ML17284A679

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Insp Rept 50-397/98-09 on 980426-0606.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML17284A679
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 07/02/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17284A677 List:
References
50-397-98-09, 50-397-98-9, NUDOCS 9807130346
Download: ML17284A679 (39)


See also: IR 05000397/1998009

Text

U.S. NUCLEAR REGULATORYCOMMISSION

REGION IV

Docket No.:

50-397

License No.: 'PF-21

Report No.:

Licensee:

Facility:

Location:

Dates:,

Inspector(s):

Approved By:

50-397/98-09

Washington Public Power Supply System

Washington Nuclear Project-2 --

Richland, Washington

April26 through June 6, 1998

S. A. Boynton, Senior Resident Inspector

J.

E. Spets, Resident Inspector

G. W. Johnston, Senior Project Engineer

G. M. Good, Senior Emergency Preparedness

Inspector

S. C. Burton, Resident Inspector, ANO

C. E. Skinner, Resident Inspector, CNS

H. J. Wong, Chief, Reactor Projects Branch E

AiTACHMENT:

Supplemental Information

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Washington Nuclear Project-2

NRC Inspection Report 50-397/98-09

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The routine shutdown for Refueling Outage R13 was properly executed with a detailed

preevolution brief and good command and control.

Operations performance in

monitoring and controlling the cooldown was improved over that observed during the

March 1998 forced outage (Section 01.1).

ai

Both the reactor disassembly and the fuel shuffle were generally well executed between

the control room and the refueling floor. However, two instances of weak procedure use

resulted in: 1) the failure to identify an incorrect precaution in the maintenance

procedure for the reactor building overhead crane, and 2) failure to verify that

appropriate minimum temperature requirements were being met prior to liftingthe

drywell upper shield blocks (Section M1.2).

The licensee's actions to address previously-identified weaknesses

in implementing

their foreign material controls (FMC) program for plant systems and containment have

been effective in raising the sensitivity and improving performance of plant personnel

(Section M1.3).

Licensee performance in implementing FMC for the spent fuel pool, reactor cavity and

reactor pressure vessel (RPV) was mixed. Weaknesses

were identified mainly in the

administrative controls of foreign materials.

These included the failure to perform

inventories of the spent fuel and equipment pools prior to removal of the RPV head.

The failure to perform the inventories eliminated an objective measure of the

effectiveness of FMC and was identified as a noncited violation of Plant Procedure 6.1.1

(Section M1.3).

Personnel performance in the conduct of testing excess flowcheck valves was

inadequate,

as evidenced by: 1) multiple examples of poor procedural adherence

and

procedure adequacy, 2) personnel knowledge deficiencies on testing requirements and

plant impact, 3) weak use of procedures in the field, and 4) weak command and control.

In one case, performance deficiencies resulted in the initiation of an engineered safety

features actuation signaI and plant transient.

Two violations of TS 5.4.1.a, each with

two examples, were identiTied regarding adequacy and use of surveillance procedures.

The violations included inadequate procedure guidance for establishing and restoring

from test conditions and failure to independently verify a valve location prior to valve

manipulation (Section M1.4).

The Division I emergency diesel generator (EDG) experienced multiple material

deficiencies during Refueling Outage R13 which resulted in several failures to run and/or

load. The material deficiencies included:

(1) the failure of the mechanical. governor'

-3-

motor operated potentiometer, (2) failure of the lube oil low pressure switch to reset, and

(3) failure of the diesel generator output breaker to close due to improper setting of the

breaker's trip latch check switch. The licensee's short-term corrective actions for the

failures were appropriate.

Long-term actions willbe reviewed in future inspection

activities (Section M1.5).

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During the fuel shuffle, the licensee accepted the condition of a partially elevated fuel

. assembly in the spent fuel pool without fullyevaluating its impact. Weak understanding

and review of the plant's design basis failed to identify that full insertion of the spent fuel

assembly is a condition of the spent fuel criticality analysis described in the Final Safety

Analysis Report (FSAR) (Section M1.2).

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The licensee decreased

the effectiveness of its emergency plan between February 1997

and April 1998, when it reduced on-shift health physics expertise and overburdened the

chemistry technician with health physics responsibilities during emergencies.

A violation

of 10 CFR 50.54(q) was identified. The licensee returned a third health physics

technician to on-shift following notification of the noncompliance (Section P3).

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The plant began the inspection period in Mode 5, with core alterations in progress.

Upon

completion of in-vessel maintenance,

reactor pressure vessel reassembly was completed and

the plant reentered Mode 4 on May 27. The plant remained in Mode 4 for the balance of the

inspection period.

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Conduct of Operations

01.1

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The inspectors observed portions of the reactor plant shutdown and cooldown in

preparation for Refueling Outage R13. Focus of the inspection was on command and

control of the evolution and procedural implementation.

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Reactor shutdown was commenced on April 18, in accordance with Plant

Procedure 3.2.1, Revision 32, "Normal Shutdown to Cold Shutdown." The preevolution

brief was observed and found to be sufficiently detailed to establish proper expectations

for the significant actions to be performed.

Senior management presence

in the control

room was noted.

RPV cooldown and initiation of shutdown cooling were properly executed with notable

improvement on the control of the cooldown as compared to the forced outage in March

1998. Weak control of RPV cooldown'during the March forced outage led to changes

in

Plant Procedure OSP-RCS-C102,

"RPV Cooldown Surveillance." The changes,

including a higher resolution pressure-temperature

curve and the addition of a table of

minimum temperature versus pressure, were considered an effective component in

controlling the R13 coo!down evolution.

The inspectors noted that Plant Procedure 4.12.1.1, Revision 9, "Control Room

Evacuation and Remote Cooldown," was not revised to include similar enhancements

for controlling cooldown. Also, discrepancies were identified between the pressure and

temperature limits provided in Attachment 8.1 of Procedure 4.12.1.1, those in

Procedure

OSP-RCS-C102,

andTechnicalSpecifications(TS).

