ML17300A965

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Insp Repts 50-528/87-17,50-529/87-18 & 50-530/87-19 on 870510-0620.Violations & Deviations Noted.Major Areas Inspected:Review of Plant Activities,Esf Sys Walkdown, Surveillance Testing & Temporary Instructions
ML17300A965
Person / Time
Site: Palo Verde  
Issue date: 07/24/1987
From: Ball J, Fiorelli G, Ivey K, Richards R, Zimmerman R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17300A961 List:
References
50-528-87-17, 50-529-87-18, 50-530-87-19, NUDOCS 8708100487
Download: ML17300A965 (39)


See also: IR 05000528/1987017

Text

'0

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION V

Report Nos:

Docket Nos:

License

Nos:

Licensee:

50-528/87"17,

50"529/87"18, 50-530/87-19

50"528, 50-529,

50"530

NPF-41,

NPF-51,

NPF"65

Arizona Nuclear Power Project

P. 0.

Box 52034

Phoenix,

AZ. 85072-2034

Ins ection Conducted:

May

0,

987 -

une 20,

1987

Inspectors:

si ent Inspector

C.

Approved By:

G. Fiorelli, Resident

Inspector

Ivey, Resident

nsp

or

R. Z'rman, Senior Resident Inspector

S.

Richards,

Chief, Engineering Section

at

ig ed

z

g7

D te

igned

7

Date

S gned

Date Signed

Summary:

Ins ection

on

Ma

10

1987 - June

20

1987

Re ort Nos. 50-528/87-17

50-529/87-18

and 50-530/87-19.

Areas Ins ected:

Routine,

on site, regular and backshift inspection

by

the four resident

inspectors.

Areas inspected

included:

followup of

previously identified items;

review of plant activities; plant tours;

engineered

safety feature

system walkdowns; surveillance testing; plant

maintenance;

licensee

event report followup; temporary instructions;

refueling water tank gravity flow into containment;

refueling water tank

gravity flow into the auxiliary building; auxiliary operator/radiation

technician

communication problem;

system train outages;

steam generator

blowdown sample valve operating experience;

periodic and special

reports

review.

During this inspection the following Inspection

Procedures

were covered:

I

25573,

25587,

30703,

61302,

62700,

61726,

62703,

70441,

71707,

71709,

71710,

71881,

90712,

90713,

92700,

92701,

92702,

92703,

93701,

93702.

8708100487

876724~

PDR

ADQCK 05000528

8

PDR

Results:

Of the thirteen areas

inspected,

one violation (paragraph

7)

and one deviation (paragraph

10) were identified.

DETAILS

1.

Persons

Contacted:

The below listed technical

and supervisory

personnel

were

among

those contacted:

Arizona Nuclear

Power Pro ect

ANPP

~R.

Adney

  • J. Allen

L. Brown

R. Buckhalter

J.

R.

Bynum

J.

Dennis

  • D. Gouge

"J.

G.

Haynes

~M.

E.

Ide

  • R. Nelson

"G. Perkins

"J. Pollard

F. Riedel

"T. Shriver

L. Souza,

"E.

E.

Van Brunt,

"R. Younger

"0. Zeringue

Operations

Superintendent,

Unit 2

Operations

Manager

Radiation Protection

and Chemistry Manager

Outage

Management

Superintendent,

Unit 3

PVNGS Plant Manager

Operations

Supervisor,

Unit 1

Operations

Superintendent,

Unit 3

Vice President,

Nuclear Production

Corporate guality Assurance

Manager

Maintenance

Manager

Radiological Services

Manager

Operations

Supervisor,

Unit 2

Operations

Supervisor,

Unit 3

Compliance

Manager

Assistant guality Assurance

Manager

Jr.

Executive Vice President

Operations

Superintendent,

Unit 1

Technical

Support Manager

The inspectors

also talked with other licensee

and contractor

personnel

during the course of the inspection.

"Attended the Exit Meeting on June 18,

1987.

2.

Previousl

Identified Items

Unit 1

a.

Closed

Followu

Item

528/84-15-02

"All Units -

U date

Documentation

To Reflect Desi

n Chan

e In Number of RV Holddown

Bolts."

This item concerned

the completion of design

changes

committed

to by Combustion Engineering

(CE) in CE letter V-CE-10727 of

July 1, 1980.

Completion of the changes

was verified in

inspection report No. 50-528/86-04.

However, this item

remained

open pending

a review of CE's timeliness

in completing

the changes.

The licensee

and

CE have exchanged

correspondence

on this item

and the inspector

concluded that the changes

were completed

as

requited.

This item is closed.

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The following items were previously left open pending

NRR

review and acceptance

of the licensee's

submittals

on the

associated

subjects.

The inspector discussed

these

items with

the

NRR Project Manager

and cognizant

NRR fire protection

personnel

to verify the acceptance.

From the discussions

and

reviews of the Palo Verde Safety Evaluation Report

(SER), the

inspector determined that each item had been reviewed

and the

acceptance

was either documented

or implied by references

in

various supplements

to the

SER.

Therefore,

these

followup

items are closed:

(1)

528/84-62-01:

"Auxiliary Building Firewater

Modification."

(2)

528/84"62-03:

(3)

528/84-62"04:

"NRR To Document Preaction

System

As

Acceptable."

"APS To Resolve With NRR About The Spray

Chemical

Accumulator Room."

(4)

528/84"62-05:

(5)

528/85-06-01:

"APS To Resolve Actuation Method of

Preaction Sprinklers With NRR."

"Spurious Actuation Analysis For Fire In

Containment"

(6)

528/85"06-04:

"Evaluation of Fire Detectors

Extended

From

Ceiling Bays To Be Submitted

To

NRR For

Review."

(7)

528/85-06-06:

"Commitment To Achieve Cold Shutdown Within

72 Hours To Be Submitted to NRR."

C.

Closed

Followu

Item

528/84-62-06

"APS Trainin

Needs

~Udatin ."

