur when the engine is fully warmed

up.

Additionally, the licensee

has modified their monthly

surveillance test procedures

to run the diesels for four

hours

when practical rather than just one hour.

In

addition,

Cooper-Bessemer

has generated

service bulletins

which recommend

loading and unloading profiles which the

licensee

is evaluating for inclusion in diesel testing

and

operating procedures.

According to the system engineer,

a

final root cause of failure has not been fully agreed

on

by Cooper-Bessemer

and the ow'ner's group.

The licensee is

following testing

and other actions being taken

by

Susquehanna

and Cooper-Bessemer

and

has stated that as

further lessons

are learned

from these

events,

they will

receive service bulletins,

owner's

group comments,

and if

warranted,

amended

or additional

10 CFR Part 21 reports.

The inspector

concluded that the licensee

appears

to be

taking appropriate

action.

This item is closed.

(Closed

10 CFR Part 21

Re ort (89-31-P

and

LER (528/

enr

ratt

om an

a ve

al ures

nsts

This item involved the intergr'anular cracking

and failure

of spiral pins

used to attach the disk of butterfly valves

to the stem.

This issue

was addressed

in Inspection

Report 528/529/530/89-49,

paragraph

12.

The inspector

reviewed supplement

1 to the initial 10 CFR'art

21 Report

and

had

no further questions.

This item is closed.

3.

Review of Plant Activities (71707

and 93702}

A.

Unit 1

B.

Unit 1 entered this reporting period operating at 100 percent

power.'n January

12,

1991, the unit was downpowered

and the

reactor manually tripped to commence

a scheduled

39 day

surveillance test outage.

Maj or outage activities included

performance of 18 month surveillance tests

(Integrated

Safeguar ds surveillance,

Emergency Diesel

Generator

inspection,

snubber inspections,

Emergency

Safeguards

Features

Battery

surveillance

and others},

ASME Section

KI pump and valve

inspections,

rewiring and testing of many motor operated

valve

operators, circuit breaker testing,

implementation of some site

modifications,

and performance of many corrective maintenance

work items.

The outage

was completed three

days

ahead of

schedule,

with Mode 4 and

Mode

3 entered

on February

13,

1991,

Mode

2 and

Mode 1 on February 16,

and synchronization to the

grid on February

16.

Power ascension

was in progress

at the

end of the reporting period.

Unit 2

Unit 2 operated at essentially

100 percent

power throughout

this reporting period.

Unit 3

D.

Unit 3 operated at essentially

100 percent

power throughout

this reporting period.

Plant Tours

The following plant areas

at Units 1,

2 and

3 were toured by

the inspector during the inspection:

Auxiliary Building

Control

Complex Building

Diesel Generator Building

Radwaste Building

Technical

Support Center

Turbine Building

Yard Area and Perimeter

The following areas

were observed

during the tours:

1.

0 eratin

Lo s and Records - Records

were reviewed against

ec naca

peel

)catsons

and administrative control

procedure

requirements.

Monitorin

Instrumentation - Process

instruments

were

observe

for corre ation between

channels

and for

conformance with Technical Specifications

requirements.

~Sic f

R <> .'ction warranted

and will review the IIR when

complete

(Fol 1 owup Item 529/91-01-01).

No violations of NRC requirements

or deviations

were identified.

Emer enc

Diesel Generator Air Start

S stem

Leaka

e - Unit 3

61 26 and

62 03

The inspector performed walkthrough inspections

of Unit 1 and Unit 3

Emergency Diesel Generator

(EDG) buildings and the site maintenance

shop.

The repaired Unit 1

EDG inner cooler was observed

in the

maintenance

shop awaiting reassembly

and testing.

The inspector

noted that

a significant amount of coating (appeared

to be belzona)

had been recently applied over portions of the inner cooler flanges

and excess

coating appeared

to have

been applied over portions of

the inner cooler

tube openings.

The system engineer

observed

the

condition concurrently

and requested

maintenance

shop personnel

to

remove the excess

material.

Mhile no surveillance

testing

was observed

in progress,

the

inspector

reviewed records for the most recent testing of Unit 3

EDG

air star t receiver relief valves

PSV-5, 6,

7 and

8 and inlet check

valves V-066, -067, -068 and -069.

