ML17305B129

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Insp Repts 50-528/90-28,50-529/90-28 & 50-530/90-28 on 900715-0825.Violations Noted
ML17305B129
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 09/24/1990
From: Wong H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17305B123 List:
References
50-528-90-28, 50-529-90-28, 50-530-90-28, NUDOCS 9010250028
Download: ML17305B129 (55)


See also: IR 05000528/1990028

Text

'0

Re ort Nos.:

Docket Nos.:

'l

License Nos.:

Licensee:

Facilit

Name:

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION

V

50-528/90-28,

50-529/90-28

and 50-530/90-28

50-528,

50-529,

50-530

NPF-41,

NPF-51,

NPF-74

Arizona Public Service

Company

P.

0.

Box 53999, Station

9012

Phoenix,

AZ. 85072-53999

Palo Verde Nuclear Generating Station Units

1, 28

3

Ins ection Conducted:

July 15 through August 25,

1990

Ins ectors:

D. Coe,

F.

Ringwald,

J.

Sloan,

C.

M

rs,

Senior Resident

Inspector

Resident Inspector

Resident Inspector

R sident Inspector

(Rancho

Seco)

A

roved

8

ong)

1

Reactor Projects

Branch,Section II

ga

at

cygne

Ins ection

Summar

Ins ection

on Jul

15 throu

h Au ust 25

1990

Re ort Numbers

an

e

Areas Ins ected:

Routine, onsite,

regular and backshift inspection

by

t e t ree ress

ent inspectors

and one inspector

from the Region

V staff.

Areas inspected

included: previously identified items; review of plant

activities; engineered

safety feature

system walkdowns; monthly

surveillance testing; monthly plant maintenance;

reactor trip and restart

- Unit 1;

damaged

reactor trip breaker - Unit 1; alarming dosimeter

issued incorrectly - Unit 1; main steam pressure

safety valve testing-

Unit 2; post refueling restart - Unit 2; restart reactor physics

evaluation - Units 1 and 2; main feedwater isolation valve alignment-

Unit 3; improper 0-ring material in Anchor Darling four-way hydraulic

valves

Unit 3; plant shutdown forced by slipped control element

assembly - Unit 3; spent fuel pool activities - Units 1,

2 and 3; motor

operated

valve maintenance

and testing - Units 1,

2 and 3; review of

licensee

event reports - Units 1,

2 and 3; and review of periodic and

special

reports - Units 3.,

2 and 3.

During this inspection the following Inspection

Procedures

were utilized:

30703,

37700,

37828,

40500,

61705,

61706,

61707,

61708,

61710,

61726,

62703,

71707,

71710,

72700,

86700,

92700,

92701,

92702,

and 93702.

'I

90<02~002S

P00PZ~

PDR

ADOCK 05000528

Q

PbC

Results:

Of the 18 areas

inspected,

one violation was identified and is

being cited.

This violation related to an improperly set alarming

dosimeter.

Three non-cited violations involve two missed surveillance

tests

and one missed Technical Specification Action Statement.

General

Conclusions

and

S ecific Findin s

Si nificant Safet

Hatters:

None

Summar

of Violations:

Summar

of Deviations:

1 Cited Violation (Unit 1) and

3 Non-Cited Violations (Unit 2)

None

0 en Items

Summar

16 items closed,

2 items left open,

and

7 new items opened.

Persons

Contacted:

DETAILS

The below listed technical

and supervisory personnel

were

among-

those contacted:

Arizona

ublic Service

Com an

  • R.

J.

F.

H.

AT

p.

p.

0

A'p

W.

)hE

J.

R.

S

"K.

R.

  • p

+W.

  • S

J.

J.

W.

)kG

  • J

"R.

  • C

E.

J.

T.

J.

J.

"W.

E.

R.

G.

D.

C.

L.

J.

R.

Adney,

Bail ey,

Buckingham,

Bieling,

Bradish,

Brandjes,

Caudill,

Carnes,

Coffin,

Conway,

Dotson,

Draper,

Flood,

Guthrie,

Hall,

Henry,

Hughes,

Ide,

Kanter,

Levine,

LoCicero,

Marsh,

Minnicks,

Overbeck,

Reynolds,

Rouse,

Russo,

Sandhoff,

Schmadeke,

Shriver,

Scott,

Sills,

Simko,

Simpson,

Snell,

Sowers,

Stover,

Stewart,

Templeton,

Fogar ty,

Younger,

Plant Manager,

Unit 3

Vice President,

Nuclear Safety

8 Licensing

Operations

Manager,

Unit 2

Emergency Plan/Fire Prevention

Manager

Compliance

Manager

Central

Maintenance

Manager

Site Services Director

Operations Shift Supervisor,

Unit 3

Compliance

Engineer

Executive Vice President - Nuclear

Director, Site Engineering

8 Construction

S.C.E., Site Representative

Plant Manager, Unit 2

Deputy Director, Quality Assurance/QC

El Paso Electric Engineer

Salt River Project, Site Representative

General

Manager,

Radiation Protection

Plant Manager, Unit 1

Participant Services,

Senior Coordinator

Vice President,

Nuclear

Power Production

Independent

Safety Engineering

Manager

Plant Operations

8 Maintenance Director

Maintenance

Manger, Unit 3

Technical

Support Director

I8C Maintenance

Manger, Unit 3

Compliance Supervisor

.

Quality Control Manager

QAQl, Engineer

Work Control Manager,

Unit 3

Work Control Manager,

Unit 1

General

Manager, Site Chemistry

Rad. Protection Tech/Svcs.

Acting Manager

Maintenance

Manager, Unit 2

Vice-President of Engineering

8 Construction

Chairman-Arizona Public Service

Company

Engineering Evaluations

Manager

Nuclear Safety Manager

Employee

Concerns

Program

Manager

I. S. E., Senior Engineer

Work Control Manager,

Unit 2

Plant Standards

and Control Manager

The inspectors

also talked with other licensee

and contractor

personnel

during the course of the inspection.

4

"Attended the Exit meeting held with NRC Resident

Inspectors

on,

August 30,

1990.

2.

Previousl

Identified Items - Units 1

2

and

3

92701

92702)

Unit

a.

(Closed)

Enforcement

Item

528/89-43-02

"Plant Review

oa

evlews

-

nl

b.

This item involved the failure of the

PRB to document

their review of Technical Specification violation events,

ensure

adequate

corrective actions

were taken,

and to

document their determination if unreviewed safety

questions

existed.

The inspector

reviewed

LERs which were

issued

since the corrective actions for this violation

were implemented.

Between January

5, 1990,

and July 17,

1990, the

PRB reviewed

19

LERs and had not reviewed

15

LERs issued during this time period.

As a result of

the inspector's

questions

the

PRB scheduled

a meeting

on

August 29, 1990, to review the backlog of LERs but was

unable to hold it due to schedular conflicts.

The

inspector

acknowledges

the fact that the

PRB has recently

undergone

a reorganization

which required

a Technical

Specification

amendment

and revised their program for LER

reviews

by having

a Compliance

Engineer present

issued

LERs to the

PRB at their meetings.

At the exit meeting

the licensee

acknowledged that

LERs can

be reviewed in a

more timely fashion.

The inspector will continue to

review this area

as part of the routine inspection

program.

This item is closed.

(Closed)

Enforcement

Item

528/90-12-01:

"Deener izin

our

anne

s

0

0 arl

mlc

ower

xcore

eu ron

ux

nstrumentatson

-

nit

e

Thi s item involved the

1 icensee'

intentional

deenergization

of all four channels of Logarithmic Power

Excore Neutron Flux Instrumentation.

The licensee

restored

one channel

approximately five days after'all

channels

were deenergized.

This returned the plant to a

condition covered

under Technical Specifications.

The

Plant Director issued Plant Guideline

No. 12, "Entry Into

Conditions Not Defined by Technical Specifications"

which

expressly prohibits voluntary plant operation in any

'...condition not explicitly addressed

by the Technical

Specification."

The guideline does not prevent operators

from exercising their discretion under 10 CFR Part 50.54x.

The inspector concluded that the action and the

APS and

Region

V management

discussions

on March 30, 1990,

appear

to address this concern.

This item is closed.

p

~

0

~,

Unit 2:

a.

(Closed)

Followu

Item

529/89-30-02):

"Feedwater

Suction

s )n

as

ure

-

n)t

Piping associated

with valves

CDN-V628 and

FWN-V110 failed

on July 4, 1989, while the unit was at power,

and forced

a

plant shutdown.

This item was opened pending the

corn)letion of technical analysis,

documented

in

Engineering Evaluation Request

(EER) 89-FW-013.

The

inspect'or

reviewed this

EER, which concluded that the

cause of the failures were .indeterminate.

The

EER stated

that the failures appeared to be due to cyclic stresses

which resulted in fatigue cracking.

Both calculations

and

field observations

supported this conclusion,

though the

. deflection was less than the predicted failure amplitude.

The vibrations appeared

to have been

caused

by reverse

flow through the "B" feedwater

pump bypass valve, which

was found approximately 3/4 inch open.

The licensee

determined in EER 89-FW-021 that additional procedural

controls were needed to prevent excessive

vibration in the

bypass

lines.