However, thelimitsin

Procedure 4.12.1.1 were more restrictive than those in TS and, therefore, the

discrepancy was not considered safety significant. The inconsistencies between

Attachment 8.1 of Procedure 4.12.1.1 and Procedure OSP-RCS-C102 and TS, indicated

a weakness

in the licensee's procedure maintenance process.

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-2-

The routine shutdown for Refueling Outage R13 was properly executed with a detailed

preevolution brief and good command and control.

Operations performance in

monitoring and controlling the coo!down was improved over that observed during the

March 1998 forced outage.

02

02.1

Operational Status of Facilities and Equipment

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The inspectors walked down accessible portions of the following EFS:

Low Pressure Core Spray

Residual Heat Removal (RHR) A

Division I EDG and Starting Air

Standby Service Water A

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focus of the walkdowns was on Division I systems which received the majority of

maintenance during Refueling Outage R13. System configurations for operability were

verified following system restoration from maintenance.

No discrepancies were

identified. Licensee-identified material condition concerns with the Division I emergency

diesel generator are discussed

in Section M1.4.

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Conduct of Maintenance

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The inspectors. observed and/or reviewed the following work activities:

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SLC-RV-29A Replacement

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Removal and Testing of Relief Valve RHR-RV-25C

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Removal and Testing of Relief Valve RHR-RV-30

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Calibration of Diesel Lube Oil Level Switch DLO-LS-1A1

Additional niaintenance activities were observed and are discussed

in Sections M1.2

through M1.7.

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Proper use of FMC was noted in each of the activities observed.

Where appropriate,

adequate radiological controls and practices were noted.

During observations of the replacement of the RHR relief valves, the inspectors noted

that the workers were not documenting their progress in the field copy of the work order.

Although no discrepancies were noted with performance of the activities, placekeeping

. is a management expectation.

Failure to track work progress in the field was also

observed during testing of excess flow check valves (see Section M1.4) and, in one

instance, resulted in a partial reactor protection system actuation.

Following the installation of relief Valve SLC-V-29A, the inspectors observed sodium

pentaborate solution leaking from the bonnet cap of the valve. Valve SLC-V-29A

provides overpressure

protection of the standby liquid control (SLC) system piping

downstream of the positive displacement SLC pump. The discharge of the relief valve

returns to the suction of the pump. The leakage observed was a result of both stroke

testing of, and minor leakage past the SLC tank outlet Valve SLC-V-1A. The leakage

path was via the suction piping of the SLC pump, to the discharge of relief

Valve SL'C-V-29A', and to the valve bonnet.

From a maintenance perspective, the

leakage was of concern in that neither the work order, nor the worker involved,

recognized the need to properly torque the valve's bonnet cap due to the installation

configuration.

From a safety perspective, the'impact of the leakage was indeterminate.

However, over time with the condition remaining uncorrected, the potential existed for

sodium pentaborate to precipitate in the valve bonnet and affect the valve's operation.

To address the leakage concerns, the licensee properly tightened the valve bonnet and

initiated a change to the valve's setpoint data sheet to identify the requirement of

tightening the bonnet after valve installation. With the bonnet properly tightened, the

licensee also quantified the leakage past the SLC tank outlet valves and determined that

the leakage was small, but acceptable.

The inspectors reviewed the licensee's

justification for accepting the leakage and found it to be technically sound.

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FMC and practices were properly implemented in each of four maintenance activities.

Weak tracking of work progress in the field was noted in several instances and was a

generic problem during Refueling Outage R13, as noted in Section M1.4. In not

recognizing the impact of having the SLC pump relief valve discharge return to the

pump's suction, maintenance personnel failed to properly tighten the valve bonnet

resulting in system leakage.

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The,ihspectors observed portions of the reactor disassembly process and the fuel

shuffle. Inspection emphasis was on equipment rigging, FMC, radiological protection,

and command and control.

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The inspectors observed the following evolutions, as. described in Plant

Procedure 10.3.21, Revision 3, "RPV Disassembly:"

Drywell shield plug removal

Drywell head removal

RPV head lift

Dryer/separator removal

Reactor cavity flood-up

The inspection results of the licensee's FMC associated with the reactor disassembly

are discussed

in Section M1.3.

Overall, the reactor disassembly was well coordinated between operations and the

refuel floor coordinator. With the exception of the inadvertent loss of a drywell head nut

in the fuel pool cooling drain system for the reactor-cavity, few operational challenges

arose during the evolution. However, several procedural concerns were identified.

Following the liftof the first two upper shield blocks, the inspectors questioned, rigging

personnel on the refueling floor regarding the temperature prerequisites for performing

the lifts. Personnel indicated that the temperature on the refueling floor must be greater

than 55'F.

Plant Procedure 10.4.12, Revision 9, "Crane, Hoist, Lifting Device and

Rigging Program Control," requires, when using the overhead crane (MT-CRA-2), that

temperature be greater than 64'F prior to liffingloads of greater than 50 tons. If

temperature is below 64'F, Procedure 10.4.12 requires that the RSE be contacted.

The

weight of each of the upper shield blocks is approximately 100 tons. Although the use

of Procedure 10.4.12 is referenced. in the precautions and limitations for control of heavy

loads, refuel floor personnel were unfamiliar with the more restrictive temperature

requirement.

As local temperature indication was unavailable on the refuel floor, reactor

building supply air temperature was requested from the control room and was

determined to be 55'F, below the minimum requirements for liftingthe upper shield

blocks.= The RSE had not been contacted prior to the initial lift. Subsequently,

the

refueling fioor personnel obtained a contact pyrometer and determined that ambient

temperature on the refueling floorwas 66'F.

-5-

From discussions with the RSE, it was determined that the limitingtemperature of 64'F

was based upon temperatures

utilized in fracture toughness testing of the material

utilized for the overhead crane's main girders.

Thus, use of the crane at lower

temperatures

potentially places the crane in an unanalyzed condition. However, the

RSE indicated that safety margins for the overhead crane would not be significantly

impacted by the conditions noted by the inspectors.'The

RSE's conclusion that the

safety significance of the issue was low appeared to be reasonable.

The precautions

and limitations of Procedure 10.3.21 were revised to include the temperature limits of

Procedure 10.4.12. The failure to verify that the'refuel floortemperature was within the

, limits of Procedure 10.4.12 was identified as a violation of TS 5.4.1.a

(VIO 50-50397/9800-01).