Review of the applicable test

records

and procedures

indicated that the testing

had been

satisfactorily accomplished.

During the inspection of the Unit 3

EDG building, the inspector

noted

an oily substance

leaking from both of the

EDG "A" air start

receiver

manway cover gaskets

and, to a lesser extent,

from both of

the

EDG "B" air start receiver

manway cover gaskets.

The inspector

noted that work request

tags

(WR 396845

and

MR 396847)

on the

EDG

"A" air receivers

had identified "oil bubbling from access

covers."

The air pressure

of all in service receivers

(one

was being taken

out of service for 'compressor

maintenance)

were being maintained

by

their corresponding

compressors

at 240 to 250 psig.

The inspector

discussed

the noted condition with the system engineers,

the Unit 3

operations

supervisor,

compliance

and gA.

The inspector inquired

about the ability of the

EDG air start

system in Unit 3 to perform

its design functions specified in UFSAR Section

9. 5. 6.

Specifically, the inspector attempted to determine if a technical

evaluation

had been performed for the noted condition taking into

consideration

the following:

a)

The air receivers

were being maintained at their required

pressure

by a non-safety-related,

non-seismic,

non-class

1E

powered

compressor.

The ability of the leaking air cylinders

to maintain sufficient pressure

to accomplish all its design

functions without the assistance

of the compressors

was

unknown.

The amount of allowable leakage

and the magnitude of

16

the identified leakage

necessary

to be able to make this

determination,

were

unknown.

b)

Evaluations

were not performed to determine

the substa'nce

leaking from the air cylinder manway cover gaskets,

the source

of the substance,

and the possible deleterious

effects of the

substance

on any part of the air start system

such that it

would preclude it from performing its function.

The

PVNGS Updated

FSAR, Section 9.5.6. 1, Design Bases,

states

in

part that "the

DGSS [diesel generator start system] shall provide

a

stored

compressed air supply sufficient for accomplishing diesel

generator

cranking cycle

5 times without starting the'iesel

generator air compressors,"

and "the

DGSS shall

remain functional

during and after an SSE."

The inspector discussed

the above

noted observations

and was

informed of the following by the system engineers,

the operations

supervisor,

gA, and compliance:

A.

WRs 396845

and 396847 were written in Nay 1990

and were

cancelled

by work planning in October

1990 because

inspection

and cleaning of air receiver internals

were scheduled for

January

14,

1991 and February

17,

1991 by W.O. s 458522

and

458523.

The W.O.s were subsequently

rescheduled

for

performance in February

1991.

Since

WRs 396845

and 396847

had been cancelled,

the record for

those work requests

were

no longer available

and the only

records available

relating to the work request

was the

SINS

computer annotation that it had

been cancelled

and included in

W.O.s 45822

and 45823

and the

WR tags that had

been

inadvertently left hanging

on the two

EDG "A" air receiver.

manway cover gaskets.

B.

The air receivers

are not periodically tested'and

the leak rate

from the

manway cover gaskets

had not been determined for the

conditions identified by WRs 396845

and 396847.

The existing

, leak rate, at the time of the

NRC inspection,

was

unknown.

C.

The system engineers

and the operations

supervisor

considered

the leaking air receivers

to be operable.

They were unable to

state

what the manway cover gaskets

leak rates

were nor how

much leakage

was acceptable

for the receivers to be still

capable of performing its design functions.

The engineers

and

supervisors

claimed that the leakage

was acceptable

as long as

the low receiver air pressure

alarm in the control

room had not

activated.

It

D.

There

was

no indication that any monitoring of the leakage

was

being performed to assure that the leaking

manway cover

gasket

was not deteriorating

and the leakage

had not increased

since

the condition was identified eight months earlier.

The

inspector

recognized that control

room operators

would become

~

~

17

aware of low pressure

in the receivers

when the low pressure

alarm was annunciated.

However, the inspector also recognized

that as long as the compressors

were available

and the leak

rate did not exceed

the capacity of the compressors,

the alarm

would not activate

and

a deteriorating condition would not be

evident.

E.

F.

The system engineers felt that the leaking substance

was oil,

was coming from the compressors,

and did not feel that the oil

had any deleterious

effects

on any part of the air start

system.