These controls

have

been incorporated

and

procedure

4XOP-XZZ14, "Feedwater

and Condensate,"

revised

for all three units.

Additionally, the other-small

pipe

welds in the vicinity were dye penetrant tested

and

no

crack indications were identified.

The inspector

reviewed Incident Investigation Report (IIR)

3-2-89-031.

IIR 3-2-89-031 concluded that the feedwater

pump bypass

valve had been improperly left partially open,

even though

an Auxiliary Operator

(AO) had signed

a step

in a valve alignment during plant startup verifying the

valve was closed.

The discrepancy

resulted

from

miscommunication

among the three

AOs, who jointly

performed the lineup, in determining which valves

had been

checked.

The

AOs involved were counseled

regarding the

necessity for formal communication

when performing

evolutions.

The inspector concluded that the licensee's

actions with

respect to this event were adequate.

This item is closed.

(Closed

Followu

Item

529/89-30-03):

"Work on

Re ulator

er

er

a

nstructlon

-

nest

9

This item was reviewed in Inspection Report 50-529/89-49,

paragraph 2.f, and Inspection

Report 50-529/89-54,

paragraph

2.g,

and was left open pending completion of the

licensee's

equality Assurance

review of programmatic

controls of vendor supplied information.

The licensee

completed its review of these controls

and concluded that

changes

which had been previously. made were ineffective.

Two Corrective Action Reports

(CARs) were issued to

address

identified deficiencies related to this topic.

CAR CS89-0058 pertains to Work Orders

(WOs) being issued

containing out of date

or unapproved

information from

vendor technical

manuals.

This

CAR resulted in several

procedure

revisions,

some training,

and several

additional

procedui e changes

were proposed

but evaluated

as not being

necessary.

CAR CS89-0059 pertains to inadequate

controls regarding

the control, approval

and issuance

of vendor technical

manuals.

This

CAR resulted in procedural

changes

intended

to insure that only "Status

1" vendor technical

manuals

(those with no outstanding

licensee

comments following

review) may be used

as reference

material to support work

at Palo Verde.

This issue

was also addressed

in

NRC

Inspector

Followup Item 529/89-30-04

and closed in

Inspection

Report 529/89-23.

Based

on the implementation

of, these corrective actions

and the continuing long-term efforts of the licensee's

Vendor Technical

Manual Project, this item is closed.

Closed)

Followu

Item

529/89-36-02

"Post-Tri

Reactor

estart Crstersa

-

nit 2

2 01

During review of actions following the July 12,

1989 trip

of Unit 2, the inspectors

noticed discrepancies

and

informalities in the licensee's

decision making prior to

restart of the unit.

In response

to the inspector's

c'oncerns,

the licensee

strengthened

the administrative

controls regarding unit restart determinations

and

included specific criteria to be used for the restart

decision.

These

changes

are

documented in procedures

79DP-OIP01, "Incident Investigation Report Preparation,"

and 79AC-OIP01, "Incident .Investigation Category

1 and

2

Incidents."

In reviewing these revised procedures,

the inspector noted

an administrative error in the "Restart Criteria" section

of 79AC-OIPOl.

The criteria are divided into two cases,

depending

on whether or not the cause of the trip is

known.

However,

due to errors in the paragraph

numbering,

this division is not clear,

and as written, could lead to

a reactor restart without the intended reviews.

The

licensee

stated that it is unlikely that a restart would

occur without the intended reviews

because of the

management

attention given to both reactor trips and

restarts.

The licensee

committed to include clarifying

changes to these

procedures

in major revisions

expected

to be completed

by March 31, 1991.

The

NRC inspectors

routinely monitor post-trip actions

and restart

activities,

and

no related deficiencies

were identified

during the recent Unit 1 post-trip .restart decision;

therefore, this item is closed.,

Unit

a.

3

~

Closed)

Followu

Item (530/89-21-01):

"Loss of

S ent Fuel

oo

eve

-

nit

This item resulted

from an inadvertent loss of Spent

Fuel

Pool

(SFP) level

due to inaccurate

control

room valve

status

drawings.

This event occurred

on May 22, 1989,

and

in response

the licensee

committed to a broad review of

system status

control requirements.

On August 2, 1989,

Unit 1 experienced

a loss of SFP level

due to an improper

valve alignment.

This was. documented in NRC Inspection

Report 528/89-36

and resulted in a Notice of Violation

(528/89-36-01).

In the licensee's

response

to the Notice

dated

November 21, 1989, the licensee

reported that the

review of system status control

had been completed

and

also described

changes that were planned.

On January

23,

1990, the licensee transmitted the schedule for

implementing these

changes

to the

NRC.

Additionally, on

June

14, 1990, the licensee transmitted to the

NRC the

list of separate

SFP operating procedures

to provide

clearer,

more detailed directions for operators.

These

were originally expected to be in place

by January

10,

1990, but subsequently

the licensee

revised this date to

August 20,

1990.

These procedure's

have

been

implemented.

Based

on the licensee's

progress

on this 'issue,,this

item

is closed.

However, the inspector will review these

changes

when reviewing item '(528/89-36-01) for closure.

b.

(Closed

Enforcement

Item

530/89-36-01:

"Emer enc

iese

enerator

xcess

ow

ec

a ves

o

so ate

as

e uvre

-

n)t

This item resulted

from an interim disposition of an

Engineering Evaluation

Request

(EER) which required that

Excess

Flow Check valves

on all EGG's

be isolated pending

further engineering analysis

and final

EER disposition.

The required isolation was put into effect in Units 1 and

2, but was not implemented in Unit 3.

The inspector

noted

that the licensee's

corrective action to prevent

recurrence

was to issue

a policy memorandum to all system

engineers

requiring formal written transmittal of any

immediate action required by an

EER interim or final

disposition.

Although some weaknesses

in the engineering

communication to user groups

have

been noted in Inspection

Report 530/90-12 since the event in'question,

none

have

involved the failure to implement immediate required

actions.

This item is closed.

C.

(0 en) Followu

Item (530/89-36-02):

"Surveillance Test

ro rammat) c

an es

-

n)

The inspector reviewed the report of a complete

programmatic review of the Surveillance Test (ST) program

prepared

by a .licensee

outside contractor.

The licensee

has not yet incorporated

the recommendations

of this

report into the procedures

governing the

ST program.

Training for the approved procedure

changes

was in

progress

at the end of the inspection report period.

This

item will remain

open pending review of programmatic

"

changes

resulting from the con'tractor's

report.

(Cl'osed)

Enforcement

Item

530/89-36-03

"RCS

S ill

ue

o

a ve

e uencsn

rror

-

ns

This item resulted

when an, Auxiliary Operator

(AO)

performed

a valve lineup in which the improper sequencing

of valves being positioned allowed an inadvertent

RCS flow

path resulting in a primary coolant spill.

The inspector

noted the licensee's

actions to prevent recurrence

included discussions

with Unit 3 operating

crews regarding

communications practices

and identification of- important

valving sequences

when appropriate.

In addition,

a

"sequence"

column was added to the valve lineup sheet

used

to document

and control valve alignments.

This lineup

sheet

was subsequently

discontinued

and replaced

by a form

incorporated

in the Conduct of Shift Operations

procedure,

40AC-90P02, for "special variance" alignments which

includes

a sequence

column.

The inspector

reviewed

several

of these

forms in plant files and also reviewed

clearance

restoration

forms,

and concluded that licensee

personnel

were specifying alignment sequence

on these

documents.

This item is closed.

(Closed

Followu

Item (530/89-54-01:

"Sandblast Grit

oun

) n

nstrument

s r

ose

-

ns t

This item resulted

from the licensee's

investigation of an

improperly operating feedwater control valve, which

determined that a significant quantity of sandblast grit

was present in the air operator

boosters

relay.

The source

of this grit was traced to a newly installed air hose.

The licensee

determined that the grit came from sand-

blasting the end fittings of the hoses prior to brazing

the end connectors

into place.

The grit remained inside

the hose

when the supplier capped the ends

and delivered

them to APS.

The inspector

reviewed

EER 90-IA-004, which analyzed

and

confirmed the source of the grit and initiated corrective

actions.

These actions consisted of quarantining

and

cleaning other hoses

purchased

from the

same supplier

and

changing the configuration item description for applicable

class

and item numbers.

In addition, the licensee

confirmed that similar hoses

purchased

from this supplier

were not installed in other plant systems

and completed

a

training briefing for maintenance

personnel

in all units

on the need for thoroughly inspecting

new components prior

to installation.

The licensee

determined that

a change to

the Conduct of Maintenance

procedure

was not warranted.

The inspector

concluded these actions

were appropriate.

This item is closed.

3.

Review of Plant Activities (71707

and 93702)

a.

b.

Unit 1

The Unit began the report period in Mode 1 at 100 percent

power.

Operational

concerns

included:

electrical

problems with CEA 30 which were corrected;

an increase

in

containment

gases

caused

by minor leaks; frequent alarms

from the loose parts vibration monitoring system which has

deceased

during the report period and appears

to have

stabilized;

and inoperable diesel

generator fuel oil tank

cathodic protection resulting from the const uction of the

Operations

Support Building.

A reactor trip occurred

on

August 14, 1990,

as discussed

in Paragraph

7.

