05000335/LER-1981-018-03, /03L-0:on 810416,after Reactor Trip Due to Transformer Failure,Block Valve VL403 for Power Operated Relief Valve Would Not Close.Possibly Caused by Tight Adjustment to Packing Gland

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/03L-0:on 810416,after Reactor Trip Due to Transformer Failure,Block Valve VL403 for Power Operated Relief Valve Would Not Close.Possibly Caused by Tight Adjustment to Packing Gland
ML17266A458
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 05/18/1981
From: Pace P
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17209B111 List:
References
LER-81-018-03L, LER-81-18-3L, NUDOCS 8105270116
Download: ML17266A458 (2)


LER-1981-018, /03L-0:on 810416,after Reactor Trip Due to Transformer Failure,Block Valve VL403 for Power Operated Relief Valve Would Not Close.Possibly Caused by Tight Adjustment to Packing Gland
Event date:
Report date:
3351981018R03 - NRC Website

text

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