ML17264A484
| ML17264A484 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 05/08/1996 |
| From: | Doerflein L NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17264A480 | List: |
| References | |
| 50-244-96-01, 50-244-96-1, NUDOCS 9605170158 | |
| Download: ML17264A484 (65) | |
See also: IR 05000244/1996001
Text
U. S.
NUCLEAR REGULATORY CONMISSION
REGION I
Inspection Report 50-244/96-01
License:
Facility:
Inspection:
Inspectors:
Approved by:
R.
E. Ginna Nuclear Power Plant
Rochester
Gas
and Electric Corporation
(RGSE)
January
28,
1996 through March 23,
1996
G. Smith, Senior
P.
D. Drysdale,
Senior Resident
Inspector,
Ginna
E.
C. Knutson,
Resident
Inspector,
Ginna
S.
K. Chaudhary,
Senior Reactor Engineer,
Materials,
RI
T. A. Moslak, Project Engineer,
Branch
1, Division of
Reactor
Projects
(DRP),
RI
D.
M. Silk, Senior
Emergency
Preparedness
Specialist,
Division of Reactor Safety
(DRS),
RI
N. McNamara,
Laboratory Specialist,
DRS,
RI
J. Jang,
Senior
Radiation Specialist,
DRS,
RI
hysical
ecurity Inspector,
DRS,
RI
awrence
.
oer
ein,
e
Reactor Projects
Branch
1
Division of Reactor Projects
ate
Ins ection
Summar
Core, regional initiative, and reactive
inspections
performed
by the resident
and region-based
inspectors
during plant activities are documented
in the
areas of plant operations,
maintenance,
engineering,
and plant support.
~Resu ts:
See Executive
Summary.
9605170158
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Technical Specifications
(ITS).
No problems
were noted in the transition.
The reactor
was manually tripped from approximately
50 percent reactor
power
due to a secondary plant transient that was caused
by the loss of a main
circulating water pump.
Operator response
to this event
was very good
and the
plant was promptly stabilized in hot shutdown.
Several
emergent
maintenance
activities required the plant to remain shut
down for three days.
During the
forced outage,
operator
response
to a failed-open
atmospheric
relief valve was excellent,
and the subsequent
plant startup
was well
controlled.
However, during the outage,
inadequate
implementation, of a
temporary procedure
change to a maintenance
procedure,
and poor communications
and coordination
between the operations
and maintenance
organizations,
caused
both power operated relief valves'(PORVs)
to be inoperable
simultaneously.
The failure to properly implement the temporary procedure
change
process
was
a
violation of Technical Specification Section 5.4. 1.
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test requirement
under the old technical specifications
and required various
"tests to meet the surveillance
requirements of the ITS.
One test revealed
a
significant flow blockage in the A-train.
The cause
was determined to be
corrosion particles in the orifice of a pressure
regulating valve.
The valve
was cleaned
and A-train testing
was successfully
completed.
The licensee
determined that
an inservice test for the service water suction
check valve to the C-standby auxiliary feedwater
(AFW) pump was not performed
within the time frame required
by an
ASHE Code relief request.
Specifically,
the valve was to be disassembled
every other year during
a refueling outage.
Although the valve was disassembled
within the last two years, it was not done
during
a refueling outage.
The inspector witnessed
the subsequent
valve
disassembly
and testing.
The valve was operable
as-found,
and no significant
degradation
was'noted.
As a result of AFW system operation during the forced outage,
the A-motor
driven auxiliary feedwater
(NDAFW) pump discharge
check valve was found to
have excessive
seat
leakage.
The valve seat
and disc were replaced
and the
valve was tested satisfactorily;
however, during routine surveillance testing
a week later, the valve again demonstrated
excessive
seat
leakage.
The
licensee
determined that the cause
was
an earlier modification to the valve
body that had not been
accounted for during the previous maintenance.
The
licensee is performing
a root cause
analysis of this problem.
During an attempted
reactor startup,
operators
observed that the step counter
for control
bank
C group I did not operate.
Subsequent
troubleshooting
involved replacement
of the step counter module
and several
iterations of
11
single/multiple circuit card replacements
in the rod control cabinet.
The
problem was ultimately traced to a circuit card malfunction;
however,
troubleshooting
had
been complicated
by a second malfunction that was
introduced
by the replacement
step counter module.
The inspectors
considered
that earlier involvement by front line management
may have provided better
overall direction and
a more prompt resolution.
The A-emergency diesel
generator
(EDG) fuel oil transfer
pump recirculation
valve failed due to degradation of the solenoid operator.
The operations,
maintenance,
and engineering
departments
initiated prompt and extensive
actions to evaluate
the condition from a safety
and regulatory perspective,
and to restore the A-EDG to service
by installing a temporary modification.
A
suitable replacement for the failed valve was identified,
and expeditiously
installed
and tested.
A control
room operator noted that the two main control board instruments for
B-NDAFW pump discharge
flow were showing erratic indication shortly after the
pump was secured.
Review of archived data revealed that this type of
indication had
been occurring for both
HDAFW pumps for a long period.
The
inspectors
considered that the licensee did not initially respond aggressively
to the
8-MDAFW pump anomalous
flow indication, in that
a condition that
potentially affected the operability of a safety system
was not promptly
entered into the corrective action system.
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project has
been excellent.
A temporary work facility was erected
near the
station warehouse
to house the
new steam generators
during preparation for
installation.
Installation of the upper support ring and the preparation of
pipe nozzles for welding is in progress.
The
Lampson Transilift crane
assembly
was completed
and
a load test
was performed.
Although some welder
qualifications
have
been
behind 'schedule,
overall coordination
and preparation
for the project has
been very good
and
on time.
One channel of reactor coolant system
(RCS) average
coolant temperature
(Tavg)
and differential temperature
(hT) was indicating lower than the other three.
The
RCS loop A hot leg temperature
detector for the affected Tavg/hT channel
had
shown
some minor inconsistency
during the previous
annual calibration
check.
Subsequent
testing indicated that the detector
had drifted about 2.5'F
lower since the beginning of the current operating cycle.
Nuclear Engineering Services
performed
of the
affected reactor
protection
system
(RPS)
channel
temperatures.
The assessment
determined that the effect of the drift on the
OThT and
OPhT setpoints
was in
the non-conservative
direction, but were still within the
UFSAR limits.
The
assessment
recommended
that
a delta
T span adjustment
be, performed for the
channel to reduce the non-conservative drift effect on the calculated
values
of OThT and
OPdT.
The inspectors
concluded that nuclear engineering
services
provided timely, conservative
support in resolving the TE-401A drift.problem.
The licensee's
response
to a failure of instrument
bus inver ter A was
excellent.
The use of sophisticated
monitoring equipment
made it possible for
I8C technicians
to record
a short duration event that led to identification of
the problem.
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radioactive liquid and gaseous
effluent control programs, sufficient to
protect the publi'c health
and safety
and the environment.
The Chemistry staff
demonstrated
good knowledge
and ability.
Sufficient management
oversight
and
control
and technical attention
was directed to the monitoring program for
potential
leakage affecting the steam generator
blowdown tank and the spent
fuel pool.
The licensee
continues to maintain
a good emergency
preparedness
program.
The
emergency
plan
and emergency
plan implementing procedures
were current
and
effectively implemented.
The emergency facilities, equipment,
instruments
and
supplies
were found to be maintained in a state of readiness.
All required
1995 surveillance
were completed.
A sampling of emergency
response
organization
personnel
training records
indicated that training and
qualifications were current.
guality Assurance
Department audit reports of
the
EP program satisfied
NRC requirements;
however,
the inspectors
questioned
the independence
of the audit process.
A violation was issued for not having
procedures
to utilize the Assessment
Facility as
a radiological laboratory.
In addition, that facility and its functions
have never
been exercised
during
a drill or exercise.
The inspectors
also identified several
minor
discrepancies
between the licensee's
practices
and procedures
and statements
in the emergency
plan.
Two previously identified follow-up items were closed.
A preimplementation
review of the
SG replacement
project security program
found that the licensee's
proposed
plans
and procedure
changes
were adequate.
Safet
Assessment
ualit
Verification:
The inspectors
observed receipt
inspection of new fuel assemblies
by a licensee quality control
(gC)
inspector.
The
gC inspector identified two fuel assemblies
with bent tabs
on
their grid straps
during the receipt inspection.
The condition was not
significant enough to reject the assemblies;
a fuel vendor representative
came
to the Ginna Station to perform a repair of the tabs.
After the repair was
made,
a complete receipt inspection
was reperformed with satisfactory results
on the two assemblies.
The inspectors
reviewed the
gC records after the
receipt inspection
was completed
on all assemblies.
The documentation
was
accurate
and complete.
Overall the receipt inspection
process for the
new
fuel was thorough
and well controlled.
TABLE OF CONTENTS
EXECUTIVE SUMMARY .
TABLE OF CONTENTS
.
1.0
OPERATIONS (Inspection
Procedure
(IP) 71707)
1.1
Operations
Overview....................
1.2
Implementation of Improved Technical Specifications
.
.
.
.
1.3
Control of Operations
.
.
.
.
.
.
.
.
.
.
.
.
.
.
.
.
.
.
.
1.4
Manual Reactor Trip due to Loss of a Hain Circulating Water
P ump
1.5
Both Pressurizer
Power Operated Relief Valves Hade
During Stroke Time Adjustments
.
.
.
.
.
.
.
.
.
1.6
Failure of the A-Steam Generator
Atmospheric Relief Valve
While Shutdown
2.0
MAINTENANCE .
2. 1
Maintenance Activities (IP 62703)
.
.
.
.
.
2. 1.1 Routine Observations
2.2
Surveillance
and Testing Activities .
.
.
.
2.2.1 Routine Observations
(IP 61726)
.
.
.
2.2.2 A-Emergency Diesel
Generator
Fuel Oil
Failed Surveillance
.
.
.
.
.
.
.
.
.
2.2.3 Motor Driven Auxiliary Feedwater
Pump
Discharge
Flow
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Transfer
Pump
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Anomalous
7
7
,
7
8
8
3.0
4.0
ENGINEERING .
3. 1
(Update)
Replacement
Project (IP 50001)
3.1.1 Project Status
3. 1.2 Observations
3.2
Reactor Coolant System Average Coolant Temperature
Instrument Drift (IP 37551)
3.3
Instrument
Bus Inverter
A Failure (IP 37551)
PLANT SUPPORT
.
4. 1
Emergency
Preparedness
(IP 82701)
.
.
.
.
.
.
.
.
.
.
.
.
.
4. 1. 1 Conduct'of Emergency
Preparedness
(EP) Activities .
.
4. 1.2 Status of EP Facilities,
Equipment
and Resources
4. 1.3
EP Procedures
and Documentation
.
.
4.1.4 Staff Knowledge
and Performance
in
.
4. 1.5 Staff Training and gualification in
4. 1.6 Organization
and Administration
.
4. 1.7 guality Assurance
in
EP Activities
4. 1.8 Miscellaneous
EP Issues
.
.
.
.
.
.
.
.
.
.
.
.
.
.
.
4.2
Radioactive Liquid and Gaseous
Effluent Control
Programs
(IP 84750)
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4.2.1
Management
Controls
.
.
.
.
.
.
.
.
.
.
.
.
.
.
.
.
.
4.2.2
Review of Off-Site Dose Calculation
Manual
(ODCH)
.
.
4.2.3 Radioactive Liquid And Gaseous
Effluent Control
Programs
..
12
12
12
12
13
14
15
15
15
17
18
19
19
20
20
21
24
24
24
25
4.3
4.2.4
Blowdown Tank and Spent
Fuel
Leakages
4.2.5
NRC Assessment
and Planned
Licensee Action
4.2.6 Calibration of Effluent/Process
.
.
.
.
4.2.7 Air-Cleaning Systems
Radioactive
Waste Storage,
Processing
Systems,
and
(IP 71750)
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(SG)
Replacement
Security
Program
4.4.1 Plant Modifi'cations
.
.
.
.
.
.
.
.
.
.
.
.
4.4.2 Procedures
4.4.3 Security Organization
.
.
.
.
.
.
.
.
.
.
.
Pool
~
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~
Equi
~
~
~
pment
25
27
28
28
30
32
32
33
33
5.0
SAFETY ASSESSMENT/OUALITY VERIFICATION (IP 71707)
5.1
.Reactor
Fuel Receipt Inspection
.
.
.
.
.
.
5.2
Periodic Reports
.5.3
Licensee
Event Reports
6.0
ADMINISTRATIVE (IP 71707)
6.1
Senior
NRC Management Site Visits
6.2
Review of UFSAR Commitments
.
.
.
6.3
'Exit Meetings
.
.
.
.
.
.
.
.
.
.
ATTACHMENT 1
Attachment
1
Review of the
NERP and
33
33
34
34
35
35
35
35
DETAILS
1.0
OPERATIONS (Inspection
Procedure
(IP)
71707)'.1
Operations
Overview
At the begi'nning of the inspection period, the plant was operating at full
power (approximately
97 percent).
On March 7,
1996, the reactor
was manually
tripped from approximately
50 percent reactor
power due to a secondary plant
transient that was caused
by an automatic trip of a main circulating water
pump motor.
All engineered
safety features
equipment functioned
as required
and operators
promptly stabilized the plant in hot shutdown.
A plant startup
was performed
on March ll, 1996,
and the plant operated
at full power for the
remainder of the inspection period.
There were no other significant
operational
events or significant challenges
to plant equipment during the.
inspection period.
Overall, operator
performance
was very good during the
reporting period.
1.2
Implementation of Improved Technical Specifications
On February
24,
1996, the licensee
implemented
Amendment
61 to the operating
license for the
R.