Prerequisites of Plant Procedure 10.4.5, Revision 4, "Reactor (MT-CRA-2) and Turbine

Building (MT-CRA-1) Overhead Traveling Crane Inspection, Maintenance and Testing,"

require the verification that caution Tag 95-03-066 has been placed on the local

disconnect switch for MT-CRA-2, located on the refuel floor. The caution tag was

desigried to warn personnel of potential overload concerns for Motor Control

Center E-IVIC-7CBwhen the local disconnect is closed. A review of the licensee's active

clearance order log found that caution Tag 95-03-066 was cleared and no longer

hanging on the local disconnect.

From subsequent discussions with operations

personnel it was determined that the caution tag was replaced with caution labels at

E-MC-7CB. Although Procedure 10.4.5 was performed prior to reactor disassembly, the

erroneous reference in the procedure was not brought to the attention of the site rigging

coordinator, nor was it corrected.

This was considered a weakness

in procedure use.

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Execution of the greater than 1000 movements associated with the fuel shuNe was

accomplished without error. The licensee's implementation of the requirements of Plant

Procedure 6.3.2, Revision 13, "Fuel Shuffling and/or ONoading and Reloading," was

independently verified. Good command and control was demonstrated

by both the

control room and the refueling supervisor throughout the evolution. Although several

malfunctions. of the refueling bridge crane were experienced, the problems were

appropriately'addressed

prior to resumption of fuel movement.

Qualification of the

personnel involved was spot-checked and verified.

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One weakness was identified in Section 6.5 of Procedure 6.3.2.

Prior to withdrawing a

high worth control rod for a subcritical check, Step 6.5.6 states that fuel movement

should be suspended.

-The use of the term "should," which allows flexibilityin.

implementing the procedural step, is inconsistent with the requirements of-TS 3.9.3,

"Control Rod Position." Specifically, TS 3.9.3 rabies fuel movement into the core be

suspended

when one or more control rods are withdrawn. The inspector reviewed the

licensee refueling activities and found that Section 6.5 of Procedure 6.3.2 was not

utilized during the outage.

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Potential foreign material concerns were noted in the spent fuel pool during the

movement of fuel. Specifically, three separate fuel assemblies,

including one Asea

Brown Boveri (ABB) SVEA-96'assembly, were identified that would not fullyinsert into

their storage rack location. The tops of each of the assemblies were between 2 and

3 inches higher than adjacent assemblies that were fullyinserted.

Without-a detailed

investigation, the licensee had concluded that objects at the bottom of the racks were

preventing the full insertion of the assemblies.

The licensee believes that the objects

are likelyfuel channel fasteners, which would not adversely impact cooling of the spent

fuel.

In reviewing Problem Evaluation Request (PER) 298-0424, which documents the

condition of the three fuel assemblies,

it was noted that the licensee had no operability

concerns due to the fact that the assemblies were not in the core and did not pose

.interference concerns with movement of other fuel. The fuel assemblies were left in

their as-found condition. The inspectors discussed the as-found condition with the

licensee's engineering personnel responsible for the spent fuel pool criticality analyses,

focusing on the impact of the condition on the analyses.

From that discussion, the

inspectors determined that the licensee had not identified inconsistencies

between the

as-found condition and the parametric requirements of the ABB criticality analysis

described in Section 9.1 of the Final Safety Analysis Report (FSAR). Section 9.1.2.3.1.2

states, in part, that the criticality safety of the spent fuel storage rack, with SVEA-96 fuel,

is assessed

subject to the condition that, when stored, the fuel assemblies must be fully

inserted into the fuel storage boxes.

Although the ABB SVEA-96 fuel assembly did not

meet the analyzed condition of Section 9.1.2.3.1.2, the bundle was neither relocated to

another storage rack location, nor was an evaluation performed to document the

acceptability of the as-found condition.

Subsequent to the discussion, the licensee reviewed Section 9.1 of the FSAR and

agreed that an evaluation was required for leaving the ABB assembly in its abnormal

condition. A followup assessment

of operability was performed that demonstrated,

with

the fuel assembly partially elevated, the reactivity, described in terms of k-effective,

would be less than 0.9 (design limitis 0.95 k-effective). The licensee's operability

evaluation was found to be technically sound and the safety significance of the issue

was considered low. However, the failure of the licensee to promptly identify and

address the discrepancy between the condition of the fuel assembly and the

assumptions of the spent fuel pool criticality analysis indicated a weak understanding

and review of the plant's design and licensing basis.

The failure to properly identify and

address the condition, without prompting from the inspectors, was identified as a

violation of 10 CFR Part 50, Appendix B, Criterion XVI,"Corrective Actions"

(VIO 50-397/98009-02).

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Both the reactor disassembly and the fuel shuffle were generally well executed between

the control room and the refueling fioor. However, two instances of weak procedure use

resulted in: 1) the failure to identify an incorrect precaution in the maintenance

-7-

procedure for the reactor building overhead crane, and 2) failure to verify that

appropriate minimum temperature requirements were being met prior to liftingthe

drywell upper shield blocks.

During the fuel shuffle, the licensee accepted the condition of a partially elevated fuel

assembly in the spent fuel pool without fullyevaluating its impact. Weak understanding

'nd

review of the plant's design basis failed to identify that full insertion of the spent fuel

assembly is a condition of the spent fuel criticality analysis described in the FSAR.

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The inspectors observed or reviewed selected maintenance activities during the plant's

1998 refueling outage (R13) to evaluate the licensee's implementation of its FMC

program.

The scope of the inspection activities was adequate to address NRC

Inspection Followup Item 50-397/97009-02.

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Overall, the implementation of FMC on the refueling floorwas acceptable.

However,

several lapses in FMC resulted in operational challenges and procedural

noncompliances.

At the beginning of the reactor disassembly evolution, it was observed that the refueling

bridge was not properly posted as an FMC area boundary.

Specifically, the stairs

leading onto the refueling bridge were not posted while the bridge was within the spent

fuel pool FMC area.