FSAR Section 13.2. 1.5 contains

commitments to provide certain

fire protection training for station personnel

and security

personnel.

The training program at the time of the previous

inspection

needed to be updated to reflect the plant situation

after fuel loading and cover the handling of offsite fire

department personnel.

The inspector

reviewed the training program and lesson plans

for general

employee training (GET) and security training on

vehicle access

controls for the protected

area.

The inspector

verified that the following topics are covered in the training

program:

0

'o.

0

0

0

Fire Alarm Sounds

Evacuation

Plan and Postings

Fire Reporting

Ignition Source. Control

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Security Verification of Emergency Vehicles

o,

Escorting Firemen

The inspector concluded that the training program had been

updated to reflect the plant situation after fuel load and to

cover the handling of offsite fire department

personnel.

This

item is closed.

Closed

Followu

Item

528/85-20-01:

"Inservice Testin

of

Pum

s and Valves - Procedural

Meaknesses.

This item relates to weaknesses

identified in some procedures

used to perform required

ASME Section

XI periodic inservice

pump and valve tests.

During this inspection,

the inspector

reviewed changes

to the procedures

that, were previously

reviewed to determine if comments

regarding these

procedures

had been incorporated into the current revisions.

The

inspector

found that the licensee

had incorporated

the comments

which had previously been

made.

At the conclusion of this

inspection,

the licensee

was,

however, evaluating the need for

additional

improvements in the surveillance test procedures

in

light of problems

experienced

during recent test performances.

The licensee stated that the contemplated

changes will not

effect the technical

content of the procedures.

Additional

changes

to the licensee's

program and procedures will be

reviewed

as

a part of future routine inspection efforts.

This

item is closed.

Closed

Followu

Item

528/85-20-02

"Inservice Testin

.Pum

Test Records.

'his

item relates

to the

need for the licensee

to develop,

formalize and finalize summaries

of inservice testing of pumps

in order to permit proper engineering evaluation

and trending.

Meaknesses

in documentation clearly detailing reference

values

and the date/source

of their development

were also noted.

During this inspection,

the inspector

reviewed the status of

the licensee's

efforts with regard to compiling the needed

data.

The licensee

has developed

or is in the process

of

developing

an "Inservice Test Plan and

Pump Record" for each

pump included in the licensee's

Section XI program.

The

inspector reviewed draft copies of a number of these test plans

and records

and found them to contain information which was

previously considered

lacking.

The licensee's

efforts to date

were found to be satisfactory although additional effort needs

still to be expended in this area.

Review of the licensee's

continuing efforts in this area will be conducted in the future

as

a part of the routine inspection

program.

This item is

closed.

Closed

Fol'lowu

Item

528/85-20-03

"Inservice Testin

Valve Test Records."

This item relates

to some weaknesses

noted in Section

XI valve

inservice testing records.

The need for developing detailed

summaries of valve testing

was identified as

a particular

weakness.

Tracking of main stream

and pressurizer relief

valves

by serial

number was also found to be a needed

program

improvement.

During this inspection,

the inspector

reviewed

the status of the licensee's

efforts in these

areas.

The

licensee

has developed or is in the process

of developing

an

"Inservice Test Plan

and Valve Record" for all valves included

in the licensee's

test program.

Changes to the licensee's

program were also,

found to have been

made which require

tracking of relief valves

by serial

number

as well as system

designation.

Review of the licensee

s continuing efforts in

developing detailed

summaries of valve testing will be

conducted in the future as

a part of the routine inspection

program.

This item is closed.

Closed

Followu

Item

528/85-31-07

"Licensee

To Determine

Size of Fuses."

Temporary Modification (TM) 1-85-SA-134 installed

a temporary

cooling fan in an electronic cabinet

and provided fuse

protection between the fan and a cabinet power supply.

The

documentation

was confusing in that one section of the

paperwork indicated the fuse size to be 1/2

amp while another

section indicated

1 amp fuses

were to be used.

The licensee

was still reviewing this apparent

discrepancy at the conclusion

of the previous inspection.

The licensee's

review determined that the fuse size

was to be

1/2

amp initially but was changed

by the system engineer to

1 amp before the

TM was approved or installed.

The

TM was

installed using 1 amp fuses

and associated

documentation

reflected the correct fuse size.

This item is closed.

Closed

Fol 1 owu

Item

528/85-31-10:

"Inser vice Testin

of

Pum

s and Valves - Relief

Re uests."

This item related to the need for the licensee to seek

NRC

approval of certain relief requests

from ASME Section XI

inservice

pump and valve testing requirements.

On May 28,

1987, the licensee

met with the

NRC staff and its consultants

to discuss

the status of the licensee's relief requests

and to

answer questions

regarding these requests.

During this

meeting, substantial

agreement

was reached

on most points of

the licensee's

proposed

program implementation.

The licensee

has committed to respond formally to the staff's request for

additional information by September

1, 1987.

Although the

staff's review is ongoing,

based

on the efforts of the licensee

to date, this item is closed.

Unit 2

Closed

Ins ector Fol 1 owu

Item

529/85-20-01:

"Check

Licensee's

Verification Sam le For Bulletin and Circulars."

Based

on inspector findings related to the licensee's

"incomplete followup actions associated

IE Circular 80-14, the

licensee's

gA staff selected

a sample of 14 completed

IE

Bulletins. and Circulars to determine whether a programmatic

problem exists.

The inspector

observed that the audit reports

dealing with the circulars

and bulletins indicated

no further

followup actions

were necessary.

The licensee

concluded

a

programmatic

problem did not exist.

This item is closed.

b.

Closed

Ins ector Followu

Item

529/86-32-02

"Cooldown

Problem with Two Char in

Pum

s In Meetin

Technical

S eci-

fications."

C.

A Technical Specification

change

request

was submitted to the

NRC on May 6, 1987,

by the licensee.

This change would permit

the licensee to achieve

a cold shutdown condition in 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />

without the need for reaching

a hot standby condition in six

hours

when entering into a 3.0.3 action statement.