E. Ginna Station.
The Amendment comprised
a complete
revision of Appendix A to the license which contained the Improved Technical
Specifications
(ITS) that were approved
by the
NRC on February
13,
1996.
The
ITS imposed .several
new program changes
on the licensee
(see
NRC Inspection
Report 50-244/95-21)
and required
a total of 1380 new and revised station
procedures
prior to implementation.
Prior to February
24, the inspector
verified that all necessary
new and revised procedures
were completed,
reviewed,
and approved.
On February
24, the inspector verified that all
materials
(procedures,
etc.) in the control
room pertaining to the old
technical specifications
were removed,
and that all materials pertaining to
the
ITS were in place available for use
by operating personnel.
1.3
Control of Operations
The inspectors
observed plant operation to verify that the facility was
operated
safely
and in accordance
with licensee
procedures
and regulatory
requirements.
This review included tours of the accessible
areas of the
facility, verification of engineered
safeguards
features
(ESF)
system
operability, verification of proper control
room and shift staffing,
verification that the plant was operated
in conformance with technical
specifications
and appropriate
action statements
for out-of-service
equipment
were implemented,
and verification that logs and records
were accurate
and
identified equipment status
or deficiencies.
One operational
inadequacy
occurred
when the on-shift operating
crew authorized
work that physically made
both pressurizer
power operated relief valves simultaneously
as
discussed
in section
1.5 of this report.
'he
NRC inspection
manual
procedure or temporary instruction that was
used
as inspection
guidance is listed for each applicable report section.
t
1.4
Manual Reactor Trip due to Loss of a Nain Circulating Water
Pump
The main circulating water system supplies cooling water to the main
condensers
to condense
exhaust
steam
from the'wo low pressure
turbines.
The
system consists of two headers,
each of which is supplied
by a circulating
water
(CW) pump.
Each header supplies
The headers
are
cross-connected
upstream of the main condensers
to allow for reduced
power
operations with a single operating
CW pump.
After passing
through the main
condensers,
main circulating water is returned to the lake via a common
discharge
canal.
At 6:15 p.m.
on March 7,
1996, the
B-CW pump motor tripped.
Control
room
operators
were alerted to the problem by the associated
main control board
Turbine load was rapidly reduced to approximately
50 percent in
accordance
with abnormal
procedure
AP-CW.1, "Loss of a Circulating Water
Pump."
The reduction in heat
removal
from the B-main condenser
from reduced
circulating water flow caused
an increase
in the associated
turbine
backpressure.
The low pressure
turbines
are not designed to operate at the
high backpressure
conditions that existed following the
B-CW pump trip. A
vendor-recommended
limitation of five minutes of operation applies
under high
backpressure
conditions.
The rapid power reduction, caused
(SG) water levels to decrease
(i.e., "shrink").
Although the actual
feedwater requirement
was reduced,
the
automatic
control system overcompensated
for the shrink in an
attempt to restore
normal
SG water levels,
and the water levels in both
began to rise.
Due to the response
time of the automatic feedwater control
system relative to the rate of SG water level increase,
level continued to
rise to the engineered
safety features
(ESF) feedwater isolation setpoint of
67 percent.
After several
high level
ESF isolations
had occurred
on both SGs,
levels
began to stabilize.
Although backpressure
in the B-main condenser
was
also recovering, it did not occur quickly enough to avoid exceeding
the five
minute turbine operating restriction.
At 6:22 p.m., the shift supervisor
directed that the reactor
be manually tripped.
Plant response
to the trip was
normal.
All safety
systems
and equipment
responded
as required, with the
exception of one source
range nuclear instrument channel
(N-31), which failed
to indicate after it was energized.
Operators
promptly stabilized plant
conditions in hot shutdown.
Investigation revealed that the
B-CW pump breaker
had tripped due to actuation
of the power factor relay.
The relay trip setpoint
was checked
and found to
'e
correctly set.
Inspection
and testing of the breaker
and the
B-CW pump
motor revealed
no obvious problems.
from review of available data for the
B-CW pump, the licensee
determined that the motor power factor had
been
gradually decreasing
over
a period of months.
The licensee attributed this to
development of an oxide layer at the wiper contact. for the variable
transformer that supplies
the exciter field.
This resulted
in reduced
voltage,
and therefore
reduced current supplied to the exciter and
a lagging;
motor power factor.
The licensee
determined that the likely cause of the
power factor trip had
been the gradual
decrease
in the exciter current,
combined with normal variation in the
4KV supply bus voltage.
In this case,
a
voltage incr ease
also caused
the power factor to decrease.
As corrective
3
action, the exciter variable transformer
was cleaned.
Additionally,
operations
instituted
a requirement to record
B-CW pump power factor and
exciter field current whenever
4KV bus voltage changed
by 50 volts.
This was
intended to provide early indication of a downward trend in power factor and
allow for adjustment of the exciter field current before the power factor trip
set point was approached.,
The inspectors
noted that the secondary
plant transient during this event was
significantly, different from the loss of the
B-CW pump event that occurred in
August 1995.
In both cases,
increased
backpressure
in the B-main condenser
resulted in condensate
being transferred
from the B-hotwell to the A-hotwell
via the
common header that supplies the 'condensate
pumps.
On the earlier
occasion,
the hotwell level transient resulted in a loss of net positive
suction
head
(NPSH) to the condensate
and main feedwater
pumps,
and the plant
was manually tripped based
on concern that these
pumps could be damaged
by
cavitation.
On this occasion,
NPSH was adequate
throughout the transient.
The inspectors
considered that the most likely cause of the difference
was
that power had
been
reduced
more rapidly during the recent event than it had
during the August
1995 event.
As a result, the maximum backpressure
was lower
than in the August event
and
a water, seal
was maintained
between the condenser
and the condensate
pumps suction.
No pump cavitation
was evident during this
event.
Source
range nuclear instrument channel
N-31 was required to be operable prior
to conducting
a reactor startup.
Troubleshooting
indicated that the detector
had failed.
Also, the initial replacement
detector
was found to be defective
following replacement. 's
a result,
time was available to conduct several
other maintenance activities prior to startup.
Among these activities -were
adjustment of the pressurizer
power operated relief valve
(discussed
in section
1.5 of this report)
and replacement of valve internals
for the A-motor driven auxiliary feedwater
pump discharge
CV-4009.
Following completion of planned maintenance
on the evening of
March 9,
1996, failure of the A-steam generator
atmospheric relief valve
further delayed startup; this item is discussed
in section
1.6 of this report.
Problems
encountered
with the control rod step counters during attempted
startup
(discussed
in section
2. 1. 1 of this report) delayed reactor startup
until the morning of March ll, 1996.
A reactor startup
was successfully
completed
on March 11,
1996, with
criticality being achieved at 3:54 a.m.
The main generator
was paralleled to.
the grid and power was escalated.
Full power was achieved at 9:22 a.m.
on
March 12,
1996.
The inspectors
considered that the operator's
response
to loss of the
B-CW
pump was very good.
Through discussions
with licensee
personnel
and review of
archived plant data,
the inspectors
concluded that the plant responded
normally to the reactor trip, with the exception of source
range nuclear
instrument
channel
N-31.
A four-hour non-emergency
report was
made to the
NRC
as required
by 10 CFR 50.72
and was subsequently
reported in LER 96-003
on
April 8,
1996.
Operator performance during the reactor startup
and power
escalation
was very good; communications, were precise
and actions
were
deliberate.
The inspectors
had
no additional
concerns
on this matter.
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E"
4
1.5
Both Pressurizer
Power Operated Relief Valves
Made Inoperable During
Stroke Time Adjustments
During the March 7-10 forced outage,
the licensee
performed maintenance
on the
pressurizer
power operated relief valves
(PORVs).
As discussed
in inspection
report 50-244/95-17,
the
PORV block valves
have
been closed for most of the
operating
cycle to control minor
PORV seat
leakage.
Earlier attempts to stop
this leakage
had involved mechanical
("benchset")
adjustment of the
PORVs, .
which, in turn,
had affected their stroke times.
The
PORVs also serve
as
relief valves for the low temperature
overpressure
protection
(LTOP) system
(only used while the reactor is shut
down and cooled down),
a function in
which stroke time is a critical parameter.
The purpose of the
maintenance
conducted
on March 8,
1996,
was to make adjustments
to the valves
and verify their stroke times, in preparation for placing the
LTOP system in
service during the upcoming refueling outage.
The work was to be conducted
in accordance
with maintenance
procedure
M-37.150,
"Copes-Vulcan/Blaw-Knox Air Operated
Control Valves Inspection
and
Refurbishment."
A work package
had already
been prepared to
accomplish this work during the upcoming outage.
Conducting this maintenance
with the plant at normal operating temperature
(rather than during plant
cooldown) required work in a higher temperature
environment than would
normally be the case.
To minimize the amount of time that the worker s would
have to spend in this adverse
environment,
M-37. 150 was modified to allow work
on both
PORVs simultaneously.
The procedure
involved disconnecting
the
normal'ir/nitrogen
supply from the
PORV actuator.
While the normal air/nitrogen
supply was disconnected,
operation of the
PORV from the main control board
would not possible.
Therefore,
an inadvertent result of the procedure
change
was that both
PORVs would simultaneously
be made inoperable.
Based
upon subsequent
discussions
with the licensee,
the inspectors
noted the
on-shift operations
personnel
reviewed the
PORV maintenance
package prior to
authorizing work to begin.
Operators
apparently believed,
in error, that the
maintenance
would only affect the ability to operate
the
PORVs with air,
and
that they would still be able to operate
the valves using nitrogen.
They
concluded that
PORV operability would not be affected
and authorized the work
to begin.
At approximately 2:55 p.m.
on March 8,
1996,
both
PORVs were made inoperable
when the air/nitrogen supply lines were disconnected
from the valve actuators.
The maintenance
was completed
and the air/nitrogen supply lines were
reconnected
by approximately 4:32 p.m. causing
both
PORVs to be physically
.
inoperable for a total of
1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 37 minutes.
Technical Specification
LCO 3.4.11 requires that both
be operable
in Modes 1, 2,
and 3;
and actions
required if both
PORVs are inoperable
are
1) immediately initiate action to
restore
one
2) within one hour, close
and remove
power from the associated
block valves,
and 3) within eight hours,
be in Mode
3 with Tavg less than
5004F.
The unavailability of both
PORVs above
500
F
represents
the loss of the available vent path safety function and invalidates
other assumptions
in the accident analysis for a steam generator
tube rupture.
e
The change to procedure
M-37.150 that allowed-work to be done
on both
PORVs at
the
same time was accomplished
by adding
a note to an existing temporary
procedure
change
(PCN 96-T-0055) that had
been developed
as part of the
original work package.
However, the
10 CFR 50.59 applicability review was not
reperformed.
The entire change
received
a subsequent
independent
review as
required
by A-601.3, "Procedure
Control
Temporary Changes."
According to
this procedure,
the independent
reviewer is responsible for reviewing the
10 CFR 50.59 Safety Review Form for adequacy
and completeness.
The shift
supervisor also reviewed
and approved the change;
according to A-601.3, review
responsibilities
included
a review of the temporary
change for impact on plant
operations.
However, in this case neither the independent
reviewer nor the
shift supervisor
adequately
accomplished
the review.
Technical Specification Section 5.4. 1 requires that written procedures
be established,
implemented
and
maintained covering the applicable
procedures
recommended
in Regulatory
Guide
1.33, Revision 2, Appendix A, February
1978.
Regulatory
Guide 1.33
recommends
a written administrative
procedure
covering procedure
adherence
and temporary
procedure
changes.
Administrative procedure A-601.3, "Procedure Control
Temporary Changes,"
was established
to meet this recommendation.
The failure
to properly implement procedure
A-601.3 for the temporary procedure
change for
the
PORV maintenance
is
a violation of TS Section 5.4.1
(VIO 50-244/96-01-01).
Stroke time testing
on the
PORVs was completed at approximately 5:59 p.m.
and
was immediately followed by seat
leakage testing.
The first PORV tested,
PCV-430, exhibited significant leakage
(on the order of 20 gallons per
minute).
Since the benchset
on the other
PORV (PCV-431C)
had
been similarly
adjusted,
operators
concluded that it would also
have excessive
seat
leakage;
therefore,
a seat
leakage test
was not performed
on PCV-431C.
Technical specification (TS) 3.4. 13 states
that identified leakage
from the reactor
coolant system shall
be limited to 10 gallons per minute.
Based
on this
requirement,
operators
declared
both
PORVs inoperable at 7:40 p.m.
Accordingly, power was removed from the block valves (to meet
TS 3.4. 11)
and
work was initiated to readjust
the
PORV benchsets
to their original values.
Acceptance testing
was completed
and the
PORVs were declared
operable at 1:23
a.m.,
March 9,
1996.
Both instances
of PORV inoperability were reported to
the
NRC in LER 96-003
on April 8,
1996.
The inspectors
concluded that the licensee's
preparations
for maintenance
on
the
on March 8,
1996 were not thorough.
The procedure
change that
authorized
simultaneous
maintenance
on the
PORVs did not account for the
TS
operability requirements,
and this was not identified during preparation,
approval,
or implementation of the change.
The
PORV operability problem was
recognized after the
PORVs were leak tested,
and the licensee
then took prompt
action to comply with TS
LCO 3.4. 11.
The licensee is performing
a human performance
review of this event.
However,
the inspectors
considered that
an apparent
lack of communication
and
coordination
between
the maintenance
and operations
organizations
also
contributed significantly to this event.