No MNCRs regarding the condition were issued.

The

gC manager

indicated that the condition appeared

to be normal wear and

tear

and as

such did not require

an

MNCR, as allowed by the

MNCR procedure.

10 CFR Part 50, Appendix B, Criterion XVI, requires that measures

be

established

to assure

that conditions

adverse

to quality such

as

deficiencies

and malfunctions

be promptly identified and corrected.

The noted air receiver

manway cover gaskets

leakage

were not

corrected for approximately eight months,

the amount of leakage

for the receivers

to still be capable of performing its specified

functions

had not been determined,

and the actual

leak rate of the

manway cover gaskets

had not been determined.

This appears

to be

a

violation of 10 CFR Part 50, Appendix B, Criterion XVI.

(Enforcement

Item 50-530/90-01-02).

Violation of Surveillance

Re uirement

To Perform

Emer enc

Diesel

enerator

G

ns ect)ons

urban

ant

ut own -

nit

3)

During this inspection period the inspector

noted that recent Unit 3

EDG inspections

recommended

by the manufacturer

were performed to

meet Technical Specification Surveillance

Requirement

(SR)

4.8. 1. 1.2. d. 1, but were not performed during unit shutdown

conditions

as required

by the

SR.

This is an apparent violation of

the

SR (Enforcement

Item 530/91-01-01).

The licensee

performed

some inspections with the unit operating

because

the required

18-month surveillance intervals would have

expired prior to the next refueling outage in March 1991.

In

addition, with the manufacturer's

concurrence,

the licensee

waived

several

of the required mechanical

inspections until the refueling

outage,

as justified in Engineering Evaluation Request

90-DG-07.

The

SR allows the

EDG manufacturer to specify the required

inspections.

The

SR specifies to perform the manufacturer's

recommended

inspections "at least

once per 18 months during shutdown."

The

licensee

meets this requirement

by implementing two Surveillance

Test (ST) procedures,

31ST-9DGOl (for the mechanical

inspections)

and 32ST-9PE01 (for the electrical

generator

inspections).

In

addition, the manufacturer's

recommended

18-month instrumentation

calibrations

and air filter replacements

are performed

by preventive

18

maintenance

tasks.

The inspector also noted that among the manufacturer's

recommended

"annual" inspections

is a task to perform diesel

generator

instrument calibrations.

These calibrations

are covered

by the

licensee's

PM program.

However, the

PM program specified

a

'~g outage

frequency for these calibrations.

This is

inconsistent with the manufacturer's

recommended

"annual" inspection

interval (allowed by the manufacturer to be

12 to 18 months),

especial> lv when prolonged outages

extend the operating cycle.

The

licensee

should determine the required frequency for the instrument

calibrations

and appropriately reflect the frequency in the

scheduling

system.

The licensee

acknowledged

the inspector's

findings at the exit

meeting

and stated that they had determined that performance

of EDG

inspections for SR 4.8. l. 1.2.d.1 with the unit operating at power

was

a reportable

event per 10 CFR 50.73.

In addition, the licensee

committed to the following:

1)

A review of this and other Technical Specifications

surveillance

requirements

which require specified plant

conditions to ensure

they are being properly scheduled

and

performed in accordance

with these

requirements.

2)

A review of the scheduling of EDG instrumentation calibration

PM tasks to ensure

manufacturer's

recommended

intervals are

met.

3)

A review of all

PM tasks

being used to meet surveillance

requirements

to ensure that the required tests

and

verifications are scheduled

and performed within specified

surveillance

intervals.

The licensee

stated that their review would be documented

in

Incident Investigation Report 3-1-91-017A.

One violation of NRC requirements

was identified.

12.

Use of an

En ineerin

Evaluation

(EER

Re uest Not Formall

A

roved

- Unst

3

71707

On January

8, 1991, Unit 3 operations staff removed Spray

Pond

(SP)

Train "B" from service to restore

a temporary modification such that

normal

power cables for the spray

and bypass

valves could be

~

~

0

re-terminated.

Because

the Essential

Chi lier s (EC) use the

SP

system

as

a heat sink, operators

also entered

the Action Statement

for EC train "B" inoperable

(Technical Specifications 3.7.6).