The unit

entered

Mode 2 on August 19, 1990:

The plant ended the

report period at 100 percent

power.

Unit 2

Unit 2 entered this period in Mode 2, having just

completed.its

Cycle

3 refueling outage.

The unit entered

Mode 1 on July 18, 1990,

and synchronized to the grid on

July 19,

1990 (Paragraph ll).

The generator

was brought

briefly off-line for turbine overspeed testing

and was

synchronized to the grid again

on July 19, 1990.

Power

ascension

was performed in conjunction with routine

post-refueling reactor physics testing, but was

hampered

by problems with the Core Operating Limits Supervisory

System, vibrations of a Hain Feedwater

Pump

(MFP) "B"

bearing,

and improper operation of the

HFP "A" miniflow

recirculation valve.

High condenser

hotwell sodium levels forced a power

reduction to 40 percent

on July 30 to allow leaking

condenser

tubes to be identified and plugged.

The power

ascension

was

resumed

on August 2 and full capacity

was

attained

on August 9.

Power was reduced to about

85 percent

on August 16 after power was lost to No.

3

Cooling Tower (CT) as

a result of heavy rains.

Following

the return of CT "3" to service,

condensate

pump "B"

tripped on August 15, 1990, for an undetermined

reason,

while the unit was at 93 percent

power, resulting in

another

unplanned

downpower.

The unit was returned to

100 percent

power on August 16, 1990.

A failure of the

Core Operating Limits Supervisory

System

(COLSS)

on

August 16, 1990, forced a power reduction to 78 percent.

COLSS was restored to service

and the unit returned to

full power the following day.

The unit remained at

essentially

100 percent

power for the rest of the

reporting period.

c.

Unit 3

Unit 3 began this report period operating at 100 pe'rcent

and continued until August 5, 1990,

when an orderly

shutdown

was completed following an unsuccessful

attempt

to restore

a slipped

CEA.

A faulty circuit card

w'as

identified and replaced

and the Unit was restarted

on

August 7, 1990 (see

Paragraph

15).

Full power operation

was restored

by August 9, 1990,

and the unit continued at

full power through the end of the inspection report

period.

d.

Plant Tours

The following plant areas at Units 1,

2 and

3 were toured

by the inspector during the inspection:

Auxiliary Building

Containment Building

Control

Complex Building

Diesel Generator Building

Radwaste Building

Technical

Support Center

Turbine Building

Yard Area and Perimeter

The following areas

were observed

during the tours:

. l.

0 eratin

Lo s and Records - Records

were reviewed

against

ec n)ca

peer

scations

and administrative

control procedure

requirements.

2.

Monitorin

Instrumentation - Process

instruments

were

o serve

or corre at>on

etween channels

and for

conformance with Technical Specifications

requirements.

3.

Shift Staffin

- Control

room and shift staffing were

o serve

or conformance with 10 CFR 50.54.(k),

Technical Specifications,

and administrative

procedures.

4.

E ui ment Lineu s - Various valves

and electrical

rea ers were verified to be in the position or

condition required by Technical Specifications

and

administrative procedures for the applicable plant

mode.

5.

~Ei ti

i

-Sl td

pip t,f

hih

tagging requests

had been =initiated,

was observed to

~

~

verify that tags

were in place

and the equipment

was

in the condition specified.

6.

= General

Plant

E ui ment Conditions - Plant equipment

was

o serve

or sn scatsons

o

system leakage,

improper lubrication, or other conditions that would

prevent the systems

from fulfillingtheir functional

requirements.

7.

Fire Protection - Fire fighting equipment

and

~b

df

i hi hi

Specifications

and administrative procedures.

8.

Plant Chemistr

- Chemical analysis results

were

revsewe

or conformance with Technical

Specifications

and administrative control procedures

9.

Securit

- Activities observed for conformance with

regu atory requirements;

implementation of the site

security plan,

and administrative procedures

included

vehicle and personnel

access,

and protected

and vital

area integrity.

10.

Plant,Housekee

in

- Plant conditions

and

materia

equipment storage

were observed to determine

the general

state of cleanliness

and housekeeping.

ll.

Radiation Protection Controls - Areas observed

inc u

e

contro

po)nt operation,

records of

licensee's

surveys within the radiological controlled

areas,

posting of radiation and high radiation areas,

compliance with Radiation Exposure Permits,

personnel

monitoring devices

being properly worn, and personnel

frisking practices.

During this reporting period,

a primary resin sluicing

operation in Unit 1 resulted in unexpectedly

high radiation

levels in the

Radwa te Building.

Levels reached

the threshold

for posting

as

a Locked High Radiation Area.

Licensee

personnel

were prompt in identifying this condition as it

occurred

and in securing

and posting the area.

The inspector

sent the licensee's

incident investigation report to

NRC Region

V for. review by the Health Physics staff.

No violations of NRC requirements

or deviations

were

identified.

4.

En ineered Safet

Features

S stem Walkdowns - Units 1

2 and

3

Selected

engineered

safety features

systems

(and systems

important to safety)

were walked down by the inspector to

confirm that the systems

were aligned in accordance

with plant

procedures.

10:-

Dur ing this inspecti on peri od the inspector s walked down

accessible

portions of the following systems.

Un.it 1

o 'igh Pressure

Safety Injection

Unit 2

o

High Pressure

Safety Injection

Unit 3

o

High Pressure

Safety Injection

No violations of,NRC requirements

or deviations

were

identi fied.

5.

Monthl

Surveillance Testin

- Units 1

2 and

3

61726)

ao

b.

Selected

surveillance tests

required to be performed

by

the Technical Specifications

(TS) were reviewed

on a

sampling basis to verify that:

1) the surveillance tests

were correctly included

on the facility schedule;

2) a

technically adequate

procedure

existed for performance of

the surveillance tests;

3) the surveillance tests

had been

performed at the frequency specified in the TS; and 4)

test results satisfied acceptance

criteria or were

properly dispositioned.

Specifically, portions of the following surveillances

were

observed

by the inspector during this inspection period:

Unit 1

~roce ure

o 41ST-1AF02

o 72ST-9RXOl

o 72ST-1RX13

o 72ST-9RX02

Descri tion

AFA-P01 Surveil lance

Core Reactivity Balance

Monthly Core Performance

Surveillance

99 Percent

MTC Determination

Unit 2

~roce

ure

Descri tion

o 36ST-9SB04

o 77ST-2SBll

Plant Protection

System

(PPS)

Hot

Functional Test

Control Element Assembly Calculator

(CEAC)

No.

1 Functional Test

Unit 3

~roce

ure

Descri tion

o 73ST-3XI16

Feedwater

Isolation Valve No.

174 Fast

Stroke Test

No violations of NRC requirements

or deviations

were

identified.

6.

Monthl

Plant Maintenance - Units 1

2 and

3 (62703

a 0

b.

During the inspection period, the inspector observed

and

reviewed selected

documentation

associated

with

maintenance

and problem investigation activities listed

below 'to verify compliance with regulatory requirements,

compliance with administrative

and maintenance

procedures,

required equality Assurance/equality

Control involvement,

proper

use of safety tags, .proper equipment alignment

and

use of jumpers,

personnel

qualifications,

and proper

retesting.

The inspector verified that reportability for

these activities was correct.

Specifically, the inspector witnessed portions of the

following maintenance activities:

Unit 1

Descri tion

o

Control

Element Drive Mechanism

Power Switch

Connection Troubleshooting

Unit 2

Descri tion

o

Troubleshooting

Steam

Bypass Control Valve SGN-1007

o

Troubleshooting/Repair

SGN-1007 Electronics

o

Troubleshooting/Repair

Diesel Generator

"A" Starting

Air Pressure

Annunciator

Unit 3

Descri tion

o

Rebuild four-way valve for 3SGA-UV-177

o

Install four-way valve for 3SGA-UV-181

No violations of NRC requirements

or deviations

were

identified.

7.

Reactor Tri

and Restart - Unit 1

71707

and 93702

a ~ ~RT

T

R

On August 14, 1990, at 10:23

PM (MST), Unit 1 experienced

an automatic reactor trip from 65 percent reactor

power

t

12

due to high pressurizer

pressure.

The operations staff

had just completed

a rapid power reduction to 65 percent

and

had manually trip~ed the main turbine due to loss of

cooling to the

Phase

'B" Main Transformer.

Prior to the event,

the unit was operatin~ at 100 percent

power.

At 9:23

PM, a Main Transformer

"B

trouble alarm

was received.

An Auxiliary Operator found the supply

breaker for cooling system control power to the Main

Transformer tripped.

Attempts to restore control power to

the cooling system were unsuccessful.

At 9:59 AH, personnel

observed that

no cooling fans were

operating

on Main Transformer "B".

The Hain Transformer

alarm response-procedure,

41AL-1MAOl, directed the

operators

to de-energize

the transformer within 30

minutes.

A rapid power reduction

was

commenced at

10: 02,PM.

The operations staff realized the time limit

would not be met and prepared for a manual turbine trip.

A brief tailboard was conducted

and at 10:23

PH the main

turbine was manually tripped from 65 percent reactor

power.

A Steam

Bypass Control System

(SBCS) quick open signal

was

received

and the seven in-service valves

opened

as

designed.