1.6
Failure of the A-Steam Generator
Atmospheric Relief Valve While Shutdown
During the March 7-10 forced outage,
maintenance
was performed
on the A-motor
driven auxiliary feedwater
(MDAFW) pump discharge
check valve (discussed
in
section 2.1. 1 of this report).
During the outage,
reactor
coolant system
(RCS) temperature
was being controlled by steam release
through the steam
generator
atmospheric relief valves
(ARVs).
Operators
had closed the A-main
steam isolation valve
(MSIV) and were controlling
RCS temperature
using only
the
B-SG and
B-MDAFW pump, since the work isolation for the check valve
maintenance
made adding feedwater .to the A-SG difficult.
At 9:20 p.m.
on March 9,
1996,
when resto} ing from the
A-MDAFW pump
maintenance,
operators
attempted to establish
steam flow in the header
and
slightly opened the A-SG ARV to assist
in opening the A-MSIV.
However, rather
than opening slightly, the
ARV failed open to. approximately
60 percent.
After
the valve opened,
controls
on the main control 'board
had
no further affect on
valve position.
RCS temperature
and pressure,
and
SG water levels, all began
to lower.
Level in the A-SG was initially low (22 percent)
due to no
feedwater addition during the
AFW pump maintenance,
and reached
the
17 percent
low level
ESF setpoint approximately three minutes into the event.
This
generated
a reactor trip signal (all rods were already fully inserted)
and
caused
an automatic start of the non-operating
B-MDAFW pump.
Operators
responded
to the event
by shutting the A-MSIV and dispatching
an
auxiliary operator
(AO) to manually isolate the A-ARV.
Two AOs responded;
one
begari to shut the manual isolation valve while the other attempted to close
the
ARV using its manual
operator.
The isolation valve was fully closed in
approximately
3$ minutes
and stopped
the steam release.
As a result of this transient,
RCS temperature
dropped
approximately
15 degrees
Fahrenheit ('F),
RCS pressure
dropped
approximately
120 psi,
and
water level in the A-SG reached
approximately six percent.
The low level in
the A-SG made the A-RCS loop inoperable for heat removal.
Technical
Specification
LCO 3.4.5 allows 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> to restore operability,
and the
A-RCS
loop was restored to operability at 9:40 p.m.
when
SG water level
was returned
to zl6 percent.
The cause of the A-SG ARV failure was determined to be
a failed air system
volume booster relay that translates
the control air signal into operating air
for the valve.
The relay was replaced,
and the
ARV was returned to service
on
March 10,
1996.
The inspector
was in the control
room throughout this event
and assessed
that
operator
response
was excellent.
Control
room operators rapidly determined
the cause of the transient
and took action to isolated the fault by shutting
the A-MSIV and dispatching operators.
The AOs responded
quickly into an
extremely harsh
noise environment
and rapidly isolated the failed ARV.
A
four-hour non-emergency
report was
made to the
NRC as required
by 10 CFR 50.72
and was subsequently
reported in LER 96-004
on April 8,
1996.
The inspectors
had
no additional
concerns
on this matter.
2.0
NAINTENANCE
2.1
Naintenance Activities (IP 62703)
, 2.1.1 Routine Observations
The inspectors
observed
portions of plant maintenance activities to verify
that the correct parts
and tools were utilized, the applicable industry code
and technical specification requirements
were satisfied,
adequate
measures
,were in place to ensure
personnel
safety
and prevent
damage to plant
structures,
systems,
and components,
and to ensure that equipment operability
was verified upon completion-of post maintenance
testing.
The following
maintenance activities were observed:
~
Hydrogen recombiner
corrective maintenance
Prior to implementing
Improved Technical Specifications
(ITS) at the
Ginna Station
on February
24,
1996, the licensee
required that all
surveillance tests
included in the
ITS be current.
Since the
containment
hydrogen recombiners
did not have
a surveillance test
requirement
under the old technical specifications,
these
systems
needed
a 24 month functional test to meet surveillance
requirements
SR 3.6.7. 1
and
SR 3.6.7.2 of the ITS.
Several
functional tests
were performed
on the A- 5 B-recombiner
system
trains before February 24,
1996.
One test revealed
a significant flow
blockage in the A-train that caused
flow to be less than the system's
minimum requirements.
The inspectors
observed
the troubleshooting
and
disassembly of portions of the A-train components.
After identifying
the blocked region
as
an orifice near pressure
regulating valve V-10200,
approximately one-half cup of iron oxide particles
was removed
when the
valve was disassembled.
After the system
was restored,
the A train was
successfully flow tested.
All maintenance
and testing
on the
recombiners
was well controlled
and the procedures
used for these
activities were available
and followed.
Operations
personnel
made the
necessary
systems
isolations
and tagouts with independent verifications
for=-the maintenance
and test work.
'
C-standby auxiliary feedwater
(SAFW) pump service water check valve
CV-9627A inspection for missed
IST observed
on February
23,
1996
On February
15,
1996, the licensee
determined that
an inservice test for
. check valve 9627A was not performed in the time frame identified in a
relief request
(VR-5) for ASME Code,
Section
IX test requirements
(See
section
5.3 of this report).
The valve is in the service water suction
line to the
C-SAFW pump,
and the required inspection involves
disassembly
and full stroke exercising the valve every other refueling
outage.
The inspectors
witnessed
the valve disassembly
and testing
activity on February
22,
1996.
A small
amount of silt was noted
around
the ledge of the valve seat
and at the bottom of the valve body.
However, it did not appear
that the amount of material
present
would
have prevented full valve closure.
The licensee
exercised
the valve
disk and observed
freedom of motion through its complete range.
The
valve disk was then blue checked
and full seat contact
was confirmed.
The valve was reassembled
and properly torqued in accordance
with
procedure
requirements.
All portions of this work were performed in the
presence
of a
gC inspector
and all inspection verifications were
properly made.
The valve was subsequently
restored to operability.
The
inspectors
concluded that this work was timely and well controlled in
accordance
with procedure
requirements.
~
pump discharge
check valve CV-4009 final bonnet
torquing,
observed
on March 9,
1996
AFW system operation during the March 7-10 forced outage revealed that
the
A-HDAFW pump discharge
CV-4009,
had excessive
seat
leakage.
The valve seat
and disc were replaced
and the valve was tested
satisfactorily
on March 9,
1996;
however,
on March 20,
1996, during
routine surveillance testing,
the valve again demonstrated
excessive
seat
leakage.
During rework, the licensee
determined that the cause
was
that
an earlier modification to the valve body in the area that accepts
the seat ring had not been
accounted for during the March 9 maintenance,
and the seat ring in the replacement
valve internals
was not modified.
This resulted
in an improper reassembly that caused
the test failure on
March 20.
The licensee is performing
a root cause
analysis
(AR 96-0172)
of the CV-4009 maintenance
problems.
(IFI 50-244/96-01-02).
~
Control rod step counter troubleshooting,
observed
on March 10,
1996
During an attempted reactor startup,
operators
observed that the step
counter for control
bank
C group
1 did'ot operate.
Replacement of the
counter module failed to correct the problem.
Subsequent
troubleshooting
involved several
iterations of single
and multiple
circuit card replacements
in the rod control cabinet.
The problem was
ultimately traced to a circuit card malfunction;
however,
troubleshooting
had
been complicated
by a second malfunction that was
introduced
by the replacement
step counter module.
Correction of this
problem delayed the reactor startup
by approximately
one day.
The
technicians
demonstrated
a high level of technical
competence;
however .
their initial troubleshooting efforts lacked
a systematic
approach to a
resolution of the root cause
and resulted, in a time delay (approximately
24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />) in restarting the reactor plant.
System engineering
and
maintenance
management
eventually
became
involved in the troubleshooting
efforts and
a prompt resolution
was achieved.
The inspectors
considered
that earlier involvement by system engineering
and maintenance
management
may have provided better overall direction,
a more systematic
approach to the troubleshooting,
and
a more prompt resolution.
2.2
Surveillance
and Testing Activities
2.2.1 Routine Observations
(IP 61726)
Inspectors
observed
portions of surveillances
to verify proper calibration of
test instrumentation,
use of approved
procedures,
performance of work by
qualified personnel,
conformance to limiting conditions for operation
(LCOs),
I'
,4
0
9
and correct post-test
system restoration.
The following surveillances
were
observed:
~
M-72. 1. 1, "Reactor Coolant
Loop
RTD [Resistance
Temperature
Detector]
Integrity Check," observed
February 7,
1996
Testing of loop A average
temperature
(Tavg) hot leg (Th)
RTD, TE-401A,
performed
because
the associated
instrument
was indicating lower than
the three other channels.
This item is discussed
further in section 3.2
of this report.
~
Performance
Test (PT)-12.2,
B," observed
February
15,
1996
~
Instrument Calibration Procedure
(CPI)-SPAN-5.10, "Calibration Alignment of
Delta T Dana Amplifier at
70X Power or Greater,
Channel
1,
Loop A,"
observed
February
15,
1996
Performed to compensate
for drift in Tavg/hT
RTD element
TE-401A,
as
discussed
in section 3.2 of this report
~
PT-32A, "Reactor Trip Breaker Testing
"A" Train," observed
March 1,
1996
Included troubleshooting for R-29 (containment
high range radiation
monitor) spiking, noted during previous reactor'trip breaker testing;
troubleshooting
is on-going
~
PT-169-B, "Auxiliary Feedwater
Pump
B quarterly," observed
March 9,
1996
Partial, retest for the CV-4009 repairs
~
PT-6.2,
"N.I.S.
[Nuclear Instrumentation
System]
Intermediate
Range
Channels
N-35 and N-36," observed
March 9,
1996
N-35 calibration check
The inspectors
determined
through observing the above surveillance tests that
operations
and test personnel
adhered to procedures,
that test results
and
equipment operating
parameters
met applicable
acceptance
criteria,
and that
redundant
equipment
was available during testing for emergency operation.
2.2.2 A-Emergency Diesel Generator
Fuel Oil Transfer
Pump Failed Surveillance
On February
1,
1996, during quarterly in-service
(ASME Section XI) performance
testing
(PT-12.6,
"Diesel Generator
Fuel Oil Transfer
Pump Tests"
of the
A-Emergency Diesel
Generator
(EDG) fuel oil transfer
system,
the fuel oil
transfer
pump failed to achieve the required discharge
pressure
and flow (16
psig
and 23.27
gpm achieved;
vs. 17.7-20.9 psig and 25.8-29.9
gpm acceptable).
As a result, the
A-EDG was declared
placing the plant in a seven
day Limiting Condition for Operation
(LCO).
Subsequent
troubleshooting
by
operations
and maintenance
personnel
concluded that the apparent
cause of the,
pump's low discharge
pressure
was failure of the
pump recirculation valve
10
SOV-5907A to tightly close, resulting in pressure
and flow losses
during
filling of the day tank.
Since the failed valve was original plant equipment
and
a replacement
was not
readily available,
operations
and engineering
evaluated
the impact on plant
safety
and
A-EDG reliability.
As a precautionary
measure,
the fuel oil
transfer
system
was temporarily modified by securing
SOV-5907A in the open
position.
In this configuration, flow to both the day tank and fuel storage
tank (recirculation flow) will result when filling the day tank.
This
condition is acceptable
since the positive displacement, transfer
pump can
still deliver the minimum required flow to the day tank (>2.62 gallons per
.
minute,
as stated in the Updated Final Safety Analysis Report,
section 9.5.4).
'o
confirm adequate
flow, PT-12.6
was performed following deenergizing
the
valve;
a discharge
pressure
of 15 psig and
a flow of 20'.23
gpm were obtained.
Accordingly, the
A-EDG was'eturned
to service
on February 3,
1996.
Prior to performing this reconfiguration,
the proposed
Permit (96-007)
and supporting Safety Evaluation
(SEV 1059) were reviewed
and
approved
by system engineering,
operations,
and the Plant Operations
Review
Committee
(PORC).
Reconfiguring
was considered
precautionary
since it was
postulated that the degraded
valve could cause
an electrical failure that
could fail the control fuses
and disable the entire 'A-EDG fuel oil transfer
system.
The temporary modification disconnected
the power leads for
SOV-5907A, isolated the valve from the control circuit, and eliminated the
possibility of fuse failure due to coil degradation.
To reestablish
A-EDG
operability, the licensee
used guidance contained in Generic Letter 91-13,
Technical
Guidance
9900 "Operability."'here the
ASME Section
XI acceptance
criteria is more conservative
than the regulatory limit, this guidance states
that the corrective action
may be
an analysis to demonstrate
that the specific
degradation
does not impair system operability and the component will still
fulfillits function.
The licensee
purchased
a commercial
grade replacement
valve since
an identical
valve was
no longer manufactured.
Therefore,
the dedication
process
was
used
to qualify the replacement
valve and the solenoid operator.
Procurement
engineering
completed
a comparative analysis,
establish
valve performance
requirements,
and identified the critical attributes that the quality
assurance
department
would verify prior to accepting
the replacement
valve for
installation.
Receipt inspection of the part number, voltage,
power. rating,
dimensions,
and coil resistance
was to provide assurance
that the item ordered
was the item received.-
On February
13,
1996, the failed valve
(ASCO model
8210A35)
was replaced with
an
ASCO model
HC8210C35.
The inspector
observed
the installation of the
replacement
valve and post-installation testing of the fuel oil transfer
system.
Relevant documentation
reviewed included the work package,
commercial
grade dedication technical evaluation for the replacement
valve
(TE 96-505),
temporary modification permit, tagging order (to remove the system from
service),
ACTION report,
and
UFSAR section 9.5.4.