The

existing Technical Specification cooldown requirement is

extremely difficult to achieve with only two operable

charging

pumps.

This item is closed.

C'losed

Ins ector Followu

Item

529/86-33-02

"Cable Tra

Su

ort Desi

n Criteria Evaluation."

This item pertains to discrepancies

which were found to exist

between the maximum span criteria as stated in the design

criteria for cable tray supports

and the actual

layout of

installed cable trays.

As a result of the noted discrepancies,

the licensee

committed to review the basis for the

maximum span

criteria and to evaluate

on a sampling basis

the acceptability

of deviation from the stated criteria.

During this inspection,

the inspector

reviewed the licensee's

evaluation.

In all cases

the deviations

from the criteria were found to be acceptable

with all tray spans

and associated

hangers

found to be within

the allowable design stress criteria

The licensee

determined

that the maximum span criteria had been

added to the design

criteria manual

subsequent

to the completion of plant design

work and as

such

need not have

been included.

The licensee

has

removed the specific reference to a maximum allowable distance

between tray supports

since this criteria was not included in

the original plant design.

This item is closed.

Closed

Ins ector Followu

Item

529/86-33-11):

"Trouble-

shootin

Procedure Criteria."

The licensee

was requested

to review work control procedures

so

as to enhance

the quality of work instruction associated

with

troubleshooting activities.

Procedure

30AC-9ZZ01, "Work

Control" was revised to include additional

guidance

and

direction to assist in the development of work procedures

involving troubleshooting activities.

This item is closed.

e.

Closed

Ins ector Followu

Item

529/87-01-01:

"Licensee

Followu

of Emer enc

Li htin

S stem."

This matter deals with a licensee

commitment to conduct

an

evaluation of emergency lighting systems to confirm that proper

system testing

was completed to meet regulatory commitments.

The inspector confirmed that the licensee

had conducted

an

independent, evaluation of the emergency lighting systems

and

has

documented

the findings in an internal report.

The report

concluded the emergency lighting system

has

been successfully

tested to demonstrate

conformance with regulatory commitments.

The report also lists recommendations

for possible

program

improvements

and has

been forwarded to ANPP management for

review.

The report has also

been reviewed by operations

engineering for comments

and followup actions.

This item is

closed.

f.

Closed

Ins ector Followu

Item

529/87-11-02

"Pressurizer

Level Erratic 0 erations."

This matter was discussed

by the licensee with Region

Y

management

during their meeting

on May ll, 1987.

The

discussions

did not result in the need for fur ther licensee

or

regulatory actions.

This item is closed.

Unit 3

Closed

Unresolved

Item

530/86-03-20

"Masonr

Block Wall

Adecduacy."

During this inspection,

the inspector verified the completion of

modifications to the masonry block wall located at elevation

74 feet

in Unit 3 as committed to by the licensee

by letter

dated

October 31,

1986,

and as accepted

by the

NRC by letter dated

December

19,

1986.

The inspector

reviewed the work documentation

associated

with the modifications

and visually inspected

the wall

modifications for conformance to design.

No discrepancies

were

noted.

This item is closed.

3.

Review of Plant Activities

a 0

Unit 1

The unit operated at full power until May 22,

when power was

reduced to 80K for core protection calculator

(CPC)

computer

software changes.

Power was increased

to 100K on May 25.

On

May 30 a reactor

power- cutback

(RPCB) occurred

when the "A"

train main feedwater

pump turbine

(FWPT) tripped during weekly

overspeed

testing.

The

FWPT tripped when

a failed limit switch

prevented

the lockout of the test trip signal.

The reactor

e

~ ten

7'hen

tripped on variable overpower

(VOPT), as anticipated,

due

to the power increase that results

from the negative

moderator.

temperature coefficient (MTC) following a

RPCB actuation.

Near

the end of core life, the rate of power increase is greater

than the rate at which the

VOPT trip setpoint

can increase,

resulting in a reactor trip.

The licensee

has submitted

a

Technical Specification

change to prevent unnecessary

reactor

trips during

RPCB events.

The unit returned to power on May 31 and operated at full power

for the remainder of the reporting period.

n.

Unit 3

On May 10, Unit 2 experienced

a turbine generator trip as

a

result of a loss of power to the generator protection circuitry

cabinet during the testing of the power system stabilization

circuit.

Unrelated to the turbine generator trip, the unit was

required to shutdown

by Technical Specification 3.8.3. 1 due to

the failure of the channel

"C" 120V AC vital inverter the

previous

day.

The inability to return the inverter to service

within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> required the unit to be shutdown to Mode 5.

The inverter was found to have several silicon controlled

rectifier units which were not positioned properly, causing the

inverter fuse to blow.

This condition was corrected

and the

unit returned to 100K power on May 17.

The plant operated at 10(C until June 4,

when the reactor

tripped as

a result of low steam generator level.

The low

steam generator

level was caused

by a malfunction in the

automatic feedwater control system during system

troubleshooting/testing.

A subsequent

overcooling of'he

reactor coolant system

(RCS) resulted in low pressurizer

pressure

causing

a safety injection and containment isolation

actuation.

During the recovery to power on June

7 a turbine trip occurred

as

a result of an

EHC leak.

This condition was corrected

and

the unit returned to 100K power on June

8.

The plant has

operated at 100K power throughout the remainder of the report

period.

C.

Unit 3

The plant remained in Mode 5 throughout the reporting period.

Initial fill and venting of the reactor coolant system

was

completed during this period.

Retesting of the Train "B"

Diesel Generator which was

damaged

during preoperational

testing in December,

1986 was also started during this period.

On June 5, 1987 the "B" Diesel Generator failed to start during

its second post maintenance

run.

Licensee investigation

identified a through wall crack in both the

8R cylinder head

and piston liner.

Cause of the

damage is still under review by

the licensee.