The lack of a visible posting could have allowed access to the

bridge without implementing the proper FMC requirements.

This was considered a

weakness

in implementing Plant Procedure 1.3.18, Revision 15, "FMC Around the Spent

Fuel Pool, the Reactor Cavity and the Dryer Separator Pit," which provides, in part,

guidance on posting of the FMC area boundary.

Other weaknesses

in implementing

Procedure 1.3.18 were:

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refueling bridge provides two separate personnel access points into the

FMC area, contrary to the guidance in Procedure 1.3.18 which states that the

FMC boundary should have a single opening.

I

Routine audits of the spent fuel pool FMC log were not being performed during

nonoutage periods as outlined in Procedure 1.3.18.

It was also identified that the licensee had failed to perform an inventory of the spent

fuel and equipment pools prior to removal of the RPV head.

This inventory is required

by Plant Procedure 6.1.1, Revision 4, "Spent Fuel and Equipment Pools Inventory," to

-8-

establish a baseline of material in the pools and provide confidence that the material

was not introduced into the RPV while the vessel head was removed.

Without a baseline inventory for the Refueling Outage R13, the inspectors reviewed the

documented inventories performed in the Refueling Outage R12.

In reviewing those

inventories, it was noted that the number of control rod blades inventoried prior to RPV

head removal was 32, while the number inventoried after RPV head reinstallation was

31.Resolution of the discrepancy was not documented in the latter inventory. From

discussions with the engineer who performed both inventories, the discrepancy

. apparently resulted from'personnel error in documenting the second inventory.

Subsequently, the engineer verified that the second inventory should have shown a total

of 32"control rod blades.

Both the error and the failure to identify it during review

reduced the value of the inventories in supporting FMC. The failure to perform the spent

fuel and equipment pool inventories prior to removing the RPV head during Refueling

Outage R13 did not result in a loss of control of foreign materials.

This failure

constitutes a violation of minor significance and is being treated as a noncited violation,

, consistent with Section IVof the NRC Enforcement Policy (NCV 50-397/98009-03).

Weaknesses

were also noted in work practices for the prevention of introducing foreign

materials into the spent fuel pool, reactor cavity, and the RPV.

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During removal of the drywell head, one of its fastener nuts was inadvertently

kicked into a reactor cavity drain line. Retrieval of the nut required significant

resources and resulted in an additional cumulative outage dose of

0.32 person-rem.

During removal of the RPV head, an o-ring retaining clip was lost in the vessel.

Also, during core shroud weld inspections, damage to the inspection equipment

resulted in the loss of a small spring and several ball bearings into the RPV. As

retrieval was not practical, the licensee performed a loose parts evaluation to

determine the potential impact of the foreign material during plant operation.

The licensee concluded that the material did not present a safety concern.

The

,inspectors reviewed the licensee's analyses and found the conclusions to be

acceptable.

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During inspection activities involving maintenance of breached systems, the inspectors

observed the implementation of FMC in accordance with Plant Procedure 10.1.13,

Revision 15, "FMC For Systems And Components."

FMC for systems and components

were noted to be improved over Refueling Outage R12. Adequate controls were being

implemented in all activities observed.

A selected review of completed work orders also

noted that system closeout inspectioris were being performed, an area where

weaknesses

were identified in 1997 (Refueling Outage R12).

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The inspectors conducted three separate tours of the drywell and one tour of the wetwell

to assess

both material condition of structures, systems, and components in the areas

and control of foreign material.

One of the inspections included the drywell closeout

tour,. Overall, the licensee's efforts to control foreign materials in the containment were

effective. Although the licensee identified several discrepancies

in foreign material

accountability process, the licensee's cleanup efforts in the drywell adequately

compensated for any shortcomings in the accountability of materials.

The drywell

. closeout inspection verified that the cleanup efforts were effective and found that

performance in this area continued to improve over past outages.

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licensee's actions to address previously identified weaknesses

in implementing their

FMC program for plant systems and containment have been effective in raising the

sensitivity "and improving performance of plant personnel.

Inspection Followup

Item (IFI) 50-397/97009-02 is closed.

Licensee performance in implementing FMC for the spent fuel pool, reactor cavity, and

RPV was mixed. Weaknesses

were identified mainly in the administrative controls of

foreign materials.

These included the failure to perform inventories of the spent fuel and

equipment pools prior to removal of the RPV head.

The failure to perform the

inventories eliminated an objective measure of the effectiveness of FMC and was

identified as a noncited violation of Plant Procedure 6.1.1.

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The inspectors observed and/or reviewed surveillance testing of several EFC valves to

evaluate the adequacy of the procedures, the performance of personnel involved, and

performance of equipment.

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The following surveillances were reviewed:

ISP-EFC-B102, Revision 1, Testing EFC Valves For Main Steam Leakage

Control

ISP-EFC-B103, Revision 0, EFC Valves Testing of Jet Pump, RPV Drain and

Core Plate Flow

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ISP-EFC-B108, Revision 0, EFC Valve Test of Containment Atmosphere And

Suppression

Pool Level Instrument Sensing Lines

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ISP-EFC-B108:

On May 19, while performing Plant Procedure ISP-EFC-B108, an

unexpected half-scram was initiated.

In reviewing the cause of the scram signal, the

licensee determined that in performing testing on EFC 62b, the instrumentation and

controls (l&C)technicians had not properly isolated an associated

reactor protection

system pressure switch in accordance with the procedure.

The failure to isolate the

switch was due to a combination of miscommunications between the l&Ctechnicians

and inadequate tracking of,surveillance progress on the field copy of the procedure.

Through discussions with the Maintenance Manager and the I&C Supervisor it was

determined that procedure placekeeping is a management expectation.

The failure to

. properly implement the requirements of Plant Procedure ISP-EFC-B108 was identified

as the first example of a violation of TS 5.4.1.a (VIO 50-97/98009-04).

ISP-EFC-B102:

On May g6, during a routine plant tour, the inspectors observed

I&C

technicians performing testing on EFC 18B utilizing Plant Procedure ISP-EFC-B102. A

number of discrepancies were identified with regard to p'ersonnel knowledge and

performance iri implementing the procedural requirements:

II

The I&Ctechnician operating the test cart was unable to identify the required

pressure to be maintained while testing the EFC (85 -110 psi).