Mechanical
maintenance
personnel
installed the valve in a professional
manner,
using foreign material
exclusion controls
on open piping, complying with
11
procedural
requirements for bolt tightening, flange fit-up and closely
coordinating procedural
hold point verifications with the quality control
inspector.
I&C technicians
reterminated
solenoid wiring with the control
circuit using skill-of-the-craft techniques.
Following installation,
Results
and Test
(R&T) technicians
had operations
personnel
realign the system. for
testing.
Testing
was conducted
in conformance with the test procedure
and
system performance
parameters
met acceptance criteria.
Although the performance criteria of PT-12.6 were met during post-installation
testing, during system recirculation,
high pump discharge
pressure
(44 psig)
caused
the system relief valve
(RV-5959) to lift. This condition did not
compromise
system operability; however, it indicated that SOV-5907A had
been
in a degraded
condition (that is, not fully closing) prior to the IST baseline
parameters
for the
FO transfer
pump being established
in 1992.
An ACTION
report (96-0088)
was generated
to document
and resolve this condition.
Subsequent
to returning the fuel oil transfer
system to service,
the inspector
interviewed the procurement
engineer regarding the commercial
grade dedication
of the replacement
valve.
Through this discussion,
the inspector determined
that
a prompt and thorough evaluation
was completed for suitable
replacement
components.
The engineer
adhered to the relevant engineering
and
administrative
procedures
in establishing critical valve performance
attributes
and by identifying quality control receipt inspection criteria.
Additionally, the inspector interviewed the cognizant
system engineer
regarding installation of the temporary modification following the initial
valve failure.
Through this discussion
and review of the supporting
documentation,
the inspector concluded that the fuel oil transfer
system
was
capable of performing its intended safety function following deenergizing
SOV-5907A.
Upon identifying that
SOV-5907A had failed, prompt and extensive
actions
were initiated by the operations,
maintenance,
and engineering
departments,
to evaluate
the condition from a safety
and regulatory
perspective,
to restore the A-EDG to service
by installing a temporary
modification, to qualify a suitable
replacement for the failed valve,
and to
expeditiously install/test the replacement.
These activities were effectively
coordinated with appropriate
management
and
gA oversight.
2.2.3 Notor Driven Auxiliary Feedwater
Pump Anomalous Discharge
Flow
On February
12,
1996, the licensee
performed monthly surveillance testing
on
the
B-MDAFW pump.
Approximately one-half hour after the
pump was secured,
a
control
room operator
noted that the two main control board instruments for
B-MDAFW pump discharge
flow were showing erratic indication.
The operator
documented
the condition in a work request/trouble
report
(WR/TR 013045).
The following day, the inspector noted the
WR/TR concerning the
8-MDAFW flow
indication.
The inspector
reviewed archived data from the plant computer
and
noted that,
although erratic,
both flow instruments
showed the
same pattern at
the
same time.
About one-half hour after the
pump was stopped,
flow went from
zero to about
25 gallons per minute for about
20 minutes,
and then returned to
zero.
The inspector considered
that this indicated that flow had actually
occurred,
as
opposed to the condition being the result of coincident
12
~
~instrument failures.
The inspector discussed
this situation with the
licensee,
and the licensee initiated an ACTION report (96-0086) to investigate
the problem.
Further
review of archived data
by the licensee
revealed that the
same
indications that were observed
on February
12,
1996,
had been occurring for at
least several
months with both
MDAFW pumps.
The licensee
assessed
this
condition as not affecting
MDAFW pump operability.
At the close of the
inspection period, the licensee
planned further investigation of this
condition, to be performed during normally scheduled
surveillance testing.
The inspectors
considered that the licensee did not initially respond
aggressively to the
B-MDAFW pump anomalous
flow indication, in that
a
condition that potentially affected the operability of a safety system
was not
promptly entered into the corrective action system.
Subsequent
licensee
actions
appeared
to be appropriate,
and the licensee's
corrective action
process'ill track the condition through appropriate resolution.
3.0
ENGINEERING
3.1
(Update)
Replacement
Project (IP 50001)
3.1.1 Project Status
RGKE's project to replace
both steam generators
(SGs) during the next
refueling outage (April 1996) is currently on schedule
and onsite preparation
activities are ongoing.
Overall, the project continues to be well managed
and
coordinated
between
RGKE and Bechtel.
3.1.2 Observations
The inspectors
reviewed documentation
and observed
various phases of the
preparation for the replacement of the steam generators,
including
reinstallation of liner on the training mockup, training of welders
on the
automatic welding machine, qualification of the "cadweld" rebar splicing
process
and crews, splice installation,
and receipt inspection of both new
at the site.
The inspectors
observed
the following activities:
~
The welding of the liner reinstallation in the "mockup" had not been
completed;
however, welding of two sides
had been finished.
The two
radiographs
on the completed
weldments disclosed
some rejectable defects
(lack of fusion) in the root, although the fit-up appeared
satisfactory.
The licensee
was in the process of evaluating
and resolving the discrepancy
and developing
a fix to eliminate
such defects
from the liner welding
process.
~
The inspectors
observed
the training of welders
on automatic welding
machines.
There were six machines onsite.
Five out of the six were being
used for training and one was kept as
a backup.
Ten crews of three persons
each
were being trained
on the machine in two shifts.
13
~
Eight cadweld splicers
had
been qualified.
Each splicer had made two
splices in horizontal,
and two splices in vertical/slope position.
The
qualification splices
had been visually examined
by Bechtel quality control
(gC)
and the vendors representative/trainer,
and were found acceptable.
The inspectors
observed
the tensile testing of the splices
in the onsite
universal testing machine.
All the tested splices
met or exceeded
the
acceptance
criterion of the splices.
~
Both new steam generators
were delivered to the site
on January
7 and 17,
1996.
A temporary work facility was erected
near the station warehouse to
house the generators
during preparation for installation.
The steam
generators
were receipt inspected,
and installation of the upper support
ring a'nd the preparation of pipe nozzles for welding is in progress.
~
The Lampson Transilift crane
assembly
was completed
and
a load test
was
performed
on March 21-22,
1996.
The test load was 440 tons,
and the load
was raised
and lowered through the full range of the main
boom and over the
path that will occur
when the steam generators
are lifted.
The inspectors
observed
the operation of the crane during the load test,
and the survey of
the crawlers
and main
boom while under load.
The test
was satisfactory
and
no deficiencies related,to
the crane
assembly
were noted.
The inspectors
concluded that. the licensee's
planning, preparation,
and
related activities in the area of engineering
and construction well support
the steam generator
replacement
in the coming refueling outage starting
April 1,
1996.
Overall,
RG&E's management of the steam generator
replacement
has
been excellent.
Although some welder qualifications
have
been
behind
schedule,
overall coordination
and preparation for the project has
been very
'ood
and
on time.
3.2
Reactor Coolant System Average Coolant Temperature
Instrument Drift
(IP 37551)
Over
a period of several
months,
operators
noted that one channel of reactor
coolant system
(RCS)
average
coolant temperature
(Tavg)
and differential
temperature
(dT) was indicating slightly lower than the other three.
This was
a potential operational
concern
because
Tavg is used
as
an input to the
automatic rod control system,
and potentially affected the reactor protection
system
(RPS)
as well.
Tavg and
hT are inputs for determining the
overtemperature
and overpressure
differential temperature
(OThT and
OPhT)
setpoints.'nstrument
and Control
(I&C) personnel
investigated
the condition and noted
that the
RCS loop A hot leg temperature
detector
(TE-401A) for the affected
Tavg/hT channel
(RPS channel
1) had
shown
some minor inconsistency
during the
previous
annual calibration check.
Although the detector
had
been within
allowable tolerance,
they had initiated action to replace
TE-401A during the
next refueling outage.
To assess
the detector's
current condition,
technicians
performed precision
measurements
of the
RCS loop A Tavg
RTDs per
M-72.1.1,
"Reactor
Coolant
Loop
RTD Integrity Check."
This test
showed that
TE-401A was indicating about 7.0oF lower than the other loop A Tavg hot leg,
RTD (TE-405A).
Testing at the beginning of the operating cycle showed that
P
14
TE-401A indicated
about 4.54F lower than TE-405A; therefore, it was concluded
that TE-401A had drifted about 2.5'F lower since the beginning of the
operating cycle.
Nuclear Engineering Services
performed
an operability a'ssessment
of the
channel
1 temperatures.
The assessment
determined that the effect of the
TE-401A drift on the
OThT and
OPhT setpoints
was in the non-conservative
direction, but that the resultant
values
were still within the
UFSAR limits.
The assessment
concluded that channel
1 OThT and
OPhT were still operable
and
that
an existing
MCB alarm (annunciator
F-24),
"RCS Delta T Deviation 3'F,"
should
be used to indicate that the limiting acceptable
value of drift had
been reached.
The assessment
further recommended that
a delta
T span
adjustment
be performed for RPS channel
1.
This would not affect the
temperature
indication provided by TE-401A, but would reduce the
non-conservative drift effect from the calculated
values of OThT and
OPhT.
The calibration
was satisfactorily performed
on February
15,
1996.
The inspectors
reviewed the licensee's
assessment
of the
RPS channel
1
temperatures
and evaluation of OThT and
OPhT setpoint margin,
and noted
no
discrepancies.
To further assess
the licensee's
evaluation of instrument
drift, the inspector
reviewed design analysis
DA-EE-95-0109, "Evaluation of 24
Month Instrument Surveillance Intervals."
The licensee
performed this design
analysis to provide justification for extending surveillance intervals in
support of an
18 month operating cycle.
The design analysis
was performed
pursuant to the guidance of Generic Letter 91-04,
"Changes
in Technical
Specification Surveillance Intervals to Accommodate
a 24-Month Fuel Cycle."
The inspector
noted that the licensee's
method for projecting instrument drift
was different than the methods
contained
in Instrument Society of Americ'a
(ISA) Standard
S67.04,
"Setpoints for Nuclear Safety-Related
Instrumentation."
Conformance to this standard is not
a requirement;
however,
in most cases that
the inspector reviewed,
the licensee's
method
was adequately
conservative for
assessing
instrument drift.
The inspector
concluded that nuclear engineering
services
provided timely,
conservative
support in resolving the TE-401A drift problem.
TE-401A will be
replaced during the
1996 refueling outage.
The inspectors
had
no additional
concerns
on this matter.
3.3
Instrument
Bus Inverter
A Failure (IP 37551)
At 2:23 p.m.
on March 12,
1996,
a failure of instrument
bus inverter
A
occurred.
Operators
were alerted to the condition by MCB annunciator
E-3,
"Inverter Trouble."
As designed,
power transferred
automatically through the
automatic static transfer switch to the associated
constant voltage
transformer,
so power to instrument
bus
A was not lost.
Failure of the A
inverter placed the licensee
in a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> shutdown action statement
per TS 3.8.7.
Investigation revealed that the inverter output fuses
had blown and that there
were
numerou's failed solid state electrical
components
in the inverter,
including diodes
and silicon controlled rectifiers
(SCRs).
The damaged
components
were replaced
and the inverter operated satisfactorily;
however,
15
after about
45 minutes,
the output fuses
blew again.
During subsequent
troubleshooting,
a vendor representative
noted that the inverter output
voltage
was slightly high.
This was due to a group of capacitors
whose
capacitance
had decreased
with age,
together with other capacitors that were
replaced during the
1995 refueling outage.
By the vendor,'s direction, the
total capacitance
was reduced to reduce the output voltage.
This appeared
to
correct. the problem,
and the inverter was declared
operable at 10:29 p.m.
on
March 14,
1996.
However, at 10:48 a.m the following day, the inverter failed
.
again.
The licensee
reentered
TS action statement
3.8.7 with 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br />
and
54 minutes of the original
72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> remaining.
Through the use of sophisticated
monitoring equipment during subsequent
troubleshooting,
ILC technicians
were able to capture
and record
an event in
which inverter output frequency went from 60 Hz to 120
Hz and inverter current
doubled.
The cause of this event
was traced to a defective integrated circuit
(IC) chip on an oscillator board.
The oscillator board
was replaced
and the
inverter operated satisfactorily.
Inverter
A was declared
operable at 2:11
a.m.
on March 16,
1996, with 31 minutes remaining in the action statement.
'he
problem with inverter A was determined to be the defective
IC chip that
was randomly initiating the inverter startup
sequence.
The inverter
initially'tarts
up with a 120
Hz output
(60 Hz during normal operation)
and does
so by
doubling the normal
SCR firing rate.
The resultant
high current
when this
occurred during normal operation
caused
the inverter output fuses to blow.
Shop testing later demonstrated
that the problem was temperature
induced.
This complicated troubleshooting,
which was performed with the cabinet
open
and therefore at relatively cool temperatures.
An earlier attempt to use
infrared thermography for troubleshooting
had
shown the chip to have
a "hot
spot," but it was not recognized
as the source of the problem, partly because
there
was
no baseline
information to compare it to.
The inspectors
considered that the licensee's
response
to the inverter A
failure was e'xcellent with very good management
direction and involvement.
The vendor was promptly consulted
and appropriately utilized during the
extensive troubleshooting effort.
The use of sophisticated
monitoring
equipmeht
made it possible for 18C technicians to record
a short duration
event that led to identification of the problem.
The inspector
had
no
additional
concerns
on this matter.
4.0
PLANT SUPPORT
4.1
Emergency
Preparedness
(IP 82701)
4.1.1 Conduct of Emergency
Preparedness
(EP) Activities
The inspectors
reviewed the, effectiveness
of various licensee controls to
maintain
and manage
the
EP program.
The inspectors
conducted
interviews,
reviewed documentation,
and investigated specific activities to assess
this
aspect of the licensee's
performance.