The damaged piston liner and cylinder head were

replaced

by licensee

and

a successful

22 hour2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br /> run at 100K rated

load followed by a 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> run at llOX load were completed

on

June ll, 1987.

On June 12, 1987, during the first of a planned

35 consecutive start attempts,

the diesel

generator tripped on

high main bearing temperature.

The No.

2 main bearing

was

removed from the engine for the purpose of conducting further

examinations

and replaced with a new bearing.

The licensee

again ran the engine

on June 18, 1987.

The engine ran

successfully

unloaded for 15 minutes;

however,

the engine

tripped again

on high bearing temperature

on the

No.

2 main

bearing.

The licensee is continuing to review the cause for

the No.

2 main bearing problem.

Initial criticality is currently scheduled

to occur in August,

1987.

Plant Tours

The following plant areas

at Units 1,

2 and

3 were toured by

the inspector during the course of the. inspection:

0

0

0

0

0

0

0

0

Auxiliary Building

Containment Building

Control Complex Building

Oiesel Generator Building

Radwaste

Building

Technical

Support Center

Turbi ne Bui 1 di ng

Yard Area and Perimeter

The following areas

were observed

during the tours:

1.

0 eratin

Lo s and Records

Records

were reviewed against

Technical Specification

and administrative control pro-

cedure

requirements.

2.

Monitorin

Instrumentation

Process

instruments

were

observed for correlation

between

channels

and for con-

formance with Technical Specification requirements.

observed for conformance with 10 CFR 50.54.(k), Technical

Specifications,

and administrative procedures.

4.

E ui ment Lineu

s

Valve and electrical

breakers

were

verified to be in the position or condition required

by

Technical Specifications

and Administrative procedures

for

the applicable plant mode.

This verification included

routine control board indication reviews

and conduct of

partial

system lineups.

5.

E ui ment Ta

in

Selected

equipment, for which tagging

requests

had been initiated,

was observed to verify that

6.

7.

tags were in place

and the equipment in the condition

speci fied.

General

Plant E'i ment Conditions

Plant equipment

was

observed for indications of system leakage,

improper

lubrication, or other conditions that would prevent the

system from f'ulfillingtheir functional requirements.

Fire Protection

Fire fighting equipment

and controls were

observed for conformance with Technical Specifications

and

administrative procedures.

8.

9.

for conformance with Technical Specifications

and admin-

istrative control procedures.

~Secorit

Activities observed for conformance with

regulatory requirements,

implementation of the site

security plan,

and administrative

procedures

included

vehicle and personnel

access,

and protected

and vital area

integrity.

10.

Plant Housekee

in

Plant conditions

and material/

equipment storage

were observed to determine the general

state of cleanliness

and housekeeping.

Housekeeping

in

the radiologically controlled area

was evaluated with

respect to controlling the spread of surface

and airborne

contamination.

The inspector

noted during tours of Unit 2, the existence

of excessive

amounts of boric acid crystals

on insulation,

piping, and valves in the Train "B" HPSI

pump room,

as

a

result of valve packing leaks.

Also noted

was the

requirement that anti-contamination clothing be worn for

entry into the mechanical

wrap-around

rooms.

This

condition also exists at Unit 1.

Licensee

management

was

informed that it. would be prudent to cleanup the areas to

prevent increased potential for the spread of

contamination,

as well as eliminate the impediment to free

access

to the mechanical

wrap-around

rooms

so as to

facilitate the checking of the equipment conditions in the

rooms.

Radiation Protection Controls

Areas observed

included

control point operation,

records of licensee

surveys

within the radiological controlled areas,

posting of

radiation

and high radiation areas,

compliance with

Radiation

Exposure Permits,

personnel

monitoring devices

being properly worn, and personnel

frisking practices.

No violations of NRC requirements

or deviations

were identified.

4.

En ineered Safet

Feature

S stem Walk Down - Units 1

2

and 3.

Selected

engineered

safety feature

systems

(and systems

important to

safety) were walked down by the inspector to confirm that the

systems

were aligned in accordance

with plant procedures.

During

the walkdown of the systems,

items

such

as hangers,

supports,

electrical cabinets,

and cables

were inspected to determine that

they were operable,

and in a condition to perform their required

f'unctions.

The inspector also verified that the system valves were

in the required position and locked as appropriate.

The local and

remote position indication and controls were also confirmed to be in

the required position and operable.

Unit 1

Accessible portions of the following systems

were walked

down on the

indicated date.

~Setem

Containment

Spray System,

Trains "A" and "B"

Date

May 14

High Pressure

Safety Injection,

~ Trains "A" and B"

May l4

125V

DC Electrical Distribution,

Channels

"A" and "B"

May 19

Chemical

Spray System,

Channels

"A" and "8"

May 19

Essential

Cooling Water System,

Trains "A" and "B"

May 19

Essential

Chilled Water System,

Trains "A" and "B"

June

4

Diesel Generator

System,

Trains "A" and "B"

June

13

Essential

Spray Ponds,

Trains "A" and "B"

June

13

Auxiliary Feedwater

System,

Trains "A" and "B"

June

19

Unit 2

Accessible portions of the following systems

were walked down on the

indicated dates.

~Setem

Shutdown Cooling, Train "A"

Essential

Spray Ponds,

Trains "A" and "B"

Date

May 14

May 18,

June 12-13

Auxiliary Feedwater

System,

Train "A"

May 28

Diesel Generator

System,

Trains "A" and "B"

June

13

Auxiliary Feedwater

System,

Train "A"

June

18

Unit 3

Accessible portions of the following systems

were walked down on the

indicated dates.

Boron Injection Flow Paths

125V DC Electrical Distribution,

Channels

"A" and "C"

May 20

May 27

Diesel Generator

System,

Train "A"

Low Pressure

Safety Injection Aligned

for Shutdown Cooling, Train "A"

June

3

June

10

No violations of NRC requirements

or deviations

were identified.

5.