The

Action Statement

requires,

in part, that within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> normal

HVAC

is verified to provide space cooling to train "B" ESF

rooms

served

by EC.

Earlier the operators

l.;," <<.~estioned

the ability of HVAC to

provide acceptable

cooling since the normal (nonessential)

chilled

water loop in the associated

Air Handling Unit (AHU) had recently

frozen and broken,

and was then isolated.

Operations,

including an

Operations

Supervisor,

were aware that an Engineering

Evaluation

Request

(EER) was being written to determine whether the broken

cooling coils would impact the ability to meet Technical

Specifications

requirements.

Based

on

a verbal discussion with the

final engineering

reviewer/approver,

and prior to his final review

and signature,

operations

proceeded

to remove the

SP

and

EC trains

from service to complete the maintenance.

Subsequently,

the

EER was

approved

as written and specified certain temperature

limits,

outside of which would be required routine temperature

monitoring of

affected

ESF equipment, rooms.

The inspector questioned

the decision

making process

which used

an

EER which had not been formally approved for the following reasons.

1)

The maintenance

was planned,

but was discretionary.

There

was

no apparent

or compelling reason

why the train outage could not

wait for the final

EER disposition.

2)

Engineering

was

aware that the unapproved

EER was being

used

for the operations

decision.

Although the inspector did not

identify any weakness

in the final disposition,

in general

such

,practice

may result in pressur e to complete the document

as

written, without further critical review.

3)

The inspector

noted that in NRC Inspection Report 529/90-46

paragraph

10 a review was

made of an incorrect Night Order

issued

on the basis of a draft MNCR.

The

MNCR was later

changed

but the Night Order was not, causing initial confusion

on the part of operations staff responsible for ensuring the

provisions of the

MNCR were met.

The inspector

noted that management

decision making based

on

incomplete or unapproved

engineering

documents

is

uncommon at

PVNGS,

but that it has

caused

confusion in the past

and potentially could

cause

more serious

problems.

The specific case referred to here

appears

not to have created

any problem, but if the practice

becomes

more prevalent it may lead to less than careful, thorough,

and

formal engineering

inputs to the decision making process.

Licensee

management

acknowledged

these

comments

and stated that

their intent was to include all appropriate

supporting

group inputs

to the management

decision making process,

and that such inputs

be

formal and complete

when appropriate.

No violations of NRC requirements

or deviations

were identified.

20

Potential for Small Break

LOCA Due to Tube

Ru ture in the Reactor

oo ant

um

ea

oo er -

n)ts

and

During review of NRC Information Notice No. 89-54 "Potential

Overpressurization

of the

Component Cooling Mater System,"

APS

identified

a s::;;:."

in which a break in the reactor

coolant

pump

High Pressure

Seal

Coolers

(HPSC) could potentially result in a

Reactor Coolant System

(RCS) leak being released

outside of the

containment building.

The scenario

involves

a leak from the reactor

coolant

pump

HPSC into the lower pressure

Nuclear Cooling water

(NC)

system.

The resulting leak could potentially overpressurize

the

NC

system.

If this were to occur,

and the

NC containment isolation

valises were unable to shut against the pressure

or flow, and the

operators

were unable to identify the leaking seal

cooler and

isolate the leak with the seal

cooler isolation valves, it could

result in reactor coolant being discharged

from the

NC surge tank

relief valve on the auxiliary building roof.

APS performed

an

analysis of this scenario

and determined that continued operation is

justified.

This justification was documented

in a JCO sent to the

NRC on January

18,

1991 (letter 161-03709-MFC/JST).

This

JCO is being reviewed by the

NRC (Followup Item

528/91-01"03).

No violations of NRC requirements

or deviations

were identified.

Probablistic

Risk Assessment

- Units 1

2

and

3

71707)

Pursuant to the requirements

of NRC Generic Letter 88-20 to perform

an Individual Plant Examination of the relative risks of plant

transients

and equipment malfunctions to the overall probabilistic

risk of core

damage,

the licensee

determined, preliminarily, that

event

sequences

leading to a loss of the "A" 125 vdc Class lE bus

contributed over 80 percent of the total core

damage

frequency

(CDF).