The inspectors
reviewed the licensee's
efforts associated
with the
EP support
to the steam generator
replacement
project
(SGRP).
Prior to this inspection,
16
the inspectors
reviewed
an inter-office memo from the Onsite
Emergency
Planner
(OEP) to the Corporate Nuclear
Emergency
Planner
(CNEP),
Manager
Nuclear
Assessment
(MNA), and the Radiation Safety Communications
Coordinator that
discussed
several
contingencies
which were planned for EP's
involvement in the
SGRP.
The contingencies
addressed
scenarios
including a fire,
a radioactive
release,
mass casualty,
drop,
a'dverse
weather,
isolating
containment penetrations,
and loss of electrical
power.
The licensee's
planning for these contingencies
included procedures,
equipment
and
facilities, personnel,
and offsite support.
The inspectors
concluded that the
licensee
was proactive in this effort and
had properly considered
and
satisfactorily planned'to
support the
SGRP effort.
The inspectors
reviewed the licensee's
1996 business
plan (dated
March 1,
1996)
and identified several
EP projects that were included.
The plan
includes
such items
as developing joint EP capabilities with other utilities,
benchmarking
the Nuclear
Emergency
Response
Plan
(NERP) public information
program, utilizing an auto-dial
system for off-hour call-outs,
supporting the
SGRP,
implementing
a severe
accident
management
program,
conducting "train the
trainer" sessions
for Nuclear
Emergency
Response
Plan
(NERP) instructors,
and
improving the process for tracking
NERP responder qualifications.
Based
upon
the review of the business
plan, the inspectors
concluded that licensee
management
has
addressed
EP functions
and needs
in its plan.
The inspectors
reviewed the Commitment
and Action Tracking System
(CATS) and
the
EP items currently in the system.
There were
15 open items (nine were
from the December
1995 exercise)
and none were overdue.
All items were
assigned
to the low priority status,
except for
an item- about the Reactor
Vessel
Level Indicating System.
The inspectors
agreed with the assigned
priorities and
had
no concerns
or questions
regarding the use of CATS for EP
items.
The inspectors
reviewed the licensee's
activities regarding
a licensee-
identified problem pertaining to its call-out drills.
The call-out drills
implement three
Emergency
Plan Implementing Procedures
(EPIPs)
(1-5,
Notifications (Onsite); 3-6, Corporate Notifications;
and 4-5, Public Affairs
Notifications) to notify responders
via a telephone tree.
During the last
NRC
inspection of the licensee's
EP program (Inspection
Report
No. 50-244/95-10),
the licensee
was modifying its'otification process
to place one-hour
responders
earlier in the telephone tree
so that they could meet the one hour
response
goal.
Since that inspection,
the licensee
conducted
three quarterly
call-out drills without fully satisfying all of the intended objectives.
In
each drill, there
was
a different reason for not meeting the drill objectives.
In one, certain responders
exceeded
the one hour goal
by several
minutes
and
in the others,
portions of the telephone tree were not completed
due to a mis-
communication
and
an individual failing to follow procedures.
The inspectors
did not- consider these failures to be individually significant, but were
concerned that the licensee
continues to be unsuccessful
in meeting objectives
for this drill.
The licensee
plans to implement
an auto-dialer
system before
the end of 1996 to notify the responders
in a more timely and reliable manner.
This will be reviewed in a future inspection (IFI 50-244/96-01-03).
'
17
The inspectors
concluded that the licensee
was actively involved in the
function.
Sufficient controls were implemented to monitor and assess
EP group
performance.
The
EP group is responsive
to assigned
CATS items
and was
appropriately self-critical regarding the call-out drill problems.
Overall,
-the licensee's
performance
in this area
was assessed
as satisfactory.
4. 1.2 Status of EP Facilities,
Equipment
and Resources
The inspectors
conducted
an audit of emergency
equipment in the Station
Control
Room, Technical
Support Center
(TSC), Operations
Support Center
(OSC),
Survey Center
(SC), Assessment
Facility (AF) and
(EOF).
The inspectors
also reviewed records of various equipment inventory
activities
and test surveillances
conducted during the past year
and reviewed
the capabilities of the licensee's
communication
system.
The inspectors
checked
several
emergency
equipment kits and emergency
cabinets
in the emergency facilities and found them to be appropriately stocked
as
directed
by the licensee's
procedures.
The inspectors verified that survey
meters,
personnel
dosimetry
and respirator canisters
were calibrated
and were
operationally ready.
The inspectors
reviewed equipment inventories
and surveillance
test reports
for 1995
and determined that equipment inventories
were conducted
at specified
frequencies
and checklists
were properly completed
and reviewed.
Inventory
lists included identified deficiencies
and .corrective actions
were well
documented.
While touring the
EOF, the inspectors
examined the survey team closet that
contained radiological instrumentation,
thermoluminescent
dosimeters
(TLDs)
and field emergency kits. It was noted that five TLDs used for survey team
members
were in close proximity to an unshielded
Cs-137 radioactive point
source
used for instrument
response
checks.
The inspectors
discussed. with the
licensee
the potential
exposure
to the TLDs from the point source,
possibly
causing
erroneous
dose results.
The licensee
committed to placing the point
source in a lead shield to prevent exposing the TLDs while in storage.
The Assessment
Facility (AF) is located in the licensee's
Training Center
East.
It has
a sample preparation
laboratory
and
a counting laboratory with a
whole body counter,
an alpha/beta
gas flow proportional
counter
and
a high
resolution
gamma spectrometry
system with two detectors.
The AF is routinely
used
as
an envir'onmental
laboratory during normal plant operations.
However,
in accordance
with the Nuclear
Emergency
Response
Plan
(NERP), Section 6.3.9,
the AF is to be used for receiving
and analyzing environmental
samples
collected
by field survey teams during an emergency
and, per Section 4.3.12,
serves
as
a backup laboratory for analyzing post-accident
sampling
system
(PASS)
samples, if the in-plant laboratory should
become inaccessible.
In
discussions
with members of the chemistry department,
the inspectors
determined that, while the licensee's
instrumentation
in the AF is calibrated
to analyze
a
PASS sample,
there were no procedures for activating this
facility as
a radiological laboratory during an emergency
nor were there
procedures for analyzing radioactive
samples
in the AF.
Further discussions
with the
OEP revealed that the following activities have never
been exercised
0
18
at*the AF in an emergency drill:
1) transporting potentially contaminated
offsite environmental
samples
from the
SC to the AF; 2) analyzing offsite
samples;
and 3) handling, transporting
and analysis of a
PASS sample.
The
lack of procedures
and failure to exercise this facility are violations of
and
(14) which require emergency facilities and
equipment
be provided
and maintained,
and periodic exercises
be conducted to
evaluate major portions of the emergency
response
capability.
(VIO 50-244/96-01-04).
The inspectors
reviewed the licensee's
communication
system capabilities
by
interviewing the Manager,
Communications
Design
and Support.
The purpose of
the interview was to obtain additional information for NRC evaluation
on the
communication
systems
and to follow-up on. information gathered
during the
previous
EP program inspection.
The licensee's
system
appeared
to be
sufficiently redundant to ensure that
a communication link could be maintained
with offsite agen'cies
during severe
natural conditions.
The CNEP's
and OEP's direct program oversight
has resulted in an excellent
equipment inventory and surveillance test program.
With the exception of the
violation regarding the AF, the emergency facilities and equipment
were
maintained in a state of operationally readiness.
4.1.3
EP, Procedures
and Documentation
The inspectors
reviewed recent
NERP and
EPIP changes
to assess
the impact on
the effectiveness
of the
EP program.
The inspectors
also assessed
the process
which the licensee
uses to review EPIPs
and changes
made to them.
The inspectors
reviewed recent
changes
to the licensee's
NERP and
and
determined that the changes
did not reduce the effectiveness
of the program.
The inspectors
randomly selected
an
EPIP that had
been
changed
and reviewed it
against the licensee's
10 CFR 50.54(q) review process,
as well as the process
described
in administrative
procedure
A-205.2,
"Emergency
Plan Implementing
Procedures
'Committee."
The inspectors
found that the licensee
also performs
a
10 CFR 50.59 safety review for procedure
changes.
No problems
were
identified.
The inspectors
also reviewed
NERP and
EPIP changes
in the regional office.
Those are listed in Attachment
1.
The inspectors
determined that none of the
changes
decreased
the effectiveness
of the
NERP.
The inspectors
also reviewed the frequency of NERP and
EPIP reviews against
Section 7.2 of the
NERP, Annual
Review and Revision of the Plan
and Procedures
and A-601.4,
"Procedure
Control - Periodic Review."
The inspectors verified
that the licensee
conducts
annual
reviews of the
NERP and that
PORC has
reviewed the EPIPs within a five year period.
However, the inspectors
identified that the wording in the
NERP was misleading with respect to the
frequency of EPIP reviews
and should
be clarified,to reflect the intended
review cycle.
The licensee
agreed.
19
The licensee's
NERP and
EPIPs are sufficient to implement the
EP program.
The
changes
made to those
documents
and the change review process
were acceptable.
Overall, this area
was assessed
as satisfactory.
4.1.4 Staff Knowledge and Performance
in EP
The
CNEP and
OEP have two opportunities annually to broaden their
experiences.
Both had recently visited other licensees
to participate in
audits
or peer evaluations
and
had attended
industry seminars pertaining to
to maintain their proficiency.
The inspectors
interviewed four TSC directors to assess
the quality of NERP
training that these individuals received.
The inspectors
had each director
classify four events
and explain the'ir responses
to making protective action
recommendations
(PARS) under changing plant conditions
and
how RVLIS values
corresponded
to core uncovery.
The directors
answered all of'the questions
correctly.
4.1.5 Staff Training and gualification in EP
The inspectors
reviewed
EP training records,
training procedures,
lesson
plans,
and the licensee's
NERP to evaluate
the licensee's
EP Training
Program.
The inspectors
also reviewed chemistry procedures
and training
records for operating the Post Accident Sampling System
(PASS).
Using the
ERO list, the inspectors
randomly selected
50 individuals'raining
attendance
records
from the Training Department files.
The records
indicated
that all of the selected
ERO personnel
had received their annual training and
were qualified to fill their assigned
emergency
response
positions.
The
inspectors verified that the
CNEP had removed individuals from the
ERO list
who failed to meet training requirements,
and that
new
ERO members
had
received the required training.
The inspectors
reviewed various
EP lesson
plans
and determined that they met the objectives set forth in the Nuclear.
Emergency
Response
Plan Training Program Procedure,
TR C.22.
The inspectors
reviewed training agendas
provided by the licensee
and their
contractor to local hospitals,
township fire departments,
sheriff offices and
ambulance services'gainst
NERP, Section
7. 1.4, Special Training for
Participating Agencies,
and found them to be very comprehensive.
State
and
. local agencies
appear to be kept well informed of any
NERP changes.
The
licensee
also participated
in numerous
town meetings providing support to
local agencies.
The inspectors
also reviewed chemistry procedures
for operating the
PASS and
found them to be comprehensive.
The training records
indicated that chemistry
technicians
received
both classroom
and hands-on training annually.
In
addition, the chemistry supervisor recently
began to test technicians
monthly
on operating the
PASS to maintain their proficiency.
In 1995, the licensee
conducted
a semi-annual
Health Physics drill to specifically test the adequacy
of the
and found performance to be acceptable.
Also, in October
1995,
the
NRC performed
a radiological confirmatory measurements
inspection
(NRC
'I
20
Inspection
Report
No. 50-244/95-18).
During that inspection,
the inspectors
observed
the licensee
successfully taking
a
PASS reactor coolant sample.
The inspectors
determined that the licensee
maintained
a good onsite training
program
and noted that the licensee is very diligent in providing training,
conducting drills and maintaining
an excellent rapport with state,
local
and
emergency
support entities.
The licensee
was fully capable of operating the
PASS and technicians
were well trained.
4.1.6 Organization
and Administration
The licensee's
EP organization
and
ERO have remained essentially stable
since
the last program inspection
when
a corporate reorganization
had occurred.
There were no changes
in the management
reporting chain for the
EP group.
The
OEP,
who has
been in his position for over
a year, reports to the
CNEP,
who
reports to the
MNA who then reports to the Vice President
Nuclear Operations.
The inspectors
interviewed the
CNEP and the
MNA separately
regarding the
program,
program initiatives and significant issues.
All responses
were
consistent;
therefore,
the inspectors
concluded that good communications exist
within the
EP group.
Neither the
HNA or the
CNEP has
been
assigned
additional responsibilities
since the last inspection.
However, the inspectors
observed
a minor
discrepancy
in the organization chart in Figure 7.1 of the
NERP.
The chart in
the
NERP does not include Process
Improvement
as
a reporting function to the
HNA.
The inspector's
determined this to be insignificant and the licensee
agreed to revise the
NERP chart.
According to-the
CNEP, offsite personnel
and organizations
remained the
same
except that the director of the State's
emergency
management
organization
was
replaced.
The individuals who report to the director have remained the same.
The inspectors
concluded that offsite support
has not been significantly
effected
by personnel
changes.
The inspectors
found that there were no changes
to personnel
in key
positions since the last
EP program inspection
and each
ERO position is
staffed with at least three qualified individuals.
Overall, staffing of the
licensee's
organization
and offsite entities
have
been stable.
4.1.7 guality Assurance in EP Activities
The inspectors
reviewed Audit Reports
AINT-1996-0001-NAB and
AINT-1995-0007-GFS, of the'EP Department,
conducted
in 1996 and
1995,
respectively.
The inspectors
also reviewed audit plans, checklists,
procedures
and interviewed personnel
from the
gA Department regarding the
process for conducting
a program audit.