Surveillance Testin

- Units 1

2

and 3.

ae

Surveillance tests

required to be performed by the Technical

Specifications

(TS) were reviewed

on a sampling basis to verify

that

1) the surveillance tests

were correctly included

on the

facility schedule;

2) a technically adequate

procedure

existed

for performance of the surveillance tests;

3) the surveillance

tests

had been performed at the frequency specified in the TS;

and 4) test results satisfied

acceptance criteria or were

properly dispositioned.

b.

Portions of the following surveillances

were observed

by the

inspector

on the dates

shown:

Unit 1

Procedure

41ST-IOG01.

Oescri tion

Dates

Performed

Diesel Generator

"A" Test -

May 14

4.8.1.1. 2.a.

36ST" 1SE06

41ST" 1ZZ33

41ST" 1ZZ23

Unit 2

Log Power Functional Test.

Mode 1 Surveillance

Logs.

CEA Position Data Log.

May 21

June 18-19

June

19

Procedure

36ST"2SE03

Descri tion

Excore Safety Linear

Channel Quarterly

Calibration.

Dates

Performed

May 13

73ST-9CL06

36ST"9SB02

Containment Ventilation

Purge Isolation Valves.

PPS Bistable Trip

Functional Test.

May 18

May 28

Unit 3

36ST-9SB41

PPS Transmitter Time

Response

Test

32ST-9PK03

18 Month Surveillance

of Station Batteries-

Channel

"B"

Dates

Performed

May 13

June

17

No violations of NRC requirements

or deviations

were identified.

6.

Plant Maintenance

Unit 1

2

and 3.

a4

During the inspection period, the inspector

observed

and re-

viewed documentation

associated

with maintenance

and problem

investigation activities to verify compliance with regulatory

requirements,

compliance with administrative

and maintenance

procedures,

required

QA/QC involvement, proper

use of safety

tags,

proper equipment alignment

and use of jumpers,

personnel

qualifications,

and proper retesting.

The inspector verified

reportability for these activities was correct.

b.

The inspector witnessed portions of the following maintenance

activities:

Unit 1.

Descri tion

Dates

Performed

o

Rework Fuel

Rack Lever Linkage

on Diesel Generator "A".

May 12

13

o

Monthly PH Inspection of Battery

Charger "B".

o

Remove/Replace

AFN-P01 Due To Test

Failure.

May 19

June

3

o

Troubleshoot/Replace

K-111 Relay-

CSAS Valve Activation Logic.

o

PM - Inspect/Adjust

Reactor Trip

Breaker "D".

June

4

June

12

o

Remegger

Reactor Trip Breaker "D".

June

12

Unit 2

Descri tion

o

"C" Channel

Inverter Transfer

Switch Troubleshooting.

Dates

Performed

May 14

o

PM of Loose Parts

and Vibration

May 21

Instrumentation.

o

Replace

"0" Rings

on Multi Stud

Hay 28

Tensioner Hydraulic Unit.

Unit 3

Dates

Performed

o

Reactor Coolant

Pump Journal

Bearing

and Seal

Replacement.

May 14 and 29

o

Maintenance of Medium Voltage

Switchgear - Train "B" High

Pressure

Safety Injection Pump

Breaker 3EPBB-S04E.

May 18

o

Motor Operated

Valve Testing of

Hay 27

Auxiliary Feedwater

Isolation

Valve - 3AFA HV-0034.

o

Troubleshoot

Diesel Generator

"B" To Find Jacket Mater Leak.

June

5

No violations of NRC requirements

or deviations

were identified.

7.

Refuelin

Mater Tank Gravit

Flow Into Containment - Units 1 and 2.

On May 19, 1987, in Unit 2, during the performance of ASME

Section

XI valve stroke timing per procedure

73ST-2ZZ10,

approximately

270 gallons of water drained

from the refueling water

tank

(RMT) to the containment building through the containment

spray

14

(CS) headers

located below the

140 foot elevation.

This occurred

during testing of the

CS header discharge

valves

(SIA-UV672 and

SIB-UV671), when associated

upstream

valves in the spr ay lines

(SIA-HV687, - HV688, and SIB-HV693,

HV695) were not closed to

isolate the header valves from the

RWT.

The licensee

determined

the cause of the event to be the failure of

the operator to follow a caution step

and the use of action tasks

within caution statements,

which was contrary to 70AC-OZZ01

"Procedure Writers Guide".

Procedure

73ST-2ZZ10 contains detailed

instruction appendices

for each train of spray valves to be tested

(M or N).

Each appendix contains

a caution statement

to ensure

the

closure of associated

upstream

spray line valves before opening the

discharge

valve.

However, the operator

used Appendix "S" during the

performance of the test

as it is used to record the test data

and

contains

an abbreviated

set of instructions.

Appendix "S" does not

contain the caution to ensure

the closure of the associated

spray

line valves.

The licensee's

event investigation report recommended

changing

73ST-2ZZ10

(73ST-1ZZ10 for Unit 1 and 73ST-3ZZ10 for Unit 3) prior

to the next performance of the surveillance in any unit by adding

action steps,

with sign-offs, to assure that the spray header would

remain isolated during the performance of the test.

The procedure

revision was given

a due date of May 26,

1987.

The inspector

noted

that the Unit 1 Surveillance Test Schedule for June,

1987,

issued

on

May 20,

had 73ST-1ZZ10 scheduled for performance

on June l.

On June 1, 1987,

an almost identical event occur red in Unit I.

During the performance of surveillance test 73ST-1ZZ10,

approximately

100 gallons of water drained from the

RWT to the

containment building when

an upstream

spray line valve (SIB-HV695)

was left open during stroke timing of the "B" train header

discharge

valve (SIB-UV671).

A review of this event revealed that the

procedure revision recommendations

had not been

made

and the

operator

had not been counseled

on the procedure

concerns.

The

inspector

noted that the licensee

provided immediate corrective

action by issuing

a Temporarily Approved Procedure

Change Notice

(TPCN) to change the closure of the associated

spray line valves

from a caution to required action steps with sign-offs.