In fact,

inattention on the part of the technician allowed the air-operated test pump to

raise test pressure to 60 psi above the required band, as noted on the pressure

gage initiallyby the inspector.

Contrary to the guidelines of Site Wide Procedure

SWP-PRO-1, Revision 1, "Description and Use of Procedures and Instructions,"

Step 3.6.3.e, the l8C technician did not have a copy of the governing test

procedure for reference.

Additional review of Procedure ISP-EFC-B102 identified that the demineralized

water system header is stipulated to be utilized as the water source for testing

EFC 18B. The use of the air-operated test pump is not described as an option.

The steps of Procedure ISP-EFC-B102 that specifically require the connection of

the demineralized water header were initialed as being completed, as written,

without clarifying comments on the use of the test pump. Subsequent

discussions with I&Csupervision indicated that the technicians had utilized the

test pump because they, were unable to obtain the required test pressure with

the demineralized water header.

It was also indicated that this was a

non-proceduralized,

accepted practice. The inspector reviewed the operating

characteristics of the demineralized water system and determined that, in fact,

the system could not provide the required pressure for performing the test. The

failure of Procedure ISP-EFC-B102 to specify the need for a water source other

than the demineralized water header for testing EFC 18B was identified as the

first example of a violation of TS 5.4.1.a for inadequate procedure

(VIO 50-397/98009-05).

A second I&Ctechnician, responsible for manipulating valves downstream of the

EFC'to stroke the valve closed, failed to ensure that an independent veriTication

was performed prior to'anipulation of the valves. Additionally, although the

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second technician did have a copy of the governing procedure, he was not

documenting the progress of the surveillance on his copy. The failure to

implement the independent verification requirements of

Procedure ISP-EFC-B102 was identified as the second example of a violation of

TS 5.4.1.a (VIO 50-397/98009-04).

~

.

The lead technician for controlling the testing, located in the control room, was

not fullycognizant of actions being taken in the field by the other technicians.

Command and control of the evolution was weak as evidenced by differing

perceptions on the part of the technicians involved as to where they were in the

test procedure.

Specifically; the lead technician believed that, at the time of the

inspector's observations, the surveillance test was in progress.

Contrary to that

perception, the technicians in the field believed they were still troubleshooting the

failure of the valve's closed position indication that was identified a day earlier.

The failure of the maintenance personnel to track their progress in the field copies of the

governing procedure was a recurring problem in both of the above surveillances and has

been identified as a potential generic problem by the licensee's maintenance

'rganization.

Followup discussions with the maintenance manager and I&Csupervisor

found that the number of discrepancies

identified for the testing of EFC 18B were

attributable to several factors. These included field troubleshooting of the valve that was

performed outside of the 'defined requirements of the procedure and without an

approved troubleshooting plan and weak control of the evolution by the lead technician

in the control room.

ISP-EFC-B103:

On May 30, during backfill operations of the instrument lines

associated with EFC Valves 44Be and 44BI, an unexpected engineered safety feature

(ESF) actuation and scram were initiated. The ESF actuation resulted in the automatic

start of both the Division I and Division III emergency diesel generators (EDGs), and the

initiation of Division I (low pressure core spray and low pressure coolant injection A) and

Division III (high pressure core spray (HPCS)) emergency core cooling systems

(ECCS).

Both Division I ECCS pumps injected into the vessel.

The HPCS pump did not

start due to removal of the control power fuses to its associated

motor supply breaker.

This configuration was consistent with.plant conditions at the time of the event.

In response to the transient, operators secured the operating control rod drive pump to

limitthe pressure rise in the RPV. -.Following verification that the ESF signal was invalid,

operators also secured the Division.l ECCS pumps.

During the transient, RPV pressure

increased from initially100 psig to a maximum of 425 psig, approximately the shutoff

head of the low pressure ECCS pumps.

RPV temperature and pressure remained

within allowable limits. The operating crew's actions were timely and appropriate.

Subsequent

investigation ofthe transient by the licensee determined that the cause of

the event was an improper lineup to backfill the instrument lines associated with EFC

Valves 44Be'and 44BI. Plant Procedure ISP-EFC-B103, which governs the backfill of

these instrument lines followin'g testing of the check valves, did not provide adequate

g r..

-12-

guidance on the location of the backfill injection point. Recognizing the lack of specificity

in the procedure, the l8C technicians performing the evolution concluded that they

should backfill the instrument lines from each of the three instruments supplied by EFC

Valves 44Be and 44BI. The 18C'technicians did not reference a piping and

instrumentation diagram when determining the appropriate backfill lineup(s) to be used.

As such, they failed to recognize that, in backfilling the low side of level

Transmitter MS-T~A, they would be backfilling a reference leg that was shared by

several other Division I and Division Ill,instruments. When the air-operated pump was

utilized to backfill the low side of MS-LT-44A, the pressure perturbations from the pump

. action were transmitted to the other instruments, generating erroneous outputs to ESF

actuation relays. The inspector concluded that both inadequacies

in

Procedure ISP-FC-103 and an over-reliance on skill-of-the-craft knowledge for-

backfilling the instruments contributed to the event. The failure of

Procedure ISP-FC-B103 to identify the specific lineup for backfilling Valves EFC 44Be

and 44BI was identified as the second example of a violation of TS 5.4.1.a for

inadequate procedure (VIO 50-397/98009-05).

c.

QoOnclusl

s

Personnel performance in the conduct of testing EFC valves was inadequate,

as

evidenced by: (1) multiple examples of poor procedural adherence and procedure

adequacy, (2) personnel knowledge deficiencies on testing requirements and plant

impact, (3) weak use of procedures in the field, and (4) weak command and control.

In

one case, performance deficiencies resulted in the initiation of an engineered safety

features actuation signal and plant transient.

Two violations of TS 5.4.1.a, each with

two examples, were identified regarding adequacy and use of surveillance procedures.

The violations included inadequate procedure guidance for establishing and restoring

from test conditions, and failure to independently verify a valve location prior to valve

manipulation.