Approximately 27 seconds after the turbine

trip, a reactor trip due to high pressurizer

pressure

was

received.

The unit was stabilized in Mode 3 and the event

was classified

as

an uncomplicated reactor trip.

Post-Tri

Investi ation

The licensee

conducted

an investigation into this event,

documented

in Incident Investigation Report (IIR)

2-1-90-003.

This investigation determined that the cause

of the Main Transformer cooling system failure was

an

internally faulted control power transformer.

The root

cause of this failure is being pursued

by the licensee.

The

SBCS was expected to prevent

a reactor trip on loss of

load.

However, it was later determined that a trip would

likely occur with one

SBCS valve out of service

upon loss

of load at approximately

70 percent

power or at

approximately

30 percent power.

One

SBCS valve was out of service

based

on a vendor

recommendation

to prevent overcooling due to excess

SBCS

capacity

upon loss of load from 100 percent power.

This

recommendation

was implemented

on February 4,,1989.

Post-Restart

Action Item No. 807, resulting from the

March 3, 1989, Unit 3 reactor trip event, further

addressed

this issue

by requiring a third party review of

SBCS optimization be conducted.

A May 3,

1989 report,

"SBCS Detailed System Investigation," performed

by the

13

licensee,

recommended

that the vendor evaluate

the

SBCS

"to obtain margin to reactor trip actuation for loss of

load and loss of feed

pump events."

Licensee

engineers

reviewed the vendor's evaluation

and found no substantive

problems,

and Post Restart

Item No.

807 was closed

on

April 17,

1990.

Following the August 14, 1990, trip, the

inspector

found that the evaluation report was

and

curgeptly remains in draft form, although its status

had

been questioned

by the

NRC inspector

on June 5, 1990.

The

licensee

stated that the vendor evaluation

had not been

substantially

changed

since the April 17,

1990 review,

and

that the information regarding the absence

of a margin to

reactor trip upon loss of load at 30 percent

power and

..70 percent

power,

was probably available at that time.

equality Deficiency Report ((DR) No. 90-0329

was issued to

evaluate

the discrepancy

between the Updated Final Safety

Analysis Report, which describes

a full load rejection

capability,

and the actual plant inability to withstand

a

loss of load without a reactor trip at certain power

levels

(30 and 70 percent power).

Additionally, the

licensee

committed to determine

why their review of the

vendor evaluation failed to identify the zero margin to

trip, which was

one of the central

purposes

of the

evaluation.

The inspector will review the results of

these evaluations

when available,

followup item

(528/90-28.-01).

Additionally, the inspector is concerned with the

licensee's

closure of Post Restart

Item No. 807 based

on a

draft report.

These

issues

appear to demonstrate

a lack

of thoroughness

in engineering

evaluations

and assurance

of the adequate

resolution of post-restart

issues.

The

inspector will continue to review Post-Restart

Action

Items as part of the routine inspection program.

Unit Restart

Following completion of repairs to the transformer cooling

control

system

and other minor maintenance,

the licensee

restarted

the reactor, with criticality achieved

on

August 18, 1990.

Mode 1 was entered

on August 19 and the

generator

was synchronized to the grid later the

same

day.

The licensee

considered

the higher risk of a reactor trip

if a loss of load occurred at near

30 percent or 70

percent

power 'with one out of eight

SBCS valves out of

service.

However, the licensee

also considered that the

reactor is generally not operated

in these

ranges for very

long and evaluated

the risk of experiencing

an unnecessary

Safety Injection following a reactor trip from any power

level

due to overcooling by all eight

SBCS valves.

The

licensee's

conclusion

was that continued

removal of one

SBCS valve from service

was warranted.

The inspector

concluded that the licensee's

actions

were acceptable

while long term remedies

were considered.

No violations of NRC requirements

or deviations

were

identified.

Dama

ed Reactor Tri

Breaker - Unit 1 (93702

On August 18, 1990, the licensee

discovered

bent linkage in

Reactor Trip Breaker "B".

The breaker could not be closed

during the preparations

to restart the reactor

and

some bent

'inkage

was discovered

when the breaker

was racked out and

inspected.

A spare

breaker

was obtained

from the warehouse;

however,

not all necessary

surveillance tests

could be

performed prior to going to Mode 2.

Licensee

personnel

with

licensee

management

input and after evaluation of Technical

Specification requirements

concluded that changing to Mode 2

was not prohibited with the trip breaker not racked in and

tagged out and not yet demonstrated

to be fully operable.

Mode

2 was entered

and the trip breaker subsequently

declared

operable.

The inspector

noted that

a Root Cause of Failure-

Engineering Evaluation Request

was issued

and was not complete

at the end of the report period.

This event review will remain

open

as

an inspector followup item (528/90-28-02)

pending

completion of EER 90-SB-046.

No violations of NRC requirements

or deviations

were

identified.

Alarmin

Dosimeter Issued Incorrectl

- Unit 1

71707)

On August 14, 1990, the

NRC inspector

was issued

an alarming

dosimeter

by a Shift Radiological Protection

(RP) Technician at

the

RP "island" as required

by the Radiological

Exposure

Permit

(REP) for a high radiation area.

The inspector observed

the

technician turn the dosimeter

on, check the batteries,

reset

the alarm setpoint switches to 50 millirem, and then issue the

dosimeter.

The inspector questioned

the technician

as to

whether the alarm setpoint

was changed

by moving the switches

with the unit on or whether the unit would have to be reset or

have the power cycled off, then on, for the

new alarm setpoint

to be in effect.

The technician admitted to not knowing and

subsequent

discussions

revealed that the power would have to be

cycled off then

on for the

new setpoint to be in effect.

Therefore,

the alarming dosimeter

issued to the inspector

was

not set to the alarm setpoint required by the

REP.

This is a

violation of NRC requirements,

Enforcement

Item (528/90-28-03).

The inspector brought this to the attention of the Unit RP

Manager

who surveyed

RP Technicians

in all three units and

determined that approximately 20-30 percent of the

RP

Technicians

did not know the correct

sequence

for setting

up an

alarming dosimeter.

The inspector also met with an

RP

Technician at the

RP Calibration Facility and confirmed that

15

new alarm settings

are not effective until either the power is

cycled off, then on, or the reset button is pressed..

The

inspector

noted that there

was

no APS procedure for setting the

alarming dosimeter

and that the technical

manual did specify

the correct sequence.

Initial RP technician training given to new

RP technicians

does

address, specific instructions

on setting the alarming

dosimeters.

For continuing training, the inspector 1dentified

two concerns:

(1) during the last

RP Continuing Training done

in April 1989, the

Z Tech alarming dosimeter

was in predominant

use

and not the presently

used Dositech dosimeter (different

procedures

for setting the alarm setpoints);

and (2)

experienced

RP Technicians

were "grandfathered"

when this

course

began

and therefore did not receive this training.

The

next Continuing

RP Training course is scheduled for April 1991,

which will include proper alarming dosimeter

setup.

The Unit 1

RP Manager issued

a

memo to all Unit 1

RP Technicians with

copies to Units 2 and

3

RP Mangers.

Site

RP is considering

whether additional

procedura1

requirements

are necessary.

Unit 1

RP also reviewed all individuals who received

a dose

greater

than

50 millirem since the beginning of 1990.

In no

case did an individual receive

a dose greater than that for

which the alarming dosimeter

should

have

been set.

The inspector

noted that during the Unit 1 outage dosimetry was

issued

by contract Dosimetry Technicians

who appeared

to set

alarming dosimeters

properly.

When the outage

ended,

the Shift

RP Technicians

took over this responsibility.

It appears

that

the turnover of this responsibility was incomplete

and

some

Shift Technicians

issuing alarming dosimeters

did not receive

adequate training to assure that the alarming dosimeters

would

consistently

be issued in accordance

with the applicable

REPs.

One violation of NRC requirements

was identified.

/

Main Steam

Pressure

Safet

Valve (PSV

Testin

- Unit 2

The inspector

reviewed the documentation

associated

with

performance of Surveillance Test 73ST-9ZZ18,

"Main Steam

PSV

Set Pressure Verification," which was completed in July 1990,

in Unit 2.

In discussing

the interpretation of chart recorder

data with personnel

who performed the test,

the inspector

observed that the charts alone were inadequate

to determine the

liftpressure

in some cases.

The test personnel

explained that

the test performer

had to listen for indications of the

PSV

lifting and that this information was

used in conjunction with

the chart information to determine the percent of load cell

capacity at which the

PSV began to lift. This figure is then

used in calculations to determine the liftsetpoint of the

valve.

J

h

g

S

Upon reviewing the procedure,

the inspector

noted that there

are

no instructions

regarding

how to actually perform the test,

or how to set

up the Trevitest equipment

on the

PSV.

There are

also

no notes or other guidance to clarify the test

methodology.

The procedure

simply. instructs the vendor

representative

to perform the test.

, According to licensee

personnel

involved with the test,

the vendor does not have or

use

any procedures

in setting

up the Trevitest equipment or in

performihg'the test.

A vendor technical

manual is available

but was not referred to during the test.

The licensee

stated that the vendor representatives

who

actually perform the test are extremely well trained

and

experienced with respect to the Trevitest method of PSY set

pressure verification.

