05000335/LER-1981-015-03, /03L-0:on 810323,acoustic Flow Position Indicator Was Found to Be Inoperable During Routine Surveillance. Probably Caused by Transducer or Associated Cable.Spare Transducer & Cable Installed

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/03L-0:on 810323,acoustic Flow Position Indicator Was Found to Be Inoperable During Routine Surveillance. Probably Caused by Transducer or Associated Cable.Spare Transducer & Cable Installed
ML17266A445
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 04/16/1981
From: Pace P
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17209A988 List:
References
LER-81-015-03L-02, LER-81-15-3L, NUDOCS 8104270354
Download: ML17266A445 (1)


LER-1981-015, /03L-0:on 810323,acoustic Flow Position Indicator Was Found to Be Inoperable During Routine Surveillance. Probably Caused by Transducer or Associated Cable.Spare Transducer & Cable Installed
Event date:
Report date:
3351981015R03 - NRC Website

text

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A spare transducer and cable were installeci on the PORV piping to return the monitor to service and full operability.

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