M1.5

iv sion

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62

The inspectors observed and/or reviewed the following work activities:

~

OSP-ELEC-M701, Revision 2, Diesel Generator

1 - Monthly Operability Test

~

TSP-DG1/LOP-B501, Revision 0, Standby Diesel Generator DG1 Loss of Power

'est

~

Plant Procedure 10.25.122, Revision 4, Locating and Identifying DC Distribution

System Grounds

-13-

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F 'lu

On May 2, 1998, the Division I EDG was tested in accordance with surveillance test

Procedure TSP-DG1/LOP-8501, "Standby Diesel Generator DG1 Loss of Power Test,"

Revision 0. During the test procedure, the EDG was loaded per Step 7.5.11 by

paralleling the EDG to meet a requirement for a 24-hour run at certain loads.

The EDG

tripped while the operators were adjusting the load, and the problem was traced to the

, motor-operated potentiometer in the speed governor. The motor-operated

potentiometer had an apparent "dead" area in the resistive portion of the potentiometer.

'he "dead" portion of the potentiometer affected the EDG, so that as the load was

changed, the unit'experienced a sudden change of load as the dead area of the

potentionmeter was passed.

This sudden decrease

in demand caused the diesel

generator to.trip on reverse power. The speed governo's motor-operated potentiometer

was replaced and a subsequent

start and 24-hour run of the EDG were successful.

The inspector's review of the governor circuit determined that the effect that this failure

would likely have had on the EDG met the criteria for a valid failure to load for the EDG.

The reason for this determination was that the motor-operated potentiometer is required

for the speed governor to control engine speed when the EDG is running in the

isochronous mode as it would on an engineered safety feature actuation.

The test was

conducted in the droop mode for parallel operation of the EDG and had the effect of

causing a sudden change in load demand.

e

w'c

On May 19, 1998, during an attempt to start, the Division I EDG tripped from a

generator lockout relay actuation.

During the investigation, the system engineer

determined that a lube oil pressure switch had failed to open prior to the 1-minute time

delay in the start circuit. With the switch contacts closed, this completed the logic for the

actuation of the generator lockout relay, resulting in a trip of the EDG. The inspector

observed the investigation of the switch during the troubleshooting effort. The switch

appeared to have failed to open when its setpoint pressure was met. The testing did not

identify an apparent cause for the failure. There was no indication of an actual low lube

oil pressure during the" actual EDG start.

From these conditions, and the fact that the

lube oil pressure switch is bypassed

in the engineered safety feature start of the EDG,

the inspector concluded that the failure of the EDG to run in this instance did not meet

the criteria for a valid failure to run in the EDG reliability program.

f,

DD

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On May 19, 1998, while performing OSP-ELEC-M701 "DG-1 Monthly Operability Test,"

the output Breaker E-CB-DG1/7 failed to close during the portion of the test where the

EDG is paralleled to the plant electrical system.

Normal practice is to perform a slow

start to idle of the diesel engirie, and after a period of warmup to load and.parallel the

-14-

unit. Subsequent

investigation identified what appeared to be loose leads in the

synchronizing circuitry that were suspected of contributing to the problem. The leads

were tightened, and a subsequent attempt to parallel and load the diesel resulted in a

successful paralleling of the unit. The unit was unloaded and another attempt to parallel

the unit failed. The unit was left in the as-tested condition and was subjected to a

troubleshooting plan. The previously identified loos'e terminal leads were determined

not to be the cause.

The observed condition was determined to be a design feature of

the terminals. The troubleshooting efforts identified the probable cause as the latch

check switch, which'was confirmed through a test that was observed by the inspector.

f

The latch check switch is a micro-switch that closes when the trip mechanism is properly

latched.

This protects the breaker from closing without a properly latched trip

mechanism.

The apparent cause of the breaker failure to close was an improperly

adjusted lever arm on the latch check switch. The lever arm was inspected and

adjusted as specified in the procedure to a tolerance of 1/8 to 3/16 inch, as described in

Step 7.2.23 of Plant Procedure 10.25.13, "4160/6900 Circuit Breakers 4 Year

Inspection." This is the intended range within which the'switch is expected to close, to

indicate that the trip latch pawl is made up, therefore indicating that the trip mechanism

is properly latched.

The latch check switch lever arm was determined to be out of

adjustment during this investigation. The switch lever arm was adjusted and the breaker

cycled several times to assure proper functioning.

The licensee staff was still pursuing the root cause of the misadjustment at the time of

the inspection.

Possible causes were an inadequate procedure, personnel error,

or'ome

other factor undetermined at the time. Based on the observations and

discussions, the inspectors concluded that the two failures of the breaker to close

represented

valid failures of the EDG to load.

D

'il'he

inspector discussed the repeated failures of the Division I EDG during the. outage

with cognizant system engineering staff. The licensee indicated that, based on their

preliminary analysis, the Division I EDG was likelyto be placed in a goal-setting status,

as required by.10 CFR 50.65(a)(1) and their Diesel Generator Reliability Program.

The licensee's Diesel Generator Reliability Program was established to help ensure a

reliability level of 0.95 for the EDGs. To accomplish this, the program directs action to

be taken when either 3 or more failures are experienced

in 20 demands, or 5 in 50, or 8

in 100. The reliability program goal of 0.95 equates to a demand/run failure rate of 0.05,

while the trigger value of 3 failures in 20 demands equates to a failure rate of 0.15.

Additionally, the licensee's individual plant examination assumes

a demand failure rate

of 0.03. The reason(s) for the discrepancies

between the failure rates could not readily

be determined.

The adequacy of the licensee's performance criteria and reliability

trigger values to support the assumptions of the individual plant examination, and the

licensee's long-term actions to address the recent reliability concerns for.the Division I

EDG, willbe reviewed in a future inspection (IFI 50-397/98009-06).

-15-

c.

~~ciao

The Division I EDG experienced multiple material deficiencies during Refueling

Outage R13 which resulted in several failures to run and/or load. The material

'eficiencies

included:

(1) the failure of the mechanical governor's motor operated

potentiometer, (2) failure of the lube oil low pressure switch to reset, and (3) failure of

the diesel generator output breaker to close due to improper setting of the breaker's trip

latch check switch. The licensee's short-term corrective actions for the failures were

appropriate.