Based
on document review and interviews, the inspectors
determined that the
audits were conducted utilizing an audit plan
and checklists
and that the
audit team included
a technical specialist
from another nuclear utility.
The
1996 Audit Report, stated that program deficiencies identified in 1995 were
corrected with the exception of the licensee failing to keep telephone lists
i
21
current.
The licensee is currently working to resolve this matter
and it has
been entered
into the tracking system.
Overall', the audits
addressed
the
areas
specified in 10 CFR 50.54(t).
'owever,
the inspectors identified that
gA had never audited the contractor
used to audit, train,
and provide radiological medical consultations
to local
hospitals,
although other licensee contractors
had
been audited.
The
inspectors
stated that
an audit of the
EP contractor,
although not a
requirement,
would be beneficial to the program.
While interviewing the
gA Manager
and the Independent
Assessor,
the inspectors
were informed that pre-audit interviews were conducted with the supervisor of
the departments
being audited.
In accordance
with gA Procedure
gA-1803,
"Performance of guality Assurance Audits," the pre-audit conference with the
'supervisor is intended to "solicit scope additions
and management
concerns."
According to the
gA Manager, this conversation
is used to solicit additional
information,
such
as department deficiencies
and problems,
and is then
added
to the audit plan
and checklist.
The inspectors
reviewed the audit plans
and
checklists
from 1996
and 1995,
and could not determine if information from the
pre-audit interview was
added to either the audit plan or checklist or what
portion of the audit focused
on the identified deficiencies or problems.
The
licensee
stated that the pre-audit interview makes
them aware of already
existing problems which serves to better utilize the time spent in an audit.
III
The guideline in Section 4.3 of ANSI/ASME N45.2.12-1977,
states that,
"a brief
pre-audit conference
shall
be conducted with the cognizant organization
manager.
The purpose of the conference
shall
be to confirm the audit scope,
present
the audit plan, introduce auditors,
meet counterparts,
discuss
audit
sequence
and plans for the post-audit conference,
and establish
channels of
communications."
Also, Section 4.3.2.2 states,
"objective evidence shall
be
examined for. compliance with quality assurance
program requirements."
The
inspectors
agreed that
a pre-audit conversation
to discuss
the scope of the
audit is an acceptable
practice,
but having the audited supervisor identify
deficiencies
and problems could raise questions
about the capability of the
audit team to identify program problems independently.
Also, the inspectors
questioned
the audit team's capability of remaining objective in reaching its
conclusions if an issue
has already
been characterized
as
a problem by the
supervisor prior to the audit.
While the contents of the audit, reports satisfied
requirements,
the inspectors
was not able to determine if the audit was unduly
biased
by the pre-audit interview.
Although the gA Manager believes this
practice to be acceptable,
he agreed to review the matter.
.4. 1.8 Miscellaneous
EP Issues
U dated Final Safet
Anal sis
Re ort
I consistencies
Since the Ginna
UFSAR does not specifically include
EP requirements,
the
inspectors
compared
licensee activities'to the
NERP, which is the applicable
document.
The following inconsistencies
were noted
between
the emergency
plan
and licensee activities by the inspectors.
f,
22
1. The inspectors
reviewed Section 8.1 of the licensee's
NERP describing
recovery
and noted that the Plant Operations
Review Committee
(PORC) is-
responsible for evaluating plant conditions,
reviewing decontamination
activities
and necessary
repairs prior to giving approval for plant
reentry.
The inspectors
reviewed the
PORC charter
and noted that it did
not mention their recovery
phase responsibilities.
Also, per the
NERP,
.
members of the recovery organization will be given recovery training
, annually.
The inspectors
discussed
exercising recovery actions with the licensee.
The licensee
stated that at the conclusion of every exercise,
the recovery
manager
discusses
recovery actions with his staff.
Additionally, the
inspectors
determined that recovery training is included in the annual
emergency
response
requalification training.
However, the licensee
could
not provide assurance
that all
PORC members
are part of the
ERO,
and
therefore,
are receiving the emergency
response
requalification training.
The licensee
stated that the
ERO and the training records
would be reviewed
to determine whether all
PORC members receive the necessary
training
regarding their recovery
phase responsibilities
and the
PORC Charter will
be revised to be consistent with the
NERP.
2. The Nuclear
Emergency
Planning Organizational
Chart listed
on
NERP Figure
7.1 was
compared to the
EP departmental
organization chart
and it was
determined that
a minor discrepancy
existed
(See Section 4. 1.6).
3.
The licensee
has never exercised
the Assessment
Facility for analyzing both
onsite
and offsite samples
during an emergency.
Also, the licensee
does
not have procedures for using this facility as
a radiological laboratory.
These
are required
by Section 7. 1.5 and Section 6.3.9 of the
NERP
(See
Section 4. 1.2 and Notice of Violation).
Closed
IFI 50-244 95-19-01
Reactor
Vessel
Level Indication
S stem
Discre ancies
During the December
1995 exercise,
confusion arose
among participants
pertaining to RVLIS.
Specifically, it was uncertain
what RVLIS value
corresponded
to the top of the fuel.
The lead inspectors
called two licensee
personnel
to obtain the correct value.
The inspectors
was given three
different RVLIS values for the top of the fuel - 1)
42 percent
was the value
from the licensee's
Emergency
Response
Data System
(ERDS); 2)
55 percent
was
from an engineering
drawing;
and 3) 68 percent
was from the emergency
operating
procedures
(EOPs) setpoint
book when in adverse
containment
conditions.
The lead inspector
asked the licensee to resolve the confusion
and to ensure that the concept of adverse
containment conditions,
and its
implication for all instrumentation
readings,
were understood
by engineers
in
the
TSC and
EOF.
The licensee
agreed to correct the
EROS RVLIS value
and to
review all
ERDS parameters
to ensure
accuracy.
The licensee
also agreed to
ensure that the correct values
and the concept of adverse
containment
condition values
would be properly incorporated into all procedures.
Since that time, the licensee
conducted training and revised the core
damage
procedure
and appropriate
EAL basis to clarify the issue.
The value to be
23
used for the top of the fuel is 68 percent,
which is the value used in the
and which incorporates
instrument uncertainties
associated
with adverse
containment conditions.
During this inspection,
the inspectors verified the
effectiveness
of the licensee's
training by questioning four TSC directors
about
Their answers
were correct
and consistent with licensee
expectations.
The licensee
also revised
EPIP 2-16,
"Core Damage Estimation,"
by cautioning users to utilize the setpoints
and instructions
found in the
and to consider
temperatures,
in addition to water
level,
when analyzing core conditions.
The licensee
also
added
an engineering
diagram depicting
RVLIS values to their corresponding
reactor
vessel
location
to assist
personnel
in assessing
core uncovery.
The licensee
changed
the
wording in several
emergency
action level basis
documents to clarify minimum
level for core cooling.
The licensee is currently reviewing and revising its
EROS data point library to ensure that RVLIS and other values
are correct.
Based
upon the licensee's
corrective action to this issue, this item is
closed.
C osed
U I 50-2
93-18-02
U t
m l
r tec i e
t o
e
o
e
d tio
During the November
1993 exercise,
an area for potential
improvement
was noted
regarding a,failure to issue
a timely PAR.
When
a General
Emergency
(GE) is
declared,
a
PAR is to be issued with the 15-minute notification.
The
licensee's
notification form listed four choices for PARs:
1) There is no
need for protective actions outside the site boundary;
2)
Need for protective
action is under evaluation;
3) Sheltering
recommended;
and 4) Evacuation
recommended.
During the exercise,
the
GE was declared at approximately
10: 15 a.m.
At 10:25 a.m., the licensee
issued
the
"Need for protective
action is under evaluation."
The licensee
was prepared to issue
a
PAR based
on plant conditions at the time of the
GE declaration;
however, prior to
making the offsite notifications, plant conditions
changed
such that the
also changed.
The licensee
took time to evaluate
the latest plant and
radiological conditions to make the appropriate
PAR,
and correctly issued
the
PAR to shelter at 10:55 a.m.
This was '40 minutes after the
GE had
been
declared
and did not meet the
15 minute goal.
During inspection
94-21, the inspectors
determined that the licensee
deleted
"Need for protective action is under evaluation"
as
a
PAR option.
..This
removed the implication that
PAR issuance
can
be delayed.
Also, the
inspectors
reviewed requalification training lesson
plans
and confirmed that
the objective of issuing
a
PAR within 15 minute of the
GE declaration
had
been
emphasized
to potential decision-makers.
However,
due to the potential public
impact of delaying
a-PAR, this issue
remained
open pending the timely and
accurate
PAR issuance
by the licensee
during an
NRC evaluated
exercise.
During the licensee's
December
6,
1995 full-participation exercise
(Inspection
Report 95-19), the licensee
successfully
demonstrated
the timely and accurate
issuance of PARs.
Due to an administrative oversight, this item was not
closed at that time.
The inspectors
determined that the licensee's
performance
during the December
1995 exercise
was sufficient to close
URI 50-
244/93-18-02.
I
I
4.2
Radioactive Liquid and Gaseous
Effluent Control
Programs
(IP 84750)
4.2.1 Nanagement
Controls
o
am
C
a
es
The inspector reviewed the organization -and administration of the radioactive
liquid and,gaseous
effluent control programs.
The inspector
determined that
there were no changes
to the radioactive effluent control
programs
since the
last inspection
conducted
in July 1994.
The Chemistry Department
has primary
responsibility for conducting the radioactive liquid and gaseous
effluent
control programs.
Other responsible
groups for the programs
are:
1) Operations,
2) Instrument
and Controls (I&C), 3) System Engineers,
4)
Results
and Test
(R&T), and 5) Radwaste
Operations.
ualit
Assurance
A
Audits
The inspector
reviewed the
1995
gA audit report (Report No. AINT-1995-0010
-GFS), required
by Section 6.5.2.8 of the technical specifications
(TS).
The
gA audit covered eight areas,
including radioactive liquid and gaseous
.
effluent control programs, radiation protection,
and the Radiological
Environmental Monitoring Program.
There were
no audit findings or
deficiencies identified by the
1995 audit team for the effluent control
programs.
Based
on the
1995 audit report review, the inspectors
determined
that the licensee
met the
TS requirement.
eview of Semiannual
Annual
Rad oactive
E f uent
Re
o ts
The inspector reviewed the
1994 semiannual
and the
1995 annual radioactive
effluent release
reports.
These reports provided data indicating total
released
radioactivity for liquid and gaseous
effluents.
These reports also
summarized
the assessment
of the projected
maximum individual
and population
doses resulting from routine radioactive airborne
and liquid effluents.
Projected
doses
were well below the
TS limits.
The inspector determined that
there were no obvious anomalous
measurements
or omissions
in the reports.
4.2.2 Review of Off-Site Dose Calculation Nanual
(ODCN)
The inspector
reviewed the licensee's
current
ODCM (effective date
February
24,
1996).
The
ODCM provided descriptions of the sampling
and
analysis
programs that are established
for, quantifying radioactive liquid and
gaseous
effluent concentrations
and for calculating projected
doses. to the
public.
All necessary
parameters,
such
as effluent radiation monitor setpoint
calculation methodologies,
site-specific dilution factors,
and dose factors,
were listed in the
ODCM.
The licensee
adopted other necessary
parameters
from
Regulatory Guide
1,. 109.
,,Based
on the above review, the inspector determined that the licensee's
contained all necessary
information and instruction to establish
and implement
the radioactive liquid and gaseous
effluent control programs
and the
Radiological
Environmental Monitoring Program.
r
25
4.2.3 Radioactive Liquid And Gaseous
Effluent Control
Programs
To determine the implementation of the
TS and the
ODCM requirements,
the
inspectors
toured the plant,
reviewed the following selected
licensee's
procedures,
and reviewed selected
radioactive liquid and gaseous
discharge
permits:
~
CH-RETS-Minipurge
~
CH-RETS-Purge-CV
~
CH-RETS-PV-Release
~
CH-RETS-GDT-Release
~
CH-RETS-LIg-Release
During the tour, the inspector noted that all effluent radiation monitoring
systems
at the time of this inspection.
During the review
of the above radioactive liquid and gaseous
effluent procedures,
the inspector
noted that the procedures
were easy to follow and contained sufficient level
of detail.
The inspector also determined that the reviewed discharge
permits were
complete
and met the
TS/ODCM requi} ements for sampling
and analyses
at the
required frequencies
and met the lower limits of detection established
in the
ODCM.
4.2.4 Steam Generator
Blowdown Tank and Spent
Fuel
Pool
Leakages
This portion of the inspection evaluated
the licensee's
efforts to accurately
quantify and characterize
suspected
leakage
from the steam generator
blowdown
tank and the spent fuel pool system,
and potential
dose
consequences
of any
releases
to the environment.
This evaluation
focused
on the licensee's
actions
and their results in this area since January
1996 and future plans
with respect to the steam generator
blowdown tank and the spent fuel pool
system.
S
G
Blowdown Tank Leaka
e
On January
5,
1996, the licensee
noted that small
amounts of iodine-131
(I-131) and iodine-133 (I-133) were measured
in grab samples
taken from the
turbine building retention tank and the intermediate
subbasement
ground water
in-leakage.
Further licensee
investigation results revealed that the origin
of the leakage
was from the discharge
piping of the steam generator
(SG)
blowdown tank.
The retention tank, also
known as the turbine building drains
tank, is located in the turbine building and collects drainage
from
miscellaneous
drains
such
as roof drains
and floor drains.
The licensee
was
not able to determine
the leak rate,
because
there is no flow measurement
instrument installed for measuring
the flow rate downstream of the blowdown
tank.