The

APS engineering

group responsible for this probabilistic

risk analysis

(PRA) presented their preliminary results to licensee

management

in May 1990.

Management

was informed that conceptual

engineering

work was

underway to determine the best design

changes

to mitigate the severity of these

sequences.

Although the

preliminary overall

CDF was only 0.001 per reactor year {one core

damage

event expected within 1000 years of operation),

elimination

of this event sequence

was expected to reduce the

CDF by nearly

a

factor of 10.

However, in November 1990, the licensee

Plant

Modifications Committee

(PMC) reviewed the Plant

Change

Requests

which resulted

from the conceptual

engineering

work and,

although

they were approved for detailed engineering

design work in 1991,

they were given

a low priority.

However, in February

1991 following

a presentation

of this event

sequence

to plant operations staff, the

priority was increased

and engineering

design work commenced

immediately.

The inspector

noted the reason for the large contribution to the

CDF

was primarily that loss of this

DC bus caused

closure of main steam

and feedwater isolation valves

and initial loss of control power for

21

two out of three auxiliary feedwater

pumps.

This leaves

the only

remotely controlled source of feedwater

to be the "B" auxiliary

feedwater

pump, since all normal

feed sources

are isolated

by the

closure of the Feedwater

isolation valves.

While the probability of

the "B" auxiliary feedwater

pump being out of service is small, this

potential

could result in a total loss of all feedwater

and is

consequently

a ~ip~ f'J)F ~ask due to the sensitivity of the

PVNGS

design to total loss ot ieeawater with no primary power operated

relief valves.

While the licensee

proceeds

with engineering

design work on plant

changes

to mitigate this event sequence,

the licensee

has stated

that current

Emergency Operating

Procedures will provide sufficient

guidance

for operators

to take manual control of the failed motor

driven auxiliary feedwater

pump and the failed closed valves in its

flowpath.

The inspector noted that general

guidance exists in the

Functional

Recovery Procedures

for the condition of loss of all

feedwater

and consists primarily of instructions to gain manual

control of available

pumps

and flowpaths.

The abnormal

operating

procedure. for loss of DC bus "A" assumes

the "B" auxiliary feedwater

pump remains available

and therefore

gives

no guidance for manual

restoration of unavailable

auxiliary feedwater.

The licensee

is

evaluating further procedural

and maintenance

policy changes

as

compensatory

measures

until design

changes

are final. It is

expected that these

changes

would reduce the risk of AFW

unavailability should this event occur,

as well as provide operators

with better guidance

recovering

from the worst case

scenario (i.e.

loss of DC bus with loss of all feedwater).

No violations of NRC requirments

or deviations

were identified.

Plant Review Board Activities

During the inspection,

the inspector

questioned

an observation that

the Plant Review Board

(PRB) had not reviewed

a revised

administrative procedure.

Discussions with the licensee identified

that the Technical Specifications, for each unit had been

amended

such that

PRB review of administrative

procedures

and changes

was

no

longer required.

In addition, the inspector

reviewed the procedure in question

(01PR-DAP01; Administrative Controls Program).

The inspector

questioned

the intent of a step regarding the issuance

of letters,

memoranda,

and orders to provide management

guidance

on a temporary

basis.

The intent was discussed

with licensee

personnel.

The

inspector found that while the wording of step 3.7.6

was consistent

with ANSI N18.7 (1976), the wording was not clear with regard to the

limitations of use.

The licensee

agreed to evaluate

the wording and

revise,

as necessary.

No violations of NRC requirements

or deviations

were identified.

22

16.

Review of Licensee

Event

Re orts - Units

1

2 and

3 (92700)

The following LER was reviewed

by the Resident

Inspectors.

Unit 1

528/89-18-LO/Ll (Closed

"Henr

Pratt

Com an

Valve Failures"

- Units 1

2

and

3

This event is described

and reviewed in paragraph

2.C.5 of this

inspection report.

Based

on this review, this

LER is closed.

17.

~Ei

5h

The inspectors

met with licensee

management

representatives

periodically during the inspection

and held an exit meeting

on

February

21,

1991.

The licensee

did not identify as proprietary

any

materials provided to or reviewed

by the inspectors

during the

inspection.