Long-term actions willbe reviewed in future inspection activities.

M1.6

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S

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iners

a.

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5

Inspectors observed portions of installation and removal of RHR pump suction strainers

located in the suppression

pool. Maintenance activities were located in the suppression

pool under water and was performed from May 4-14. Maintenance was controlled by

Work Order GYC9. Inspection activities included observation of installation activities,

inspection of new strainers, and review of design changes for RHR Pump RHR-P-28's

suction strainer.

Inspectors observed portions of maintenance for the installation of several strainers that

were modiTied. Maintenance was performed in the suppression

pool and could be

observed via a closed circuit camera mounted to the diver's helmet.

No deficiencies

were noted with observed maintenance.

The RHR Pump RHR-P-28 suction strainer

could not be installed as originally'designed.

Due to a small inaccuracy in initial

measurements

in the distance between a structural support column and the strainer

flange, the RHR-P-28 strainer was manufactured slightly larger than the space allowed

for. The vendor modified one edge of the suction strainer by reducing the length to

accommodate the structural support column. The inspectors qualitatively evaluated the

modification and concluded that the change had an insignificant impact on the ability of

the strainer to perform its safety function.

Inspectors observed portions of the installation of the modified strainer for

Pump RHR-P-28 performed under Work Order GYC9, Task 7, on May 12. Technicians

had completed and properly tracked steps outlined within the work package.

Quality

control inspectors were observed performing verification of torquing requirements.

Inspectors reviewed the methodology for validation of torque wrench values, which

ensured that the use of the torque wrenches in an underwater environment were

accounted for.

-16-

c.

QggcIt~io s

The installation of the new ECCS suppression

pool suction strainers was well executed.

An unanticipated interference identified during the installation of the RHR Loop B suction

strainer was appropriately addressed.

M1.7

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627 7

From May 5-22, inspectors reviewed MSRVtesting performed during reactor shutdown

for Refueling Outage R13. The inspection included a review of MSRV performance

history, applicable procedures, engineering interviews, and associated

TS.

i

sa

The inspectors reviewed relief valve test data for 18 MSRVs tested during the'shutdown

for Refueling Outage R13. Test data indicated that 3 of 18 valves were found low out of

tolerance.

Four additional valves were not tested due to inoperable installed test

devices.

Ofthe four valves not tested, three were removed from service due to leakage

and the remaining valve was demonstrated

to be within tolerance during power

ascension.

Valve performance was within the requirements of TS 3.4.3, which requires

that 12 of 18 valves be operable for operation above 25 percent power.

Cause,

corrective actions, and generic implications for the MSRVs that failed were properly

tracked under PER 298-0390.

Procedure ISP-MS/IST-R101, Revision 0, "MSRVSetpoint Verification Using Set

Pressure Verification Device," indicates that the MSRVs are required to be tested at a

rate of 4 valves every 24 months and 100 percent of the population every 5 years.

The

inspectors noted that valve testing has multiple requirements associated with tracking

and evaluation.

One requirement was that valves in the test sample be selected from

the valves with the longest interval since the test was last performed. Additionally,

inspectors questioned meth'odologies fortracking valves rotated with spares.

Currently

the licensee tests 100 per'cent of installed valves every outage.

The inspectors found

that the practice of performing a 100 percent verification each outage significantly

reduced the burden associated with tracking various

requirements.'he

inspectors reviewed maintenance rule tracking with the applicable engineer and

found that the system is tracked as a function of the TS Surveillance and associated

requirements.

The maintenance rule database for all systems was under review and

revision to better quantify component requirements.

The licensee indicated that as a

part of the review process MSRVs were being evaluated for individual tracking and

establishment of specific performance criteria.

c.

QoOl~sio

-17-

Main steam safety relief valve testing demonstrated

that the safety relief system met TS

operability requirements."

The licensee's current practice of performing a 100 percent

verification during each outage eased the tracking burden associated with specific

testing requirements.

I

En

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E1

Conduct of Engineering

E1.1

aeValv

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Inspectors reviewed modifications to Valves RHR-V-42A, RHR A.injection valve, and

HPCS-V-15, HPCS suppression

pool suction valve. The inspectors reviewed

'odiTication

documentation including: Plant ModiTication Record, 94-0043-2, Pressure

Locking Bypass Modification; Work Order, JBM9 01, HPCS -V-15 Bypass Line

Installation; and B'asic Design Change, El 2.8, Modify Pressure

Locking Susceptible

Valves; RHR-V-42A and HPCS-V-15.

b.

b

i n

F

Generic Letter (GL) 95-07, "Pressure Locking and Thermal Binding of Safety-Related

Power-Operated

Gate Valves," further addresses

pressure locking and thermal binding

'ssues

originally identified in GL 89-10. As a result of the licensee's review of GL 95-07,

several valves considered operable, but possessing

minimal margins to operability

under certain operating configurations, were designated as requiring modifications.

Safety-related double disk gate Valves RHR-V-42A and HPCS-V-15 were two of the

valves identified as requiring modifications and scheduled for modifications during

Refueling Outage R13.

Modifications were performed to provide relief path from the bonnet of the valve to the

high pressure side piping. The inspectors reviewed the modification-packages and

interviewed engineering.

Several changes were made to Work Order JBM9 01 to

accommodate the extraction of a drill bit that broke off in the bonnet during initial drilling.

Interviews with engineering indicated that the broken parts were recovered without

incident. The inspectors reviewed nondestructive test data collected for HPCS-V-15 and

found the data to be complete.

The engineering evaluation, associated

design detail

drawings, drawing change notices, design safety analysis and screening provided

sufficient detail for installation and proper documentation of the modification.

-18-

Design changes to split disc gate Valves RHR-V-42A, and HPCS-V-15, which

addressed

pressure locking and thermal binding issues identified in response to

GL 95-07, were properly evaluated and developed.

Postmaintenance

testing

requirements were sufficient to ensure that the integrity of the associated systems was

maintained.