Additionally, licensee test technicians

must complete training on Section XI testing in accordance

with

procedure

73DP-OTROl, "qualification and Training Requirements

for Component

and Specialty Engineering."

However,

one of the

lead engineers

assigned

as Test Director for a licensee test

team was

a contractor qualified to ANSI N3.1-1978, but lacked

any prior experience with this type of testing.

He was only

given oral briefings of the test methodology

and procedure

prior to performing the Surveillance Test (ST).

The inspector

concluded that given the minimum training requirements

(ANSI

N3. 1-1978), the procedure

lacked sufficient detail.

A previous revision of the

ST procedure

had more detail

regarding conduct of the test.

However, these

steps

were

removed

because

each step

was too time consuming

and

interrupted the normal progress

of these relatively quick

moving test activities.

However, the inspector concluded that

the absence

of any procedural

steps

addressing

the setup of the

Trevitest equipment or the conduct of the test resulted in

final test data which did not appear consistent.

As a result of these discussions,

the licensee

committed to

revising procedure

73ST-9ZZ18 to include adequate

detail to

assure

consistent

and meaningful test performance

and results.

Instruction Change

Request

No.

38052 was submitted

on

August 10, 1990, to this effect.

The inspector

had no further

questions

and will follow implementation of the licensee's

procedural

improvements,

Followup Item (529/90-28-01).

No violations of NRC requirements

or deviations were

identified.

Post Refuelin

Restart - Unit 2 (71707

The inspector

observed activities

on July 19, 1990, associated

with turbine generator

overspeed testing

and synchronizing the

generator to the grid.

These activities were, in general,

well

controlled and completed in an acceptable

manner.

During the

operation of the turbine and associated

systems,

the inspector

observed

a control

room operator operate

the control

17

e

(MTN-HS-242) for the valves associated

with turbine stop valve

before seal drains,

using

a pair of needle-nose

pliers, since

the

knob for the switch had broken

and not been replaced.

The

Operations

Manager stated that the control board discrepancy

was noted

a week earlier and that replacement

parts were not

readily available.

The inspector

noted that the switch was

replaced

a few days after the startup.

During the'ower ascension,

on July 20, 1990, licensee

engineers

noted problems

wi~th the performance of the Core

Operating Limits Supervisory

System

(COLSS).

The power

ascension

was interrupted for several

hours while these

problems

were being resolved.

The first problem resulted

from

a point in a database

being deleted in a manner which

ultimately caused all later values to be offset by one location

in the database,

so that the

COLSS software went to the wrong

database

location to retrieve required information for

.processing.

The operators

noted the abnormal

COLSS power

limit.

The second

problem involved an apparent transposition

of information from the vendor into the Plant Computer via a

Work Order.

The Core Monitoring Computer was unaffected.

This

error affected the incore sensitivity files in such

a way that

the azimuthal tilt alarm did not clear during startup.

The

licensee is investigating both 'these

problems in Incident

Investigation

Reports (IIRs) 3-2-90-30

and 3-2-90-31.

The

.

inspector will review licensee

actions

and conclusions with

respect to these

events,

Followup Item (529/90-28-02).

High vibration was observed

by the licensee in the "B" Main

Feedwater

Pump

(MFP) on July 26, 1990, while the Unit was at

about 70 percent

power.

This forced

a downpower to 65 percent

to allow the

HFP bearings to be replaced.

The "A" HFP miniflow valve was isolated

on July 26, 1990, after

it unexpectedly

opened.

Problems

were later found in its

controller.

Operators

were sensitized to the need to trip the

reactor

and the

HFP if a loss of load occurred while the

miniflow was isolated to the only operating

HFP.

Power was reduced to about 40 percent

on July 30, 1990,

due to

elevated

sodium levels in the condenser

hotwells.

Water box

inspections

revealed

considerable

debris, including pieces of

plywood, in one train of Circulating Water (CW).

Additionally,

several

tubes

were found to be leaking and were plugged.

The power ascension

was

resumed

on August 2, 1990,

and

100 percent

power was reached

on August 9, 1990.

No violations of NRC requirements

or deviations

were

identified.

e

18

12.

Restart

Reactor

Ph sics Evaluation - Units

1 and

2

61705

1

0 an

, The inspector

observed

the Unit 1 Reactor Startup, portions of

the Unit 1 and

2

Low Power

Physics Testing,

and portions of the

Power Ascension Testing.

The following procedures

were

reviewed:

Units 1 hnd 2:

72PY-9RX01

72PA-9ZZ07

72PA-9RX03

72PA-9SB01

72PA-9RX01

Unit 1

Onl

Reload Criticality and

Low Power

Physics Testing

Reload

Power Ascension Testing

Secondary Calorimetric Power Verification

Core Protection Calculator/Core

Operating Limits

Supervisory

System Input Inter-comparison

Power Calibration

720P-ORX05,

72ST-9RX02

Unit 2 Onl

Return to Criticality During Low Power Physics

Testing

99 percent Hoderator Temperature Coefficient

Determination

13.

72PY-9RX31

Reactivity Computer Checkout

In addition the inspector discussed

testing with several

Reactor

Engineers to evaluate their prepartion

and

understanding

of the testing process.

No violations of NRC requirements

or deviations

were

identified.

Main Feedwater Isolation Valve

FMIV) Ali nment.-.Unit

3

On August 6, 1990, with the unit in Mode 3, Feedwater

Isolation

Valve (FWIV) 3SG-UV-174,

was being tested per 73ST-3XI16,

"Section XI Valve Stroke Timing, Partial Stroke Exercise

and

Position Indication Verification'- Mode 1 thru 6 - FWIV's

(Economizer)."

Following the fast closure of the

FWIV, it could not be

reopened.

A normally throttled and locked hydraulic control

valve ("F") on the

FMIV was found fully closed,

which prevented

another hydraulic control valve from shifting as necessary

to

open the FMIV.

The "F" valve is normally locked 1/8 turn open,

though the locking device

does not prevent it from being

inadvertently shut.

It had last been verified throttled open

in December

1989.

However,

much work had taken place

on and

around the

FWIV since then,

and the licensee

concluded that it

19

was possible that the "F" valve was inadvertently closed while

operators

or mechanics

worked on or around the valve.

The "F" valve being closed

does

not affect the safety function

(quick close) of the

FWIY.

However, it is required to be open

to allow reopening the

FWIV.

The licensee

performed

a 50 percent verification of all Unit 3

locked valves

and confirmed that valves were being properly

controlled.

Because of the vulnerability of the,FWIV 'F" valve

to inadvertent positioning,

measures

are being considered

by

the licensee to reduce the potential of the valve being

unintentionally repositioned.

Additionally, Problem Report

System

(PRS)

number 612 was initiated for trending purposes.

No violations of NRC requirements

or deviations were

identified.

Im ro er 0-rin

Material in Anchor Darlin

AD

Four-Wa

rau )c

a ves -

n)

Following the failure of the partial stroke surveillance test

on Feedwater Isolation Valve (FWIV) SGA-UV-177 on July 5, 1990,

the licensee identified via lab analysis,

on July 23, 1990,

that several

0-rings

used in one of two installed

AD four-way

valves were of a polysulfide material which swells in the

presence

of the Fyrquel hydraulic fluid and can cause

operational

problems with the four-way valve and hence the

FWIV.

The correct material for these 0-rings is Viton.

The

0-rings in both four-way valves associated

with SGA-UV-177 had

been verified in March 1990 by the licensee to have not been

purchased

from AD under rebuild kit serial

numbers that

AD

suspected

of having improper 0-ring material.

AD had issued

a

Part 21 report in January

1990 to inform its purchasers

and

specified the Purchase

Orders

(POs) which could possibly

have

Buna-N O-rings, which are susceptible to swelling in the

presence

of hydraulic fluid.

Based

on= the Part 21 report, the

licensee identified 14 four-way valves in Unit 3 which

contained parts from rebuild kits from POs affected

by the

Part 21 notification.

These valves were replaced in. March

1990, with 10 Main Steam Isolation Valve (MSIV) four-way valves

and four FWIV four-way valves affected.

However,

SGA-UV-177

was not affected.

Later analyses

determined that the backup

0-rings in only one of these

four-way valves (for an FWIV) was

not the proper material.

The licensee's

review of the failed SGA-UV-177 four-way valve

revealed that .it was purchased

under Purchase

Order (PO)

60177315 which contained

20 MSIV 0-ring kits and four FWIV

0-ring kits.

All four FWIV four-way valve rebuild kits had

been installed in Unit 3 on FWIVs 174 and 177.

Ten MSIV

four-way valve rebuild kits had been installed in Unit 3 on

MSIVs 170,

177 and 181.

There are four "four-way valves per

20

MSIV.

Seven

MSIV kits were

used in Unit 1 on MSIVs 170 and

180'he

remaining

MSIV kit was not installed.

The licensee

determined that the swollen 0-ring caused

the

operational

problem with FWIV 177 .in Unit 3, then labeled all

other four-way valves with 0-rings procured

under the

same

PO

as suspect

and replaced

the other three suspect Unit 3 FWIV

four-way valves

on July 28 and 29th.