This TPCN

was issued

on June 2, 1987;

one day after the event.

The failure to provide effective corrective actions to preclude the

reoccurrence

of a significant condition adverse to quality is a

violation of 10 CFR Part 50, Appendix B, Criterion XVI, "Corrective

Action" (528/87-17-02).

Refuelin

Water Tank Gravit

Flow Into The Auxiliar Buildin

Unit 1.

On May 29, 1987, during refilling of the "A" train containment

spray

(CS) system,

approximately

9000 gallons of water drained from the

refueling water tank

(RWT) into the

70 foot and 40 foot elevations

of the auxiliary building through two open vent valves

(SIA-V089 and

15

SIA-V807, located in the shutdown cooling heat exchanger

room on the

70 foot elevation).

The "A" train

CS had been

removed from service

and drained

on May 26 for a planned maintenance

outage.

The two

vent valves were removed

and replaced

during the outage

and were,

therefore,

not tagged out on the system clearance

log or identified

on the system status

drawings.

This led to the valves being

overlooked during the clearance

release

and system restoration

following completion of the outage.

The licensee

has performed

an investigation into this event

and

initiated corrective actions to prevent recurrence.

The licensee

has also decontaminated

the affected areas

of the auxiliary

building.

This item will remain unresolved

pending further review

of this event

and the licensee's

corrective actions

(528/87-17-03).

Auxiliar

0 erator/Radiation

Technician

Communication Problem-

Unit 1

On May 29, 1987,

an auxiliary operator

was observed entering the

40'levation

of the Unit 1 auxiliary building.

Major portions of the

elevation

had been contaminated

about eight hours ear1ier

when

approximately 9,000 gallons of water from the refueling water tank

was inadvertently spilled in the auxiliary building and temporarily

overfilled the

sump

(documented

in paragraph

8).

Virtually no

standing water remained

on the 40'levation at the time of the

operator's

entry to conduct

a check of the public address

system.

The individual, who was dressed

out in protective clothing,

was

noted to not be wearing a respirator.

The radiation exposure permit

that the operator

signed in on required

him to contact Radiation

Protection for entry requirements.

Based

on the inspector's

conversation with the auxiliary operator

and members of the

RP

department, it was determi,ned that poor communication

between

the

personnel

involved resulted in the operator

entering the

40'levation

without a respirator,

which would have

been required by

RP.

A subsequent

whole body count of the operator did not indicate

any internal or external

contamination.

The inspector

informed

plant management

that this was the second

instance

observed

by NRC

inspectors

in the past six months at Unit 1, where

an auxiliary

operator

was in a specific portion of the radiologically controlled

area

(RCA) without RP knowledge.

Although no radiological

problems

resulted

from either instance,

the inspector stated that better

communication

between the

RP department

and the auxiliary operators

appeared

warranted.

The licensee

has planned several

corrective

actions including: steps to reduce periods of congestion

in the

RP

office; ensuring the shift supervisor is fully aware of changes

in

radiological status;

enhancing postings in the

RCA, particularly

with regard to differentiating between "airborne" and "respiratory

protection required" postings;

and meeting with the auxiliary

operators to stress

the need for good communication with RP.

These

actions which are planned at all three units are expected to be

completed

by August 1, 1987.

The inspector will follow the

licensee's

action through general

observations

as part of the

routine inspection

program.

No violations of NRC requirements

or deviations

were identified.

Closed

Tem orar

Instruction 2515/88 - "Ins ection of Licensee's

Actions Taken to Im lement

NRC Guidelines for Protection

from

Floodin

of

E ui ment

Im ortant to Safet ".

Units 1

2 and

3

The purpose of this inspection

was to verify actions

committed to by

the licensee to insure that equipment important to safety would not

be damaged

due to the rupture of a non-safety related

system

component or pipe to the extent that engineered

safety features

would not perform their design functions.

As a part of this

inspection,

the inspector

reviewed applicable sections of the

licensee's

FSAR and

NRC staff SER's in order to ascertain

the nature

of the licensee

s commitments in this area.

This review identified

design features

committed to by the licensee to include separation

of redundant

equipment in different subcompartments,

sealing of

penetrations

between

subcompartments,

installation of floor drains

and curbing and water level alarms

and sealing of equipment

enclosures.

The presence

of these

features

was verified on a sample

basis in each of the three units by the review of system drawings

and inspection of various areas within the plants.

In addition, the

licensee

committed in response

to

NRC

FSAR questions

410.4

and 410.5

by letter dated

March 8, 1982, to include specific features for

termination of blowdown of the auxiliary steam line should

a break

occur in any of a number of areas

in the auxiliary building through

which it passes.

The staff's review of the licensee's

response

is

documented

in Supplement

2 to NUREG-0857 "Safety Evaluation Report

related to operation of the Palo Verde Nuclear Generating Station",

Section 3.6. 1.

Design modifications committed to by the licensee

added differential pressure

switch actuated, air operated

redundant

isolation valves in the auxiliary steam line upstream of the

auxiliary building.

These modifications are indicated

on system

drawing 13-M-ASP-001,

Revision 12.

The inspector

sought to locate

these features initially in Unit 3.

During this inspection,

the inspecto~ identified 6 of 20 installed

differential pressure

switches to be inoperable in that plastic

plugs installed on the end of the sensing

tubes for protection from

intrusion of debris during construction

had not been

removed.

Consequently,

the required actuation of the redundant isolation

valves would not have occurred

had a break occurred in the auxiliary

steam line in three different areas.

Subsequently,

inspections

by

the licensee identified a number of inoperable

switches in Units 1

and

2 which rendered portions of the actuation

systems in those

units inoperable

as well.

The failure to assure

the operability of

the auxiliary steam line isolation actuation

systems

is considered

a

deviation from the licensee's

commitment to include these

design

features

(Deviation 530I87-19-01).

At the end of this inspection,

the licensee

had returned the

isolation system to operable status

in each of the units.

