05000335/LER-1980-009-03, /03L-0:on 800208,during Normal Operation,Rcs Leakage Was Determined to Be 4.38 Gpm Unidentified Leakage. Caused by Relief Valve Rv 2115 on Vol Control Tank Oscillating Open & Closed W/Charging Pump Pulsations

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/03L-0:on 800208,during Normal Operation,Rcs Leakage Was Determined to Be 4.38 Gpm Unidentified Leakage. Caused by Relief Valve Rv 2115 on Vol Control Tank Oscillating Open & Closed W/Charging Pump Pulsations
ML17266A154
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 03/07/1980
From: Schoppman M
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17207A893 List:
References
LER-80-009-03L, LER-80-9-3L, NUDOCS 8003170475
Download: ML17266A154 (2)


LER-1980-009, /03L-0:on 800208,during Normal Operation,Rcs Leakage Was Determined to Be 4.38 Gpm Unidentified Leakage. Caused by Relief Valve Rv 2115 on Vol Control Tank Oscillating Open & Closed W/Charging Pump Pulsations
Event date:
Report date:
3351980009R03 - NRC Website

text

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