V

la

Su

o

P3

Emergency Preparedness

Procedures and Documentation

a.

nS

o

0

By memorandum dated June 28, 1997, Region IVrequested the Office of Nuclear

Reactor Regulation to review Washington Nuclear Project-2 Emergency Plan Revisions

17 (partial),.18, and 19, via Task Interface Agreement (TIA97-017). The licensee

submitted the revisions-on August 5, 1996, October 23, 1996, and April 3, 1997,

respectively.

The licensee determined that the changes did not decrease the

effectiveness of the. emergency plan.

The Emergency Preparedness

and Radiation Protection Branch completed its review of

the revisions on March 23, 1998. The resulting safety evaluation was transmitted to

Region IVon April 13, 1998. The safety evaluation was forwarded to the licensee by

letter dated April 16, 1998.

b.

b

i

s

Regarding the Revision 17 drill program description (the subject of the partial review),

the safety evaluation stated that during a November 13, 1997, telephone conversation

the licensee agreed to modify drill requirements in the next emergency plan revision to

clarify that annual radiological monitoring drills are not used to replace one semiannual

health physics drill. This response was considered acceptable.

Regarding Revision 18, the safety evaluation confirmed that the licensee had

satisfactorily fulfilleda commitment to designate an alternate emergency operations

facility location in the emergency plan. A Notice of Deviation concerning this matter was

identified in NRC Inspection Report 50-397/96-14, dated October 25, 1996.

In contrast, the safety evaluation concluded that the licensee decreased

the

effectiveness of its emergency plan in Revision 19 when it reduced on-shift health

physics expertise and overburdened the on-shift chemistry. technician with health

physics responsibilities during emergencies.

The on-shift chemistry technicians were

given responsibility for health physics emergency response

in February 1997.

10 CFR 50.54(q) permits licensees to make emergency plan changes, without prior

J.

-19-

NRC approval, only ifthe changes do not decrease the effectiveness of the plan. The

failure to receive NRC approval prior to reducing the level of on-shift health physics

expertise was identified as a violation of 10 CFR 50.54(q) (VIO 50-397/98009-07).

The licensee was informed of the Office of Nuclear Reactor Regulation's determination

during an April 16, 1998, conference call with the NRC's Region IVstaff. The Plant

Support Branch Chief and Senior Emergency Preparedness

Analyst represented

the

NRC, and the licensee's Emergency Preparedness

Manager and one emergency

planner represented

the licensee.

During the conference call, the Emergency

. Preparedness

Manager stated that immediate corrective actions had been taken in

anticipation of the outcome.

Corrective actions included returning to three on-shift

health physics technicians and issuing a PER to validate the reduction. The licensee

was informed that the corrective actions alleviated the NRC's immediate concern.

c..

~oclu~i

Based on information provided by the licensee, Revision 17 continued to meet drill

guidance criteria. Revision 18 fulfilleda commitment to designate an alternate

emergency operations facility location. The licensee decreased

the effectiveness of its

emergency plan between February 1997 and April 1998, when it reduced on-shift health

physics expertise and overburdened the chemistry technician with health physics

responsibilities during emergencies.

A violation of 10 CFR 50.54(q) was identified. The

licensee returned a third health physics technician to on-shift following notification of the

noncompliance.

V

a

a ement

ee

s

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management on

June 24, 1998. The licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary.

No proprietary information was identified.

4

~cerise

Supplemental Information

PARTIALLIST OF PERSONS CONTACTED

R. Barbee, Instrumentation and Controls Supervisor

S. Bian, Reactor Engineering

D. Coleman, Regulatory Affairs Manager

D. Giroux, System Engineering

D. Hillyer, Radiation Protection Manager

P. Inserra, Licensing Manager

S. Oxenford, Operations Manager

G. Sanford, Maintenance Manager

G. Smith, Plant General Manager

J. Kane, Acting Engineering Manager

R. Webring, Acting Chief Executive Officer

INSPECTION PROCEDURES USED

~

IP 37551:

IP 61726:

IP 62707:

IP 71707:

IP 71750:

IP 82701:

IP 92902:

Onsite Engineering

Surveillance Observations

Maintenance Observations

Plant Operations

Plant Support

Emergency Preparedness

Program

Followup - Maintenance

ITEMS OPENED, CLOSED, AND DISCUSSED

50-397/98009-01

'IO, failure to verify that the refuel floortemperature was within the

limits of Procedure 10.4.12 prior to lifting loads greater than 50

tons.

50-397/98009-02

50-397/98009-03

50-397/98009-04

VIO

failure to identify and address design requirements of a partially

elevated fuel assembly with regards to the spent fuel pool

criticality analysis

NCV

failure to perform the spent fuel and equipment pool inventories

prior to removing the RPV head

VIO

two examples of failure to properly implement procedural

requirements for testing EFC valves

t~

0

J

C5

0

-2-

50-397/98009-05

VIO

two examples of inadequate procedures for performing testing of

EFC valves

50-397/98009-06

IFI

licensee actions to address failures of the Division I EDG and

adequacy of EDG performance criteria

50-397/98009-07

VIO

failure to receive NRC approval prior to making an emergency

plan change that decreased

the effectiveness of the plan

goad

50-397/97009-02

50-397/98009-03

IFI

adequacy of foreign material controls

NCV

failure to perform the sperit fuel and equipment pool inventories

prior to removing the RPV head.

jl

LIST OF ACRONYMS USED

ABB

ECCS

EDG

EFC

ESF

FMC

FSAR

GL

HPCS

'I&C

IFI

MSRV

NCV

NRC

PER

RHR

RPV

RSE

SLC

TS

VIO

WNP-2

Asea Brown Boveri

emergency core cooling system

emergency diesel generator

excess flow check

engineered safety feature

foreign material controls

Final Safety Analysis Report

Generic Letter

high pressure core spray

instrumentation and control

inspection followup item

main safety relief valve

noncited violation

U.S. Nuclear Regulatory Commission

problem evaluation request

residual heat removal

reactor pressure vessel

rigging system engineer

standby liquid control

Technical Specifications

violation

Washington Nuclear Project-2

l

0