The root

cause for this deviation and the possibility for the existence of

similar deviations is still under review by the licensee.

17

S stem Train Outa

es - Units 1 and

2

In an effort to maintain reliability of equipment,

the licensee

periodically removes

a train of a particular safety related

system

from service in order to perform preventive

and corrective

maintenance.

The work activities are pre-planned

and appropriate

Technical Specification action statements

are voluntarily entered

'nd satisfied.

The mini-outages

appear to be well managed,

and

assist in relieving the existing maintenance

backlog.

The inspector

noted that the number of train outages

during power operation

has

increased

recently as the plant availability has

improved.

The

inspector discussed

these

outages with plant management,

and stated

that although there are safety benefits to an aggressive

maintenance

program,

there is also

an inherent risk when

a train is taken out of

service.

The licensee

acknow'ledged

the comment and stated that they

would revise administrative control procedures

to ensure that

contingency plans for quickly restaging the train to service, if

necessary,

are considered prior to removing the equipment

from

service.

Although responsible

licensee

personnel

indicated that

contingency plans,

such

as the prestoring of spare

equipment,

have

been carried out in the past, it was agreed that formalizing the

process

would be beneficial.

The licensee

stated that the

administrative controls should

be in place

by August 1, 1987.

The

inspector will review the licensee's

revised administrative controls

(528/87-.17-01).

12.

No violations of NRC requirements

or deviations

were identified.

Steam Generator

Blowdown

Sam le Valve 0 eratin

Ex erience - Unit 2.

On June

10,

1987, the Unit 2 operating staff attempted to conduct

an'SME

Section XI stroke time test

on valve SG-UV-228.

The 1/2" valve

is one of the two Technical Specifications

(TS) identified isolation

valves in the steam generator

cold leg blowdown sample line.

Surveillance Test procedure

73ST-2ZZ10, "Section XI Valve Stroke

Timing -

SG and SI (Mode 1 thru 4)" directed that the valve be timed

closed.

The valve is timed from the moment of switch operation

until the green light on the valve hand switch goes

on.

There is no

minimum closure time required

by TS.

Ouring several

attempts to

conduct the test,

the operator noted that when the

hand switch was

operated,

the "open" red light immediately extinguished;

however,

the green "close" light did not come .on.

This valve previously

operated properly during the June 4, 1987, reactor trip and safety

injection actuation which resulted in an automatic closure of the

valve.

Several

members of the on shift staff, after discussing

the .

matter,

concluded the problem to be related to improper adjustment

of the position indication switch.

A work request to repair the

condition was written and the unsuccessful

test results

were noted

in the test procedure.

Based

on later discussions

with the plant

staff,, the inspector

was informed that a followup action to confirm

the position of the valve when placed in a closed position was not

taken

because

similar problems previously experienced

with this

valve design revealed the valves to be closed

and the problem

associated

with the position indication switches.

.18.

On June

16', the Section XI stroke times test

was again attempted.

Thi's time when the valve hand switch was operated

to close the

valve, the red "open".light. did not extinguish'and

the green "close"

light did not light up.

Based

on this observation,

the operating

staff checked that the valve had not closed,

entered

the

TS action

statement

and closed

and removed power from the second isolation

valve in the sample line.,

Following the second test attempt

a subsequent

check of the valve

position switch adjustment

was checked.

No positive conclusion

could be made because

the valve stem did not appear to move.

The

valve was then disassembled

and the spring, which presses

on the

stem to close the valve when the solenoid is deenergized,

was found

broken.

Based

on this finding and the fact that the red "open"

light extinguished during the initial test,

but did not extinguish

during the second test,

the licensee

concluded the valve was

operable

during the initial testing.

The licensee

supports this

conclusion with the fact that the spring is required to start the

stem movement,

once the spring moves into the flow stream the stream

pressure will assist

the closure of the valve.

The licensee attributes

the spring failure to a mi,sappl'ication of

the spring material which is 17-7 ph stainl'ess

steel.

This problem

was described in a IE Information Notice No. 86-72, "Failure 17-7 ph

Stainless

Steel

Springs in Valcor Valves

Due to Hydrogen

Embrittlement".

The licensee's

engineer ing staff is reviewing this

matter

on a generic basis.

Future actions

taken by the licensee

on

this issue will be followed as part of the normal inspection

program.

In discussing this matter, the licensee

was informed that not

confirming whether the valve was closed during the first test

following the failure of .the green "close" light to come

on was

regarded

as

an non-conservative

action.

Additionally the licensee

was informed that previous operating experiences

with this valve

should not have been

used

as

a basis for concluding the valve would

close.

This action was regarded

by the

NRC staff as lacking proper

concern for equipment operability requirements,

and that the

operating staffs should

be informed that future problems of this

type should require prompt followup invest1gations

to confirm

equipment operability.

The licensee

has instructed operating staffs

of the three units of the concern.

Discussions

with licensee

management

personnel

indicated that in

.reviewing the event,

the licensee

determined that the affected

penetration

was always isolated

by a closed

manual

valve during the

period in question

and therefore the licensee

has concluded that the

technical specifications

were not violated.

No violations of NRC requirements

or deviations

were identified.

19

13.

Followu

on Disablin

of an

En ineered Safet

Feature - Unit 1

As documented

in paragraph

7 of inspection report 50-528/87-10,

on

January

20, 1987, the operating shift at Unit 1 intentionally

disabled the Main Steam Isolation System

(MSIS), while the unit was

in mode 4 and cooling down to cold shutdown conditions.

The unit

Technical Specifications

require the MSIS to be operable in mode 4,

and therefore the shift personnel

had deliberately entered into

limiting condition for operation

(LCO) 3.0.3, which provides actions

required to be taken

when

an ACTION statement

of a system specific

LCO is not met.

During this inspection period, the inspector reviewed the licensee's

procedures

related to this event to ascertain

whether

a violation of

a regulatory requirement or a procedural

requirement

had occurred.