Therefore,
the total
amount of leakage to the soil under the turbine
building floor was not known.
The licensee
speculated
that the leakage
was
small,
because
iodine activities from the retention tank and the intermediate
subbasement
ground water in-leakage
were very low.
During the outage in
April 1996, the licensee
plans to modify the discharge
piping, which is
expected to stop this leakage
pathway.
26
The licensee
took routine grab samples
from the
SG blowdown tank and analyzed
them for gamma emitters
and tritium.
The licensee
also performed the
projected
dose
assessment,
as required
by the
TS and the
ODCH.
The inspector
reviewed the analytical results
and the projected
dose
assessment
results,
which were calculated
based
on the total release of the
SG blowdown tank for
the period of January to February
1996.
Major gamma emitters
were
radioiodines with range of lE-6 to lE-7 pCi/cc.
Tritium activity was about
1E-4 pCi/cc.
The maximum projected thyroid doses for January
and February
was
1.99E-2
mrem and 2.58E-2
mrem, respectively.
These values
were well below
regulatory limits.
The licensee
suspects
that
a small fraction of
radioiodines
(mainly I-131 and I-133) may be dep'osited
in soil under the
turbine building floor, while tritium may be migrating into ground water.
Based
on the above reviews
and short half-life of radioiodines,
the inspectors
determined that the leakage
was not currently of sufficient magnitude to
affect public health
and safety or the environment.
S ent Fuel
Pool
Leaka
e
During previous inspections
(Inspection
Rep'ort Nos:
50-244/95-20
and 95-21),
an
NRC inspector
reviewed the licensee's
investigation results for the
suspected
fuel pool leakage,
including planned future actions.
t
There are three on-site environmental wells located northeast
(Well C),
southeast
(Well B), and southwest
(Well A) of the plant.
Analytical results
of tritium at Wells A and
B suggested
that tritium activities
had not
increased
since
November
1995.
But tritium activities at Well
C had increased
since September
1995,
as
shown in Table 1.
Table
1 - Analytical Results of Tritium for On-Site Environmental
Wells
Unit: pCi cc
Date
9-1-95
10-16-95
11-8-95
11-17-95
11-28-95
12-15-95
1-18-96
1-25-96
2-7-96
2-23-96
"
Well A
No Measurement
No Measurement
1.74E-8
6.31E-8
-3.80E-8
6.58E-7
No Measurement
No Measurement
No Measurement
No Measurement
Well
B
No Measurement
No Measurement
4.98E-7
No Measurement
3.45E-7
1.96E-6
No Measurement
No Measurement
No Measurement
No Measurement
Well
C
1.76E-6
6.90E-7
No Measurement
2.02E-7
-1.74E-7
2.05E-6
4.16E-6
3.40E-6
1.53E-5
1.75E-5
27
- Below the minimum detection level.
Normal environmental
background is
approximately
1E-7 pCi/cc.
Mell
C was the optimum location to monitor possible
environmental
release
through ground water due to the prevalent northeasterly direction of ground
water flow.
Analytical results of Wells A and
B were used
as environmental
background,
since they are upstream of the underground water flow.
During this inspection,
the inspector discussed
the site hydrology with the
licensee
and
a consultant.
The consultant
(Dr. R. Poreda,
Associate
Professor,
University of Rochester)
presented
tritium underground migration
study results,
and desc} ibed the underground water mixing ratio.
The high-
mixing ratio indicated relatively low underground
water movement.
The mixing
ratio at the Mell
C was the highest
and suggested
that the underground
water
movement
was slow at this location.
This study supports
the slow tritium
increase
seen at Well C,
as illustrated in Table l.
The depth of Well
C is about
20 feet from ground level.
In order to assess
the underground
water movement better,
a new deep well adjacent to Well
C has
been
recommended
by the licensee's
consultant to obtain better
characterization
and representation
of suspected
leakage to the environment.
4.2.5
NRC Assessment
and Planned
Licensee Action
Based
on reviews of limited analytical data
and interviews with the licensee
and its contractor,
the inspector
made the following conclusions:
~
The sources of contamination
at Mell
C may be multiple, such
as leakage
from the spent fuel pool
and
SG blowdown tank.
Routine discharge
pathways,
such
as condenser air ejector effluents, might also contribute to the
tritium activity at Well C; and,
~
The suspected
leakage
from the spent fuel pool
and the
SG blowdown tank,
do
not currently impact public health
and safety
and the environment.
In an effort to provide for assessment
of suspected
leakage,
the licensee
plans to:
~
Install
a deeper monitoring well (or a multi-level monitoring well)
adjacent to Well
C and analyze
ground water samples;
~
Continue to monitor and analyze
samples
from on-site Wells A, B,
and
C;
~
Continue to monitor and evaluate
the ground water movement;
and,
~
Determine actions for resolution of remediation of suspected
leakage.
~
Apply an epoxy coating to the bottom of the fuel transfer canal to stop
leakage
through the foundation bolts supporting the fuel transfer cart
rails.
~
~
A
28
The inspector
found the licensee's
current action plan to be appropriately
scoped.
4.2.6 Calibration of Effluent/Process
The inspector reviewed the most recent calibration results for the following
effluent/process
RHS to determine the implementation of the
TS requirements:
~
RE-10A, Containment
Gamma Detector
~
RE-12,
Containment
Gas Detector
~
R-12A, Containment
Purge
(SPING-4)
~
R-14A, Plant Vent (SPING-4)
~
R-15A, Condenser Air Ejector
(SPING-4)
~
RE-17,
Component
Cooling Water Detector
~
RE-18, Liquid Waste Disposal
~
RE-19,
Blowdown
~
RE-20 ALB, Spent
Fuel Pit Service Water Detectors
The
18C Department
and the RP/Chemistry
Department
had the responsibility to
perform electronic
and radiological calibrations,
respectively, for the above
radiation monitors.
All reviewed calibration results
were within the
licensee's
acceptance criteria.
The inspector discussed
the maintenance
of operability/reliability with the
members of the
18C and RP/Chemistry staff.
From these interviews, the
inspector determined that these individuals had good knowledge of the
relative to operability requirements
and performance history.
The inspector
noted that the
RHS read-out devices in the control
room were replaced with
digital devices.
Consequently,
calibration results
are more reliable because
more accurate
readings
can
be obtained.
The inspector also noted that the
licensee
performed daily trending analysis for the above
RHS in the main
control room.
The licensee plots
RMS readings
twice in a day on the control
charts to track any changes.
The inspector stated that the tracking of RHS
readings
was
an excellent effort to verify the system operability and
reliability.
Based
on the above reviews,
the inspector determined that the licensee's
performance
and achievements,
relative to calibration of the
RHS and the
upgrading projects,
were sufficient to demonstrate
good operability and
reliability of the system.
4.2.7 Air-Cleaning Systems
ir-Clean n
S stems
e uired
b
the Technical
S ecification
The inspector
determine the
emergency 'air
-The inspector
reviewed the licensee's
most recent surveillance
test results to
implementation of TS requirements for the:
1) control
room
supply systems,
and 2) containment air recirculation system.
reviewed the following surveillance test results:
~
Visual Inspection
~
In-Place
HEPA Leak Tests
29
~
In-Place Charcoal
Leak Tests
~
Air Capacity Tests
~
Pressure
Drop Tests
~
Laboratory Tests for the Iodine Collection Efficiencies
All test results
were within the licensee's
TS acceptance
criteria.
The
inspector
had
no further questions
in the above surveillance tests.
ir-Cleanin
S stems
Oescr
bed in the
U dated Final Safet
nal sis
e ort
During the reviews of other air-cleaning
systems
committed
by the
UFSAR, the
inspector
noted that the licensee's
procedure did not have acceptance
criteria
for the airflow capacity test
and resulted deviations
from the
commitments.
The current industry practice for the acceptance criteria of the
airflow capacity test is +10 percent of the designed flow.
These
acceptance
criteria are also listed in ANSI N510-1986.
The following was noted:
~
UFSAR 6.4.2.2.1:
Airfloh capacity for the Control
Room during the
normal operation is 8,045 cfm.
Surveillance Results:
~
UFSAR 12.3.3.2:
2-5-94
12,821
4-13-95:
-
10,431
Airflow capacity for the Plant Vent is 75,000 cfm.
The value is being used for the setpoint calculation,
as defined in the
ODCH.
Surveillance
Results:
3-31-92:
66,554
scfm for A-Train
68,819
scfm for B-Train
3-8-94:
67,364
scfm for A-Train
75,662
scfm for B-Train
3-21-95:
63,139
scfm for A-Train
68,247
scfm for B-Train
10-5-95:
61,660
scfm for A-Train
No data for B-Train
~
Auxiliary Building Ventilation System:
No airflow capacity
was defined in
the
Therefore,
the licensee
assumed,
based
on nominal air flow per
filter (84
HEPA filters x 1,000 cfm per filter
84,000 cfm).
The inspector noted that the
UFSAR did not provide any acceptance
criteria for
the air capacity test,
and the listed values for the above
systems
were vague
relative to design requirements.
Although these
apparent
discrepancies
between surveillance
tasks
and the values listed in the
UFSAR do not have
a
significant impact
on public health
and safety
and the environment,
the
inspector
stated that:
1) airflow capacity test procedures
should
be updated
to follow the industry practice;
2) design-base
airflow capacity should
be
retrieved from the original design basis,
rather than
assumed
(e.g., auxiliary
I
30
building ventilation system);
and,
3)
UFSAR should
be reviewed
and updated to
reflect the current plant designs
and configurations.
This item is considered
unresolved
pending further review (URI 50-244/96-01-05).
The licensee
stated
that the
UFSAR is being reviewed
and will be updated.
4.3
Radioactive
Waste Storage,
Processing
Systems,
and Equipment (IP 71750)
The Waste Disposal
System
(WDS) at the Ginna Station consists of three
subsystems
used to collect and process all potentially radioactive liquid,
gaseous,
and solid waste.
All the equipment for these
subsystems
has
been in
place since original plant construction,
except for the
a liquid waste
evaporator that was removed from service
and abandoned
in place in 1990
and
an
ultra filtration unit physically removed from the plant in 1980.
Radioactive
fluids entering the
WDS are collected in sumps
and tanks until a determination
is made
on the type
and level of treatment
necessary.
The fluids are
sampled
and analyzed to determine the level of radioactivity before
any discharge
is
made.
Liquid wastes requiring cleanup before release
are collected
and
processed
by a vendor supplied demineralization
system.
All solid waste is.
packaged
and stored
on site until they are shipped offsite for disposal.
Gaseous
waste is pumped to a gas
decay tank where it is held for a suitable
decay period.
The gases
are then discharged intermittently at
a controlled
rate through
a monitored plant vent.
The principle components of the
WDS
include the following:
1) Miscellaneous
Waste Disposal
System (radio chemistry laboratory drain tank
and discharge
pump; laundry hot shower tanks;
intermediate building sump
pump)
2) Liquid waste drains,
waste holdup tank (auxiliary building equipment
and
floor drains)
3) Spent resin tanks
and cubicle
4) Liquid waste evaporator
and waste
condensate
tanks
(abandoned
in place,
no
maintenance
required)
5) Reactor coolant drain tank
6)
Gas waste disposal
system
(gas compressors,
compressor
moisture separators
and compressor
seal
heat exchangers,
and gas
decay tanks)
The inspector
discussed
the radiological conditions present
in the
WDS
equipment with the principle health physicists at the station.
There are
currently no hot spots or high exposure
areas that are accessible
to
personnel,
and no spills of radioactive material
have occurred
from the
WDS
since
an incident in 1983.
No residual effects from that incident appear to
remain.
No excess
personnel
exposure
or contamination incidents
have occurred
in recent years
from the use of these
systems.
The system engineer for the waste disposal
systems
conducts quarterly walkdown
inspections.
For each walkdown, the engineer
documents
the condition of the
equipment
and identifies any,deficient conditions that require corrective
action follow-up.
The most recent
walkdowns were performed in February
1996
and no conditions requiring immediate maintenance
were identified.
Minor
discrepancies
were noted
and were scheduled for routine maintenance.
Portions
of the radwaste
systems
already
have established
performance criteria since
they will fall within the scope of 10 CFR 50.65
(Maintenance
Rule) in July
~
~
31
1996.
The system engineer
performed
a two year historical evaluation of these
systems
and documented
the amount of corrective maintenance
and the
modifications
made over that period.
The inspector reviewed this
documentation
and determined that the amount of corrective maintenance
and the
number of modifications have not been significant.
The inspector
reviewed the
P8 IDs for these
systems
and conducted visual
inspections of all accessible
equipment.
Overall, these
systems
are well
maintained
and do not appear to represent
a significant radiological
hazard to
plant personnel.
All areas
and equipment
observed
are serviced
by the
filtered ventilation system for the auxiliary building,
and fire protection
systems
also were present
in these
areas.
Section 1.2.6 of the
UFSAR for the
Ginna Station contains
a brief description of the purpose
and
use of the Waste
Disposal
System.
The description indicates that the system collects
and
processes
for disposal all potentially radioactive liquids, gaseous,
and solid
waste resulting from reactor operation
and cleans
up all effluents released
to
the environment to concentration
levels below those required
by 10 CFR 20.
Operating procedures
are designed to limit normal effluents to within the
limits required
Solid wastes
produced at the Ginna
Station are packaged
and shipped for disposal
at authorized locations.
The
inspector
concluded that no inconsistencies
appear to exist between the
description of the waste disposal
system
and its use,
and the system installed
and
used in the plant.