Because

the replacement

of, four-4'ay valves in FWIVs requires

more time per valve than

allowed per Technical Specification Limiting Condition for

Operation 3.6.3,

a Temporary Waiver of Compliance

was requested

and granted

by Region

Y on July 27,

1990.

The work was

completed in Unit 3 on

FWIVs 174 and 177 with correct 0-rings

by July 29.

On August 1, the licensee

received

a lab report which confirmed

that 0-rings from these three

FWIV four-way valves were also

the incorrect material.

The licensee

subsequently

replaced all

suspect

MSIV four-way valves in Units 1 and 3.

Subsequent

testing of the suspect

MSIV 0-rings

showed that the proper

material

had been

used.

All AD four-way valves currently

installed in all units

have

now had their 0-rings verified to

be the correct material.

The inspector

observed

the disassembly

of a spare

FWIV four-way

valve which had been

assembled

by AD.

Several

0-rings were

found to have been sliced or shaved,

and one was offset from

its proper position.

The valve also appeared to have

an

excessive

amount of grease.

The licensee tested the 0-rings

from this valve and confirmed that they were of the proper

material.

The licensee

also disassembled

and tested parts

from

three other spare

four-way valves assembled

by AD and found

other discrepancies,

including some missing wave washers

in .one

valve.

However, all the 0-rings were determined to be Viton.

Analyses of all backup 0-rings from the MSIV four-way valve

rebuild kits procured

under the suspect

PO was performed.

The

tested 0-rings were determined to be of the correct material.

The licensee is planning to issue

a 10 CFR Part 21 report on

this issue.

'NRC Generic

Communication

and Vendor Branches

have

been alerted to this issue

by Region

V management.

The inspector

concluded that licensee

actions with respect to

this issue

were pr udent

and effective in providing confidence

in the operability of AD four-way valves currently installed in

all units.

No violations of NRC requirements

or deviations were

identified.

Plant Shutdown

Forced

b

Sl:i

ed Control Element Assembl

CEA)

nit

On August 5, 1990, during the performance of CEA exercise

testing, while the unit was operating

near

100 percent

power,

CEA 68 slipped almost fully into the core to about

5 inches

withdrawn.

CEA 68 slipped the rest of the way -in while

operators

attempted to retrieve it.

Because

these

attempts

were uns'4ccessful,

the unit was shutdown to troubleshoot

and

do

repairs.

After the initial slip of CEA 68, operators

began reducing

power,

as required

by Technical Specifications

(TS) to less

than 80 percent.

After the further attempts to recover the

CEA

were unsuccessful,

a unit shutdown

was initiated to comply with

the TS.

The turbine was taken off line at 6:15

PM, and

a

reactor

shutdown

began at 6:48

PM.

All regulating

CEAs were

fully inserted

by 8:09

PM.

The inspector confirmed that TS

requirements

were met during the transient.

The licensee

had performed Control Element Drive Mechanism

.

(CEDM) traces,

in accordance

with procedure

36MT-9SF15,

"CEDMCS

CEA Coil Traces at Power Operation,"

a few hours before the

event.

The System Engineer stated that while this monitoring

can detect

many kinds of problems before they result in CEA

slip or drop events,

the monitoring method also

has

limitations.

In particular,

the

CEDMs are paralleled to the

hold bus during the monitoring, which in effect masks

problems

associated

with the Upper Gripper.

In this event,

a faulty

coil driver circuit card was identified and replaced,

which

successfully

resolved the problem.

The System Engineer also

stated that this problem is very difficult to identify.

Earlier during the

CEA exercising, part length

CEA 30 failed to

move.

In this case,

a faulty timer card was identified and

replaced while at power.

The licensee is evaluating

changes to the

CEDM Control

System

to reduce the risk of dropped or slipped

CEAs.

The unit performed minor maintenance

and testing while

shutdown,

and then started

up and achieved

Mode 1 on August 7,

1990.

100 percent

power was reached

on August 9.

No violations of NRC requirements

or deviations

were

identified.

S ent Fuel

Pool

(SFP

Activities - Units 1

2 and 3

86700)

The inspector verified by direct observation that the

SFP water

level was greater than the minimum level, that the Fuel

Building was at a negative pressure,

and that the

SFP

temperature

was within the limits of licensee

procedures.

No

discrepancies

were observed of these physical conditions.

22

No violations of NRC requirements

or deviations

were

identified.

17.

Motor 0 crated

Val ve Maintenance

and Testin

- Units I

2

and

37700,

37828 92 01

a.

S rin

Pack Relaxation in Limitor ue Actuators

Spring pack relaxation is a degradation

which has

been

observed

in certain Limitorque actuators.

This relaxation

may cause

premature actuation of the torque switch.

Under

design basis

maximum operating conditions, this deficiency

could result in a failure of the valve to fully stroke to

perform its safety function.

IN

I)

~kk

d

Certain motor operated

valves are actuated

by

Limitorque motor operators

which incorporate

a

belleville washer spring pack in conjunction with a

torque switch to limit valve stem thrust.

The torque

switch is adjusted to allow sufficient thrust to

operate

the valve under design basis conditions but

limit the thrust to preclude

excessive

wear or damage

to the valve or actuator.

The spring pack consists of an assembly of belleville

washers

which is preloaded

in compression

by the

manufacturer

and not normally adjusted in the field.

In operation,

as the actuator develops thrust, the

spring pack further compresses

after the preload is

exceeded.

The additional

compression of the spring .

pack actuates

the torque switch to interrupt the

motor control circuit to stop the actuator.

The

resultant total stem thrust is determined

by the

combination of the initial spring pack preload

and

the subsequent

spring pack compression

during

operation.

Reduction of the spring pack preload over

time would allow the torque switch to actuate at

a

lower valve stem thrust than initially established.

Under design basis

maximum differential pressure

conditions, this could cause the valve to

"torque-out" early, resulting in incomplete valve

travel.

This degradation is not readily apparent

because it

may only affect valve performance

under maximum

design basis conditions.

In less

severe conditions,

which include normal operating conditions

and routine

testing,

some

amount of spring pack relaxation

may

not prematurely stop valve travel.

In the case of

gross degradation of spring pack function (i.e.,

collapse of the washers),

operation of the valve

under

normal or test conditions

may also

be affected.

i

23

While this problem is not completely understood at

this time by the manufacturer,

the nature

and extent

of the problem is being investigated to determine

Part

21 applicability.

Several

Limitorque notices

have

been issued

on the .problem to alert the industry

to the potential for the problem and these

notices

also

recommended

replacement of the spring packs

as

, corrective action.

Indications of potential

degradation

of the spring pack assembly

due to

relaxation include:

a 0

b.

C.

d.

e.

Loose belleville washers

in the spring pack

assembly,

No apparent

spring pack preload,

Excessive

spring pack gap,

Increased

torque switch settings,

or

Underthrust identified in the as-found condition

of the valve during testing.

2)

Licensee's

Ex erience

In discussions

with cognizant licensee

engineering

representatives

regarding the problem of spring pack

relaxation in Limitorque actuators,

the inspector

found that engineering

personnel

were generally

aware

of the problem but did not consider the problem to

have occurred to any significant degree at Palo

Verde.

They indicated that the current

MOV test

procedures

and diagnostic

equipment

(MOVATS) enable

them to detect degradation

of the spring pack.

They

stated that there

had been

no instances

of a detected

loss of preload

due to spring pack relaxation in any

of the baseline testing performed pursuant to IE

Bulletin (IEB) 85-03.

The inspector

reviewed the licensee's

procedures

for

MOVATS testing

and maintenance

of motor operated

valves.

These procedures

included the following:

Procedure

No.

Title

32NT-9ZZ48,

Rev.

3

Maintenance of Limitorque Motor

Operated

Valves

32NT-9ZZ55,

Rev.

1

Valve Motor Operator

Performance

Signature Acquisition using

MOVATS equipment

The inspector found that the licensee's

procedures

included detailed inspection for a condition

identified as spring pack gap

(SPG).

A SPG was

indicative of improper adjustment of a stop collar in

the actuator which restrained

axial movement of the

spring pack assembly.

The licensee

considered that

24

the'xistence

of a

SPG

was

due to mis-assembly

of the

actuator

and readjustment

of the stop collar was the

appropriate corrective action.-

Using

MOVATS testing

to establish

the requi'red output thrust, the licensee

considered

a

SPG to be inconsequential

to the oVerall

operability of the valve.

The inspector

found that the licensee's

procedures

addressed

a loss of preload in the spring pack

as

an

expected

maintenance

condition.

As such,

the

condition did not appear to be recognized

as

a

significant abnormality which jeopardized

the

operability of the valve.

The inspector

reviewed the work control documentation

involving several

instances

in which spring pack

replacement

or adjustment

had been performed.

This

review of selected

documents

included instances

in

which additional instructions

had been requested

from

L'imitorque regarding proper preloading of the spring

pack.

The following work orders

were reviewed:

Work

Order

Date

Valve ID

Descri tion

307873

5/89

419517

6/90

2JSIAHV0685

2JRCEHV0431

312013

12/89

8

1JSIAUV0634

4/90

LPSI-CTHT Spray

PP

Cross

RCP Controlled

Bleedoff

SIT Isol. Disch.

