ML17266A115

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LER 79-015/03L-1:on 790507,RCS Boron Concentration Was Below Tech Spec Limit.Caused by Vendor Workers Unknowingly Cutting Steam Generator During Rim Cut Mods.Tubes Plugged & Concentration Restored
ML17266A115
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 10/22/1979
From: Schoppman M
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17207A643 List:
References
LER-79-015-03L, LER-79-15-3L, NUDOCS 7912130457
Download: ML17266A115 (1)


Text

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