The inspector also determined that there
does not
appear to be
a need for enhanced
inspection of these
systems
beyond
the'outine
inspections currently performed.
ontaminated
Stora
e Buildin
CSB
The licensee
maintains
a separate facility at the Ginna Station with a
controlled environment for storing contaminated
and reusable tools and
equipment.
Equipment that can
be decontaminated
to less
than 8 mR/hr on
contact is stored in containers that protect the equipment
and personnel.
The
general
area
background levels inside the
CSB are currently about
1 mR/hr.
The
CSB also contains
a specially designed
work area for decontaminating
the
stored
items after they are used.
The wor k area contains
the appropriate
facilities for filtered ventilation and collection sinks for capturing liquids
and solids
removed during the decontamination
work.
The inspector toured the
CSB and observed
the arrangement
of stored
equipment
and plant personnel
'andling
and processing materials
and equipment returning to storage.
The
radiological controls in place
appeared
to be effective and the general
state
of housekeeping
in the
CSB was very good.
Video Ins ection of S ent Resin Tank Roo
The two spent resin tanks at Ginna are located inside
a cubicle in the lower
level of the Auxiliary Building adjacent to the charging
pump room.
The
cubicle
has
been
blocked off to personnel
access
since late
1970 due to the
high radiation levels present
inside the cubicle after the first plant
operating- cycle.
An unsealed
concrete
block barrier completely fills the
inner doorway into this area
and provides shielding from the high radiation
inside.
The outer doorway in front of the concrete
blocks is maintained
as
a
The cubicle was last entered for a radiological
32
n
survey in 1993 after all spent resin stored onsite
was shipped
away for
disposal.
The cubicle contains
two 150 ft'apacity resin tanks
and
associated
piping to store contaminated
spent resin from the
CVCS purification
system demineralizers.
Routine entries for surveys
are not made into the cubicle since all valves
and
operator controls for the equipment
are located outside the cubicle.
However,
on Harch 20,
1996, the licensee
removed
one row of concrete
blocks at the top
of the doorway to gain access
for a remote= radiation survey,
and for a remote
color video inspection.
The inspector
observed
the inspection
on a remote
monitor and noted the material condition of the cubicle.
Host areas
were
visible to the camera
except directly under the two tanks. 'ne tank contained
approximately
40 ft'fspent resin
and was creating
a radiation field of 400
mR/hr just on the insi'de surface of the block wall.
Both tanks
and all of
their associated
piping are stainless
steel.
The equipment also appeared
to
be in very good condition,
and was not'deteriorating.
There were no signs of
current leakage of any liquid or resin from any of the piping. or" tanks.
The
walls and floors of the cubicle were dry.
A padlock and small piece of sheet
metal
were noted
on the floor; however,
the cubicle was otherwise clean,
and
was not being
used to store
any waste material in barrels or other containers.
Overall, the cubicle appeared
to be in very good condition and did, not
represent
a potential
hazard to personnel.
The 40 ft'fspent resin in one
tank represents
the total stored inventory onsite at the present
time.
The auxiliary building also contains
a "DI Vault" which houses
several
deionization vessels
used in the
CVCS purification system,
the
SFP cleanup
system,
and other purification systems
in the plant.
This vault was also
blocked off to personnel
access
in 1970 due to the very high radiation levels
inside.
The last radiological
survey available for this vault was taken in
February
1988
and indicated that tank surface contact readings varied from
, 2 10 R/hr.
The survey also indicated the'resence
of a small, amount of
water on the floor that was apparently leaking from a pipe in the overhead, of
the vault.
The licensee
was not able to confirm whether there is currently
any water present
in the vault, or if any maintenance
was performed
on
interior piping in 1988.
However, the inspector
observed that the block wall
in the access
doorway was not sealed,
and there
was
no water present at the
exterior base of the wall.
The licensee
agreed to perform a remote video
inspection of the vault during the current refueling outage,
and will document
the general
condition of equipment
and the radiation levels in the room.
4.4
(SG) Replacement
Security Program
4.4.1 Plant Nodifications
The inspector
reviewed the licensee's
proposed-security
program modifications
necessary
for the
SG replacement
program.
The modifications were designed to
include devitalizing the containment
vessel for a period during the
replacement
project,
and then revitalizing the containment after its integrity
is reestablished
and appropriate verifications of systems
and equipment
are
complete.
~
~
~
33
The containment is being devitalized
because
the
SG replacement
project
requires cutting large holes into the top of containment
(a vital area
barrier).
Implementation of adequate
compensatory
measures
for the degraded
barrier was
deemed impractical.
The containment devitalization program requires the installation of a new door
to provide a new access
route to containment that does not require passing
through other vital areas.
In addition to the installation of a new door,
temporary barriers installed around the containment
personnel
entry area were
intended to separate
the de-vitalized area
from adjacent vital areas.
At the
conclusion of the inspection,
the installation of the door was not complete
and the installation of the temporary barriers
had not begun;
however, the
inspector's
walkdown of area to be modified and review of the proposed
modifications identified no apparent
weaknesses
in the proposal.
4.4.2 Procedures
The inspector reviewed security post orders
developed for the security posts
at the containment
personnel
hatch.
The post orders
were developed for use
when the containment is vital and also when it is devitalized.
No weaknesses
were noted in the post orders.
The modifications to the NRC-approved security plan for the
SG replacement
program were submitted to the
NRC, in accordance
with the provisions of 10 CFR 50.54(p),
on January
15,
1996.
The
NRC notified the licensee
by letter, dated
March 18,
1996, that the changes
had
been reviewed
and were determined to be
consistent with the provision of 10 CFR 50.54(p)
and were acceptable for
inclusion in the security plan.
4.4.3 Security Organization
The inspector's
review determined that the licensee
had
augmented
the existing
security organization with eight temporary security officers to support the
replacement
project.
The inspector
reviewed the training records for four of
the eight officers and determined that they had
been trained
and qualified as
unarmed guards,
in accordance
with the provisions of the NRC-approved security
training and qualification plan.
No weaknesses
were noted during the review of the training records of the
temporary officers.
5.0
SAFETY ASSESSNENT/EQUALITY VERIFICATION (IP 71707)
5. 1
Reactor
Fuel Receipt Inspection
The licensee
received four separate
shipments of new reactor fuel
on
February
22 and 27,
and March
1 and 8,
1996.
A total of forty new fuel
assemblies
were delivered with ten assemblies
in each shipment.,
On
February
28 and March 1; 1996 the inspector's
observed receipt inspection of
new assemblies
by a
gC inspector during unpacking from the shipping containers
and during temporary storage.
After being unpacked,
each
assembly
was placed
into a designated
storage
rack inside
an enclosure
designed specifically for
a
'
'I
34
new fuel storage.
The enclosure
was maintained locked for restricted
access
and foreign material
exclusion controls were in effect with fuel present.
Each shipping container
was inspected for damage,
seal
and shock mount
integrity, tight closure
hardware
and clamps,
and the internal accelerometers
were verified to be unactuated.
Each assembly
was carefully rigged out of its
container,
unwrapped,
and set into its storage
rack prior to receipt
inspection.
A detailed visual examination'f
each
assembly
was performed
by the
gC
inspector to verify the assembly identification and ANSI numbers,
the lack of
physical distortion or damage,
the lack of foreign material,
and the condition
of the assembly grid straps.
The
gC inspector identified two fuel assemblies
(F56 and F72) with bent tabs
on their grid straps
during the receipt
inspection.
It did not appear that the bent tabs
caused
damaged to any of the
adjacent
fuel pins, but they did not allow for the required
gap around
each
pin.
The
gC inspector
documented
these conditions
and initiated an ACTION
Report to initiate corrective actions.
The condition was not significant
enough to reject the assemblies;
however,
a fuel vendor representative
came to
the Ginna Station
on March 1,
1996 to perform
a repair of the tabs.
After the
repair was made,
a complete receipt inspection
was reperformed with
satisfactory results
on the two assemblies.
The inspectors
reviewed the
gC records after the receipt inspection
was
completed
on all assemblies.
The documentation
was accurate
and complete.
Overall the receipt inspection
process for the
new fuel was thorough
and well
controlled.
5.2
Periodic Reports
Periodic reports
submitted
by the licensee
pursuant to Technical Specification 6.9.1 were reviewed.
The inspectors verified that the reports contained
information required
by the
NRC, that test results
and/or supporting
information were consistent with design predictions
and performance
specifications,
and that reported information was accur'ate.
The following
reports'ere
reviewed:
~
Monthly Operating
Reports for January
and February
1996
No unacceptable
conditions were identified.
5.3
Licensee
Event Reports
A Licensee
Event Rep'ort
(LER) submitted to the
NRC was reviewed
and the
inspectors
determined that the details were clearly reported,
the cause
was
properly identified,
and the corrective actions
were appropriate.
The
inspectors
also determined that the potential safety consequences
were
properly evaluated,
the generic implications were indicated,
events that
warranted additional follow-up were identified,
and the licensee
met the
applicable requirements
of 10 CFR 50.73.
The following LER was reviewed
(date indicated is event date):
35
~
LER 96-001,
Inservice Test Not Performed During Refueling Outage,
Due to
Inadequate
Tracking of Surveillance
Frequency,
Resulted
in Violation of
Technical Specification
(May 4,
1995)
This event represented
a violation of the technical specification requirement
to implement
an inservice test -program.
In this case,
the violation was of a
condition of a relief request,
which'specified that the valve at issue
be
disassembled
for the purpose of IST every other year during a refueling
outage;
although the valve had
been disassembled
for this purpose less than
two years earlier, it had not been
done during
a refueling outage.
The
licensee
noted that the valve at issue
was in an IST group with a maximum
acceptable
inspection interval of six years.
This violation is not being
cited because it was of minimal safety significance,
and the valve was
inspected within a two year interval.
This event is further discussed
in
Section 2. 1. 1 of this report.
LER 96-001 is closed.
6.0
ADMINISTRATIVE (IP 71707)
6.1
Senior
NRC Management Site Visits
During this inspection period,
two senior
NRC managers
visited Ginna Station.
On March 4,
1996,
Mr. Richard
W. Cooper, Director of the Division of Reactor
Projects,
Region I, toured the site
and met with senior lic'ensee
management.
On February
12-14,
1996,
Mr. Lawrence T. Doerflein, Chief of Reactor Projects
Branch
No. 1, Region I, toured .the site
and met with senior licensee
management.
6.2
Review of UFSAR Commitments
A recent discovery of a licensee
operating their facility in a manner contrary
to the Updated Safety Analysis Report
(UFSAR) description highlighted the need
for a special
focused review that compares plant practices,
procedures
and/or
parameters
to the
UFSAR description.
While performing the inspections
discussed
in this report, the inspectors
reviewed the applicable portions of
the
UFSAR that related to the areas
inspected.
Inconsistencies
were noted
between the wording of the
UFSAR and the plant practices
procedures,
and/or
parameters
observed
by the inspectors
in the areas of emergency
preparedness
and air cleaning
systems
as described
in sections
4.1.8
and 4.2.7,
respectively.
6.3
Exit Meetings
At periodic intervals
and at the conclusion of the inspection,
meetings
were
held with senior station
management
to discuss
the scope
and findings of
inspections.
The exit meeting for the steam generator
replacement
project
engineering
preparations
(section 3.1 of this report,
conducted
February 5-9,
1996)
was held by Mr. Suresh
Chaudhary
on February 9,
1996.
The exit meeting
for the effluents monitoring program inspection
(section 4.2 of this report,
conducted
March 4-8,
1996)
was held by Mr. Jason
Jang
on March 8,
1996.
The
exit meeting for the emergency
preparedness
program inspection
(section 4. 1
36
of this report,
conducted
March 11-14,
1996)
was held by Mr. David Silk on
March 14,
1996.
The exit meeting for the current resident
inspection report
50-244/96-01
was held on March 29,
1996.
a
I
ATTACHMENT 1
REVIEW OF THE NERP
AND EPIPs
An in-office review of revisions to the
NERP and
EPIPs submitted
by the
licensee
was completed.
A list of the specific revisions reviewed are
included in Attachment
1.
The inspectors
concluded that the revisions did not
reduce the effectiveness
of the
NERP and were acceptable.
oc d
e
o.
rocedure
't e
Revision
s
EPIP 1-0
EPIP 1-5
EPIP 1-9
EPIP 1-10
EPIP 1-11
EPIP 1-14
EPIP 2-2
EPIP 2-3
EPIP 2-4
EPIP 2-6,
EPIP 2-9
EPIP 2-16
EPIP 2-18
EPIP 3-3
EPIP 3-6
EPIP 4-1
EPIP 4-3
EPIP 5-2
EPIP 5-3
EPIP 5-4
Nuclear Emergency
Response
Plan
Ginna Station
Event Evaluation
and Classification
Notifications
Technical
Support Center Activation
Operational
Support Center
(OSC) Activation
Survey Center Activation
Station Call List
Obtaining Meteorological
Data
and Forecasts
and
Their Use in Emergency
Dose Assessment
Emergency
Release
Rate Determination
Emergency
Dose Projections
Manual
Method
Emergency
Dose Projection - Midas Program
Administration of Potassium
Iodine KI
Core
Damage Estimation
Control
Room Dose Assessment
Immediate Entry
Corporate Notifications
Public Information Response
to an Unusual
Event
Accidental Activation of Ginna Emergency Notification
System Sirens
Onsite
Emergency
Response
Facilities
and Equipment
Periodic Inventory Checks
and Testing
Testing the Ability to Notify Primary
NERP Responders
Emergency
Plan
Implementing Procedure
(EPIP)
Training Program
15
21,22
25
7
5
10
8
7
8
9
7
2
6
8
3
22
5
12,13
14
15
-F i