421017

5/90

405988

4/90

378798

8/89

2JSIBHV0609

2JRCEHV0430

1JSIBUV0656

HPSI

.Pump

Long

Term Cooling

RCP Controlled

Bleedoff

S/D Cooling Cont.

Isol.

The inspector

found that in these

cases

a degradation

of the spring pack had been observed during

maintenance

or testing.

A summary of the spring pack

deficiencies is provided below.

a.

WO 307873 - the spring pack was identified to be

fatigued.

The licensee

was unable to eliminate

an as-found spring pack gap and requested

additional instructions

from Limitorque to

adjust the preload of the spring pack to

compensate

for the spring pack gap.

tq

25

C.

WO 419517 - identified possible collapsed

belleville spring washers with a large spring

pack gap which could not be 'eliminated.

Also,

the, spring pack was observed to have

no preload.

WO 312013 - the spring pack was identified as

fatigued with loose belleville washers

and

a

spring rate lower than comparable

spring packs.

d.

WO 421017 - loose belleville 'washers with one

washer

compressed flat were identified.

e.

WO 405988 - no preload

on the spring pack was

identified.

f.

WO 378798 - excessive

spring pack gap was

identified.

The

NRC inspector discussed

the repeated

occurrences

of spring pack degradation with licensee

engineering

representatives

and found that the licensee

had

considered

the conditions to be

a mis-assembly

problem which was corrected within the scope of

normal maintenance.

The inspector

was concerned that

the licensee

had not recognized

the time dependent

degradation

of the spring packs

and was treating the

condition as expected

normal wear and tear within

their maintenance

program.

As a result of the inspector's

concern,

the licensee

reviewed documentation of previous work activities

on

. MOVs specifically to identify if spring pack

relaxation

may have

been evident.

The licensee

reviewed all

EERs from 1987 through 1990 on all

systems with MOVs and identified that 14 instances

of

spring pack gaps

were reported.

In addition, the

licensee

reviewed the detailed baseline testing

records for 28 MOVs under

IEB 85-03 which had been

baseline

tested twice and found 9 instances

of

apparent

reduction in the spring rate (K-factor) of

the spring pack indicating a potential

loss of

preload

due to fatigue.

As a result of these

findings, the licensee initiated

EER 90-XE-072 to

document the review and will evaluate the findings by

October 15, 1990.

This

EER will be reviewed

when the

licensee's

evaluation is complete,

Followup Item

(528/90-28-04).

The inspector

found the current licensee

actions to

be adequate

to deal with the potential

problem of

spring pack relaxation.

Previous

work activities did

not appear to adequately

evaluate

spring pack

deficiencies to identify time-dependent

degradation.

The inspector found this weakness

appeared

to be

26

,caused

by an over-emphasis

on the baseline testing of

MOVs for future evaluations

rather than the

verification and demonstration

of the as-found

operability of the valves.

This weakness

is further

discussed

in Paragraph

b. of this section.-

b.

Documentation of Deficiencies

The>inspector's

review of the documentation of the

limitorque actuator deficiencies

found that in all six

cases

a Material Nonconformance

Report

(MNCR) had not been

written nor was

a root cause evaluation performed, related

to the spring pack deficiencies,

to establish corrective

actions to preclude

recurrence.

Rather,

an Engineering

Evaluation Request

had been written to request

Engineering

guidance

regarding the acceptability for continued

use of

the spring pack.

The inspector reviewed the working copy documentation

of

the work activity involved in each instance

and found

additional deficiencies

and nonconformances

which were not

identified in the subsequent

EER or any

MNCR.

The

inspector's

findings are summarized

below.

1)

M0307873

a.

The as-found

opening thrust value was only 78K

of the required

minimum.

b.

The as-found closing thrust value exceeded

the

maximum specified

by 76K.

c.

The as-found torque switch bypass

value of 7.6X

of valve stem travel did not meet the required

minimum limit switch setting of 20-25K.

These deficiencies directly affect the ability of the

valve to perform its safety function under design

basis conditions.

Over-thrusting in the closed

direction can increase

the force required to

subsequently

open the valve and can potentially

damage the valve and actuator.

Under-thrusting in

the open direction can prematurely stop valve travel.

Under-bypassing

of the open torque switch may cause

actuation of the open torque switch prematurely

during valve travel before the peak unseating

loads

have

been experienced.

This may cause

premature

stopping of valve travel.

The inspector noted that

none of these conditions were identified or evaluated

in an

MNCR or EER.

27

2)

W0419517

a.

A large spring

pack

gap of .035" was found with

the preload adjusting nut fully tightened.

b.

After verification by Limitorque of the proper

assembly of the spr ing pack under

EER 90-RC-57,

the as-found torque switch settings of 1.5

open/1.5 close were insufficient to allow

complete valve travel.

Adjustment of the torque

switch setting

up to the limiter plate

maximum

of 2.5/2.5

was required to achieve full valve

stroke.

These deficiencies directly affect the capability of

the valve to perform its safety function.

However,

none of these conditions were identified or evaluated

in an

NNCR or EER.

3)

W0312013

a.

The as-found

open thrust value was only 30%

of the required minimum.

b.

The as-found closing thrust value was only 86%

of the required

minimum.

c

The as-found

apparent

spring rate of the spring

pack was only 51K of similar spring packs

on

three other NOVs.

EER 90-SI-060 did evaluate

the continued

use of the spring pack, but did

not evaluate

the as-found operability or root

cause of the deficiency.

As in previously described

cases,

these deficiencies

also directly affect ability of the valve to perform

its safety function.

The valves, which were affected

by these work orders,

were

restored to an operable status.

10 CFR Part 50, Appexdix B, Criterion XVI, requires that

for significant conditions adverse to quality that

measures

shall assure that the cause of the condition is

determined,

corrective actions

are taken to preclude

repetition,

and that these

be documented

and reported to

appropriate levels of management.

The failure to document

the above noted valve deficiencies for engineering

evaluation

and determine

the root cause

appears

to be

a violation of NRC requirements,

Enforcement

Item

(528/90-28-05).

In discussions

with licensee

engineering representatives,

the inspector

found that there

appeared

to be

some

confusion

among licensee

personnel

as to under which

28

conditions

an

EER was appropriate

and which conditions

'equired

an

MNCR.

The inspector

found that the licensee

had recently revised

Procedure

60AC-OQQ01 to more clearly

establish

the separate

reporting requirements

and

appropriate

uses of both documents.

However, the

inspector

found instances

of the problem to have occurred

after the current revision.

The'inspector

found that there

appeared

to be

some

misinterpretation of the design specification

requirements

for the setpoint of limitorque actuators.

According to

the licensee's

program,

the actuator switch setpoints

are

controlled design specifications

communicated to the plant

under the Controlled Motor Operator

Data Base Description

(Design Drawing 13-J-ZZI-004).

For adjustments

outside

the specified range,

a design

change

document

was required

(DCP or S-Mod).

As such,

the specified setpoints

represent

the engineering output to assure

the design

basis operability of the valve.

However, the inspector

noted that the licensee's

handling of as-found

deficiencies in MOVs was inconsistent with the

significance associated

with the specified design

requirement.

A design

change

document

was required to

adjust the switches outside the specified target range.

However, setpoints

found to be outside the specified

target range were not identiifed as nonconforming with

respect to the design requirements.

The inspector

found

this weakness

in engineering

communication with the

operations

and maintenance

personnel

resulted in a lack of

recognition of the operational

significance of these

setpoints.

The inspector discussed

his concern with licensee

management

who acknowledged

the prior inconsistency

in

their program

and committed to initiate MNCR documentation

for deviations from design specifications

incorporated in

Design Drawing 13-J-ZZI-004.

During MOV baseline testing

in support of establishing

the appropriate setpoint

range

for incorporation into Design Drawing 13-J-ZZI-004, the

licensee

committed to initiate either

MNCR documentation

.

or equivalent programmatic controls to assure that

as-found deviations

from the setpoints specified in the

controlling engineering

documents

were evaluated to

address

as-found design basis operability.

Follow-up of Unresolved Item 528/90-12-02:

AFW Isolation

Valve Setpoints

The inspector

reviewed

a previous observation of an

apparent conflict in -license

commitments regarding

Limitorque actuator setpoints for the

AFW isolation valves

(AF-034 through 037).

The inspector

had reviewed

EER

87-AF-42 which identified a failure to fully close

under

maximum differential pressure

for

AFW valve 3JAFBUV0034 on

I 4

29

May 22,

1987.

The actuator

was determined to be

undersized for the application,

however the condition was

determined to be acceptable

based

on a two-phase

Justification for Continued Operation

(JCO) of Units

1 and

2.

Phase

1 of the

JCO identified that the

AFW isolation

valves would continue to be adjusted to seat

based

on a

torque switch setting in excess

of maximum actuator

rating. It further identified that the valve was not

expected

to be able to close under

maximum differential

pressure

conditions, but that operator actions

could be

credited to prevent overfilling the steam generator.

Phase

2 of the

JCO identified that the actuators

of the

valves would be modified to seat

based

on the limit switch

setting, with the torque switch adjusted

the same as. Phase

l.