ANPP procedure

36MT-9SB03,

"PPS Bistable Input Simulation," which

was used

by the shift to vender the MSIS feature inoperable states

the purpose of the procedure

in paragraph

1. 1 to be as follows:

"To provide direction for simulating an input to a

PPS Bistable

as warranted

by plant conditions or for testing."

Sub-paragraph l. 1. 2 provides additional amplification on the purpose

of the procedure

and reads:

"This procedure

may be used to untrip a bistable during Reactor

shutdown to allow closure of the Reactor Trip Switchgear to

allow Rod Testing.

Bistables

not required,

per Technical

Specification

LCO 3.3.1 and 3.3. 2, for the plant mode at that

time are the only bistables

which maybe simulated into an

untripped condition."

The inspector questioned

whether paragraph

1. 1.2 prohibited the

use

of the procedure to defeat the

MSIS feature, in that

LCO 3.3.2

requires

the MSIS feature to be operable

in Mode 4.

The licensee

stated that the paragraph

only addressed

control rod testing

and

therefore did not apply to the action'aken

by the shift.

The inspector questioned

what controls were in place to govern the

actions of the shift personnel.

The licensee

responded

that

paragraph

5.3 of the procedure

requires

the Shift Technical Advisor

(STA) to verify that the action taken by the procedure is allowed by

the Technical Specifications.

That paragraph

reads

as follows:

"Request the Shift Technical Advisor to initiate a TSCCR to

identify that the modification accomplished

by this procedure

is properly identified and has verified the Technical

Specifications

allows the modification to be performed in the

present plant mode."

The

STA stated to the inspector that

he

had verified that in taking

the action,

the unit would be complying with LCO 3.0.3.

He further

stated that

he had concluded that the

MSIS feature

was not

technically required to be operable

in the condition the unit was

20

in, because

the

TS allow the

MSIS trip setpoint to be set

200 psi

below the actual

steam line pressure.

With the unit at

approximately

25 psig when the feature

was disabled,

the trip

setpoint could have theoretically

been set at

0 psia,

which would

have effectively rendered

the feature inoperable.

The

STA also

stated that

he would not have signed off paragraph

5.3 if the steam

line pressure

was above

200 psig.

The licensee

also stated that work order 000203545

was written,

approved,

and implemented,

in accordance

with the station work

control procedure,

to provide additional administrative controls

on

the work performed to disable

the MSIS feature.

As previously

discussed

in inspection report 50-528/87-10,

the licensee

did agree

that additional controls

on intentional entry into

LCO 3.0.3

was

prudent

and warranted.

During this inspection,

the licensee

again

strongly reinterated their position

on entry into

LCO 3.0.3.

The

licensee's

conduct of shift operations

procedure

has

been

significantly revised to clearly state the licensee's

policy in this

area.

The inspector closely reviewed the documentation

associated

with

this event

and concluded that the licensee

had complied with the

applicable

approved

procedures

and technical specif'ications,

and

therefore

no violation of requirements

had resulted

from the event.

As documented

in inspection report 50-528/87-10,

the inspector also

concluded that the event did not place the unit in an unsafe

condition.

Based

on these conclusions,

unresolved

item 528/87-10-01

is closed.

14.

Licensee

Event

Re ort

LER

Followu

- Units 1

2

and 3.

The following LERs associated

with operating events

were

reviewed by the inspector.

Based

on. the information provided

in the report it was concluded that reporting requirements

had

been met, root causes

had been identified,

and corrective

actions were appropriate.

The below listed

LERs are considered

closed.

Unit 1

LER NUMBER

DESCRIPTION

LER 85"66- LO/L1

LER 85"96" LO

LER 86-38-LO

Inoperable

Containment

Access

Inner Door.

Unanalyzed Fire Areas

Due To Engineering

Oversight.

Missed Channel

Check

On Two Radiation

Monitors Due To Personnel

Error.

LER 86"41-LO

Missed Channel

Check

On

A Radiation

Monitor.

LER 86-43-LO/Ll

Technical Specification Violation Due To

Video Camera

Use For Fire Watch Patrol.

LER 86-52-LO

HLER 86-57-LO

RCS

Low Flow Trip Set Non-Conservatively.

Fire Patrol

Performed

Late Due To Personnel

Error.

LER 86-59-LO

LER 87"03-LO

Emergency Lighting Power Supplies

Did Not

Meet New Acceptance Criteria.

Operator Error During Feedwater

Transient

Causes Trip.

LER 87"ll"LO

Firewatch Patrol

Missed

Due To Personnel

Error.

LER 87-13" LO

Entry Into Technical Specification 3.0.3

Due To Personnel

Error.

LER 87-15" LO

Surveillance Interval

Exceeded

For Three

Containment Isolation Valves

Due To

Personnel

Error.

No violations of NRC requirements

or deviations

were identified.

15.

Review of Periodic and

S ecial

Re orts - Units 1

2

and 3.

Periodic

and special

reports submitted

by the licensee

pursuant to

Technical Specifications 6.9. 1 and 6.9.2 were reviewed by the

inspector.

This review included the following considerations:

the report

contained the information required to be reported

by

NRC require-

ments; test results and/or supporting information were consistent

with design predictions

and performance specifications;

and the

validity of the reported information.

Within the scope of the

above,

the following reports

were reviewed by the inspector.

Unit 1

o

Monthly Operating Reports for April and May, 1987.

Unit 2

o

Monthly Operating

Report for April and May, 1987.

No violations of NRC requirements

or deviations

were identified.

16.

Unresolved

Items

Unresolved

items are matters

about which more information is re"

quired to determine whether they are acceptable,

violations or

22.

deviations.

An unresolved

item is addressed

in this inspection in

paragraph

8 of'his report.

~Ei

The inspector

met with licensee

management

representatives

period-

ically during the inspection

and held an exit on June

18,

1987.

The scope of the inspection

and the inspector's

findings,

as noted

in this report,

were discussed

and acknowledged

by the licensee

representatives.