As in Phase

1, the

JCO identified that despite

the

modification, the valve was not expected

t'o be able to

fully close under

maximum differential pressure.

The inspector discussed

the interim operability and limit

seating modification with various licensee operations

personnel

and found that operations

personnel

were vaguely

aware of the modification activity, but did not consider

it to have any operational

significance.

Operations

management

had been

involved in the review of the

JCO and-

operations

personnel

considered that existing procedures

covered the potential for overfilling the steam generators

and therefore specific notification to operations

personnel

of the potential for the

AFW valves not to go

fully closed under

some conditions

was not considered

necessary.

Under current conditions, this situation would

be described, in an

MNCR and would be reviewed

by operations

personnel.

The inspector reviewed the licensee's

final report for IEB 85-03, dated January

15, 1988, which reported satisfactory

test results for the

AFW isolation valves.

After a review

of the

MOY design basis operating conditions, the licensee

identified maximum design conditions for both the opening

and closing function of the valves.

Note

9 of Appendix

B

of the licensee's

submittal stated:

"The closing forces for. torque seating of the

auxiliary feedwater isolation valves (1, 2,

3

JAFUV0034, 35, 36, 37) as determined

by test

on

1JAFCUV0036 and

3JAFBUV0035 have

been

reduced

by

position stopping rather than torque seating ensuring

these valves

open (which is the safety function)

during worst case accident conditions".

The inspector

noted that limit switch seating

was

reflected in the controlled setpoint

document

(13-J-ZZI-004) in Note 12.

Thi s itern is cons idered cl os ed.

f

30

18.

Review of Licensee

Event

Re orts - Units 1

2 and

3 (92700)

The following LERs were reviewed by the Resident Inspectors.

, It was noted that four 'LERs (529/90-02,

529/90-06,

529/90-08,

and 530/89-, ll) involved missed surveillance tests.

These

missed tests

have occurred since

December

1989.

While it

appears

that the corrective actions

are appropriate for each

incident< the underlying reason

for the missed test should

be

reviewed and, if any trends identified, corrective actions

should

be taken.

Unit 1:

a.

528/90-07-LO

Closed

"Safet

In 'ection Tanks Vent Val ves

rove

e

ower

ontrar

to

ec naca

ecs

>cation

e uirements

, This licensee

event

was discussed

in Inspection

Report

528/90-23,

Paragraphs"'.c.

and 13.

No new information was

provided by this Licensee

Event Report.

This

LER is

closed.

b.

528/90-08-LO

Closed)

"Main Steam Isolation

Due to

roce ura

na

e uac

This licensee

event

was discussed

in Inspection

Report

528/90-23,'Paragraph

12.

The inspector

reviewed Incident

Investigation Report (IIR) 2-1-90-002 which addressed

this

event which occurred

when operators

placed the

SBCS in

automatic with a demand signal present.

The IIR addressed

operator inappropriate action,

inadequate self checking

and corrective action associated

with the individual

operators

involved.

The

LER states

on page

4 of 5,

paragraph I.I., "The event was not the result of a

cognitive personnel error..."

This was not consistent

with the IIR.

However, the

LER indicated corrective

actions included briefing all operators

on the need to

match controller output with demand prior to placing the

controller in automatic.

The inspector noted that

operator training emphasizes

this point.

The inspector

concluded that the licensee's

IIR investigation

and

corrective actions

appeared

to properly characterize

and

treat the extent to which personnel

performance

contributed to this event.

Thus, the inspector

concluded

from the above that licensee

management

was willing to

recognize

and address

operator

performance

issues.

The

inspector

urged licensee

management

to clearly

characterize all casual

factors in LERs to the

NRC.

Licensee

management

acknowledged

these

comments.

This

LER

is closed.

t

g ~

t'

7

31

Unit

a ~

2:

529/90-02-LO (Closed

"Missed Surveillance Test

or

uxor )ar

ee water

stem

Sur veillance Requirements

(SR) 4.7.1.2.a.2

and 4.7.1.2.a.3

were inadvertently not performed during the required

interval for the Train "A" auxiliary feedwater =pump,

AFA-P01.

Personnel

incorrectly documented that

SR 4.7.1.2.a

had been completed

on January

16, 1990,

when in

fact, it had only been partially accomplished.

The error

was not discovered. until after the successful

performance

of the test

on February 7, 1990.

The missed

SRs

had last

been accomplished

on December

20, 1989.

The, licensee

determined that cognitive personnel

errors

caused the-

event.

Appropriate corrective actions

appear to have been

taken.

The failure to perform surveillance tests in the required

interval is a violation of NRC requirements.

This

licensee identified violation is not being cited because

the criteria specified in Section

V.G. of the Enforcement

Policy were satisfied.

This

LER is closed.

b.

529/90-06-LO (Closed

"Missed Surveillance Test For

eutron

ux

arms

Surveillance

Requirement

(SR) 4. 1.2.7.b for the startup

channel

high neutron flux alarms

Boron Dilution Alarm

System

(BDAS) was not performed within the required

interval.

It had been performed

on May 9, 1990,

and was

due by June 17, 1990.

The error was identified by the

licensee

on June 18,

1990.

Cognitive personnel

errors

caused

the event,

as the group responsible for performing

the

SR did not do the test despite

reminders

from the

Surveillance

Program Coordinator.

The failure of

operations

personnel

to cancel

a troubleshooting

work

order on the

BDAS also complicated the issue,

as the ILC

personnel

who were to perform the

SR apparently thought

that the

BDAS was inoperable

because

of the outstanding

work order.

However, the appropriate

communications

did

not occur which would have clarified the operability of

the

BDAS and averted the missed

SR.

Also, the personnel

involved (Surveillance Test Coordinator

and ILC) were not

attentive or responsive

enough to prevent the

SR from

being missed,

or to identify the error until about

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> later.

This is

a violation of NRC requirements.

However, this

licensee identified violation is not being cited because

the criteria of Section

V.G. of the Enforcement Policy

were satisfied.

32

529/90-07-LO (Closed

"Inadvertent Control

Room

ents

at>on

so ation

n ineere

a et

eatures

c ua

son

This

LER describes

a June

25, 1990, Control

Room

Ventilation Isolation Actuation Signal

(CRYIAS) received

when .a Control

Room Operator lightly tapped the

CRYIAS

Test/Bypass

pushbutton during preplanned

maintenance

to

determine if an unlit indicator lamp was loose.

The

license could not recreate

the actuation

by similar

tapping during troubleshooting

and

no hardware

deficiencies

were identified.

The licensee

concluded that

the cause

was indeterminate.

This

LER is closed.

529/90-08-LO

Closed

"RCS Boron

Sam le Late Resultin

sn

ssse

ction

Backup samples of the Reactor Coolant System

(RCS) are

required whenever

one startup

channel

high neutron flux

alarm Boron Dilution Alarm System

(BDAS) is inoperable.

On July 4, 1990, with the Unit in Mode 3, and one

BDAS

channel

inoperable for surveillance testing,

a second

charging

pump was started.

The required sampling

frequency

changed

from once per six hours to once per two

and one-half hours

as

a result of the operation of the

charging

pump.

However, the reactor operator forgot about

this requirement at the time and did not recognize it

until the next

RCS boron sample results

were received,

28 minutes later than required.

The licensee

performed

an

investigation

and documented this in Incident

Investigation Report (IIR) 3-2-90-026.

The IIR closely

matches

the

LER, except that the IIR documents

an

additional corrective action,

e. g., to add

a step to

procedure

42ST-2ZZ24, "Startup Channel

High Neutron Flux

Alarm Inoperable

3. 1.2.7," to require caution tags

be hung

on the charging

pump if a startup

channel

or BOAS alarm is

inoperable.

The licensee's

actions

appear to be

consistent with the identified root causes.

The Technical

Specification requirement for RCS sampling was not met.

However, the licensee identified violation is not being

cited because

the criteria specified in Section V.G. of

the Enforcement Policy were satisfied.

0

V

33

Unit 3:

a.

530/89-11-LO/Ll

0 en

"Missed

ASME Surveillance Test

on

enerator

ir tart

s

em

ec

a ve

This event involved a missed

ASME Surveillance. Test

(ST)

'n the "A" Train air start system

check valve for the "B"

diesel

generator.

The inspector requested

additional

information from the licensee to enable

a more complete

evaluation of this event.

This

LER remains

open.

18.

Review of Periodic

and

S ecial

Re orts - Units 1

2 and

3

Periodic

and special

reports

submitted

by the licensee

pursuant

to Technical Specifications (TS) 6.9. 1 and 6.9.2 were reviewed

by the inspector.

This review included the following considerations:

the report

contained the information required to be reported

by NRC

requirements;

test results

and/or

supporting information were

consistent with design predictions

and performance

specifications;

and the validity of the reported information.

Within the scope of the above,

the following reports

were

reviewed by the inspector.

Unit 1

o

Monthly Operating

Report for July 1990.

Unit 2

o

Monthly Operating

Report for July 1990.

Unit 3

, o

Monthly Operating

Report for July 1990.

No violations of NRC requirements

or deviations

were

identified.

19.

Exit Meetin

(30703

The inspector

met with licensee

management

representatives

periodically during the inspection

and held an exit meeting

on

August 30, 1990.